ML19350F055
| ML19350F055 | |
| Person / Time | |
|---|---|
| Site: | Brunswick |
| Issue date: | 06/01/1981 |
| From: | Harrison F CAROLINA POWER & LIGHT CO. |
| To: | |
| Shared Package | |
| ML19350F054 | List: |
| References | |
| NUDOCS 8106240143 | |
| Download: ML19350F055 (10) | |
Text
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APPENDIX'B AVERAGE DAILY POWER. LEVEL DOCKET NO. 050-0325 UNIT BRUNSWICK UNIT 1 DATE 06/01/81 COMPLETED BY FRANCES HARRISur TELEPHONE 919-457-9521 MAY-~8I DAY AVG.' DAILY POWER LEVEL
- D AY --
AVG. DAILY POWER LEVEL (MWE-NET)
(MWE-NET) lc I
-5.
l7
-4 2
-4 18
-5.
-3
-4.
19
-4.
4
-5.
20
-5.
5~
-4.
21-
-5.
6
-5.
-22
-5.
7
-5.
23
-5.
o-
-5.
24.
-4 V
-4.
' 25
-5.
10
-5. -
26
-4.
11
-4 27
-5.
12
-4 28
-5.
13
-4.
29
-4.
I4
-5.
30
-5.
15-
-5.
31
-5.
16
-5.
1.16 - 8 8106240l%
4-OPERATING DATA REPORT -
DOCKET NO. 050-0325 DATE 06/01/81 COMPLETED BY FRANCES HARRISq" TELEPHONE 919-45.7-9521 OPERATING STATUS 1.
UNIT NAME: BRUNSWICK UNIT I I NOTES I
2.
REPORTING PERIOD: MAY 81 I
I
- 3. LICENSED THERMAL POWER (MNT): 2-436 I
I 4.
NAMEPLATE RATING (GROSS MWE): 867.0 I
I
- 5. DESIGN ELECTRICAL RATING (NET MWE): 821.0 I
I 6.
MAX DEPENDABLE CAPACITY (GROSS MWE): 815.0 I I
- 7. MAX DEPENDABLE CAPACITY (NET MWE): 790.0 8.
IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS 3 THRU 7) SINCE LAST REPORT, GIVE REASOtlS:
V.
POWER LEVEL TO WHICH RESTRICTED IF ANY (NET - MWE): f.IONE 10.' REASONS FOR RESTRICTION IF ANY:
THIS YR TO CUMUL MONTH DATE ATIVE II. HOURS IN REPORTING PERIOD 7 44.0 3623.0 36864.0
- 12. NUMBER OF HOURS REACTOR WAS CRITICAL 0.0 2134.3 25936.4
- 13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 1647.1
- 14. HOURS GENERATOR ON LINE 0.0 2056.8 24438.7
- 15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
- 16. CROSS THERMAL ENERGY GENERATED (M?lH) 0.0 3841575.6 49965308.5
- 17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 0.0 l 256185. 0 16581779.0 id. NET ELECTRICIAL ENERGY GENERATED (MWH)
-3384.0 1203366.0 15950800.0
- 19. UNIT SERVICE FACTOR 0.0 56.8 66.3
- 20. UNIT AVAILABILITY FACTOR 0.0 56.8 66.3
- 21. UNIT CAPACITY FACTOR (USING MDC NET)
-0.6 42.0 54.8
- 22. UNIT CAPACITY FACTOR (USI?:0 DER NET)
-0.6 40.5 52.7
- 23. UNIT FCRCED OUTAGE RATE 100.0 31.1 l9.4
- 24. SHUTLOWNS SCHEDULED OVER NEXT 6 M3NTHS (TYPE, DATE, AND DURATION OF EACH)
- 25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF START UP:
6/20/81
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERICIAL OPERATION): FORCAST ACHEIVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERICIAL OPERATION I.16 - 9 P00RDRGINAL
.~.
~
BRUNSWICK UNIT I 06/01/81 MAX HOURLY ELEC GEN 0.0 flVCLEAR BTUS 0.0 HEAT RATE 0.0 THERMAL GENERATION 0.0 EFFECTIVE FULL POWER DAYS 0.0 ELEC OUTPUT FACTOR 0.0 CIRC WATER INLET TEMP MAX / MIN 0.0/125.0 CIRC WATER OUTLET TEMP MAX /!(IN 0.0/125.0 AMB TEMP MAX / MIN / AVG 72.0/ 49.0/ 6I.6 m
i t' a
x 4
APPENDIX B AVERAGE-DAILY POWER LEVEL DOCKET NO. 050-0324 UNIT BRUNSWICK UNIT 2 4.
