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{{#Wiki_filter:,2+**ti September 1, 2011EA-11-174Mr. Robert G. SmithSite Vice PresidentEntergy Nuclear Operations, Inc.Pilgrim Nuclear Power Station600 Rocky Hill RoadPlymouth, MA 02360-5508PILGRIM NUCLEAR POWER STATION . NRC SPECIAL INSPECTIONREPORT 05000293/2011012: PRELIMINARY WHITE FINDING
{{#Wiki_filter:,2+**ti UNITED STATES N UCLEAR REGU LATORY COMM ISSION REGION I 475 ALLENDALE ROAD KING OF PRUSSIA. PENNSYLVANIA 19406-1415 September 1, 2011 EA-11-174 Mr. Robert Site Vice President Entergy Nuclear Operations, Inc.Pilgrim Nuclear Power Station 600 Rocky Hill Road Plymouth, MA 02360-5508 PILGRIM NUCLEAR POWER STATION . NRC SPECIAL INSPECTION REPORT 05000293/2011012:
PRELIMINARY WHITE FINDING


==Dear Mr. Smith:==
==Dear Mr. Smith:==
On July 2Q,2011, the U.S. Nuclear Regulatory Commission (NRC) completed a SpecialInspection at your Pilgrim Nuclear Power Station (PNPS). The inspection was conducted inresponse to the May 10,2011, reactor scram event that occurred due to an unrecognizedsubcriticality and subsequent unrecognized return to criticality. The NRC's initial evaluation ofthis event satisfied the criteria in NRC Inspection Manual Chapter (lMC) 0309, "Reactivelnspection Decision Basis for Reactors," for conducting a Special Inspection. The SpecialInspection Team (SlT) Charter (Attachment 2 of the enclosed report) provides the basis andadditional details concerning the scope of the inspection. The enclosed inspection reportdocuments the inspection results, which were discussed at the exit meeting on July 20,2011,with you and other members of your staff.The inspection team examined activities conducted under your license as they relate to safetyand compliance with Commission rules and regulations and with the conditions of your license.The inspection team reviewed selected procedures and records, observed activities, andinterviewed personnel. In particular, the inspection team reviewed event evaluations, causalinvestigations, relevant performance history, and extent of condition to assess the significanceand potential consequences of issues related to the May 10 event.The inspection team concluded that the plant operated within acceptable power limits, and noequipment malfunctioned during the power transient and subsequent reactor scram.Nonetheless, the inspection team identified several issues related to human performance andcompliance with conduct of operations and reactivity control standards and procedures thatcontributed to the event. The enclosed chronology (Attachment 3 of the enclosed report)provides additional details regarding the sequence of events.
On July 2Q,2011, the U.S. Nuclear Regulatory Commission (NRC) completed a Special Inspection at your Pilgrim Nuclear Power Station (PNPS). The inspection was conducted in response to the May 10,2011, reactor scram event that occurred due to an unrecognized subcriticality and subsequent unrecognized return to criticality.


R, Smith 2This report documents one finding that, using the reactor safety Significance DeterminationProcess (SDP), has preliminarily been determined to be White, or of low to moderate safetysignificance. The finding involves the failure of Pilgrim personnel to implement conduct ofoperations and reactivity control standards and procedures during a reactor startup, whichcontributed to an unrecognized subcriticality followed by an unrecognized return to criticality andsubseq uent reactor scram.This finding was assessed using NRC IMC 0609, Appendix M, "Significance DeterminationProcess Using Qualitative Criteria," because probabilistic risk assessment tools were not wellsuited to evaluate the multiple human performance errors associated with this issue.Preliminarily, the NRC has determined this finding to be of low to moderate safety significancebased on a qualitative assessment. There was no significant impact on the plant following thetransient because the event itself did not result in power exceeding license limits or fueldamage. Additionally, interim corrective actions were taken, which included removing thePilgrim control room personnel involved in the event from operational duties pendingremediation, providing additional training for operators not involved with the event, and providingincreased management oversight presence in the Pilgrim control room while long termcorrective actions were developed.The finding involved one apparent violation (AV) of NRC requirements regarding TechnicalSpecification 5.4, "Procedures," that is being considered for escalated enforcement action inaccordance with the NRC's Enforcement Policy, which can be found on NRC's website athttp://www. nrc.qov/read inq-rom/doc-col lections/enforcemenU.ln accordance with NRC IMC 0609, we will complete our evaluation using the best availableinformation and issue our final determination of safety significance within 90 days of the date ofthis letter. The SDP encourages an open dialogue between the NRC staff and the licensee;however, the dialogue should not impact the timeliness of the staff's final determination. Beforewe make a final decision on this matter, we are providing you with an opportunity to (1) attend aRegulatory Conference where you can present to the NRC your perspective on the facts andassumptions the NRC used to arrive at the finding and assess its significance, or (2) submityour position on the finding to the NRC in writing. lf you request a Regulatory Conference, itshould be held within 30 days of your response to this letter, and we encourage you to submitsupporting documentation at least one week prior to the conference in an effort to make theconference more efficient and effective. lf a Regulatory Conference is held, it will be open forpublic observation. lf you decide to submit only a written response, such submittal should besent to the NRC within 30 days of your receipt of this letter. lf you decline to request aRegulatory Conference or submit a written response, you relinquish your right to appeal the finalSDP determination, in that by not doing either, you fail to meet the appeal requirements statedin the Prerequisite and Limitation Sections of Attachment 2 of IMC 0609.Please contact Mr. Donald E. Jackson by telephone at (610) 337-5306 within 10 days from theissue date of this letter to notify the NRC of your intentions. lf we have not heard from youwithin 10 days, we will continue with our significance determination and enforcement decision.The final resolution of this matter will be conveyed in separate correspondence. Because the NRC has not made a final determination in this matter, no Notice of Violation isbeing issued for this inspection finding at this time. Please be advised that the number andcharacterization of the apparent violation described in the enclosed inspection report maychange as a result of further NRC review.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room and from the Publicly Available Records (PARS) component ofNRC's document system, Agencywide Documents Access and Management System (ADAMS),ADAMS is accessible from the NRC Website at http://www.nrc.qov/readinq-rm/adams.html (thePublic Electronic Reading Room).Division of Reactor SafetyDocket No. 50-293License No. DPR-35
The NRC's initial evaluation of this event satisfied the criteria in NRC Inspection Manual Chapter (lMC) 0309, "Reactive lnspection Decision Basis for Reactors," for conducting a Special Inspection.
 
The Special Inspection Team (SlT) Charter (Attachment 2 of the enclosed report) provides the basis and additional details concerning the scope of the inspection.
 
The enclosed inspection report documents the inspection results, which were discussed at the exit meeting on July 20,2011, with you and other members of your staff.The inspection team examined activities conducted under your license as they relate to safety and compliance with Commission rules and regulations and with the conditions of your license.The inspection team reviewed selected procedures and records, observed activities, and interviewed personnel.
 
In particular, the inspection team reviewed event evaluations, causal investigations, relevant performance history, and extent of condition to assess the significance and potential consequences of issues related to the May 10 event.The inspection team concluded that the plant operated within acceptable power limits, and no equipment malfunctioned during the power transient and subsequent reactor scram.Nonetheless, the inspection team identified several issues related to human performance and compliance with conduct of operations and reactivity control standards and procedures that contributed to the event. The enclosed chronology (Attachment 3 of the enclosed report)provides additional details regarding the sequence of events.
 
R, Smith 2 This report documents one finding that, using the reactor safety Significance Determination Process (SDP), has preliminarily been determined to be White, or of low to moderate safety significance.
 
The finding involves the failure of Pilgrim personnel to implement conduct of operations and reactivity control standards and procedures during a reactor startup, which contributed to an unrecognized subcriticality followed by an unrecognized return to criticality and subseq uent reactor scram.This finding was assessed using NRC IMC 0609, Appendix M, "Significance Determination Process Using Qualitative Criteria," because probabilistic risk assessment tools were not well suited to evaluate the multiple human performance errors associated with this issue.Preliminarily, the NRC has determined this finding to be of low to moderate safety significance based on a qualitative assessment.
 
There was no significant impact on the plant following the transient because the event itself did not result in power exceeding license limits or fuel damage. Additionally, interim corrective actions were taken, which included removing the Pilgrim control room personnel involved in the event from operational duties pending remediation, providing additional training for operators not involved with the event, and providing increased management oversight presence in the Pilgrim control room while long term corrective actions were developed.
 
The finding involved one apparent violation (AV) of NRC requirements regarding Technical Specification 5.4, "Procedures," that is being considered for escalated enforcement action in accordance with the NRC's Enforcement Policy, which can be found on NRC's website at http://www.
 
nrc.qov/read inq-rom/doc-col lections/enforcemenU.
 
ln accordance with NRC IMC 0609, we will complete our evaluation using the best available information and issue our final determination of safety significance within 90 days of the date of this letter. The SDP encourages an open dialogue between the NRC staff and the licensee;however, the dialogue should not impact the timeliness of the staff's final determination.
 
Before we make a final decision on this matter, we are providing you with an opportunity to (1) attend a Regulatory Conference where you can present to the NRC your perspective on the facts and assumptions the NRC used to arrive at the finding and assess its significance, or (2) submit your position on the finding to the NRC in writing. lf you request a Regulatory Conference, it should be held within 30 days of your response to this letter, and we encourage you to submit supporting documentation at least one week prior to the conference in an effort to make the conference more efficient and effective.
 
lf a Regulatory Conference is held, it will be open for public observation.
 
lf you decide to submit only a written response, such submittal should be sent to the NRC within 30 days of your receipt of this letter. lf you decline to request a Regulatory Conference or submit a written response, you relinquish your right to appeal the final SDP determination, in that by not doing either, you fail to meet the appeal requirements stated in the Prerequisite and Limitation Sections of Attachment 2 of IMC 0609.Please contact Mr. Donald E. Jackson by telephone at (610) 337-5306 within 10 days from the issue date of this letter to notify the NRC of your intentions.
 
lf we have not heard from you within 10 days, we will continue with our significance determination and enforcement decision.The final resolution of this matter will be conveyed in separate correspondence. Because the NRC has not made a final determination in this matter, no Notice of Violation is being issued for this inspection finding at this time. Please be advised that the number and characterization of the apparent violation described in the enclosed inspection report may change as a result of further NRC review.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room and from the Publicly Available Records (PARS) component of NRC's document system, Agencywide Documents Access and Management System (ADAMS), ADAMS is accessible from the NRC Website at http://www.nrc.qov/readinq-rm/adams.html (the Public Electronic Reading Room).Division of Reactor Safety Docket No. 50-293 License No. DPR-35  


===Enclosure:===
===Enclosure:===
Inspection Report 05000293/201 1012
Inspection Report 05000293/201 1012  


===w/Attachments:===
===w/Attachments:===
Supplemental Information (Attachment 1 )Special Inspection Team Charter (Attachment 2)Detailed Sequence of Events (Attachment 3)Appendix M Table 4.1 (Attachment 4)cc w/encl: Distribution via ListServ
Supplemental Information (Attachment 1 )Special Inspection Team Charter (Attachment 2)Detailed Sequence of Events (Attachment 3)Appendix M Table 4.1 (Attachment 4)cc w/encl: Distribution via ListServ  


Sincerely,&
Sincerely,&
R, SmithBecause the NRC has not made a final determination in this matter, no Notice of Violation isbeing issued for this inspection finding at this time. Please be advised that the number andcharacterization of the apparent violation described in the enclosed inspection report maychange as a result of further NRC review.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room and from the Publicly Available Records (PARS) component ofNRC's document system, Agencywide Documents Access and Management System (ADAMS).ADAMS is accessible from the NRC Website at http://www.nrc.qov/readinq-rm/adams.html (thePublic Electronic Reading Room).
R, Smith Because the NRC has not made a final determination in this matter, no Notice of Violation is being issued for this inspection finding at this time. Please be advised that the number and characterization of the apparent violation described in the enclosed inspection report may change as a result of further NRC review.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room and from the Publicly Available Records (PARS) component of NRC's document system, Agencywide Documents Access and Management System (ADAMS).ADAMS is accessible from the NRC Website at http://www.nrc.qov/readinq-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/Christopher G. Miller, DirectorDivision of Reactor SafetyDocket No. 50-293License No. DPR-35
Sincerely,/RA/Christopher G. Miller, Director Division of Reactor Safety Docket No. 50-293 License No. DPR-35  


===Enclosure:===
===Enclosure:===
lnspection Report 05000293/201 1012
lnspection Report 05000293/201 1012  


