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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E2061994-05-11011 May 1994 LER 93-025-01:on 931205,Loop a MSIVs Exceeded TS Leakage Limit.Caused by Failure of Fastner Locking Devices.Seating Surface of Main Disc in MSIV 1A Machined & Successfully Pass LLRT on 940116.W/940511 Ltr ML17352B2501993-10-0101 October 1993 LER 93-014-00:on 930902,discovered That IRM 11 & APRM Both in Bypassed Condition W/O Half Scram Being Inserted Due to Work Practices.Irm 11 Taken Out of Bypassed Condition & Individual Involved counselled.W/931001 Ltr ML17352B2511993-10-0101 October 1993 LER 93-019-00:on 930903,RHR Pump 1A Inadvertently Started Due to Personnel Error.Pump Immediately Secured & Individual Involved Counselled on Importance of self-check.W/931001 Ltr ML20046A1801993-07-21021 July 1993 LER 92-007-00:on 930624,Toxic Gas Analyzer Inoperable Due to Personnel Error Caused by Lack of Procedural Adherence. Isolated CR Ventilation,Restarted Sample Pump & Restored CR Ventilation Sys to Outside Air suction.W/930721 Ltr ML20045H5781993-07-13013 July 1993 LER 93-013-00:on 930613,internal Electrical Fault within Main Power Transformer Tripped & Caused Reactor Scram & Unexpected Group I Isolation.Caused by Turbine Stop Valve Closure.Transformer replaced.W/930713 Ltr ML20045G7291993-07-0909 July 1993 LER 93-005-00:on 930609,numerous Alarms Received in CR, Including HPCI Turbine Rupture Disc High Pressure Alarm. Caused by Ruptured Disk,Releasing Steam/Water Mixture. Test Will Be Conducted on Rupture disks.W/930709 Ltr ML20045G0951993-07-0202 July 1993 LER 93-011-00:on 930602,HPCI Declared Inoperable in Order to Perform Qcos 2300-13.Caused by MSC Stem & Stem Gear Being Scored & Worn from Age Causing Excessive Friction.C/As Include Disassembling Gearbox Every 10 yrs.W/930702 Ltr ML20045F3321993-06-30030 June 1993 LER 93-012-00:on 930601,U-2 DG Cooling Water Pump Inoperable Due to Inadequate lubrication.U-2 DG Cooling Water Pump replaced.W/930630 Ltr ML20045F3251993-06-28028 June 1993 LER 93-007-01:on 930307,B Loop MSIV Exceeded TS Leakage Limits for Containment Isolation Valves Caused by Damaged Flexitalic Bonnet Gasket.Replaced Bonnet Gasket & Valve Successfully Retested (WR Q061987).W/930622 Ltr ML20044E6171993-05-14014 May 1993 LER 93-006-00:on 930420,Unit 2 Nso Inadvertently Started Unit 1 DG When Attempting to Start Shared (1/2) Dg.Caused by Personnel Error.Unit 1 DG Shut Down & 1/2 DG Started & Loaded successfully.W/930514 Ltr ML20044C9511993-05-0707 May 1993 LER 93-009-00:on 930408,technician Discovered That Estimate of Sample Flow for U2 Reactor Bldg Vent Sampler Flow Rate Monitor Not Calculated.Caused by Personnel Error.Technician counseled.W/930428 Ltr ML20024G6811991-04-19019 April 1991 LER 91-008-00:on 910322,reactor Bldg Ventilation Isolation Occurred.Caused by Lightning Strike.Control Room Vents Reset & Toxic Gas Sample Point a Selected.Addl Trips Associated W/ Lightning Strike Immediately reset.W/910418 Ltr ML20029C1241991-03-0808 March 1991 LER 91-005-01:on 910131,1/2 B Standby Gas Treatment Sys Autostart During RPS B Power Swap Due to an Inadequate Procedure.Nso Reset 1/2 Scram & 1/2 Groups II & III isolations.W/910306 Ltr ML20029B5901991-03-0808 March 1991 LER 91-004-00:on 910211,standby Liquid Control Sys of Unit 1 & 2 Inoperable.Caused by Inadequate Mod Testing.Engineering Dept Evaluating Data & Temporary Procedure 6589 Generated. W/910308 Ltr ML20028H7841991-01-23023 January 1991 LER 90-032-00:on 901224,1/2A Diesel Fire Pump Taken out-of- Svc on 901217 & Not Returned to Svc Before Seven Day Time Allotment Expired.Caused by Mgt Deficiency.Fire Pump Successfully Tested & Returned to svc.W/910123 Ltr ML20028H6831991-01-21021 January 1991 LER 90-034-00:on 901223,high Chlorine Concentration Caused Control Room Ventilation Manual Isolation & ESF Actuation. Caused by Instrument Error Code & Misinterpretation of Analyzer Indication.Flow reduced.W/910121 Ltr ML20028G9141990-09-28028 September 1990 LER 90-018-00:on 900829,plant Outside Design Spec for Electrical Separation Criteria for Two Redundant Safety Sys. Caused by Inadequate Engineering Review During Leads installation.W/900928 Ltr ML20044B2401990-07-12012 July 1990 LER 90-012-00:on 900612,control Room Ventilation Emergency Air Filtration Unit Declared Inoperable.Caused by Heater Malfunction.Work Request initiated.W/900712 Ltr ML20044B0091990-07-11011 July 1990 LER 90-011-00:on 900611,diesel Fire Pump 1/2 a Out of Svc for Period Exceeding 7 Days Reporting Criteria,To Install New Suction Line.Caused by Required Maint Work.Repairs Completed & Pump Tested & Returned to svc.W/900711 Ltr ML20043H4831990-06-21021 June 1990 LER 90-010-00:on 900522,while Returning RWCU Sys