ML19163A294

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GE Hitachi Nuclear Energy - NRC Inspection Report 050-00018/2019-001; 050-00070/2019-001; 050-00183/2019-001 and Notice of Violation
ML19163A294
Person / Time
Site: Vallecitos, Vallecitos Nuclear Center
Issue date: 06/24/2019
From: Greg Warnick
Division of Nuclear Materials Safety IV
To: Feyrer M
GE-Hitachi Nuclear Energy Americas
S. Anderson
References
IR 2019001
Download: ML19163A294 (21)


See also: IR 05000018/2019001

Text

June 24, 2019

Mr. Matt Feyrer, Site Manager

Vallecitos Nuclear Center

GE Hitachi Nuclear Energy

6705 Vallecitos Road

Sunol, CA 94586-8524

SUBJECT: GE HITACHI NUCLEAR ENERGY - NRC INSPECTION REPORT

050-00018/2019-001; 050-00070/2019-001; 050-00183/2019-001 AND NOTICE

OF VIOLATION

Dear Mr. Feyrer:

This letter refers to the U.S. Nuclear Regulatory Commission (NRC) inspection conducted on

March 25-28, 2019, at your Vallecitos Nuclear Center in Sunol, California. The inspection

covered the following shutdown reactors under the subject licenses, Vallecitos Boiling Water

Reactor (VBWR), General Electric Test Reactor (GETR), and Empire State Atomic Development

Associates Incorporated Vallecitos Experimental Superheat Reactor (EVESR). A debrief

meeting was conducted on March 28, 2019, with you and members of your staff, and

representatives from the Wilmington, North Carolina office. The NRC inspectors performed

further in-office evaluation of the violations identified during the inspection. Upon completion of

the in-office evaluation, the NRC inspectors presented the results of the inspection and the

significance of the violations identified during the inspection to you and members of your staff,

during a final, telephonic exit meeting on May 16, 2019. The inspection results are documented

in the enclosure to this letter.

During this inspection, the NRC inspectors examined activities conducted under your licenses

as they relate to public health and safety, the environment, and to confirm compliance with the

Commissions rules and regulations, as well as with the conditions of your license. Within these

areas, the inspection consisted of the examination of selected procedures and representative

records, tour of the reactors and supporting equipment, independent radiation surveys, and

interviews with personnel.

Based on the results of this inspection, the NRC has determined that four Severity Level IV

violations of NRC requirements occurred. These violations were evaluated in accordance

with the NRC Enforcement Policy. The current NRC Enforcement Policy is included on the

NRCs Web site at (https://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html).

The violations are cited in the enclosed Notice of Violation (Notice) and the circumstances

surrounding them are described in detail in the subject inspection report. The violations are

being cited in the Notice because they were identified by the NRC and corrective actions had

not been fully articulated on the docket at the time of the final exit meeting. Therefore, you are

required to respond to this letter and should follow the instructions specified in the enclosed

M. Feyrer 2

Notice when preparing your response. If you have additional information that you believe the

NRC should consider, you may provide it in your response to the Notice. The NRC review of

your response to the Notice will also determine whether further enforcement action is necessary

to ensure compliance with regulatory requirements.

In accordance with 10 CFR 2.390 of the NRCs Agency Rules of Practice and Procedure, a

copy of this letter, its enclosures, and your response will be made available electronically for

public inspection in the NRC Public Document Room or from the NRCs Agencywide

Documents Access and Management System (ADAMS). ADAMS is accessible from the NRCs

Website at http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your response

should not include any personal privacy or proprietary, information so that it can be made

available to the Public without redaction.

Should you have any questions concerning this inspection, please contact Stephanie Anderson,

Health Physicist, at 817-200-1213 or the undersigned at 817-200-1223.

Sincerely,

/RA/

Gregory G. Warnick, Chief

Reactor Inspector Branch

Division of Nuclear Materials Safety

Docket Nos.: 050-00018; 050-00070;

and 050-00183

License Nos.: DPR-1; TR-1; and DR-10

Enclosures:

1. Notice of Violation

2. Inspection Report 050-00018/2019-001;

050-00070/2019-001; 050-00183/2019-001

w/Attachment: Supplemental Information

cc:

S. Murray, GE Hitachi Nuclear Energy Americas, LLC.

NOTICE OF VIOLATION

GE Hitachi Nuclear Energy Docket Nos.: 050-00018;

Vallecitos Boiling Water Reactor 050-00070; 050-00183

GE Test Reactor License Nos.: DPR-1; TR-1;

ESADA Vallecitos Experimental Superheat Reactor DR-10

During an NRC inspection conducted on March 25-28, 2019, four violations of NRC

requirements were identified. In accordance with the NRC Enforcement Policy, the violations

are listed below:

A. NRC License No. DPR-1, Amendment 21, License Condition 3.a. requires, in part, that

the licensee shall possess the facility in the condition described in the Final Report on

Deactivation of Vallecitos Boiling Water Reactor, dated February 5, 1965.

Final Report on Deactivation of Vallecitos Boiling Water Reactor,Section V., states, in

part, that the condition, security, and integrity of the retired facility will be checked during

the inspection, and the integrity of the reactor vessel will be verified.

Licensee Procedure 6.2, Patrols and Inspections, Revision 11, implements the license

requirements as stated above, and establishes the periodicity of the inspections.

Section 4.6, Annual Inspections and Radiation Surveys states, in part, that an

inspection, radiation and contamination surveys, and other surveillance activities for the

deactivated area, including the interior of the containment building for Vallecitos Boiling

Water Reactor (VBWR) are required to be performed by the facility license. The

conditions/requirements described in the Final Report on Deactivation of Vallecitos

Boiling Water Reactor include the following, in which the basement will be inspected for

water intrusion and sump pump system is properly functioning.

Contrary to the above, on September 13, 2018, the licensee failed to properly adhere to

License Condition 3.a., and adequately inspect the condition, security, and integrity of

the retired facility during the annual inspection. Specifically, during the licensees annual

inspection, the licensee failed to adequately inspect the spent fuel pit area of the VBWR

containment building, and as a result the licensee failed to identify standing water in the

spent fuel pit area of VBWR. Per the Final Report on Deactivation of Vallecitos Boiling

Water Reactor, dated February 5, 1965, the spent fuel pit was drained, the fuel racks

removed, and a cover had been installed on the top.