===w/Attachments:===
===w/Attachments:===
Supplemental Information (Attachment 1 )Special Inspection Team Charter (Attachment 2)Detailed Sequence of Events (Attachment 3)Appendix M Table 4.1 (Attachment 4)cc w/encl: Distribution via ListServDistribution: See next pageSUNSI Review Complete: rrm* (Reviewer's Initials)DOCUMENT NAME: G:\DRS\Operations Branch\M0KINLE\lPilgrim SIT June 20'11\lnspection Report Drafts\Pilgrim SIT Concurrence\Pilgrim2011 SIT Report Final.docxAfter declaring this document "An Official Agency Record" it will be released to the Public.MLI12440't00To teceivs a coov of this documGnt. indicate in the box: "C" = CoDy without attachmenvenclosure "E" = Copy with attachmenvenclosure 'N" = NoOFFICE RIiDRSRI/DRSRI/ORARI/DRPRI/DRPNAME RMcKinley/rrm*Prior concurrenceDJackson/dej*Prior concurrenceDHolody/aed for*Prior concurrenceRBellamy/tcs for*Prior concurrenceDRoberts/djr-Prior concurrenceDATE 08t19t1108t19t1108t19t1108/ t1108/30/1 1OFFICE RI/DRSNAME CMiller/cgmDATE 08131111OFFICIAL RECORD COPY Docket No.:License No.:Report No,:Licensee:Facility:Location:Dates:Team Leader:Team:Approved By:U. S. NUCLEAR REGULATORY COMMISSIONREGION I50-293DPR-3505000293/2011012Entergy Nuclear Operations, IncPilgrim Nuclear Power Station (PNPS)600 Rocky Hill RoadPlymouth, MA 02360May 16 through July 20,2011R. McKinley, Senior Emergency Response CoordinatorDivision of Reactor SafetyB. Haagensen, Resident Inspector, Division of Reactor ProjectsD. Molteni, Operations Engineer, Division of Reactor SafetyDonald E. Jackson, ChiefOperations BranchDivision of Reactor SafetyEnclosure
Supplemental Information (Attachment 1 )Special Inspection Team Charter (Attachment 2)Detailed Sequence of Events (Attachment 3)Appendix M Table 4.1 (Attachment 4)cc w/encl: Distribution via ListServ Distribution:
See next page SUNSI Review Complete:
rrm* (Reviewer's Initials)DOCUMENT NAME: G:\DRS\Operations Branch\M0KINLE\lPilgrim SIT June 20'11\lnspection Report Drafts\Pilgrim SIT Concurrence\Pilgrim 2011 SIT Report Final.docx After declaring this document "An Official Agency Record" it will be released to the Public.MLI12440't00 To teceivs a coov of this documGnt.
 
indicate in the box: "C" = CoDy without attachmenvenclosure "E" = Copy with attachmenvenclosure  
'N" = No OFFICE RIiDRS RI/DRS RI/ORA RI/DRP RI/DRP NAME RMcKinley/rrm*
Prior concurrence DJackson/dej*
Prior concurrence DHolody/aed for*Prior concurrence RBellamy/tcs for*Prior concurrence DRoberts/djr-
Prior concurrence DATE 08t19t11 08t19t11 08t19t11 08/ t11 08/30/1 1 OFFICE RI/DRS NAME CMiller/cgm DATE 08131111 OFFICIAL RECORD COPY Docket No.: License No.: Report No,: Licensee: Facility: Location: Dates: Team Leader: Team: Approved By: U. S. NUCLEAR REGULATORY COMMISSION REGION I 50-293 DPR-35 05000293/2011012 Entergy Nuclear Operations, Inc Pilgrim Nuclear Power Station (PNPS)600 Rocky Hill Road Plymouth, MA 02360 May 16 through July 20,2011 R. McKinley, Senior Emergency Response Coordinator Division of Reactor Safety B. Haagensen, Resident Inspector, Division of Reactor Projects D. Molteni, Operations Engineer, Division of Reactor Safety Donald E. Jackson, Chief Operations Branch Division of Reactor Safety Enclosure


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
lR 0500029312011012; 0511612011 - 071201201 1; Pilgrim Nuclear Power Station (PNPS);lnspection Procedure 93812, Special Inspection.A three-person NRC team, comprised of two regional inspectors and one resident inspector,conducted this Special lnspection. One finding with potentialfor greater than Green safetysignificance was identified. The significance of most findings is indicated by their color (Green,White, Yellow, or Red) using lnspection Manual Chapter (lMC) 0609, "SignificanceDetermination Process" (SDP). The cross-cutting aspect was determined using IMC 0310,"Components Within the Cross-Cutting Areas." Findings for which the SDP does not apply maybe Green or be assigned a severity level after NRC management review. The NRC's programfor overseeing the safe operation of commercial nuclear power reactors is described inNUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.NRC ldentified and Self Revealing Findings
lR 0500029312011012; 0511612011 - 071201201 1; Pilgrim Nuclear Power Station (PNPS);lnspection Procedure 93812, Special Inspection.
 
A three-person NRC team, comprised of two regional inspectors and one resident inspector, conducted this Special lnspection.
 
One finding with potentialfor greater than Green safety significance was identified.
 
The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using lnspection Manual Chapter (lMC) 0609, "Significance Determination Process" (SDP). The cross-cutting aspect was determined using IMC 0310,"Components Within the Cross-Cutting Areas." Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.NRC ldentified and Self Revealing Findings  
 
===Cornerstone: Initiating===
 
Events. Preliminary White: A self-revealing finding was identified involving the failure of Pilgrim personnel to implement conduct of operations and reactivity control standards and procedures during a reactor startup, which contributed to an unrecognized subcriticality followed by an unrecognized return to criticality and subsequent reactor scram.The significance of the finding has preliminarily been determined to be White, or of low to moderate safety significance.
 
The finding is also associated with one apparent violation of NRC requirements specified by Technical Specification 5.4, "Procedures." There was no significant impact on the plant following the transient because the event itself did not result in power exceeding license limits or fuel damage. Additionally, interim corrective actions were taken, which included removing the Pilgrim control room personnel involved in the event from operational duties pending remediation, providing additional training for operators not involved with the event, and providing increased management oversight presence in the Pilgrim control room while long term corrective actions were developed.
 
Entergy staff entered this issue, including the evaluation of extent of condition, into its corrective action program (CR-PNP-2011-2475)and performed a Root Cause Evaluation (RcE).The finding is more than minor because it was associated with the Human Performance attribute of the Initiating Events cornerstone and affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during power operations.
 
Specifically, the failure of Pilgrim personnel to effectively implement conduct of operations and reactivity control standards and procedures during a reactor startup caused an unrecognized subcriticality followed by an unrecognized return to criticality and subsequent reactor scram. Because the finding primarily involved multiple human performance errors, probabilistic risk assessment tools were not well suited for evaluating its significance.
 
The inspection team determined that the criteria for using IMC 0609, Appendix.M, "Significance Determination Process Using lll
 
Qualitative Criteria," were met, and the finding was evaluated using this guidance, as described in Attachment to this report. Based on the qualitative review of this finding, the NRC has preliminarily concluded that the finding was of low to moderate safety significance (preliminary White).The inspection team determined that multiple factors contributed to this performance deficiency, including:
inadequate enforcement of operating standards, failure to follow procedures, and ineffective operator training.
 
The Entergy RCE determined that the primary cause was a failure to adhere to established Entergy standards and expectations due to a lack of consistent supervisory and management enforcement.


===Cornerstone: Initiating Events. Preliminary ===
The inspection team concluded that the finding had a cross-cutting aspect in the Human Performance cross-cutting area, Work Practices component, because Entergy did not adequately enforce human error prevention techniques, such as procedural adherence, holding pre-job briefs, self and peer checking, and proper documentation of activities during a reactor startup, which is a risk significant evolution.
White: A self-revealing finding was identified involving the failure of Pilgrimpersonnel to implement conduct of operations and reactivity control standards andprocedures during a reactor startup, which contributed to an unrecognized subcriticalityfollowed by an unrecognized return to criticality and subsequent reactor scram.The significance of the finding has preliminarily been determined to be White, or of low tomoderate safety significance. The finding is also associated with one apparent violationof NRC requirements specified by Technical Specification 5.4, "Procedures." There wasno significant impact on the plant following the transient because the event itself did notresult in power exceeding license limits or fuel damage. Additionally, interim correctiveactions were taken, which included removing the Pilgrim control room personnel involvedin the event from operational duties pending remediation, providing additional training foroperators not involved with the event, and providing increased management oversightpresence in the Pilgrim control room while long term corrective actions were developed.Entergy staff entered this issue, including the evaluation of extent of condition, into itscorrective action program (CR-PNP-2011-2475) and performed a Root Cause Evaluation(RcE).The finding is more than minor because it was associated with the Human Performanceattribute of the Initiating Events cornerstone and affected the cornerstone objective oflimiting the likelihood of those events that upset plant stability and challenge criticalsafety functions during power operations. Specifically, the failure of Pilgrim personnel toeffectively implement conduct of operations and reactivity control standards andprocedures during a reactor startup caused an unrecognized subcriticality followed by anunrecognized return to criticality and subsequent reactor scram. Because the findingprimarily involved multiple human performance errors, probabilistic risk assessment toolswere not well suited for evaluating its significance. The inspection team determined thatthe criteria for using IMC 0609, Appendix.M, "Significance Determination Process Usinglll


Qualitative Criteria," were met, and the finding was evaluated using this guidance, asdescribed in Attachment 4 to this report. Based on the qualitative review of this finding,the NRC has preliminarily concluded that the finding was of low to moderate safetysignificance (preliminary White).The inspection team determined that multiple factors contributed to this performancedeficiency, including: inadequate enforcement of operating standards, failure to followprocedures, and ineffective operator training. The Entergy RCE determined that theprimary cause was a failure to adhere to established Entergy standards andexpectations due to a lack of consistent supervisory and management enforcement. Theinspection team concluded that the finding had a cross-cutting aspect in the HumanPerformance cross-cutting area, Work Practices component, because Entergy did notadequately enforce human error prevention techniques, such as procedural adherence,holding pre-job briefs, self and peer checking, and proper documentation of activitiesduring a reactor startup, which is a risk significant evolution. Additionally, licensedpersonnel did not effectively implement the human performance prevention techniquesmentioned above, and they proceeded when they encountered unceftainty andunexpected circumstances during the reactor startup [H.4(a)]. (Section 2)ivEnclosure 1.
Additionally, licensed personnel did not effectively implement the human performance prevention techniques mentioned above, and they proceeded when they encountered unceftainty and unexpected circumstances during the reactor startup [H.4(a)]. (Section 2)iv
 
1.


