ML20217L831

From kanterella
Jump to navigation Jump to search
Insp Rept 50-443/98-01 on 980201-0328.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support
ML20217L831
Person / Time
Site: Seabrook NextEra Energy icon.png
Issue date: 04/27/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20217L038 List:
References
50-443-98-01, 50-443-98-1, NUDOCS 9805040311
Download: ML20217L831 (25)


See also: IR 05000443/1998001

Text

.

~

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No.: 50-443

License No.: NPF-86

Report No.: 50-443/98-01

Licensee: North Atlantic Energy Service Corporation

Facility: Seabrook Generating Stetion, Unit 1

Location: Post Office Box 300

Seabrook, New Hampshire 03874

Dates: February 1,1998 - March 28,1998

Inspectors: Ray K. Lorson, Senior Resident inspector

Javier Brand, Resident inspector

Robert Summers, Project Engineer

Approved by: Curtis J. Cowgill, Chief, Projects Branch 5

Division of Reactor Projects

,

cP8050403tt H30427

PDR ADOCK 0 4j3

G

.

.

EXECUTIVE SUMMARY

Seabrook Generating Station, Unit 1

NRC Inspection Report 50-443/98-01

This inspection included aspects of licensee operations, engineering, maintenance, and

plant support. The report covers a 9-week period of resident inspection.

= Ooerations:

e The licensee had a method for evaluating spent fuel pool (SFP) liner integrity based

on the SFP sump in-leakage. However, in one instance licensee personnel did not

identify that the SFP sump level alarm was non-functional which precluded use of

this redundant method for monitoring the spent fuel pool liner integrity.

'o The inspectors noted good operator performance during motor driven emergency

.

feedwater pump (EFW) testing and during venting of the emergency core cooling -

system (ECCS) discharge piping. The operators performed these activities in q

accordance with the applicable procedures and demonstrated an excellent

questioning attitude,

e .The safety system walkdowns were a positive initiative to improve the plant I

material condition. l

Maintenance:

e An electrician demonstrated excellent attention to detail and a questioning attitude,

to detect and identify the incorrect installation of two operating mechanism springs

on a safety-related breaker. The licensee determined that this condition did not

render the breaker (or any other similar breakers used at Seabrook) inoperable, and

initiated a plan to inspect and correct any additional non-conforming conditions prior

to the end of the next refueling outage.

e The licensee performed the planned freeze seal activities well. The work package,

and associated on-line maintenance and freeze seal evaluations, and management

oversight were effective. The inspector identified that the level of detail provided in

the freeze seal thawing instructions could have been enhanced. The licensee

promptly enhanced the work instructions to address this' concern.

e Safety-related degraded voltage bus testing was performed well, and the test

results satisfied technical specification requirements.'

e The licensee reported several examples of failure to develop adequa:e surveillance

test procedures. The licensee subsequently revised the test procecures and

properly tested each component. This licensee identified violation of failure to

ii

4 , ,

.. . . .. . . . . . . . .

.

,

..

.

'

develop adequate test procedures is being treated as a non-cited violation. (NCV

98-01-01)

Enaineerina;

o The licensee failed to implement adequate design controls to ensure that the safety-

related components within the residual heat removal system pump room would

remain within their required temperature limits prior to modifying the room

ventilation system. A subsequent licensee analysis, performed after the NRC

identified this deficiency, indicated that the modification reduced the room

ventilation flow by about 50%, however, the room temperature limits would not

have been exceeded. This is a violation of 10 CFR 50, Appendix B Criterion lli

(NOV 98-01-02)-

o The licensee promptly reviewed and evaluated the identification of boric acid

accumulation on a RHR drain line. The identification of this condition reflected

positively on the licensee's new system walkdown program. The inspector noted

that the licensee's response to this condition did not include identification of the

- other plant areas potentially susceptible to periodic wetting. The licensee

l implemented appropriate actions to address this concern.

e Operations personnel performed well by identifying the safety injection accumulator

l-

L nitrogen leaks. The licensee promptly investigated the leakage and implemented

j appropriate repairs to reduce the leakage. Engineering properly assessed the impact

l of this minor leakage on the accumulatcr operability.

i

e The licensee determined that incorrectly installed coupling hubs (a condition which

occurred during initial installation), caused a degraded EFW motor outboard bearing

condition. The pump remained operable in this condition and the licensee

implemented appropriate corrective actions to address this deficiency.

Plant Suooort:

,

e ' The inspector that identified four workers were performing maintenance on the "B"

I

containment spray pump in a posted as a contaminated area without wearing any

'

protective clothing as required by the radiation work permit and posted

instructions. 'The licensee promptly evaluated this issue and implemented adequate

corrective actions. This is a violation of Technical Specification 6.10.1. (NOV 98-

01-03)-

iii

.

TABLE OF CONTENTS

EAGA

EX EC UTIV E SU M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii

TA8LE OF CONTENTS .............................................. iv

l . Ope ratio n s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 ,

02 Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . . 1

02.1 Safety System Walkdowns and Status . . . . . . . . . . . . . . . . . . . . 1

04 Operator Knowledge and Performance .........................2 l

04.1 Operator Performance During Surveillance Testing . . . . . . . . . . . . 2

04.2 Spent Fuel Pool Liner integrity Monitoring . . . . . . . . . . . . . . . . . . 2 .l

08 Miscellaneous Operations issues (92901) . . . . . . . . . . . . . . . . . . . . . . . 3 i

08.1 (Closed) Unresolved item 50-443/97-06-01 . . . . . . . . . . . . . . . . . 3

II . Mainte na nce . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

M1 Conduct of Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

M1.1 incorrect Spring Location on Safety Related Breakers . . . . . . . . . . 5

M1.2 Freeze Seal to Support Repair.of a Chemical and Volume Control

Valve...........................................6

M1.3 Safety Bus Degraded Voltage Surveillance Testing . . . . . . . . . . . . 7

M8 Miscellaneous Maintenance issues (92902) . . . . . . . . . . . . . . . . . . . . . . 7

