ML031220044
ML031220044 | |
Person / Time | |
---|---|
Site: | Hatch |
Issue date: | 05/01/2003 |
From: | Brian Bonser NRC/RGN-III/DRP/RPB2 |
To: | Sumner H Southern Nuclear Operating Co |
References | |
IR-03-002 | |
Download: ML031220044 (24) | |
See also: IR 05000321/2003002
Text
May 1, 2003
Mr. H.L. Sumner, Jr.
Vice President - Hatch Plant
Southern Nuclear Operating Company, Inc.
P. O. Box 1295
Birmingham, AL 35201-1295
SUBJECT: EDWIN I. HATCH NUCLEAR POWER PLANT - NRC INTEGRATED
INSPECTION REPORT 50-321/03-02 AND 50-366/03-02
Dear Mr. Sumner:
On April 5, 2003, the US Nuclear Regulatory Commission (NRC) completed an inspection at
your Hatch Units 1 and 2. The enclosed integrated inspection report documents the inspection
findings which were discussed on April 15, 2003 with Mr. Dennis Madison and other members
of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel. Based on the results of this inspection, no findings of significance were identified.
In accordance with 10 CFR 2.790 of the NRCs Rules of Practice, a copy of this letter and its
enclosure will be available in the NRC Public Document Room or from the Publicly Available
Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible
from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic
Reading Room).
Sincerely,
/RA/
Brian R. Bonser, Chief
Reactor Projects Branch 2
Division of Reactor Projects
Docket Nos.: 50-321, 50-366
Enclosure: Inspection Report 50-321, 366/03-02
w/Attachment: Supplemental Information
cc w/encl: (See page 2)
SNC 2
cc w/encl:
M. J. Ajluni, Licensing
Services Manager, B-031
Southern Nuclear Operating
Company, Inc.
Electronic Mail Distribution
D. E. Grissette
General Manager, Farley Plant
Southern Nuclear Operating
Company, Inc.
Electronic Mail Distribution
J. D. Woodard
Executive Vice President
Southern Nuclear Operating
Company, Inc.
Electronic Mail Distribution
State Health Officer
Alabama Department of Public Health
RSA Tower - Administration
Suite 1552
P. O. Box 303017
Montgomery, AL 36130-3017
M. Stanford Blanton
Balch and Bingham Law Firm
P. O. Box 306
1710 Sixth Avenue North
Birmingham, AL 35201
William D. Oldfield
Quality Assurance Supervisor
Southern Nuclear Operating Company
Electronic Mail Distribution
Distribution w/encl: (See page 3)
SNC 3
Distribution w/encl:
F. Rinaldi, NRR
C. Evans (Part 72 Only)
L. Slack, RII EICS
RIDSNRRDIPMLIPB
PUBLIC
OFFICE DRP/RII DRP/RII DRP/RII DRS/RII DRS/RII DRS/RII DRS/RII
SIGNATURE cr ng via e-mail wb via e-mail sr et via e-mail ab (for) jk
NAME CRapp:vyg NGarrett WBearden SRose ETesta DForbes JKreh
DATE 5/1/2003 5/1/2003 5/1/2003 5/1/2003 5/1/2003 5/1/2003 5/1/2003
E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO
PUBLIC DOCUMENT YES NO
OFFICIAL RECORD COPY DOCUMENT NAME: C:\ORPCheckout\FileNET\ML031220044.wpd
U. S. NUCLEAR REGULATORY COMMISSION
REGION II
Docket Nos: 50-321, 50-366
Report No: 50-321/03-02 and 50-366/03-02
Licensee: Southern Nuclear Operating Company, Inc. (SNC)
Facility: Hatch Nuclear Plant, Units 1 and 2
Location: P.O. Box 2010
Baxley, Georgia 31515
Dates: January 5, 2003 - April 5, 2003
Inspectors: N. Garrett, (Acting) Senior Resident Inspector (SRI)
C. Rapp, Senior Project Engineer
W. Bearden, SRI, Browns Ferry Unit 1 (Section 1R08)
S. Rose, Operations Engineer (Section 1R11)
E. Testa, Senior Health Physics Inspector
(Sections 2OS1, 2OS2, and 2PS2)
D. Forbes, Health Physics Inspector
(Sections 2OS1, 2OS2, and 2PS2)
J. Kreh, Health Physics Inspector (Sections
2OS1, 2OS2, 2PS2)
R. Moore, Senior Reactor Inspector (Section 4OA5.2)
Approved By: Brian R. Bonser, Chief
Reactor Projects Branch 2
Division of Reactor Projects
Enclosure
SUMMARY OF FINDINGS
IR 05000321/2003-002, 05000366/2003-002; Southern Nuclear Operating Company, Inc.;
1/05/2003 - 4/05/2003; Edwin I. Hatch Nuclear Plant, Units 1 & 2, routine integrated report.
The report covers a three month period of inspection by resident inspectors and a senior project
engineer, and announced inspections by a regional in-service inspection (ISI) inspector,
regional health physics inspectors, a regional operations engineer, and a regional senior reactor
inspector. No findings of significance were identified. The NRCs program for overseeing the
safe operation of commercial nuclear power reactors is described at its Reactor Oversight
Process website at http://www.nrc.gov/reactors/operating/oversight/index.html.
A. Inspector Identified and Self-Revealing Findings
None
B. Licensee Identified Violations
None
Report Details
Summary of Plant Status
Unit 1 operated at or near 100 percent rated thermal power (RTP) during this inspection period.
