IR 05000250/2007002

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IR 05000250-07-002 and IR 05000251-07-002 on 04/19/2007 Turkey Point Nuclear Plant
ML071090366
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 04/19/2007
From: Ernstes M
NRC/RGN-II/DRP/RPB3
To: Stall J
Florida Power & Light Co
References
IR-07-002
Download: ML071090366 (30)


Text

ril 19, 2007

SUBJECT:

TURKEY POINT NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000250/2007002 AND 05000251/2007002

Dear Mr. Stall:

On March 31, 2007, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Turkey Point Units 3 and 4. The enclosed integrated inspection report documents the inspection findings which were discussed on April 10, 2007, with Mr. W. Jefferson and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, no findings of significance were identified. However, a licensee identified violation which was determined to be of very low safety significance is listed in this report. NRC is treating this violation as a Non-cited Violation consistent with Section VI.A.1 of the NRC Enforcement Policy because of the very low safety significance of the issue and because it is entered into your corrective action program. If you wish to contest this non-cited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Turkey Point.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the

FP&L 2 NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (The Public Electronic Reading Room).

Sincerely,

/RA/

Michael E. Ernstes, Chief Reactor Projects Branch 3 Division of Reactor Projects Docket Nos. 50-250, 50-251 License Nos. DPR-31, DPR-41

Enclosure:

Inspection Report 05000250/2007002 and 05000251/2007002 w/Attachment: Supplemental Information

_________________________

OFFICE RII:DRP RII:DRP RII:DRP ORA NRR NRR SIGNATURE SON JSS1 TCK by email WGR1 AZ by email JM by email NAME SNinh SStewart TKolb WRogers AZoulis JMitman DATE 04092007 04162007 04/12/2007 04/16/2007 04/12/2007 04/12/2007 4/ /2007 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICE RII:DRS RII:DRS RII:DRS RII:DRS SIGNATURE LXC by email SWF DLM4 LXC by phone for NAME MCain WFowler DMas Penaranda CEven DATE 04/12/2007 04/16/2007 04/16/2007 04/12/2007 4/ /2007 4/ /2007 4/ /2007 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

FP&L 3

REGION II==

Docket Nos: 50-250, 50-251 License Nos: DPR-31, DPR-41 Report No: 05000250/2007002, 05000251/2007002 Licensee: Florida Power & Light Company (FP&L)

Facility: Turkey Point Nuclear Plant, Units 3 & 4 Location: 9760 S. W. 344th Street Florida City, FL 33035 Dates: January 1 - March 31, 2007 Inspectors: S. Stewart, Senior Resident Inspector T. Kolb, Resident Inspector W. Rogers, Senior Reactor Analyst, RII (4OA5.2)

A. Zoulis, Risk & Reliability Analyst, NRR (4OA5.2)

J. Mitman, Risk & Reliability Analyst, NRR (4OA5.2)

M. Cain, Senior Reactor Inspector (1R02, 1R17)

W. Fowler, Reactor Inspector (1R02, 1R17)

D. Mas Penaranda, Reactor Inspector (1R02, 1R17)

C. Even, Reactor Inspector (1R02, 1R17)

Approved by: M. Ernstes, Chief Reactor Projects Branch 3 Enclosure

SUMMARY OF FINDINGS

IR 05000250/2007-002, 05000251/2007-002; 01/01/2007 - 03/31/2007; Turkey Point Nuclear

Power Plant, Units 3 and 4; Routine Integrated Report.

The report covered a three-month period of inspection by resident inspectors. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. Inspector Identified & Self-Revealing Findings None

Licensee Identified Violations

A violation of very low safety significance, identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and corrective actions are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status:

Unit 3 began the period at or near full power. Power was reduced to 40 percent on March 1, for main turbine valve testing and other planned maintenance. The unit returned to full power on March 3.

Unit 4 operated at or near full power during the inspection period with the following exception:

Unit 4 was shutdown on February 7 for planned primary system maintenance. On February 9, the unit was taken critical at 1910 hours0.0221 days <br />0.531 hours <br />0.00316 weeks <br />7.26755e-4 months <br /> then continued to Mode 1 operation on the same day.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity (Reactor-R)

1R01 Adverse Weather Protection

a. Inspection Scope

During the week of February 26, the inspectors verified the status of licensee actions in accordance with licensee off-normal procedure 0-ONOP-103.2, Cold/Hot Weather Conditions. This was the annual review of cold weather verification and included physical walkdowns of the following plant areas to check for any specific cold weather vulnerabilities and reviews of operator actions used to mitigate cold weather. The inspectors checked technical specifications and the Updated Final Safety Analysis Report (UFSAR) for cold weather design features and monitored the periodic testing of the diesel driven instrument air compressors during lower temperature weather.

