ML19350F055

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Monthly Operating Repts for May 1981
ML19350F055
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 06/01/1981
From: Harrison F
CAROLINA POWER & LIGHT CO.
To:
Shared Package
ML19350F054 List:
References
NUDOCS 8106240143
Download: ML19350F055 (10)


Text

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I APPENDIX'B ,

AVERAGE DAILY POWER. LEVEL DOCKET NO. 050-0325 UNIT BRUNSWICK UNIT 1 DATE 06/01/81 COMPLETED BY FRANCES HARRISur TELEPHONE 919-457-9521 MAY-~8I DAY AVG.' DAILY POWER LEVEL - D AY -- AVG. DAILY POWER LEVEL (MWE-NET) (MWE-NET) lc l7 -4 I -5.

2 -4 18 -5.

-3 -4. 19 -4.

4 -5. 20 -5.

5~ -4. 21- -5.

6 -5. -22 -5.

7 -5. 23 -5.

o- -5. 24. -4 V -4. ' 25 -5.

10 -5 . - 26 -4.

11 -4 27 -5.

12 -4 28 -5.

13 -4. 29 -4.

I4 -5. 30 -5.

15- -5. 31 -5.

16 -5.

1.16 - 8

!- 8106240l%

4-OPERATING DATA REPORT -

DOCKET NO. 050-0325 DATE 06/01/81 COMPLETED BY FRANCES HARRISq" TELEPHONE 919-45.7-9521 OPERATING STATUS

1. UNIT NAME: BRUNSWICK UNIT I I NOTES I
2. REPORTING PERIOD: MAY 81 I I
3. LICENSED THERMAL POWER (MNT): 2-436 I I
4. NAMEPLATE RATING (GROSS MWE): 867.0 I I
5. DESIGN ELECTRICAL RATING (NET MWE): 821.0 I I
6. MAX DEPENDABLE CAPACITY (GROSS MWE): 815.0 I I
7. MAX DEPENDABLE CAPACITY (NET MWE): 790.0
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS 3 THRU 7) SINCE LAST REPORT, GIVE REASOtlS:

V. POWER LEVEL TO WHICH RESTRICTED IF ANY (NET - MWE): f.IONE 10.' REASONS FOR RESTRICTION IF ANY:

THIS YR TO CUMUL

. MONTH DATE ATIVE II. HOURS IN REPORTING PERIOD 7 44 .0 3623.0 36864.0

12. NUMBER OF HOURS REACTOR WAS CRITICAL 0.0 2134.3 25936.4
13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 1647.1
14. HOURS GENERATOR ON LINE 0.0 2056.8 24438.7
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
16. CROSS THERMAL ENERGY GENERATED (M?lH) 0.0 3841575.6 49965308.5
17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 0.0 l 256185. 0 16581779.0 id. NET ELECTRICIAL ENERGY GENERATED (MWH) -3384.0 1203366.0 15950800.0
19. UNIT SERVICE FACTOR 0.0 56.8 66.3
20. UNIT AVAILABILITY FACTOR 0.0 56.8 66.3
21. UNIT CAPACITY FACTOR (USING MDC NET) -0.6 42.0 54.8
22. UNIT CAPACITY FACTOR (USI?:0 DER NET) -0.6 40.5 52.7
23. UNIT FCRCED OUTAGE RATE 100.0 31.1 l9.4
24. SHUTLOWNS SCHEDULED OVER NEXT 6 M3NTHS (TYPE, DATE, AND DURATION OF EACH)
25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF START UP: 6/20/81
26. UNITS IN TEST STATUS (PRIOR TO COMMERICIAL OPERATION): FORCAST ACHEIVED INITIAL CRITICALITY INITIAL ELECTRICITY ----

COMMERICIAL OPERATION ,

I.16 - 9 P00RDRGINAL l

- - - - . . . , , .~. ___ _

~ -

BRUNSWICK UNIT I 06/01/81 MAX HOURLY ELEC GEN 0.0 flVCLEAR BTUS 0.0 HEAT RATE 0.0 THERMAL GENERATION 0.0 EFFECTIVE FULL POWER DAYS 0.0 ELEC OUTPUT FACTOR 0.0 CIRC WATER INLET TEMP MAX / MIN 0.0/125.0 CIRC WATER OUTLET TEMP MAX /!(IN 0.0/125.0 AMB TEMP MAX / MIN / AVG 72.0/ 49.0/ 6I.6 m

i t'