This is a Severity Level IV violation (Section 6.3).

B. 10 CFR 20.1501(a) requires, that the licensee shall make or cause to be made, surveys

of areas, including the subsurface, that: (1) may be necessary for the licensee to comply

with the regulations in this part; and (2) are reasonable under the circumstances to

evaluate: (i) the magnitude and extent of radiation levels; (ii) concentrations or quantities

of residual radioactivity; and (iii) the potential radiological hazards of the radiation levels

and residual radioactivity detected.

10 CFR 20.1003 defines survey, as an evaluation of the radiological conditions and

potential hazards incident to the production, use, transfer, release, disposal, or presence

of radioactive material or other sources of radiation. When appropriate, such an

evaluation includes a physical survey of the location of radioactive material and

Enclosure 1

measurements or calculations of levels of radiation, or concentrations or quantities of

radioactive material present.

Contrary to the above, on September 13-14, 2018, the licensee failed to make or cause

to be made, surveys of areas, including the subsurface, that: (1) may be necessary for

the licensee to comply with the regulations in this part; and (2) are reasonable under the

circumstances to evaluate: (i) the magnitude and extent of radiation levels; (ii)

concentrations or quantities of residual radioactivity; and (iii) the potential radiological

hazards of the radiation levels and residual radioactivity detected. Specifically, during

annual entries into the VBWR, General Electric Test Reactor (GETR), and Empire State

Atomic Development Associates Incorporated Vallecitos Experimental Superheat

Reactor (EVESR) containment buildings, the licensee failed to perform adequate

surveys in these buildings to demonstrate compliance with 10 CFR 20.1902, which

contains the posting requirements for radiation areas, high radiation areas, very high

radiation areas, airborne radioactivity areas, and areas or rooms in which licensed

material is used or stored. On March 26, 2019, multiple postings were observed by the

NRC inspectors in the VBWR, GETR, and EVESR containment buildings that did not

reflect current radiological conditions in those buildings because the licensee had not

fully evaluated the magnitude and extent of radiation levels in the areas that were

posted.

This is a Severity Level IV violation (Section 6.7).

C. 10 CFR 20.1501(c) requires, that the licensee shall ensure that instruments and

equipment used for quantitative radiation measurements (e.g., dose rate and effluent

monitoring) are calibrated periodically for the radiation measured.

Contrary to the above, on September 13-14, 2018, the instruments and equipment used

for quantitative radiation measurements during the annual surveys of the VBWR, GETR,

and EVESR containment buildings were not calibrated for the radiation measured

because the licensee failed to determine the radionuclide composition in these buildings.

Specifically, the licensee had not sampled and analyzed for hard-to-detect radionuclides

(i.e., low-energy beta emitters such as carbon-14 and nickel-63) or transuranics in the

reactor buildings, even though such radionuclides could exist in the buildings due to the

sites operational history.

This is a Severity Level IV violation (Section 6.7).

D. 10 CFR 20.1703(c)(1) requires, that the licensee shall implement and maintain a

respiratory protection program that includes air sampling sufficient to identify the

potential hazard, permit proper equipment selection, and estimate doses.

Contrary to the above, the licensee failed to implement and maintain a respiratory

protection program that includes air sampling sufficient to identify the potential hazard,

permit proper equipment selection, and estimate doses, as evidenced by the following

two examples:

1. On December 3, 2018, February 1 and 26, 2019, and March 26-28, 2019, the

licensee allowed workers to access multiple floors of the VBWR, GETR, and EVESR

containment buildings (including radioactively contaminated areas) but did not take air

2

samples on each floor level as required by Procedure 6.1, Access Control, Revision

8. In Appendix A, B, and C of Procedure 6.1, Access Control, Revision 8, there is a

step that states, in part, samples for air activity, lower explosive limit, and O2 should

be taken at each floor level visited. The licensee only took air samples on the entry

floor level of each containment building and failed to assess potential airborne

radiological hazards to workers on the other floor levels of the containment buildings.

2. On March 22, 2019, the licensee did not perform air sampling during non-routine

work activities that involved cleaning and vacuuming radioactively contaminated

sediment from the floor of the VBWR basement. Because no air sampling was

performed, the licensee failed to identify whether airborne radioactive material was

generated during these activities, and thus failed to identify the potential hazards to

workers. In addition, the failure to identify what airborne concentrations of radioactive

material may have been generated from the activities, resulted in a failure to estimate

potential doses to the workers.

This is a Severity Level IV violation (Section 6.7).

Pursuant to the provisions of Title 10 Code of Federal Regulation (CFR) 2.201, GE Hitachi

Nuclear Energy is hereby required to submit a written statement or explanation to the

U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,

DC 20555-0001, with a copy to the Regional Administrator, Region IV, 1600 E. Lamar Blvd.,

Arlington, TX 76011-4511, within 30 days of the date of the letter transmitting this Notice of

Violation (Notice). This reply should be clearly marked as a "Reply to a Notice of Violation and

should include for each violation: (1) the reason for the violation, or, if contested, the basis for

disputing the violation or severity level; (2) the corrective steps that have been taken and the

results achieved; (3) the corrective steps that will be taken; and (4) the date when full

compliance will be achieved.

Your response may reference or include previously docketed correspondence, if the

correspondence adequately addresses the required response. If an adequate reply is not received

within the time specified in this Notice, an order or a Demand for Information may be issued

requiring information as to why the license should not be modified, suspended, or revoked, or why

such other action as may be proper should not be taken. Where good cause is shown,

consideration will be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001, with a copy to the Regional

Administrator, Region IV.

Your response will be made available electronically for public inspection in the NRC Public

Document Room or in the NRCs Agencywide Documents Access and Management System

(ADAMS), accessible from the NRC Web site at: http://www.nrc.gov/reading-rm/adams.html.

To the extent possible, your response should not include any personal privacy, proprietary or

safeguards information so that it can be made available to the public without redaction.

In accordance with 10 CFR 19.11, you may be required to post this Notice within two working

days of receipt.