Unit 2 operated at or near 100 percent RTP until March 1 when the unit was shut down for a
refueling outage. The unit was restarted on March 28 and reached 100 percent RTP on April
3. The unit operated at or near 100 percent RTP for the remainder of the inspection period.
1. REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
1R04 Equipment Alignment
a. Inspection Scope
The inspectors performed partial walkdowns of the following three systems to verify the
availability of redundant or diverse systems, and components and to verify that
defense-in-depth was maintained during periods when safety equipment was
inoperable. The inspectors compared system configuration to the associated licencee
procedures, system and component checklists, and system P&IDs to verify systems
and components were properly aligned. Additionally, the inspectors reviewed selected
Condition Reports (CRs) to verify that equipment alignment issues were being identified
and adequately resolved. Documents reviewed are listed in the Attachment.
- 2A Core Spray (CS) and 2A, 2B, 2C, and 2D Residual Heat Removal (RHR) Systems
- 1A, 2A, and 2B Standby Gas Treatment System
- 1B and 2A Emergency Diesel Generator (EDG)
b. Findings
No findings of significance were identified.
1R05 Fire Protection
a. Inspection Scope
The inspectors toured the following six risk significant areas, identified in the licensees
Independent Plant Evaluation for External Events, to assess the material condition of
the fire protection and detection equipment and to verify fire protection equipment was
not obstructed. The inspectors reviewed licensee procedure 40AC-ENG-008-OS, Fire
Protection Program, and conducted area walkdowns to assess the licensee's control of
transient combustibles. The inspectors also reviewed the Site Fire Hazards Analysis
and applicable Pre-fire Plan drawings to verify that the necessary fire fighting
equipment, such as fire extinguishers, hose stations, ladders, and communications
equipment, was in place. Documents reviewed are listed in the Attachment.
- Intake Structure Unit 1 & 2 Fire Area 0501
2
- Diesel Generator Building Fire Areas, 2A EDG, Switchgear 2E, and Hall, Fire Areas
2401, 2402, 2403, 2404, 0401
- Unit 2 158' Reactor Building, Fire Areas 2203K, 2205I, 2205H, 2205N, 2210, 2211
- Unit 2 185' and 203' Reactor Building, Fire Areas 2203I, 2205Q, 2205R, 2205S,
2205T, 2205U, 2205Y, 2205Z
- Diesel Generator Building Fire Areas 1A EDG room, Switchgear rooms 2G and 1E.
Fire Areas 1411, 1412, and 2409
- Unit 1 & 2 Cable Spread Room, Fire Area 0024A
b. Findings
No findings of significance were identified.
1R07 Heat Sink Performance
a. Inspection Scope
The inspectors observed the licensees inspection activities for the 2C EDG jacket
coolant, oil cooler, and air coolant heat exchangers. The inspectors observed licensee
inspection activities to verify licencee implementation of licensee procedures 52PM-R43-
001-0, Diesel, Alternator, and Accessories Inspection and 42IT-TET-012-2S, Plant
Service Water (PSW) and RHR Service Water Piping Inspection Procedure.
b. Findings
No findings of significance were identified.
1R08 Inservice Inspection (ISI)
a. Inspection Scope
The inspectors observed in-process ISI work activities on Unit 2 and reviewed selected
ISI records. The observations and records were compared to the Technical
Specifications (TS) and the applicable Code (ASME Boiler and Pressure Vessel Code,
Sections V and XI, 1989 Edition), to verify compliance. The inspectors reviewed non-
destructive examination (NDE) reports for the following completed liquid penetrant (PT),
visual (VT1), and ultrasonic testing (UT) examinations:
- S03H2U001, RPV head to vessel stud ligaments 21 to 40
- S03H2U002, RPV head to vessel studs 21 to 40
- S03H2U004, Main Steam piping weld, 2B21-1MS-24A-18
- S03H2U008, Main Steam piping weld, 2B21-1MS-24B-10
- S03H2V008, RPV Head Vent N6A Nozzle inner radius
- S03H2V009, RPV Head Vent N6B Nozzle inner radius
- S03H2V010, RPV Head Vent N7 Nozzle inner radius
- S03H2P001, Main Steam piping weld, 2B21-1MS-24B-10
Ongoing dry powder Magnetic Particle (MT) examinations of the 24 inch ASME Class 1
Main Steam piping welds 2B21-1MS-24-18 and 2B21-1MS-24A-20 along with the PT
3
examination of the 28 inch ASME Class 1 Recirculation Pump Suction piping weld 2B31-
1RCM-28AS-9 were observed.
The inspectors also reviewed video recordings of various completed augmented
inspections included in the licensees Vessel Internals Program (VIP). This included
remote visual inspection of welds on 1P7 weld 10 and 4P5 weld 37 on CS Sparger
downcomer piping; 1P1 weld 2, 1P2 weld 3, 1P3 weld 4, 1P3 weld 17, and 2P1 weld 31
on T-Box junctions on the on the CS sparger piping; and steam dryer lifting eye and
lifting rod.