=REPORT DETAILS=
=REPORT DETAILS=
Backoround and Description of EventIn accordance with the Special Inspection Team (SlT) Charter (Attachment 2), theinspection team conducted a detailed review of the May 10, 2011, reactor scram event atPilgrim Nuclear Power Station, including a review of the Pilgrim operators' response tothe event. The inspection team gathered information from the plant process computer(PPC) alarm printouts and parameter trends, interviewed station personnel, observed on-going control room activities, and reviewed procedures, logs, and various technicaldocuments to develop a detailed timeline of the event (Attachment 3).On May 10,2011, following a refueling outage, the reactor mode switch was taken tostartup at 0626, and control rod withdrawal commenced at 0641. The control room crewconsisted of the following personnel (additional licensed operators were present in thecontrol room conducting various startup related activities):o Assistant Operations Manager (AOM-Shift) - Senior Line Management oversightr Shift Manager (SM)- management oversight. Reactivity Senior Reactor Operator (SRO/Control Room Supervisor (CRS) -command and controlo Assistant Control Room Supervisor (ACRS). Reactor Operator At-The-Controls (RO-ATC)o Reactor Operator (Verifier)
Backoround and Description of Event In accordance with the Special Inspection Team (SlT) Charter (Attachment 2), the inspection team conducted a detailed review of the May 10, 2011, reactor scram event at Pilgrim Nuclear Power Station, including a review of the Pilgrim operators' response to the event. The inspection team gathered information from the plant process computer (PPC) alarm printouts and parameter trends, interviewed station personnel, observed on-going control room activities, and reviewed procedures, logs, and various technical documents to develop a detailed timeline of the event (Attachment 3).On May 10,2011, following a refueling outage, the reactor mode switch was taken to startup at 0626, and control rod withdrawal commenced at 0641. The control room crew consisted of the following personnel (additional licensed operators were present in the control room conducting various startup related activities):
* ATC verifierr Reactor Engineer (RE). RE in TrainingAt 1212, the reactor was made critical when control rod 38-19 was moved to position 12.Power continued to rise to the point of adding heat (POAH), and the POAH wasachieved at 1227. Once the POAH was achieved, the RO-ATC operator inserted rod38-19 to position 10 to obtain lntermediate Range Monitor (lRM) overlap correlationdata. Following the data collection, the RO-ATC operator withdrew rod 38-19 back toposition 12.At approximately 1231, the Reactivity SRO/CRS and the RO-ATC operator wererelieved by other licensed operators who continued with plant startup. The crewwithdrew control rods to establish a moderator heat-up rate. The RO-ATC operatorwithdrew control rods 14-35, 38-35 , 14-19 and 22-43 from position 08 to 12 withoutincident.The RO-ATC operator continued with the rod withdrawal sequence and tried to withdrawcontrol rod 30-11 from position 08 to 12, but the control rod would not move usingnormal notch withdraw commands. The RO-ATC then attempted to withdraw control rod30-11 using a "double-clutch" maneuver in accordance with procedures; however, thecontrol rod inadvertently inserted and settled at position 06. As stated during interviewswith the NRC inspectors, the RO-ATC operator, the ATC verifier, and the ReactivitySRO/CRS all saw the control rod in the incorrect position. However, the operators didnot enter and follow Pilgrim Nuclear Power Station (PNPS) Procedure 2.4.11, "ControlRod Positioning Malfunctions" as required. This procedure required the operators toassess the amount of the mispositioning to determine the appropriate course of remedial 2action before proceeding, and it also required the issue to be documented in a conditionreport. The operators did not perform an assessment, and they moved the control rodback to position 08 and ultimately to position 12, which was the correct final position inaccordance with reactor engineering maneuvering instructions. During interviews withthe NRC inspectors, the three operators each indicated that there was confusion in theirmind regarding whether or not the control rod met the definition of a mispositionedcontrol rod because the control rod was only out of position by one notch from the initialposition, but none of the operators referred to the procedure, and there was nodiscussion or challenge regarding the proper course of action among the operators. Thecondition was not logged, and a condition report was not generated until the issue wasidentified by NRC inspectors. In addition, the problem of the mispositioned control rodwas not discovered by the licensee during the post trip review.Following withdrawal of the five control rods (ten control rod notches), the RO-ATCobserved the process computer displaying a high short{erm (five minute average)moderator heat-up rate reading of 18'F per 5 minutes that he mistakenly believedcorresponded to an hourly heat-up rate of 216"Flhr (the actual hourly heatup rate was50"F/hr). The heat-up rate concern was discussed among the SM, Reactivity SRO/CRS,RO-ATC operator, Verifier and AOM-Shift. After the discussion, the SM directed thecrew at the controls to insert control rods to reduce the heat-up rate. This direction didnot include specific guidance or limitations regarding the number of control rod notchesto insert, At this point, the AOM-Shift and SM left the front panels area of the controlroom.The RE and RE-in-training were working at their computer terminals in the control roomperforming procedurally required calculations related to the startup. The REs had beenoccupied with these tasks from the time criticality had been achieved and had not beenconsulted on the plan to insert control rods to reduce the heatup rate. The RE-in-training overheard the operator conversation about inserting control rods. He informedthe RE, who in turn, questioned the SM about the decision to insert rods. The SMresponded that the actions were necessary to control heat-up rate. No furtherdiscussion occurred between the SM and the RE regarding the number of controlrods/notches to be used to control the heat-up rate or if there was a need to modify thereactor maneuvering plan. During interviews with the NRC inspectors, the SM and theAOM-Shift stated that they both discussed that there was a need to be careful to avoidtaking the reactor subcritical and that the action of inserting control rods had thepotential to cause the reactor to become subcritical. However, this important informationwas never communicated to any of the operators at the controls, including at the timewhen the SM directed the at-the-controls crew to insert control rods to reduce theheat-up rate.As a result of the previous control rod withdrawal, moderator temperature was 40"Fhigher than it was at initial criticality resulting in slightly increased control rod worth.The crew did not factor this increased control rod worth into their decision regarding thenumber of control rod notches to insert.Over the next three minutes, the RO-ATC operator proceeded to re-insert the followingcontrol rods from positions 12 to 8 (10 notches total) that had been previously withdrawnEnclosure 2.3to establish the heat-up: 30-1 1 , 22-43, 14-19,38-35 and 14-35. At the end of the rodinsertion evolution, the SM directed the Reactivity SRO/CRS and the RO-ATC operatorto keep reactor power on IRM range 7. This communication was not acknowledged bythe RO-ATC operator. During interviews with the NRC inspectors, none of the operatorsrecalled receiving such instructions. The SM then left the control room to take a break.The AOM-Shift left the controls area to get lunch in the control room kitchen.As a result of the control rod insertions, reactor power lowered, thus requiring theRO-ATC operator to range the lRMs down to range 7 and then to range 6. The reactorhad become subcritical, but the crew did not recognize the change in reactor status.Approximately four minutes after the control rods were inserted to reduce the heat-uprate, the RO-ATC operator observed the process computer displaying a 0'F/hr heat-uprate. At this time, the SRO who had previously been relieved, returned and re-assumedhis role as Reactivity SRO/CRS. The Reactivity SRO/CRS and the RO-ATC operatordecided to once again withdraw control rods to re-establish the desired heat-up rate.Three of the same control rods (14-35, 38-35, and 14-19) were withdrawn from positions8-12 resulting in a rising IRM count rate that was observed by the operators. However,the crew did not recognize that the reactor status had changed from subcritical to critical.At this point, the AOM-Shift returned to the reactor panel area. The RO-ATC operatorcontinued rod withdrawal with control rod 22-43 from position 08 to 10. The RO-ATCoperator and the Verifier ranged the lRMs up as reactor power increased. The RO-ATCoperator then withdrew control rod 22-43 from position 10 to 12. The operators did notrecognize the increasing rate of change in IRM power.Finally, the RO-ATC operator selected and withdrew control rod 30-11 from position 8 to10. At 1318, IRM readings rose sharply and an IRM Hi-Hi flux condition wasexperienced on both Reactor Protection System (RPS) channels resulting in anautomatic reactor scram at approximately 1
o Assistant Operations Manager (AOM-Shift) - Senior Line Management oversight r Shift Manager (SM)- management oversight. Reactivity Senior Reactor Operator (SRO/Control Room Supervisor (CRS) -command and control o Assistant Control Room Supervisor (ACRS). Reactor Operator At-The-Controls (RO-ATC)o Reactor Operator (Verifier)
* ATC verifier r Reactor Engineer (RE). RE in Training At 1212, the reactor was made critical when control rod 38-19 was moved to position 12.Power continued to rise to the point of adding heat (POAH), and the POAH was achieved at 1227. Once the POAH was achieved, the RO-ATC operator inserted rod 38-19 to position 10 to obtain lntermediate Range Monitor (lRM) overlap correlation data. Following the data collection, the RO-ATC operator withdrew rod 38-19 back to position 12.At approximately 1231, the Reactivity SRO/CRS and the RO-ATC operator were relieved by other licensed operators who continued with plant startup. The crew withdrew control rods to establish a moderator heat-up rate. The RO-ATC operator withdrew control rods 14-35, 38-35 , 14-19 and 22-43 from position 08 to 12 without incident.The RO-ATC operator continued with the rod withdrawal sequence and tried to withdraw control rod 30-11 from position 08 to 12, but the control rod would not move using normal notch withdraw commands.
 
The RO-ATC then attempted to withdraw control rod 30-11 using a "double-clutch" maneuver in accordance with procedures; however, the control rod inadvertently inserted and settled at position 06. As stated during interviews with the NRC inspectors, the RO-ATC operator, the ATC verifier, and the Reactivity SRO/CRS all saw the control rod in the incorrect position.
 
However, the operators did not enter and follow Pilgrim Nuclear Power Station (PNPS) Procedure 2.4.11, "Control Rod Positioning Malfunctions" as required.
 
This procedure required the operators to assess the amount of the mispositioning to determine the appropriate course of remedial 2 action before proceeding, and it also required the issue to be documented in a condition report. The operators did not perform an assessment, and they moved the control rod back to position 08 and ultimately to position 12, which was the correct final position in accordance with reactor engineering maneuvering instructions.
 
During interviews with the NRC inspectors, the three operators each indicated that there was confusion in their mind regarding whether or not the control rod met the definition of a mispositioned control rod because the control rod was only out of position by one notch from the initial position, but none of the operators referred to the procedure, and there was no discussion or challenge regarding the proper course of action among the operators.
 
The condition was not logged, and a condition report was not generated until the issue was identified by NRC inspectors.
 
In addition, the problem of the mispositioned control rod was not discovered by the licensee during the post trip review.Following withdrawal of the five control rods (ten control rod notches), the RO-ATC observed the process computer displaying a high short{erm (five minute average)moderator heat-up rate reading of 18'F per 5 minutes that he mistakenly believed corresponded to an hourly heat-up rate of 216"Flhr (the actual hourly heatup rate was 50"F/hr).
 
The heat-up rate concern was discussed among the SM, Reactivity SRO/CRS, RO-ATC operator, Verifier and AOM-Shift.
 
After the discussion, the SM directed the crew at the controls to insert control rods to reduce the heat-up rate. This direction did not include specific guidance or limitations regarding the number of control rod notches to insert, At this point, the AOM-Shift and SM left the front panels area of the control room.The RE and RE-in-training were working at their computer terminals in the control room performing procedurally required calculations related to the startup. The REs had been occupied with these tasks from the time criticality had been achieved and had not been consulted on the plan to insert control rods to reduce the heatup rate. The RE-in-training overheard the operator conversation about inserting control rods. He informed the RE, who in turn, questioned the SM about the decision to insert rods. The SM responded that the actions were necessary to control heat-up rate. No further discussion occurred between the SM and the RE regarding the number of control rods/notches to be used to control the heat-up rate or if there was a need to modify the reactor maneuvering plan. During interviews with the NRC inspectors, the SM and the AOM-Shift stated that they both discussed that there was a need to be careful to avoid taking the reactor subcritical and that the action of inserting control rods had the potential to cause the reactor to become subcritical.
 
However, this important information was never communicated to any of the operators at the controls, including at the time when the SM directed the at-the-controls crew to insert control rods to reduce the heat-up rate.As a result of the previous control rod withdrawal, moderator temperature was 40"F higher than it was at initial criticality resulting in slightly increased control rod worth.The crew did not factor this increased control rod worth into their decision regarding the number of control rod notches to insert.Over the next three minutes, the RO-ATC operator proceeded to re-insert the following control rods from positions 12 to 8 (10 notches total) that had been previously withdrawn Enclosure 2.3 to establish the heat-up: 30-1 1 , 22-43, 14-19,38-35 and 14-35. At the end of the rod insertion evolution, the SM directed the Reactivity SRO/CRS and the RO-ATC operator to keep reactor power on IRM range 7. This communication was not acknowledged by the RO-ATC operator.
 
During interviews with the NRC inspectors, none of the operators recalled receiving such instructions.
 
The SM then left the control room to take a break.The AOM-Shift left the controls area to get lunch in the control room kitchen.As a result of the control rod insertions, reactor power lowered, thus requiring the RO-ATC operator to range the lRMs down to range 7 and then to range 6. The reactor had become subcritical, but the crew did not recognize the change in reactor status.Approximately four minutes after the control rods were inserted to reduce the heat-up rate, the RO-ATC operator observed the process computer displaying a 0'F/hr heat-up rate. At this time, the SRO who had previously been relieved, returned and re-assumed his role as Reactivity SRO/CRS. The Reactivity SRO/CRS and the RO-ATC operator decided to once again withdraw control rods to re-establish the desired heat-up rate.Three of the same control rods (14-35, 38-35, and 14-19) were withdrawn from positions 8-12 resulting in a rising IRM count rate that was observed by the operators.
 
However, the crew did not recognize that the reactor status had changed from subcritical to critical.At this point, the AOM-Shift returned to the reactor panel area. The RO-ATC operator continued rod withdrawal with control rod 22-43 from position 08 to 10. The RO-ATC operator and the Verifier ranged the lRMs up as reactor power increased.
 
The RO-ATC operator then withdrew control rod 22-43 from position 10 to 12. The operators did not recognize the increasing rate of change in IRM power.Finally, the RO-ATC operator selected and withdrew control rod 30-11 from position 8 to 10. At 1318, IRM readings rose sharply and an IRM Hi-Hi flux condition was experienced on both Reactor Protection System (RPS) channels resulting in an automatic reactor scram at approximately 1
 
===.7 o/o reactor power.Operator Human Performance===
 
Inspection Scope The inspection team interviewed the Pilgrim control room personnel that responded to the May 10,2011, event including the SM, AOM-Shift, CRS, ACRS, RO-ATC, RO verifier, and the REs to determine whether these personnel performed their duties in accordance with plant procedures and training.
 
The inspection team also reviewed narrative logs, sequence of events and alarm printouts, condition reports, PPC trend data, procedures implemented by the crew, and procedures regarding the conduct of operations.
 
a.Enclosure 4 b. Findinqs/Observations Failure to lmplement Procedures durinq Reactor Startup
 
=====Introduction:=====
A self-revealing finding was identified involving the failure of Pilgrim personnel to implement conduct of operations and reactivity control standards and procedures during a reactor startup, which contributed to an unrecognized subcriticality followed by an unrecognized return to criticality and subsequent reactor scram. The significance of the finding has preliminarily been determined to be White, or of low to moderate safety significance.
 
The finding is also associated with one apparent violation of NRC requirements specified by Technical Specification 5.4, "Procedures."
 
=====Description:=====
On May 10,2011, following a refueling outage, operators were in the process of conducting a reactor startup. During the course of the startup, multiple licensed operators failed to implement written procedures as described below:. Entergy procedure EN-OP-1 15, "Conduct of Operations," Revision 10, Section 4.0, states that the SM is to "provide oversight of activities supporting complex and infrequently performed plant evolutions such as plant heat-up [and] startup." Additionally, the SM is responsible for ensuring "conservative actions are taken during unusual conditions
... when dealing with reactivity control," However, the SM did not oversee the activities in progress during reactor heatup and left the control room when the heat-up rate was being adjusted with control rod insertion, The SM did not ensure the actions taken to reestablish or adjust the reactor heatup rate were conservative nor did he reinforce those actions with the operating crew.r Entergy procedure EN-OP-1 15, "Conduct of Operations," Revision 10, Section 4.0, states that the CRS is required to "Ensure Pre-Evolution Briefings are held [and]plant operations are conducted in compliance with administrative and regulatory requirements." PNPS procedure 1.3.34, "Operations Administrative Policies and Procedures," Revision 1 17, Section 6.10.1


===.7 o/o reactor power.Operator Human PerformanceInspection ScopeThe inspection team interviewed the Pilgrim control room personnel that responded tothe May 10,2011, event including the SM, AOM-Shift, CRS, ACRS, RO-ATC, ROverifier, and the REs to determine whether these personnel performed their duties inaccordance with plant procedures and training. The inspection team also reviewednarrative logs, sequence of events and alarm printouts, condition reports, PPC trenddata, procedures implemented by the crew, and procedures regarding the conduct ofoperations.a.Enclosure===
===.1 states, "All complex or infrequently===