to Svc, Nonregenerative HX High Temp Alarm Received,Challenging ESF Logic & Causing Group III Isolation.Caused by Leaking RWCU Check Valves.Work Requests issued.W/900621 Ltr ML20043H2931990-06-18018 June 1990 LER 90-009-00:on 900518,determined That Various Containment Vols Not Leak Rate Tested Due to Recent 10CFR50,App J Interpretation Re Licensing Design Criteria.Mod M4-1(2)-89-167 initiated.W/900618 Ltr ML20043H9521990-06-13013 June 1990 LER 90-016-01:on 900411,motor Control Ctr Relay 28/29-5 Setpoint Drift Occurred,Resulting in Analyzed Plant Condition.Caused by Utilizing Wrong Relay & Inadequate Review of GE Svc Info Ltr.Relay replaced.W/900613 Ltr ML20043E9121990-06-0707 June 1990 LER 90-006-00:on 900508,Unit 2 RCIC Declared Inoperable Due to Unstable Operation of RCIC Pump Flow Controller.Caused by Proportional Band of Controller Being Set to Respond to Changes in Flow Too Quickly.Flow controlled.W/900607 Ltr ML20043F2341990-06-0101 June 1990 LER 90-001-01:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Test Program.Caused by Misinterpretation of 10CFR50,App J Requirements.Required Vents & Test Taps Will Be installed.W/900601 Ltr ML20043F2161990-06-0101 June 1990 LER 89-024-01:on 891214,main Turbine Unexpectedly Tripped Following Isolation of Reactor Water Level Switch (Lits). Caused by Channel B Lits Having Been Previously Replaced W/ Switch That Operated Reverse function.W/900601 Ltr ML20042E4991990-04-17017 April 1990 LER 90-007-00:on 900318,ESF Actuation Occurred.Caused by Mgt Deficiency in Not Providing Sufficient Guidance for Review of Work Package After Scope Changed.New Work Package Preparation Procedures initiated.W/900417 Ltr ML20012C7231990-03-15015 March 1990 LER 90-004-00:on 900213,loss of Emergency Bus 23-1 Occurred Due to Shorted Conductor Cable While Performing Wiring Verification.Caused by Personnel Error & Improper Installation.Electric Power Supplies recovered.W/900315 Ltr ML20012C7171990-03-15015 March 1990 LER 90-003-00:on 900213,unit Diesel Generator Tripped on Overspeed Upon Manual Startup for Testing.Caused by Misadjustment of Diesel Generator Governor.Diesel Generator Equipment Reset & Governor adjusted.W/900315 Ltr ML20012B2931990-03-0505 March 1990 LER 90-002-00:on 900204,determined That Only Reactor Bldg Differential Pressure of 0.24-inch Water Vacuum Could Be Obtained,In Violation of Tech Spec Required 0.25 Inch.Caused by Testing Deficiency.Leak Paths sealed.W/900305 Ltr ML20012B2961990-03-0505 March 1990 LER 90-003-00:on 900205,determined That Leakage Rate for HPCI Sys Steam Exhaust Check Valve Exceeded Tech Spec Limits.Caused by Excessive Leakage.Check Valve Replaced W/ Mission Check Valve W/Carbon Steel springs.W/900305 Ltr ML20011E1821990-01-30030 January 1990 LER 90-002-00:on 900102,during Annual Water Sprinkler Sys Valve Position Insp,Discovered That Valve 2-4199-072 Not Cycled Per Tech Spec Surveillance Requirement 4.12.Caused by Procedural Deficiency.Procedure to Be revised.W/900130 Ltr ML19354D9431990-01-15015 January 1990 LER 89-025-00:on 891220,determined That Reactor Bldg Overhead Auxiliary Hook May Have Contacted Side of New Fuel Bundle on 891214,causing Extensive Damage.Caused by Personnel Error.Bundle Shipped Back to GE.W/900115 Ltr ML19354D9481990-01-15015 January 1990 LER 89-023-00:on 891219,identified Deficient Temporary Procedures Which Altered Intent of Original Procedure QAP 1100-7.Caused by Mgt Oversight in Preparation of Tech Spec Change.Temporary Procedures revised.W/900115 Ltr ML20005F5881990-01-0808 January 1990 LER 90-001-00:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Testing Program.Caused by Misinterpretation of 10CFR50,App J Testing Requirements.Mod of Sys to Be Performed as necessary.W/900108 Ltr ML20005G0231990-01-0202 January 1990 LER 88-020-01:on 880619,improper Valving Sequence Occurred Which Resulted in Various ESF Actuations.Caused by Inadequate Equipment out-of-svc Procedure.Procedure Revised & Training Lesson Plan developed.W/900102 Ltr ML20005E4531989-12-28028 December 1989 LER 89-022-00:on 891128,HPCI Declared Inoperable Following Unexpected Actuation of HPCI Pump Room Deluge Sys.Actuation Caused Dc Sys Grounds Due to Moisture Intrusion in Electrical Equipment.Equipment dried.W/891228 Ltr ML20005D9551989-12-22022 December 1989 LER 89-021-00:on 891124,HPCI Deluge Sys Functional Test Not Completed within Tech Spec Interval of 6 Months.Caused by Mgt Deficiency & Insufficient Procedure.Procedures Revised to Better Control Tech Specs.W/891222 Ltr ML19351A6391989-12-15015 December 1989 LER 89-020-00:on 891117,full Reactor Scram Occurred Due to Simultaneous Loss of Power to 1A & 1B 24/48-volt Distribution Panels During Panel Transfer.Caused by Personnel Error.Personnel Trained Re