Qualification and certification records for examiners, equipment and consumables, and
NDE procedures for the above ISI examination activities were reviewed. Three licensee
audits associated with ISI activities and the VIP program were reviewed. Additionally,
two CR associated with ISI activities which had been documented in the licensees
corrective action program were reviewed. Documents reviewed are listed in the
Attachment.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification
a. Inspection Scope
Resident Observation: The inspectors observed the performance of simulator scenario
LT-SG-50431, Loss of Off-Site Power. The inspectors reviewed licensee procedures
10AC-MGR-019-0S, Procedure Use and Adherence, and DI-OPS-59-0896N, Operations
Management Expectations, to verify formality of communication, procedure usage,
alarm response, control board manipulations, group dynamics, and supervisory
oversight. The inspectors also reviewed licensee procedure 73-EP-EIP-001-0,
Emergency Classification and Initial Actions, to verify that the event action level was
correctly identified and reported. The inspectors attended the post exercise critique of
operator performance to assess if the licensee identified issues were comparable to
issues identified by the inspectors.
Annual Operating Test Results: The inspectors reviewed the overall pass/fail results of
the individual Job Performance Measure operating tests, and the simulator operating
tests (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee during
calender year 2002. These results were compared to the thresholds established in
Manual Chapter 609 Appendix I, Operator Requalification Human Performance
Significance Determination Process.
b. Findings
No findings of significance were identified.
4
1R12 Maintenance Rule Implementation
a. Inspection Scope
The inspectors conducted a detailed review of the following two systems. The
inspectors performed a system walkdown and interviewed the system engineer to
determine the existing system configuration and deficiencies. The inspectors reviewed
the system health reports, maintenance work orders (MWO), CRs, and system
modifications to assess overall system condition and maintenance related issues.
Additionally, the inspectors reviewed the licensees MR reports and scoping documents
to determine that the systems were properly scoped, in the proper maintenance rule
category, and appropriate actions were being taken on the system. Documents
reviewed are listed in the Attachment.
- Unit 1 Reactor Core Isolation Cooling (RCIC) System
- Unit 2 Off-Gas System
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Evaluation
a. Inspection Scope
The inspectors reviewed the five licensee Plan of the Day (POD) documents listed
below and the daily risk management evaluation to verify that risk assessments were
performed prior to components being removed from service. In addition, when
emergent work was identified, the inspectors held discussions with licensee personnel
and walked down plant systems to verify that actions were taken to minimize the
probability of an initiating event and to maintain the functional capability of mitigating
systems. Documents reviewed are listed in the Attachment.
- POD for Week of 1/25 - 31
- POD for Week of 2/1-7
- POD for Week 2/15 - 21
- POD for Week 2/22-28
b. Findings
No findings of significance were identified.
5
1R14 Personnel Performance During Non-Routine Plant Evolutions
a. Inspection Scope
For the two events described below, the inspectors observed control room operator
actions, reviewed operator logs, and reviewed plant procedures to verify that operator
actions were taken in accordance with plant procedures.
- On January 24, 2003, the Emergency Notification Network and Emergency Notification
System phones systems were disabled when a Bell South fiber cable was severed
between the plant and Baxley, Georgia. The inspectors observed the Main Control
Room (MCR) response to the loss of communication and subsequent event
notification to the NRC.
- On March 25, 2003, a radiological event was declared when a hot spot was formed in
the Spent Fuel Pool Cooling system piping on the 185 foot level of the reactor
building. The inspectors observed the MCR response to the event to assess the
licensees implementation of 73EP-RAD-001-0, Radiological Event, 34AB-D11-001-2,
Radiological Release Control, and 34AB-T22-003-0, Secondary Containment Control.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
a. Inspection Scope
The inspectors reviewed the following five operability evaluations to assess the technical
adequacy of the evaluation and verify if continued operability was justified. The
evaluations were compared to the requirements identified in TS and the UFSAR as
required to ensure that operability was adequately assessed and the system or
component remained available to perform its intended function. In addition, the
inspectors assessed the adequacy and implementation of compensatory measures
resulting from the evaluation. The inspectors verified that the operabiity determinations
were performed in accordance with licensee procedure 00AC-REG-006-0, Operability
Determinations.
- LR-REG-001-0203, Unit 2 Diesel Generator 2A, PSW valve 2P41-F339A not fully
closing
- LR-REG-001-0103, Unit 2 Scram Discharge Volume Inboard Vent and Drain Valves
2C11-F011, 2C11-F010A, and 2C11-F010B
- LR-REG-011-0203, Missed ASME Code Section XI Inspection following replacement
of valve 1G11-F020
- CR 2003002130, 11 Tubes Plugged on Control Room Chiller - 1Z41-B008A
- LR-REG-004-0103, Unit 2 RHR & CS Pump Room Cooler - 2T41-B002B
6
b. Findings
No findings of significance were identified.
1R19 Post Maintenance Testing
a. Inspection Scope
The inspectors either observed personnel performance or reviewed the test results for
the following five maintenance testing activities to verify the scope of testing
demonstrated that the work performed was correctly completed and the affected
equipment was functional and operable. The inspectors reviewed the maintenance
package to verify procedural requirements were met. The inspectors reviewed
equipment status and alignment to verify the system or component was available to
perform the required safety function. Documents reviewed are listed in the Attachment.
- MWO 10300065, Replace Unit 1 RCIC EGR
- MWO 20203138, 20203139, and 20204149, Rebuild and troubleshooting of
2C11F010B and 2C11F011
Generator
- MWO 20300072 Clean/Repair/Replace 2P41-F036B
- MWO 20300821 Replacement of 2P41-F339B Flange
b. Findings
No findings of significance were identified.