4b. Findinqs/ObservationsFailure to lmplement Procedures durinq Reactor StartupIntroduction: A self-revealing finding was identified involving the failure of Pilgrimpersonnel to implement conduct of operations and reactivity control standards andprocedures during a reactor startup, which contributed to an unrecognized subcriticalityfollowed by an unrecognized return to criticality and subsequent reactor scram. Thesignificance of the finding has preliminarily been determined to be White, or of low tomoderate safety significance. The finding is also associated with one apparent violationof NRC requirements specified by Technical Specification 5.4, "Procedures."Description: On May 10,2011, following a refueling outage, operators were in theprocess of conducting a reactor startup. During the course of the startup, multiplelicensed operators failed to implement written procedures as described below:. Entergy procedure EN-OP-1 15, "Conduct of Operations," Revision 10, Section 4.0,states that the SM is to "provide oversight of activities supporting complex andinfrequently performed plant evolutions such as plant heat-up [and] startup."Additionally, the SM is responsible for ensuring "conservative actions are takenduring unusual conditions ... when dealing with reactivity control," However, the SMdid not oversee the activities in progress during reactor heatup and left the controlroom when the heat-up rate was being adjusted with control rod insertion, The SMdid not ensure the actions taken to reestablish or adjust the reactor heatup ratewere conservative nor did he reinforce those actions with the operating crew.r Entergy procedure EN-OP-1 15, "Conduct of Operations," Revision 10, Section 4.0,states that the CRS is required to "Ensure Pre-Evolution Briefings are held [and]plant operations are conducted in compliance with administrative and regulatoryrequirements." PNPS procedure 1.3.34, "Operations Administrative Policies andProcedures," Revision 1 17, Section 6.10.1
performed activities warrant a pre-evolution briefing." Section 6,10.1.1[8]
lists an Infrequently Performed Tests or Evolutions Briefing as one type of pre-evolution briefing, and Section 6.10.1


===.1 states, "All complex or infrequentlyperformed activities warrant a pre-evolution briefing." Section 6,10.1.1[8] lists anInfrequently Performed Tests or Evolutions Briefing as one type of pre-evolutionbriefing, and Section 6.10.1 .1 [4] states, "lnfrequently Performed Tests or EvolutionsBriefings for the performance of Procedures classified as "lnfrequently PerformedTests or Evolutions" (IPTE) should be performed with Senior Line Manager oversightas specified in EN-OP-116, "lnfrequently Performed Tests or Evolutions." EntergyProcedure EN-OP-116, Revision 7, Attachment 9.1 identifies "Reactor Startup" as anIPTE. However, in this case, the licensee conducted a reactor startup withoutperforming an IPTE briefing or any other type of pre-evolution briefing as defined inPNPS procedure 1.3.34. lt is noteworthy to point out that an IPTE briefing packagewas previously prepared, approved, and scheduled; however, the IPTE briefing wasnever performed as required by the procedures described above. In addition, anIPTE briefing was also not performed for the startup following this event. Finally, theCRSs did not ensure the administrative requirements of the conduct of operationsprocedures or the regulatory requirement to implement the control rod mispositioningprocedure were met. This issue was identified by the NRC inspectors.Enclosure===
===.1 [4] states, "lnfrequently===


5Entergy procedure EN-OP-115, "Conduct of Operations," Revision 10, Section 5.2,states control room operators are required to "develop and implement a plan thatincludes contingencies and compensatory measures" and when implementing thoseplans the "crew ... continuously evaluates the plan for changing conditions" and"Human Performance (HU) tools (..., peer/cross-checking, oversight, questioningattitude, etc.) are utilized ..." In addition, "When the control room team is faced witha time critical decision: Use all available resources...do not proceed in the face ofuncertainty..." However, the control room operators failed to develop contingencyplans or compensatory measures for adjusting reactor heat-up rate or addressinghigher than expected reactor heat-up rates. The crew also failed to develop orimplement contingencies for control rods which were difficult to maneuver when theywere at low reactor power. Additionally, the use of human performance tools wasineffective in addressing the actions or conditions that led to the unexpected reactorheatup rate and the mispositioning of control rod 30-11. Specifically, failures in theuse of peer checking and questioning the conditions that led to the unexpectedreactor heat-up rate directly contributed to the mispositioned control rod and thesubsequent reactor scram. Lastly, the control room team did not use all availableresources by involving Reactor Engineering staff in its decision-making, andproceeded in the face of uncertainty by failing to consider the consequences of thereactivity changes.Entergy procedure EN-OP-115, "Conduct of Operations," Revision 10, Section 5.4states that reactor operators are expected to perform reactivity manipulations "in adeliberate, carefully controlled manner while the reactor is monitored to ensure thedesired result is obtained." However, the reactor operators did not adequatelymonitor the conditions of the reactor while attempting to establish and adjust thereactor heat-up rate. Although the reactor operators were watching the response ofboth the lRMs and the computer point displaying a five minute average reactorheatup, they were moving control rods faster than the plant temperature couldrespond and therefore taking actions to continue control rod movement before thedesired result of their manipulations could be assessed. Additionally, after insertingcontrol rods to adjust the reactor heat-up rate, the operators had sufficient indicationsthat the reactor was significantly subcritical as evidenced by the required rangingdown of lRMs, the drop in Source Range Monitor (SRM) count rates, andestablishing a negative reactor period. The operator's failure to adequately monitorthe status of the reactor led to an unrecognized subcritical condition and subsequentreturn to criticality resulting in an eventual reactor scram.PNPS procedure 1.3.34, "Operations Administrative Policies and Procedures,"Revision 1 17, Section 6.7.5 states, "Any relief occurring during the shift (eithershort-term or for the remainder of the shift) will be recorded in the CRS log." ltfurther states, "...a verbal discussion of plant status and off-normal conditions mustbe conducted." However, several people in watch standing positions changed fromthe start of the shift, but none of those changes were entered into the control roomlog. In addition, when the ACRS was turning over to the CRS, there was nodiscussion of the mispositioning of control rod 30-11.Enclosure
Performed Tests or Evolutions Briefings for the performance of Procedures classified as "lnfrequently Performed Tests or Evolutions" (IPTE) should be performed with Senior Line Manager oversight as specified in EN-OP-116, "lnfrequently Performed Tests or Evolutions." Entergy Procedure EN-OP-116, Revision 7, Attachment 9.1 identifies "Reactor Startup" as an IPTE. However, in this case, the licensee conducted a reactor startup without performing an IPTE briefing or any other type of pre-evolution briefing as defined in PNPS procedure 1.3.34. lt is noteworthy to point out that an IPTE briefing package was previously prepared, approved, and scheduled; however, the IPTE briefing was never performed as required by the procedures described above. In addition, an IPTE briefing was also not performed for the startup following this event. Finally, the CRSs did not ensure the administrative requirements of the conduct of operations procedures or the regulatory requirement to implement the control rod mispositioning procedure were met. This issue was identified by the NRC inspectors.


===6. PNPS Procedure 2.4.11, "Control Rod Positioning Malfunctions," Revision 35,Section 5.4 defines a mispositioned control rod as "a control rod found to be left in aposition other than the intended position $ a control rod that moves more than onenotch beyond its intended position." Attachment 4 Step [3] and Step [a] of the sameprocedure requires the operators to assess the degree of mispositioning and take theappropriate remedial action depending on the degree of mispositioning. Attachment4 Step [5] also states, "lf the control rod is determined to be mispositioned, thenrecord the event as a condition report." In this case, the RO-ATC attempted towithdraw control rod 30-11 from position 08 to position 10 (intended position), but therod inadvertently insertbd to position 06. Upon recognizing the error, the operatorsdid not enter the procedure when control rod 30-11 was found to be left in a positionother than the intended position and which was more than one notch from theintended position. The operators did not assess the amount of the control rodmispositioning in accordance with the procedure, nor was there any discussion aboutthe mispositioning on the crew. Furthermore, the event was not logged, nor was acondition report generated. Instead, the operators did not enter and follow theprocedure, and they continued on with the startup in the face of uncertainty. Thisissue was not detected during the licensee posttrip review. lt was identified by theNRC inspectors.o PNPS Procedure 2.1.1, "Startup from Shutdown," Revision 173, Page 53, Caution 2states, "ln the event the reactor goes subcritical after achieving initial criticality, thenreturn to step [53] and re-perform the steps to restore the Reactor to a criticalcondition." In addition, PNPS Procedure 2.1.4, "Approach to Critical," Revision 26,Section 5.0 states, "ln the event the reactor goes subcritical after achieving initialcriticality, then with Reactor Engineering guidance, re-perform Section 7.0 Steps [6]and [7] to restore the Reactor to a critical condition." However, the operators did notrecognize that the reactor had become subcritical and did not re-perform theprocedural steps mentioned above to restore the reactor to a critical condition in acontrolled manner under the guidance of Reactor Engineering. There was sufficientinformation available to the operators to identify that the reactor had becomesubcritical. In addition, REs were available in the control room, but they were notconsulted by the operators.Analvsis: The inspection team determined that the failure of Pilgrim personnel toimplement conduct of operations and reactivity control standards and procedures duringa reactor startup was a performance deficiency that was reasonably within Entergy'sability to foresee and prevent. The finding is more than minor because it was associatedwith the Human Performance attribute of the Initiating Events cornerstone and affectedthe cornerstone objective of limiting the likelihood of those events that upset plantstability and challenge critical safety functions during power operations. Specifically, thefailure of Pilgrim personnel to effectively implement conduct of operations and reactivitycontrol standards and procedures during a reactor startup caused an unrecognizedsubcriticality followed by an unrecognized return to criticality and subsequent reactorscram.Enclosure ===
5 Entergy procedure EN-OP-115, "Conduct of Operations," Revision 10, Section 5.2, states control room operators are required to "develop and implement a plan that includes contingencies and compensatory measures" and when implementing those plans the "crew ... continuously evaluates the plan for changing conditions" and"Human Performance (HU) tools (..., peer/cross-checking, oversight, questioning attitude, etc.) are utilized ..." In addition, "When the control room team is faced with a time critical decision:
Use all available resources...do not proceed in the face of uncertainty..." However, the control room operators failed to develop contingency plans or compensatory measures for adjusting reactor heat-up rate or addressing higher than expected reactor heat-up rates. The crew also failed to develop or implement contingencies for control rods which were difficult to maneuver when they were at low reactor power. Additionally, the use of human performance tools was ineffective in addressing the actions or conditions that led to the unexpected reactor heatup rate and the mispositioning of control rod 30-11. Specifically, failures in the use of peer checking and questioning the conditions that led to the unexpected reactor heat-up rate directly contributed to the mispositioned control rod and the subsequent reactor scram. Lastly, the control room team did not use all available resources by involving Reactor Engineering staff in its decision-making, and proceeded in the face of uncertainty by failing to consider the consequences of the reactivity changes.Entergy procedure EN-OP-115, "Conduct of Operations," Revision 10, Section 5.4 states that reactor operators are expected to perform reactivity manipulations "in a deliberate, carefully controlled manner while the reactor is monitored to ensure the desired result is obtained." However, the reactor operators did not adequately monitor the conditions of the reactor while attempting to establish and adjust the reactor heat-up rate. Although the reactor operators were watching the response of both the lRMs and the computer point displaying a five minute average reactor heatup, they were moving control rods faster than the plant temperature could respond and therefore taking actions to continue control rod movement before the desired result of their manipulations could be assessed.


