ML20052B863

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LER 82-014/03L-0:on 820320,valve 267A Found Leaking.Two Boric Acid Transfer Pumps & Boric Acid Storage Sys Isolated in Order to Isolate Valve for Repairs.Caused by Diaphragm Failure.Valve Repaired
ML20052B863
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 04/19/1982
From: Fitzpatrick R
CONSOLIDATED EDISON CO. OF NEW YORK, INC.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20052B856 List:
References
LER-82-014-03L, LER-82-14-3L, NUDOCS 8205040078
Download: ML20052B863 (1)


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