M8.1 (Closed) Violation 50-443/96-04-01 . . . . . . . . . . . . . . . . . . . . . . 7

M8.2 Licensee Event Report Review: .........................7

Ill. Engineering ...................................................8

E1 Conduct of Engineering (37751) ..........,..................8-

E1.1 Residual Heat Removal System Ventilation Covers . . . . . . . . . . . . 8

E2 Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . . 10

E2.1 Accumulation of Boron on Residual Heat Removal System (RHR) Drain

Pipe Connection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

E2.2 Nitrogen Leak Of Safety injection Accumulators Supply Header . . 11

E2.3 Degraded Emergency Feedwater Motor Outboard Bearing, and

(Update) of Unresolved item 9 7-08-0 5 . . . . . . . . . . . . . . . . . . . 12 1

E8 Miscellaneous Engineering issues (92903) . . . . . . . . . . . . . . . . . . . . . . 13 l

E8.1 (Closed) Violation 50-443/96-08-01 . . . . . . . . . . . . . . . . . . . . . 13

E8.2 (Closed) Unresolved item (URI) 9 7-07-0 3, . . . . . . . . . . . . . . . . . 13

E8.3 (Closed) Escalated Enforcement issues (EEI) 97-08-02, 97-08-03, 97- ,

08-04, and 97-08-06. ..................... ........ 13 l

l

IV. Plant Support ................................................14

R1 Radiological Protection and Chemistry Controls . . . . . . . . . . . . . . . . . . 14

iv

.

R1.1 Maintenance Work In Posted Contaminated Area Without Protective

Clothing

..............................................14

S1 Conduct of Security and Safeguards Activities . . . . . . . . . . . . . . . . . . . 16

S1.1 General Comment (71707, 71750) . . . . . . . . . . . . . . . . . . . . . . 16

F8 Miscellaneous Fire Protection Issues (92904) . . . . . . . . . . . . . . . . . . . . 16

F8.1 (Closed) Violation 50-443/96-03-01 . . . . . . . . . . . . . . . . . . . . . 16

F8.2 (Closed) Violation 50-443/96-03-02 . . . . . . . . . . . . . . . . . . . . . 16

V. Management Meetings ..........................................17

X1 Exit Meeting Summary . . . . . . .. . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

X3 Other NRC Activities ....................................17

PARTIAL LIST OF PERSONS CONTACTED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

INSPECTION PROCEDU RES USED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

LIST OF ACRONYMS U SED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

l

l

v

.

.

Report Details

Summarv of Plant Stglug

The facility operated at approximately 100% of rated thermal power throughout the

inspection period with routine minor power reductions performed to support instrument

calibrations and testing.

1. Operations

01 Conduct of Operations

Using inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. In general, routine operations were performed in  ;

'

accordance with station procedures and plant evolutions were completed in a

deliberate manner with clear communications and effective oversight by shift

supervision. Control room logs accurately reflected plant activities, and observed

shift turnovers were comprehensive and thoroughly addressed questions posed by

l

the oncoming crew. Control room operators displayed good questioning ~l

l perspectives prior to releasing work activities for field implementation. The

inspectors found that operators were knowledgeable of plant and system status.

'

02 Operational Status of Facilities and Equipment

02.1 Safety System Walkdowns and Status (71707. and 62707)  ;

}

l

_ The inspectors routinely conducted independent plant tours and equipment

walkdowns of selected portions of the primary auxiliary building, emergency diesel

generator, service water, and emergency feedwater buildings. These activities ,

consisted of verification that safety-related system configurations, power supplies, j

process parameters, support systems, and operational status were consistent with  !

Technical Specification (TS) requirements, and the Updated Final Safety Analysis

Report (UFSAR) descriptions. Additionally, system, component, and general area

material conditions and housekeeping status were observed.

The inspectors observed a significant increase in the number of equipment

daficiency tags hung on safety system components during the systematic licensee

walkdowns. The inspectors reviewed selected deficiency tags and noted that the I

deficiencies identified minor system defects that did not present any operability

concerns. The inspectors concluded that the system walkdowns were a positive

licensee initiative to _ improve the plant material condition and will continue to follow  ;

licensee progress in this area.  !

l

.

.

2

04 Operator Knowledge and Performance

04.1 Operator Performance Durina Surveillance Testina

The inspectors noted good operator performance during motor driven emergency 1

feedwater pump (EFW) testing and during venting of the emergency core cooling

system (ECCS) discharge piping. The operators performed these activities in

accordance with the applicable procedures and demonstrated an excellent

questioning attitude.

The operators noted, while venting the ECCS discharge piping per operating

procedure, OX1456.02, "ECCS Monthly Valve Verification", that the procedure

acceptance criteria of "no gas observed" was not satisfied. Engineering determined

that the small bubbles were due to expansion of dissolved nitrogen in the water

during the. venting process and revised thc procedure to clarify the acceptance

criteria. The operators subsequently performed the venting activity satisfactory.

The inspectors obrerved that the EFW surveillance test procedures did not provide

i clear acceptance limits for venting the pump recirculation line. The in_spectors

discussed this issue with station management who agreed to review this procedure.

The inspectors concluded overall good operator performance during motor driven

l EFW pump testing and during venting of the ECCS discharge piping. The operators

performed these activities in accordance with the applicable procedures and

demonstrated an excellent questioning attitude.