DATE 06/16/81 COMPLETED BY FRANCES HARRISON TELEPHONE 919-457-9521 MAY 81 DAY AVG. DAILY POWER LEVEL DAY AVG. DAILY POWER LEVEL (MWE-NET)
(MWE-NET) 1
'750, 17
-10.
2 308.
18
-10.
i 3
31.
19
-11.
4 277.
20
-10.
-5 496.
21
-9.
6-79.
22
-10.
7
-13.
23
-10.
8
-11.
24
-11.
9
-11.
25
-11.
10
-11.
26
-11.
11
-11.
27
-10.
12
-11, 29
- _1g, 13
-10.
29
-11.
14
-10.
30
-10.
15
-11.
31
-10.
16
-10.
f 1
9 1.16 - 8 300R DifGINAL
OPERATING DATA REPORT DOCKET NO. 050-0324 DATE 06/16/81 COMPLETED BY FRANCES HARRISON TELEPHONE 919-457-9521 GPERATING STATUS
- 1. UNIT NAME: BRUNSWICK UNIT 2 I NOTES I
- 2. REPORTING PERIOD:-MAY 81 I
I
- 3. LICENSED THERMAL POWER (MWT): 2436 I
I 4 '. NAME? LATE RATING (GROSS MWE): 867.0 I
I
- 5. DESIGN ELEC1RICAL RATING (NET MWE): G21.0- I I
- 6. MAX DEPENDABLE CAPACITY-(GROSS MWE): 815.0 I I
- 7. MAX DEPENDABLE CAPACITY (NET MWE): 790.0 8.
IF CHANGES OCCUR IN CAPACITY RATINGS-(ITEMS 3 THRU 7) SINCE LAST REPORTr GIVE REASONS:
- 9. POWER LEVEL TO WHICH RESTRICTED IF ANY-(NET MWE): NONE
- 10. REASONS FOR RESTRICTION IF ANY:
THIS YR TO CUMUL MONTH DATE ATIVE 1~1. HOURS IN REPORTING PERIOD 744.0 3623.0 48888.0
- 12. NUMBER OF HOURS REACTOR WAS GRITICAL 125.7 1804.0 30826.3
- 13. REACTOR RESERVE SHUTDOWN. HOURS 0.0 0.0 0.0 14 HOURS GENERATOR ON LINE 104.7 1626.1 28590.3 0.0 0.0 0.0
-15. UNIT RESERVE SHUTDOWN HOURS
-16. GROSS THERMAL ENERGY GENERATED (MWH) 147278.9 2637284.5 52248655.4
- 17. GROSS ELECTRICAL ENERGY GENERATED (MWH) 49083.0 901740.0 17466186.0
- 18. NET ELECTRICIAL ENERGY GENERATED (MWH) 40297.0 852227.0- 16757456.0
- 19. UNIT SERVICE FACTOR 14.1 44.9 58.5
- 20. UNIT AVAILABILITY FACTOR 14.1 44.9 58.5
- 21. UNIT CAPACITY FACTOR (USING MDC NET) 6.9 29.8 43.4
- 22. UNIT CAPACITY FACTOR (USING DER NET) 6.6 28.7 41.8
- 23. UNIT FORCED OUTAGE RATE 85.9 52.6 17.2
- 24. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPEr DATER AND DURATION OF EACH):
l
- 25. IF SHUTDCWN AT END OF REPORT PERIOD, ESTIMATED DATE OF START UP:
6/ 4/81
- 26. UNITS IN TEST STATUS (PRIOR TO COMMERICIAL OPERATION): FORCAST ACHEIVED r
INITIAL CRITICALITY INITIAL ELECTRICITY i
COMMERICIAL OPERATION l
i 1.16 - 9
..s.
- SRUNSWICK UNIT 2 06/16/81 s
[
MAX HOURLY ELEC GEN 775.0 NUCLEAR BTUS 0.5026630E+12 HEAT RATE 12474.0 THERMAL GENERATION 6136.6 EFFECTIVE FULL POWER DAYS 2.5 ELEC OUTPUT FACTOR 48.7
. CIRC WATER INLET TEMP MAX / MIN 81.0/ 69.0 CIRC WATER OUTLET TEMP MAX / MIN 85.0/ 68.0 AMB TEMP MAX / MIN / AVG 0.0/125.0/
0.0 0
e e.
