ML20196J669

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Insp Rept 50-443/97-03 on 970415-0615.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20196J669
Person / Time
Site: Seabrook NextEra Energy icon.png
Issue date: 07/30/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20196J610 List:
References
50-443-97-03, 50-443-97-3, NUDOCS 9708050026
Download: ML20196J669 (57)


See also: IR 05000443/1997003

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                                                                       Enclosure 2
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                                            U. S. NUCLEAR REGULATORY COMMISSION
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                                                                          REGION I                                                                             ;
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            Docket No.:                  50-443
            License No.:                 NPF-86                                                                                                                j
            Report No..                  50-443/97-03
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            Licensee:                    North Atlantic Energy Service Corporation
            Facility:                    Seabrook Generating Station, Unit 1
            Location:                    Post Office Box 300

l Seabrook, New Hampshire 03874  ;

            Dates:                       April 15,1997 - June 15,1997                                                                                            l

, inspectors: William T. Olsen, Senior Resident inspector (Acting) l Cavid M. Silk, Resident Npector ! Alfred Lohmeier, Reactor Engineer, DRS

                                         John R. McFadden, Health Physicist, DRS                                                                                 j
            Accompanied by:              Javier Brand, Resident inspector intern
            Approved by:                 Richard Conte, Chief, Reactor Projects Branch No. 8
                                         Division of Reactor Projects
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          9708050026 970730
          PDR. ADOCK 05000443

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                                        EXECUTIVE SUMMARY
                               NRC Inspection Report No. 50-443/97-03                                      j
    This integrated inspection included aspects of licensee operations, engineering,                       ;
    maintenance, and plant support. The report covers an 8-week period of resident inspection              l

j from April 15 through June 15,1997. l

    Ooerations:
    A preventable reactor trip occurred during the manual shutdown of the unit to enter the
    fifth refueling outage. Plant indications available to the operators were overlooked.
    Although the safety consequences of the event were low, it did subject the plant to a
    unnecessary transient and challenge to the operators. The root cause analysis repcrt for
    this event was very thorough, however, it indicated an overall lack of appreciation by the
    staff for the impact of abnormal conditions on plant response. The inspector concluded
    that staff performance leading to the trip indicated a weak assessment of the impact of the
    IR detector current anomaly on plant operations (Section O2.1).
                                                                                                           l
    Steam Generators (SG) "B" and "C" were inadvertently drained down during feedwater                     l
    isolation valve stroke testing due to drain valves being improperly left in the open position.         l
    In addition to the system configuration control, operations personnel initially only assessed          l
    that "C" SG had drained down and failed to investigate the "B" SG low level indication
    even after being questioned by the inspectors (Section 02.2).

i Fuel handling activities were conducted according to procedure in a well controlled manner l as the entire core was off loaded and subsequently reloaded. Reactor engineering l personnel charted assembly positions during fuel movement and monitored for an approach l to criticality by developing a 1/M plot during core reloading (Section 2.3).

    Midloop activities were performed well and appropriately supervised. Safety considerations

l were manifested as activities which could have impacted the reactor coolant system or

    midloop operations were restricted (Section 2.4).

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    The licensee properly identified that the WRGM was inoperable and properly entered the
    Technical Specification action statement. The increased sampling frequency was very

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    conservative with an excellent safety perspective in evidence and the addition of the
    portable sampling equipment provided excellent backup information. The failed power
    supply was promptly repaired and returned to service. The inspector noted strong

i management involvement in the repair process to ensure that the instrument was promptly

    returned to service (Section O2.5).
    Maintenance:

l The Ten-Year In-service Inspection (ISI) Program status is within the targeted schedule and I consistent with the performance requirements for non-destructive examinations of Code '

     Class 1,2, and 3 components and their supports, and is consistent with the augmented ISI
     program indicated in the Updated Final Safety Analysis Report, Section 6.6.8. The
     program plan was well prepared, documented, and implemented (Section M1.1).
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              Executive Summary
                                                                                                                        ,
              ISI examir5tions reviewed were performed in accordance with Code and NRC regulations
              (Section M1.2).

l l The steam generator tube eddy current inspection program was conservatively planned,

              and consistent with ASME Section XI, Reg. Guide 1.83, Plant Technical Specifica*;ons,

! EPRI Examination Guidelines, and licensee responses to Generic Letter 95-03 (Section ! M1.3). ,

              Preparation for examination of the pressurizer head-to-shell weld showed good utilization of
              technical resources. Weakness was shown in allowing the utilization of nominal drawing
              dimensions, instead of as-built dimensions, to fabricate weld inspection qualification
              models. This error was self-discovered und steps were taken to provide a satisfactory

l alternate inspection procedure (Section M1.4). l

              A poor work practice was identified during work on the encapsulation vessel for the                     -i
              recirculation sump. The inspector observed workers tossing safety-related flange bolts into                ;
               a bucket which could have damaged the bolts (Section M1.5).
          - 'The foreign material exclusion program at Seabrook is excellent. Considerable manpower
               and resources have been dedicated for this effort (Section M2.1).                                           l
               On May 27, tubing installed for a temporary pressure transmitter on the charging system
               failed resulting in a radioactive spill of about 30 gallons because of under-rated tubing.
              The inspectors determined within the past 18 months four tubing ruptures had occurred
               because of under-rated tubing. This recent failure demonstrates inadequate corrective.                      )
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               action and management oversight to prevent recurrence and is a violation of NRC                             )
               requirements (Section M2.3).
                Enoineerino:

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               The licensee properly performed a significant plant modification by replacing the primary

l component cooling water heat exchangers. The modification was made to improve system '

                reliability by increasing heat exchanger capacity resistance to corrosion. The 10 CFR
                50.59 evaluation was thorough and properly documented. The work was well controlled
                and system engineers provided excellent guidance to the workers (Section E1.1).

I' While reviewing activities and documentation related to operability verification testing for j

                the main steam safety valves, the inspector determined that no 10 CFR 50.59 evaluation                     '
                was performed for the new equipment used for the test. Although there were no safety
                consequences resulting from the use of the new equipment as determined by bounding
                UFSAR accident analysis, the inspector concluded that a potential weakness may exist in
                the licensee's 50.59 process as no clear direction exists as to when an evaluation should
                be performed (Section E2.1),

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                    Executive Summary
                    Evaluation of the failed leak rate test for containment spray valve CBS-V18 and subsequent                ,
                    corrective actions to machine the valve disc and disc hanger to prevent wedging of the
                    valve disc, were adequate (Section E2.2).
                                                                                .
                    The licensee response to and assessment of the failed fuel rods was very good. Once the
                    location of the failed rods was identified, the licensee evaluated the commonalities,
                    developed probable causes, and implemented corrective actions to prevent recurrence
                    (Section E2.3).
                    Plant Suooort:                                                                                             j
                    The licensee maintained and implemented strong radioactive liquid and gaseous effluent
                    control programs, with capabilities to protect the public health and safety and the
                    environment. The management's commitments and support to the programs were noted.                         j
                    The licensee demonstrated very good effluent ALARA practices for the programs. The                        i
                    chemistry steff responded to QA audit findings and observations in a timely manner and
                    with sound technical bases (Section R1.1).

l '-The licensee continued to implement en overall effective Radiological Environmental -

                    Monitoring Program (REMP) including management controls, quality assurance audits,
radiological environmental monitoring, and meteorological monitoring program. The Offsite
Dose Calculation Manual (ODCM) was properly implemented. The 1995 and 1996 audit .

l reports effectively assessed program strengths and weaknesses. No deficiencies in the

                    Updated Final Safety Analysis Report commitments were identified (Section R1.2).
                     In the area of radiological controls, the licensee exhibited several positive performance
                    attributes in exposure monitoring and control and ALARA at the start of the outage. There
                     were two non-cited violations involving licensee-identified and corrected violations
                    pertaining to adherence to posted instructions and RWP requirements; and adherence to
                    access control procedures for radiologically controlled areas, including high radiation areas
                     (Section R1).                                                                                             j
                    The audits were of sufficient technical depth to effectively identify and assess program
                    strengths and weaknesses. The audits evaluated the technical adequacy of implementing                       l
                    procedures, TS requirements, and practices. Performance of the audits by the audit teams
                     was thorough, objective and of high quality as evidenced by the report documentation
                     (Section R7.1).
                     On May 22, the inspector identified a violation on NRC physical security requirements, in
                    that a licensee designated vehicle, inside the protected area, was left unattended with the
                     keys in the ignition and the engine running (Section S1.2).

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                                                      TABLE OF CONTENTS
                                                                                                                               Paae
          EX E C UTIV E S U M M A RY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii
          TA B LE O F C O N TE NTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . v       ;
          l. Operations ....................................................                                                       1   1
                   01    Conduct of Oper ations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1              '
                         01.1 General Comments .................................                                                   1
                   02    Operational Status of Facilities and Equipment . . . . . . . . . . . . . . . . . . . 1                        ;
                         O 2.1 Unexpected Reactor Trip .............................                                               1    j
                         02.2 Inadvertent Steam Generator Drainings . . . . . . . . . . . . . . . . . . . 3

, O2.3 Re f ueling O perations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4 !

                         O2.4 Mid-loop O perations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5
                         O2.5 Failure of Wide Range Gaseous Monitor . . . . . . . . . . . . . . . . . . . 5                            -
          II. Maintenance ..................................................                                                       6
M1 Conduct of Maintenance .................................. 6

l - M 1.1 Review of the Ten-Year ISI Program Status . . . . . . . . . . . . . . . . 6

                         M1.2 Observation of inservice inspection (ISI) Activity ............                                      7
                         M1.3 Steam Generator Tube Eddy Current inspection Preparation ....                                        9
                         M 1.4 Pressurizer Head-to-Shell Ultrasonic Test . . . . . . . . . . . . . . . . . 10
                         M1.5 Encapsulation Vessel for Recirculation Sump Isolation Valves
                                   (CBS-V8 and V-14) ................................                                             11
                   M2    Maintenance Support of Facilities and Equipment . . . . . . . . . . . . . . . . 12
                         M2.1 Foreign Material Exclusion (FME) Controls . . . . . . . . . . . . . . . . 12

l M2.2 -Diesel Generator-1 A Monthly Operability Surveillance Run . . . . . 13

                         M2.3 Pressure Tube Failure (Radiological Spill)in Primary Auxiliary
                                   Building     ........................................                                          14
          Ill . Enginee rin g . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15
                   El    Conduct of Engineering ..................................                                                15
                         E1.1 Modification of Primary Component Cooling Water Heat
                                   Exch an g e rs . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15        l
                   E2    Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . 16
                         E2.1 Main Steam Safety Valves Testing .....................                                              16
                          E2.2 Leak Rate Test Failure of Containment Isolation Check Valve
                                   CBS-V18         .......................................                                        18
                          E2.3 Operating Cycle 5 Failed Fuel Rods . . . . . . . . . . . . . . . . . . . . . 19
                          E2.4 Failure of Unitized Starters During Surveillance . . . . . . . . . . . . . 22                            i

l IV. Plant Support ................................................ 23 ! R1 Radiological Protection and Chemistry (RP&C) Controls . . . . . . . . . . . . 23 .

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R1.1 Implementation of the Radioactive Liquid and Gaseous Effluent j
Control Programs ................................. 23  ;
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               R1.2 Implementation of the Radiological Environmental Monitoring

i Program ........................................ 25

               R1.3 Meteorological Monitoring Program (MMP) . . . . . . . . . . . . . . . . 27
               R1.4 Refueling Outage Radiological Controls-External Exposure . . . . . 28
               R1.5 Refueling Outage Radiological Controls-Internal Exposure .....                                 30
               R1.6 Refueling Outage Radiological Controls-Radioactive Materials,
                      Contamination, Surveys, and Monitoring . . . . . . . . . . . . . . . . . 30                     .
R1.7 Refueling Outage Radiological Controls-As Low As Reasonably '

l Achievable (ALARA) ............................... 32 ,

               R1.8 Other Changes to the RP Program . . . . . . . . . . . . . . . . . . . . . . 32                    j

i R2 Status of RP&C Facilities and Equipment ..................... 33 i

               R2.1 Calibration of Effluent / Process Radiation Monitoring Systems

l (RMS)................... ..................... 33

               R2.2 Calibration of Area Radiation Monitoring Systems (ARMS) . . . . . 34
               R 2.3 Air Cle aning Syste m s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 35         )
         R3    RP&C Procedures and Documentation . . . . . . . . . . . . . . . . . . . . . . . . 35                   i
         R5    Staff Training and Qualification in RP&C . . .                       ..................             36

l R6 RP&C Organization and Administration ....................... 37 -

               R6.2 Management Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 38
         R7    Quality Assurance in RP&C Activities                  ............. ..........                      38
               R7.1   Quality Assurance Audit Program . . . . . . . . . . . . . . . . . . . . . . 39
               R7.2 Quality Assurance of Analytical Measurements ............                                      40 l
         R8    Miscellaneous RP&C issues ...............................                                           41 !
               R8.1 Review of Updated final Safety Analysis Report (UFSAR)                                            I

l C o m mit m e nts . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 41 l R8.2 (Closed) LER 50-443/96-009-00: Missed surveillance PCCV/ l rate of change monitor alarm. . . . . . . . . . . . . . . . . . . . . . . . . . 41 , l R8.3 (Closed) LER 50-443/97-005-00: Misposition of Main Steam l

                      Line Radiation Monitors. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 42           ;
         S1    Conduct of Security and Safeguards Activities . . .                            ..... ........       42
               S1.1 General Comments (71707, 71750)                            ....................                42
               S1.2 Uncontrolled Vehicle in Protected Area . . . . . . . . . . . . . . . . . . 42
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   V. Management Meetings . . . . . . . . . . .       ....... ......................                               43 l
         X1    Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . .                        ........ .. 43
         X3    Other NRC Activities . ............... ..................                                           44
   PARTIAL LIST OF PERSONS CONTACTED                  .. ..... . ...................                               45

i INSPECTION PROCEDURES USED . . . . . . ... .......................... 47 !

   LIST OF ACRONYMS USED       ............... .........................                                           48
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                                             Report Details
   Summarv of Plant Status
   At the beginning of this inspection period, the facility operated at 100% rated thermal
   power for 62 days, with routine minor power reductions performed to support instrument
   calibrations and turbine valve testing. Operators shutdown the unit on May 5 to begin the
   fifth refueling outage (OR05).
                                              1. Operations
   01       Conduct of Operations                                                                      i
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   01.1 General Comments (71707)
   The inspectors routinely conducted independent plant tours and walkdowns of selected

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   portions of safety-related systems during the inspection period. These activities consisted
   of the verification that system configurations, power supplies, process parameters, support
   system availability, and current system operational status were consistent with Technical
   Specifications (TS) requirements and Updated Final Safety Analysis Report (UFSAR)
   descriptions. Additionally, system, component, and general area material conditions and
   housekeeping status were noted.                                                                     l

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   In general, routine operations were performed in accordance with station procedures and             l
   plant evolutions, and were completed in a deliberate manner with clear communications
   and effective oversight by shift supervision. Control room logs accurately reflected piant
activities. Shift turnovers were comprehensive and thoroughly addressed questions posed

l by the oncoming crew. Control room operators generally displayed good questioning l attitude prior to releasing work activities for field implementation. The inspectors found. l that operators were knowledgeable of plant and system status.