Although the licensee had initiated cold weather mitigation using the ONOP, there were no actual cold weather conditions at the site.

  • Unit 3 charging pump room
  • Unit 4 charging pump room

b. Findings

No findings of significance were identified.

1R02 Evaluations of Changes, Tests, or Experiments

a. Inspection Scope

The inspectors reviewed selected samples of evaluations to confirm that the licensee had appropriately considered the conditions under which changes to the facility, UFSAR, or procedures may be made, and tests conducted, without prior NRC approval. The inspectors reviewed evaluations for eight changes and additional information, such as calculations, supporting analyses, the UFSAR, and drawings to confirm that the licensee had appropriately concluded that the changes could be accomplished without obtaining a license amendment. The eight evaluations reviewed are listed in the Attachment.

The inspectors also reviewed samples of changes for which the licensee had determined that evaluations were not required, to confirm that the licensees conclusions to screen out these changes were correct and consistent with 10CFR50.59. The sixteen screened out changes reviewed are listed in the Attachment.

The inspector also reviewed programmatic Condition Reports (CRs) to confirm that problems were identified at an appropriate threshold, were entered into the corrective action process, and appropriate corrective actions had been initiated.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

1. Partial Equipment Walkdowns

a. Inspection Scope

The inspectors conducted partial alignment verifications of the three safety-related systems listed below. These inspections included reviews using plant lineup procedures, operating procedures, and piping and instrumentation drawings, which were compared with observed equipment configurations to verify that the critical portions of the operable systems were correctly aligned.

  • Unit 4, high head safety injection during 4A safety injection pump planned maintenance per work order 35020536-01. The walkdown was done using licensee procedure 4-OP-62, Safety Injection System.
  • Unit 3, Intake cooling water during planned replacement of the 3C intake cooling water pump per work order 35030563. The walkdown was done using licensee procedure 3-OP-019, Intake Cooling Water System.
  • Unit 3, Auxiliary feedwater system during repair of controller HIC-3-14578B, as documented in CR 2007-6555. The walkdown was done using licensee procedure 3-OP-075, Auxiliary Feedwater System.

b. Findings

No findings of significance were identified.

.2 Complete System Walkdown

a. Inspection Scope

The inspectors conducted a detailed walkdown/review of the alignment and condition of the Unit 3 Residual Heat Removal System to meet the requirements for low head safety injection and coolant recirculation should automatic safety injection be required. The inspectors utilized licensee procedure 3-OP-050, Residual Heat Removal System, and drawings 5613-M-3050 (Residual Heat Removal System) and 5613-M-3062 (Safety Injection System), as well as other licensing and design documents, when verifying that the system alignment was correct. During the walkdown, the inspectors verified, as appropriate, that:

(1) valves were correctly positioned and did not exhibit leakage that would impact the function of any valve;
(2) electrical power was available as required;
(3) major portions of the system and components were correctly labeled, cooled, and ventilated;
(4) selected hangers and supports were correctly installed and functional; (5)essential support systems were operational;
(6) ancillary equipment or debris did not interfere with system performance;
(7) tagging clearances were appropriate; and (8)valves were locked as required by the Turkey Point locked valve program. Pending design and equipment issues were reviewed to determine if the identified deficiencies significantly impacted the systems functions. The system health report for system 50, Residual Heat Removal; was used in the review. In addition, the inspectors reviewed the licensees corrective action program to ensure that the licensee was identifying and resolving equipment alignment problems.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors toured the following nine plant areas during this inspection period to evaluate conditions related to control of transient combustibles and ignition sources, the material condition and operational status of fire protection systems including fire barriers used to prevent fire damage or fire propagation. The inspectors reviewed these activities using provisions in the licensees Procedure 0-ADM-016, Fire Protection Plan, and 10 CFR Part 50, Appendix R. The licensees fire impairment lists, updated on a daily basis were routinely reviewed. In addition, the inspectors reviewed the condition report database to verify that fire protection problems were being identified and appropriately resolved. The following areas were inspected:

  • Unit 3 and Unit 4 spent fuel pool pump and heat exchanger rooms
  • Unit 4 125 VDC battery rooms
  • Unit 4 Inverter room
  • Main control room
  • Unit 4 charging pump room

b. Findings

No findings of significance were identified.