event.W/891215 Ltr ML19332E7581989-12-0505 December 1989 LER 89-019-00:on 891105,half Group II & III Isolation Occurred While Performing Valve Flow Check Surveillance. Caused by Leaky Isolation Valve on Transmitter.Surveillance Methods Will Be Reviewed & Procedures revised.W/891205 Ltr ML19332C7581989-11-20020 November 1989 LER 89-017-00:on 891022,discovered That 6-month Functional Test Procedure Qos 500-3 Re Functional Test for Reactor Protection Sys Electrical Assemblies Not Completed in Required Time.Caused by Mgt deficiency.W/891120 Ltr ML19327C0701989-11-0909 November 1989 LER 89-018-00:on 891012,notification Given of Potential Single Failure of Diesel Generator Voltage Regulator That Could Result in Loss of All But One ECCS Loop.Caused by Design Deficiency.New Procedure developed.W/891109 Ltr ML19327C0951989-11-0404 November 1989 LER 89-005-00:on 891012,reactor Scram Occurred Due to Turbine Stop Valve Closure.Caused by Personnel Error in That Work Analyst Overlooked Removal of Two Connections on Limit Switch.Maint Workers Immediately counseled.W/891104 Ltr ML19327C2631989-11-0101 November 1989 LER 87-009-01:on 870801,reactor Scram Occurred from Turbine Generator Load Mismatch Due to Generator Trip.Caused by Electrical Fault in Main Transformer C Phase Windings.Main Transformer Replaced w/spare.W/891103 Ltr ML19325E8261989-10-30030 October 1989 LER 87-012-01:on 870918,while Performing Qos 1600-1, Vacuum Breaker 2-1601-33E Remained Open After Testing.Caused by Binding in Test Cylinder Portion of Vacuum Breaker. Nuclear Work Requests completed.W/891030 Ltr ML19325E5921989-10-24024 October 1989 LER 87-017-01:on 870805,Group IV Isolation Received Which Resulted in Closure of HPCI Steam Supply Valves.Caused by Failed HPCI Steamline Differential Pressure Transmitter Due to Loss of Oil in Sensing cell.W/891024 Ltr ML19325E5971989-10-24024 October 1989 LER 88-003-01:on 880301,while Performing RCIC Monthly Test, RCIC Pump Could Only Achieve 400 Gpm Against Discharge Pressure of 500 Psig.Caused by Failed Hydraulic Actuator on Turbine Governor Valve.Actuator replaced.W/891024 Ltr ML19327B7901989-10-18018 October 1989 LER 89-016-00:on 890921,during Transfer of New Fuel,Fuel Assembly Released from Refueling Grapple & Fell Upon Spent Fuel Racks.Caused by Personnel Error & Procedural Deficiency.Fuel Handling Procedures Revised ML19327B0491989-10-16016 October 1989 LER 89-015-00:on 890916,during Transfer,Loss of Power to Off Gas Monitor a Caused Contacts to Open Giving Upscale Radiation Signal,Thus Starting Off Gas Timer.Caused by Inadequate Procedures.Off Gas Sys reset.W/891016 Ltr ML19325C5341989-10-0202 October 1989 LER 89-014-00:on 890910,determined That Combined Leakage Rate from All Penetrations & Valves Exceeded Tech Spec Limit.Root Cause Unknown.No Corrective Action Taken. Supplemental Rept Will Be issued.W/891002 Ltr ML18052B5541987-08-24024 August 1987 LER 87-015-00:on 870731,capacitor Failed on 1B Reactor Bldg & Refuel Floor Radiation Monitors Resulting in Safety Feature Actuation.Caused by Normal Aging.Capacitor replaced.W/870825 Ltr 1994-05-11
[Table view] Category:RO)
MONTHYEARML20029E2061994-05-11011 May 1994 LER 93-025-01:on 931205,Loop a MSIVs Exceeded TS Leakage Limit.Caused by Failure of Fastner Locking Devices.Seating Surface of Main Disc in MSIV 1A Machined & Successfully Pass LLRT on 940116.W/940511 Ltr ML17352B2501993-10-0101 October 1993 LER 93-014-00:on 930902,discovered That IRM 11 & APRM Both in Bypassed Condition W/O Half Scram Being Inserted Due to Work Practices.Irm 11 Taken Out of Bypassed Condition & Individual Involved counselled.W/931001 Ltr ML17352B2511993-10-0101 October 1993 LER 93-019-00:on 930903,RHR Pump 1A Inadvertently Started Due to Personnel Error.Pump Immediately Secured & Individual Involved Counselled on Importance of self-check.W/931001 Ltr ML20046A1801993-07-21021 July 1993 LER 92-007-00:on 930624,Toxic Gas Analyzer Inoperable Due to Personnel Error Caused by Lack of Procedural Adherence. Isolated CR Ventilation,Restarted Sample Pump & Restored CR Ventilation Sys to Outside Air suction.W/930721 Ltr ML20045H5781993-07-13013 July 1993 LER 93-013-00:on 930613,internal Electrical Fault within Main Power Transformer Tripped & Caused Reactor Scram & Unexpected Group I Isolation.Caused by Turbine Stop Valve Closure.Transformer replaced.W/930713 Ltr ML20045G7291993-07-0909 July 1993 LER 93-005-00:on 930609,numerous Alarms Received in CR, Including HPCI Turbine Rupture Disc High Pressure Alarm. Caused by Ruptured Disk,Releasing Steam/Water Mixture. Test Will Be Conducted on Rupture disks.W/930709 Ltr ML20045G0951993-07-0202 July 1993 LER 93-011-00:on 930602,HPCI Declared Inoperable in Order to Perform Qcos 2300-13.Caused by MSC Stem & Stem