1R20 Refueling and Outage Activities
a. Inspection Scope
The inspectors reviewed the overall outage safety assessment for the refueling outage
and the outage schedule to verify the licensees use of risk management, operating
experience and past lessons learned for the Unit 2 refueling outage conducted from
March 1 - 30, 2003. The inspectors reviewed the outage safety assessment procedure
to verify the licensee was correctly maintaining required equipment in service in
accordance with the overall outage safety assessment. In addition, the inspectors
reviewed the outage safety assessment to verify the licensee had contingency plans and
equipment to maintain defense in depth. During the refueling outage the inspectors
monitored licensee control over outage activities listed below. Documents reviewed are
listed in the Attachment.
- Plant shutdown including insertion of manual scram and the following reactor coolant
system cooldown to verify the cooldown rate did not exceed TS limits.
- Various clearances to verify implementation of the clearance process and the
associated equipment was properly configured to support the function of the
clearance.
7
- Calibration of reactor instrumentation used to monitor reactor water within surveillance
requirements.
- Monitoring of decay heat removal by the decay heat removal and fuel pool cooling
systems.
- Reactor water inventory sources controlled in accordance with the outage risk
assessment.
- Refueling activities, including portions of core offload, fuel shuffles, and core reload to
verify these activities were performed in accordance with TS and plant procedures and
verify fuel movements were tracked.
- TS and licencee procedures to verify mode change requirements were met.
- Walkdown of the drywell to verify material conditions supported plant operations.
- Plant startup, heatup, and power ascension
- Licensee determination of the shutdown margin determination to verify adequate
shutdown margin in the core configuration.
- Licensee identification and resolution of problems related to refueling outage activities.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors reviewed the following six surveillance test procedures and either
observed personnel performance or reviewed test results to verify the scope of the test
adequately demonstrated that the affected equipment was operable. The inspectors
reviewed the activities to assess for preconditioning of equipment, procedure
adherence, and valve alignment following completion of the surveillance. The
inspectors reviewed licensee procedure AG-MGR-21-0386N, Evolution and Pre-and
Post-Job Brief Guidance, and attended selected briefings to determine if procedure
requirements were met.
- 34SV-E11-004-1, RHR Service Water Pump Operability (IST)
- 34SV-R43-006-1S, Diesel Generator 1C Semi-Annual Test
- 34SV-E11-001-2, Residual Heat Removal Pump Operability
- 42SV-TET-001-2, Primary Containment Periodic Type B and Type C Leakage Tests,
2E41-F102/F103/F104 (CI valves)
- 42SV-TET-001-2, Primary Containment Periodic Type B and Type C Leakage Tests,
2P33-F224 and 2T33-X11 (CI valves)
b. Findings
No findings of significance were identified.
8
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
a. Inspection Scope
The inspectors witnessed an emergency drill conducted on January 29. The inspectors
observed licensee activities in the simulator and Technical Support Center to verify
implementation of 10AC-MGR-006-0S, Hatch Emergency Plan. The inspectors
reviewed 73EP-EIP-001-0, Emergency Classification and Initial Actions, to verify the
licensee properly classify the simulated event and developed the proper protective
action recommendations. The inspectors also reviewed 73EP-EIP-073-0, Offsite
Emergency Notification, to verify the licensee made proper offsite notifications. The
inspectors attended the post-drill exercise critique to assess the licensees effectiveness
in identifying areas of improvement.
b. Findings
No findings of significance were identified.
2. RADIATION SAFETY
Cornerstone: Occupational Radiation Safety
2OS1 Access Control To Radiologically Significant Areas
a. Inspection Scope
Access Controls: The licensees procedures for controlling access to airborne
radioactivity areas, radiation areas, high radiation areas, and very high radiation areas
were evaluated. The licensees activities and guidance for posting, surveying, and
access controls to radiologically significant areas listed in the report Attachment were
evaluated against applicable 10 CFR Part 20 and TS requirements. During tours
conducted March 3-7, 2003, and March 17-21, 2003, the inspectors evaluated
radiological postings, barricades, and surveys associated with the Unit 1 and Unit 2
reactor, turbine, plant stack building areas, and the Independent Spent Fuel Storage
Installation (ISFSI). Dose rates at various locations in the Unit 1 and Unit 2 buildings
and around the spent fuel pool area were independently surveyed by the inspectors and
compared to current licensee survey map data.
The inspectors evaluated eight Radiation Work Permits (RWPs) used for work in
radiologically significant areas associated with the 2003 Unit 2 refueling outage and one
associated for non-outage work. The selected RWPs were evaluated for incorporation
of access controls, and specified electronic dosimeter (ED) set point alarms were
evaluated against RWP criteria for appropriateness with regard to the expected work
area dose rates.
The inspectors conducted interviews concerning RWP requirements and ED set points
with radiation workers. Radiological worker and radiation protection technician
9
training/skill level, adherence to access control procedures and RWP specified access
controls were observed and evaluated by the inspectors during selected job site reviews
and tours throughout the radiological control area (RCA). The inspectors attended the
RWP 03-2209 briefing for work activities associated with a diver entering the reactor
vessel to remove a potential loose part from the steam dryer support seat. In addition,
the inspectors interviewed management personnel associated with the Unit 2 vessel
diving operation, observed the dive mock-up facility and diving operation to assess the
radiological controls implemented, and attended the pre-job brief and diver debrief
conducted by the licensee to review lessons learned from the evolution. The inspectors
also evaluated the radiological controls and surveys for the expected airborne work
areas established for the Unit 2 replacement of control rod drive mechanisms.