   O2       Operational Status of Facilities and Equipment

l l 02.1 Unexpected Reactor Trip

      a.     Insoection Scop _e
    On May 10, while performing a normal shutdown to enter the fifth refueling outage, the
   reactor tripped from approximately 8% power due to an intermediate range (IR) high flux
   trip actuation when permissive P-10 reset. Control room operators appropriately responded
   to the reactor trip and implementd the applicable procedures. The inspector reviewed the

j root cause analysis (RCA), the circumstances, and activities related to the reactor trip to l assess licensee response to this transient. ,

      b.     Observations and Findinas
    The licensee determined that the reactor trip occurred due to the high-neutron-flux trip
    signal from detector IR N35 not being cleared prior to P-10 reinstating the IR high neutron
    flux trip. Permissive P-10 blocks the IR high-neutron-flux trip when operating at power
    levels greater than 10% and reinstates the trip when i ower is below 8%. The licensee
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    determined that the flux trip signal had not cleared because of changes in IR N35 detector
    current and a drift in its power supply. The net effect was that indicated power on the IR
    detector was higher than actual power. Based upon the effects of the detector current
    changes and power supply drift, the trip signal from IR N35 would have reset at
    approximately 7% power. IR N36 was affected in a similar manner, however, its trip
    signal had cleared prior to the resetting of P-10.
    The licensee determined the root causes to be inadequate monitoring and trending of IR
    channels, a lack of knowledge of the effect of detector current on reset and trip setpoints,
    and a lack of detail in the shutdown proceduro that created an over-reliance on operators
    to diagnose an imminent reactor trip. Several staff personnel were aware of the unusual IR
    detector currents, but did not initiate actions to assess or address the condition. The
    change in the detector currents was caused by an outward radial shift of neutron flux. The
    licensee had become aware of detector power supply drifts that had affected the power
    range and source range detectors but did not consider the effect on the IR detectors. The
    shutdown procedure cautioned the operators about the significance of P-10 and operators
    did have indication on the Reactor Protection System Bistable Panel that a trip condition
    existed for IR high flux. The operator, however, failed to stop the power decrease and         ;
    clear the trip condition before going below 8% power.
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    The RCA indicated that severallicensee personnel were aware of precursors and therefore        !
    had an opportunity to prevent the trip. The training staff, who maintain the training
    simulator, compare plant parameters with simulated parameters. The staff noted the
    change in the IR detector current and had incorporated it on the simulator's IR detectors.
    During subsequent licensed operator training for low power scenarios, crews experienced
    several effects (IR flux trip and IR rod stop at lower than expected values) from the change
    in the IR detector currents. The licenseo failed to appreciate the significance of these
    effects in the simulator scenario to assess the potential impact upon the plant. No ACR.
     was generated as a result of occurrences in the simulator.
    To prevent recurrence of this event, Operations management initiated the following
     corrective actions:                                                                           j
     e       Revise the shutdown procedure to verify the IR high-neutron-flux trip bistable lights l
             have de-energized prior to decreasing power below 10%.
     e       Evaluate the effect of core flux changes on nuclear instrumentation, adjust the       l
             monitoring frequency as necessary, and develop a strategy based on the evaluation.
     e       Increase the frequency of monitoring IR for power supply degradation.
     e       Incorporate the lessons learned from this event into operator training.
The inspector determined that the corrective actions appeared to address the root causes

l of this event. Further, the inspector determined that the RCA report was very good. l System conditions and licensee staff performances related to this event were thoroughly l evaluated.

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    c.       Conclusions
  A preventable reactor trip occurred during the manual shutdown of the unit to enter the
  fif th refueling outage. Hant indications available to the operators were overlooked.
  Although the safety consequences of the event were low, it did subject the plant to a
  unnecessary transient and challenge to the operators. The RCA report for this event was
  very thorough, however, it indicated an overall lack of appreciation by the staff for the
  impact of abnormal conditions on plant response. The inspector concluded that staff
  performance leading to the trip indicated a weak assessment of the impact of the IR
  detector current anomaly on plant operations.
  02.2 Inadvertent Steam Generator Drainings
     a.      Insoection Scope (71707)
  On June 13, with the unit in Mode 6 (refueling), a Lo Lo Stea>n Generator (SG) level (14%
  narrow range) condition occurred on the 'C' SG due to a feedwater system drain valve
  being inadvertently left open. The inspector reviewed the licensee's response and
  circumstances related to the inadvertent draining of the 'B' and 'C' steam generators. -.
     b.      Observations and Findinos
  While perforrning a stroke test on the 'C' SG Feedwater Isolation Valve, FW-V-48, SG level
  dropped from approximately 40% to 14% causing an emergency safeguards feature
  actuation. A reactor trip and emergency feedwater actuation occurs at 14% SG level. The
  loss of SG inventory was due to drain valve FW-V-116 which was inadvertently left in the
  open position. -The water drained from the SG discharged to the circulating water system
  and ultimately to the ocean. Drain valve FW-V-116 should have been closed to maintain
  the system boundary. (The feedwater check valve, FW-V-332, upstream of FW-V-116,
  was the intended system boundary.) The licensee is investigating this event to determine
  the root cause. (IFl 50-443/97-03-01)
  Operators were not cognizant of the loss of SG inventory due to the SG level deviation
  alarms already being present at 40% level. The deviation alarms occur at i 5% from
  50% NR level. The inspector noted about two hours after this event, that the 'B' SG level
  was approximately 20% while the levels in 'A' and 'D' SG were approximately 40%. The
  inspector questioned the operators about the discrepancy. The operators stated that
  nothing was unusual about the situation and attributed the lowering of 'B' SG level to
  chemistry sampling. However, on June 14, the inspector was informed that 'B' SG level
  had decreased from 40% due to the same reason as the 'C' SG The drain valve (FW-V-
   115) between the feedwater isolation valve and check valve had been open and was a
  release path for 'B' SG inventory when that isolation valve was stroke tested.
     c.      Conclusions
  The inspector concluded that insufficient system configuration control contributed to the
  event occurrence. Operations personnel initially only assessed that SG 'C' had drained
  down and failed to investigate the SG "B" low level indication even after being questioned
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          a
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                                           by the inspector. More importantly, the ineffective operato, awareness of SG level / trend
                                           contributed to the slowness in detecting the inadvertent draindown of both SGs. Due to
                                           the condition of the plant, the inspector determined that the safety significance to the
                                           event was low because the SGs were not required to function as a heat sink.
                                           02.3 Refueling Operations
                                             a.    Insoection Scone
                                           The inspector reviewed licensee procedure RS0721, Refueling Administrative Control, and
                                           observed licensee refueling related activities in the control room and in containment to
                                           assess compliance with regulations and the licensee's performance in this area.
                                             b.    Observations and Findinas
                                           The licensee adhered to the procedural guidance and cautions in the procedure during fuel
                                           movement. Activities were conducted in an orderly and professional manner. Fuel
                                           assembly movements and positions were monitored and tracked by reactor engineering
                                           personnel in the control room and 1/M plots were performed appropriately to monitor
                                           approaches to criticality.
                                           While in containment, the inspector did not notice the audible source range detector
                                           indication. According to the licensee, the detector scale was set at x1000 and was
                                           providing an audible signal about every 60 to 90 seconds. The licensee is to suspend fuel
                                           handling operations if the system becomes inoperable. However, at that scale setting and
                                           frequency, the signal was unnoticed by the inspector in containment. (Only four
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                                           assemblies remained to be loaded into the core at that time). The inspector was concerned    '
                                           that it would be difficult to recognize if the signal became inoperable. Therefore, the
                                           inspector considered the high scale setting to not be a good work practice as the purpose
                                           of the audible signal was diminished.                                                        l
                                           The inspector verified that the licensee was in compliance with the TS regarding criticality
                                           concerns in the spent fuel pool (SFP). T.S. 3.9.13 specifies the identification and storage  j
                                           location of three types of assemblies within the SFP. The inspector verified that the
                                           licensee had identified the assemblies according to type and that the restrictions regarding ;
                                           their relative storage location in the SFP were met.
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                                             c.    Conclusions
                                           Overall, the inspector determined that the licensee's refueling activities were performed    l
                                            well and in accordance with procedure. The licensee agreed to review the setting of the
                                           audible source range detectors.

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    02.4 Mid-loop Operations
      a.    Insoection Scoce
    On May 16 and 17, the inspector observed portions of the reactor coolant system (RCS)
    drain down to mid-loop (RCS level below the top of the hot leg nozzles, which is between
    minus 71 to minus 73.5 inches), to install the SG nozzle dams for eddy current testing, in
    accordance with operations procedure OS1000.12, Operation with RCS at Reduced
    inventory /Midloop Conditions. This activity was started after the fuel was fully offloaded
    from the core into the SFP.
    The inspector reviewed the procedure, attended pre-evolution briefings, walked down test
    equipment and verified installation of levelindicators inside containment, and verified
    proper indication in control room. In addition, the inspector verified proper residual heat
    removal (RHR) system operation.
      b.    Observations and findinas
    The inspector noted good coordination, communication, and management oversight during
    the activity. Personnel were knowledgeable of the procedure, plant conditions and
    required termination criteria of the evolutions to address abnormal conditions if required.
    Adequate RCS levelindication and redundancy was provided by four separate level
    indicators. Operators maintained excellent focus regarding RCS inventory and decay heat
    removal throughout mid-loop operations.
      c.    Conclusion
    The inspector determined that Seabrook Station personnel properly performed the critical

l

    evolution of drain down to allow removal of the SG nozzle dams, in a safe and controlled

! manner. Adequate measures, briefings, and activities were implemented to prevent ,

    previous industry problems which have occurred while performing similar evolutions. No

l deficiencies were identified by the inspector.

    02.5 Failure of Wide Range Gaseous Monitor

l a. Insoection Scone l l On April 30, Seabrook Station declared the station exhaust Wide Range Radioactive

    Gaseous Radiation Monitor (WRGM) inoperable due a failed power supply. The inspector
    verified the licensee's actions to comply with station TS and attended a Station Operations

l Review Committee (SORC) meeting.

      b.    Observations and Findinas
    The Seabrook Station operations and radiation controls departments properly evaluated the
    problem with the WRGM and entered the remedial actions of TS 3.3.3.9 as required. The
    TS action statement requires grab samples every 12 hours and sampling every 24 hours
     when the equipment is out of service. The station initiated sampling every 6 hours and
       .       . _ _ _ _ _ _ _ _ _ _ _  __    _      _ _ _ . _ _ _ _ . . _ _ _ . _ _ _ _ _               _ . _
   ,
  .
                                                               6
         analysis every 12 hours. In addition, a station temporary modification was initiated to
         provide a method er continuous gas sampling of the primary vent stack in the event of a
         failure of the WRGM low range monitor. A temporary portable gas radiation monitor was
         installed at tha WRGM grab sample lines in the primary auxiliary building elevation 53 foot.
         The temporary portable gas sampling monitor provided continuous monitoring for                        '
         indication / trending only.

l A SORC meeting was convened to approve a temporary modification to install a portable {

         continuous radioactive gas monitor to provide additional backup monitoring of station        -
                                                                                                                i
         exhaust during the period that the WRGM was out of service. During the SORC meeting

l station management asked very detailed questions regarding the effects of the temporary

         equipment on other permanently installed equipment and the duration of the temporary

,

         installation. It was determined that no safety hazards existed from the installation of the

! temporary equipment. On May 6, a new WRGM power supply was received from the l vendor, was installed and tested satisfactorily, and the unit was retumed to service. The l inspector verified the proper installation and operation of the temporary gas sampling I

         equipment in the primary auxiliary building. The equipment was properly labeled as being a
         temporary modification.
         The inspector noted that this radiation monitor power supply was previously placed in

l maintenance rule category A.1 due to repeated failures of the power supply. The station is l continuing to monitor the equipment performance.

                                                                                                                I
            c.      Conclusions                                                                                 l

l The inspector determined that the licensee properly identified that the WRGM was i inoperable and properly entered the action statement. The increased sampling frequency l ' ~ was very conservative with an excellent safety perspective in evidence and the addition of

         the portable sampling equipment provided excellent backup information. The failed power

l supply was promptly repaired and returned to service. The inspector noted strong

         management involvement in the repair process to ensure that the instrument was promptly

'

         returned to service.
                                                 II. Maintenance
         M1          Conduct of Maintenance
          M1.1 Review of the Ten-Year ISI Program Status

l l a. Insoection Scope ,

         The inspector reviewed the status of Seabrook Station first ten-year American Society of
;         Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (B&PVC) Section XI
inservice inspection (ISI) program plan at the beginning of the third period of the first ten-

4

          year interval. The inspector reviewed the quality of preparation for monitoring the program

i ! L __

                                  . _ . -      .  - -.         . _ - - -.     -             - .-

l ! l- !

                                                     7
  and the status of the inspection activities targeted for program completion at the end of
  the second period of the first ten-year interval.
    b.    Observations and Findinas
  The inspector found that the program plan in effect at Seabrook Station meets the

l '

  regulatory requirements of 10 CFR 50.55a(g). The first ten-year interval ISI program has       !
                                                                                                 '
  been in effect since the start of commercial operations, 8/19/90. The schedule was found
  to be in accordance with Program B of IWA-2400, ASME B&PVC Section XI,1983 Edition
  and Addenda through Summer 1983.
                                                                                                 l
  The inspector found that the program plan covered the first ten-year interval performance
  requirements for non-destructive examinations (NDE) of Code Class 1,2, and 3                   i
  components and their supports under ASME B&PVC Section XI Subsections IWA., IWB,               !
  IWC, IWD, and IWF. Also, in effect at Seabrook Station is the augmented ISI program
  indicated in the Updated Final Safety Analysis Report (UFSAR), Section 6.6.8. to protect
  against failure of high energy lines penetrating the containment structure.
  In the Seabrook ISI program plan, the inspector found a comprehensive listing of applicable
  codes, programs, manuals, and administrative controls (personnel qualification, procedures,
  records, and reports). Exceptions to ASME B&PV requirements were indicated for Class 1,        l
  2, and 3 system components and their supports. The programs, manuals, administrative           i
                                                                                                 I
  plans were found to clearly document inspection expectations.
  The inspector found the implementation of all elements of the program to be on schedule,
  and in accordance with rules of ASME B&PVC Section XI Program B of IWA-2400.
  Licensee expectations for completion of the program elements at the conclusion of the first
   10 year interval is good,
    c.    Conclusions
  The first ten-year ASME Section XI ISI program plan status at the beginning of the 3rd         i
  period of the first interval is within the targeted schedule and consistent with the
  requirements of Section XI of the ASME B&PVC, and 10 CFR 50.55a(g). Licensee
  expectations for completion of the program elements at the conclusion of the first 10 year
  interval is good. The program plan was well prepared, documen+ed, and implemented.
  M1.2 Observation of Inservice inspection (ISI) Activity
    a.    insoection Scooe
  The inspector observed and/or reviewed the results of ISI at the plant planned during

i OROS. This included the following: l l l l

                                                                                                 1
                                                                                   __       _
   ,
  .
                                                  8
       b.    Observations and Findinos
     ISI of Reheat System Pioe-to-T Weld
     The inspector reviewed the penetrant testing (PT) and ultrasonic testing (UT) of the Reheat
     System (RHS) pipe to T weld, Component RH0180-01-01, Class 2, Drawing 1-NHY-
     800180lSI Revision 5, Joint #1. The PT included cleaning, lighting used, surface
     condition, surface temperature, gage identification, and post examination cleaning. The
     examination used Spotchek SKC-S cleaner / remover, SKL-HF penetrant, and SKD-S2
     developer. The weld and .5 inches on each side were examined. The examination was
     properly performed. Qualification and review signatures were verified. No reportable
     indications were noted.
     The inspector reviewed the UT process and examined the calibration data for the Stavely
     Sonic 13b instrument and the KRA (.5 inch 2.25 mhz shear) and Megasonics (.14x.30 4
     mhz longitudinal) search unit using Sonotech Ultragel 11 couplant. The examination was      ;
     properly performed. Qualification and review signatures were verified. No reportable
                                                                                                 '
     indications were noted.
     ISI of Main Steam Line Elbow-to-Pioe Weld
     The inspector observed and reviewed the main steam line (MSL) elbow-to-pipe weld MS
     4000-02 09 magnetic particle test (MT) and UT results on weld MS 4000-02 09, class 2,
     and code category augmented C5.51, as required in the UFSAR, Section 6.6.8.
     The inspector observed the MT examination performed on the MSL elbow-to-pipe weld and
     found the examination to be correctly performed in conformance to procedure No.
     ES1807.003 using a Parker Yoke and dry red particles under a flashlight and drop light.-
     The joint was examined in as-welded condition. No reportable indications were noted.
     The inspector reviewed the qualifications of the NDE examiners and found them to be
     acceptable.
     The inspector observed the UT examination performed on the MSL elbow-to pipe weld.
     The UT calibration record for the Stavely Sonic 136 instrument, and the KBA 2.25 mhz
     shear wave search unit, were reviewed and found to be acceptable. No reportable
     indications were noted. The inspector reviewed the qualifications of the NDE examiners
     and found them to be acceptable.
     ISI of Reactor Coolina System "C" Pumo Fivwheel
     The inspector reviewed the results of a UT inspection on the reactor cooling system (RCS)
     "C" pump flywheel. The ultrasonic calibration record shown on data sheet 97-25-053 for

! the Stavely Sonic 136 instrument, and KBA 2.25 mhz longitudinal pickup were found to be l acceptable. The qualification and review signatures were verifiM. No reportable

     indications were noted.
,

! l l l l

          ___--__                  _     _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - . _ _ _ _ _          _
,

.