Dated this 24th day of June 2019

3

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.: 050-00018; 050-00070; and 050-00183

License Nos.: DPR-1; TR-1; and DR-10

Report Nos.: 050-00018/2019-001; 050-00070/2019-001; and 050-00183/2019-001

Licensee: GE Hitachi Nuclear Energy

Facility: Vallecitos Boiling Water Reactor (VBWR)

GE Test Reactor (GETR)

ESADA Vallecitos Experimental Superheat Reactor (EVESR)

Location: 6705 Vallecitos Road

Sunol, California

Inspection Dates: March 25-28, 2019

Inspectors: Stephanie G. Anderson, Health Physicist

Reactor Inspector Branch

Division of Nuclear Materials Safety

Chris D. Steely, Health Physicist

Reactor Inspector Branch

Division of Nuclear Materials Safety

Jack D. Parrott, Senior Project Manager

Reactor Decommissioning Branch

Office of Nuclear Materials Safety and Safeguards

Anthony M. Huffert, CHP, Senior Health Physicist

Reactor Decommissioning Branch

Office of Nuclear Materials Safety and Safeguards

N. Jeff Griffis, CHP, Senior Health Physicist

Specialized Technical Training & Support Branch

Office of the Chief Human Capital Officer

Accompanied By: Bruce A. Watson, CHP, Branch Chief

Reactor Decommissioning Branch

Office of Nuclear Materials Safety and Safeguards

Approved By: Gregory G. Warnick, Branch Chief

Reactor Inspector Branch

Division of Nuclear Materials Safety

Enclosure 2

EXECUTIVE SUMMARY

GE Hitachi Nuclear Energy

NRC Inspection Report 050-00018/2019-001; 050-00070/2019-001; and 050-00183/2019-001

This U.S. Nuclear Regulatory Commission (NRC) inspection was a routine, announced inspection

of licensed activities being conducted at the three permanently defueled reactors at the Vallecitos

Nuclear Center. In summary, the inspectors identified four Severity Level IV violations and opened

one unresolved item, associated with various regulatory and license requirements. Other than the

four identified violations and one unresolved item, the licensee was conducting site activities in

accordance with regulatory, license, and procedure requirements.

Decommissioning Performance and Status Review at Permanently Shutdown Reactors and

Class III Research and Test Reactors

  • The licensee conducted annual inspections and audits of the three shutdown reactors in

accordance with regulatory, license, and procedure requirements, with one exception. The

inspectors identified a violation of license requirements associated with the adequacy of the

annual inspection of the Vallecitos Boiling Water Reactor containment building. (Section 1.2)

Organization, Management and Cost Controls at Permanently Shutdown Reactors

  • The NRC inspectors concluded that the licensee was adequately implementing their

organization that reflected the shutdown reactors license requirements and adequately

managed the workload to support the shutdown reactors activities. One unresolved item

was identified by the inspectors related to regulatory compliance of 10 CFR 50.71(e)(4)

requirements for submitting a revision to the final safety analysis report every 24 months.

(Section 2.2)

Safety Reviews, Design Changes, and Modifications at Permanently Shutdown Reactors

  • The licensee implemented its safety review program in accordance with its procedures and

regulatory requirements. (Section 3.2)

Self-Assessment, Auditing, and Corrective Action at Permanently Shutdown Reactors

  • The NRC inspectors concluded that the licensee had not been fully implementing the

corrective action program Procedure, CP-16-108, Corrective Action Program, Revision 11,

and that licensee personnel were not consistently identifying conditions adverse to quality or

conditions needing improvement. These findings are not considered violations of the

regulations or the Vallecitos Boiling Water Reactor license requirements, however, the

failure to fully implement the corrective action program procedure should be entered into the

licensees corrective action program for resolution. (Section 4.2)

Occupational Radiation Exposure

  • The inspectors concluded that the licensee conducted its radiation control program in

accordance with license conditions and regulatory requirements, with three exceptions.

The inspectors identified three violations in program areas related to occupational radiation

exposure. (Section 5.2)

2

Report Details

Summary of Plant Status

The GE Hitachi Nuclear Energy Americas, LLC (GEH or Licensee) continued to maintain the

three shutdown reactors, Vallecitos Boiling Water Reactor (VBWR), General Electric Test

Reactor (GETR), and Empire State Atomic Development Associates Incorporated Vallecitos

Experimental Superheat Reactor (EVESR) in a possession-only, safe storage (SAFSTOR)

condition, with no fuel remaining in the reactors or spent fuel pools. The condition of SAFSTOR

is a decommissioning alternative in which the licensee is authorized to maintain the facility in a

condition that allows the nuclear facility to be safely stored and subsequently decontaminated to

levels that permit release for unrestricted use within 60 years of permanent cessation of

operations. Licensees who choose the SAFSTOR option must meet all NRC financial and safety

regulations, both prior to and during the SAFSTOR period.

On April 24, 2015 (ADAMS Accession Number Nos. ML15114A437 and ML15114A438) the

licensee submitted a request for a partial site release of approximately 610 acres of non-impacted

property on the northern section of Vallecitos Nuclear Center (VNC) site, for unrestricted use

pursuant to Title 10 Code of Federal Regulation (CFR) 50.83(b). The NRC approved the partial

site release of 610 acres by letter dated May 3, 2016 (ADAMS Accession Number No.

ML16007A348). The property continues to remain under the ownership of GEH.

On December 15, 2015, the licensee submitted a request for license continuance under

10 CFR 50.51(b) for reactor licenses DR-10 and TR-1 (ADAMS Accession Number No.

ML15349A045). That request was approved by letter dated January 2, 2019 (ADAMS

Accession Number No. ML18352A450). The licensee also submitted a request on July 10,

2015 (ADAMS Accession Number No. ML15195A088) for an alternate decommissioning

schedule as described in 10 CFR 50.82(a)(3) and 50.82(b)(4)(i), using the exemption criteria of

10 CFR 50.12.

On May 16, 2017, the NRC staff issued a request to GEH for additional information on the

structural integrity of the reactor buildings and how the integrity would be ensured during the

extended decommissioning period, in order to assess whether the request would result in undue

risk to public health and safety (ADAMS Accession Number No. ML17138A121). The licensee

responded to this request by letter dated July 31, 2017 (ADAMS Accession Number No.