.2 Annual Fire Drill

a. Inspection Scope

On January 12, 2007, the inspectors observed the licensee fire brigade respond to a simulated fire involving a hydrogen explosion at the Unit 3 turbine exciter. The inspectors verified that the drill was administered in accordance with licensee procedures FPAD-010, Fire Brigade and Mutual Aid Drill Scenario Development and 0-ONOP-016.10, Pre-Fire Plan Guidelines and Safe Shutdown Manual Actions. The inspectors checked the brigades communications, ability to set-up and execute fire operations, and their use of fire fighting equipment. The inspectors observed the implementation of 0-EPIP-20101, Duties of the Emergency Coordinator, in determining the Alert Emergency Action Level (EAL) classification for this drill. The inspectors checked CR 2007-1346 that was written for inconsistent emergency classifications when the drill was run with differing crews. The inspectors verified that the licensee consider the aspects as described below, when the brigade conducted the firefighting activities and during the post-drill critique. The inspectors checked that licensee personnel documented drill observations in CR 2007-953.

  • The brigade, including the fire brigade leader, consisted of five team members.
  • The team members acquired and donned the appropriate turnout gear.
  • Self contained breathing apparatus (SCBA) were available and properly used.
  • SCBA program evaluated for proper storage, training, expectations for use, and maintenance.
  • Control Room personnel verified and announced the fire location. The fire alarm was sounded and fire brigade personnel were dispatched.
  • Fire brigade leader maintained control. Members were briefed (including potential hazards), discussed plan of attack, received individual assignments, and performed communications checks.
  • Fire brigade arrived at the scene in a timely manner, taking the appropriate access route specified in the strategies and procedures.
  • Command and control was established near the fire location. Communications were established with the control room personnel.
  • Communications were efficient and effective between the control room, command post, plant operators and fire brigade members.
  • Fire hose lines were capable of reaching the fire area, the lines were laid out without flow restrictions and were simulated as being charged. Use of additional fire equipment (i.e., monitor water canon, foam cart) was simulated.
  • The fire area was entered in a controlled manner using the two person rule.
  • The fire brigade arrived with sufficient fire fighting equipment to perform its fire fighting duties.
  • The fire brigade checked for fire victims and propagation into other plant areas.
  • The drill scenario was followed and the drill acceptance criteria were met.
  • A post-drill critique was held to identify strengths and weaknesses.
  • All fire-fighting equipment associated with the drill was returned to a state of readiness following completion of the drill.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

On January 14, 2007, the inspectors observed and assessed licensed operator training activities in the plant specific simulator to verify that operator performance was adequate and that evaluators were identifying and documenting crew performance problems. The simulated events were done per Scenario 750006501, which involved a reactor coolant system leak followed by a total loss of AC power. The inspectors observed the operators use of procedures 3-EOP-E-0, Reactor Trip and Safety Injection, 3-ECA-0.0, Loss of All AC Power, 3-ONOP-041.3, Excessive Reactor Coolant System Leakage, and 3-ONOP-100, Fast Load Reduction. Event classifications (including Unusual Event, Alert, and Site Area Emergency) were checked for proper classification using licensee procedure 0-EPIP-20101, Duties of the Emergency Coordinator. The licensees management observation 2007-1245 was reviewed. The simulator board configurations were compared with actual plant control board configurations including recent modifications. The inspectors specifically evaluated the following attributes related to operating crew performance:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of off-normal and emergency operation procedures
  • Control board operation and manipulation, including high-risk operator actions
  • Oversight and direction provided by supervision, including ability to identify and implement appropriate technical specification actions, regulatory reporting requirements, and emergency plan classification and notification
  • Crew overall performance and interactions

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the following two equipment problems and associated condition reports to verify that the licensees maintenance efforts met the requirements of 10 CFR 50.65 (Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants) and Administrative Procedure 0-ADM-728, Maintenance Rule Implementation.

The inspectors efforts focused on maintenance rule scoping, characterization of maintenance problems and failed components, risk significance, determination of (a)(1)classification, corrective actions, and the appropriateness of established performance goals and monitoring criteria. The inspectors also interviewed responsible engineers and observed corrective maintenance activities. Furthermore, the inspectors verified that equipment problems were being identified and entered into the corrective action program.