- a x 4

APPENDIX B AVERAGE-DAILY POWER LEVEL DOCKET NO. 050-0324 UNIT BRUNSWICK UNIT 2

4. DATE 06/16/81 COMPLETED BY FRANCES HARRISON TELEPHONE 919-457-9521 MAY 81 DAY AVG. DAILY POWER LEVEL DAY AVG. DAILY POWER LEVEL (MWE-NET) (MWE-NET) 1 '750, 17 -10.

i 2 308. 18 -10.

3 31. 19 -11.

4 277. 20 -10.

-5 496. 21 -9.

6- 79. 22 -10.

7 -13. 23 -10.

8 -11. -

24 -11.

9 -11. 25 -11.

10 -11. 26 -11.

11 -11. 27 -10.

12 -11, 29 _1g, 13 -10. 29 -11.

14 -10. 30 -10.

15 -11. 31 -10.

16 -10.

f 1

9 1.16 - 8

300R DifGINAL

OPERATING DATA REPORT DOCKET NO. 050-0324 DATE 06/16/81 COMPLETED BY FRANCES HARRISON TELEPHONE 919-457-9521 GPERATING STATUS

1. UNIT NAME: BRUNSWICK UNIT 2 I NOTES I
2. REPORTING PERIOD:-MAY 81 I I I
3. LICENSED THERMAL POWER (MWT): 2436 I 4 '. NAME? LATE RATING (GROSS MWE): 867.0 I I
5. DESIGN ELEC1RICAL RATING (NET MWE): G21.0- I I
6. MAX DEPENDABLE CAPACITY-(GROSS MWE): 815.0 -------------------------------

I I

7. MAX DEPENDABLE CAPACITY (NET MWE): 790.0
8. IF CHANGES OCCUR IN CAPACITY RATINGS-(ITEMS 3 THRU 7) SINCE LAST REPORTr GIVE REASONS:
9. POWER LEVEL TO WHICH RESTRICTED IF ANY-(NET MWE): NONE
10. REASONS FOR RESTRICTION IF ANY:

THIS YR TO CUMUL MONTH DATE ATIVE 1~1. HOURS IN REPORTING PERIOD 744.0 3623.0 48888.0

12. NUMBER OF HOURS REACTOR WAS GRITICAL 125.7 1804.0 30826.3
13. REACTOR RESERVE SHUTDOWN. HOURS 0.0 0.0 0.0 14 HOURS GENERATOR ON LINE 104.7 1626.1 28590.3

-15. UNIT RESERVE SHUTDOWN HOURS -

0.0 0.0 0.0

-16. GROSS THERMAL ENERGY GENERATED (MWH) 147278.9 2637284.5 52248655.4

17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 49083.0 901740.0 17466186.0
18. NET ELECTRICIAL ENERGY GENERATED (MWH) 40297.0 852227.0- 16757456.0
19. UNIT SERVICE FACTOR 14.1 44.9 58.5
20. UNIT AVAILABILITY FACTOR 14.1 44.9 58.5
21. UNIT CAPACITY FACTOR (USING MDC NET) 6.9 29.8 43.4
22. UNIT CAPACITY FACTOR (USING DER NET) 6.6 28.7 41.8
23. UNIT FORCED OUTAGE RATE 85.9 52.6 17.2
24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPEr DATER AND DURATION OF EACH):

l

25. IF SHUTDCWN AT END OF REPORT PERIOD, ESTIMATED DATE OF START UP: 6/ 4/81
26. UNITS IN TEST STATUS (PRIOR TO COMMERICIAL OPERATION): FORCAST ACHEIVED r INITIAL CRITICALITY -------- --------

INITIAL ELECTRICITY -------- --------

i ,

, COMMERICIAL OPERATION -------- --------

l i 1.16 - 9

..s. - ,.

, - SRUNSWICK UNIT 2 06/16/81 s

[ MAX HOURLY ELEC GEN 775.0 NUCLEAR BTUS 0.5026630E+12 HEAT RATE 12474.0 THERMAL GENERATION 6136.6 EFFECTIVE FULL POWER DAYS 2.5 ELEC OUTPUT FACTOR 48.7

. CIRC WATER INLET TEMP MAX / MIN 81.0/ 69.0 CIRC WATER OUTLET TEMP MAX / MIN 85.0/ 68.0 .