Gear Being Scored & Worn from Age Causing Excessive Friction.C/As Include Disassembling Gearbox Every 10 yrs.W/930702 Ltr ML20045F3321993-06-30030 June 1993 LER 93-012-00:on 930601,U-2 DG Cooling Water Pump Inoperable Due to Inadequate lubrication.U-2 DG Cooling Water Pump replaced.W/930630 Ltr ML20045F3251993-06-28028 June 1993 LER 93-007-01:on 930307,B Loop MSIV Exceeded TS Leakage Limits for Containment Isolation Valves Caused by Damaged Flexitalic Bonnet Gasket.Replaced Bonnet Gasket & Valve Successfully Retested (WR Q061987).W/930622 Ltr ML20044E6171993-05-14014 May 1993 LER 93-006-00:on 930420,Unit 2 Nso Inadvertently Started Unit 1 DG When Attempting to Start Shared (1/2) Dg.Caused by Personnel Error.Unit 1 DG Shut Down & 1/2 DG Started & Loaded successfully.W/930514 Ltr ML20044C9511993-05-0707 May 1993 LER 93-009-00:on 930408,technician Discovered That Estimate of Sample Flow for U2 Reactor Bldg Vent Sampler Flow Rate Monitor Not Calculated.Caused by Personnel Error.Technician counseled.W/930428 Ltr ML20024G6811991-04-19019 April 1991 LER 91-008-00:on 910322,reactor Bldg Ventilation Isolation Occurred.Caused by Lightning Strike.Control Room Vents Reset & Toxic Gas Sample Point a Selected.Addl Trips Associated W/ Lightning Strike Immediately reset.W/910418 Ltr ML20029C1241991-03-0808 March 1991 LER 91-005-01:on 910131,1/2 B Standby Gas Treatment Sys Autostart During RPS B Power Swap Due to an Inadequate Procedure.Nso Reset 1/2 Scram & 1/2 Groups II & III isolations.W/910306 Ltr ML20029B5901991-03-0808 March 1991 LER 91-004-00:on 910211,standby Liquid Control Sys of Unit 1 & 2 Inoperable.Caused by Inadequate Mod Testing.Engineering Dept Evaluating Data & Temporary Procedure 6589 Generated. W/910308 Ltr ML20028H7841991-01-23023 January 1991 LER 90-032-00:on 901224,1/2A Diesel Fire Pump Taken out-of- Svc on 901217 & Not Returned to Svc Before Seven Day Time Allotment Expired.Caused by Mgt Deficiency.Fire Pump Successfully Tested & Returned to svc.W/910123 Ltr ML20028H6831991-01-21021 January 1991 LER 90-034-00:on 901223,high Chlorine Concentration Caused Control Room Ventilation Manual Isolation & ESF Actuation. Caused by Instrument Error Code & Misinterpretation of Analyzer Indication.Flow reduced.W/910121 Ltr ML20028G9141990-09-28028 September 1990 LER 90-018-00:on 900829,plant Outside Design Spec for Electrical Separation Criteria for Two Redundant Safety Sys. Caused by Inadequate Engineering Review During Leads installation.W/900928 Ltr ML20044B2401990-07-12012 July 1990 LER 90-012-00:on 900612,control Room Ventilation Emergency Air Filtration Unit Declared Inoperable.Caused by Heater Malfunction.Work Request initiated.W/900712 Ltr ML20044B0091990-07-11011 July 1990 LER 90-011-00:on 900611,diesel Fire Pump 1/2 a Out of Svc for Period Exceeding 7 Days Reporting Criteria,To Install New Suction Line.Caused by Required Maint Work.Repairs Completed & Pump Tested & Returned to svc.W/900711 Ltr ML20043H4831990-06-21021 June 1990 LER 90-010-00:on 900522,while Returning RWCU Sys to Svc, Nonregenerative HX High Temp Alarm Received,Challenging ESF Logic & Causing Group III Isolation.Caused by Leaking RWCU Check Valves.Work Requests issued.W/900621 Ltr ML20043H2931990-06-18018 June 1990 LER 90-009-00:on 900518,determined That Various Containment Vols Not Leak Rate Tested Due to Recent 10CFR50,App J Interpretation Re Licensing Design Criteria.Mod M4-1(2)-89-167 initiated.W/900618 Ltr ML20043H9521990-06-13013 June 1990 LER 90-016-01:on 900411,motor Control Ctr Relay 28/29-5 Setpoint Drift Occurred,Resulting in Analyzed Plant Condition.Caused by Utilizing Wrong Relay & Inadequate Review of GE Svc Info Ltr.Relay replaced.W/900613 Ltr ML20043E9121990-06-0707 June 1990 LER 90-006-00:on 900508,Unit 2 RCIC Declared Inoperable Due to Unstable Operation of RCIC Pump Flow Controller.Caused by Proportional Band of Controller Being Set to Respond to Changes in Flow Too Quickly.Flow controlled.W/900607 Ltr ML20043F2341990-06-0101 June 1990 LER 90-001-01:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Test Program.Caused by Misinterpretation of 10CFR50,App J Requirements.Required Vents & Test Taps Will Be installed.W/900601 Ltr ML20043F2161990-06-0101 June 1990 LER 89-024-01:on 891214,main Turbine Unexpectedly Tripped Following Isolation of Reactor Water Level Switch (Lits). Caused by Channel B Lits Having Been Previously Replaced W/ Switch That Operated Reverse function.W/900601 Ltr ML20042E4991990-04-17017 April 1990 LER 90-007-00:on 900318,ESF Actuation Occurred.Caused by Mgt Deficiency in Not Providing Sufficient Guidance for Review of Work Package After Scope Changed.New Work Package Preparation Procedures initiated.W/900417 Ltr ML20012C7231990-03-15015 March 1990 LER 