05000247/LER-1981-013-01, /01T-0:on 810520,low Flow from Two Motor Driven Auxiliary Boiler Feed Pumps at Hot Shutdown Discovered During Surveillance Testing.Caused by New Trim in Generator Level Control Valves Restricting Auxiliary Feedwater Flow

From kanterella
(Redirected from ML20004E929)
Jump to navigation Jump to search
/01T-0:on 810520,low Flow from Two Motor Driven Auxiliary Boiler Feed Pumps at Hot Shutdown Discovered During Surveillance Testing.Caused by New Trim in Generator Level Control Valves Restricting Auxiliary Feedwater Flow
ML20004E929
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 06/03/1981
From: Rosh D
CONSOLIDATED EDISON CO. OF NEW YORK, INC.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20004E928 List:
References
LER-81-013-01T, LER-81-13-1T, NUDOCS 8106160186
Download: ML20004E929 (2)


LER-1981-013, /01T-0:on 810520,low Flow from Two Motor Driven Auxiliary Boiler Feed Pumps at Hot Shutdown Discovered During Surveillance Testing.Caused by New Trim in Generator Level Control Valves Restricting Auxiliary Feedwater Flow
Event date:
Report date:
2471981013R01 - NRC Website

text

$

LICENSEE EVENT REPORT CONTROL DLOctt: l l

l l

l 1

ih (PLEASE PRINT OR TYPE ALL REQUIRED l% FORMATION) l NlYl IlP [5l2 gl6 0l 0 l-l 0 [ 0l 0 l 0l 0 l-l 0 l0 lgl4l1llj 1l l jg l

lg o

9 LICENSEE CODE is 1

UCENSE NWtiEH 26 2t>

UCU.SE TYPC JO 47 CAT LJ e

8 CON'T lolil sM i n l@l0 is 10 I o f of 21 41 7 !@l o is l a lo I R 11 l@l o l e, I o l, I n li l@

V d

60 61 COCKET NUYSEp 6J 63 EVENT DATE I4 7b REFORT DATE 63 EVENT DESCRIPTION AND PROGABLE CONSECUENCES h lo 1:1 l During testing of the two motor driven auxiliary boiler feed pumps at l

[o # 3 l l hot shutdown, flow from the pumps was less than reauired flow. There l

Iol4l l were no adverse consequences of the failure of the pumps to reach l

[ o i f. l l recuired flows.

l r

l e 161 1 I

l0 !7j l l

lois i l 7

8 3 80 SYSTEV

CAUSE

CAU3E CCYP.

VA;VE C00E C00E SUECODE COVPONENT COCE EUSCOOE SU3000!

10191 I clu l@ l a l@ Lp_l@ I v i ^I t I vie I xl8 I nlG LoJ @

7 8

9 10 11 12 12 18 19 R

'E CL E NT; A L OCCURPE*.CE REFORT REv'SiON E'. ENT v EA R R EPCRT NO.

CCCE TYPE

  • O.

O."LE A 20!_ d 11 !

l-l I O 11 13I l/l I 4 1I I Tl l-l i oi

.g; _v n

n u

a v

2, n

u 2:

u A *, ON

1. % 51 EF ECT
a !0 0 t,.

ATT 40HYINT N8 3 0-4 PRiVE 00*ce.

0 0V F O*.E*. T T/.V. E N ACT:0N CN FL A*.T YETr0; 4Las 2.

SL3VITTED FORM nt.

S 77L;E i YAN c 0*;=Em i P!

! ZI@

lZl@

lZ!h I O!0lOl0l l '11 @

lNl@

l A l@

l C l 6l 3 Sly A,

a a

  • n s'

s2

<3 as c

CAUSE DESCRIPTiCN AND CCRRECTIVE ACTIONS M li l t l l New trim in the level control valves installed in feedwater supnly linest l'.

II to the four steam generators restricted auxiliarv feedwater flow.

A

- ji plant cooldown was initiated.

The trin of the four (4) valves was

[

l' Ill l modified and the numns retested satisfactorily.

l i4 i I l

7 a a s0 STATUS N PC/.ER OT-EPST/.TUS

    • e YET' 00 08 F AOrttTV O!!O7 9 O'SCOVIPY DESOP'PTION 3.

l' !;l l c lh IO ! 010 l@l UA l

lB l@lperiodic Surveillance Test l

ACTIVITY CO TENT DELEASEC OF PELE ASE AYOUNT OF ACTIVFV LOCATION OF PELEACE I

d 3 1 C.

11

__j l

nA I

li ic i l Z l @ !Z l@l nA 44 45 SJ PE ASONNEL E XPOSungs YJY2ER TYPE OE00 At* TION @

l i 171 101 Ol 0_j@L 2j31 nA I

7 a 9 u

i.

u so etc.sowt Nnron

.. men c Escu rier. c Ii l l 0 1 0! O ! O I NA I

p9

. ~ - - ~

tc; or on oavAct to FACiury Tv*E CE00RIPT104 I

MA l

11 l'> l I Z l@l 7

1 J

IQ 6'J

'w u C' T v nne ect o t <

~

,E v.m o re,n -

l?lol w(5 l l

l!Il!lI'I!l ! I'

/

'r A o e Donald Rosh (914)997-6000 X215 N A*.*F OF PHC P Artt H p,,0.; g.

810 6 I 6 0 lF(0 -

D Docket No. 05000247 Consolio$ted Edison of 'N.Y.,

Inc.

LER 81-013/OlT-0 Indian Point Unit No. 2 During testing of the motor driven auxiliary boiler feed pumps, flow from the pumps was less than required flow.

The plant was at hot shutdown conditions.

There were no adverse con-sequ6nces caused by the pump not producing the required flow.

1 New feedwater regulating valve trim in four (4) lines leading to the steam generators, was installed during the Cycle 4/5 refueling and maintenance outage and was determined to be the cause of the restricted feedwater flow.

A plant cooldown was initiated.

The valve trim in each valve was modified to correct the condition.

The test was re-run with each motor driven auxiliary boiler feed pump, and the data indicated that each pump met flow requirements.

4 i