04.2 Soent Fuel Pool Liner Intearity Monitorina

l-

a. Inspection Scooe

The inspectors reviewed the licensee's method for utilizing the spent fuel pool (SFP)

system sump to evaluate the SFP liner integrity, and also the basis for concluding

that identified leakage out of two SFP sump leak detection pipes was groundwater.

b. Observations and Findinas

"

The SFP sump was designed to collect any leakage from the SFP liner. Seabrook

USAR Section 9.1.2.2 states, in part, that, "The SFP is monitored for leakage by a

series of leak detection channels located adjacent to each liner seam weld," and "by

monitoring the leakege rate, any change in the integrity of the liner can be

established." The inspector noted that this method of monitoring SFP liner integrity

was independent to SFP level indication system.

A deficiency tag, dated February 20,1998, stated that "two spent fuel pool leak

detection pipes have groundwater leaking." The inspector reviewed the applicable

system drawing and confirmed that the two potential leakage sources included:

I

.

'

3

groundwater and the spent fuel pool. The inspector questioned operations -

personnel and the system engineer regarding the basis for concluding that this

leakage was groundwater and learned that chemistry personnel had analyzed the

sump contents and determined that the leakage was not SFP water. The inspector

concluded that the licensee had properly evaluated this leakage.

1

The system engineer indicated that the SFP sump was equipped with a level alarm

set to actuate at one foot of water above the sump floor, and this volume of water

was equivalent to an approximate 0.25 inch decrease in SFP water level. The SFP

sump alarm response procedure required the checking of indications to confirm the i

'

SFP liner integrity. The inspector concluded that the licensee had established a )

method for using SFP sump in-leakage to evaluate the SFP liner condition.

,

The inspector questioned whether the SFP level alarm was functioning properly

however, based on a report from a radiation waste technician that approximately

four feet of water had been recently pumped out of the SFP sump. The licensee

reviewed the alarm database and determined that the SFP sump level alarm had not

actuated since January 1996. The licensee subsequently determined that the alarm

level switch was not functional. The licensee replaced and verified the switch to be

operational. The period of time that the alarm was non-functional was

indeterminate since no data was available regarding the actual sump conditions

during this period of time. The inspector concluded that the recent example where -

the licensee did not identify that the SFP sump alarm failed to actuate demonstrated

a weakness in the identification of degraded equipment. The licensee initiated an

adverse condition report (ACR) to review the program for monitoring the SFP sump.

c. Conclusions

The licensee had a method for monitoring SFP sump in-leakage as an independent

confirmation of the SFP liner integrity, however, in one example, licensee personnel

failed to identify that the SFP sump level alarm was non functional which prevented

use of this method.

08 Miscellaneous Operations issues (92901)

08.1 (Closed) Unresolved item 50-443/97-06-01: review of licensee decision to reduce

power during September 15,1997 feed pump oscillation event. This item refers to

the operational decision to contiriue with a planned power reduction to about 90%

power during the subject event after experiencing a failure of the rod control

system. An abnormal operating procedure for the rod control system required that

power evolutions be stopped when an urgent failure of the rod control system

occurs. At the time of the event the "A" main feed pump governor controls were

oscillating, resulting in associated high pressure steam supply pipe oscillations.

While the operators had determined that this condition did not warrant an

immediate plant trip or shutdown, there was concern about the possible adverse

effect of the oscillations on the equipment. As a result, plans were implemented to

A

.

4

reduce power to either eliminate the oscillations or remove the "A" main feed pump

from service so that repairs could be effected.

When the operators initiated the power reduction a failure in the rod control system

occurred, such that the control rods could not be manually inserted. After

determining that the control rods were still able to perform the plant trip function

and that adequate shutdown margin was available, the decision was made to

continue with the planned power reduction using chemical shim injection (through

the emergency boration flow path). The basis for this decision was that, excepting

the feed pump oscillations, the plant was stable; and, that l&C recommended that a

small change in power may fix the feed pump control problem, or at least reduce

the risk of the oscillations causing equipment damage. The operators were also

briefed at the time that if, during the down power evolution, they believed the plant

was not stable, or if they were excessively challenged, that a plant trip should be

initiated.

As allowed by station procedures, the shift manager (a senior licensed operator)

authorized initiating a 10% power reduction to reduce the feed pump oscillations.

The basis for this decision comes from Station Management Manual Chapter 2,

which permits noncompliance with procedures for very limited conditions involving

either protection of the health and safety of the public, prevention of personnel

injury or life threatening situations, or prevention of damage to major plant

equipment. Operators concluded that the deviation from the abnormal operating

procedure was acceptable in order to avoid possible damage to the main feed

pump, or the associated steam supply pipe and resultant plant transient condition,

i Operators maintained all associated technical specification requirements within

allowable conditions, such as shutdown margin and axial flux difference. The

evolution was well controlled and at about 92 % power, the feed pump oscillations

were significantly reduced, removing the threat to this major plant equipment.

l

in NRC inspection report 50-443/97-06, the inspectors questioned the

appropriateness of the operator actions during the September 15 event. An

unresolved item was issued pending review of the licensee's ACR findings. The

licensee noted that an ACR had not been immediately initiated following the

operator's decision to deviate from the operating procedure. At the time, the

licensee's ACR process did not explicitly require an evaluation for this type of

event. As a result, the licensee subsequently revised the guidance to require that

an ACR be initiated for events where this Station Management Manual guidance

was implemented. The inspectors determined during this current inspection that

the operator actions were taken in accordance with station procedures. This

unresolved item is closed.

!~

1

!

-

.

I g-

5

11. Maintenance

M1 Conduct of Maintenance -

M1~ 1. incorrect Sorina Location on Safety Related Breakers

.

a; inspection Scone:

I

On February 25, during refurbishment of a " spare" 4160 volt breaker, an electrician

identified that two breaker operating mechanism springs had been incorrectly

interchar.ged by the manufacturer (ABB Services Inc.), during a previous breaker

refurbishment. The springs, which included the charging carrier reset spring and 1

the third toggle tension spring, are very similar in appearance, however one of the d

l

springs provides a greater tension force. The inspector evaluated the licensee's  !

response to this issue, reviewed applicable documentation, and met with electrical

engineering personnel. 1

b .- Observations and Findinas:

The licensee disassembled the breaker and the springs were installed as

recommended by the manufacturer. The final configuration was consistent with the

L Seabrook breaker refurbishment . procedure, and the vendor drawing. The vendor

l indicated that originally, these two springs were identical, but in about 1984, the

charging carrier spring had been redesigned to address a concern with their use in a - J

L

different style of breaker, however, the part replacument was effected on several of

the vendor supplied breakers to eliminate duplicity.