Access control procedures for locked high radiation areas (LHRAs) were reviewed and
discussed with radiation protection management and supervision. The inspectors
reviewed documentation of the licensees weekly inspections which verified the status of
the locked doors and independently assessed LHRA doors status during plant tours.
Implementation of key controls for Very High Radiation Areas (VHRAs) and LHRAs and
controls for accessing posted VHRAs also was assessed.
The inspectors verified the postings located on the fence of the ISFSI and independently
surveyed and verified the dose rates on the storage spent fuel casks located on the
storage pads. The environmental thermoluminescent dosimeters (TLD) fence line
doses at the ISFSI were evaluated for compliance with 10 CFR 20, Subpart D. The
inspectors evaluated the Edwin Hatch Nuclear Plant ISFSI Annual Radioactive Effluent
Release Report, dated February 11, 2003, and the ISFSI Occupancy Factor White
Paper dated November 21, 2002.
Problem Identification and Resolution: Licensee CRs associated with access controls to
radiologically significant areas were reviewed. Six CRs listed in the Attachment were
reviewed and evaluated in detail for issues identified.
b. Findings
No findings of significance were identified.
2OS2 As Low As Reasonably Achievable (ALARA) Planning and Controls
a. Inspection Scope
ALARA: Implementation of the licensees ALARA program during the Unit 2 refueling
outage was observed and evaluated by the inspectors during the periods March 3-7 and
March 17-21, 2003. The inspectors reviewed, and discussed with licensee staff, ALARA
planning, dose estimates, and prescribed ALARA controls for selected outage work
activities expected to or had the potential to incur significant collective doses. Those
activities included replacement and transfer of control-rod drives, drywell in-service
inspections, drywell valve work, diving activities, and drywell local leak-rate tests.
Incorporation of the planning, work controls, and expected dose and dose rates into the
most current RWPs and ALARA pre-job briefings for those activities also was reviewed.
A proposed increase in the overall projected outage exposure (from 124 to 136 person-
10
rem) was reviewed and discussed with licensee staff prior to being considered by the
Plant ALARA Review Committee (PARC). The inspectors also reviewed the minutes of
the 2002 PARC meetings and the lessons learned from the 2002 Unit 1 outage. These
elements of the ALARA program were evaluated for consistency with the methods and
practices delineated in applicable licensee procedures.
The inspectors observed a pre-job ALARA briefing associated with control-rod-drive
(CRD) replacement, and made observations of limited under-vessel activity (preparatory
to the CRD work) via a closed-circuit video monitoring system.
The plant collective exposure history for the years 1999 through 2001, based on the
data reported pursuant to 10 CFR 20.2206 (c), was reviewed and discussed with
licensee staff, as were established goals for reducing collective exposure. The
inspectors also reviewed the licensees program for declared pregnant workers,
although at the time of the inspection there were no declarations.
Through the above reviews and observations, the licensees ALARA program
implementation and practices were evaluated by the inspectors for consistency with TS Section 5.4.1, Procedures, and Section 5.7, High Radiation Area Controls;
10 CFR Part 20 requirements; and procedural guidance documented in the Attachment.
Problem Identification and Resolution: Licensee CRs and PARC ALARA activities were
reviewed and assessed. The inspectors evaluated the licensees ability to identify,
characterize, prioritize, and resolve the identified issues. Documents reviewed and
evaluated in detail for the identified issues are listed in the Attachment.
b. Findings
No findings of significance were identified.
Cornerstone: Public Radiation Safety
2PS2 Radioactive Material Processing and Transportation
a. Inspection Scope
Waste Processing and Characterization: During the weeks of March 3-7, 2003 and
March 17-21, 2003, the configuration status and operability of selected radioactive
waste (radwaste) processing systems and equipment were evaluated. Inspection
activities included document review, direct inspection of processing equipment, and
interviews with plant personnel.
The document review of radwaste systems included evaluation of program guidance for
waste classification and procedures for processing spent resin. The inspectors
reviewed the licensees 10 CFR Part 61 contract laboratory sample gamma analysis
results for the waste streams. The 2003 data were evaluated for consistency with the
most current 10 CFR Part 61 sample data collected in 2002. The licensees use of
scaling factors for hard-to-detect nuclides was assessed for the primary resin waste
stream. The inspectors reviewed the licensees procedure for clearing clean trash from
11
the RCA. The inspectors reviewed procedures for transferring and de-watering spent
resin to ensure compliance with the process descriptions in the Process Control
Program (PCP) and the system diagrams in the Updated Final Safety Analysis Report
(UFSAR), Section 11. Documents reviewed are listed in the Attachment.
The direct inspection of radwaste equipment included walk-downs of resin lines and
observation of abandoned radwaste equipment. Observations were conducted of clean
trash monitoring, Low Level Waste Storage Building activities and inspection of the
solidification dewatering operation.
Licensee personnel were interviewed regarding waste classification analyses and
radwaste processing equipment. The inspectors assessed the individuals knowledge of
regulations, understanding of licensee procedures, and familiarity with radwaste
systems. The inspectors reviewed and evaluated the Licensing Action Report (LAR) 91-
006, Safety Evaluation for Authors Document Incorporation Form (ADIF) 12A-001 dated
July 13, 1993. The inspectors reviewed the revised drawing and observed the current
operational and configuration status of the radwaste processing equipment during
system walk-downs. Waste stream sampling frequency, response to changing plant
conditions, and laboratory counting techniques were also discussed and assessed.