ML17212B019).

Based on this response and a site visit conducted by NRC on September 13, 2017, the NRC

determined that certain additional information must be provided by GEH to show how the

licensee is ensuring the confinement of residual radioactivity associated with the shutdown

reactors at the VNC and evaluating and monitoring the long term physical safety of the reactor

structures. The NRC requested more detailed information by letter dated January 18, 2018

(ADAMS Accession Number No. ML17312B359). On March 28, 2018 (ADAMS Accession

Number No. ML18087A384) GEH provided a response indicating that it would provide an interim

status report for the hydrological and structural analyses in approximately 6 months and

anticipated completing the actions within approximately 12 months, which would be March 2019.

On May 31, 2018 (ADAMS Accession Number No. ML18151A861), GEH submitted a partial

response to the request for additional information. On October 23, 2018 (ADAMS Accession

Number No. ML18296A159), GEH provided an interim status report on the efforts to respond to

the two-remaining request for additional information. On March 28, 2019 (ADAMS Accession

Number No. ML19087A221), GEH provided the response to the additional information to the

3

NRCs request for the information needed to support the exemption request for an alternate

decommissioning schedule.

On December 14, 2018 (ADAMS Accession Number No. ML18348A425), the licensee

submitted a request for a partial site release of approximately 7 acres of non-impacted property

along Vallecitos Road to be made available to Alameda County Transportation Commission to

support road development and widening. The NRC held a public meeting in Dublin, CA on

March 28, 2019, as required by 10 CFR 50.83, Release of part of a power reactor facility or site

for unrestricted use, to discuss the request for the partial site release.

1 Decommissioning Performance and Status Review at Permanently Shutdown

Reactors (71801) and Class III Research and Test Reactors (69002)

1.1 Inspection Scope

The inspectors reviewed the licensees control and oversight of the three shutdown

reactors.

1.2 Observations and Findings

a. Status and tours of the shutdown reactors

1. Vallecitos Boiling Water Reactor

Vallecitos Boiling Water Reactor (VBWR) is a possession-only reactor under License

No. DPR-1, Amendment 21. It was a 50-megawatt (MW) power reactor that achieved

full power operations in 1957, after receiving its Construction Permit No. CPPR-3 on

May 14, 1956. It was shutdown on December 9, 1963, for an extended period of time

and subsequently was deactivated. All fuel has been removed from the facility.

The possession-only facility license DPR-1, License Condition 4 states in part, that

there should be an audible control device maintained on the doors to the containment

building. In addition, License Condition 5 authorizes GE Hitachi (GEH) to dispose of

component parts or devices from the VBWR facility in accordance with the provisions

of 10 CFR Part 20. The licensee removed extensive components from the facility

between October 2007 and November 2008. All reactor systems have been removed

except for the reactor vessel. The licensee monitored the water level in the reactor

vessel and the inspectors confirmed that it had remained essentially constant at

approximately 95 inches of water, since the last NRC inspection conducted in August

2018. Due to groundwater intrusion, the licensee has installed a sump pump and piping

in the basement of containment in order to remove any groundwater intrusion or

condensation to a transfer tank located adjacent to the containment structure. This

water is ultimately transferred to the onsite waste evaporator plant (WEP) for processing.

The inspectors toured the facility with licensee representatives. The inspectors

confirmed there was an audible control device functioning on the manual doors to the

containment building that provided an alarm at the 300-area alarm panel and at the

Central Alarm Station. The inspectors observed that the roll-up door was secured, which

was installed in place of the equipment hatch. The inspectors entered the basement

level to observe the condition and integrity of the retired facility. The inspectors

observed crack formation and water seepage down the walls. The cracks are being

4

monitored by the licensee to determine growth rate. During the tour, the NRC inspectors

questioned the condition and integrity of the spent fuel pit area, which had accumulation

of water at least several inches deep after observing it from the main floor of the VBWR

containment building looking down between the gaps in the steel plates covering the

area. This area had not been previously identified by the licensee during the annual

surveys to have standing water. The Final Report on Deactivation of Vallecitos Boiling

Water Reactor,Section V., states, in part, that the condition, security, and integrity of

the retired facility will be checked during inspection and the integrity of the reactor vessel

will be verified. Also, per the Final Report on Deactivation of Vallecitos Boiling Water

Reactor, the spent fuel pit was drained, the fuel racks removed, and a cover had been

installed on the top.

License Condition 3.a. states, in part, that the licensee shall possess the facility in the

condition described in the Final Report on Deactivation of Vallecitos Boiling Water

Reactor dated February 5, 1965. Procedure 6.2, Patrols and Inspections,

Revision 11, implements the license requirements as stated above. Section 4.6, Annual

Inspections and Radiation Surveys states, in part, that inspections, radiation and

contamination surveys, and other surveillance activities for the deactivated area,

including the interior of the containment building for VBWR are required to be performed

by the facility license. The conditions/requirements described in the Final Report on

Deactivation of Vallecitos Boiling Water Reactor include the following, in which the

basement will be inspected for water intrusion and sump pump system is properly

functioning. The inspectors determined that during the licensees annual inspection, the

licensee failed to adequately inspect the spent fuel pit area of the VBWR containment

building, and as a result the licensee failed to identify standing water in the spent fuel pit

area of VBWR, and as described above, this is considered a violation of License

Condition 3.a. (VIO 0500018/2019001-01).

During the previous NRC inspection in August 2018, the NRC inspectors identified a

violation (VIO 05000018/2018001-01) associated with License Condition 3.a., which

requires the licensee to possess the facility in the condition described in the Final

Report of Deactivation of Vallecitos Boiling Water Reactor. Licensee Procedure 6.2,

Patrols and Inspections, Revision 7, required the licensee to inspect the condition and

integrity of the retired facility and verify the integrity of the reactor vessel during the

annual inspection, as well as on a weekly basis check the VBWR reactor vessel water

level (ADAMS Accession No. ML18261A410).