                                                                                                        9
    Snubber Functional Test Failure
    The inspector examined the results of a failed MSL class NNS-1 snubber 5929-RM-1
    functional high drag test. The failure was due to internal corrosion, and the snubber will be
   replaced with a Phoenix Hydraulic Snubber. Functional tests were performed of 10% of
   the same size and type of snubber. This expanded sample all passed their functional tests.
      c.          Conclusions
   ISI examinations found no reportable defects under PT, MT, and UT. Reheat System Pipe-
   to-T Weld, Main Steam Line Elbow-to-Pipe Weld, and Main Steam Line Elbow-to-Pipe Weld.
   The snubber ISI found only one case of failing the functional test, and the snubber was
   replaced. The tests were performed in accordance with ASME B&PVC Section XI rules and
   NRC regulations. No defective welds were found.
   M1.3 Steam Generator Tube Eddy Current inspection Preparation
     a.           Insoection ScoR2
   The inspector reviewed the history of plugged SG tubes since the beginning of commercial
   operation including review of the plugging history of eddy current (E/C) inspection of SG
   tubes, and the basis for the planned E/C inspection during OR05.
     b.           Observations and Findinas
   The inspection was directed at an assessment of the tube plugging history to-date, and the
   plans for the E/C inspection of SG tubes which was scheduled to start shortly.
   On review of the plugging history of SG tubes, the inspector found the following tubes
  have been plugged:
                         Steam Generator "A"                                                         12 tubes
                         Steam Generator "B"                                                         6 tubes
                         Steam Generator "C"                                                         13 tubes
                         Steam Generator "D"                                                         5 tubes
  Although the number of tubes requiring plugs is low, the inspector recognized that the
  operating life is less than 7 years. Most steam generator degradation problems have been
  found only after longer periods of operation. The E/C results to date indicate wall thinning
  attributable to flow induced vibratory relative motion between the tube and its intended
  support.
  The SG E/C inspection during OROS will consist of full length bobbin inspection of 100%
  of the tubes in SGs "B" and "C". All these tubes had been previously inspected, and all
  tubes with identified anti-vibration bar (AVB) wear from previous inspections were
  reinspected in May, 1994. 24 AVB flaws were detected in SG "B" and 44 AVB flaws
  were detected in SG "C". On the basis of assessments of flaw growth rates, the licensee
  estimated the remaining wall after two cycles of operation and concluded that four tubes in
                                                                                                                - _____________ _
      ..                                                 .. .         .        .          .
 3
                                             .                                                    _
 .
                                                  10
   SG "B" and 6 tubes in SG "C" will require plugging during this outage in addition to 3 more
   tubes in each of SGs "B" and "C" having more than one AVB flaw of at least 20%.
   Additionally, Seabrook plans to perform rotating plus point probe inspection at the top of
   the tubesheet on 50% of the hot leg tubes of SGs "B" and "C", where circumferential
   cracking can occur, 50% rotating probe inspection of the row #1 U-bends, and a small
   sample of rntating probe inspection of dents, dings, tangential flag signals, and free-span
   signals. Two plugs will be changed in SG "B", and 3 plugs will be changed in SG "C",
   both in the cold side due to material susceptibility to cracking.
   Most of the plugged tubes are a result of AVB wear or a result of manufacturing defects.
   AVB degradation can occur when the AVB clearances are excessive, and allow the
   supposedly restrained tubes to move in a vibratory manner when acted upon by the flow
   stream. This was a phenomenon carefully investigated by Westinghouse at the Research
   and Development Laboratories in tests of U-tubes in flow environments simulating that in a
   SG.
     c.    Conclusions
   The inspection program was conservatively planned, and consistent with ASME Section XI,
   Reg. Guide 1.83, Plant Technical Specifications, Electric Power Research Institute (EPRI)
   Examination Guidelines, and licensee responses to Generic Letter 95-03. Seabrook
   engineering has prepared an E/C inspection based on an engineering evaluation of wall
   thinning rates estimated by past E/C data and an acceptance criteria established for
   remaining wall required for continued operation.
                                                                                                    1
   M1.4 Pressurizer Head-to-Shell Ultrasonic Test                                             -     I
     a.    Insoection Scoce
   The inspector reviewed preparation for pressurizer upper head-to-shell weld UT
   examination using Time of Flight Diffraction (TOFD) technique qualified at the EPRI NDE
   Center in Charlotte N.C. expressly for this application. (This inspection was documented in
   NRC Inspection Report No. 50-443/97-02, Section Ill.E. 2.1.)
   NRC inspection of the UT data evaluation for the pressurizer shell to upper head weld was
   done on June 11-12, at the Seabrook site, after the UT data acquisition was complete and
   the data evaluation was in progress,
     b.    Observations and Findinas
   The inspector reviewed the results of the qualification tests conducted at the EPRI in order
   to form a basis of comparison of the qualification process at the Seabrook site. A

l

    calibration block was constructed for the Charlotte qualification process that duplicated the
    nominal dimensions and materials of the pressurizer. Because of the sloping geometry at
   the head to shell taper, it was necessary to use the UT technique called TOFD to have
    repeatable capability for near-full volumetric flaw detection.
                                                                     --                . . _ . . ..
 .
                                                  11
   The inspector walked-down the TOFD set-up within the containment after shut down of
   the plant for ORO5. The equipment used was identica! to that used in Charlotte, as were
   the three NDE technicians who were qualified using the same equipment. The inspector
   asked the technicians to reproduce the image of a weld flaw found in Charlotte, and found
   the resulting picture was identical to that taken during the initial qualification process.
   During the requalification process within the containment, the licensee found that the
   mockup used in the process qualification was built to nominal drawing dimensions of the
   pressurizer, and not to the "as-built" dimensions of the pressurizer at the head-to-shell
   juncture weld. As a result, the licensee used an alternate procedure to provide for an
   acceptable weld examination. During the inspection, the inspector reviewed the UT
   transducer positions used during the weld examination, sampled the UT findings and
   compared the UT responses from pre-existing reflectors in the weld area for the techniques
   used. The data from the TOFD,0,60 and 70 degree examinations were appropriately
   confirmatory. No service induced indications were identified in the weld area and the pre-
   existing indications were within construction acceptance limits.
                                                                                                    l
      c.    Conclusions                                                                             I
    Preparation for examination of the pressurizer head-to-shell weld showed good capability in
   utilization of technical resources. Weakness was shown in allowing the utilization of
   nominal drawing dimensions, instead of as-built dimensions, for weld inspection
   qualification models. This error was self-discovered, and steps were taken to provide a
    satisfactory alternate inspection procedure for the pressurizer head-to-shell weld ISI
   requirements.
                                                                                                    1
    M1.5 Encapsulation Vessel for Recirculation Sump Isolation Valves (CBS-V8 an't V-14)            I
      a.    Insoection Scone (62707)
    On June 11, the licensee made a 4 hour Non-Emergency Report to the NRC under 10 CFR
    50.72 (b)(2)(i), to document the failed leak rate test for the Encapsulation Vessel for         i
    Recirculation. Sump Isolation Valves CBS-V8 and V14. On June 16, the inspector
    inspected the work being performed on these valves. The Local Leak Rate Test (LLRT)
    requires that the valves to maintain a test pressure of 52 psig. The leakage on both
    vessels were from joints that were not disassembled during this outage. The encapsulation
    vessels consist of three flanged sections, joined at two places, each with a groove and an

i O-ring to prevent leakage.

      b.    Observations and Findinas
    The inspector identified in the -26'O elevation mechanical penetration area of the Primary
    Auxiliary Building (PAB), that maintenance workers were tossing the bottom flange bolts of
    the encapsulation vessel for valve CBS-V14 into a bucket. These safety-related bolts were
    landing on top of each other and some were missing the bucket and hitting the wall. The
    inspector questioned the workers about this practice. They responded that they were
    awara that these bolts and the encapsulation vessel were safety-related components,

, however, they did not feel that tossing the bolts had the potential for causing damage to ! t

   .
  .
                                                     12

,

     the bolts, and increasing the possibility for flange leakage. The inspector then expressed
     his concern and informed the workers that this was not an acceptable practice. The

,

     workers then proceeded with their work in an acceptable manner.

4

     Management directed that the bolts be inspected for damage and initiated an adverse
     condition report (ACR) to evaluate the poor maintenance practice. All 48 bolts were
     inspected and tested. The licensee determined that none of the bolts exhibited damage
     from the poor work practice that was observed by the inspectors. However, a total of 25
     bolts were replaced due to corrosion. After the first repairs were made to prevent flange
     leakage, the vessel for valve CBS-V8 failed the LLRT test once more while the vessel for
     valve CBS-V14 failed two more times after repairs were made. The licensee issued Minor
     Maintenance (MMOD) 97-0577 to redssign the gasket to address these repeated failures.
     The inspector found this document to be adequate. After implementation of this                 )
<
     modification, the encapsulation vessels passed the required leak test.                         '

J

     Per UFSAR, Section 6.2.4.1, and Technical Clarification TS-009, dated 3/2/94, the subject

, encapsulations are not required to be in place to ensure containment integrity, because

     they are not in direct contact with containment atmosphere, but rather, they are designed
     to prevent release of any leakage from the recirculation sump isolation valves CBS-V8 and
     V14, or related piping to the environment during design basis accident conditions. The-
     valves are, however, designed to withstand the maximum calculated containment internal         j
     pressure (50 psig) for the design basis loss of coolant accident, as described in the UFSAR.
                                                                                                     l
                                                                                                     l
        c.    Conclusion
     The inspector concluded that the tossing of the safety-related encapsulation vessel flange
     bolts was a very poor maintenance practice and could have contributed to further flange
     leakage. Furthermore, the fact that the workers did not think that this was a bad practice
      when questioned by the NRC staff, is of concern. However, since this incident appears to
      be an isolated case at this time, the corrective actions performed by the licensee to inspect
      all 48 flange bolts, to counsel the individuals and the entire mechanical maintenance crew,
      were found to be adequate.                                                                    )
     M2        Maintenance Support of Facilities and Equipment
      M2.1 Foreign Material Exclusion (FME) Controls
      a.       Insoection Scooe (71707, 62707)
                                                                                                    l
                                                                                                    l
     The inspector evaluated Seabrook Station administrative controls to prevent foreign            l
      material intrusion into plant structures, systems, and components. These observations
      took place prior to and during OR05. The objective was to follow-up and evaluate the
      adequacy of Seabrook's corrective actions and enhancements implemented to address a
      previous NRC violation identified in inspection Report 96-02. This violation was closed by
      NRC Inspection Report 97-01 in April 1997.
                                                                   - - - - . - - - - - - - - -
   ,
  .
                                                    13
      The inspector reviewed the foreign material exclusion (FME) procedure (MA 3.4),
      interviewed personnel, and performed several plant walkdowns in all plant areas, including
      the spent fuel pool and the containment. Major evolutions observed included; core offload
      and reload, emergency diesel generator (EDG) overhauls, main turbine and generator work,
      primary cooling water heat exchanger replacement, emergency feedwater turbine driven       j
      pump governor valve replacement, reactor coolant pumps motor maintenance, and main
      steam safety valve testing.
                                                                                                 1
      b.      Observations and Findinas
      The inspector determined that Seabrook personnel, including contractors and vendors, had
      embraced a very aggressive FME controls program, and that extensive manpower and
      resources were dedicated for this effort. The inspector observed that boundaries which
      included FME tape, signs, and rope were established to monitor and control every object,
,
      tool, or equipment used to perform the tasks. A designated and well trained individual was

'

      dedicated and posted at each job site for this purpose. In addition, every small tool was
      secured with a lanyard to the worker to prevent it from being inadvertently dropped into
      the system or component. The inspector also observed that prompt notification and
      corrective were taken to document and address issues of deficient FME controls. For
      example, on May 9, the inspector noted that two out of three replacement safety valves
      stored in the east steam pipe chase had lost their FME covers. The licensee promptly
     evaluated the situation, replaced the FME covers and ensured that a visual inspection was
      performed prior to installing these valves. Also, when an operator inadvertently dropped a
     pen into the reactor cavity, fuel movement was suspended until the item was recovered.
     An ACR was initiated for each issue identified.
     c.       Conclusion
     The inspector concluded that the current FME program at Seabrook is excellent and that
     considerable manpower and resources have been dedicated for this effort.
     M2.2 Diesel Generator-1 A Monthly Operability Surveillance Run
        a.    Insoection scooe
     On April 30, the inspector observed a portion of the monthly diesel generator operability
     run for emergency diesel generator (DG-1 A) as directed by station procedure OX1426.01,
     DG-1 A Monthly Operability Surveillance, in the control room and in the diesel generator
     room. The inspector observed the performance of the control room operator during the
     surveillance testing and verified the proper operation of the diesel generator support
     equipment during the surveillance run in the diesel generator room.
       b.    Observations and findinas
     The inspector observed that the station operator conducting the testing in the control room
     was knowledgeable of the procedure requirements and was properly monitoring the
     equipment parameters on the main control board. All required diesel parameters were
     taken during the test run with no abnormal readWs identified during the test. The
                    _ _ _ _ _
                                           . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
,

.

                                                                                   14
    inspection tour in the diesel generator identified no discrepancies and it was observed to
   operate properly. The room was found clean with no fire hazards present and no visible oil
   leaks. The testing concluded satisfactorily with no deficiencies identified by the inspector.
             c.            Conclusions
   The inspector determined that Seabrook Station operations personnel properly tested an
   important safety-related system as directed by station procedures in a safe and deliberate
   manner. All equipment was observed to operate properly and the testing was
   accomplished satisfactory.
   M2.3 Pressure Tube Failure (Radiological Spill)in Primary Auxiliary Building
             a.            Josoection Scone
   The inspectors reviewed the licensee's actions to recover from a spill of radioactive water
   in the PAB that occurred on May 27, due a failure of an under-rated instrument test tygon
   tube. The failure occurred in the tubing for Flow Transmitter CS-FT-121 in the reactor
   coolant charging system after a temporary pressure gauge with a much lower pressure
   rating was installed for Emerg icy Core Cooling System (ECCS) valve testing. The
   inspector also reviewed the licensee's actions to past tubing failures to determine if the
   previous corrective actions were appropriate for the event to prevent reoccurrence. The
  inspector also reviewed the ACR documenting the event and interviewed the instrument           i
   and controit (l&C) personnel involved in the installation of the temporary tubing.            I
           b.              O_bservations and Findinas
  The inspector determined that the licensee's initial response to the event was good. A
  station engineering supervisor was egressing through the area and identified the leak. He
  promptly informed the control room and remained in the area to prevent anyone from
   walking through the contaminated area. The radiation controls personnel promptly
  responded to the event and limited personnel access to the contaminated area. Cleanuo
  efforts were promptly initiated and radiation boundaries were installed to limit access to
  the contaminated area. The highest contamination reading was 200,000 counts per
  minute above background. Approximately 30 gallons of water were spilled. The inspector
  verified that the area was properly monitored with appropriate surveys and radiation
  postings.
  The licensee determined that the person involved did not install the appropriate tubing for
  the pressure application, in spite of departmental supervisory guidance and coaching. The
  installed tubing was rated for 250 pounds per square inch (psi) instead of the high pressure
  tubing (3000 psi) required for the task. The high pressure tubing has a very distinctive
  color from the one that was used and the department supervisor could give no apparent
  reason for the error. The l&C Supervisor did determine that the person did not willfully
  install the incorrect tubing. In addition, it was identified that several similar events had
  previously occurred.
     - _ _ _ _ _ _ _ - _ _
     . - -       - - - - - _._.--                                           - . . -     _
                                                                                           - . - . . . . . .          .-
 t
; .-
 !
  i
                                                                  15
            The inspector determined that the following events have previously occurred involving

j temporary tubing failures:

             *            December 6,1995: Tubing burst for RH-FE-610 due to tubing with an inadequate

} rating - Installed 250 psi tubing vice 3000 psi tubing

j            *            June 20,1995: Tubing burst for the filtration unit for Main Steam isolation Valve -

l high pressure hydraulic fluid -Installed 100 psi tubing vice 3000 psi tubing

;            *            June 1,1995: Tubing burst for 345 KV circuit breaker air trouble alarm due to
'
                          improper valve lineup - Installed 250 psi tubing

4 4 * April 15,1994: Tubing burst for Local Leak Rate Testing test panel due to opening

 !
                          the valve on the nitrogen bottle too fast
            The inspector reviewed the root cause evaluation for the December 6,1995, spill event

? - that was attributed to improper test tubing. Human error was the root cause determined to i be the major causal factor. This analysis failed to determine if a programmatic issue

            existed or if other procedural modifications were necessary.
c. Conclusions

.