AMB TEMP MAX / MIN / AVG 0.0/125.0/ 0.0 0

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P00R DRIBNAL

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. APPESTIX i

DOCKET NO: 050-0325 '

UNIT: Brunswick No.~1-

DATE
June 1981 COMPLETED BY: Frances Harrison OPERATIONS

SUMMARY

BRUNSWICK UNIT NO.1 I Brunswick Unit' No. I was off the line for the entire month of May for a planned- -

maintenance outage.

-There are 476 BWR and 160 PWR spent fuel bundles in the Brunswick Unit No.1 fuel pool.

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4 APPENDIX DOCIET NO: 050-0324 UNIT: Brunswick No. 2 DATE: June 1981 COMPLETED BY: - Frances Harrison OPERATIONS

SUMMARY

BRUNSWICK UNIT NO. 2 2

Brunswick Unit No. 2 operated'at a 14.1% availability factor for the month of May with a 6.9% capacity factor. There were two "off-11ae" outages this month,-

both are detailed in Appendix D, the unit shutdowns saa power reductions log.

There are 264 BWR-and 144 PWR spent fuel bundles its the Brunsw.'ck Unit No. 2 fuel-

.. pool .

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y 050-0324 ,

  • DOCKET NO. .

UNIT SilUIDOWNS AND POWER R8 DUCT 10NS UNIT N ANIE __ Brunswick No. 31:

DATE _ June 1981 g; CO5tPLETED BY Frnnr-on Harrino e

  • REPORT 510N111 May 1981 TELEPIIONE (414) 457-9521u C =
  • Cause & Currective S h ..? ; 5 r,

-, .$ i; 3yU Licensee Event  ;; ? E.U Action to O

g 3g 4 No. Date H $Ej $ Ji g5 Report 80 [3 Prevent Recurrence C" -

B32-F051 valve packing was leaking 2 21.00 A 2 N/A SF VAL'.7EX excessive 1y.81-015 81 05 03 ,

Tighten packing for minimal leakcge.

Repack valve during next outage. .

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3 4

2 Method: Exhibit G Instructions I for Prcparation of Data F: Forced Reamn:  ! 41anual A-1ilmpment railure(Explain) Entry Sheets for Licensee

-S: Scheduled 2 Manual Scrain. Event Report (LER) File (NUREG.

ll Mainiciunce oi Test

  • C Itcfuchng 4 Continuations 0161)

D Regulatory Restriction E-Operator Trainmg1 License Examination 5-Load Reductions 5 F Adminisiniive 6-Other Exhits: I Ssine Source

  • G-Operational Error (Explain) -

ll Other (Ewplain)

(9/77) t

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C 050-0324

. DOCKET NO.

Brunswick No. 2 ED UNIT SilUTDOWNS AND POWER REDUCTIONS UNIT N.OIE DATE June 1981 g .

i COMPLETED BY Frances. Harrison g REPORT MONTil May 1981 TELEPilONE (919) 457-9521 M

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C E

E Cause & Corrective 1

b

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, n? o3 Action to ME $ = E s'~' Event No. Date F-4 Report # N0 $U Prevent Recurrence

, $$ $ 3,e ih: u .

d .

SF HTEXCil Growth of oystero in the nuclear 1 618.3 A 3 N/A conventional service water system 81-016 81 05 06

  • restricted heat exchanger flow.

Shell growth was cleaned from the conventional aud nuclear system pipitig

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and components,

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I 2 Exhibit C Instructions

< 1 Method: for Preparation of Data I F: Ferced Resum: 14fanual A.I'qmpment Failure (Explain) , 24f anual Scrarn. Entry Sheels for Liecusec

! S: SeneJuled Esent Report (LER) File (NUREG.

  • n.Mainten.inee of Test 3 Automatic Scram.

C Itcfueling l 4 Continuations 01611 l ,

D Itegulatoi> ltestriction  ;

E Operator Training & License Examination 5-Load Reduccions 5 J ~

F Administrative t

6-Other Exhibit 1.Same Sousa *

' ' C Operational Error (Explains l llother (Explain) i (9/77)  !

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