05000354/LER-1997-034, Forwards LER 97-034-01, Condition Prohibited by Ts:Missed EDG Surveillance. Util Commitments to NRC Re Subj LER Encl

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Forwards LER 97-034-01, Condition Prohibited by Ts:Missed EDG Surveillance. Util Commitments to NRC Re Subj LER Encl
ML20216C931
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 04/06/1998
From: Bezilla M
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20216C937 List:
References
LR-N980178, NUDOCS 9804150106
Download: ML20216C931 (2)


LER-2097-034, Forwards LER 97-034-01, Condition Prohibited by Ts:Missed EDG Surveillance. Util Commitments to NRC Re Subj LER Encl
Event date:
Report date:
3542097034R00 - NRC Website

text

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a,.

PSEG Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit APR 0 61998 LR-N980178 U. S. Nuclear Regulatory Commission Document Control Desk Washington,DC 20555

Dear Sir:

liOPE CREEK GENERATING STATION DOCKET NO. 50-354 UNIT 1 LICENSEE EVENT REPORT 97-034-01 ,

ihis supplement to Licensee Event Report entitled " Condition Prohibited by Technical j Specifications: Missed Emergency Diesel Generator Surveillance" is being submitted pursuant to the requirements of 10CFR50.73(a)(2)(i)(B).

Sincerely, - l

- i fl '/

Mark Bezilla General Manager -

Ilope Creek Operations CEM C (

Distribution LER File f )ph 2

C 9804150106 900405 PDR ADOCK 05000354 l S PDR-

. The pMerisillyotir hands.

n e a ntv m

l j Document Control Desk l ' LR-N980178 Attachment A j The following items represent the commitments that the Public Service Electric and Gas Company is making to the Nuclear Regulatory Commission relative to LER 354/97-034-01:

l 1. By August 15,1998, procedure changes will be made to ensure that online - .

l maintenance and surveillances are properly considered during outage planning. I

2. We have evaluated the PM deferral process and will implement appropriate ,

enhancements by June 1,1998.

J i 3. A multi-discipline root cause team has been tasked with conducting an aggregate review of recent missed Technical Specification surveillances. The corrective I

' actions identified during this root cause investigation will be tracked in i accordance with our Corrective Action Program.

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