The licensee responded to the Notice of Violation (NOV) by letter dated October 19,

2018 (ADAMS Accession No. ML18292A751). During a telephonic conference on

December 19, 2018, between GE Hitachi and NRC staff, the licensee was requested to

submit additional information to describe their corrective actions. The supplemental

information regarding GE Hitachis response to the NOV was received by letter dated

January 23, 2019 (ADAMS Accession No. ML19023A306). The licensees corrective

actions included revising Procedure 6.2, Patrols and Inspection, to inspect the

condition and integrity of retired facility monthly to check for water intrusion in the VBWR

basement. The licensee also installed a transfer tank in the building next to the VBWR

containment building and installed a sump pump in the basement, to pump the water

from the basement to the transfer tank. The licensee replaced the broken manometer

and purchased a spare manometer to measure water in the VBWR reactor vessel on the

required weekly basis. The implementation of these corrective actions closes the

violation.

5

2. ESADA Vallecitos Experimental Superheat Reactor

The ESADA Vallecitos Experimental Superheat Reactor (EVESR) is a possession-only

reactor under License No. DR-10, Amendment No. 7. The EVESR was a light water

moderated, steam cooled, superheat, experimental research reactor that used slightly

enriched uranium dioxide as fuel. It operated at a maximum of 17 MW thermal and was

initially licensed in 1963. It achieved full power operation in 1964, and was shut down on

February 1, 1967, and subsequently deactivated. All fuel and other special nuclear

material has been removed and shipped offsite. In addition, a significant amount of

equipment used to operate the reactor, such as nuclear instrumentation, piping, pumps,

and valves had been removed.

The inspectors toured the facility with licensee representatives. The inspectors

confirmed there was an audible control device functioning on the airlock door to the

containment building that provided an alarm at the 300 feet elevation area alarm panel

and at the Central Alarm Station. The licensee had a portable dehumidifier to remove

significant quantities of condensation that tended to build-up in the facility. The licensee

had temporary lighting installed and it was operating sufficiently to ensure the

passageways and stairs were safely lit. The stack was no longer operational, and the

licensee was using a portable ventilation system.

The radiation levels were generally less than 1 milliroentgen per hour (mR/hr) throughout

the facility, except in certain areas. The inspectors measured 1.8 mR/hr on the two

emergency cooling discharge valves located on the 534-ft level, using a Thermo

Scientific RadEye G gamma survey meter (Serial No. 30728, calibration due date of

December 12, 2019). The licensee maintained concrete blocks over the reactor vessel

and the head/shield plug storage pit. In addition, a wooden cover was installed over the

empty spent fuel storage pool, with an installed railing to prevent entry since the wooden

cover was not designed to support a load. The licensee maintained control of the keys

to the locked cover installed over the stairwell that provided access to areas below the

main 549-ft level.

3. General Electric Test Reactor

The General Electric Test Reactor (GETR) is a possession-only reactor under License

No. TR-1, Amendment No. 17. The reactor was a 50 MW thermal experimental test,

development, and isotope production reactor that utilized highly enriched plate fuel and

was initially licensed to operate in 1959. The reactor was shutdown in 1977 and

subsequently deactivated. All fuel and isotope production targets containing special

nuclear material have been removed from the facility and shipped offsite. The reactor,

systems and piping, and spent fuel pool have been drained of water. The licensee

explained that the containment polar crane was functional, and only required

recertification for it to be considered operable.

The tank farm located outside the control room building had three underground tanks

and one above ground tank, with each one having a capacity of 25,000 gallons. The

licensee stated the underground tanks were monitored on a quarterly basis. As needed,

the water from the tanks was transferred by piping to the above ground tank and the

water was subsequently transported by a mobile tank to the onsite WEP for processing.

6

The inspectors toured the containment building and GETR auxiliary buildings

immediately adjacent to the containment structure. It was noted by inspectors that

Building 202, which was empty of equipment and personnel, was in very poor physical

condition with the structure being open to the elements via degradation of the roof and

sides. This allows rain intrusion and animals ingress and egress to/from the structure

with the possibility of potentially contaminated material being carried away to outside the

structure. A radiation survey of the wash-outs and boundary area near the building did

not identify any radiological contamination.

As GETR has been shutdown since 1977 there are no licensed operators nor a

requalification program which is appropriate for the plant conditions. Staffing was

appropriate to meet the required weekly surveillance patrols which were being

conducted in accordance with site procedures.

1.3 Conclusions

The licensee conducted annual inspections and audits of the three shutdown reactors in

accordance with regulatory, license, and procedure requirements, with one exception.

The inspectors identified a violation of license requirements associated with the

adequacy of the annual inspection of the VBWR containment building.

2 Organization, Management and Cost Controls at Permanently Shutdown Reactors

(36801)

2.1 Inspection Scope

The inspectors evaluated the licensees organizational structure to support licensed

activities and regulatory requirements.

2.2 Observations and Findings

The licenses for the three shutdown reactors require in part, that activities involving

access to the facility area and use of any area shall be conducted under the direction of

a designated facility manager with functional responsibility and commensurate authority

to maintain the facility in a safe and secure condition at all times. The NRC inspectors

reviewed the licensees organization and discussed the organizational structure with

members of the licensees organization. The Vallecitos Nuclear Center (VNC)

organization was structured under two divisions, identified as Operations and

Support. The VNC Site Manager had operational and support experience as a result of

past work experience in multiple areas within the GEH system. The Manager reported

to Services Operations in Wilmington, North Carolina. The inspectors observed there

was good communications and support between the VNC facility and operations in

Wilmington, North Carolina. Based on discussions and observations, the NRC

inspectors determined that the individual fulfilling the licensed responsibility as the facility

manager for the defueled reactors, adequately met the license condition requirements.

The NRC inspectors reviewed the routine activities performed at the three defueled

reactors and reviewed the organization structure that supported those activities. Based

on the review and discussions with licensee representatives, there had not been any

significant changes to the organization or new personnel hired to perform the routine

radiological safety activities at the shutdown reactors. Since the last inspection, GEH

7

hired a new regulatory affairs and licensing lead to be onsite at GEH. The inspectors

observed that the staff have a great deal of historical knowledge of processes that may

not be completely captured in training documents or procedures.

The inspectors completed a review of various license and regulatory requirements while

onsite. The inspectors were unable to complete the review of the decommissioning files

required to be maintained by the licensee pursuant to 10 CFR 50.75(g).