7The inspection team determined that multiple factors contributed to this performancedeficiency including: inadequate enforcement of operating standards, failure to followprocedures, and ineffective operator training. The Entergy RCE documented that theprimary cause was a failure to adhere to established Entergy standards and expectationsdue to a lack of consistent supervisory and management enforcement. In addition, theEntergy RCE specified a number of condition reports and self assessment reports writtenin the months preceding this event that demonstrated that the performance deficiencyexisted over an extended period of time and affected all operating crews. While theperformance deficiency manifested itself during this particular low power event, therewas the potential for the performance deficiency to result in a more consequential eventunder different circumstances.Because the finding primarily involved multiple human performance errors, probabilisticrisk assessment tools were not well suited for evaluating its significance. The inspectionteam determined that the criteria for using IMC 0609, Appendix M, "SignificanceDetermination Process Using Qualitative Criteria," were met, and the finding wasevaluated using this guidance as described in Attachment 4 to this report. Based on thequalitative review of this finding, the NRC concluded that the finding was preliminarily oflow to moderate safety significance (preliminary White). The completed Appendix Mtable is attached to this report (Attachment 4). There was no significant impact on theplant following the transient because the event itself did not result in power exceedinglicense limits or fuel damage. Additionally, interim corrective actions were taken, whichincluded removing the Pilgrim control room personnel involved in the event fromoperational duties pending remediation, providing additional training for operators notinvolved with the event, and providing increased management oversight presence in thePilgrim control room while long term corrective actions were developed.This finding had a cross-cutting aspect in the Human Performance cross-cutting area,Work Practices component, because Entergy management and supervision did notadequately enforce human error prevention techniques, such as procedural adherence,holding pre-job briefs, self and peer checking, and proper documentation of activitiesduring a reactor startup, which is a risk significant evolution. Additionally, licensedpersonnel did not effectively implement the human performance prevention techniquesmentioned above, and they proceeded when they encountered uncertainty andunexpected circumstances during the reactor startup [H.a(a)].Enforcement: Technical Specification 5.4, "Procedures," states, in part, that writtenprocedures shall be established, implemented, and maintained covering the applicableprocedures recommended in Appendix "A" of Regulatory Guide (RG) 1.33, February,1978. RG 1.33, Appendix "A," requires that typical safety-related activities listed thereinbe covered by written procedures. Contrary to the above, on May 10,2011, as reflectedin the examples listed in the description section of this finding, the licensee failed toimplement safety-related procedures related to RG 1.33, Appendix "A," Paragraph 1,"Administrative Procedures;" Paragraph 2, "General Plant Operating Procedures;" and,Paragraph 4, "Procedures for Startup, Operation, and Shutdown of Safety-Related BWRSystems."Enclosure 3.IFollowing a review of the event, the licensee documented the condition in the correctiveaction program (CR-PNP-2011-2475). There was no significant impact on the plantfollowing the transient because the event itself did not result in power exceeding licenselimits or fuel damage. Additionally, interim corrective actions were taken, which includedremoving the Pilgrim control room personnel involved in the event from operationalduties pending remediation, providing additional training for operators not involved withthe event, and providing increased management oversight presence in the Pilgrimcontrol room while long term corrective actions were developed.Pending determination of final safety significance, this finding with the associatedapparent violation will be tracked as AV 05000293/2011012-01, Failure to lmplementGonduct of Operations and Reactivity Gontrol Procedures during Reactor Startup.Fitness for DutvInspection ScopeThe inspection team interviewed the control room personnel that were directly involvedwith the May 10,2011, reactor scram event as well as management personnel involvedwith the immediate post event investigation. The inspection team also reviewed EntergyFitness for Duty (FFD) program requirements contained in the corporate and siteprocedures.Fi nd i nos/ObservationsNo findings were identified.TraininqInspection ScopeThe inspection team interviewed personnel, reviewed simulator modeling andperformance, and reviewed training material related to Just in Time Training (JITT)material for the initial and subsequent startups, remedial training for the operatorsinvolved with the event, and training plans for startups and reactivity maneuvers.Fi nd i nqs/ObservationsNo findings were identified.The inspection team observed that the JITT training that was provided prior to the initialstartup was very limited in scope in that it only covered the approach to criticality up tothe POAH. lt did not cover the full range of reactor heat-up, and it covered very littleOperating Experience. In addition, several operators that were directly involved with thisevent did not attend the JITT training including the SM, the ACRS who temporarilyrelieved the CRS prior to the scram, and the RO who was at the controls when thescram occurred.a.h4.a.b.Enclosure 5.IOrqanizational Responselmmediate ResponseInspection ScopeThe inspection team interviewed personnel, reviewed various procedures and records,and observed control room operations to assess immediate response of stationpersonnel to the reactor scram event.Fi nd i nqs/ObservationsNo findings were identified.The inspection team observed that Entergy's initial response to the event was notappropriately thorough and was narrowly focused. lmmediately foilowing the event,operators were debriefed in an attempt to ascertain the cause of the event. Initially,Entergy personnel focused on a potential IRM malfunction as the potential cause of theevent despite the fact that multiple IRM channels accurately tracked reactor power alongwith operator reactivity inputs. lmmediate post event interviews with the crew did notprobe human error as a potential cause even though the SM, the AOM-Shift, and theREs had expressed concerns just prior to the scram regarding the insertion of controlrods so near the point of criticality. Operators involved with the event were dismissed forthe day as the investigation continued to incorrectly focus on equipment malfunction asthe most likely cause of the event. Several hours passed before it became clear to sitemanagement that human error was the cause of the event. As a result, the operatorsinvolved with the event were not thoroughly interviewed to ensure that all of the humanperformance aspects were fully understood prior to proceeding with the next startup. Inaddition, the inspection team identified that the posttrip review failed to identify that acontrol rod had been mispositioned just prior to the scram and that an IPTE briefing hadnot been conducted for the startup. Consequently, additional human performanceissues were not evaluated, and the licensee again failed to perform an IPTE briefingprior to the subsequent startup as required by Entergy procedures.Post-Event Root Cause Evaluation and ActionsInspection ScopeThe inspection team reviewed Entergy's Root Cause Evaluation (RCE) report for theevent to determine whether the causes and associated human performance issues wereproperly identified. Additionally, the inspection team assessed whether interim andplanned long term corrective actions were appropriate to address the cause(s).61a.b.5.2a.Enclosure b.10Find inqs/ObservationsNo findings were identified.The RCE was thorough and appeared to identify the underlying causal factors. Theassociated proposed corrective actions appeared to adequately address the underlyingcausal factors. Entergy identified the root cause as a lack of consistent supervisory andmanagement enforcement of administrative procedure requirements and managementexpectations for command and control, roles and responsibilities, reactivitymanipulations, clear communications, proper briefings, and proper turnovers.The RCE also identified contributing causes including weaknesses in monitoring plantstatus and parameters as well as weaknesses in operator proficiency with regards to lowpower operations.Meetinqs. Includinq ExitExit Meetino SummarvOn July 20,2011, the inspection team discussed the inspection results with Mr. R. Smith,Site Vice President, and members of his staff. The inspection team confirmed thatproprietary information reviewed during the inspection period was returned to Entergy.40A6Enclosure Enterov PersonnelR. SmithJ. DreyfussD. NoyesJ. MacdonaldR. ProbascoJ. CoutoS. AndersonT. TomonJ. ByronJ. HayhurstS. BethayJ. LynchT. WhiteF. McGinnisR. ByrneV. FallacaraS. ReininghausJ. HouseV. MagnattaR. ParanjapeA,1-1
Additionally, after inserting control rods to adjust the reactor heat-up rate, the operators had sufficient indications that the reactor was significantly subcritical as evidenced by the required ranging down of lRMs, the drop in Source Range Monitor (SRM) count rates, and establishing a negative reactor period. The operator's failure to adequately monitor the status of the reactor led to an unrecognized subcritical condition and subsequent return to criticality resulting in an eventual reactor scram.PNPS procedure 1.3.34, "Operations Administrative Policies and Procedures," Revision 1 17, Section 6.7.5 states, "Any relief occurring during the shift (either short-term or for the remainder of the shift) will be recorded in the CRS log." lt further states, "...a verbal discussion of plant status and off-normal conditions must be conducted." However, several people in watch standing positions changed from the start of the shift, but none of those changes were entered into the control room log. In addition, when the ACRS was turning over to the CRS, there was no discussion of the mispositioning of control rod 30-11.Enclosure  


=SUPPLEMENTAL INFORMATION=
===6. PNPS Procedure ===


==KEY POINTS OF CONTACTS==
2.4.11, "Control Rod Positioning Malfunctions," Revision 35, Section 5.4 defines a mispositioned control rod as "a control rod found to be left in a position other than the intended position $ a control rod that moves more than one notch beyond its intended position." Attachment 4 Step [3] and Step [a] of the same procedure requires the operators to assess the degree of mispositioning and take the appropriate remedial action depending on the degree of mispositioning.
ite Vice PresidentGeneral Manager Plant OperationsManager, OperationsAssistant Manager, OperationsShift Manager, OperationsShift Supervisor, OperationsShift Supervisor, OperationsReactor Operator, OperationsReactor Operator, OperationsReactor Operator, OperationsDirector, Nuclear Safety AssuranceManager, LicensingManager, Quality AssuranceEngineer, LicensingSenior Engineer, LicensingDirector, EngineeringManager, TrainingSupervisor, Operations TrainingLead lnstructor, Operations TrainingReactor Engineer
 
4 Step [5] also states, "lf the control rod is determined to be mispositioned, then record the event as a condition report." In this case, the RO-ATC attempted to withdraw control rod 30-11 from position 08 to position 10 (intended position), but the rod inadvertently insertbd to position 06. Upon recognizing the error, the operators did not enter the procedure when control rod 30-11 was found to be left in a position other than the intended position and which was more than one notch from the intended position.
 
The operators did not assess the amount of the control rod mispositioning in accordance with the procedure, nor was there any discussion about the mispositioning on the crew. Furthermore, the event was not logged, nor was a condition report generated.
 
Instead, the operators did not enter and follow the procedure, and they continued on with the startup in the face of uncertainty.
 
This issue was not detected during the licensee posttrip review. lt was identified by the NRC inspectors.
 
o PNPS Procedure 2.1.1, "Startup from Shutdown," Revision 173, Page 53, Caution 2 states, "ln the event the reactor goes subcritical after achieving initial criticality, then return to step [53] and re-perform the steps to restore the Reactor to a critical condition." In addition, PNPS Procedure 2.1.4, "Approach to Critical," Revision 26, Section 5.0 states, "ln the event the reactor goes subcritical after achieving initial criticality, then with Reactor Engineering guidance, re-perform Section 7.0 Steps [6]and [7] to restore the Reactor to a critical condition." However, the operators did not recognize that the reactor had become subcritical and did not re-perform the procedural steps mentioned above to restore the reactor to a critical condition in a controlled manner under the guidance of Reactor Engineering.
 
There was sufficient information available to the operators to identify that the reactor had become subcritical.
 
In addition, REs were available in the control room, but they were not consulted by the operators.
 
Analvsis:
The inspection team determined that the failure of Pilgrim personnel to implement conduct of operations and reactivity control standards and procedures during a reactor startup was a performance deficiency that was reasonably within Entergy's ability to foresee and prevent. The finding is more than minor because it was associated with the Human Performance attribute of the Initiating Events cornerstone and affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during power operations.
 
Specifically, the failure of Pilgrim personnel to effectively implement conduct of operations and reactivity control standards and procedures during a reactor startup caused an unrecognized subcriticality followed by an unrecognized return to criticality and subsequent reactor scram.Enclosure 7 The inspection team determined that multiple factors contributed to this performance deficiency including:
inadequate enforcement of operating standards, failure to follow procedures, and ineffective operator training.
 
The Entergy RCE documented that the primary cause was a failure to adhere to established Entergy standards and expectations due to a lack of consistent supervisory and management enforcement.
 
In addition, the Entergy RCE specified a number of condition reports and self assessment reports written in the months preceding this event that demonstrated that the performance deficiency existed over an extended period of time and affected all operating crews. While the performance deficiency manifested itself during this particular low power event, there was the potential for the performance deficiency to result in a more consequential event under different circumstances.
 
Because the finding primarily involved multiple human performance errors, probabilistic risk assessment tools were not well suited for evaluating its significance.
 
The inspection team determined that the criteria for using IMC 0609, Appendix M, "Significance Determination Process Using Qualitative Criteria," were met, and the finding was evaluated using this guidance as described in Attachment 4 to this report. Based on the qualitative review of this finding, the NRC concluded that the finding was preliminarily of low to moderate safety significance (preliminary White). The completed Appendix M table is attached to this report (Attachment 4). There was no significant impact on the plant following the transient because the event itself did not result in power exceeding license limits or fuel damage. Additionally, interim corrective actions were taken, which included removing the Pilgrim control room personnel involved in the event from operational duties pending remediation, providing additional training for operators not involved with the event, and providing increased management oversight presence in the Pilgrim control room while long term corrective actions were developed.
 
This finding had a cross-cutting aspect in the Human Performance cross-cutting area, Work Practices component, because Entergy management and supervision did not adequately enforce human error prevention techniques, such as procedural adherence, holding pre-job briefs, self and peer checking, and proper documentation of activities during a reactor startup, which is a risk significant evolution.
 
Additionally, licensed personnel did not effectively implement the human performance prevention techniques mentioned above, and they proceeded when they encountered uncertainty and unexpected circumstances during the reactor startup [H.a(a)].Enforcement:
Technical Specification 5.4, "Procedures," states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix "A" of Regulatory Guide (RG) 1.33, February, 1978. RG 1.33, Appendix "A," requires that typical safety-related activities listed therein be covered by written procedures.
 
Contrary to the above, on May 10,2011, as reflected in the examples listed in the description section of this finding, the licensee failed to implement safety-related procedures related to RG 1.33, Appendix "A," Paragraph 1,"Administrative Procedures;" Paragraph 2, "General Plant Operating Procedures;" and, Paragraph 4, "Procedures for Startup, Operation, and Shutdown of Safety-Related BWR Systems." Enclosure 3.I Following a review of the event, the licensee documented the condition in the corrective action program (CR-PNP-2011-2475).
 
There was no significant impact on the plant following the transient because the event itself did not result in power exceeding license limits or fuel damage. Additionally, interim corrective actions were taken, which included removing the Pilgrim control room personnel involved in the event from operational duties pending remediation, providing additional training for operators not involved with the event, and providing increased management oversight presence in the Pilgrim control room while long term corrective actions were developed.
 
Pending determination of final safety significance, this finding with the associated apparent violation will be tracked as AV 05000293/2011012-01, Failure to lmplement Gonduct of Operations and Reactivity Gontrol Procedures during Reactor Startup.Fitness for Dutv Inspection Scope The inspection team interviewed the control room personnel that were directly involved with the May 10,2011, reactor scram event as well as management personnel involved with the immediate post event investigation.
 
The inspection team also reviewed Entergy Fitness for Duty (FFD) program requirements contained in the corporate and site procedures.
 
Fi nd i nos/Observations No findings were identified.
 
Traininq Inspection Scope The inspection team interviewed personnel, reviewed simulator modeling and performance, and reviewed training material related to Just in Time Training (JITT)material for the initial and subsequent startups, remedial training for the operators involved with the event, and training plans for startups and reactivity maneuvers.
 
Fi nd i nqs/Observations No findings were identified.
 
The inspection team observed that the JITT training that was provided prior to the initial startup was very limited in scope in that it only covered the approach to criticality up to the POAH. lt did not cover the full range of reactor heat-up, and it covered very little Operating Experience.
 
In addition, several operators that were directly involved with this event did not attend the JITT training including the SM, the ACRS who temporarily relieved the CRS prior to the scram, and the RO who was at the controls when the scram occurred.a.h 4.a.b.Enclosure 5.I Orqanizational Response lmmediate Response Inspection Scope The inspection team interviewed personnel, reviewed various procedures and records, and observed control room operations to assess immediate response of station personnel to the reactor scram event.Fi nd i nqs/Observations No findings were identified.
 
The inspection team observed that Entergy's initial response to the event was not appropriately thorough and was narrowly focused. lmmediately foilowing the event, operators were debriefed in an attempt to ascertain the cause of the event. Initially, Entergy personnel focused on a potential IRM malfunction as the potential cause of the event despite the fact that multiple IRM channels accurately tracked reactor power along with operator reactivity inputs. lmmediate post event interviews with the crew did not probe human error as a potential cause even though the SM, the AOM-Shift, and the REs had expressed concerns just prior to the scram regarding the insertion of control rods so near the point of criticality.
 
