ML20040E431

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LER 81-031/03L-0:on 811223,during Surveillance Test PT-MI/PC-MI at 100% Power,Value for Q (Upper) on Channel N44 Was Found Incorrect.Caused by Transcription Error.Channel Recalibr & Retested Satisfactorily
ML20040E431
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 01/21/1982
From: Mooney J
CONSOLIDATED EDISON CO. OF NEW YORK, INC.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20040E427 List:
References
LER-81-031-03L, LER-81-31-3L, NUDOCS 8202040321
Download: ML20040E431 (1)


Text

N LICENSEE EVENT REPORT

. CONTROL BLOCK: l 1

1 1 I I  ! Ih 6

(PLEASE PRINT OR TYPE ALL REQUIRED IRFORMATIOM)

[O Til I "I 'llI I P in l 2 I@l o f 01 -10 ILICENSE o l clNuveEl 0 : ni l ni n I@l e l il , ! ,1,1@lb7 G!A f tdl@

14 15 25 26 uCENSE TYPE Jo 7 8 9 LICENSEE CODE CON'T 101 1 ."ZRC; "

I L @l 01510 f 0101 :I 4171@! 63

!!EVMT 21 OATE

'l li -l, @lnl1 I 'l, 74 5 REPCA T O ATE I o!' l@ oJ 7 8 00 $1 COCK ET a.wa ta sd EVENT DESCRIPTION AND PROSA3LE CONSECUENCES h Gile ccnductini nurm ill.,nce test DT "I /N' "I 1qne r n , c- e c - -c.m,

,t

,n,2, g

, ,,, ,the value for n (urner) on Channel " V vas Seura to be i n ~, r r n - l

, , , , , , (TS 2.3.1.D (5)). There ucre no adverse effects since channenin  !

,,,3, ,

U41, I:42 and :143 we're found operatiner correctly, providino adenuate i

,,g,j reactor protection against an excessive flux tilt. (Sinilar evnnen - I

,g,,, ,

A.O. 73-2-10 and RO 76-2-21) . J I

101811 SYSTEM CAUSE CAUSE COMP. VALVE COCE CODE SU8CODP COMPONENT COCE SUSCOCE SUSCOCE 10191 7 8 l I l^ l@ In l@ l l@ l t In I ci- I n_le l@ W@ l 11 @

9 10 11 12 13 18 1s 20 SEbvENTIAL OCCURRENCE REPORT REVISION EVENT YE AR REPORT NO. CCCE TYPE NO.

LER

@ ,ago,/RO g I 8111 1-1 101 3111 L_J ' o l 11 LIJ I-I lol

_ 21 22 23 24 26 27 3 a 30 31 32 SHUTDOWN ATTACHufNT NPRO4 PRIME COMP. COMPONENT ACTION PUTURE EPPECT MANUPACTURER TAKEN ACTION ON PLANT METHOO MOURS SU8MITTED PCRM bu8. SUPPLIER LE_j@l z l@

33 34 Iz l@

3S Izl@

36 l_ 01010 31 01 40 l'il@ lj @ [nj@ l u li l o i nl@

41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h li l o l i Due to a transcrintion error. incn-rn-* " ,1 . , n ,- w,a den, ,- , i a

  • F- _

I

,a*ul g l Channel M44 when it was calibrated the r,revic,u: ,n-+k. " -w

, 2 1 Delta-T' penalty setpoint for Ch 44 to be conservativo snr na- pi"n I

,,i3i l values and non-conservative for r'ositive vaines nf nvial # 1 'iv A i # #--a ~4 g lThe channel was recalibrated and rotestod s$tisfactnn41" 80 l

7 8 9 A 4 POWER OTHER STATUS IS O RY DISCOVERY DESCRIPTION i s lEl@ l11 0]Ol@l MA l W @l46 Tnchnician nbservation I 7 8 9 to 12 13 de 45

  • 83 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY
  • LOCATION OF RELEASE
  • i a l,z j @ l z l@l nA I I nn i 7 8 9 to t1 44 46 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION LLW8 101 Ol 01@l zl@l13 na l 80 7 9 11 12 PERSONNE L (NJURIES NUM8ER DESCRIPTION "A I li t a8 l l 010 h l@l 7 'J 11 !2

$7 LC*S OP 04 %e arm,TO F ACILITV v Q

.u _ m .n .

l8 l '3 ll'$l PUwCIry 8202040321 820122 NRC use cNLY PDR ADOCK 05000247 2 o 'SSUEO@ nDESCRIPTION l :l l S PDR l lIIII!Iff' i ' ! :*

2 8 9 to 63 69 - S Janes " coney (914) 526-5181  ;

NAME OF PREPARER PHONE: -o

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