  • CR 2005-16678, 3A high head safety injection pump failed to develop 300 gpm flow during surveillance testing, Unit 3 System Health Report 2006-4, for system 62, Safety Injection was reviewed.
  • CR 2006-13427, Unit 3 pressurizer high pressure reactor trip comparator outside of acceptance criteria, Unit 3 System Health Report 2006-4 for system 63, Engineering Safety Feature Actuation System (ESFAS) was reviewed.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors completed in-office reviews and control room inspections of the licensees risk assessment of six emergent or planned maintenance activities. The inspectors compared the licensees risk assessment and risk management activities against the requirements of 10 CFR 50.65(a)(4) and the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3. Implementation of licensee procedures 0-ADM-068, Work Week Management; and O-ADM-225, On Line Risk Assessment and Management were also verified. The inspectors reviewed the effectiveness of the licensees contingency actions to mitigate increased risk resulting from the degraded equipment. The inspectors evaluated the following risk assessments during the inspection:

  • January 4, 2007 risk assessment for failure of LT-4-495, Unit 4 steam generator C narrow range level. CR 2007-240.
  • January 24, 2007 risk assessment for PT 3-496, Unit 3, C S/G pressure transmitter failure. Bi-stables tripped within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. CR 2007-1970.
  • February 1, 2007 risk assessment for failure of SV-4-2906, Unit 4 ECF spray solenoid valve, failure to close. CR 2007-3082.
  • February 7, 2007, risk assessment for removal of 3A intake cooling water pump when 3D 4160 volt bus was aligned to 3A bus. Prior to start of work, the 3D bus was realigned to the 3B bus.
  • March 23, 2007, risk assessment during load reject testing of Unit 5.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed six interim disposition and operability determinations associated with the following condition reports to ensure that Technical Specification operability was properly supported and the system, structure or component remained available to perform its safety function with no unrecognized increase in risk. The inspectors reviewed the UFSAR, applicable supporting documents and procedures, and interviewed plant personnel to assess the adequacy of the interim condition report disposition.

  • CR 2007-738, Unit 4 AFW steam piping below minimum nominal acceptance criteria at hanger 80117-H-334-15.
  • CR 2005-16678, 3A high head safety injection pump failed to develop 300 gpm flow during surveillance testing, Unit 3 System Health Report 2006-4, for system 62, Safety Injection was reviewed.
  • CR 2007-1339, Latent error in ICW pump net positive suction head calculation due to low intake level. The final safety analysis report and a Sulzer pump evaluation and operability assessment were reviewed.
  • CR 2007-2312, cracks on actuator yoke for 3-50-344, 3B ICW Basket Strainer Inlet Valve. FPL calculation PTN-BFSM-02-006, Rev.0 was reviewed.
  • CR 2007-3932, potential operability issue with 125VDC battery charger supply breakers. In-rush current traces for 3A2 battery charger used along with FSAR Section 8 were reviewed.
  • CR 2007-7246, shunt trip time exceeded acceptance criteria during reactor protection testing. Drawing 5613-M-430-146, sheet 6A was used.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

a. Inspection Scope

The inspectors evaluated design change packages for nine modifications, in the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstone areas, to evaluate the modifications for adverse effects on system availability, reliability, and functional capability. The modifications and the associated attributes reviewed are as follows:

PTN-ENG-SEMS-05-058, Revised Maintenance Intervals of Selected Mechanical Tasks from 24 Months to 48 Months Based on Revisions to the ESI-EMD Owners Group Maintenance Program into Units 3 & 4 Emergency Diesel Generators Maintenance Program (Mitigating Systems)