Operators involved with the event were dismissed for the day as the investigation continued to incorrectly focus on equipment malfunction as the most likely cause of the event. Several hours passed before it became clear to site management that human error was the cause of the event. As a result, the operators involved with the event were not thoroughly interviewed to ensure that all of the human performance aspects were fully understood prior to proceeding with the next startup. In addition, the inspection team identified that the posttrip review failed to identify that a control rod had been mispositioned just prior to the scram and that an IPTE briefing had not been conducted for the startup. Consequently, additional human performance issues were not evaluated, and the licensee again failed to perform an IPTE briefing prior to the subsequent startup as required by Entergy procedures.
 
Post-Event Root Cause Evaluation and Actions Inspection Scope The inspection team reviewed Entergy's Root Cause Evaluation (RCE) report for the event to determine whether the causes and associated human performance issues were properly identified.
 
Additionally, the inspection team assessed whether interim and planned long term corrective actions were appropriate to address the cause(s).61 a.b.5.2 a.Enclosure b.10 Find inqs/Observations No findings were identified.
 
The RCE was thorough and appeared to identify the underlying causal factors. The associated proposed corrective actions appeared to adequately address the underlying causal factors. Entergy identified the root cause as a lack of consistent supervisory and management enforcement of administrative procedure requirements and management expectations for command and control, roles and responsibilities, reactivity manipulations, clear communications, proper briefings, and proper turnovers.
 
The RCE also identified contributing causes including weaknesses in monitoring plant status and parameters as well as weaknesses in operator proficiency with regards to low power operations.
 
Meetinqs.
 
Includinq Exit Exit Meetino Summarv On July 20,2011, the inspection team discussed the inspection results with Mr. R. Smith, Site Vice President, and members of his staff. The inspection team confirmed that proprietary information reviewed during the inspection period was returned to Entergy.40A6 Enclosure Enterov Personnel R. Smith J. Dreyfuss D. Noyes J. Macdonald R. Probasco J. Couto S. Anderson T. Tomon J. Byron J. Hayhurst S. Bethay J. Lynch T. White F. McGinnis R. Byrne V. Fallacara S. Reininghaus J. House V. Magnatta R. Paranjape A,1-1
 
=SUPPLEMENTAL
INFORMATION=
 
==KEY POINTS OF CONTACT==
Site Vice President General Manager Plant Operations
Manager, Operations
Assistant
Manager, Operations
Shift Manager, Operations
Shift Supervisor, Operations
Shift Supervisor, Operations
Reactor Operator, Operations
Reactor Operator, Operations
Reactor Operator, Operations
Director, Nuclear Safety Assurance Manager, Licensing Manager, Quality Assurance Engineer, Licensing Senior Engineer, Licensing Director, Engineering
Manager, Training Supervisor, Operations
Training Lead lnstructor, Operations
Training Reactor Engineer  
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
Ooened05000293/2011012-01 AV Failure to lmplement Conduct of Operations andReactivity Control Procedures during ReactorStartup (Section 2)
Ooened
==LIST OF DOCUMENTS REVIEWED==
: 05000293/2011012-01
Procedures:1.3.34, "Operations Administrative policies and Procedures," Revision 1 191 .3.37 , "Post-Trip Reviews," Revision 271.3,63, "Conduct of Event Review Meetings," Revision 251.3.109, "lssue Management," Revision 82.1.1, "Startup from Shutdown," Revision 1732.1.4, "Approach to Critical," Revision 262.1.7, "Vessel Heat-up and Cool Down," Revision 542.4.11, "Control Rod Positioning Malfunctions," Revision 352.4.11.1, "CRD System Malfunctions," Revision 21Attachment 1
AV Failure to lmplement
: A-1-2SUPPLEMENTAL INFORMATIONNOP96A3, "Reactivity Management Peer Panel," Revision 10EN-FAP-AD-OO1, "Fleet Administrative Procedure (FAP) Process," Revision 0EN-FAP-OM-006, "Working Hour Limits for Non-Covered Workers," Revision 2EN-FAP-OP-008, "Reactivity Management Performance Indicator Program," Revision 0EN-FAP-OP-01 1, "Operator Human Performance Indicator Program," Revision 0EN-HU-102, "Human Performance Tools," Revision 5EN-HU-103, "Human Performance Error Reviews," Revision 4EN-NS-102, "Fitness for Duty Program," Revision 9EN-OM-119, "On-Site Safety Review Committee," Revision 7EN-OM-123, "Fatigue Management Program," Revision 3EN-OP-103, "Reactivity Management Program," Revision 5EN-OP-1 15, "Conduct of Operations," Revision 10EN-OP-1 16, "lnfrequently Performed Tests of Evolutions," Revision 7EN-RE-214, "Conduct of Reactor Engineering," Revision 0EN-RE-215, "Reactivity Maneuver Plan," Revision 1EN-RE-219, "Startup sequence Criticality Controls (BWR)," Revision 0Condition Reports:CR-PNP-2011-02475 and associated Root Cause Evaluation Report, Revision 1CR-PNP-201
Conduct of Operations
: 1-02488cR-PNP-2011-02493cR-PNP-2011-02504CR-PNP-201
and Reactivity
: 1-02506CR-PNP-2011-02546CR-PNP-201
Control Procedures
: 1-02568CR-PNP-2011-02572cR-PNP-2011-02577CR-PNP-201
during Reactor Startup (Section 2)
: 1-03598Self Assessments:LO-PNPLO-2009-00071, "Focused Assessment on Reactivity Management"LO-PNPLO-2010-00106, "Snapshot Assessment on Reactivity Management ProcedureRevision lmplementation"LO-PNPLO-2010-00106, "Snapshot Assessment on SOER 07-01 Recommendation 4 ReactivityManagement Operations Training"Technical Specifications:3.5.C, "HPCI System"3.5.D,'RCIC System"5.4.1, "PROCEDURES"Traininq Material:lnstructional Module, Reactor Startup and Criticality (& Main Turbine Overspeed) Just in TimeTraining used for
==LIST OF DOCUMENTS==
: 0511012011 and
REVIEWED Procedures:
: 0511112011 Startup JITTInstructional Module, Reactor Startup and Criticality May 2011 Just in Time Training used for051
: 1.3.34, "Operations Administrative policies and Procedures," Revision 1 19 1 .3.37 , "Post-Trip Reviews," Revision 27 1.3,63, "Conduct of Event Review Meetings," Revision 25 1.3.109, "lssue Management," Revision 8 2.1.1, "Startup from Shutdown," Revision 173 2.1.4, "Approach to Critical," Revision 26 2.1.7, "Vessel Heat-up and Cool Down," Revision 54 2.4.11, "Control Rod Positioning Malfunctions," Revision 35 2.4.11.1, "CRD System Malfunctions," Revision 21 Attachment
: 1812011 Startup JITTAttachment 1
: A-1-2 SUPPLEMENTAL
: A-1-3SUPPLEMENTAL INFORMATIONJust in Time Training PowerPoint used for 05/1812011 Startup JITTlnstructor Lesson Plan JITT
: INFORMATION
: RFO 18 Hydro 2.1 .8.5Simulator JITT Reactor Shutdown 2.1.5 and Vessel Cooldown 2.1.7 , Revised 0410112011Simulator JITT Reactor Shutdown 2.1.5 and Vessel Cooldown 2.1 .7 , Revised 0211912011Training Schedules for Outage Training Cycle
: NOP96A3, "Reactivity Management Peer Panel," Revision 10
: 0311412011 -0410712011Training Schedules for Training Cycle 020211312011 -0211712011Training Schedules for Training Cycle 01
: EN-FAP-AD-OO1, "Fleet Administrative
: 1112212010 - 0112212011Training Records and Remediation Training for Current Licensed Operatorslnitial License Class 2009-2011 Class ScheduleO-RO-03-02, "Reactor Plant Startup Certification Unit Guide," Revision 10O-RO-03-01-19, "Reactivity Management and Control Instructor/Student Guide," Revision 2O-RO-03-01 -20, "Simulator Scenario, Operations Standards," Revision 0O-RO-03-02-01, "lnstructional Module - Day One Cold Reactor Startup," Revision 7O-RO-03-02-02, "lnstructional Module - Day Two Hot Reactor Startup," Revision 7O-RO-03-02-03, "lnstructional Module * Day Three Cold Reactor Startup," Revision 3O-RO-03-02-04, "lnstructional Module - Day Four Hot Reactor Startup," Revision 3O*RO-03-02-05, "lnstructional Module - Day Five Cold Reactor Startup," Revision 3O-RO-03-02-06, "lnstructional Module - Day Six Cold Reactor Startup," Revision 3O-RO-03-02-07, "lnstructional Module - Day Seven 905 Certification Practice," Revision 3O-RO-03-02-08, "lnstructional Module * Day Eight 905 Certification Practice," Revision 2O-RO-03-02-09, "lnstructional Module - Day Nine Reactor Power Operations," Revision 1O-RO-03-02-51, "lnstructional Module - SOER 90-3 Nuclear Instrument Miscalibration,"Revision 3Miscellaneous:Crew Briefing Sheet from May 10,2011 SCRAMOperations Section Standing Order 11-03OSRC Meeting 2011-008 Meeting MinutesPost-Trip Review Package from May 10,2011 SCRAM with Attachments and Supporting Data"EN-OP-116 Attachment 9,3 ITPE Supplemental Controls," developed for Post-RefuelingOutage StartupReactor Engineer's calculations pertaining to criticality prior to the reactor SCRAMeSOMS Control Room Logs from
===Procedure===
: 0510912011 through 0511112011SRM and Moderator Temperature Traces with Calculated SRM Period 0511012011Control Room Personnel Chart Dayshift 0511012011Control Rod Notch History from Reactor Critical to Reactor SCRAM 0511012011Control Rod Notch Worth Calculations for 05/1012011 Reactor StartupPower Maneuver Plan Cycle 19-01Attachment 1
(FAP) Process," Revision 0
: A-1-4SUPPLEMENTAL INFORMATION
: EN-FAP-OM-006, "Working Hour Limits for Non-Covered Workers," Revision 2
: EN-FAP-OP-008, "Reactivity Management Performance Indicator Program," Revision 0
: EN-FAP-OP-01  
: 1, "Operator Human Performance Indicator Program," Revision 0
: EN-HU-102, "Human Performance Tools," Revision 5
: EN-HU-103, "Human Performance Error Reviews," Revision 4
: EN-NS-102, "Fitness for Duty Program," Revision 9
: EN-OM-119, "On-Site Safety Review Committee," Revision 7
: EN-OM-123, "Fatigue Management Program," Revision 3
: EN-OP-103, "Reactivity Management Program," Revision 5
: EN-OP-1 15, "Conduct of Operations," Revision 10
: EN-OP-1 16, "lnfrequently Performed Tests of Evolutions," Revision 7
: EN-RE-214, "Conduct of Reactor Engineering," Revision 0
: EN-RE-215, "Reactivity Maneuver Plan," Revision 1
: EN-RE-219, "Startup sequence Criticality Controls (BWR)," Revision 0 Condition Reports:
: CR-PNP-2011-02475
and associated Root Cause Evaluation Report, Revision 1
: CR-PNP-201
: 1-02488 cR-PNP-2011-02493
cR-PNP-2011-02504
: CR-PNP-201
: 1-02506 CR-PNP-2011-02546
: CR-PNP-201
: 1-02568 CR-PNP-2011-02572
cR-PNP-2011-02577
: CR-PNP-201
: 1-03598 Self Assessments:
: LO-PNPLO-2009-00071, "Focused Assessment on Reactivity Management"
: LO-PNPLO-2010-00106, "Snapshot Assessment on Reactivity Management
===Procedure===
: Revision lmplementation"
: LO-PNPLO-2010-00106, "Snapshot Assessment on SOER 07-01 Recommendation Reactivity Management Operations Training" Technical Specifications:
: 3.5.C, "HPCI System" 3.5.D,'RCIC  
: System" 5.4.1, "PROCEDURES" Traininq Material: lnstructional Module, Reactor Startup and Criticality  
(& Main Turbine Overspeed)  
: Just in Time Training used for
: 0511012011
and
: 0511112011  
: Startup JITT Instructional Module, Reactor Startup and Criticality May 2011 Just in Time Training used for 051
: 1812011 Startup JITT Attachment
: A-1-3 SUPPLEMENTAL
: INFORMATION
: Just in Time Training PowerPoint used for 05/1812011  
: Startup JITT lnstructor Lesson Plan JITT
: RFO 18 Hydro 2.1 .8.5 Simulator
: JITT Reactor Shutdown 2.1.5 and Vessel Cooldown 2.1.7 , Revised 0410112011
: Simulator
: JITT Reactor Shutdown 2.1.5 and Vessel Cooldown 2.1 .7 , Revised 0211912011
: Training Schedules for Outage Training Cycle
: 0311412011  
-0410712011
: Training Schedules for Training Cycle 020211312011  
-0211712011
: Training Schedules for Training Cycle 01
: 1112212010 - 0112212011
: Training Records and Remediation Training for Current Licensed Operators lnitial License Class 2009-2011  
: Class Schedule O-RO-03-02, "Reactor Plant Startup Certification Unit Guide," Revision 10 O-RO-03-01-19, "Reactivity Management and Control Instructor/Student Guide," Revision 2 O-RO-03-01  
-20, "Simulator Scenario, Operations Standards," Revision 0 O-RO-03-02-01, "lnstructional Module - Day One Cold Reactor Startup," Revision 7 O-RO-03-02-02, "lnstructional Module - Day Two Hot Reactor Startup," Revision 7 O-RO-03-02-03, "lnstructional Module * Day Three Cold Reactor Startup," Revision 3 O-RO-03-02-04, "lnstructional Module - Day Four Hot Reactor Startup," Revision 3 O*RO-03-02-05, "lnstructional Module - Day Five Cold Reactor Startup," Revision 3 O-RO-03-02-06, "lnstructional Module - Day Six Cold Reactor Startup," Revision 3 O-RO-03-02-07, "lnstructional Module - Day Seven 905 Certification Practice," Revision 3 O-RO-03-02-08, "lnstructional Module * Day Eight 905 Certification Practice," Revision 2 O-RO-03-02-09, "lnstructional Module - Day Nine Reactor Power Operations," Revision 1 O-RO-03-02-51, "lnstructional Module - SOER 90-3 Nuclear Instrument Miscalibration," Revision 3 Miscellaneous:
: Crew Briefing Sheet from May 10,2011 SCRAM Operations Section Standing Order 11-03 OSRC Meeting 2011-008 Meeting Minutes Post-Trip Review Package from May 10,2011 SCRAM with Attachments and Supporting Data"EN-OP-116  
: 9,3 ITPE Supplemental Controls," developed for Post-Refueling Outage Startup Reactor Engineer's calculations pertaining to criticality prior to the reactor SCRAM eSOMS Control Room Logs from
: 0510912011
through 0511112011
: SRM and Moderator Temperature Traces with Calculated  
: SRM Period 0511012011
: Control Room Personnel Chart Dayshift 0511012011
: Control Rod Notch History from Reactor Critical to Reactor SCRAM 0511012011
: Control Rod Notch Worth Calculations for 05/1012011  
: Reactor Startup Power Maneuver Plan Cycle 19-01 Attachment
: A-1-4 SUPPLEMENTAL
: INFORMATION
==LIST OF ACRONYMS==
==LIST OF ACRONYMS==
ACRS Assistant Control Room SupervisorADAMS Agency-wide Documents Access and Management SystemAOM Assistant Operations ManagerATC At the ControlsAV Apparent ViolationBOP Balance of PlantCCDP Conditional Core Damage ProbabilityCFR Code of Federal RegulationsCR Condition ReportCRD Control Rod DriveCRS Control Room SupervisorDRP Division of Reactor ProjectsDRS Division of Reactor SafetyFFD Fitness for DutyHEP Human Error ProbabilityHPCI High Pressure Coolant InjectionHUR Heatup RateIMC lnspection Manual ChapterIPTE Infrequently Performed Tests or EvolutionsIRM Intermediate Range MonitorJITT Just in Time TrainingNRC Nuclear Regulatory CommissionOPS
ACRS Assistant
: [[MGR]] [[Operations Manager]]
Control Room Supervisor
PARS Publicly Available RecordsPD Performance DeficiencyPNPS Pilgrim Nuclear Power StationPOAH Point of Adding HeatPPC Plant Process ComputerPRA Probabilistic Risk AssessmentRCE Root Cause EvaluationRCIC Reactor Core lsolation CoolingRE Reactor EngineerRG Regulatory GuideRO Reactor OperatorRO-ATC Reactor Operator at the ControlsRPS Reactor Protection SystemSDP Significance Determination ProcessSM Shift ManagerSRI Senior Resident InspectorSRM Source Range MonitorSRO Senior Reactor OperatorSIT Special Inspection TeamSTA Shift Technical AdvisorTS Technical SpecificationAttachment 1
ADAMS Agency-wide
A-2-1SPECIAL
Documents
: [[INSPEC]] [[TION]]
Access and Management
System AOM Assistant
Operations
Manager
: [[ATC]] [[At the Controls]]
: [[AV]] [[Apparent Violation]]
: [[BOP]] [[Balance of Plant]]
CCDP Conditional
Core Damage Probability
: [[CFR]] [[Code of Federal Regulations]]
CR Condition
Report
: [[CRD]] [[Control Rod Drive]]
: [[CRS]] [[Control Room Supervisor]]
: [[DRP]] [[Division of Reactor Projects]]
: [[DRS]] [[Division of Reactor Safety]]
: [[FFD]] [[Fitness for Duty]]
: [[HEP]] [[Human Error Probability]]
: [[HPCI]] [[High Pressure Coolant Injection]]
HUR Heatup Rate IMC lnspection
Manual Chapter IPTE Infrequently
Performed
Tests or Evolutions
IRM Intermediate
Range Monitor
: [[JITT]] [[Just in Time Training]]
NRC Nuclear Regulatory
Commission
: [[OPS]] [[]]
MGR Operations
Manager PARS Publicly Available
Records PD Performance
Deficiency
: [[PNPS]] [[Pilgrim Nuclear Power Station]]
: [[POAH]] [[Point of Adding Heat]]
: [[PPC]] [[Plant Process Computer]]
PRA Probabilistic
Risk Assessment
: [[RCE]] [[Root Cause Evaluation]]
RCIC Reactor Core lsolation
Cooling
: [[RE]] [[Reactor Engineer]]
RG Regulatory
Guide
: [[RO]] [[Reactor Operator]]
RO-ATC Reactor Operator at the Controls RPS Reactor Protection
System SDP Significance
Determination
Process
: [[SM]] [[Shift Manager]]
: [[SRI]] [[Senior Resident Inspector]]
: [[SRM]] [[Source Range Monitor]]
SRO Senior Reactor Operator SIT Special Inspection
Team STA Shift Technical
Advisor TS Technical
Specification
 