            The inspector determined that the radiation protection department personnel properly

j responded to the event and provided the proper controls to recover the area that was j contaminated. The I&C department installation of improper tubing in spite of severa' past

i           problems temporary tubing appears to have serious implications concerning inadequate

l corrective actions and management oversight to prevent reoccurrence. The potential for l serious personnel injury is a major concern. This situation is considered a significant

weakness in the licensee corrective action program, and is considered a violation of 10CFR

l 50, Appendix B, Cnterion XVI, Requirements. (Violation 50-443/97-03-02)

.
                                                           Ill. Enaineerina

l E1 Conduc of Engineering ] '

            E1.1           Modification of Primary Component Cooling Water Heat Exchangers
l
               a.          Insoection Scoce
            On May 21, the inspector observed a portion of the work activities in the PAB,in
,           preparation for replacement of the "A" primary component cooling water (PCCW) heat

! exchanger, as directed :,tation design change request (DCR 96-016). The heat exchangers l' are being replaced due to repetitive degradation of the heat exchanger tube material which

l           required retubing. The original tube material was a 90/10 copper nickel composition. The
j           new heat exchanger tube materialis titanium, which has better corrosion resistance
 i
             characteristics. The inspector also reviewed the DCR package for completeness and

! reviewed the accompanying safety evaluation screening documentation. The work site ,

!
                                    -  __      _
                                                  .                   -         __                            -. . _.
    . ._      .            __     _ _.     _ _.              . __   __       . _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ __
  ,
 .
                                                         16                                                         I
         was inspected during preparations for removal of the 'B' train heat exchanger and also
         during the installation of the 'A' train heat exchanger. The inspector also verified FME
         controls and control of contractors during the inspection. Interviews were also conducted
         with the task construction supervisor on several occasions in the field on work progress,
           b.    Observations and Findinas

!

         The inspector noted a very strong management oversight of contractor personnel and of
         work activities performed during the installation phase of the heat exchanger replacement.
         The proper FME controls were in place for the system piping and new heat exchanger. A                      l
         fire watch was stationed in the area during welding / cutting operations and security                      I

l '

         personnel were controlling access when the building roof hatch was opened. The control
         of the crane for lifting the old and new heat exchangers was well controlled, and when a
         question regarding the lifting capacity of the crane was raised, the lifting work was

,

         stopped until all questions were resolved. The licensee demonstrated excellent job                         ,

l planning when it was determined that a portion of the heat exchanger support plate would ' f

         interfere with permanently installed piping during removal of the old heat exchanger. The
new heat exchanger was modified to allow proper installation without in field modification.

l The work area was kept in a very clean condition during the period of removal and l installation of the heat exchangers. The inspector verified that the opposite train of PCCW

         was maintained in an operable status during the replacement process.

I c. Conclusions j The inspector determined that the licensee properly performed a very significant

         modification to the stations permanently installed equipment. The work was well
         controlled and the safety evaluation was thorough and properly documented. The system
         engineers were directly involved in the task and provided excellent guidance to the
         personnel that were installing the equipment. The inspector did not identify any
         deficiencies during inspection of this activity.
         E2      Engineering Support of Facilities and Equipment
         E2.1    Main Steam Safety Valves Testing
           a.    Insoection Scooe (71707)
         On May 9, the inspector witnessed portions of the operability verification test for the Main
         Steam Safety Valves (MSSVs). This test was performed during Mode 1 with the plant at
         approximately 70% of rated thermal power, using operating procedure EX1804.041, Main
         Steam Safety Valve In-place Setpoint Verification, and work request RTS 97RE00119001.
         The procedure requires as found set point verification within i 3% of the lift setting, and
         provides instruction for subsequent lift setpoint adjustments if necessary to meet the
         values described in TS Table 3.7-2. The test also verifies that the as-left lift setpoint is
         within i 1 % of the lift setting. This test is performed using the Furmanite Trevitest
         System.

1 !

  .
 .
                                                     17
        b.      Observations and Findincs
     The inspector attended the pre-avolution briefing, held discussions with involved licensee
     and the applicable contractor (Farmanite) personnel, reviewed the procedure, and
     observed testing of four safety valves. The inspector reviewed the test results and found
     that as-found and as-left acceptance criteria were met. The inspector noted excellent
     planning and control by the test coordinator, good communication with the control room,
      and management oversight. In addition, adequate personnel safety measures were                 l
     implemented to prevent injury to personnel in case of equipment malfunction. During pre-
      briefing, the licensee demonstrated strong safety measures by including identified industry
     experience / problems in their discussions and taking applicable corrective actions to prevent
     similar events.
      During this review, the inspector noted that the Furmanite test equipment had been
     upgraded and was different from the original test equipment. The licensee had performed         ,
     a safety evaluation (SE) per 10 CFR 50.59 requirements for the original test equipment, but     I
     did not perform a new SE for the upgraded test equipment. Upon review, the inspector            i
      concluded the new equipment is much lighter and permits the valve being tested to fully
     lift, if required, unlike the original equipment. With the original equipment, the valve had to
      be declared inoperable for the test duration, because the valve lift was limited to 50% of
      full travel. The original evaluation takes credit for the limited valve lift of 50% so that in
     the unlikely event that a safety valve were to stick in the open position, the total steam
     released would be less than the maximum release of 970,000 lbs/hr as analyzed in UFSAR,
      Section 15.1.4. It also states that the lifting of a maximum capacity safety valve is
      bounded by the analysis.
    ' Followup inspection revealed that station procedure PA3.5, Administisi.on of Procedures
      and Forms, controls the preparation and revision of station procedures. The existing
      procedure that was used to test the main steam safety valves was revised prior to this
      outage. The document review and approval cover sheet on the procedure lists four 10
      CFR 50.59 applicability questions which may be answered under specified conditions.
      Answering no to these questions eliminates the need for further 50.59 screening. These
      conditions require that the procedure is prepared using the safety evaluation of another
      docrnent such as Design Coordination Report (DCR), Minor Modification Temporary
      Modification (MMTM), Temporary Setpoint Change on prior revision of the procedure. The
      safety evaluation must have been reviewed and remain valid for the procedure and also the
      procedures references the DCR/MMOD, temporary modifications, temporary setpoint
      change, prior revision of the procedure or other documents used to prepare the procedure.
      The inspection determined that using this guidance , licensee personnel were not required
      to document a current review if it was decided that a prior revision of the document
      contained an appropriate SE review.

! c. Conclusions l

      The inspector determined that although no SE was performed for the new test equipment,
      there were no safety consequences, because the inadvertent lift of a Safety Valve is
      bounded by the accident analysis presented in the UFSAR, Section 15.1.4.2. However,
      the in.spector concluded that the reliance on an or:ginal SE presents a potential weakness in
                                 ,_
                                                                                                __

.

                                                18
 the licensee's SE process. The inspector determined that a programmatic issue may exist
 in the station procedure revision process and this item will be inspected in a subsequent
 inspection. (IFl 50-443/97-03-03)
 E2.2 Leak Rate Test Failure of Containment isolation Check Valve CBS-V18
    a.    Insoection Scoce
 The inspector evaluated Seabrook's actions to address the Local Leak Rate Test (LLRT)
 f ailure of the containment building spray (CBS) check valve CBS-V18, the subsequent
 valve internal visual inspection, the corrective actions performed to repair the valve, and
 the correctness of Seabrook's reportability of this issue. CBS-V18 is the 'B' CBS train
 inside containment isolation valve for penetration (X-15). This penetration is also provided
 with an outside containment isolation motor operated valve (CBS-V17). A similar
 arrangement exists for the 'A' CBS train penetration (X-14), where motor operated valve
 CBS-V11 and check valve CBS-V12 provide the containment isolation boundary.
    b.    Observations and Findinos
 On May 17, with the Unit in Mode 6 (refueling) valve CBS-V18 failed the LLRT. Procedure
 EX1803.003, " Reactor Containment Type B and C Leakage Rate Tests", requires that nc              ,
 individual penetration leak rate exceeds 37 scfh. A visual inspection performed by tne            l
 licensee, on June 5, determined the valve disc was stuck in the "Open" position.
  Inspection of similar valve in the opposite train (valve CBS-V12), revealed that although the
 disc was in the proper " Closed" position, and the valve passed the LLRT test, it was also
 susceptible to binding when the disc was manually activated to the open position. On
 June 10, the licensee made a 1 hour non-emergency report to the NRC under 10 CFR ,                l
  50.72 (b)(2)(i).                                                                                 l
  Both valve CBS-V12 and V18, are 8"-forged body, swing type, check valves manufactured            ,
  by Velan Corporation. There are seven simi;ar valves installed at Seabrook, with only            !
 these two valves being used in a safety-related system (Containment Building Spray), and          !
 the remaining five being used in the Condensate and Main feedwater Systems. The
  licensee considers valves CBS-V12 and V18, unique because they were modified during
  the construction phase, under Engineering Change Authorization (ECA) # ECA-19802647B,
  dated May 19,1986, to replace the valve's disc, hanger, and hanger ring. The inspector
  verified that both valves have satisfactorily passed all six (6) LLRT tests performed
  previously. The licensee's inspection performed on June 5, per ACR 97-1448, determined           l
  that the disc in both valves, were impacting the valve body at several points in the upper
  throat. Preliminary evaluations performed by the licensee, determined that an incorrect
  disc hanger may have been installed on both valves during the construction phase under
  ECA-19802647B. To correct this problem, the licensee machined both the incorrect
  hangers and the back side of the valves discs to eliminate any contact points with the
  valve body, as recommended by the valve manufacturer. Both valves passed the post
  modification LLRT on June 10. CBS-V18 was last disassembled and inspected in 1995
  during the fourth refueling outage, and the penetration passed the LLRT test. The licensee
  concluded that CBS-V18 failed during one of the quarterly stroke testing of the up-stream
  (outside containment isolation valve) MOV-CBS-V17, performed during the last operating
   --     - - - - _ _ -           . _ - . - _ - - - - - . _ - - . -             ..           -        _ - _ - . - -
                                                                                                                    f
 .
                                                                    19
        cycle (cycle 5), since the pressure head of the Reactor Wcter Storage Tank (RWST) is
        enough to open the check valve. The licensee's root cause evaluation will be reviewed by
        the inspector at a later time, and will be tracked as a follow-up item. (IFl 50-443/97-03-04)
        The inspectors initial concern was the timing of the reportability made by the licensee on
        6/10/97, for the failed valve, which was first identified on 5/17/97 via the LLRT. The
        licensee had initially taken the position that no reporting requirements exist for the failed
        LLRT test on valve CBS-V18, based on NRC's Ruling No. RIN 3150-AF 18, which states in
        part that reporting "would be required when the total containment as- found, minimum                        ,
        pathway leak rate exceeds the limiting condition for operation (LCO)in the facilities
                                                                                                                     '

l Technical Specification.", and incorporated this criteria in their LLRT test program, which is l implemented under procedure EX1803.003, and the Station Leakage Test Reference

        Manual (SLRT). TS Section 6.15, " Containment Leak Rate Testing Program", states that

l

        for type B and C tests (which valves CBS-V12 and 16 are) the acceptance criteria for total

i leakage of all combined penetrations shall be less than 0.60 La (443.6 scfh). To meet this - l

        requirement, the licensee's program has stabilized a limit to each individual penetration at                ;
         <37 scfh (.05La). Since the local leak rate testing demonstrated that MOV met the
                                                                                                                     '

,

        leakage criteria for this penetration ( < 37 scfh), the licensee determined that no

l reportability under the LLRT program was required. The licensee did determine that this l

        condition was reportable pursuant to 10 CFR 50.72 utilizing NUREG-1022 Draft Rev.2,
        which identifies a similar situation being reportable under 10 CFR 50.72 (b)(2)(i), as an                   ;
        event, found while shutdown, that had it occurred while the reactor was in operation,

! ' would have resulted in the nuclear power plant, including its principal safety barriers, being .

                                                                                                                    '
        seriously degraded or being in an unanalyzed condition that significantly compromises plant
        safety". This guidance lists the loss of containment isolation valve function during plant                  ;

l operation as a condition that results in a loss containment function or integrity. The failure

        of the check valve in the open position is significant because during a design basis loss of
        coolant accident (LOCA), coincident with a loss of power and a single failure of the "B"
        EDG a leakage path through penetration X-15 (lost of containment boundary) would have                        i
        been possible via the failed check valve (CBS-V18).
          c.            Conclusion                                                                                   ,
        The inspector concluded that Seabrook's evaluation of the failed LLRT for containment
        spray valve CBS-V18, the subsequent corrective actions to machine the valve disc and
        disc hunger, to prevent wedging of the valve disc with the body were adequate. Also the
        implementation of the applicable corrective actions for similar identified valve CBS-V12
        was prudent. However, the inspector concluded that the licensee's failure to promptly.
        report this self-identified situation as required by 10 CFR 50.72 is a minor violation and is
        treated as a non-cited violation due to meeting the requirements of Section IV of the NRC
        Enforcement Policy. (NCV 50-443/97-03-05)                                                                   '

I

        E2.3 Operating Cycle 5 Failed Fuel Rods
           a.           Insoection Scoce

l The inspectors reviewed the licensee's response to the identification of leaking fuel  ; i assemblies during Cycle 5 operations. The findings and recommendations of the root 1

                                -                                      .
  *
                                                                                                  !
                                                                                                  l
                                                                                                  .
 *                                                                                                l
                                                    20
    cause investigation team were reviewed to determine the appropriateness of the findings
    and to determine if a generic failure was involved due to this type of failure mechanism.
      b.    Observations and Findinos
    On December 10,1996, the licensee identified that reactor coolant system noble gas and
    iodine activity had increased by a significant factor from the previous steady state levels.
    These increases were well below the TS limit of 1 microcurie per gram dose equivalent l-
    131. However, this was a very clear indication of a failed fuel rods. From the date of the
    original observation until the end of the cycle, the reactor coolant system (RCS) fission
    product activity continued to slowly increase. in addition, there were indications that
    additional fuel pins had also f ailed. At this time it was believed that the failed fuel pins
    were located in the second burn fuel batch.
    Subsequently, during core offload special fuel sipping equipment revealed that four fuel      l
    assemblies from a first burn batch of Westinghouse Vantage 5H Zirlo clad fuel ~ assemblies    '
    contained f ailed rods. After the identified leaking fuel assemblies were transported to the
    SFP, followup ultrasonic testing of the assembly fuel pins determined that five failed fuel

,

    pins existed among the four assemblies. (One failed pin in three assemblies and two failed

l pins in one assembly). The leaking fuel rods were identified to be first burn fuel

    assemblies, Westinghouse Vantage 5H with Zirlo Cladding, 4.8% enrichment, assemblies

l with 128 IFB A (boron burnable poison coated fuel pellets) fuel rods, next to thimble guide l tubes and fuel rods exposed to above average core power. When the licensee's personnel

attempted to remove the leaking fuel pins, three were found broken in the mid point of the
    rod, approximately at the same area, between the assembly fourth and fifth grid. The
    other two leaking rods were successfully removed from the fuel assembly and stored in the
    spent fuel pool. The two intact fuel pins were also found to have breaches of the fuel
    cladding, but not in the same area as the broken fuel rods.
    The safety consequences of a breach in the fuel cladding is that fission product gases in
    the fuel rods are released into the RCS and this increased radioa       ity represents a
    potential impact on the plant safety analysis. The inspector rev. .ed several daily plant

l

    radiochemistry logs for the time period that the leakage was occurring and determined that

! station TS limits were not exceeded as the highest reading was approximately 6% of the

    limit.
    The inspectors requested that NRC headquarters review the licensee's root cause

l evaluation to determine the appropriateness of the conclusions and corrective actions and l to determine if a generic issue existed. The regional request was for the determination to l be made prior to plant restart. !

     On June 17, an NRC headquarters Division of Reactor Regulation fuels specialist met with
     Seabrook Station, Yankee Atomic Energy Company, and Westinghouse personnel at the
     station to discuss the findings and licensee's conclusions of the Fuel Failure Root Cause
     Evaluation Report. The specialist determined that although this was the first time this
     many failures occurred in the first burn of the Vantage SH fuel, the failures were well
     enveloped by the plant safety analysis and TS. The licensee root cause evaluation
     determined that a probable cause of the fuel failures was the combined effects of power
                                                 _         _                         -
  ,
 .
                                                   21
    history, core design, and an operational strategy that resulted in interaction between the
    fuel pellets and the fuel cladding. The affected fuel assemblies apparently carried a very
    large load (produced high power) for all of the last cycle. Another potential cause which
    could not be completely eliminated is crud induced corrosion. The most probable cause
    will be determined by future eddy current testing and/or possible hot cell testing.
    The licensee uses incore nuclear instrumentation to assess nuclear peaking factors and to
    perform core flux mapping. Tha inspectors inquired if the licensee had observed excessive
    nuclear peaking factors in the core during Cycle 5 and was informed that no limits had
    been exceeded during any of the regular surveillance. The inspectors had determined that
    the licensee had not extensively reviewed incore nuclear instrumentation data to
    investigate the cause of the failed fuel because no limits had been exceeded during the
    surveillance. The inspectors then inquired where the incore nuclear instrumentation was
    located relative to the fuel assemblies which contained the failed fuel rods. The inspectors
    were informed that assembly G69 (which contained a failed fuel rod) was an instrumented
    assembly. The inspectors reviewed axial flux maps generated from data collected by the       ;

l detector in assembly G69 for December 1995, July 1996, December 1996, and March

     1997.
                                                                                                 l
    Although no limits were exceeded, the inspector observed some unusual fluctuetions in the    !