Title 10 CFR 50.71(e)(4) requires in part, subsequent revisions of the final safety

analysis report (FSAR) must be filed annually or 6 months after each refueling outage

provided the interval between successive updates does not exceed 24 months. The

revisions must reflect all changes up to a maximum of 6 months prior to the date of

filling. For nuclear power reactor facilities that have submitted the certifications required

by 10 CFR 50.82(a)(1), subsequent revisions must be filed every 24 months. During the

review of the requirements of 10 CFR 50.71(e)(4) and applicability to the two shutdown

power reactors, VBWR and EVESR, the inspectors concluded that there was not enough

information to determine if the licensee was in compliance with the regulatory

requirement, and this issue was identified as an unresolved item

(URI 05000183/2019-001).

2.3 Conclusions

The NRC inspectors concluded that the licensee was adequately implementing

their organization that reflected the shutdown reactors license requirements and

adequately managed the workload to support the shutdown reactors activities.

One unresolved item was identified by the inspectors related to regulatory compliance

of 10 CFR 50.71(e)(4) requirements for submitting a revision to the FSAR every

24 months.

3 Safety Reviews, Design Changes, and Modifications at Permanently Shutdown

Reactors (37801)

3.1 Inspection Scope

The inspectors reviewed the licensees control and oversight of the safety review

program to ensure design changes, tests, experiments and modifications are effectively

conducted, managed, and controlled during plant decommissioning.

3.2 Observations and Findings

Within the past three years, the licensee has only made one modification to the existing

plant systems of VBWR, EVESR, and GETR. This is due to the length of time since

shutdown for VBWR, EVESR, and GETR that most, if not all, reactor systems, with the

exception of the vessels, have been removed. All three reactors have been in

SAFSTOR status for several decades.

In 2018, the licensee added a sump pump and transfer piping from the basement sump

of the VBWR to an outside adjacent transfer tank to collect accumulated water, which

will then be transferred to the WEP for processing. The inspectors were able to review

the process of this modification against licensee Procedure 2.0, Change Authorization,

8

Revision 18. This procedure adequately details the necessary change process and

management reviews in order to safely modify any existing equipment.

The inspectors determined that the addition of the sump pump and transfer piping from

the VBWR basement to the outside transfer tank was properly planned, performed, and

managed through the licensee change process. At the time of the inspection, the

automatic function of the sump pump was not in operation but was performed manually

on an as needed basis.

3.3 Conclusions

The licensee implemented its safety review program in accordance with its procedures

and regulatory requirements.

4 Self-Assessment, Auditing, and Corrective Action at Permanently Shutdown

Reactors (40801)

4.1 Inspection Scope

The inspectors reviewed the licensees corrective action program related to the oversight

of the three shutdown reactors.

4.2 Observations and Findings

At the time of the inspection the licensee was implementing its corrective action program

under procedure CP-16-108, Corrective Action Program, Revision 11. The procedure

applies to the GEH nuclear sites and facilities at VNC. According to the procedure, any

employee may initiate a condition report.

The priority levels for issues identified in the corrective action program ranged from A

to D, with A being a significant condition adverse to quality, B was a condition

adverse to quality, C was similar to broke/fix or conditions that had minimal effect on

the safe or reliable operation of a component or facility, and D was considered an

improvement item.

A condition report of a Priority Level B, was initiated by GEH from the observation made

by the NRC during the August 2018 inspection that water discovered and left for an

extended period of time in the basement of the VBWR was evidence of a failure to

implement procedure 6.2, Patrols and Inspections, Revision 7, for the activities

associated with VBWR, which was a violation of license requirements.

According to procedure CP-16-108, Corrective Action Program, Revision 11, the

resolution of the Level B condition report written in response to the violation required the

licensee to conduct an extent of condition review of water intrusion into the VBWR.

Contrary to that requirement, and the requirement in the license to fully inspect the

condition and integrity of the retired facility, the area of the VBWR identified as the spent

fuel pit had an accumulation of water at least several inches deep that had gone

unidentified by the licensee and was only identified when the NRC inspectors questioned

the condition of that area after observing it from the main floor of the VBWR containment

building looking down between gaps in the steel plates covering that area. On

9

September 13, 2018, the VBWR annual survey was completed with one abnormality

observed, which was approximately one inch of water on the basement floor.

However, this corrective action program observation, of failure to perform an extent of

condition review when evaluating the violation from August 2018 per the corrective

action program procedure, CP-16-108, Corrective Action Program, Revision 11 is not a

violation. The VBWR license does not have a license condition to require the site to

implement procedures, therefore failing to follow a procedure cannot be a violation of the

VBWR license and therefore is described here as an inspection observation.

The inspectors also reviewed a summary of the condition reports generated since the

January 1, 2017, for those whose scope focused primarily on the shutdown reactors at

VNC. Six condition reports were identified that were primarily focused on the shutdown

reactors. Review of these condition reports revealed that they were all written in

response to NRC observations made during inspection of the facility or were in response

to NRC questions in relation to the licensee request for an alternate decommissioning

schedule for the shutdown reactors. In other words, none of the shutdown reactor

specific condition reports identified and reviewed by the NRC inspectors were initiated

directly from licensee personnel observations of the conditions of the shutdown reactors.

Even though NRC inspectors and technical reviewers have observed and identified

apparent conditions adverse to safety at these facilities, none were identified and

documented by site personnel.

4.3 Conclusions

The NRC inspectors concluded that the licensee had not been fully implementing the

corrective action program Procedure, CP-16-108, Corrective Action Program,

Revision 11, and that licensee personnel were not consistently identifying conditions

adverse to quality or conditions needing improvement. These findings are not

considered violations of the regulations or the VBWR license requirements, however, the

failure to fully implement the corrective action program procedure should be entered into

the licensees corrective action program for resolution.

5 Occupational Radiation Exposure (83750)

5.1 Inspection Scope

The inspectors reviewed the licensees radiation protection program related to the

oversight of the three shutdown reactors.

5.2 Observations and Findings

Each of the shutdown reactors have license conditions that require annual surveys be

performed and submitted to the NRC. On September 13-14, 2018, the licensee entered

the VBWR, EVESR, and GETR containment buildings to perform the annual surveys.