The licensees program for classifying and processing solid radwaste was evaluated
against 10 CFR Part 61, the Branch Technical Position on Waste Classification and
Waste Form, the Process Control Program, the UFSAR, Section 11, Radioactive Waste
Management, and licensee procedures.
Transportation: The inspectors evaluated the licensees activities related to
transportation of radioactive material. The evaluation included document review and
direct observation of shipping activities.
The document review consisted of evaluation of licensee procedures, review of shipping
records, and assessment of worker training. Records for five shipments, listed in the
Attachment, were reviewed for compliance with regulations and consistency with
licensee procedures. Training records for two technicians qualified to ship radioactive
material were evaluated for completeness. In addition, training curricula provided to
these workers were assessed. The inspectors discussed Department of Transportation
(DOT) training and shipping paper requirements with the Radioactive Material Control
supervisor.
On March 4, 2003, the inspectors directly observed the preparation of resin for shipment
to a vendor for volume reduction. The inspectors assessed the technicians
performance in completing the required documentation and characterization using the
RADMAN computer code and in conducting appropriate surveys of the loaded package.
Transportation program guidance and implementation were reviewed against
regulations detailed in 10 CFR Part 71, 49 CFR Parts 170-189, and licensee
procedures. In addition, training activities were assessed against Subpart H of 49 CFR
Part 172 and the guidance documented in NRC Bulletin 79-19.
12
Problem Identification and Resolution: Licensee CRs associated with radwaste
processing and transportation were reviewed. CR 2002011605, Two Sea Land
Radwaste Storage Containers Had Unexpected Corrosion, was reviewed and evaluated
in detail.
b. Findings
No findings of significance were identified.
4. OTHER ACTIVITIES
4OA1 Performance Indicator (PI) Verification
a. Inspection Scope
The inspectors reviewed the licensees Unit 1 and Unit 2 submittals for the PIs listed
below. To verify the accuracy of the PI data reported during the period, PI definitions
and guidance contained in licensee procedure 00AC-REG-005-0, Preparation and
Reporting of NRC PI Data, and NEI 99-02, Regulatory Assessment Indicator Guideline,
Revision 2, were used to verify the basis in reporting for each data element.
Occupational Radiation Safety Cornerstone
- Occupational Exposure Control Effectiveness PI
The inspectors reviewed the PI results for the period January 1, 2002, through March 5,
2002. Selected CRs issued during the review period were reviewed and assessed for
potential PI occurrences.
Public Radiation Safety Cornerstone
- Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent PI
The inspectors reviewed and discussed the PI results for the period May 1, 2002,
through March 15, 2002. For the review period, the inspectors reviewed data reported
to the NRC and evaluated selected radiological liquid and gaseous liquid and gaseous
effluent release data, out-of-service process radiation monitor and compensatory
sampling data, abnormal release results, and CRs documented in the Attachment.
b. Findings
No findings of significance were identified.
13
4OA5 Other Activities
.1 Review of Institute of Nuclear Power Operations (INPO) Evaluation Report
On February 5, the inspectors reviewed the results of an INPO evaluation of licensee
performance conducted during October/November 2002. The report was dated January
7, 2003. The report did not identify any significant licensee performance issues that had
not been previously addressed and/or reviewed by the NRC.
.2 (Closed) URI 50-366/02-06-03: Design Control of High Pressure Coolant Injection
(HPCI) System Steam Line Drain Pot
During the Safety System Design and Capability Inspection (NRC Report No.
50-321,366/02-06), the inspectors identified that, under some conditions, the HPCI
steam trap could be isolated with the potential for condensate backup into the turbine
steam supply line. It could not be determined during the inspection whether the possible
water slug inflow to the HPCI turbine would impact the operability of the HPCI pump.
Following the inspection, the licensee provided vendor test documentation which
enveloped the conditions expected by the steam trap isolation and demonstrated that
the pump would meet its safety function. The inspectors reviewed the test
documentation and concluded there is no actual safety consequence.
4OA6 Meetings, Including Exit
.1 Exit Meeting Summary
On April 15, 2003, The inspectors presented the inspection results to D. Madison and
the other members of his staff. The inspectors confirmed that proprietary information
was not provided or reviewed during the inspections.
.2 Annual Assessment Meeting Summary
On April 9, 2003, the NRCs Chief of Reactor Projects Branch 2 and the Senior Resident
Inspector assigned to the Hatch Nuclear Plant (HNP) met with Southern Nuclear
Operating Company to discuss the NRCs Reactor Oversight Process (ROP) and the
HNP annual assessment of safety performance for the period of January 1, 2002 -
December 31, 2002. The major topics addressed were: the NRCs assessment
program, the results of the HNP assessment, and NRC security activities. Attendees
included HNP site management, corporate management, and plant co-owners.