, December 1996 and March 1997 maps between the fifth and sixth grid where some clad l damage and unusual crud buildup had occurred. .The reactor engineering staff did not

    know the reason for the unusual flux maps at that location. This observation was
    forwarded to the Yankee Nuclear services Division (YNSD) for evaluation. The licensee's
    preliminary assessment attributed the fluctuations to characteristics of the computer code
    used to generate the flux maps.
    To prevent recurrence, the licensee implemented several corrective actions. The remaining
     128 IFBA assemblies were located in lower power regions for Cycle 6. Prior to restart, an
    extended Mode 4 RCS cleanup was completed to minimize crud deposition. The pre-
    conditioning power ramp rate was reduced from 3% per hour to 2% above 20% power.
    To further minimize crud deposition, RCS inventory pH will be increased from 6.9 to
    approximately 7.1 at the beginning of core life. The Vantage SH fuel assemblies that
    exhibited problems during the last cycle (128 IFBA) were removed from the high power
    region of the core to the periphery. Furthermore, no additional vantage SH fuel assemblies
    were included in the new cycle 6 core design.
      c.    Conclusions                                                                           l
    The inspectors determined that the licensee appropriately assembled a very significant root

l cause evaluation team and conducted a very thorough evaluation in an excellent manner. t

    All findings and conclusions were reasonable with very prompt corrective actions. The
    new cycle 6 core design was modified based on the above findings and the fuel assemblies
    that were found to have leak:ng fuel pins were removed from service.

.

    The inspectors had no further questions of the licensee regarding this issue at this time,
    however, core performance during Cycle 6 will be monitored by the inspectors.

4

 e

'.

                                                    22
   E2.4 Failure of Unitized Starters During Surveillance
     a.    Insoection Scope
   The inspector reviewed the licensee's current act!ons to resolve another identified problem
   with unitized starters at the station. A unitized starter failed to properly actuate during
   routine surveillance testing. This problem has been previously identified in NRC inspection
   report (50-443/97-80). Unitized electrical starters are used to e:ectrically start and stop
   motor operated valves and energize other electrical equipment such as fans and heaters.
     b.    Observations and Findinas
   On May 8, Seabrook Station technical support personnel determined that the unitized
   starter for motor operated valve service water (SW) V-140 had failed to properly actuate
   during routine surveillance testing. After station maintenance electricians inspected the
   internals of the unitized starter, a circular clip (E-clip) was found lodged in the contractor
   assembly. The source of the clip was identified as being part of the unitized starter pawl      I
   assembly. The pawl assembly pulls and locks the unitized starter onto the bus electrical
   connections. Seabrook station technical support engineering personnel discussed the             i
   problem of the with the unitized starter vendor and a modification was developed to             l
   replace the E-clip with a jam nut and different spring. Also the existing E-clip and spring     )
   were to be removed to eliminate the potential of E-clip falling into the unitized starter       l
   contractor assembly. The potential of loose parts falling into the unitized starter could
   affect safety equipment operability.
   Station Modification MMOD 97-0553, " Modification to MCC Bucket Latching device", was           l
   incorporated into Seabrook Station electrical maintenance procedure LS0557.09, Revision
                                                                                                   '
   3, "480 Volt Motor control Center inspection, Testing and PM" to perform the field
   installation. Station work orders were initiated to inspect and install the modification on all
   safety-related unitized starters as a first priority. The modification package had a 10 CFR

l

   50.59 evaluation that adequately described the change and its effect on the unitized
   starter. The inspector reviewed the modification package and determined that the proper
   reviews were conducted and that the proposed change scope was adequately described for
   implementation. The non safety-related starters will be modified as the surveillance comes      l
   due. In view of the recent identified concerns with unitized starters and subsequent            I
   category A.1 maintenance rule classification, these actions are appropriate. The licensee is
   currently considenng other options for these starters including replacement, if necessary to
   resolve this issue, and restore the equipment from the A.1 Maintenance Rule category.           i

l The inspectors will continue to review this issue in future inspections. l

     c.    Conclusions

l The inspector determined that Seabrook station personnel properly identified a serious i

   safety concern regarding the unitized starters and conducted prompt corrective actions to
   prevent recurrence.

i

 ,
 .
                                                  23
                                          IV. Plant Sucoort
   R1       Radiological Protection and Chemistry (RPf4C) Controls
   R1.1 Implementation of the Radioactive Liquid and Gaseous Effluent Control Programs
     a.     Insoection Scooe (84750-01)
   The inspection consisted of: (1) tour of radioactive liquid and gaseous effluent process
   facilities, and control room; (2) review of radioactive liquid and gaseous effluent release
   permits; (3) review of unplanned or unmonitored release pathways; (4) review of
   quantification technique for airborne tritium release; and (5) review of the effluent ALARA
   program.
      b.    Observations and Findinas

l The inspector toured control room and selected radioactive liquid and gas processing

   facilities and equipment including effluent radiation monitors and air cleaning systems. All
   equipment was operable at the time of the tour. Effluent and process radiation monitoring
   terminals in the control room and at the HP checkpoint were also operable.
   During review of selected radioactive liquid and gaseous effluent discharge permits, the
   inspector determined that discharge permits were complete and met the Technicd
   Specification /Offsite Dose Calculation Manual (TS/ODCM) requiremen'a for sampling and
   analyses at the frequencies and lower limits of detection established in the TS/ODCM.
   The in.spector noted that there were no unplanned /unmonitored radioactive liquid and gas
   releases since the previous inspection conducted in January 1996. The inspector also
   noted that the licensee had reviewed the effluent control programs continuously to

l implement the IE Bulletin No. 80-10, " Contamination of Nonradioactive System and

    Resulting Potential for Unmonitored, Uncontrolled Release of Radioactivity to Environment."
   The ins actor reviewed the chemistry study and Technical information Document No. 97-
   006," ide Range Noble Gas Monitor (WRGM) Response to Noble Gas Release." The

l Document 97-006 was prepared by tha chemistry staff for response to the ACR 97-0514, ! which dealt with exceeding the alert for the low range of the plant vent WRGM while

   performing routine monthly calibration of the waste gas oxygen monitor. Noble gas was
   purged from the waste gas system to the plant vent prior to calibration of the oxygen

I monitor, as required. The chemistry staff calculated an expected WRGM reading using l actual noble gas analytical measurement results and the conversion factor of the WRGM. l The calculated WRGM reading was 293 Ci/sec and the actual WRGM reading was 360

      Ci/sec (about 19% over responded). The inspector concluded that the comparison
    between expected and actual readings were very good and was acceptable within the
    normal characteristics of a beta scintillation detector.

,

    The inspector requested the licensee to demonstrate its capability for monitoring and
    quantifying the airborne tritium. The licensee calculated the total amount of water loss

' trom the spent fuel pool (SFP) using the makeup water inventory. The licensee assumed

 .
 .
                                                  24
   that water loss was due to an evaporation from the SFP release to the environment via the
   plant vent. The licensee calculated the airborne tritium release using SFP tritium
   measurement results. Calculated airborne tritium released through the plant vent during
   1996 was to be about 23.01 curies. The licensee reported in the 1996 Annual Effluent
   Report that 23.5 curies of airborne tritium was released. The inspector stated that the
   licensee's assumptions and calculation methodologies were good and had an excellent
   airborne tritium monitoring program.
   The licensee recognized a design deficiency of the waste gas system, which would prevent
   expeditious processing of large volumes of waste gas. Therefore, the licensee developed a
   plan to enhance the waste gas system to allow larger volumes of processing in the fall of
    1996. In December 1996, the licensee identified a small fuel defect, which requires
   additional processing capacities for waste gas. On January 10,1997, a task force
   (representatives from chemistry, HP, operations, engineering, outage management, and
   incensing) was formed to review areas where effluent releases could be minimized to as
   low as reasonable achievable (ALARA). This task force met weekly to discuss all waste
   gas systems to increase waste gas hold up time (developed in fall 1996). The inspector
   reviewed the following data to determine the soundness of the effluent ALARA program for
   the refueling outage in May 1997:
    *      iodine dose equivalent trending data and iodine inventory in the reactor coolant
           (iodine source term),
    *      entrained noble gas activities in the reactor coolant and noble gas inventory in the
           reactor coolant and waste gas systems (noble gas source term),
    *      licensee's projected dose calculation results to the public, and                     l
    *      management support to this project.
   Although the projected airborne iodine and noble gas source terms were small and could
   release directly to the environment (it would result in a fraction of TS dose limits to the
   public), the licensee management decided to implement the effluent ALARA program. For
   example, the licensee will use temporary decay tanks and slow purge of the pressurizer,      I
    which would reduce the release rate to the environment, minimizing doses to the public.     l
   The inspector stated that the licensee's effort was an excellent example for the             '
   implementation of the effluent ALARA.
      c.   Conclusions
    Based on the above reviews, the inspector determined that the licensee maintained and
   implemented excellent radioactive liquid and gaseous effluent control programs with
    capabilities to protect the public health and safety and the environment. Furthermore, the
   licensee management support to implement the effluent ALARA program was noteworthy.

l l l i l ,

          _               _       _                                                       ._    __
 ,
 .
                                                 25
   R1.2 Implementation of the Radiological Environmental Monitoring Program
      a.    Insoection Scone (84750-02)
   The Radiological Environmental Monitoring Program (REMP) was inspected against Sections
   3/4.12.1 and 3/4.12.2 of the Technical Specifications (TS) and Regulatory Guide 4.1,
   " Programs for Monitoring Radioactivity in the Environs of Nuclear Power Plants." The
   following activities were conducted to assess the licensee's capability to implement the
   program.
   -
            Review of REMP procedures and ODCM changes which pertain to REMP;
   -
            Review of the land use census results;
                                                                                                   ,
   -
            Review of sample results to confirm sample frequency and impact of the plant on
            the environment:
   -
            Assessment of the method for evaluating the results of the samples
   -
            Observation of personnel collecting samples from selected sampling locations;
   -
            Examination of air sampling equipment relative to function, operability, and
            calibration;
   -
            Review of the calibration process for the dry gas test meter, including the
            secondary standards used to calibrate the dry gas test meter; and,
   -
            Review of results of prevailing wind determination for the last ten years to assess
            any significant changes since pre-operation to the present.
      b.    Observations and Findinos
   The licensee's sampling procedures, including the contractor's (Normandeau Associates)
    sampling procedures, contained appropriate information and methods comparable to
    industry standards and good practices. The inspector observed the licensee and contractor
    personnel collect milk samples and exchange air particulate filters and charcoal canisters
    from selected air samplers, and discussed certain sample techniques not observed.
    Sampling procedures and practices were intended to minimize the chances of cross
    contamination. Samples were collected from the locations and at the frequencies required
    by the TS and OOCM. The analytical results demonstrated that the types and frequencies
    of analyses were performed as required. The inspector noted that radiological dose to the
    public was in conformance with the technical specifications. To enhance the data sourco

j of the environmental monitoring program, the licensee continued to collect and analyze i supplemental samples in addition to those required by the regulatory requirements. ! l l

 e
 .
                                                  26
   The 1996 land use census was performed by September 1996, according to the procedure
   and the TS requirement. Performance of the land use census was thorough and complete.
   No program changes (e.g., changes in sample locations) were required as a result of the
   census.
   The inspector reviewed the wind direction assessments (wind roses) from the past ten
   years and compared them to the pre-operational wind roses to detect changes, if any, in
the prevailing wind directions. No significant changes were determined. The

, environmental monitoring control stations are still valid.

   The inspector noted that the licensee established an audit program to assess results and
   maintain oversight of the contractor laboratory. The Laboratory Quality Control Audit
   Committee (LOCAC) is a combined effort of technical specialists from the five sponsor

, utilities (Seabrook, Pilgrim, Vermont Yankee, Maine Yankee, and Yankee Rowe). The

   LOCAC audit was comprehensive, covering topics such as equipment calibration and
   analytical procedures. Details of this audit are documented in Section R7.2 of this report.
   This audit program appears to effectively assess the quality of the YAEL performance.
   The air samplers were in operation and good physical condition. The licensee maintained a
   maintenance program to minimize the amount of sample loss due to mechanical failure.
   Each unit was inspected for general function every week and carbon vanes, poly-tubing,
   and power cords were replaced every 12 months. The licensee had a calibration program
   to ensure validity of samples collected. Once per year, both types of air samplers (Kurz
   and dry gas meters) were calibrated with a dry gas test meter, which is in turn calibrated
   every 3 years. The results of the calibrations were within the established acceptance
   criteria.
                                                                                               l
   Calibration of the Jry qas test meter (DGTM) was typically contracted to a vendor.
   However, when the calibration came due, the licensee learned that the vendor would no
   longer perform calibration services; and as a result, that due date of December 1996 may
   be exceeded. The licensee decided to perform the calibration in-house by the Measuring      )
   and Test Equipment (M&TE) laboratory. M&TE created a procedure utilizing the vendor         i
   manual and calibrated the DGTM by April 1997, within the 25% grace period allowed to
   calibrate the instrument. The licensee did not calibrate any air samplers until the DGTM
   had been calibrated. No air samplers exceeded the calibration due dates. The M&TE
   laboratory esta'olished knowledge in this area through review the calibration process.
   Tracofft, to National Institute of Standards and Technology (NIST) was demonstrated as
   evidenced by in,. calibration certificates of the primary standards (manometer and pressure
   gauge) used to calib, we the MKS Califlow System, which is used to calibrate the DGTM.
   Technicians' knowledge aad understanding of the above areas was very good. The
   inspector reviewed training 'nd qualification records of personnel responsible for certain
    REMP duties. The techniciart successfey completed the qualification and training
   programs provided by the trairmy, der'stment. The training program was comprehensive
    and contained sufficient detail to perform REMP duties effectively.
 &

l l* 1

                                                  27

l c. Conclusiq.nji

   Based on the above review, observation, and discussions, the inspector determined the

l licensee's performance in implementing the REMP continued to be excellent.

   R1.3 Meteorological Monitoring Program (MMP)
      a.   Insoection Scooe (84750-02)
   The Meteorological Monitoring Program (MMP) was inspected against TS
   Section 3/4.3.3.4, UFSAR Section 2.3.3.3 and Regulatory Guide 1.23 commitments. The

l

   following activities were conducted to assess the licensee's ability to implement the
   program.
   -
           Review of calibration procedures, calibration results,$nd channel check logs;
   -
           Review of calibration results of individual sensors:

! -

           Discussion of data acquisition and availability of data:                          1

l -

           Observation of the material condition of meteorological equipment; and,
   -
           Review of the normal and backup power supply to the primary tower and test
           verification.
      b.   Observations and Findinas
   Calibration results from July 1995 through December 1996 were reviewed. Calibration of
   the meteorological system (control room to sensors) was performed, in accordance with

,

   applicable procedures, at a quarterly frequency (i.e., more often than semiannual, as

l

   required by TS). Equipment tolerances were verified as described in the procedure and the

l UFSAR. Individual wind speed sensors were periodically tested and performance-verified

   by a vendor semiannually. The results were verified to be within the required tolerances.
                                                                                             l
   Channel checks were performed every shift by operations personnel, more frequently than   I
   daily frequency required by TS. The inspector selected and reviewed the shift log from
   April 1-24,1997, and noted that the channel checks were performed every shift during
   that time period.

!