Since the last annual inspection, the licensee had also performed non-routine work in

the basement of the VBWR containment building. This work involved cleaning

radioactively contaminated sediment out of the VBWR basement sump and installation

of drain lines to remove standing water. Licensee personnel wore coveralls, booties and

gloves to minimize contamination when entering the shutdown containment buildings for

both the routine surveys and non-routine work. During the inspection, the NRC

10

inspectors toured all accessible areas within the VBWR, EVESR, and GETR

containment buildings to observe radiological postings and perform independent

radiation surveys to ensure that the postings adequately reflected the radiological

hazards. During those tours on March 27, 2019, the inspectors identified multiple

postings that did not reflect the radiological conditions that currently existed in the areas

that were observed. In addition, inspectors identified multiple locked rooms within the

containment buildings that were posted as high radiation areas or airborne radioactivity

areas, and there were no documented surveys of these rooms or knowledge of the

current radiological conditions within the rooms to demonstrate that they were

appropriately posted.

Title 10 CFR 20.1501(a) requires that the licensee shall make or cause to be made,

surveys of areas, including the subsurface, that: (1) may be necessary for the licensee to

comply with the regulations in this part; and (2) are reasonable under the circumstances

to evaluate: (i) the magnitude and extent of radiation levels; (ii) concentrations or

quantities of residual radioactivity; and (iii) the potential radiological hazards of the

radiation levels and residual radioactivity detected. Title 10 CFR 20.1003 defines

survey, as an evaluation of the radiological conditions and potential hazards incident to

the production, use, transfer, release, disposal, or presence of radioactive material or

other sources of radiation. When appropriate, such an evaluation includes a physical

survey of the location of radioactive material and measurements or calculations of levels

of radiation, or concentrations or quantities of radioactive material present. The

inspectors determined that during the annual entries into the VBWR, GETR, and EVESR

containment buildings the licensee failed to perform adequate surveys in these buildings

to demonstrate compliance with 10 CFR 20.1902, which contains the posting

requirements for radiation areas, high radiation areas, very high radiation areas, airborne

radioactivity areas, and areas or rooms in which licensed material is used or stored, and

as described above, this is considered a violation of 10 CFR 20.1501(a)

(VIO 0500018/2019001-02).

In addition to the tours of the containment buildings, the inspectors reviewed the

procedures that the licensee used to quantify contamination levels within the three

containment buildings during the performance of their annual surveys. From this review

and subsequent discussions with licensee staff, inspectors determined that the licensee

had not verified the radionuclide mixture in the three containment buildings. Without

knowing the specific radionuclides that were present in the containment buildings, the

licensee could not design a survey program that could adequately detect or quantify the

radioactivity in those buildings. Also, the licensee did not have the information

necessary to determine accurate detection efficiencies for survey instruments used to

make quantitative measurements during their annual surveys.

Title 10 CFR 20.1501(c) states the licensee shall ensure that instruments and equipment

used for quantitative radiation measurements (e.g., dose rate and effluent monitoring)

are calibrated periodically for the radiation measured. The inspectors determined that

the licensee had not sampled and analyzed for hard-to-detect radionuclides (i.e., low-

energy beta emitters such as carbon-14 and nickel-63) or transuranics in the

containment buildings, even though such radionuclides could exist in the buildings due

to the sites operational history, and as described above, this is considered a violation

of 10 CFR 20.1501(c) (VIO 0500018/2019001-03).

11

The inspectors reviewed elements of the licensees radiation protection program

associated with occupational radiation safety for staff who perform work around or within

the three shutdown reactors. This included a review of the licensees procedures for

conducting radiation and contamination surveys, posting and communicating radiological

hazards to workers, air sampling, surveying and release of personnel and equipment

from contaminated areas, and calibration and use of portable radiation survey

instruments and counting equipment. In addition, the inspectors reviewed procedures

for personnel entry into the three containment buildings, and how the licensee conducted

radiological monitoring of employees who entered the containment buildings.

During interviews with the licensee, the inspectors discussed how air sampling was

performed for workers entering the VBWR, EVESR, and GETR containment buildings.

In addition, air sample results were reviewed for multiple containment building entries

from December 2018 through March 2019. The licensee considered the collection of air

samples that were gathered were routine samples that were taken in the containment

buildings prior to personnel entry into the containment buildings part of their routine

survey procedures. In some instances, air sampling was performed only on one floor

level of a given containment building, even though staff had entered other floor levels of

the containment buildings to perform work.

In addition, inspectors identified that air samples were taken prior to entry into the

containment buildings, but no air sampling was done while workers were actually

performing activities in the buildings. After further discussions with the licensee, it was

determined that workers had entered the VBWR basement on at least one occasion to

perform non-routine work that involved vacuuming and cleaning of radioactive

sediments. No air samples were taken during these non-routine activities to determine

whether radioactive material in the sediments had become airborne and posed an

internal hazard to the workers. Because no air sampling was performed, the licensee

failed to identify whether airborne radioactive material was generated during these

activities, and thus failed to identify the potential hazards to workers. In addition, the

failure to identify what airborne concentrations of radioactive material may have been

generated from the activities resulted in a failure to estimate potential doses to the

workers.

Title 10 CFR 20.1703(c)(1) states that the licensee shall implement and maintain a

respiratory protection program that includes air sampling sufficient to identify the

potential hazard, permit proper equipment selection, and estimate doses. The

inspectors determined that the licensee failed to perform sufficient air sampling to

identify potential radiological hazards to workers entering the VBWR, GETR, and

EVESR containment buildings, and as described above, this is considered a violation

10 CFR 20.1703(c)(1) (VIO 0500018/2019001-04).

During the inspection, the inspectors conducted independent radiation surveys in the

VBWR, GETR and EVESR containment buildings. The inspectors used a Thermo

Fisher Scientific Model SX with a Thermo Fisher Scientific SPA-3 sodium iodide (NaI(Tl))

detector (Serial Nos. 52210 and 19212, calibration due date March 3, 2020) for

measuring dose rates, and a Thermo Fisher Scientific E-600 with a Thermo Fisher

Scientific HP-380AB alpha-beta scintillation probe (Serial Nos. 02463 and 00906,

calibration due date November 13, 2019) for measuring alpha and beta contamination

levels. In general, dose rate levels within each containment building were consistent

with information contained in the licensees 2018 annual shutdown reactor report, dated

12

March 27, 2019 (ADAMS Accession No. ML19087A125). However, radiation levels in

specific containment building locations were elevated in comparison to information

contained in the licensees 2018 annual shutdown reactor report.