90-004-00:on 900213,loss of Emergency Bus 23-1 Occurred Due to Shorted Conductor Cable While Performing Wiring Verification.Caused by Personnel Error & Improper Installation.Electric Power Supplies recovered.W/900315 Ltr ML20012C7171990-03-15015 March 1990 LER 90-003-00:on 900213,unit Diesel Generator Tripped on Overspeed Upon Manual Startup for Testing.Caused by Misadjustment of Diesel Generator Governor.Diesel Generator Equipment Reset & Governor adjusted.W/900315 Ltr ML20012B2931990-03-0505 March 1990 LER 90-002-00:on 900204,determined That Only Reactor Bldg Differential Pressure of 0.24-inch Water Vacuum Could Be Obtained,In Violation of Tech Spec Required 0.25 Inch.Caused by Testing Deficiency.Leak Paths sealed.W/900305 Ltr ML20012B2961990-03-0505 March 1990 LER 90-003-00:on 900205,determined That Leakage Rate for HPCI Sys Steam Exhaust Check Valve Exceeded Tech Spec Limits.Caused by Excessive Leakage.Check Valve Replaced W/ Mission Check Valve W/Carbon Steel springs.W/900305 Ltr ML20011E1821990-01-30030 January 1990 LER 90-002-00:on 900102,during Annual Water Sprinkler Sys Valve Position Insp,Discovered That Valve 2-4199-072 Not Cycled Per Tech Spec Surveillance Requirement 4.12.Caused by Procedural Deficiency.Procedure to Be revised.W/900130 Ltr ML19354D9431990-01-15015 January 1990 LER 89-025-00:on 891220,determined That Reactor Bldg Overhead Auxiliary Hook May Have Contacted Side of New Fuel Bundle on 891214,causing Extensive Damage.Caused by Personnel Error.Bundle Shipped Back to GE.W/900115 Ltr ML19354D9481990-01-15015 January 1990 LER 89-023-00:on 891219,identified Deficient Temporary Procedures Which Altered Intent of Original Procedure QAP 1100-7.Caused by Mgt Oversight in Preparation of Tech Spec Change.Temporary Procedures revised.W/900115 Ltr ML20005F5881990-01-0808 January 1990 LER 90-001-00:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Testing Program.Caused by Misinterpretation of 10CFR50,App J Testing Requirements.Mod of Sys to Be Performed as necessary.W/900108 Ltr ML20005G0231990-01-0202 January 1990 LER 88-020-01:on 880619,improper Valving Sequence Occurred Which Resulted in Various ESF Actuations.Caused by Inadequate Equipment out-of-svc Procedure.Procedure Revised & Training Lesson Plan developed.W/900102 Ltr ML20005E4531989-12-28028 December 1989 LER 89-022-00:on 891128,HPCI Declared Inoperable Following Unexpected Actuation of HPCI Pump Room Deluge Sys.Actuation Caused Dc Sys Grounds Due to Moisture Intrusion in Electrical Equipment.Equipment dried.W/891228 Ltr ML20005D9551989-12-22022 December 1989 LER 89-021-00:on 891124,HPCI Deluge Sys Functional Test Not Completed within Tech Spec Interval of 6 Months.Caused by Mgt Deficiency & Insufficient Procedure.Procedures Revised to Better Control Tech Specs.W/891222 Ltr ML19351A6391989-12-15015 December 1989 LER 89-020-00:on 891117,full Reactor Scram Occurred Due to Simultaneous Loss of Power to 1A & 1B 24/48-volt Distribution Panels During Panel Transfer.Caused by Personnel Error.Personnel Trained Re event.W/891215 Ltr ML19332E7581989-12-0505 December 1989 LER 89-019-00:on 891105,half Group II & III Isolation Occurred While Performing Valve Flow Check Surveillance. Caused by Leaky Isolation Valve on Transmitter.Surveillance Methods Will Be Reviewed & Procedures revised.W/891205 Ltr ML19332C7581989-11-20020 November 1989 LER 89-017-00:on 891022,discovered That 6-month Functional Test Procedure Qos 500-3 Re Functional Test for Reactor Protection Sys Electrical Assemblies Not Completed in Required Time.Caused by Mgt deficiency.W/891120 Ltr ML19327C0701989-11-0909 November 1989 LER 89-018-00:on 891012,notification Given of Potential Single Failure of Diesel Generator Voltage Regulator That Could Result in Loss of All But One ECCS Loop.Caused by Design Deficiency.New Procedure developed.W/891109 Ltr ML19327C0951989-11-0404 November 1989 LER 89-005-00:on 891012,reactor Scram Occurred Due to Turbine Stop Valve Closure.Caused by Personnel Error in That Work Analyst Overlooked Removal of Two Connections on Limit Switch.Maint Workers Immediately counseled.W/891104 Ltr ML19327C2631989-11-0101 November 1989 LER 87-009-01:on 870801,reactor Scram Occurred from Turbine Generator Load Mismatch Due to Generator Trip.Caused by Electrical Fault in Main Transformer C Phase Windings.Main Transformer Replaced w/spare.W/891103 Ltr ML19325E8261989-10-30030 October 1989 LER 87-012-01:on 870918,while Performing Qos 1600-1, Vacuum Breaker 2-1601-33E Remained Open After Testing.Caused by Binding in Test Cylinder Portion of Vacuum Breaker. Nuclear Work Requests completed.W/891030 Ltr ML19325E5921989-10-24024 October 1989 LER 87-017-01:on 870805,Group IV Isolation Received Which Resulted in Closure of HPCI Steam Supply