   The inspector noted that the instrumentation used by Instrument & Controls (l&C) to
    calibrate the meteorological system were properly verified and validated. The system was
   checked by l&C for operability and system performance, daily. The inspector also noted
   that the strip chart recorders were in good physical condition.
   The normal and backup power supplies to the primary meteorological tower was verified by
   the inspector. The inspector reviewed schematics 1-NHY-310103 and 1-NHY-310104 to
    independently determine the electrical power sources for the meteorological tower
    instrumentation. The inspector determined the normal and backup power supply to the
 e

'. I 28

   instrumentation is from the emergency distribution system through the motor control
   center (MCC) E-523, and the gatehouse essential lighting panel, ED-MM-212C, EL32.
   Normal power is supplied by bus E5, a vital bus, supplied by the Unit Auxiliary Transformer
   (UAT). Backup power is supplied by the Reserve Auxiliary Transformer (RAT) or, if the
   RAT fails, the Train "A" diesel generator. The inspector determir:ed that the load shed was
   verified immediately prior to a refuel outage (every 18 months) as part of the surveillance
   test procedure, EX 1804.001, " Diesel Generator 1 A 18 Month Operability and Engineered
   Safeguards Pumps and Valve Response Time Testing Surveillance", Rev. 7, dated, May 07,
    1997. The inspector reviewed the procedure and noted that the load shed tests were
   performed immediately prior to the cast two outages and the results were satisfactorily
   completed and verified, as per Section 4.8.1.1.2.f.4.a of the TS.
     c.     Conclusion
   Based on the direct observations, discussions with personnel, and examination of
   procedures and records for calibration of equipment, the inspector determined that overall,
   the licensee's performance of maintaining and calibrating the meteorological monitoring       !
   instrumentation was very good. The data were available as required and were easily            l
   accessed from several locations, including the control room and the EOF as specified in the
   UFSAR. The l&C performance in this area was demonstrated through a good
   understanding of the meteorological instrumentation based on qualification, training, and
                                                                                                 l
   experiences. The backup power is supplied from the station's Train "A" diesel generator to    ;
   the equipment at the meteorological tower as described in Section 2.3.3 of the UFSAR.         j
   R1.4 Refueling Outage Radiological Controls-External Exposure                                 l
      a.    Insoection Scone (83750-02)
   The inspector reviewed the licensee's control of external exposures. Information was
   gathered through observation of activities, tours of the radiologically controlled area (RCA) j
   including the containment building (CTB), primary auxiliary building (PAB), fuel storage      I
    building (FSB), and waste processing building (WPB), discussions with cognizant personnel,   I
    and review and evaluation of procedures and documents.
      b.    Observations and Findinas
    A review of the radiation work permits (RWPs) and the observed radiological work
    activities indicated that a large amount of advanced planning for the outage by health
    physics (HP) had taken place. RWPs and a schedule of outage activities requiring HP
    coverage were posted at each control point. The inspector noted visible and active HP
    coverage within the RCA. A review of the personnel exposure status report, which was
    current as of May 21, indicated that the highest cumulative individual exposure for 1997

l was 373 millirem (mrem). No administrative dose limits had been exceeded. The badge ! records for six selected individuals were exarnined and contained the documentation

    required in 10 CFR 20.2104 and 20.2106. There was one declared pregnant worker so far
    for 1997 whose radiation exposure was being managed in accordance with 10 CFR
    20.1208.

1

,
                                                                                                l
                                                29
                                                                                                1
  The effects of the increased leakage of airborne radioactive gases due to fuel cladding       '
  defects continued after the scheduled shutdown on approximately May 10. There were 56
  personnel contamination reports (PCRs) due to noble gas from January through April 1997.      i
  Through May 20, there had been 241 PCRs due to noble gas for the outage. Due to the           l
  presence of this increased potential for immersion dose from noble gas, the licensee          l
  investigated the relative merits of various dosimeters for their noble gas monitoring         I
  capabilities. This investigation involved the use of test phantoms with various dosimeters    j
  and thicknesses of protective clothing (PC) and the generation of a Health Physics
  Study / Technical information Document (HPSTID-97-007, Technical Evaluation of Noble
  Gas Monitoring Capabilities, May 14,1997). Presently, the beta dose to the skin is            l
  monitored using air sampling analysis and stay-time calculations while the photon dose to     i
  the skin, the lens dose equivalent, and the deep dose equivalent are tracked on a daily       l
  basis by electronic dosimeters and monitored on a periodic basis by thermoluminescent         '
  dosimeters (TLDs). Seabrook Procedure HD0958.05, " Dose Assessment for Noble Gas
  Environments," establishes a lower limit of 25 mrem per hour for the tracking and
  assignment of net-beta shallow dose equivalent. A licensee evaluation of containment stay
  times indicated that workers spend, at most, 33 hours per year in noble gas environments.
  HPSTID-97-008, " Nots Gas Skin Dose Assignment for OROS," addressed the individual
  doses due to the elevated noble Oas concentrations on May 11 and 12,1997, when the
  dose rate peaked at about 28.2 mrem per hour (7.87 derived air concentrations (DACs)).
  Of the 287 workers who were in the CTB during the elevated gas conditions,11
  individuals received greater than 100 mrem beta skin dose (the maximum individual beta
  skin dose was 187 mrem). Accordingly, this beta skin dose will be assigned to the
  workers in accordance with the licensee's procedures.
  The licensee identified one incident, ACR No. 97-1169, in which contracted workers
  inadvertently performed backseating on reactor coolant pumps (RCPs) A, B, and C without
  HP coverage as required by the RWP. Previously, the workers had performed the same
  task on RCP D with HP coverage. A review indicated that the HP coverage requirement
  was misinterpreted by the workers, that there were no adverse radiological consequences,
  and that clear communication of HP coverage requirements during RWP briefings needed to
  be emphasized. An HP supervisor met with both the HP technician who provided the initial
  coverage on RCP D and the contracted supervisor to review the incident and to discuss
  RWP compliance in the future. The failure of the contracted workers to follow licensee
  procedure and to adhere to the RWP and to notify HP of the need for coverage for the
  additional work is a violation of NRC requirements. Accordingly, this licensee-identified
  and corrected violation is being treated as a Non-Cited Violation, consistent with Section
  Vll.B.1 of the NRC Enforcement Policy.
    c.    Conclusions
  Positive performance was evident in the well-managed handling of the anticipated elevated
  airborne radioactivity levels due to operation with fuel cladding defects. The licensee
  effectively investigated the relative merits of various dosimeters for their noble gas
  monitoring capabilities. A licensee-identified and corrected violation involving adherence to
  a specific RWP requirement was noted and determined to be effectively resolved.

_ .__ __ _. _ _. ___ . _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _

                                                                                                          ,
 .
                                                        30
         R1.5 Refueling Outage Radiological Controls-Internal Exposure
           a.      insoection Scooe (83750-02)
         The inspector reviewed the licensee's control of internal exposures. Information was
         gathered through observation of activities, tours of the RCA including the CTB, PAB, FSB,
         and WPB, discussions with cognizant personnel, and review and evaluation of procedures
         and documents.
           b.      Observations and Findinas
         The inspector determined that the licensee does not track DAC-hours. Justification for
         discontinuing DAC-hour tracking was provided in HPSTID-93-017, " Evaluation of the Need
         For Internal Monitoring at Seabrook Station." The justification was based on historical
         bioassay data and measurements of airborne radionuclides, which showed that annual               -
         intakes in excess of 10% of the applicable annual limits on intake were unlikely to be
         received. No dose had to be assigned as a result of internal exposure per regulatory
         requirements. The inspector rated that numerous air samples were being taken before and
       -
         during radiological work activiues, were being used for decisions on personnel access to
         airborne radioactivity areas, and were being used for area posting purposes. Whole body
         counts (WBCs) are performed for individuah before initial RCA access and before
         termination of site access, after contamination events, and on a random basis (4 or 5 -
         radiation workers per month). Additionr.4ly, the licensee's IPMs (Installed Personnel
         Monitors)/whole body frisking booths are used as passive whole body counters. HPSTID-
         93-014, " LPM Frisking Booth Sensitivity to inhaled Radioactivity," documented the IPM's
         sensitivity (DAC-hours / alarm) for an acute exposure to typically expected mixtures of
         radionuclides as being 15 to 25 DAC-hours [37 to 63 mrem, committe effective dose ,
         equivalent (CEDE)). The licensee's procedure, HD0961.29, " Internal Dosimetry
         Assessment," required that internal dose be assigned to individuals if the CEDE is greater
         than or equal to 10 mrem. The licensee reported that there had been no recordable (10
         millirem) internal exposures thus far in 1997. Based on this information, the licensee was
         in compliance with 10 CFR 20.1204, 20.1501, and 20.1502 as regards surveys,
         monitoring, and determination of internal exposure.
           c.      Conclusions
         The licensee's control of internal exposures was managed in a satisfactory and competent
         fashion.
          R1.6 Refueling Outage Radiological Controls-Radioactive Materials, Contamination,
                   Surveys, and Monitoring
           a.       Insoection Scone (83750-02)

l l The inspector reviewed the licensee's control of radioactive materials, contamination, l

          surveys, and monitoring. Information was gathered through observation of activities, tours
          of the RCA including the CTB, PAB, FSB, and WPB, discussions with cognizant personnel,

( and review and evaluation of procedures and documents, r i

                                                                                                   ~
  .
 .
                                                  31
       b.   Observations and Findinos
    Source term, external to the reactor vessel, and radiation levels were higher this outage
    than for previous outages. The licensee reported that some of the reasons for this were
    the length of the operating period (463 days), the additional crud burst due to a reactor trip
    at 8% power, and fuel cladding defects. The dose rates in the reactor coolant inner loop
    areas were twice the levels encountered in past outages, and dose rates in the steam
    generator bowls were expected to be higher than in the past. Good communication and
    cooperation between HP and operations after shutdown led to successful efforts to remove
    crud and hot spots in piping and system components where it had not been seen in the
    past. These efforts led to lower dose rates in the areas affected, including the residual         1
    heat removal (RHR) was.                                                                           l
                                                                                                      1
                                                                                                      !
    A modification was performed prior to reactor head removal, which allowed venting of the          l
    air space beneath the reactor head, and this alleviated a potential for significant airborne     .
    radioactivity upon lifting of the reactor head. Elevated noble gas (up to 8 DACs) and iodine      1
    (a few % up to 20% of a DAC) airborne levels were initially encountered in containment
    after shutdown due to leaks in valving around the pressurizer relief tank. Containment            l
    remained posted as a Caution-Airborne Radioactivity Area until May 21. As of May 23,-
    the airborne lewla of noble gas and iodine on the refueling deck in containment had
    decreased to less than 2% of a DAC, each. The licensee stated that containment air was
    being exhausted through a filtered system [11,000 cubic feet per minute (CFM)] rather
    than through the unfiltered (40,000 CFM) system until the lodine-131 in containment
    decreased to the point at which the projected dose in 31 days for continuous unfiltered
    release would be less than 0.03 mrem per month to any organ of a member of the public
    (10% of a Technical Specification requirement). The licensee was performing numerous air
    sampling operations throughout each day and demonstrated vigilant oversight of this
    situation.
    On May 17, there were two incidents involving contractors and their failure to maintain
    high radiation area (HRA) barriers (ACR Nos.97-1091 and 97-1139) in accordance with
    licensee technical specifications and procedure, and one incident involving contractors and
    their failure to follow licensee procedure and to adhere to a posted requirement to notify
    HP prict to entry into a truck containing packaged radioactive material (ACR No. 97-1099).
    These incidents were identified by the licensee, resulted in no significant adverse

i radiological consequences, and resulted in immediate and comprehensive corrective actions

     (including temporary denial of RCA access), review and evaluation of the incidents,
     meetings with the individuals involved and their management, a site-wide news article, and
    discip!inary actions. These failures of the contracted workers to adhere to a posted
    requirement to notify HP prior to entry into the truck and to maintain HRA barriers are
    violations of NRC requirements. These licensee-identified and corrected violations are
     being treated as Non-Cited Violations, consistent with Section Vll.B.1 of the NRC
     Enforcement Policy.
.

.

                                                 32
    c.    Conclusion _g
  Efforts to remove radioactive crud and hot spots from locations not required to be flushed
  in the past were successful due to good cooperation between HP and operations. The
  licensee also had been pro-active in their efforts to minimize the potential for high airborne
  radioactivity due to the reactor head lift. Licensee-identified and corrected violations
  involving adherence to HRA and RCA access and control procedures were noted and
  determined to be effectively resolved.
  R1.7 Refueling Outage Radiological Controls-As Low As Reasonably Achievable (ALARA)
                                                                                                 l
    a.    Insoection Scone (83750-02)                                                            !
  The inspector reviewed the licensee's ALARA activities. Information was gathered through
  observation of activities, tours of the RCA including the CTB, PAB, FSB, and WPB,
  discussions with cognizant personnel, and review and evaluation of procedures and
  documents.
                                                                                                 l
     b.   Observations and Findinas
  During tours of the RCA, temporary shielding (lead blankets) was evident in numerous
  areas, especially where workers would be required to spend a significant portion of their
  time and where dose rates were significantly greater than the average general area dose -
  rates. The inspector witnessed an ALARA pre-job briefing for removal of a stuck stud on
  the reactor vessel flange (5.3 person-rem goal). The inspector noted that there was good       l
  planning and preparation for this evolution, requiring significant interaction between         l
   contractors and site personnel from several different departments. The cutage person-rem
  goal appeared to a challenging one, especially considering the effects of the additional crud
   burst and fuel cladding defects on dose rates. As of May 23, the actual and projected
  outage doses were 34.8 and 33.9 person-rem, respectively.
     c.   Conclusior.s                                                                           l
   A number of positive attributes were noted in this area including the beneficial use of
   temporary shielding in containment, the extent of planning and preparation invested in the
   stuck stud task, and the setting of a challenging outage person-rem goal. The ALARA
   program appeared to be effective in maintaining occupational radiation exposures as low as
   reasonably achievable.
   R1.8 Other Changes to the RP Program
     a.    Insoection Scoce (83750-02)
   The inspector reviewed the licensee's RP program for changes since the last inspection.
   Information was gathered through observation of activities, tours of the RCA including the
   CTB, PAB, FSB, and WPB, discussions with cognizant personnel, and review and
   evaluation of procedures and documents.
   -       .=-        - -- - - -             . - - - .    -      - . -   - - - - - - - . -
 .
                                                       33
       b.      Observations and Findinas
     Approximately 5 weeks prior to this inspection, the HP organization lost a health physicist        j
     through resignation of employment. However, at the time of this inspection, there were
     three contracted health physicists and two individuals from site training providing full-time
     support to the HP group. There appeared to be sufficient health physicist staffing and
     resources in HP during this inspection. To be prepared for a potential significant increase
     in outage scope (tube inspection work in 4 rather than just 2 steam generators), the
     licensee added twelve health physics technicians to the staff.
     The scrub program (alternate type of protective clothing for prescribed types of work) had
     been implemented since the last inspection. Also, TLD bar code readers had been installed
     at the HP access control points. This change provided greater control of RCA access.
     Other program improvements included the purchase of two Merlin Gerin AM-16 area
     monitors and of four AMS-4 Eberline portable continuous air monitors, the use of cameras
     in the RHR vaults to reduce exposure, turbine building HP controls to verify the radioactive       l
     contamination status of secondary systems, automated incremental neutron dose tracking
     in the computerized access control system, and generation of a user / technical manual for
     the e.ccess control system.
        c.     Conclusions
     The HP organization appears well supported by licensee management and is continuing to
     improve the radiation protection program.
     R2        Status of RP&C Facilities and Equipment
     R2.1 Calibration of Effluent / Process Radiation Monitoring Systems (RMS)
        a.     Insoection Scooe (84750-01)
     The inspector reviewed the most recent calibration results for the following selected
     effluent / process RMS and its system flow rates. The inspector also reviewed the
     licensee's RMS self-assessment and RMS work orders.
      *        Waste Liquid Test Tanks Radiation Monitor (R-6509)
      *        Waste Liquid Test Tanks Flow Rate
      *        Steam Generator Blowdown Flash Tank Radiation Monitor (R-6519)
      *        Turbine Building Sump Pump Radiation Monitor (R-6521)

i

      a        Main Steam Line Radiation Monitors (R-6481 1&3, R-6482 2&4)

! * Primary Component Cooling Water Radiation Monitors (R-6515 & 6516)

      *        Containment Purge Radiation Monitors (R-6527 A & B)                                      ,
      o        Containment Purge Line Flow Rate                                                         l

( * Plant Vent Wide Range Noble Gas Monitor (R-6528) l .