This meeting was open to the public. The presentation material used for the discussion
is available from the NRC s document system (ADAMS) as accession number
ML030990064. ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
Betsill, J., Assistant General Manager - Plant Support
Davis, D., Plant Administration Manager
Dedrickson, R., Engineering Support Manager
Googe, M., Performance Team Manager
Hammonds, J., Operations Manager
Coleman, V., Safety Audit and Engineering Review Supervisor
Kirkley, W., Health Physics and Chemistry Manager
Lewis, J., Training and Emergency Preparedness Manager
Madison, D., Assistant General Manager - Plant Operations
Reddick, R., Site Emergency Preparedness Coordinator
Roberts, P., Outage and Planning Manager
Thompson, J., Nuclear Security Manager
Tipps, S., Nuclear Safety and Compliance Manager
Wells, P., General Manager - Nuclear Unit Superintendent
NRC Personnel
Brian R. Bonser, Chief, Divisions of Reactor Projects, Branch 2
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Closed
50-366/02-06-03 URI Design Control of High Pressure Coolant Injection System
Steam Line Drain Pot
LIST OF DOCUMENTS REVIEWED
Section 1R04: Equipment Alignment
34SO-E11-010-2, Residual Heat Removal System
34SO-E21-001-2S, Core Spray System
34SO-T46-001-1S, Standby Gas Treatment System
34SO-T46-001-2S, Standby Gas Treatment System
34SO-R43-001-1, Diesel Generator Standby AC System
34SO-R43-001-2, Diesel Generator Standby AC System
Section 1R05: Fire Protection
Plant Drawing A-43965, Sheet 109B, 115B, 120B
Plant Drawing A-43966, Sheet 5B, 27B
Drawing A-43966, Sheets 16B, 17B and 26B.
Drawing A-43965, Sheet 44B.
Attachment
2
Section 1R08: Inservice Inspection
Procedures:
Inspection and Testing Services (ITS) Procedure, VT-H-750, Visual Examination of Reactor
Pressure Vessel Internals Rev. 12
ITS Procedure, UT-H-401, Manual Ultrasonic Examination of Full Penetration Ferritic Welds
(Appendix VIII), Rev. 3
ITS Procedure, UT-H-402, Manual Ultrasonic Examination of Full Penetration Austenitic Welds
(Appendix VIII), Rev. 2
ITS Procedure, VT-H-701, Visual Examination (VT-1), Rev. 5
ITS Procedure, MT-H-500, Magnetic Particle Examination, Rev.10
ITS Procedure, PT-H-600, Solvent Removable, Color Contrast or Fluorescent Liquid Penetrant
Examination, Rev. 8
Condition Reports (CRs):
CR 2001008653, Unit 2 Condensate piping elbow below thickness values (Flow Accelerated
Corrosion action level)
CR 2003002491, Documentation of pipe elbow wall thickness reinspections as result of
engineering evaluations required by CR 2001008653
Other Documents:
SNC Audit, ENG 2001-11, Inspection and Testing Services
SNC Audit, OL-OUTAGE-1, Outage ISI Activities
SNC Special Audit, HSAER-1108, Hatch BWR Vessel Internals Program
Section 1R12: Maintenance Rule Implementation
MWO 10200032, 10300065
CR 2003000356, 2001011090
Plant Drawing H16334 and H16335
52PM-E51-004-0, RCIC System Maintenance
DCR 02-025, Off-Gas Drain Modification
Plant Drawing H-26045
Section 1R14: Personnel Performance During Non-routine Plant Evolutions
73EP-EIP-001-0, Emergency Classification and Initial Actions
31GO-OPS-013-0S, Notifications and Reports
00AC-REG-001-0S, Federal and State Reporting and Federal Document Posting Requirements
Section 1R19: Post Maintenance Testing
95IT-OTM-001-0S, Maintenance Work Order Functional Test Guideline
34SV-E51-002-1, RCIC Pump Operability
34IT-E51-003-1, RCIC Turbine Speed Control Test
S27499 - Instruction Manual for 2 inch 600# Unbalanced Cage Trim Control Valve GE-VAF-
3234-149
34SV-R43-006-2S, Diesel Generator 2C Semi-Annual Test
41IT-TET-004-0S, Operating Pressure Testing of Piping and Components
3
Section 1R20: Refueling and Outage Activities
LR-REG-14-0203, Outage Safety Assessment for the Plant Hatch Unit 2 Spring Refueling
Outage
DI-OPS-57-0393N, Outage Safety Assessment
34GO-OPS- 013-2S, Normal Plant Shutdown
Clearance 20320415, Trip test of 2R22-S005 Frame 2 and 11 breakers
Clearance 20320125, HPCI System - 2E41
Clearance 20320115, RHRSW A & B Loops for Outage Repairs and Eddy Current Tests
Clearance 20320126, RCIC System - 2E51
Clearance 20320602, Drywell and Torus 18" Vent Lines
Clearance 20320072, PSW Pump Minimum Flow
34GO-OPS-001-2, Plant Startup
42CC-ERP-010-0S, Shutdown Margin Demonstration
Section 2OS1: Access Controls to Radiologically Significant Areas
Reports, Procedures, Instructions, Radiation Work Permits, Lesson Plans and Manuals
60AC-HPX-002-0S, Personnel Dosimetry Program, Revision (Rev.)/Version 12.0,
60AC-HPX-004-0S, Radiation & Contamination Control, Rev./Version 16.8,
60AC-HPX-007-0S, Control of Radioactive Materials, Rev./Version 6.1 Dated,10-26-01