  • Materials/Replacement Components
  • Structural
  • Process Medium
  • Failure Modes PTN-ENG-SEMS-06-007, Engineering Evaluation for Modified #3 RCP Seal Design (Initiating Events)
  • Pressure Boundary
  • Energy Needs
  • Materials/Replacements Components
  • Process Medium
  • Licensing Basis PCM 05-125, CCW Pump Modification Package for Seal Design Change, Bearing Design Change and Pump Casing Vent Modification (Mitigating Systems)
  • Pressure Boundary
  • Structural
  • Materials/Replacement Components
  • Process Medium
  • Timing
  • Process Medium
  • Licensing Basis
  • Failure Modes PTN-ENC-SENS-05-008, 10 CFR 50.59 Evaluation for Potential Flooding of the Unit 3 Diesel Oil Storage Tank Area Due to Oil Pollution Control Modification; PCM 04-036, Modification for 3P10A (Mitigating Systems)
  • Energy Needs
  • Timing
  • Control Signals
  • Process Medium
  • Licensing Basis
  • Energy Needs
  • Material/Replacement Components
  • Control Signals
  • Process Medium
  • Post-Modification Test
  • Vendor Information
  • Walkdown PC/M 05-059,Core Exit Thermocouple Replacement Via In-core System Flux Thimbles at Location H1 and M3 (Barrier Integrity)
  • Control Signals
  • Pressure Boundary
  • Post-Modification Test
  • Flowpaths For selected modification packages, the inspectors observed the as-built configuration.

Documents reviewed included procedures, engineering calculations, modification design and implementation packages, work orders, site drawings, corrective action documents, applicable sections of the living UFSAR, supporting analyses, Technical Specifications, and design basis information.

The inspectors also reviewed selected CRs associated with modifications to confirm that problems were identified at an appropriate threshold, were entered into the corrective action process, and appropriate corrective actions had been initiated.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

For the six post maintenance tests listed below, the inspectors reviewed the test procedures and either witnessed the testing and/or reviewed test records to determine whether the scope of testing adequately verified that the work performed was correctly completed and demonstrated that the affected equipment was functional and operable.

The inspectors verified that the requirements of Procedure 0-ADM-737, Post Maintenance Testing, were incorporated into test requirements. The inspectors reviewed the following work orders (WO) and/or surveillance procedures (OSP):

  • Unit 4, WO 35020536-01, repair inboard seal leak on vent plug for 4A high head safety injection pump
  • Unit 4, WO 35024519-01, Replace 4P9B, intake cooling water pump 4B, tested using 4-OSP-019.1, Intake Cooling Water Inservice Test

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

.1 Unit 4 Outage

For the Unit 4 short duration Mode 3 outage that started on February 7, the inspectors evaluated licensee activities to verify the licensee considered risk in developing outage schedules, adhered to administrative risk reduction methodologies when changing plant configuration, and adhered to operating license and Technical Specification requirements that maintained defense-in-depth. The inspectors reviewed outage activities to verify that risk management strategies were implemented, including availability of safety systems, reactivity management, and containment control. The inspectors conducted a thorough walkdown of containment to check for evidence of leakage and to verify that controls were properly implemented to maintain operability of the containment including the recirculation sump. The inspectors reviewed activities during reactor restart and power escalation to verify that reactor parameters were within safety limits and that the startup evolutions were done in accordance with pre-approved procedures and plans. The inspectors verified that outage items had been entered into the licensees corrective action program at an appropriate threshold.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors either reviewed or witnessed the following seven surveillance tests to verify that the tests met the Technical Specifications, the UFSAR, the licensees procedural requirements and demonstrated the systems were capable of performing their intended safety functions and their operational readiness. In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing activities, equipment was returned to the positions/status required for the system to perform its safety function. The tests reviewed included one inservice test (IST) and one reactor coolant system leak rate determination.

  • 3-OSP-028.6, Rod Cluster Control Assembly Periodic Exercise
  • Unit 3 and 4 Test Procedure 06-041, 35-Year Containment Concrete and Tendon Inspection (observed lift test of tendon 51H35, buttress 5 end)
  • 0-OSP-062.2, Safety Injection System Inservice Test (IST)

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the Temporary System Alteration (TSA) listed below to ensure that it did not adversely affect the operation of the system. The inspectors screened temporary plant modifications for systems that were ranked high in risk for departures from design basis and for inadvertent changes that could challenge the systems to fulfill their safety function. Testing of the modification was checked for any unintended impacts. Condition reports 2006-25890 and 2006-34040 were reviewed by the inspectors. The inspectors conducted plant tours and discussed system status with engineering and operations personnel to check for the existence of temporary modifications that had not been appropriately identified and evaluated.