A-2-1
: [[SPECIA]] [[L INSPECTION]]
: [[TEAM]] [[]]
: [[TEAM]] [[]]
: [[CHARTE]] [[RUNITED STATESN]]
: [[CHARTE]] [[R]]
: [[UNITED]] [[]]
: [[STATES]] [[N]]
: [[UCLEAR]] [[]]
: [[UCLEAR]] [[]]
: [[REGULA]] [[TORY COMMISSIONREGION I475 ALLENDALE ROADKING]]
REGULATORY
: [[COMMIS]] [[SION]]
: [[REGION]] [[I 475]]
: [[ALLEND]] [[ALE]]
: [[ROAD]] [[]]
: [[KING]] [[]]
: [[OF]] [[]]
: [[OF]] [[]]
: [[PRUSSI]] [[A.]]
: [[PRUSSI]] [[A.]]
: [[PA]] [[19406-1415]]
: [[PA]] [[19406-1415]]
: [[MEMORA]] [[NDUM TO:SPECIAL INSPECTION]]
MEMORANDUM
: [[TO]] [[: SPECIAL INSPECTION]]
: [[TEAM]] [[]]
: [[TEAM]] [[]]
: [[CHARTE]] [[RMay 13, 2011Samuel]]
CHARTER May 13, 2011 Samuel L. Hansell Jr., Manager Special Inspection
: [[L.]] [[Hansell Jr., ManagerSpecial Inspection TeamRaymond R. McKinley, LeaderSpecial Inspection TeamChristopher G. Miller, Director /]]
Team Raymond R. McKinley, Leader Special Inspection
: [[RA]] [[/Division of Reactor SafetyDarrell]]
Team Christopher
: [[G.]] [[Miller, Director /]]
: [[RA]] [[/Division of Reactor Safety Darrell]]
: [[J.]] [[Roberts, Director /]]
: [[J.]] [[Roberts, Director /]]
: [[RA]] [[by Paul Krohn Acting For/Division of Reactor ProjectsSPECIAL INSPECTION]]
: [[RA]] [[by Paul Krohn Acting For/Division of Reactor Projects SPECIAL INSPECTION]]
: [[TEAM]] [[]]
: [[TEAM]] [[]]
: [[CHARTE]] [[R -PILGRIM NUCLEAR]]
: [[CHARTE]] [[R -PILGRIM NUCLEAR]]
: [[POWER]] [[]]
: [[POWER]] [[]]
: [[STATIO]] [[N OPERATORPERFORMANCE]]
: [[STATIO]] [[N OPERATOR PERFORMANCE]]
: [[DURING]] [[]]
: [[DURING]] [[]]
: [[REACTO]] [[R STARTUPON]]
: [[REACTO]] [[R STARTUP]]
: [[MAY]] [[1Q.2011]]
: [[ON]] [[]]
: [[FROM]] [[:SUBJECT:In accordance with lnspection Manual Chapter (lMC) 0309, "Reactive Inspection DecisionBasis for Reactors," a Special Inspection Team (SlT) is being chartered to evaluate operatorperformance and organizational decision-making associated with a reactor scram that occurredduring a startup on May 10,2011, The decision to conduct this special inspection was based onmeeting the deterministic criteria (the event involved questions or concerns pertaining tolicensee operational performance) and risk criteria specified in Enclosure 1 of]]
MAY 1Q.2011 FROM: SUBJECT: In accordance
: [[IMC]] [[0309. Thecalculable increase in conditional core damage probability (]]
with lnspection
: [[CCDP]] [[), which was in the low E-6range, was based on application of an Initiating Event Analysis in Sapphire 8 due to the reactorscram, which was then modified for the conditions of the reactor when the transient occurred,The]]
Manual Chapter (lMC) 0309, "Reactive
: [[SIT]] [[will expand on the event follow-up inspection activities started by the residentinspectors and augmented by a Division of Reactor Projects (]]
Inspection
DRP) inspector who wasdispatched to the site soon after the event. The Team will review the causes of the event, andEntergy's organizational and operator response during and after the event, The Team willAttachment 2t rt *.r. i
Decision Basis for Reactors," a Special Inspection
A-2-2SPECIAL
Team (SlT) is being chartered
: [[INSPEC]] [[TION]]
to evaluate operator performance
and organizational
decision-making
associated
with a reactor scram that occurred during a startup on May 10,2011, The decision to conduct this special inspection
was based on meeting the deterministic
criteria (the event involved questions
or concerns pertaining
to licensee operational
performance)
and risk criteria specified
in Enclosure
of IMC 0309. The calculable
increase in conditional
core damage probability (CCDP), which was in the low E-6 range, was based on application
of an Initiating
Event Analysis in Sapphire 8 due to the reactor scram, which was then modified for the conditions
of the reactor when the transient
occurred, The SIT will expand on the event follow-up
inspection
activities
started by the resident inspectors
and augmented
by a Division of Reactor Projects (DRP) inspector
who was dispatched
to the site soon after the event. The Team will review the causes of the event, and Entergy's
organizational
and operator response during and after the event, The Team will Attachment
t rt *.r. i
A-2-2
: [[SPECIA]] [[L INSPECTION]]
: [[TEAM]] [[]]
: [[TEAM]] [[]]
: [[CHARTE]] [[Rperform interviews, as necessary, to understand the scope of operator actions performed duringthe event. The Team will also assess whether the]]
CHARTER perform interviews, as necessary, to understand
: [[SIT]] [[should be upgraded to an AugmentedInspection Team in accordance with]]
the scope of operator actions performed
: [[IMC]] [[0309.The inspection will be conducted in accordance with the guidance contained in]]
during the event. The Team will also assess whether the SIT should be upgraded to an Augmented Inspection
: [[NRC]] [[InspectionProcedure 93812, "Special Inspection," and an inspection report will be issued within 45 daysfollowing the final exit meeting for the inspection.The Special Inspection willcommence on May 16, 2411. The following personnel have beenassigned to this effort:Manager: Samuel L. Hansell, Jr., Branch ChiefOperations Branch,]]
Team in accordance
: [[DRS]] [[, Region ITeam Leader:Team Members:Enclosure: Special Inspection Team CharterRaymond]]
with IMC 0309.The inspection
: [[R.]] [[McKinley, Senior Emergency Response CoordinatorPlant Support Branch,]]
will be conducted
: [[DRS]] [[, Region IBrian]]
in accordance
: [[C.]] [[Haagensen, Millstone Power Station Resident InspectorDivision of Reactor Projects,]]
with the guidance contained
: [[DRP]] [[, Region IDavid]]
in NRC Inspection
: [[L.]] [[Molteni, Operations EngineerOperations Branch,]]
Procedure
DRS, Region IAttachment 2
93812, "Special Inspection," and an inspection
A-2-3SPECIAL
report will be issued within 45 days following
: [[INSPEC]] [[TION]]
the final exit meeting for the inspection.
The Special Inspection
willcommence
on May 16, 2411. The following
personnel
have been assigned to this effort: Manager: Samuel L. Hansell, Jr., Branch Chief Operations
Branch, DRS, Region I Team Leader: Team Members: Enclosure:
Special Inspection
Team Charter Raymond R. McKinley, Senior Emergency
Response Coordinator
Plant Support Branch, DRS, Region I Brian C. Haagensen, Millstone
Power Station Resident Inspector Division of Reactor Projects, DRP, Region I David L. Molteni, Operations
Engineer Operations
Branch, DRS, Region I Attachment
 