Valves.Caused by Failed HPCI Steamline Differential Pressure Transmitter Due to Loss of Oil in Sensing cell.W/891024 Ltr ML19325E5971989-10-24024 October 1989 LER 88-003-01:on 880301,while Performing RCIC Monthly Test, RCIC Pump Could Only Achieve 400 Gpm Against Discharge Pressure of 500 Psig.Caused by Failed Hydraulic Actuator on Turbine Governor Valve.Actuator replaced.W/891024 Ltr ML19327B7901989-10-18018 October 1989 LER 89-016-00:on 890921,during Transfer of New Fuel,Fuel Assembly Released from Refueling Grapple & Fell Upon Spent Fuel Racks.Caused by Personnel Error & Procedural Deficiency.Fuel Handling Procedures Revised ML19327B0491989-10-16016 October 1989 LER 89-015-00:on 890916,during Transfer,Loss of Power to Off Gas Monitor a Caused Contacts to Open Giving Upscale Radiation Signal,Thus Starting Off Gas Timer.Caused by Inadequate Procedures.Off Gas Sys reset.W/891016 Ltr ML19325C5341989-10-0202 October 1989 LER 89-014-00:on 890910,determined That Combined Leakage Rate from All Penetrations & Valves Exceeded Tech Spec Limit.Root Cause Unknown.No Corrective Action Taken. Supplemental Rept Will Be issued.W/891002 Ltr ML18052B5541987-08-24024 August 1987 LER 87-015-00:on 870731,capacitor Failed on 1B Reactor Bldg & Refuel Floor Radiation Monitors Resulting in Safety Feature Actuation.Caused by Normal Aging.Capacitor replaced.W/870825 Ltr 1994-05-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30
[Table view] |
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4$.; -.
i; a- Commomssalth Edison.
Quad Cities Nuclear Power Station i 22710 206 Avenue North L ooroova, Illinois $1242 Telephone 300/664 2241 RLB-90-072 March 5, 1990 U. S. Nuclear Regulatory Commission Document Control Desk Hashington, DC 20555
Reference:
Quad Cities Nuclear Power Station Docket Number 50-254, DPR-29. Unit One Enclosed is Licensee Event Report (LER)90-002, Revision 00, for Quad Cities Nuclear Power Station.
This report is submitted in accordance with the requirements of the Code of Federal Regulations, Title 10, Part 50.73(a)(2)(1)(B): The licensee shall report any operation or condition prohibited by the plant's Technical Specifications.
Respectfully, COMMONNEALTH EDISON COMPANY QUAD CITIES NUCLEAR POWER STATION
$4-R. L. Ba)/
Station Manager RLB MJB/ekb Enclosure cc: R. Stols R..Higgins INPO Records Center NRC Region III f
$8R3228!n 88888 S
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LICENSEE EVENT REPORT (LER) Fare key 2.0 Facility Name (1) Docket Number (2) Pane f3)
' nuad citiet unit One of El el of 01 fl El 4 1 ef C E Title (4) Inability to Maintain 0.25 Inches of Water Vacuum Ouring secondary Containment Test Due to T rature Effnett.
Event Date (E) LtR Nunter (6) Recort Date f71 Other Facilities Involved fR)
Month Day Year Year g/p Sequential //j/
//
ff Revision Month Day Year Facilits Namet Docket Numberf t)
/// Number /// Number Quad citiet 01 El 01 01 01 21 61 1
~ '"
el 2 OI 4 91 0 91 0 0 10 l2 0 10 0I3 DIE 91 0 01 E l o f 01 01 l l THIS REPORT IS $ubMITTED PUR$uANT TO THE REQu!REMENTS OF 10CFR OPWW (Check one or more of the f ollowine) fll) 4 20.402(b) 20.405(c) 50.73(a)(2)(tv) _._ 73.71(b)
PodER __ 20.40$(a)(1)(1) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)
LEVEL _, 20.405(a)(1)(11) _ 50.36(c)(2) 50.73(a)(2)(v11) Other (Specify (101 0 9 1 20.405(a)(1)(tit) )L 50.73(a)(2)(1) 50.73(a)(2)(vitt)(A) in Abstract
//////////////////////////, 20.40$(a)(1)(iv) 50.73(a)(2)(11) 50.73(a)(2)(viti)(B) below and in
//////////////////////////' , 20.405(a)(1)(v) 50.73(a)(2)(111) 50.73(a)(2)(x) Text)
LItthitt CONTAtf FOR THIS LER f12)
Name T[LEPHONE NUMBf R AREA CODE
- 0. F. Sch-her. Technteal Staf f Ennineer. Ext. 2820 3 10 l9 61 El 4l -l fl 214l COMPLETE ONE LINT FOR [AtH COMP FAILURE DEstRIBt0 IN THIS REPORT (13)
CAuSE SYSTEM c0MPONENT MANuFAC- REPORTABLE CAUSE SYSTEM COMPONENT MANuFAC. REPORTABLE TURER TO NPROS TURER TO NPR01 I l I l i I I N I l l l l 1 l 1 l ! I I I I I I I I I I l SUPPLEMENTAL REPORT trP[tTED (141 Expected t!Qalh I Day l Year submission lYet (If vet. enmelete txPttit0 tusMISSION DATE) K l NO ' (1 }
l ll lI ABSTRACT (Limit to 1400 spaces, i.e. approximately fif teen single-space typewritten lines) (16)
ABSTRACT:
At 0754 hours0.00873 days <br />0.209 hours <br />0.00125 weeks <br />2.86897e-4 months <br /> on February 4, 1990, Unit One was operating in the RUN mode at 91 percent rated core thermal power. A GSEP unusual event was entered due to the results obtained while performing QTS 160-5, Secondary Containment Capability Test. It was determined that a Reactor Building differential pressure of 0.24 inches of water vacuum could be attained; whereas, an average of 0.25 inches of water vacuum is required by Technical Specification 4.7.C.I.c.