  • TSA 03-06-041-015, 3B QSPDS Cold Leg C resistance temperature detector, TE-3-430B failure.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

.1 Barrier Integrity

a. Inspection Scope

The inspectors checked licensee submittals for the two performance indicators (PIs)listed below for the period January 1, 2006 through December 31, 2006, to verify the accuracy of the PI data reported during that period. Performance indicator definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 4, were used to check the reporting for each data element. The inspector checked, operator logs and chemistry department analysis data to verify that the licensee had identified and reported the proper values for reactor activity and leakage, as applicable. In addition, the inspectors observed chemistry personnel obtain and analyze primary coolant samples from both reactor units. The inspectors checked that deficiencies affecting the licensees performance indicator program were entered into the corrective action program.

Barrier Integrity Cornerstone

b. Findings

No findings of significance were identified.

4OA2 Problem Identification and Resolution

.1 Daily Review

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of items entered daily into the licensees corrective action program. This review was accomplished by reviewing daily printed summaries of condition reports and by reviewing the licensees electronic condition report database. Additionally, reactor coolant system unidentified leakage was routinely checked to verify no substantive or unexplained changes.

b. Findings

No findings of significance were identified

.2 Annual Sample Review

a. Inspection Scope

The inspectors selected the following CR for detailed review and discussion with the licensee. The condition report was reviewed to ensure that an appropriate evaluation was performed and appropriate corrective actions were specified and prioritized. Other attributes checked included disposition of operability, resolution of the problem including cause determination and corrective actions. The inspectors evaluated the CR in accordance with the requirements of the licensees corrective actions process as specified in NAP-204, Condition Reporting.

  • CR 2006-20498 3A2 Battery charger maintenance procedure needs to be revised to reflect proper shunt.

b. Findings

No findings of significance were identified.

4OA3 Event Followup

.1 (Closed) Licensee Event Report 0500250/2006-002-01: As-Found Cycle 21 Main Steam

Safety Valve Setpoints Outside Technical Specification Limits On March 5, 2006, the licensee identified that two of the twelve Unit 3 main steam safety valves (MSSVs) were found with lift setpoints above their Technical Specification Table 3.7-2 limit of + 3 percent. The two valves were declared inoperable and the test failures were documented in CR 2006-6537 and CR 2006-6522. In the LER supplement, the licensee reported that the cause for the setpoint drift was minor corrosion or micro-bonding of the valve inner components. The corrosion or micro-bonding is a known industry issue and is repetitive at Turkey Point. The licensee took interim actions to set and retest the valves, and long term actions to prevent recurrence were planned. The licensee evaluated the safety valve capability and determined using test data that the twelve MSSVs were capable of providing steam generator overpressure protection. This finding is more than minor because the reliability of valves used to mitigate certain events (over-pressure transients) was affected. The finding affects the Mitigating Systems cornerstone and was considered to have very low safety significance having screened as Green using NRC Manual Chapter 0609.

Appendix A, Attachment 1 because no actual loss of safety function occurred due to redundant safety valves which assured adequate over-pressure protection. This licensee identified finding involved a violation of Technical Specification 3.7.1.1, Safety Valves. The enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed.

.2 (Closed) Licensee Event Report 0500250&251/2006-008-00: Incorrect Emergency

Diesel Fuel Oil Testing Program Surveillance Implementation On November 1, 2006, the licensee identified that their fuel oil testing did not check for proper color of fuel oil prior to adding fuel to the plant storage tanks. Although the licensee did a visual check of new fuel oil for sediment and water, a color verification using a colorimeter was not included in the licensees sampling program. The inspector verified that oil samples were tested in the laboratory for water and sediment, which is a redundant test, and only good fuel oil was placed in the plant storage tanks. The licensee identified the cause to be a failure to implement specific test requirements of the American Society for Testing and Materials (ASTM) standards, a lack of technical rigor, and insufficiently detailed procedures. The inspector checked the condition report and verified that licensee procedure 0-NCAP-015.4, Fuel Oil Clear and Bright Determination, had been revised to include the proper color testing. The inspector verified that a February 20, 2007 fuel oil shipment had been appropriately tested for color. Additionally, the inspector checked that the technical specification basis document had been revised to reference ASTM D1500-82 as the standard for fuel oil testing for color. No new findings were identified in the inspectors review. The finding constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section VI of the NRC Enforcement Policy. The licensee documented the issue in the corrective action program as CR 2006-31637. This LER is closed.

4OA5 Other

.1 Inspector Review of WANO Report

a. Inspection Scope

The inspectors reviewed the final report for the World Association of Nuclear Operators (WANO) plant assessment of Turkey Point Nuclear Power Plant conducted in July 2006.