62RP-RAD-001-0S, Dosimetry Issuance & Tracking, Rev./Version 12.1, Dated 3-20-02
62RP-RAD-006-0S, RWP Processing, Rev./Version 10.0 Dated 02-11-02
62RP-RAD-008-0S, Radiation & Contamination Surveys, Rev./Version 10 ED1,
62RP-RAD-009-0S, Air Sampling & Concentration Determination, Rev./Version 5.1,
62RP-RAD-016-0S, Very High & High Radiation Area Access Control, Rev./Version 19.0,
62RP-RAD-022-0, Diving Procedure, Rev./Version 8.1, Dated 10-01-02
Edwin I. Hatch Unit 2 Reactor Vessel Dive Plan, Dated March 17, 2003
Radiation Work Permits (RWPs)
RWP 03-2605, Drywell ISI and Support Work
RWP 03-2500, Unit 2 Inspection, Walkdown
RWP 03-2620, Install/Remove Shielding, Tents, and Scaffolds in Drywell
RWP 03-2600, Drywell Mechanical and Electrical and Inspections
RWP 03-2601, Health Physics and Operations Inspections, Surveillance, Sampling and Valve
Lineups
RWP 03-2611, B21-F022A-D and F028A-D Valve Inspection and Repair
RWP 03-2209, Vessel Diving Operations
RWP 03-2615, Control Rod Drive Mechanism Replacement
Corrective Action Report Documents
CR 2002009278, Workers Exceeded Alarm Set Point for Dose Rate
CR 2003000191, Locking Mechanism Problems for RWCU Room
CR 2003000524, Dose Rate Alarm During Radiographing Operation
CR 2003000524, Movement of Radioactive Source Without Hp Escort
CR 2003000727, Exposure Received During Repetitive Repairs
CR 2003000642, Unexpected High Radiation Area Identified on Pump Pedestal in Unit 1
Radwaste Area
Records and Data
4
Health Physics Day/Night Shift Turnover Logs, March 3, 2002, through March 19, 2002
High Radiation Area and Locked High Radiation Area Entries from March 3, 2002, through
March 07, 2002.
Personnel Exposure Investigation Data Sheets documented from January 1, 2003,
through March 15, 2002.
Initial Intake Assessment Data Sheets documented from January 1, 2002, through March 20,
2003
Unit 2 Control Rod Drive Survey Results, Dated 03-09-03
Unit 1 and Unit 2 Reactor Auxiliary Building Survey Results, Dated 03-04-03
Refueling Floor Survey Results, Dated 03-04-03
Unit 2 Pre-Dive Vessel Dive Survey Results, Dated 03-19-03
Unit 2 Turbine Building Survey Results, Dated 03-04-03
2OS2: ALARA Planning and Controls
Procedures
60AC-HPX-004-0, Radiation and Contamination Control, Version 16.8
60AC-HPX-009-0, ALARA Program, Version 16.1
62RP-RAD-006-0, RWP Processing, Version 10.0
62RP-RAD-012-0, Selection and Use of Temporary Shielding, Version 1.2
62RP-RAD-016-0, Very High and High Radiation Area Access Control, Version 19.0
RWP/ALARA Review Packages
001-2602, Drywell Local Leak-rate Tests
001-2605, Drywell In-service Inspections
001-2606, Drywell Valve Work (Misc.)
001-2609, Safety-relief Valves
001-2611, Main-steam Isolation Valves
001-2615, Control-rod-drive Replacement
Miscellaneous Plant Documents
Minutes of Plant ALARA Review Committee (PARC) meetings conducted on March 19,
March 25, June 28, July 11, July 12, September 17, October 14, and December 16, 2002
2002 Exposure/Goals
2002 Daily Radiation Exposure Goals
Unit 2 Year 2003 Outage - Daily Exposure/Goal
Plant Hatch Exposure Reduction Items
Lessons Learned from 2002 Unit 1 Outage
Detail/comparison of work projects and associated doses for Unit 2 refueling outages in 2001
(incurred doses) and 2003 (projected doses)
2PS2: Radioactive Material Processing and Transportation
Procedures, Instructions, Lesson Plans, and Manuals
62RP-RAD-011-OS, Shipment of Radioactive Material, Rev. 11.7
Shipment 03-5005 Resin, Dated 03/04/03
Shipment 02-5010 Resin, Dated 04/04/02
Shipment 02-0520 Resin, Dated 08/08/02
Shipment 02-2057 Scaling Factor, Dated 11/14/02
Shipment 02-2039 Charcoal Sample, Dated 09/05/02
5
System Prints and Drawings
H-27151 Rev. 11 Sheet 54 Hatch Unit 2 Radwaste System Elementary Diagram
H-27146 Rev. 13 Sheet 49 Hatch Unit 2 Radwaste System Elementary Diagram
H-27147 Rev. 8 Sheet 50 Hatch Unit 2 Radwaste System Elementary Diagram
H-27148 Rev. 6 Sheet 51 Hatch Unit 2 Radwaste System Elementary Diagram
H-26031 Rev. 28 Sheet 6 Hatch Unit 2 Radwaste System P&ID
H-26032 Rev. 28 Sheet 7 Hatch Unit 2 Radwaste System P&ID
H-26035 Rev. 18 Hatch Unit 2 Radwaste System P&ID
UFSAR Sections, License Amendments, Safety Evaluation Reports
UFSAR Unit 1 Rev. 19, Chapter 9 Radioactive Waste System
UFSAR Unit 2 Rev. 19, Chapter 11 Radioactive Waste Management
4OA1: Performance Indicator Verification
Edwin I. Hatch Nuclear Plant, Radioactive Effluent Release Report for 2001
Edwin I. Hatch Nuclear Plant, Radiological Environmental Operating Report for 2001
Various records associated with individual RCA exit doses exceeding 100 mrem from 1/1/2002
through 3/5/2003