      *        Plant Vent Exhaust Flow Rate

-

      *        Condenser Air Evacuators Discharge Monitor (R-6505)

,

      *        Waste Gas Compressor inlet Radiation Monitor (R-6503)                                    ,

,

      *        Waste Gas Compressor Discharge Radiation Monitor (R-6504)                                !
                                                                                           .-      -
                                                                                                     -.
   . _ _ - - _         __          . _ - - _       __ _                  . _ _ _   _ _ _ .       __      _ _ - ._
 .
                                                                34
                    b.    Observations and Findinos
                 The l&C department had the responsibility to perform electronic and radiological
                 calibrations for the above radiation monitors. The system engineer had the responsibility to
                 trend and track the above RMS. All reviewed calibration results were within the licensee's
                 acceptance criteria.
                 During the review of the above RMS calibration results, the inspector independently
                 calculated and compared several calibration results including linearity tests and conversion     .
                                                                                                                  '
                 factors. The comparisons were very good.
                    c.    Conclusions
                 Based on the above reviews, the inspector determined that the licensee maintained and
                 implemented a very good calibration program for the effluent / process RMS.
                 R2.2 Calibration of Area Radiation Monitoring Systems (ARMS)
                    a.    Insoection Scoce (83750)
                 The inspector reviewed the most recent calibration results for the following selected ARMS
                 described in Sections 12.3.4 and 13.5.2.3.(b).3 of the UFSAR:
                 o        PAB - High Range Area Monitors (65081 & 2)
                 e        RHR - High Range Area Monitors (65171 & 2)
                 e        FSR - High Range Area Monitor (6518)
                  e       Personnel Hatch (Post-LOCA) Area Monitors (65361 & 2)
                 The instrument calibrations were reviewed with respect to:
                 (1)      selection criteria for energy dependence, accuracy, and reproducibility; (2)
                          calibration method and testability; and (3) alarm set point methodology.
                          The inspectors also utilized the following documents as a basis to determine
                          whether the calibration procedures contained sufficient calibration steps to verify
                          the alarm set points.                                                                     l
                  *       ANSI /ANS.HPSSC-6.8.1-1981, " Location and Design Criteria for Area Radiation
                          Monitoring Systems for Light Water Nuclear Reactors,"
                  e       ANSI N42.3-1969, IEEE No. 309, "American National Standard and IEEE Standard
                          Test Procedure for Guiger-Muller Counters," and
                  e       ANSI N323-1978, "American National Standard Radiation Protection
instrurnentation Test and Calibration."

i I 1 i L -

   - . _ - _ . _ _          . .. --     .-.   . .   .    -          . - -          ..      .  .            . -  - - . - .
 .
                                                                 35
                     b.    Observations and Findinas
                   The licensee applied very good calibration methodologies for the above ARMS, including

l radiological and electronic calibrations. Alert and alarm setpoints calculation

                   methodologies were good. The licensee also emphasized maintaining minimum background

l

                   radiation level during the calibration which was excellent. Calibration procedures were
                   detailed and easy to follow for all necessary steps.
                                                                                                                          *
                     c.    Conclusions
                   Based on the above reviews, the inspector determined that the licensee implemented a
                   very good ARMS calibration program.
                   R2.3 Air Cleaning Systems                                                                              ;
                                                                                                                          i

l a. Insoection Scoce (84750-01)

                   The inspector reviewed the licensee's most recent surveillance test results (visual
                   inspection, in-place HEPA and charcoal filter leak tests, air capacity, pressure drop tcot;,
                   and laboratory tests for the iodine collection efficiencies) for the following systems:
                   o       Containment Purge Exhaust System
                   o       Primary Auxiliary Building Exhaust System
                   o       Fuel Storage Building Exhaust System (Trains A & B)
                     b.    Observations and Findinas
                   All reviewed test results were within the licensee's TS acceptance criteria. During the
                   previous inspection conducted in January 1996, the inspector recognized that the
                   responsible individual had very good knowledge not only for TS requirements, but also for
                   standard industry practices. The inspector determined that the licensee maintained and
                   implemented a very good air cleaning system surveillance program.                                      !
                     c.    Conclusions
                   Based on the above reviews, the inspector determined that the licensee maintained and
                   implemented a very good air cleaning system surveillance program.
                   R3      RP&C Procedures and Documentation
                     a.    Insoection Scope (84570-01)
                                                                                                                           !

l The inspection consisted of: (1) review of selected chemistry procedures to determine

                   whether the licensee could implement the routine radioactive liquid and gaseous effluent
                   control programs and the emergency operations; (2) review of 1995 and 1996 Annual                       i

i Radioactive Effluent Reports to verify the implementation of TS requirements; and (3) l

                   review of the contents of the ODCM for performing the effluent control programs, including

i projected dose calculation methodologies to the public. I

                                                                                -.    - .,      __
   _- -        ...              _   ._.        . - - - - . - - -          _ - -             _ - - - - - - -
                                                                                                               !
 .

l 36 , I b. Observations and Findinas i !  !

        The inspector noted that reviewed effluent control procedures were detailed, easy to                   ,
        follow, and ODCM requirements were incorporated into the appropriate procedures. The                   l

l licensee had good procedures to satisfy the TS/ODCM requirements for routine and l

        emergency operations.
                                                                                                               ~

l l

        The inspectors reviewed the 1995 and 1996 Annual Radioactive Effluent Release Reports.

l These reports provided data indicating total released radioactivity for liquid and gaseous

        effluents. The annual reports also summarized the assessment of the projected maximum                  i

j individual and population doses resulting from routine radioactive airborne and liquid s

        effluents. Projected doses to the public were well below the Technical Specification (TS)             -{
        limits. The inspectors determined that there were no anomalous measurements, omissions                 '
        or adverse trends in the reports.                                                                      ;
                                                                                                               !
        The ODCM provided descriptions of the sampling and analysis programs, which were                       ;
        established for quantifying radioactive liquid and gaseous effluent concentrations, and for
        calculating projected doses to the public. All necessary parameters, such as effluent
radiation monitor setpoint calculation methodologies, site-specific dilution factors, and dose
        factors, were listed in the ODCM. The licensee adopted other necessary parameters from

l Regulatory Guide 1.109.

           c.      Conclusions

l

        Based on the above reviews, the inspector made the following determinations:
         *         effluent control procedures were suffic;3ntly detailed to facilitate performance of all
                   necessary steps for routine and emergency operations,
         e         the licensee effectively implemented the TSiODCM requirements for reporting
                   effluent releases and projected doses to the public, and
         *         the licensee's ODCM contained sufficier,t specification, information, and instruction
                   to acceptably implement and maintain tie radioactive liquid and gaseous effluent
                   control programs.

l R5 Staff Training and Qualification in RP&C

           a.      Insoection Scooe (83750-02_1
        The inspector reviewed the qualifications and training of selected contracted HP
        technicians. Information was gathered through observation of activities, discussions with

l cognizant personnel, and review and evaluation of documents. i l l . !

                                             _         _                           __                       _
.

.

                                                  37
      b.    Observations and Findinos
    The documented qualifications of the senior HP contracted technicians were reviewed and
    were found to meet the technical specification requirements. The training of these
    technicians at the site was in compliance with site procedures.
      c.    Conclusions
    The qualifications and site training of the HP technicians contracted for the outage were
    satisfactory.
    R6      RP&C Organization and Administration                                                -
      a.    Insoection Scope (84570-01)
    The inspector reviewed the organization and administration of the radioactive liquid and
    gaseous effluent control programs and discussed with the licensee changes made since the
    last inspection, conducted in January 1996. The inspector also reviewed the management
  -
    support for the effluent control program through interviews and implementation of the        ;
                                                                                                 '
    effluent ALARA program.
      b.    Observations and Findinos                                                            i
                                                                                                )
    There were no changes since the last inspection of the effluent control programs. The        l
    chemistry department had the major responsibility to conduct the effluent control            l
    programs. Other groups (i.e., HP, operations, I&C, and system engineers) had supporting
    responsibilities to the program. Staffing levels appeared to be appropriate for the conduct  i
    of routine and emergency operations.
    The inspector interviewed the chemistry staff and management for the importance of the
    effluent control programs and implementation of the effluent ALARA program. All
    chemistry staff demonstrated very good knowledge of: (1) TS/ODCM requirements and its
    bases, (2) projected dose calculation, and (3) implementation of the TS/ODCM during
    normal and emergency operations. Management also demonstrated knowledge in these
    areas and supported the radioactive liquid and gaseous effluent control programs (see
    Section R1 of this inspection report).
      c.    Conclusions
    Staffing levels appeared to be appropriate to conduct routine and emergency operations.
    As aforementioned, management support of the effluent ALARA program was noteworthy.
                                                                                                 I
                                                                                                 !
                     ~. -        .- -. - - .- - - _ .. _ - -. - ..--                           . . .... - . . -   - .

3..-~-.-~

                                                                                                                       :
                                                                                                                       ,

l.  ;

                                                                                                                       ;

- '

                                                                                                                       l
                                                                                                                       '
                                                                     38
        R6.2 Management Controls                                                                                       !
                                                                                                                       !
          a.    Insoection Scooe (84570-02)                                                                            -
                                                                                                                       .
        The inspector reviewed organization changes and the responsibilities relative to oversight
        of the REMP and MMP, and the annual radiological environmental operating report to verify
        the implementation of the TS.                                                                                    l
          b.    Observations and Findinas

'

        The organization changes did not appear to have a negative impact on the oversight of the
        REMP. The responsibilities relative to oversight of the REMP and MMP have essentially
                 .
        remained the same.

l The annual radiological environmental monitoring reports for 1995 and 1996 (draft) )

        provided a comprehensive summary of the results of the REMP around Seabrook and met                              i
        the TS reporting requirements. No omissions, mistakes, or obvious anomalous results and
        trends were noted.

l , ,

          c.    Conclusion
        Based on the above review, the inspector determined that the licensee implemented good
        management control and oversight of the REMP and MMP and effectively implemented the
        TS requirements.

L R7 Quality Assurance in RP&C Activities j l l l a. Inspection Scone (84750-01) - t  ! l l l The inspection consists of: (1) review of the 1996 audit and its responses, if any; (2) QA  !

        policy of the measurement laboratory; and (3) implementation of the measurement
        laboratory QC program for radioactive liquid and gaseous effluent samples.

l b. Observations and Findinas l

        The inspector reviewed QA Audit Report No. 96-A10-02. The inspector noted that the
        audit team also included other technical personnel. The 1996 auait team identified one
        finding and five observations / recommendations. The finding or observations were not                            !
        safety-related, rather to enhance effluent control programs. The responses to these                              ,
        findings and observations were completed in a timely manner. The inspector noted that                            l
        the scope and technical depth of the audit was very good in assessing the radioactive
        liquid and gaseous effluent control programs.

.

        The licensee maintained very good QA policy and implemented the policy throughout the

! chemistry department, including the analytical measurement laboratory. The QA/QC  ; ! program for analyses of effluent samples is conducted by Yankee Atomic Environmental , i Laboratory (YAEL). The YAEL has interlaboratory and intralaboratory QC programs. The l l QC program consists of measurements of blind duplicate, spike, and split samples. The  ;

                                                                                                                         I
           w              -           + - >    p-                       e y-t 7    -P     +-                  4 --7-
                      ._               _ _ _ . _           _ _ _ _ . _ _ _ _ _ _ . _      . . _ _ . _ . _ . _ . . _ _ _ _
 7 __ .. . _ . ___
                             _ -_
 4
                                                                      39
                 YAEL published a QC report quarterly, semiannually, and annually. The inspector reviewed

l the QC data of the Seabrook station for intra /interlaboratory comparisons listed in the

                 quarterly OC reports and noted that the OC data were within the YAEL's acceptance
                 criteria. The inspector also noted that the YAEL evaluated analytical results for accuracy
                 and precision, which was an excellent effort for validating analytical results. When
                 discrepancies were found, the responsible licensee consulted the YAEL personnel and
                 reasons for the discrepancies were investigated and resolved.
                   c.    _Csnclusions
                 Based on the above reviews, the inspector determined that the licensee continued to
                 conduct excellent QA and OC programs for the radioactive liquid and gaseous effluent
                 control programs,
                   a.    Inspection Scooe (83750-02)                                                                      i
                 The inspector reviewed the licensee's quality assurance (QA) activities for their TLD
                 vendor's ability to accurately report radiation dose. Information was gathered through
                 discussions with cognizant personnel and review and evaluation of documents.
                   b.    Observations and Findinos
                 The vendor's National Voluntary Laboratory Accreditation Program (NVLAP) certification -
                 was available and stated that, in accordance with American National Standards Institute

l (ANSI) Health Physics Society (HPS) N13.11-1993, the UD808 and UD814 badges were ! each qualified for Categories 1,11, Illa, IllB, IV, VA, VB, VC, VI, and Vil, and that the

                 combination of the two badges was qualified for Category Vill. The licensee performed
                 blind spiking of the TLDs in the first quarter of 1997 using Cesium-137. The average
                 reported dose was within approximately 11% of the delivered dose. This result was
                 acceptable for the radiation type tested.
                   c.     Conclusions
                 The licensee's OA activities for their TLD vendor's ability to accurately report radiation
                 dose was acceptable for the radiation type tested.
                 R7.1 Quality Assurance Audit Program

' !

                   a.     Insoection Scoce (84750-02)

[ The following Quality Assurance (OA) audit reports were reviewed against Section 6.4.3.8 l of Technical Specifications. l l -

                          Nuclear Safety and Assessment (NSA) Audit Report No. 95-A09-01, " Radiological
                          Effluent Technical Specification (RETS), Radiological Environmental Monitoring
                          Program (REMP), Offsite Dose Calculation Manual (ODCM)."

,

    . - - -                                                                          .- -

I*

.

i

                                                 40
  -
           Nuclear Safety and Assessment Audit Report No. 96-A10-02, "RETS, REMP,
           ODCM."
  The 1996 Laboratory Quality Control Audit Committee (LOCAC), Audit Report was
  reviewed to evaluate the licensee's oversight and assessment of the contractor laboratory,
     b.    Observation and Findinas
  The inspector noted that the licensee conducted the NSA audits according to TS. The
  licensee used the audit procedure, OP AE 3.0, as guidance to conduct the audits. The
  scope of the audits reflected the environmental monitoring program requirements. All
  aspects of the scope were completed. The inspector noted that the audit team leader
  utilized a technical specialist to assess the REMP. The technical specialist (auditor)
  reviewed and understood the TS, ODCM, and the pertinent program procedures. The
  auditc was familiar with sampling and analytical practices and observed collection of
  certain samples and reviewed the results obtained by the analytical laboratory. The
  inspector determined that the auditor's recommendations, were appropriate and were
  suggested to refine the REMP. Followup of the 1995 findings was complete for the QA
  Assessment audits and was documented in the 1996 audit report.
  The LOCAC audit was a joint effort audit conducted by members from the five sponsor
  utilities to evaluate the programs of YAEL. During this audit, each member of the audit

i team selected an area of interest and performed a probing investigation in the area. The

  areas of interest were analytical procedures, laboratory practices, quality assurance and
  quality control program. The findings were appropriate and reasonable. The responses,
   when required, were timely and appropriate. Followup for the LOCAC audit is not yet
  complete.
     c.    Conclusions
   Based on the review of the audits and discussions with the auditors, the inspector
  concluded that the audits were of sufficient technical depth to effectively identify and
   assess program strengths and weaknesses. The audits evaluated the technical adequacy
  of implementing procedures, TS requirements, and practices. Performance of the audits by
  the audit teams was thorough, objective and of high quality as evidenced by the report
  documentation.
   R7.2 Quality Assurance of Analytical Measurements
     a.    insoection Scooe (84750-02)

l The inspector reviewed the Quality Assurance (OA) and Quality Control (OC) programs i against Section 3/4.12.3 of the TS and recommendations of Regulatory Guide 4.15, i

   " Quality Assurance for Radiological Monitoring Programs (Normal Operations) - Effluent
   Streams and the Environment" to determine whether the licensee had adequate control
   witn respect to sampling, analyzing, and evaluating data for the implementation of the
   REMP.