The licensee identified approximately 23 other similar ABB breakers (fifteen of

which are currently being used in safety related applications) that may have been

affected by the possible misassembly. The licensee performed an operability l

i

determination based on a vendor supplied analysis, which concluded that

interchanging the two springs did not affect the breaker operability. The vendor

also recommended that the springs be installed in the correct location, and

Seabrook initiated a plan to inspect all breakers and ensure adequate spring

~ installation by the end of the next refueling outage (in 1998).

^

The licensee determined that this issue was not reportable under 10 CFR Part 21, )

" Reporting Defects and Noncompliance", because the breakers were evaluated to

,

remain operable. The vendor initiated testing to demonstrate that the breakers with

the interchanged springs (incorrect spring location) will remain operable for the

entire service life (period of nine years), and is evaluating this issue for Part 21 I

applicability.

1

i

.

.

6

c. Conclusion:

The inspector concluded that a Seabrook electrician demonstrated excellent

attention to detail and a good questioning attitude, to detect and identify the

interchanged installation of two breaker operating mechanism springs on a safety

related 4160 volt breaker. The licensee determined that this condition did not

render the breaker (or any other similar breaker used at Seabrook) inoperable, and

had initiated a plan to inspect and correct the situation prior to the end of the next

refueling outage.

M1.2 Freeze Seal to Sucoort Repair of a Chemical and Volume Control Valve

a. Insoection Scope:

On March 27, the inspector observed pipe freeze seal activities performed by

mechanical maintenance technicians to support inspection and repairs on valve CS-

V-408, which isolates the boric acid transfer pump minimum flow recirculation line.

The inspector reviewed the work package, applicable procedure, interviewed the

system engineer and work supervisor, and visually inspected the activities.

L

L b. Observations and Findinas:

!

The licensee conducted briefings prior to performing the freeze seal. The work

package was thorough and included an adequate on-line maintenance assessment.

Additionally, required precautions, system lineups and contingencies were included

to prevent or mitigate the consequences of a freeze seal failure. The inspector

observed proper field coverage by fire protection, management oversight and health

physics personnel. The system engineer was knowledgeable of the evolutions, and

provided good support. The oversight group performed a liquid penetrant test of

the affected pipe before and after the freeze, which confirmed adequate pipe

conditions.

The inspector noted that the work scope included an infrequently performed activity

to speed up the freeze seal thawing process to ensure that any boron in the pipe

quickly returned to solution. A heat gun with a capacity of 500'F was used, and

~

the inspector noted that the licensee implemented controls which included

continuously monitoring the pipe surface temperature to prevent exceeding a

maximum temperature of 150'F. The inspector noted that the work procedure

instructions could have provided additional guidance to ensure that this infrequently

performed activity was performed correctly. The licensee addressed the inspector's

concerns by implementing a work scope change to include additional guidance. The

freeze seal and subsequent thawing process were completed successfully.

!'

!

>

.

1

i

-

7  !

c. Conclusion:

The licensee performed the planned freeze seal activities well and effective

management oversight and support were observed. The work package and

associated on-line maintenance and freeze seal evaluations were adequate. The

licensee implemented prompt actions to address an inspector concern regarding the

level of detail provided in the work package instructions for controlling the freeze

seal thawing activity.

M1.3 Safety Bus Dearaded Voltaae Surveillance Testina

The inspector observed electrical technicians perform safety-related bus degraded

voltage testing on February 25. The inspector noted that the test activities were

performed safely and in accordance with the test procedures. The inspector

observed good supervisory oversight, communications, and use of self-checking

practices. Measuring and test equipment were calibrated properly, and the

equipment performance satisfied the TSs surveillance requirements.

,

M8 Miscellaneous Maintenance issues (92902)

M8.1 (Closed) Violation 50-443/96-04-01: inoperable turbine driven emergency feedwater

pump as a result of inadequate installation of mechanical seals. The inspector

verified the corrective actions described in the licensee's response letter, dated

August 8,1996, to be reasonable and complete. Among the corrective actions

verified were: revisions to the associated maintenance procedures describing

greater detail for seal clearances and use of calibrated M&TE to verify adequate

clearance; submittal of a supplement to LER 50-443/96-003 to better describe the

root causes of the failure, including the repeat nature of the problem and corrective

actions for that concern; and, changes to the corrective action program to provide

root cause training to the management review team and SORC members, and to

. improve the operational experience feedback process, providing clear guidance for

the types of events requiring a formal root cause analysis. No similar problems

were identified.

M8.2 Licensee Event Reoort Review:

The following licensee event reports (LERs) are closed based on an in-office review

of the LER and the planned and completed corrective actions.

.e (Closed) LER 50-443/96-06-00: Missed Surveillance Requirement -

e (Closed) LER 50-443/97-03-00: Missed Surveillance Turbine Trip on Reactor

Trip

e (Closed) LER 50-443/97-04-00: Remote Shutdown Circuits Control Room

Isolation Function Not Tested Completely

. . . . . . . - .. . . .

..

. . .

.