At locations where elevated radiation levels were measured within VBWR and GETR,

the inspectors collected a total of fifteen dry smear samples to identify radionuclides that

were present as removable contamination on concrete surfaces. The dry smear

samples were analyzed by the U.S. Department of Energys Radiological and

Environmental Sciences Laboratory, which served as the NRCs independent

radioanalytical laboratory for this inspection. The results were evaluated to identify the

presence of radionuclides using a 95 percent confidence interval (plus and minus two

standard deviations) of the measurement result. Although the sample collection size

limited the number of radioanalytical procedures that could be performed on each dry

smear sample, collectively the analyses identified a spectrum of radionuclides in

removable surface contamination within both buildings.

The inspectors collected seven dry smear samples in VBWR. On the entry floor level of

VBWR, cesium-137 and strontium-90 were identified in the inspectors samples. On the

VBWR basement floor level, americium-241, cesium-137, cobalt-60, plutonium-238/239,

strontium-90, and uranium-234/235/238 were identified in the inspectors smear

samples. The licensee collected nine dry smear samples near the inspectors smear

sample locations and provided duplicate samples to the inspectors. Analysis of the

licensees dry smears samples by the NRCs independent radioanalytical laboratory

identified similar radionuclides as the dry smears collected by the inspectors, with the

addition of nickel-63 on a VBWR basement floor level sample.

The inspectors collected eight dry smear samples in GETR. On the entry and top floor

levels of GETR, americium-241, cesium-137, cobalt-60, strontium-90, technecium-99,

and uranium-234/235/238 were identified. Cesium-137 and cobalt-60 were identified on

the basement floor level. The licensee provided five duplicate samples of their dry

smear samples collected on the entry floor level. The NRCs independent

radioanalytical laboratory identified cesium-137, nickel-63, and technicium-99 in the

licensees samples.

5.3 Conclusions

The inspectors concluded that the licensee conducted its radiation control program in

accordance with license conditions and regulatory requirements, with three exceptions.

The inspectors identified three violations in program areas related to occupational

radiation exposure.

6 Exit Meeting Summary

On May 16, 2019, the NRC inspectors presented the final inspection results to Mr. Matt

Feyrer, Site Manager and other members of the licensees staff. The inspectors asked

the licensee whether any material examined during the inspection should be considered

proprietary information. No proprietary information was identified.

13

SUPPLEMENTAL INSPECTION INFORMATION

KEY POINTS OF CONTACT

Licensee

M. Feyrer, Site Manager

B. Lockwood, GEH Senior VP Manufacturing

J. Smyly, Environmental, Health and Safety Manager

S. Murray, GEH Licensing Manager

D. Hart, Senior VP Environmental, Health, and Safety

D. Heckman, Regulatory Affairs and Licensing Lead

K. Zanotto, Lead Manufacturing Projects

J. Ayala, Radiation Protection Supervisor

H. Stuart, Radiation Monitor Technician

INSPECTION PROCEDURES

IP 71801 Decommissioning Performance and Status Review at Permanently Shutdown Reactors

IP 69002 Class III Research and Test Reactors

IP 36801 Organization, Management, and Cost Controls at Permanently Shutdown Reactors

IP 37801 Safety Reviews, Design Changes, and Modifications at Permanently Shutdown Reactors

IP 40801 Self-Assessment, Auditing, and Corrective Action at Permanently Shutdown Reactors

IP 83750 Occupational Radiation Exposure

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000018/2019001-01 VIO Failure to implement Procedure 6.2, Patrols and

Inspections, Revision 11, for activities associated with

VBWR.05000018/2019001-02 VIO Failure to perform adequate surveys in VBWR, GETR,

and EVESR containment buildings to demonstrate

compliance with 10 CFR 20.1501(a).05000018/2019001-03 VIO Failure to ensure that instruments and equipment used

for radiation measurements in the containment

buildings are calibrated for the radiation measured in

compliance with 10 CFR 20.1501(c).05000018/2019001-04 VIO Failure to implement and maintain a respiratory

protection program, for activities associated with air

sampling of the containment buildings in compliance

with 10 CFR 20.1703(c)(1).05000183/2019001-01 URI Regulatory Compliance with 10 CFR 50.71(e)(4)

requirements for final safety analysis report.

Closed

05000018/2018001-01 VIO Failure to implement Procedure 6.2, Patrols and

Inspections, Revision 7, for activities associated with

VBWR.

Attachment

LIST OF ACRONYMS

ADAMS Agency Documents Access and Management Systems

CFR Code of Federal Regulations

CR Condition Report

EVESR Empire State Atomic Development Associates Incorporated Vallecitos

Experimental Superheat Reactor

FSAR Final Safety Analysis Report

GEH GE Hitachi Nuclear Energy Americas, LLC

GETR General Electric Test Reactor

MW Megawatt

NRC U.S. Nuclear Regulatory Commission

NOV Notice of Violation

URI Unresolved Item

VBWR Vallecitos Boiling Water Reactor

VIO Violation

VNC Vallecitos Nuclear Center

WEP Waste Evaporator Plant

2

ML19163A294

SUNSI Review ADAMS: Sensitive Non-Publicly Available Keyword

By: SGA Yes No Non-Sensitive Publicly Available NRC-002

OFFICE DNMS/RIB DNMS/RIB DNMS/MIB OCHFO

NAME SGAnderson CDSteely JFKatanic NJGriffis

SIGNATURE /RA/ /RA/via email /RA/ /RA/via email

DATE 6/17/19 6/24/19 6/14/19 6/14/19

OFFICE NMSS/RDB NMSS/RDB C:RIB

NAME JDParrott AMHuffert GGWarnick

SIGNATURE /RA/via email /RA/via email /RA/

DATE 6/18/19 6/14/19 6/24/19