The inspectors reviewed the report to ensure that issues identified were consistent with NRC perspectives of licensee performance and to verify if any significant safety issues were identified that required further NRC follow-up.

b. Findings

No findings of significance were identified

.2 (Closed) Temporary Instruction 2515/167, Assurance of Industry Implementation of Key

Shutdown Voluntary Initiatives

a. Inspection Scope

Between January 16-19, 2007, the inspectors confirmed through personnel interviews and document reviews that the licensee was continuing to implement the voluntary initiatives described in NUMARC 91-06, Guidelines for Industry Actions to Assess Shutdown Management, and the commitments contained in letters dated January 3, 1989 and February 1, 1989 responding to Generic Letter 88-17, Loss of Decay Heat Removal. This confirmation was based upon the Fall 2006 Refueling Outage. The inspectors focused on three broad areas. These were:

  • How the five key safety functions defined in NUMARC 91-06 were administratively controlled throughout plant shutdown (Modes 5 & 6) and with the core off-loaded into the spent fuel pool.
  • How the outage schedule is established and how changes, planned or emergent, are evaluated as they relate to 10 CFR 50.65(a)(4).

b. Findings

No findings of significance were identified.

4OA6 Exit

1.

Exit Meeting Summary

The resident inspectors presented the inspection results to Mr. Jefferson and other members of licensee management on April 10, 2007. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. The licensee did not identify any proprietary information.

.2 Annual Assessment Meeting Summary

On April 17, 2007, the Branch Chief and the NRCs resident staff assigned to the Turkey Point Nuclear Plant, as well as the Region II Public Affairs Officer, met with Florida Power and Light Co. (FP&L) to discuss the NRCs Reactor Oversight Process (ROP)and the Turkey Point annual assessment of safety performance for the period of January 1, 2006 - December 31, 2006. The major topics addressed were: the NRC s assessment program, the results of the Turkey Point Units 3 and 4 assessment, and future NRC inspection activities. Attendees included FP&L management and site staff.

No members of the public or news reporters were at the meeting.

This meeting was open to the public. The NRCs presentation material used for the discussion is available from the NRCs document system (ADAMS) as accession number ML071090097. The licensee did not have a handout presented at the meeting.

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (The Public Electronic Reading Room).

4OA7 Licensee Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

  • Turkey Point Technical Specification 3.7.1.1 requires all main steam code safety valves associated with each steam generator to be operable with lift settings as specified in Table 3.7-2 (of the TS). With one main steam line safety valve (in a generator) inoperable, in Mode 1, operation may continue provided that within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, reactor power shall be reduced to less than the maximum allowed of 53 percent of rated power. Contrary to the above, during Mode 1 operation prior to March 5, 2006, Turkey Point Unit 3 operated at greater than the maximum allowed power with a main steam safety valve inoperable due to having a higher than allowed lift pressure. When identified by the licensee during valve testing on March 5, power had been reduced to less than 50 percent, the valve setpoints were adjusted to within acceptable limits, and the issue was entered into the corrective action program. The finding is of very low safety significance because redundant safety valves assured that overpressure transients would be mitigated.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

J. Antignano, Fire Protection Supervisor
W. Burrows, Acting Maintenance Manager
J. Connolly, Acting Licensing Manager
S. Greenlee, Engineering Manager
D. Hoffman, Operations Superintendent
W. Jefferson, Site Vice-President
M. Moore, Corrective Actions Supervisor
M. Murray, Emergency Preparedness Supervisor
J. Molden, Operations Manager
K. OHare, Radiation Protection and Safety Manager
M. Pearce, Plant General Manager
W. Pravat, Work Controls Manager
J. Stall, Sr. Vice President, Chief Nuclear Officer
G. Warriner, Quality Manager
B. Webster, Senior Vice President, Operations

NRC personnel

NRC Commissioner J. Merrifield

V. McCree, Region II Deputy Regional Administrator
M. Ernstes, Chief, Branch 3, Division of Reactor Projects
J. Shea, Director, Division of Reactor Safety

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Closed

0500250/2006-002-01 LER As-Found Cycle 21 Main Steam Safety Valve Setpoints Outside Technical Specification Limits 0500250&251/2006-08-00 LER Incorrect Emergency Diesel Fuel Oil Testing Program Surveillance Implementation Temporary Instruction 2515/167 Assurance of Industry Implementation of Key Shutdown Voluntary Initiatives

LIST OF DOCUMENTS REVIEWED