8 -

e (Closed) LER 50-443/97-017-00: Inadequate SSPS Surveillance Testing

e (Closed) LER 50-443/98-001-00: Inadequate ECCS Venting Surveillance

Each of the licensee identified LERs listed above involved the failure to develop

adequate surveillance test procedures to ensure that all required system

components were tested properly. In each case the licensee declared the affected

system inoperable, entered TS 4.0.3 as appropriate, and successfully completed the

required testing within the allotted 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> time period. These events were of

minor significance since each system functioned properly when tested. The

inspector concluded that this was not indicative of a programmatic breakdown in

the surveillance test program. The licensee discovered these procedural deficiencies

during design basis and operational experience reviews and corrected the applicable

procedures. Additionally, the licensee implemented a generic procedure upgrade

project to identify and correct any additional potentially affected procedures. This

licensee identified violation of failure to develop adequate surveillance test

procedures is being treated as a non-cited violation consistent with Section Vll.B.1

of the NRC Enforcement Policy. (NCV 98-01-01)

lit. Enoineerina

E1 Conduct of Engineering (37751)

E1.1 Residual Heat Removal System Ventilation Covers

,

a. Insoection Scooe:

The inspectors reviewed the engineering analysis performed to install temporary

covers over the ventilation duct openings in both residual heat removal (RHR) pump

rooms. The covers were installed per work requests (WAS) 97 WOO 3878 and

97 WOO 3884 to redirect the ventilation flow to minimize the potential spread of

contamination from minor system leakage through the bonnet studs of check valves

RH-V4, and RH-V-40.

b". Observations and Findinas:

The inspectors observed that the plastic covers were securely fastened to three

sides of the RHR pump room ventilation duct openings. The covers reduced the

area for ventilation flow and introduced an approximate 90' change in the direction

of the exit flowpath. The inspectors were concerned that these covers would

reduce the ventilation flow into the RHR pump room and possibly lead to a

overtemperature condition and failure of safety-related components inside the room

during a design basis event.

.

-

9

The ventilation covers were installed per Procedure MA4.8, " Control of Temporary

Equipment", and were not intended to reduce the ventilation system flow. The

(MA4.8) evaluation provided general information and guidance and concluded that

the covers were acceptable as long as they only diverted and did not reduce the

approximate 12,700 cfm of flow required to maintain the room environmental

conditions. Neither the evaluation nor the work request provided any specific

design or installation details to ensure that the "as built" covers would meet the

design requirements.

In response to the inspector's questions, the licensee promptly removed the

ventilation covers and initiated an engineering evaluation (SS-EV-98-008) to

determine the impact of the covers on the ventilation system and RHR pump room

temperature. The evaluation calculated that the installed covers would reduce the

ventilation flow into the RHR pump rooms by about 50% to approximately 6100

cfm. This would increase the RHR pump room temperature following a loss of

coolant accident about 15'F from approximately 134*F to about 149'F.

The inspector noted that the postulated temperature increase would not have

exceeded the RHR pump room temperature limit of 189'F, and therefore would not

have rendered any of the safety related RHR pump room components inoperable.

The inspector noted that the failure to provide sufficiently detailed design i

instructions resulted in an inappropriate application of the MA4.8 program and a

significant reduction in the ventilation flow into the RHR pump room following the

installation of this modification.  ;

Appendix B Criterion lil, requires, in part, that measures be implemented to assure

that the design basis is correctly translated into specifications, drawings, 1

procedures, and instructions. Contrary to the above, adequate instructions were

riot developed to ensure that the RHR pump room ventilation system modification

would not reduce ventilation system flowrate below an unacceptance level. This is

a violation of 10 CFR 50, Appendix B, Criterion lli (VIO 50-443/98-01-02).

c. Conclusion:

l

The licensee failed to implement adequate design controls to ensure that the safety- !

related components within the residual heat removal system pump room would  ;

remain within their required temp.erature limits prior to modifying the room i

ventilation system. A subsequent licensee analysis, performed after the NRC

identified this deficiency, indicated that the modification reduced the room

ventilation flow by about 50%, however, the room temperature limits would not

have been exceeded.

.

-

10

E2 Engineering Support of Facilities and Equipment-

E2.1 Accumulation of Boron on Residual Heat Removal System (RHR) Drain Pioe

Connection

a. Insoection Scope:

The RHR system engineer identified a ring of dried boric acid accumulation on the

half-coupling for drain valve RH-V-105 on March 5,1998, during a Seabrook

Improvement Plan system inspection. The engineer initiated an adverse condition

report (ACR 98-0782) to review this condition. The drain line is immediately below

relief valve RH-V57. The boron was identified between the pipe insulation and the

branch "T" fitting where the drain line connects to the "B" Train RHR system

discharge piping. The inspector reviewed the licensee's response to this issue,

visually inspected the piping, interviewed applicable personnel, and reviewed

nondestructive test results,

b. Qbservations and Findinas:

. The licensee promptly removed the insulation and inspected the pipe. No visible

evidence of leakage.was noted. Additionally, the licensee performed liquid

penetrant testing which revealed a linear indication in the 8 inch pipe within the

heat affected area of the 3/4 inch drain line weld connection. The licensee

performed ultrasonic testing to characterize the flaw, and determined that the

indication was small and the pipe had adequate wall thickness. The licensee

elected to repair this indication. The boron residue was attributed to previous fluid

l spillage when the relief valve, located above this piping, was removed for testing.

i

The inspectors determined that the licensee responded well to this condition, and

that it did not impact plant safety. The inspectors also noted that this finding

indicated that the current system walkdown inspections were thorough, and

improved over previous licensee inspection activities. The inspector noted a minor

weakness in that the licensee's investigation of an earlier event involving a minor

through wall pipe leak below valve RC-V89 did not include a review of other plant

areas where insulation was periodically wetted. The licensee subsequently

'

identified a total of five (5) other similar configurations susceptible to periodic

,. wetting (areas relating to relief valves RH-V13, RH-V25, SI-V101, SI-V113, and SI-

( _V76). Inspections of these areas by the system engineer identified no boric acid

deposits.- Additionally, since the RC-V89 incident, workers have been instructed to

exercise care to avoid wetting of insulation during relief valve removal, and to

request replacement of insulation when wetted.

c. Conclusion:

The licensee promptly reviewed and evaluated the identification of boric acid

, accumulation on a RHR drain line. The identification of this condition reflected

l

L

,

.