Inspections of suspected leak paths were conducted and temporary seals were installed. By 1230 hours0.0142 days <br />0.342 hours <br />0.00203 weeks <br />4.68015e-4 months <br />, the reactor building differential pressure had reached 0.275 inches of water vacuum. Seven temporary seals were removed with little or no effect on the differential pressure. At 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> the differential pressure had reached 0.28 inches of water vacuum.
The cause of this event is attributed to temperature induced differences in the pressure gradients between the inside and outside of Secondary Containment, which were uncompensated for in the test procedure. Due to this effect, it is believed that Secondary Containment capability was intact throughout this event.
l At 1642 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.24781e-4 months <br />, on-site review 90-5 was performed to review the actions involved with the GSEP unusual event. At 1648 hours0.0191 days <br />0.458 hours <br />0.00272 weeks <br />6.27064e-4 months <br />, the GSEP unusual event was terminated.
This report is being submitted in accordance with 10 CFR 50.73(a)(2)(1)(B).
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i tittuttr tvtut arrant strai ttri enmitmuatinu rara may 2.0 f
FACILITY mAME (1) DOCKET WuMsER (t) Ltn utsa tt r n Pane in k Year seguential Revision name. r er j w cities unit one o I s I o I e I o i 21 51 4 910 - oIo12 - oI o el 2 or als j TEXT Energy Industry 16entification system (E!!s) codes are identified in the text as (xx] l PLANT AND SYSTEM IDENTIFICATION:
i General. Electric - Bolling Water Reactor - 2511 MWt rated core thermal power.
EVENT IDENTIFICATION: Inability to Maintain 0.25 Inches of Water Vacuum During q Secondary Containment Test Due to Temperature Effects.
l A. CONDITIONS PRIOR TO EVENT:
Unit: One Event Date: February 4, 1990 Event Time: 0754 Reactor Mode: 4 Mode Name: RUN Power Level: 91% ;
i This report was initiated by Deviation Report D-4-1-90-016 RUN Mode (4) In this position the reactor system pressure is at or above 825 psig, ,
and the reactor protection system is energized, with APRM protection and RBM ;
interlocks 1.1 service (excluding the 15% high flux scram).
B. DESCRIPTION OF EVENT: i At 0754 hours0.00873 days <br />0.209 hours <br />0.00125 weeks <br />2.86897e-4 months <br /> on February 4, 1990e Unit One was operating in the RUN mode at 91 percent of rated core thermal power, and Unit Two was in the SHUTDOWN mode for the beginning of a scheduled refueling outage. Technical Staff personnel were performing QTS 160-5, Secondary Containment [NH] Capability Test. It was ;
determined that an average of 0.25 inches of water vacuum could not be maintained in the Reactor building as required by Technical Specifications.
l Initial test results indicated 0.24 inches of water vacuum could be attained in the Reactor Building [NH). Based on this result, Technical Specifications require that within twenty four hours, both units be placed in a condition that does not require Secondary Containment. Unit Two was in cold shutdown which satisfied the requirement, and at 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br />, a shutdown of Unit one reactor was initiated at a rate of 100 MWe per hour and a GSEP unusual Event was entered. ,
OTS 160-5 was initiated at 0351 hours0.00406 days <br />0.0975 hours <br />5.803571e-4 weeks <br />1.335555e-4 months <br /> on February 4, 1990. The wind speed was approximately 8.5 miles per hour and the direction was 210 degrees. The average of 4 differential pressure indicators located at the 696' elevation of the Reactor :
Building showed 0.24 inches of water vacuum.
Between 0800 and 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />, inspections were made of suspected leak paths which Cere then temporarily repaired to determine their effect on Reactor building ;
differential pressure. By 1230 hours0.0142 days <br />0.342 hours <br />0.00203 weeks <br />4.68015e-4 months <br />, the reactor building differential pressure had increased to 0.275 inches of water vacuum.
With Reactor building differential pressure at an acceptable value, 7 of the 11 temporary seals were removed one at a time in an attempt to quantify the leakage and it was concluded that these seals had had little or no effect on the building differential pressure. At 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br />, with the average differential pressure at 0.28 inches of water vacuum, the test was successfully completed.
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LifEMitt EVENT RfPORT fLER) T[KT fDMTIMHATIhN Form Rev t.o FACILITY NAME (1) 00cKti Nupett (2) Ltk munare f 61 Paae f21 Year // sequential /// Reviston
'/p/
//
7 u"= r jff
/// u d ar med fit tes unit one o l's I o I o I e 121114 eIo . oIoIt . oI o el 3 or als TEXT Energy Industry 16enttf tcation system (E!!s) codes are 16entified in the text as [XXI At 1642 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.24781e-4 months <br /> on-site review 90-5 was performed to review the actions involved with !
the GSEP unusual event. At 1648 hours0.0191 days <br />0.458 hours <br />0.00272 weeks <br />6.27064e-4 months <br />, the GF.P unusual event was terminated, the
- Unit One shutdown was stopped and the station began returning ventilation systems -
to normal operation.
C. APPARENT CAUSE OF EVENT.
This event is being reported in accordance with 10 CFR 50.73(a)(2)(1)(B): The licensee shall report any operation or condition prohibited by the plant's -
Technical Specifications.