i

                                           - _ _ _ _ _ _ - - _ _
 .
                                                                 41
               b.     Observations and Findinas
             The performance of the contractor laboratory, Yankee Atomic Environmental Laboratory
             (YAEL), continued to be excellent. During an inspection at Millstone, the inspector visited
             the laboratory and assessed the quality assurance program. See Section R7.2 of the
             Combined Inspection Report Nos. 50-245/96-09, 50-336/96-09, and 50-423/96-09 for
             details.
             The YAEL implemented an interlaboratory comparison program, required by the TS,
             through continued participation with Environmental Protection Agency (EPA) drinking water
             program and the program provided by Analytics, Incorporated. The inspector reviewed the
             analytical results of this program and noted the results were within the established
             acceptance criteria.
               c.     Conclusion
             Based on the above observations, the inspector determined that the performance of the
             contract laboratory was excellent and the interlaboratory program was effective.
             R8      Miscellaneous RP&C lssues
             R8.1 Review of Updated final Safety Analysis Report (UFSAR) Commitments
             A recent discovery of a licensee operating their facility in a manner contrary to the Updated
             Final Safety Analysis Report (UFSAR) description highlighted the need for a special focused
             review that compares plant practices, procedures, and/or parameters to the UFSAR
             descriptions.
             While performing the inspections discussed in this report, the inspector reviewed the
             applicable portions of the UFSAR that related to the areas inspected. The inspector
             verified that the UFSAR wording was consistent with observed plant practices, pacedures,
             and/or parameters.
             R8.2 (Closed) LER 50-443/96-009-00: Missed surveillance PCCW rate of change monitor
                     alarm.
             Channel calibration of the Primary Component Cooling Water (PCCW) head tank rate of
             change monitor is required on a refueling interval by the TS. A complete calibration of the
             PCCW head tank rate of change monitor was not performed on the required frequency.
             This LER is not considered safety significant because the radiation monitor had been
             calibrated and alarms have been functional. The licensee promptly corrected this event.
             The inspector determined that, at the time of the event, missed surveillance PCCW rate of
             change monitor alarm, constituted a violation of TS Section 4.3.3.9, Table 4.3-5, Item 4a.
             This licensee-identified and corrected violation is being treated as a non-cited violation,
             consistent with Section Vll.B.1 of the NRC Enforcement Policy. (NCV 50-443/97-03-06)
                                                                                                           l

l

   _ -- ----

e

                                               42
  R8.3 (Closed) (URI 50-443/97-002-01) LER 50-443/97-005-00: Misposition of Main
           Steam Line Radiation Monitors.
  On March 14,1997, the licensee discovered that the four main steam line radiation
  monitors were positioned downstream of the atmospheric steam dump valves (ASDV)
  contrary to the descript!on in UFSAR Section 11.5.2.1. On the sarne day, the radiation
  monitors were declared inoperable and appropriate actions were initiated. On March 20,
  the licensee repositioned radiation monitors (consistent with the UFSAR) and declared them
  operable. The licensee promptly corrected this event.
  The inspector reviewed the most recent calibration results for four main steam line
  radiation monitoring systems (see R2.1 of this inspection report). All calibration results
  were within the licensee acceptance criteria.
  The inspector also toured the main steam line radiation monitors and noted that the new
  location of the radiation monitors was about 2 feet upstream of the ASDV. It should be
  noted that the radiation monitors had capabilities to monitor at the old location
  (downstream of the ASDV). This licensee-identified and corrected violation is being treated
  as a non-cited violation, consistent with Section Vll.B.1 of the NRC Enforcement Poliev.
 This item is closed. (NCV 50-433/97-03-07)
  S1      Conduct of Security and Safeguards Activities
 S1.1 General Comments (71707, 71750)
 The inspectors observed security force performance during inspection activities. Protected
 area access controls were found to be properly implemented during random observations.
 Proper escort control of visitors was observed. Security officers were alert and attentive
 to their duties.
 S1.2 Uncontrolled Vehicle in Protected Area
    a.    Indoection Scope
 The inspector conducted a routine inspection of the station physical security program by
 verifying the all vehicles in the Protected Area were locked with the keys removed when
 unattended.
   b.     Insoection Findinas
 On May 22, the inspector identified an uncontrolled designated vehicle in the Protected
 Area during a routine inspection tour. The unattended vehicle had the keys in the ignition
 and the engine running. The inspector notified a security officer of the condition and the
 individual took possession of the vshicle keys after stopping the engine. The security
 officer found the operator of the vehicle out of sight in the vicinity of the vehicle while the
 vehicle was being off loaded.
       ..    .
    _ . _ . _ _ _ . _ _ . .                _ . _ _ . _ _._ ..                     _ . _ _ . _ _ . _ _ . _ _ _ _ _ . _ . _ . _
  e
                                                                                                                               o
 .
                                                                       43                                                      j
            Station management directed that an ACR be initiated to document the finding and to
            provide recommendations for corrective actions. After the completion of the immediate                               ;
            corrective action, which was to take possession of the vehicle keys by a security person,
            several other corrective actions were implemented. These included attaching a
            " cautionary tag" on the vehicle key ring by security personnel to aid the vehicle operators                       :
            concerning the duties and responsibilities of the while being an authorized operator. Also                         ,

l the vehicle operator was coached and counselled by a security department supervisor  ; '

            concerning the event.
            The Seabrook Station Physical Security Plan, requires that procedures be developed and                             l
            implemented to control vehicles inside the station Protected Area. Security Department                             !
            Instruction, SDl002.00, " Control of Vehicles", requires in part, that all Licensee Designated                     ;
            Vehicles (LDV"s) when unattended must have the ignition locked, keys removed from the                              !
            ignition and controlled by an authorized person. Contrary to the above, on May 22, at
            approximately 10:30 am, the inspector found LDV 16-02 unattended, with the keys in the
                                                                                                                              j
                                                                                                                               j
            ignition, and the engine running and not controlled by an authorized person. This is a                             j

l violation of NRC requirements and the Station Security Plan. (VIO 50-443/97-03-08)  ! l l c. Conclusions } l

                                                                                                                               !
            The inspector determined that the licensee promptly took control of the LDV when notified                          !
            by the inspector. The licensee's response was prompt and provided adequate immediate                               l

l corrective actions. However, in view of this being the second NRC identified violation  ;

            regarding the control of LDV's in the past year.                                                                   !

l l

                                                                                                                               i
                                                              V. Mananement Meetinas

, ! ! ,

            X1              Exit Meeting Summary                                                                               l
                                                                                                                               i
The radiation physicist presented the inspection results to members of the licensee j
             management at the conclusion of the inspection on April 25. The licensee acknowledged

'

                                                                                                                               i
            the findings presented.
                                                                                                                               '
            The radiation specialist presented the inspection findings to members of the licensee
             management at the end of the inspection on May 23, and during a telephone discussion on                           ,
             May 30. The licensee acknowledged the findings.                                                                   j
                                                                                                                               r
            The inspectors covering the inservice inspection presented the results to members of                               '
             licensee management at the conclusion of the inspection on May 23. The licensee                                   ;
             acknowledged the findings presented.                                                                              ,
                                                                                                                               !
             The inspectors presented the inspection results to members of licensee management,                                j

,

             following the conclusion of the inspection period, on June 25. The licensee acknowledged                          j

l the findings presented. !  !

i

!  ! l  !

                                                                                                                               !

l  !

                                                                                                                               !
                                                                                                                               .
   . _ - - _ _ - .                  . .- .-_.        .
                                                       .    -     - ... - . - - - .. - .. - _.. -.- ... -..._ _           _.      _-_ - .
                                                                                                                                          ;
                                                                                                                                          ,
 ,
                                                                              44                                                          .
                   The inspectors asked the licensee whether any materials examined during the inspection
                   should be considered proprietary. No proprietary information was identified.
                   X3     Other NRC Activities                                                                                            ;
                   Conference calls between NRC managers and technical staff specialists and licensee
                   managers and technical staff leads were performed on the following dates.
                                                                                                                                          ,
                          5/31/97               Fuel Failure Conference Call

,

                          6/3-5/97              Site Review by Reactor Projects Chief, Branch No. 8, NRC Region I

'

                          6/16/97               Site Review by Deputy Regional Administrator, NRC Region I
                                                                                                                                          :

I l l  !

                                                                                                                                          !
                                                                                                                                          1
                                                                                                                                          :
                                                                                                                                           '

l

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( I

                          ~ - . , -           -    -                                                            . . _ . _    s- .
  .   . . .-          -          . . - .-                                       --. - - - . _ - .
                                                                                                   i
                                                                                                   !
    ,                                                                                             .
                                                                                                  l
*
                                                           45
                                          PARTIAL LIST OF PERSONS CONTACTED
             Licensee                                                                             '
                    B. Beuchel, Engineering Performance Manager                                    ,
             **
                    W. Cash, HP Dept. Supervisor                                                   '
             *
                    R. Cliche, Design Engineering Supervisor
                    W. Creb, HP Department Manager
                    M. DeBay, A.O.M.
             *
                    W. DiProfio, Station Director
             *
                    R. Donald, Senior Auditor                                                     l
             *
                    B. Drawbridge, Director of Services                                            l
                    M. Dugan, NES Manager Field Operations
             *
!
                    P. Falman, Auxiliary System Engineering Supervisor                            ,
                    R. Godbout, Instrument and Controls Supervisor                                i
             *
                    A. Giotas, Chemistry Supervisor                                               '
             *
                    J. Grillo, Oversight Manager
                    R. Gwinn, Program Support                                                      i
                    G. Kann, Program Support Supervisor
                    G. Kline, Technical Support
             *
                    D. Kochman, Senior Engineer, Licensing                                        i
             *
                    J. Kwasnik, Senior Radiation Scientist                                        !
                    W. Leland, Chemistry and HP Manager
             *
                    R. Litman, Chemistry Department Supervisor
                    J. Peterson, Maintenance Manager
                    T. Pucko, Regulatory Compliance Engineer                                      ;
                    J. Rafalowski, Chemistry and HP Project Supervisor
                    J. Savold, Senior l&C Technician                                               !
             *
                    J. Sobotka, Regulatory Compliance Manager
                    E. Soretsky, Technical Projects Supervisor
             *
                    G. St. Pierre, Operations Manager                                             ,
             *
                    B. Roach, Maintenance Manager                                                 j
             *
                    L. Tardif, Senior Chemist
                    M. Toole, instrument and Controls Supervisor
             *
                    L. Walsh, Station Staff
                    K. Whitney, Senior ISI Engineer                                               ;
             (*)    Denotes those present at the exit meeting on April 15,1997.
                                                                                                  !
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W

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  .- . . .   . . . . - . . - - - . - - - - . - . . . . - . . . - . . . - - - - . _ . . ~ . . . ~ . . . . . . . - _ . . . . . . - .

t. j i--  ! '

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                                                     46                                                                                       l
           . Yankee Atomic Nuclear
            S. Volk, NDE Level lil
                                                                                                                                              !
            HEC                                                                                                                               !
                                                                                                                                              :
            J. Macdonald, Sr. Resident inspector                                                                                              l
            D. Mannai, Resident inspector
            W. Olsen, Resident inspector
                                .
                                                                                                                                              ,
            D. Silk,                                                                                                                          !
            J. Brand, Reactor Engineer
            A. Lohmeier, Senior Reactor Engineer                                                                                              -
            J. McFadden, Radiation Specialist
            A. DeAgazio, Project Manager                                                                                                      ,i
                                                                                                                                             '!
                                                                                                                                               1

!

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! I ! l-

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l t l I' !

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l. _ - _

                                                                                      _         _                                _ . . _ _ .
   _ _ - _ _ _._.          ._  - ..            .      ._.      _ _ _ _ _ _ _ _ _ _ _ _ . ._..__ __ ._, , _ _   . . _ _ _ _ .
 .

.* ,

                                                                      47
                                                 INSPECTION PROCEDURES USED
                  IP 37551:       Onsite Engineering                                                                         l
                  IP 40500:       Effectiveness of Licensee Controls in identifying, Resolving, and Preventing               :
                                  Problems
                  IP 61726:       Surveillance Observation
                                                                                                                             l
                  IP 62707:       Maintenance Observation
                  IP 71707:       Plant Operations                                                                           ;
                  IP 71750:       Plant Support Activities
                  IP 73051:       Inservice inspection - Review of Program
                  IP 73753:       Inservice inspection
                  IP 83729:       Occupational Exposure During Extended Outages
                  IP 83750:       Occupational Radiation Exposure
                  IP 84750:       Radioactive Waste Treatment, and Effluent and Environmental Monitoring IP
                                  IP 92700:      Onsite Followup of Written Reports of Nonroutine Events at                  .
                                                 Power Reactor Facilities
                  IP 92902:       Followup - Engineering
                  IP 92903:        Followup - Maintenance
                  IP 93702:        Prompt Onsite Response to Events at Operating Power Reactors
                                            ITEMS OPENED, CLOSED, AND DISCUSSED
                  Ooened:
                  IFl 50-443/97-03-01            Review root cause of inadvertent steam generator drain-down.
                                                 (Section 02.2)
                  VIO 50-443/97-03-02            Failure to take adequate corrective actions for use of pressure
                                                 tubing. (Section M2.1)
                  IFl 50-443/97-03-03            Review station procedure revision process. (Section E2.1)
                   IFl 50-443/97-03-04           Review root cause evaluation for LLRT failure. (Section E2.2)
                  VIO 50-443/97-03-08            Designated Vehicle Left Unattended with Keys in the ignition                  1
                                                 and Running (Section S1.2).                                                   l
                   Closed:
                   NCV 50-433/97-03-05           Failure to promptly report LLRT f ailure in accordance with 10
                                                 CFR 50.72. (Section E2.2)           '
                                                                                                                               i
                   LER 96-009-00, Missed Surveillance PCCW Rate of Change Monitor Alarm. This is closed.

l (NCV 50-443/97-03-06) i ! LER 97-005-00, Misposition of Main Steam Line Radiation Monitors. This item is closed.

                   (NCV 50-433/97-03-07)

- Discussed: None

                                                          ~
  s                                                               l
 .                                                                l

',a

                                          48

( LIST OF ACRONYMS USED

    ACR    Adverse Condition Report
    ALARA  As low As is Reasonably Achievable
    ANSI   American National Standards Institute
    ASME   American Society of Mechanical Engineers
    ARMS   Area Radiation Monitoring System
    AVB    Anti-Vibration Bars
    B&PVC  Boiler and Pressure Vessel Code
    CEDE   Committed Effective Dose Equivalent
    CFM    Cubic Feet per Minute
    CFR    Code of Federal Regulations
    CMMEB  Civil, Mechanical, Metallurgical Engineering Branch
    CTB    Containment Building
    DAC    Derived Air Concentration                             i
    DRP    Division of Reactor Projects
    DRS    Division of Reactor Safety
    E/C    Eddy Current
    ED     Electronic Dosimeter
    EPRI   Electric Power Research Institute
    FSB    Fuel Storage Building
    HEPA   High Efficiency Particulate
    HP     Health Physics
    HPS    Health Physics Society
    HPSTID Health Physics Study / Technical Information Document
    HRA    High Radiation Area
    IP     inspection Procedure
    iPM    Installed Personnel Monitor
    IR     Intermediate Range
    ISI    Inservice Inspection
    La     Maximum Allowable Containment leakage Rate
    LHRA   Locked High Radiation Area
    LLRT   Leak Rate Test
    MREM   Millirem
    MSL    Main Steam Line
    MT     Magnetic Particle Test
    NDE    Non-destructive Examination
    NRC    Nuclear Regulatory Commission
    NVLAP  National Voluntary Laboratory Accreditation Program
    ODCM   Offsite Dose Calculation Manual
    OR05   Refueling Outage 5
    PAB    Primary Auxiliary Building
    PC     Protective Clothing
    PCR    Personnel Contamination Report
    PDT    Primary Drain Tank
    PT     Penetrant Test

l OA Quality Assurance

    QC     Quality Control
   .      - . - ._ _ _ - _._._.. .            . - . _ . _ _ . _    .__ . - . . _ _ _ . . . . . . _ - ___
 e

(: < !/

                                                                                                         ,
                                                                49
     RCA              Radiologically Controlled Area

i RCP Reactor Cooling Pump

     RCS              Reactor Coolant System
     RHR              Residual Heat Removal
                                                                                                         i
     RHS              Reheat System                                                                      ;
     RMS              Radiation Monitoring System                                                        '

l ROR Radiological Occurrence Report

     RP&C             Radiological Protection and Chemistry
     RSC              Radiation Safety Committee
     RWP              Radiation Work Permit                                                               ,
RWST Refueling Water Storage Tank l

!

     SAM              Small Article Monitor                                                              i
     scfh             Standard Cubic Feet per Hour                                                       '
     SG               Steam Generator                                                                    .
     TEDE             Total Effective Dose Equivalent                                                    !
                                                                                                         '
     TLD              Thermoluminescence Dosimeter
     TOFD             Time of Flight Diffraction                                                         j
                                                                                                         '
     TS               Technical Specifications
     UFSAR            Updated Final Safety Analysis Report
     UT               Ultrasonic Test

l VCT Volume Control Tank

     WBC              Whole Body Count                                                                    l
     WPB             . Waste Processing Building                                                          1
     WRGM             Wide Range Radioactive Gaseous Monitor                                             l

, . l l l l l

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l !

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