.

11

I-

positively on the licensee's new system walkdown program. The inspector noted

that the licensee's response to this condition did not include identification of the

other plant areas potentially susceptible to periodic wetting. The licensee

implemented appropriate actions to address this concern.

E2.2 Nitroaen Leak Of Safety Iniection Accumulators Sunolv Header

i

a. Insoection Scooe:

On February 2,1998, operators identified that the nitrogen pressure in the safety

injection (SI) accumulators was decreasing by approximately 13.5 psig/ day. The

licensee performed system walkdowns, tests, and evaluations to identify the nitrogen

l leak source (s) and to implement repairs as necessary. The inspector evaluated the

l- licensee's response to these issues, interviewed the system engineer and operations

l personnel, and reviewed the engineering evaluations.

!

l

b. Observations and Findinas:

'

The Sl accumulators are safety-related, and are required to inject borated water into

l

! the reactor coolant system (RCS) piping loops during certain postulated loss of

l

coolant events. Technical Specifications (TS) Section 3.5.1.1, requires the

j accumulator pressure to be maintained between 585 and 664 psig. Nitrogen is used

l to pressurize and maintain the accumulators pressure within the required range.

The inspector reviewed and found acceptable a 50.59 evaluation performed to

support the leak detection testing. During their investigation the licensee identified

several sources of leakage including valve packing, seat, and body-to-bonnet joints.

The licensee tightened the body to bonnet bolts and adjusted the packing on those

valves that could be repaired at power, and initiated work requests to repair the

remaining valves. One of the largest nitrogen leaks was through the packing of valve

NG-V14 which the inspector noted had been recently repacked. The inspector-

identified that the licensee did not question whether this repeat packing deficiency

was due to improper maintenance performance. The inspector discussed this

observation with the system engineer who then initiated ACR 98-0771 to review this

issue.

The licensee evaluated the identified seat leakage through the "D" accumulator

nitrogen supply valve NG-V23 and the header manual isolation valve NG-V123 and

determined that the accumulator remained operable with the minor amount of seat

leakage,

c. Conclusions:

Operations personnel performed well by identifying the safety injection accumulator

nitrogen leaks. The licensee promptly investigated the leakage and implemented

.

.

12

appropriate repairs to reduce the leakage. Engineering properly assessed the impact

of this minor leakage on the accumulator operability.

E2.3 Dearaded Emeroency Feedwater Motor Outboard Bearina. and (Undate) of Unresolved

Item 97-08-05

a.' Insoection Scope:

On February 4, the licensee operated the motor-driven emergency feedwater (EFW)

pump to investigate abnormal lubricating oil analysis results which indicated a high

.

tin content. The inspector reviewed these activities and the licensee's lubrication

analysis program. During this review, the inspector interviewed the system engineer

'

and the lubricating oil program coordinator, attended meetings and briefings held by

the licensee, and reviewed applicable documentation.

b. Observations and Findinas:

There are two EFW pumps at Seabrook required to supply water to the steam

generators to remove heat from the reactor coolant system during emergency

conditions. One pump is turbine driven, while the other pump is motor driven. Each

pump is capable of supplying 100% of the required flow.

The pump parameters such as flow, pressure and vibration were normal during the

run. The bearing temperature was approximately 179'F (below its design

temperature limit of 194*F) and appeared to be steady or increasing very slightly

when the run was secured. The licensee elected to open and inspcet the outboard

bearing following the run and identified that approximately .065 inches of material

had been removed from the non-load carrying motor bearing thrust face. The

licensee performed a root cause evaluation and determined the coupling hubs had

been installed backwards. The condition appeared to have existed since original

installation in 1987. The system engineer concluded, based on the pump test data,

and bearing condition that the EFW pump was operable. The inspectors

independently reviewed the data and determined that the operability _ determination

was sound.

The licensee replaced the bearing, correctly re-installed the coupling hubs and

i initiated an activity to inspect the other potential coupling hub installation problems.

!' The inspector concluded that the licensee responded well to this specific issue. -The

! inspector questioned however, whether licensee responded properly to earlier

'

indications of elevated tin concentrations within the motor bearing lubricating oil.

l Inspection report 97-08 identified potential program deficiencies involving -

l implementation of lubricating oil analysis program and opened unresolved item 97-

08-05 to review this issue. Evaluation of the licensee's response to the motor driven

EFW pump oil anomalies will be reviewed along with URI 97-08-05.

.

13

The licensee has initiated measures to address the inspectors concerns including:

initiation of an evaluation team to evaluate and redesign Seabrook's lubrication

program, . industry bench marking and acquiring external assistance. Additionally,

the oversight program performed an independent evaluation and documented

extensive findings and proposed corrective actions.

c. Conclusion:

The licensee determined that incorrectly installed coupling hubs (a condition which

occurred during initialinstallation), caused a degraded EFW motor outboard bearing

condition. The pump remained operable in this condition and the licensee

implemented appropriate corrective actions to address this deficiency.

E8 Miscellaneous Engineering issues 192903)

E8.1 (Closed) Violation 50-443/96-08-01: covering floor drains in the emergency

feedwater pumphouse without performance of a safety evaluation. The inspector

verified the corrective actions described in the licensee's response letter, dated

December 20,1996, to be reasonable and complete. Among the corrective actions

verified were: revisions to appropriate maintenance and operating procedures to

ensure that 10 CFR 50.59 evaluations are performed prior to plugging or blocking

floor drains; engineering development of a list of floor drains requiring engineering _

review prior to blocking; revisions to the Regulatory Compliance Manual to provide ,

clear management expectations regarding 10 CFR 50.59 reviews for procedure )

'

changes; and, implementation of supervisor training for procedure revision reviews

and 10 CFR 50.59 evaluations. No similar problems were identified.