The primary cause of this event has been attributed to a testing deficiency.
Contributing to the event are a number of minor air leaks which were identified during the test. ,
The test did not encompass temperature induced differences in the pressure gradients between the inside and outside of Secondary Containment. Thus, this temperature effect resulted in an apparent, but most likely not an actual loss of Secondary Containment capability.
The effects of a temperature difference between Secondary Containment and atmosphere are outlined in the Nuclear Regulatory Commission's (NRC) Information Notice No. 88-76: Recent Olscovery of a Phenomenon Not Previously Considered in the Design of Secondary Containment Pressure Control. When the temperature of the ,
atmospher(. is lower than the interior of the building, the difference in air density will create a pressure differential which changes with elevation.
i The test procedure requires the measurement of the building to atmosphere differential pressure at the 696' elevation, near the roof line. When the building temperature is higher than the outside tempere.ture, the differential pressure .
measured at this elevation can be considerably less than the differential pressure l at ground level, 595' elevation. A measured differential pressure with respect to atmosphere at the 696' elevation is more conservative than a differential pressure I based on an overall average of Reactor Building elevations.
When the GSEP unusual event was declared at 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br />, the building wat more than I 50 degrees Fahrenheit (*F) warmer than atmosphere. At this time the measured J differential pressure was 0.24 inches of water vacuum at the 696' elevation. !
Preliminary calculations performed by station Technical Staff indicated tnat the l average differential pressure of Secondary containment to atmosphere, compensated for temperature affects, was greater than 0.26 inches of water vacuum.
l Therefore, it is believed that Secondary Containment capability was intact throughout this event.
)
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i Lffluitt tVthT ktPQRT (LER) TEXT CONT 1kuATIDW Fora tev 2.o
? FACILITY NAME (1). D0cKET NuMetR (2) __ t[a uuMatt ist Pane 131 -
t Year / sequential Revision g//
/ Number //, Number
' m cities unit one o i s I o'l o I o 1 21 si 4 oIo - oIol2 - oI e of 4 or als ttxt Energy Inoustry Identification system (t!!s) codes are ioentified in the text as [XK) ,
Minor leaks were identified, temporarily sealed and left sealed until permanent repairs can be accomplished. These consisted of the Unit Two main steamline [ SEAL)
I seals and two feed water boots which were found to be degraded. These penetrations ,
connect the Main Steamline [SB) Isolation Valve (ISV) (MSIV) room, part of the Reactor building, and the High Pressure Heater (SB) Bay, part of the Turbine ,
o Building. Minor leaks were also left sealed on duct work access doors located in ,
the Drywell Torus Purge Fan [VB, FAN), Standby Gas Treatment, and MSIV room exhaust o systems [VA). These leaks are' thought to have had no significant impact on the '
l test results.
D.- SAFETY ANALYSIS OF EVENT:
L Technical Specification 4.7.C.I.c states Secondary containment capability to maintain an average 0.25 inches of water vacuum under calm wind conditions (2<uc5 cph) with a Standby Gas [BH) filter [FLT) train flow rate of not more than 4000 cfm shall be demonstrated at each refueling outage prior to refueling. Surveillance '
procedure QTS 160-5 is used to verify this requirement.
Technical Specification 3.7.C.1 states that in the event that Secondary Containment !
integrity cannot be maintained, procedures shall be initiated within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to .
place the units in a condition that does.not require Secondary Containment. These '
conditions require both units be subtritical, reactor water temperature be below 1
212*F and the reactor coolant systems vented, no activity be performed which can I reduce the shutdown margin below specified, and no movement of the fuel cask or
- irradiated fuel in the Reactor Building.
This event was of minimal safety significance because preliminary analysis of this event indicates that Secondary Containment was within the required Technical Specification limits at all times. The neasurement of the building differential ;
pressure at the high elevation of 696' is conservative. FSAR section 5.3.5 states that the reactor building to outside atmosphere average negative pressure be corrected for zero wind end zero differential temperature conditions. Additional '
conservatism was introduced by not correcting for zero differential temperature condition. Since the average differential pressure was 0.28 inches of water vacuum ,
at 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br />, there was no loss in capability to perform its design safety function of limiting a radiation release during a design basis accident.
E. CORRECTIVE ACTIONS:
f The minor leakage paths were identified, temporarily sealed, reviewed, and approved :
as satisfactory. They will be inspected on a weekly basis per on-site review 90-5 until permanent repairs are made.
The temperature effect phenomenon on Secondary containment will be further investigated under Action Item Record (AIR) 4-90-04. The Secondary containment ,
procedure. QTS 160-5, will be reviewed and revised to eliminate any deficiencies and incorporate the results of the temperature effect into this procedure (NTS 2542009001601).
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U t.1frutfr'EVtNT ttPORT fLER) TEYT CDNYtMAT10N Farm tav 2.0 [
FACILITY hAME (1) DOCKET NUMBER (2) Ltk NLSehrR fE) Paam (1) {
Year //
/ppjl ll seguential u m ar j/
/jl/
fjl Revision u'r I
. ' " etttet unit ans als!'IoIe121sia e eIo - eie12 . oI e el s or als TK5T Energy IndusVry toontification system (t!!s) cones are identified in the text as [xx]
'F. PREVIOUS EVENTS: ..
I There have been no previous events involving the failure of' Secondary Containment I
- i. testing at this station. As this event was no a component failure, a Nuclear Plant .
Reliability Data System (NPRDS) search was not performed.
l G. COMPONENT FAILURE DATA: i This event did'not involve any component failure. '
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