4 1
P00R DRIBNAL
- a J.
APPESTIX i
DOCKET NO: 050-0325 UNIT: Brunswick No.~1-DATE: June 1981 COMPLETED BY: Frances Harrison OPERATIONS
SUMMARY
BRUNSWICK UNIT NO.1 I
Brunswick Unit' No. I was off the line for the entire month of May for a planned-maintenance outage.
-There are 476 BWR and 160 PWR spent fuel bundles in the Brunswick Unit No.1 fuel pool.
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4 APPENDIX DOCIET NO: 050-0324 UNIT: Brunswick No. 2 DATE: June 1981 COMPLETED BY: - Frances Harrison OPERATIONS
SUMMARY
BRUNSWICK UNIT NO. 2 2
Brunswick Unit No. 2 operated'at a 14.1% availability factor for the month of May with a 6.9% capacity factor. There were two "off-11ae" outages this month,-
both are detailed in Appendix D, the unit shutdowns saa power reductions log.
There are 264 BWR-and 144 PWR spent fuel bundles its the Brunsw.'ck Unit No. 2 fuel-
.. pool.
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050-0324 y
DOCKET NO.
UNIT SilUIDOWNS AND POWER R8 DUCT 10NS UNIT N ANIE __ Brunswick No. 31:
DATE _ June 1981 g;
Frnnr-on Harrino e
- CO5tPLETED BY 457-9521 C =
REPORT 510N111 May 1981 TELEPIIONE (414) u Cause & Currective h.. ;
?
Licensee 5 r,
.$ i; S
E.
Action to O
[3 No.
Date g
3g 4
3yU Event
- ?
U Prevent Recurrence 80 H
$Ej Ji g5 Report C"
B32-F051 valve packing was leaking 81-015 81 05 03 2
21.00 A
2 N/A SF VAL'.7EX excessive 1y.
Tighten packing for minimal leakcge.
Repack valve during next outage.
<o I
4 3
Exhibit G Instructions I
2 Method:
F: Forced Reamn:
! 41anual for Prcparation of Data
-S: Scheduled A-1ilmpment railure(Explain) 2 Manual Scrain.
Entry Sheets for Licensee Event Report (LER) File (NUREG.
ll Mainiciunce oi Test 3 Autornatic Scram.
C Itcfuchng 4 Continuations 0161)
D Regulatory Restriction E-Operator Trainmg1 License Examination 5-Load Reductions 5
F Adminisiniive 6-Other Exhits: I Ssine Source G-Operational Error (Explain)
(9/77) ll Other (Ewplain) t
f.
O' O
Q O
W.
y=
C i
050-0324 DOCKET NO.
ED Brunswick No. 2 UNIT SilUTDOWNS AND POWER REDUCTIONS UNIT N.OIE DATE June 1981 g
COMPLETED BY Frances. Harrison g i
REPORT MONTil May 1981 TELEPilONE (919) 457-9521 M
O r
C E
1 E
Cause & Corrective
.$g 3
j I'i Licensee E r, b
No.
Date F-ME
= E s'~'
Event n?
o3 Action to N0
$U Prevent Recurrence 4
3,e ih Report #
u d
SF HTEXCil Growth of oystero in the nuclear 81-016 81 05 06 1
618.3 A
3 N/A conventional service water system restricted heat exchanger flow.
Shell growth was cleaned from the conventional aud nuclear system pipitig
~
and components,
~
i
-s r a t
1 i
b
=
t I
4 I
3 Exhibit C Instructions 1
2 Method:
I F: Ferced Resum:
14fanual for Preparation of Data S: SeneJuled A.I'qmpment Failure (Explain)
, 24f anual Scrarn.
Entry Sheels for Liecusec Esent Report (LER) File (NUREG.
n.Mainten.inee of Test 3 Automatic Scram.
C Itcfueling l
4 Continuations 01611 l
D Itegulatoi> ltestriction J
E Operator Training & License Examination 5-Load Reduccions 5
t 6-Other Exhibit 1.Same Sousa
~
F Administrative C Operational Error (Explains l
(9/77) llother (Explain) i l