E8.2 (Closed) Unresolved item (URI) 97-07-03. Maintenance rule implementation for the

control building air conditioning (CBA) system. The inspector questioned in

Inspection Report 97-07 whether the licensee should have previously categorized the

CBA system as an "A-1" system in response to a history of repeated CBA

compressor (train) failures. During this period, the inspector reviewed the issue and

noted that the Expert Panel had categorized this system as a normally operating, non-

l risk significant system. This type of system would not have required train level

monitoring and therefore previous individual compressor failures would not have

! caused the maintenance rule performance criteria to be exceeded. The inspector

l concluded that the licensee's previous decision not to classify the CBA system as an

A-1 system did rot violate the maintenance rule requirements. This unresolved item

is closed.

E8.3 (Closed) Eccalated Enforcement issues (EEI) 97-08-02. 97-08-03. 97-08-04. and 97-

08-06. Inspection report 97-08 identified fcur issues tnat were classified as

apparent violations. These issues were discussed at a pre-decisional enforcement

conference on March 24. The NRC determined that three of the issues were

violation:, of NRC Requirements and transmitted this decision in separate

correspondence. These issues included eel 97-08-03, eel 97-08-04, and eel 97-08-

[

l

_ _ _ _ _ - _ _ - _ - _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

14

06 which are being closed administratively. Followup licensee actions to these

violations will be tracked under the following enforcement action items: 98-073-

01013, 98-073-02013, and 98-073-03013.

The final issue involving operation of the safety injection system (eel-97-08-02) was

determined not to be a violation and is closed.

IV. Plant SuDDort

R1 Radiological Protection and Chemistry Controls

R1.1 Maintenance Work in Posted Contaminated Area Without Protective Clothina

a. Inspection Scone:

On March 13,1998, the inspector observed three maintenance technicians and one

engineer performing maintenance activities on the "B" containment building spray

(CBS) pump, inside a posted contamination area without any protective clothing.

The activities wHch included sampling of the pump bearing oil, and repair of the

pump inboard bearing thermocouple, were being performed under radiation work

permits (RWPs) 98 R-00002, 98-R-00004, and 98-R-00011.

b. Observations and Findinas:

The inspector observed that all four workers had reached across the contamination

boundary with their bare hands to perform or support the maintenance activ! ties. The

inspector questioned the workers whether they had consulted with the health physics

department (HP) on the acceptability of working without protection inside the

contaminated boundary. One worker indicated that he had spoken with a HP

technician and believed that he had been authorized to perform the maintenance

activities without any additional protective clothing.

The inspector reported the events to a HP technician and notified the HP Manager.

Thwe individuals stated that they expected all personnel working inside a contaminated

area to wear, as a minimum, hand protection. The inspector reviewed the applicable

radiation work permits (RWP-98-R-00002,98-R-00004, and 98-R-00011) and

confirmed that all three RWPs required the ute of nuerts, and rubber gloves.

The inspector r . Aened iP radiological surveys of the applicable areas performed before

and after this e- m' o,d noted that the survey levels were lower (approx. 409

DPM/100 m ' ' man the required posting value (Greater than 1,000 DPM/100 cm).

l However, Hf e sted these areas conservatively due to the potential for varying

radic:cgical! onditions. None of the four workers or the tools used became

contaminated during these activities. however, the inspector was concerned that

!

_ _ _ _ _ _ _ _ _

.

15

multiple workerc across a number of disciplines failed to comply with the Station HP

requirements.

On March 16,1998, HP management removed the workers' dosimetry to prevent their

entry into the RCA, and initiated a full investigation of this issue (ACR 98-0882). The

- event was thoroughly reviewed and several corrective actions were implemented

including:

o Coachin0 and counseling of allindividuals involved

  • HP management held briefings with engineering and maintenance personnel, 'o

review this incident and reinforce HP expectations.

o Performing reviews of the rad training materials for " Contaminated Areas"

boundary delineation and controls, to ensure adequate understanding of postings

and to enforce contaminated area practices.

  • Evaluating existing " Contaminated Area" postings, to ensure better delineation of

posted boundaries.

The inspector determined that the licensee addressed this issue well and that their

investigation was comprehensive.

Technical Specification (TS) 6.10.1 requires that procedures for personnel radiation

protection be prepared consistent with the requirements of 10 CFR Part 20 and shall be

adhered to for all operations involving personnel radiation exposure. Seabrook

administrative procedure RP 9.1, "RCA Access / Egress Requirements", revision 12,

dated 2/11/98, requires, in part, that personnel perform work inside the RCA in

accordance with the RWP and posted instructions. Contrary to the above, on March

13,1998, four individuals failed to comply with their RWP and posted radiological

instructions. This is violation of TS 6.10.1 (VIO 50-443/98-01-03).

c. Conclusion:

The inspector identified four workers performing maintenance on the "B" containment

spray pump which had been posted as a contaminated area without wearing any

protective clothing as required by the radiation work permit and posted instructions.

The Ucensee promptly evaluated this issue' and implemented adequate corrective

actions.

I

q

1

-(

!

16

S1 Conduct of Security and Safeguards Activities

S1.1 General Comment (71707, 71750)

The inspectors observed security force performance during inspection activities.

Protected area access controls were found to be properly implemented during random

observations. Proper est. ort control of visitors was observed. Security officers were

alert and attentive to their duties.

