ML20004E188

From kanterella
Jump to navigation Jump to search
LER 81-012/01T-0:on 810511,3/4-inch Swagelok Union in Remote Reactor Head Vent Line Parted During Test to Assure Operability of Low Power Injection/Rhr Check Valves Prior to Restart.Caused by Improper Installation.Valve Closed
ML20004E188
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 05/22/1981
From:
CONSOLIDATED EDISON CO. OF NEW YORK, INC.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20004E184 List:
References
LER-81-012-01T, LER-81-12-1T, NUDOCS 8106110316
Download: ML20004E188 (2)


Text

l l l l l (PLEAEE PHIMT OR TYPE ALL HiQUI LD ifd ORMATION)

(CONTROL DLOCX:l l t- {

[oh] I xi n i nL2JG!I, 1 nl ll,- la_Loi d a l- I o f23O!Gl L ILLNSE P.UMtik ti du 4LittN'2L lil_iDJiIGI INrE J0 I

' i L A T $8 a

le 7 8 LICENSLL CO )E 14 lb I

CON'T 0 i 0[CE l L hl 01 510 l Ol 0 l 214 17hlOl5l1111811 tA 63 EVENT DATE 74 lh[0 l ;I9 I 'In I 60l ih 7') f4LPOR T DAT E 7 8 60 61 DOCKt T NUYUE R EVENT DESCRIPTION AND PROD ABLE CONSEQUENCES h lo j al l While conducting testing to assure operanility of tne LPT/HIIR I jol3ll Check valves prior to plant restart,a3/4 inch "Swagelok" union in l J o l4 l l the remote reactor head vent line parted. At the tine of this I o 5 'l event, tne reactor coolant system temperature and pressure were l lO l6 l l appro imately .$20 r and 1200 PSIG respectively. l l

0 7 l I

101811 83 CAUSF COMP. VALVE SYSTEM CAUSE CODE CODE SU8 CODE COMPONENT CODE SUSCODE SUSCOCE lO191 8

I c In l@ In 9 to is l@ I c l@ 1911 191 ei x ix l@ U@ LzJ @

12 13 18 19 Ju 7

OCCU R R E NCE REPORT REVISION SEQUENTI AL REPGnT NO. CODE TYPE NO.

EVENT YE AR

@ REP,gRT LER RO l8 l1l l_j lU l1l2l y 27 l 0 l 1l 28 2'J lT l 30

[---J 31 J

32

_ 21 22 23 24 2b HOURS SP 11 FOH L a. S reti YAN FA T ER TA E A TO C PLA T T I33rl@Lr_J@ Lz_J@ LrJ@

36 l 01010 IoI40 3/

Ly_J@

41 Lu]@

42 LtJ@

43 lxl9I91918 '

44 47 34 33 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l

M lSince the "Swanelox" fittingn in rho romnen vnnnenv unne 1,nn unvn

, i gated at 3000 psi it is assumed tnat improper installation causea l nn operator promptly closed j

,, y ,, j the "Swagelok" union to pull apart.

g , g 3 g l the isolation valve. A "Swagelok" plug was installed immediately l l

, 4 l downstream of the isolation valve. 80 7 8 9 OTHERSTATUS ISCO HY DISCOVERY DESCRIPTION l Bl@l Operator observation uurino TestI STA 5 a. POVs E R i 5 (_pjh l n l ofol@l n/A I

ACTev TY COOTENT AVOUNT OF ACTIVITY LOCATION OF RELE ASE acLEASED OF RELE ASE N/A I W [_Z) @ [Zj@l h/ A 44 l l 45 80 7 8 9 10 tt PERSONNEL EXPOSUHES NUMBER DE SCRIPT 60N l

i 7 I I I l@lTYPE l @l PERSONNEL INJUF tES .

NUMBER DESCRIPTION -

l i a l i I l@l12 80 7 8 9 It LOSS OF OR DAYAGE TO FACILtTY Q TYPE O ESCRIPTION v I 9 N/A 60 i

7 8 9 10 PUBLICIT Y NRC USE ONLY

  • r lll1lllll1lIl1 7

2 o 8 9 U l ynD@DE SCRIPTION ISSUE to l

68 69 80 5 PHONE:

NAME OF PREPARER m8106170 % 7

~

  • ATTACl! MENT 1 Docket No. 05000247 ~ Consolidated Edison Company of New' York, Inc.

LER 8'l-012/036-0 Indian Point Unit No. 2 While conducting a test to assure operability of the LPI/RIIR, check valves prior to plant restart, a 3/4 inch "Swagelok" union in the remote reactor head vent line parted. At the

~

time of this event, the reactor coolant system temperature and pressure were approximately 3200F and 1200 psig respectively.

Since "Swagelok" fittings in the remote reactor vent line were rated for at least 3000 psi, it is assumed that faulty instal-lation caused se union to fail. An operator who was in con-tainment at et ; time promptly closed the isolation valve. A "Swagelok" plug was installed downstream of the head vent line isolation valve. Until the remote vent system is connected permanently to the reactor head vent line, the isolation valve will be kept closed to maintain a double barrier.

3 1

[

'f l

    • .,~. - ..n, ---,,:-----,Y"

, - _ ,- n. .- -- - - , - - - . , - ,