F8 Miscellaneous Fire Protection issues (92904)

F8.1 (Closed) Violation 50-443/96-03-01: two examples of staff failure to follow procedures

regarding control of combustible materials and repair of emergency lights. The first

example involved a failure to adhere to fire protection procedure 2.2, Rev 2, " Control of

Combustibles," when, on April 18,1996, three plastic pails of a Class I combustible

(epoxy primer paint) were inappropriately stored and left unattended in the turbine

building. The second example involved a failure to adhere to operations procedure

OSO443.47, Revision 5, "8 Hour Emergency Lighting Units Monthly Functional Test,"

when, on January 28,1996, three inoperable emergency lights were found, but not

properly reported to the Unit Shift Supervisor (USS), nor was a work order initiated to

restore the lights to service. The inspector verified the corrective actions described in

the licensee's response letter, dated July 12,1996, to be reasonable and complete.

Among the corrective actions verified were: procedure changes to ensure the control of

combustible materials, providing additional clarification of requirements for approved

storage; procedure changes to ensure timely notification of the USS and initiation of

work orders for inoperable emergency lighting; and, licensee records indicating that

othar required activities were completed. No similar problems were identified. This

item is closed.

F8.2 (Closed) Violation 50-443/96-03-02: one example of inadequate fire protection

procedures regarding timely restoration of inoperable emergency lighting. This violation

involved two Seabrook procedures not incorporating Seabrook Design Basis Document,

DBD-FP-01, " Emergency Lights," design criteria of returning emergency lights to an

operable status within 30-days of being identified as inoperable. The inspector verified

the corrective actions described in the licensee's response letter, dated July 12,1996,

to be reasonable and complete. Among the corrective actions verified were: procedure

changes to the associated surveilla;.ce and maintenance procedures to ensure that

inoperable emergency lighting would be assigned a priority 2 work request; completien

of an effectiveness monitoring program in the maintenance organization to ensure that

'

. this violation did not repeat; and, a re-evaluation by the maintena.1ce organization of

other similarly "self-identified" violations where corrective actions had not been fully

implemented leading to repeat violations. This latter action was considered by the

inspector as a comprehensive review and self-assessment of the corrective actions

program tracking system for maintenance concerns. No similar problems were

'

identified. This item is closed.

.. . - - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ -

.

'

17

V. Manaoement Meetinas )

X1 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management,

following the conclusion of the inspection period, on April 8,1998. The licensee

acknowledged the findings presented.

X3 Other NRC Activities

A pre-decisional enforcement conference was held on March 23,1997 at the Region I

office in King of Prussia, Pennsylvania. The conference was conducted to review four

apparent violations of 10 CFR 50 Appendix B Criterion XVI. The NRC enforcement

decision was transmitted via separate correspondence.

,

1

1

1

.

'

18 .

PARTIAL LIST OF PERSONS CONTACTED

Licensee

W. Diprofio, Unit Director

R. White, Design Engineering Manager

J. Grillo, Technical Support Manager

G. St Pierre, Operations Manager

B. Seymour, Security Manager

J. Linville, Chemistry and Health Physics Manager

J. Vargas, Engineering Director

.

_ _m _ _ ~ _- -

.

'

19

INSF'ECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observation

IP 62707: Maintenance Observation

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 92700: Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

ITEMS OPENED, CLOSED, AND DISCUSSED

Ooened

NCV 98-01-01 Failure to Develop Adequate Surveillance Test Procedures

VIO 98-01-02 Failure to implement Adequate Design Controls

VIO 98-01-03 Failure to Adhere to Radiation Work Permit and Posted Instructions

Closed

VIO 96-03-01 Failure to Follow Procedures Regarding Control of Combustible Materials

and Repair of Emergency Lights

VIO 96-03-02 Inadequate Fire Protection Procedures Regarding Timely Restoration of

Inoperable Emergency Lighting

,

VIO 96-04-01 Inadequate Emergency Feedwater Pump Maintenance

l URI 97-06-01 Review of Operator Actions Following a Main Feedwater Pump Pipo

l Oscillations

l LER 96-06-00 Missed Surveillance Requirement

l LER 97-03-00 Missed Surveillance Turbine Trip on Reactor Trip

! LER 97-04-00 Remote Shutdown Circuits Not Tested Completely

LER 97-17-00 Inadequate SSPS Surveillance Testing

LER 98-01-00 Inadequate ECCS Venting Procedurs

NCV 98-01-01 Failure to Develop Adequate Surveillance Test Procedures

VIO 96-08-01 Covering Floor Drains Without a Safety Evaluation

URI 97-07-03 Review of Maintenance Rule Characterization of Control Building Air  ;

Conditioning Compressors l

eel 97-08-02 Operation of the Safety injection System Test Header j

eel 97-08-03 Failure to implement Prompt Correctivo Action for a Degraded Pipe

eel 97-08-04 Failure to implement Prompt Corrective Actions for Degraded Control

Building Air Conditioning Compressors

eel 97-08-06 Failure to implement Prompt Corrective Actions for a Degraded Positive

Displacement Charging Pump ,

i

Discussed

URI 97-08-05 Potential Lubricating Oil Program Deficiencies

i

)

.

'

20

LIST OF ACRONYMS USED

ACR Adverse Condition Report

ASME American Society of Mechanical Engineers

CAS Central Alarm Station

CBS containment building spray

EDG Emergency Diesel Generator

. EFW Emergency Feedwater

FME Foreign Material Exclusion

gpd gallons per day

gpm gallons per minute

LCO Limiting Condition for Operation

MOV motor operated valve

MPCS Main Plant Computer System

NSARC Nuclear Safety and Audit Review Committee

psig pounds per square inch gauge

QC Quality Control

l RHR Residual Heat Removal

! SG steam generator

l SIR Station Information Report

l. SORC Station Operations Review Committee

SUFP Startup Feedwater Pump

i

SW Service Water

l TDEFW Turbine Driven Emergency Feedwater Pump

L _TS Technical Specifications

'

UFSAR Updated Final Safety Analysis Report

WR Work Request

I