A-2-3
: [[SPECIA]] [[L INSPECTION]]
: [[TEAM]] [[]]
: [[TEAM]] [[]]
: [[CHARTE]] [[RSpecial Inspection Team CharterPilgrim Nuclear Power StationOperator Performance During ReactorStartup May 10,2011Backqround:During startup from a refueling outage, Entergy operators withdrew rods to criticality theafternoon of May 10,2011 and continued to withdraw control rods to the point of adding heat(approximately 1o/o power). While continuing to increase power, operators identified a higherthan expected heat-up rate (HUR) with a five minute average]]
CHARTER Special Inspection
: [[HUR]] [[that, if allowed to continue,would have resulted in exceeding the technical specification limit. Operators made the ControlRoom Supervisor (]]
Team Charter Pilgrim Nuclear Power Station Operator Performance
: [[CRS]] [[) and Shift Manager (SM) aware of the condition and proceeded to insertfive control rods (two notches each) to lower the]]
During Reactor Startup May 10,2011 Backqround:
: [[HUR]] [[to approximately 65"F/hr. At the time, itwas not identified by the operators, reactor engineers or management oversight in the controlroom that the control rod insertions brought the reactor to a subcritical state (approximately0.35% subcritical by later calculations). After reducing the]]
During startup from a refueling
: [[HUR]] [[, the operators (withoutrecognition of the subcritical reactor condition), proceeded to withdraw the five control rods backto their previous position. While withdrawing the fifth control rod back to its original position, thereactor experienced a full]]
outage, Entergy operators
: [[SCRAM]] [[on Intermediate Range Monitor (l]]
withdrew rods to criticality
: [[RM]] [[) Hl-Hl flux signals. Allrods inserted and equipment responded as expected.Pilgrim initially investigated potential equipment related causes for the automatic scram ascommunicated to the]]
the afternoon
: [[NRC]] [[on the afternoon of May 10,2011. Subsequent analysis revealedthat human performance errors made by the operators were the cause of the scram.]]
of May 10,2011 and continued
: [[NRC]] [[wasinformed of this in the early morning hours of May 11,2011. Entergy is continuing itsinvestigation of the operator actions taken during this event. Entergy suspended thequalifications of the operators and the Shift Manager directly involved with the event while theinvestigation continues. Additional actions have been taken by Entergy that include morerestrictive controls on reactivity additions following a negative reactivity insertion of any kind,briefing to other operating crews regarding the event, and initiation of a root cause evaluation.The Pilgrim resident inspectors and a resident inspector from a different site provided follow-upto this event under the Reactor Oversight Process (ROP) baseline inspection program,Basis for the Formation of the SIT:The]]
to withdraw control rods to the point of adding heat (approximately
: [[IMC]] [[0309 review concluded that one of the deterministic criteria was met due to questionsor concerns pertaining to licensee operational performance. This criterion was met based onhuman performance errors that occurred and led to the unanticipated automatic reactor scram.The human performance errors included:. Reactor operators were focused on monitoring heatup rate (]]
1o/o power). While continuing
HUR)without appropriatefocus on power level throughout the startup event;. Reactor operators and control room supervision did not have proper sensitivity for theimpacts from negative reactivity insertions with the reactor at low power conditions;Attachment 2
to increase power, operators
A-2-4SPECIAL
identified
: [[INSPEC]] [[TION]]
a higher than expected heat-up rate (HUR) with a five minute average HUR that, if allowed to continue, would have resulted in exceeding
the technical
specification
limit. Operators
made the Control Room Supervisor (CRS) and Shift Manager (SM) aware of the condition
and proceeded
to insert five control rods (two notches each) to lower the HUR to approximately
65"F/hr. At the time, it was not identified
by the operators, reactor engineers
or management
oversight
in the control room that the control rod insertions
brought the reactor to a subcritical
state (approximately
0.35% subcritical
by later calculations).
After reducing the HUR, the operators (without recognition
of the subcritical
reactor condition), proceeded
to withdraw the five control rods back to their previous position.
While withdrawing
the fifth control rod back to its original position, the reactor experienced
a full SCRAM on Intermediate
Range Monitor (lRM) Hl-Hl flux signals. All rods inserted and equipment
responded
as expected.Pilgrim initially
investigated
potential
equipment
related causes for the automatic
scram as communicated
to the NRC on the afternoon
of May 10,2011. Subsequent
analysis revealed that human performance
errors made by the operators
were the cause of the scram. NRC was informed of this in the early morning hours of May 11,2011. Entergy is continuing
its investigation
of the operator actions taken during this event. Entergy suspended
the qualifications
of the operators
and the Shift Manager directly involved with the event while the investigation
continues.
Additional
actions have been taken by Entergy that include more restrictive
controls on reactivity
additions
following
a negative reactivity
insertion
of any kind, briefing to other operating
crews regarding
the event, and initiation
of a root cause evaluation.
The Pilgrim resident inspectors
and a resident inspector
from a different
site provided follow-up to this event under the Reactor Oversight
Process (ROP) baseline inspection
program, Basis for the Formation
of the SIT: The IMC 0309 review concluded
that one of the deterministic
criteria was met due to questions or concerns pertaining
to licensee operational
performance.
This criterion
was met based on human performance
errors that occurred and led to the unanticipated
automatic
reactor scram.The human performance
errors included:. Reactor operators
were focused on monitoring
heatup rate (HUR)without
appropriate
focus on power level throughout
the startup event;. Reactor operators
and control room supervision
did not have proper sensitivity
for the impacts from negative reactivity
insertions
with the reactor at low power conditions;
 
A-2-4
: [[SPECIA]] [[L INSPECTION]]
: [[TEAM]] [[]]
: [[TEAM]] [[]]
: [[CHARTE]] [[R. The operators did not identify or utilize available plant indications that indicated thereactor was subcritical;. Reactor operators did not follow shift manager instructions to maintain reactor powerwithin the current]]
CHARTER. The operators
: [[IRM]] [[power band while addressing the elevated]]
did not identify or utilize available
: [[HUR]] [[;. Operators and control room supervision did not engage reactor engineering staff withregard to planned rod movement after the reactor was made subcritical; ando Prior to the identification of the unexpected HUR, reactor operators did notimplemenVenter the required abnormal operating procedure for a mispositioned controlrod (Rod 30-1 1).In accordance with]]
plant indications
: [[IMC]] [[0309, the event was evaluated for risk significance because onedeterministic criterion was met, A Region I]]
that indicated
: [[SRA]] [[evaluated the transient (reactor scram)fromlow reactor power using the Initiating Event Assessment feature of Saphire 8. The lE-Transbasic event probability was set to 1.0 and all other initiating events were set to zero. Theresulting dominant core damage sequences were subsequently evaluated by the]]
the reactor was subcritical;. Reactor operators
: [[SRA]] [[toaccount for the low reactor power conditions and alternating current (]]
did not follow shift manager instructions
: [[AC]] [[) power being suppliedby off-site sources at the time of the event. The resulting conditional core damage probability(CCDP)was conservatively estimated in the low E-6 range, which is the overlap region betweenan]]
to maintain reactor power within the current IRM power band while addressing
: [[SIT]] [[and No Additional inspection required. The dominant core damage sequences involvefailure of direct current (]]
the elevated HUR;. Operators
DC) power sources and failure of residual heat removal. However, withthe low decay heat load following the refuel outage, these core damage sequences represent aconservative estimate of risk.Additionally, this event involved multiple licensed operators not recognizing the reactivity statusof an operating reactor during startup and demonstrating a poor understanding of reactorphysics in a low power condition. In light of the aforementioned human performance errors, andconsistent with the risk evaluation and Section 4.04, Region I has decided to initiate an SlT.Obiectives of the Special Inspection:The Team will review the causes of the event, and Entergy's organizational and operatorresponse during and following the event. The Team will perform interviews, as necessary, tounderstand the scope of operator actions performed during the event.To accomplish these objectives, the Team will:1. Develop a complete sequence of events including follow-up actions taken byEntergy, and the sequence of communications within Entergy and to the NRCsubsequent to the event;2. Review and assess crew operator performance and crew decision making, includingadherence to expected roles and responsibilities, the use of the command andcontrol elements associated with reactivity manipulations, the use of procedures, theuse of diverse instrumentation to assess plant conditions, response to alarms andoverall implementation of operations department and station standards;Attachment 2
and control room supervision
A-2-5SPECIAL
did not engage reactor engineering
: [[INSPEC]] [[TION]]
staff with regard to planned rod movement after the reactor was made subcritical;
and o Prior to the identification
of the unexpected
HUR, reactor operators
did not implemenVenter
the required abnormal operating
procedure
for a mispositioned
control rod (Rod 30-1 1).In accordance
with IMC 0309, the event was evaluated
for risk significance
because one deterministic
criterion
was met, A Region I SRA evaluated
the transient (reactor scram)from
low reactor power using the Initiating
Event Assessment
feature of Saphire 8. The lE-Trans basic event probability
was set to 1.0 and all other initiating
events were set to zero. The resulting
dominant core damage sequences
were subsequently
evaluated
by the SRA to account for the low reactor power conditions
and alternating
current (AC) power being supplied by off-site sources at the time of the event. The resulting
conditional
core damage probability (CCDP)was
conservatively
estimated
in the low E-6 range, which is the overlap region between an SIT and No Additional
inspection
required.
The dominant core damage sequences
involve failure of direct current (DC) power sources and failure of residual heat removal. However, with the low decay heat load following
the refuel outage, these core damage sequences
represent
a conservative
estimate of risk.Additionally, this event involved multiple licensed operators
not recognizing
the reactivity
status of an operating
reactor during startup and demonstrating
a poor understanding
of reactor physics in a low power condition.
In light of the aforementioned
human performance
errors, and consistent
with the risk evaluation
and Section 4.04, Region I has decided to initiate an SlT.Obiectives
of the Special Inspection:
The Team will review the causes of the event, and Entergy's
organizational
and operator response during and following
the event. The Team will perform interviews, as necessary, to understand
the scope of operator actions performed
during the event.To accomplish
these objectives, the Team will: 1. Develop a complete sequence of events including
follow-up
actions taken by Entergy, and the sequence of communications
within Entergy and to the NRC subsequent
to the event;2. Review and assess crew operator performance
and crew decision making, including adherence
to expected roles and responsibilities, the use of the command and control elements associated
with reactivity
manipulations, the use of procedures, the use of diverse instrumentation
to assess plant conditions, response to alarms and overall implementation
of operations
department
and station standards;
 
A-2-5
: [[SPECIA]] [[L INSPECTION]]
: [[TEAM]] [[]]
: [[TEAM]] [[]]
: [[CHARTE]] [[REvaluate the extent of condition with respect to the other crews;Review the adequacy of operator requalification training as it relates to this event,including the integration of newly licensed operators into the operator requalificationtraining program;Review the adequacy of the preparation by the operations staff for the reactor startupincluding training prior to the evolution and briefings by the operations staff.Review the adequacy of the simulator to model the behavior of the current reactorcore during startup activities and the current adequacy of the simulator for use inreactor startup training ;Assess the decision making and actions taken by the operators and stationmanagement during the initial and subsequent reactor startup to determine if thereare any implications related to safety culture;Review and assess the effectiveness of Entergy's response to this event andcorrective actions taken to date. This includes overall organizational response, andadequacy of immediate, interim and proposed longterm corrective actions. This willalso include evaluation of the root cause analysis when developed by the licensee;9. Review the adequacy of the Entergy and Site fitness for duty processes andprocedures when a human performance error has occurred;10. Evaluate Entergy's application of pertinent industry operating experience, includingINPO]]
CHARTER Evaluate the extent of condition
with respect to the other crews;Review the adequacy of operator requalification
training as it relates to this event, including
the integration
of newly licensed operators
into the operator requalification
training program;Review the adequacy of the preparation
by the operations
staff for the reactor startup including
training prior to the evolution
and briefings
by the operations
staff.Review the adequacy of the simulator
to model the behavior of the current reactor core during startup activities
and the current adequacy of the simulator
for use in reactor startup training ;Assess the decision making and actions taken by the operators
and station management
during the initial and subsequent
reactor startup to determine
if there are any implications
related to safety culture;Review and assess the effectiveness
of Entergy's
response to this event and corrective
actions taken to date. This includes overall organizational
response, and adequacy of immediate, interim and proposed longterm corrective
actions. This will also include evaluation
of the root cause analysis when developed
by the licensee;9. Review the adequacy of the Entergy and Site fitness for duty processes
and procedures
when a human performance
error has occurred;10. Evaluate Entergy's
application
of pertinent
industry operating
experience, including
: [[INPO]] [[]]
: [[SOER]] [[10-2, "Engaged, Thinking Organizations,"]]
: [[SOER]] [[10-2, "Engaged, Thinking Organizations,"]]
INPO SOER 07-1, "ReactivityManagement," and other recent events involving reactivity management errors toassess the effectiveness of any actions taken in response to the operatingexperience; and11. Document the inspection findings and conclusions in a Special Inspection Team finalreport within 45 days of inspection completion.Guidance:Inspection Procedure 93812, "Special Inspection", provides additional guidance to be used bythe SlT. Team duties will be as described in Inspection Procedure 93812. The inspectionshould emphasize fact-finding in its review of the circumstances surrounding the event. Safetyconcerns identified that are not directly related to the event should be reported to the Region Ioffice for appropriate action.The Team will conduct an entrance meeting and begin the inspection on May 16,2011. Whileon-site, the Team Leader will provide daily briefings to Region I management, who willcoordinate with the Office of Nuclear Reactor Regulation to ensure that all other pertinentparties are kept informed. The Team will also coordinate with the Region I State Liaison OfficerAttachment 23.4.5.6.7.8.
: [[INPO]] [[]]
A-2-6SPECIAL
SOER 07-1, "Reactivity
: [[INSPEC]] [[TION]]
Management," and other recent events involving
reactivity
management
errors to assess the effectiveness
of any actions taken in response to the operating experience;
and 11. Document the inspection
findings and conclusions
in a Special Inspection
Team final report within 45 days of inspection
completion.
Guidance: Inspection
Procedure
93812, "Special Inspection", provides additional
guidance to be used by the SlT. Team duties will be as described
in Inspection
Procedure
93812. The inspection
should emphasize
fact-finding
in its review of the circumstances
surrounding
the event. Safety concerns identified
that are not directly related to the event should be reported to the Region I office for appropriate
action.The Team will conduct an entrance meeting and begin the inspection
on May 16,2011. While on-site, the Team Leader will provide daily briefings
to Region I management, who will coordinate
with the Office of Nuclear Reactor Regulation
to ensure that all other pertinent parties are kept informed.
The Team will also coordinate
with the Region I State Liaison Officer Attachment
3.4.5.6.7.8.
A-2-6
: [[SPECIA]] [[L INSPECTION]]
: [[TEAM]] [[]]
: [[TEAM]] [[]]
: [[CHARTE]] [[Rto implement the Memorandum of Understanding between the]]
CHARTER to implement
: [[NRC]] [[and the State ofMassachusetts to offer observation of the inspection by representatives of the state. A reportdocumenting the results of the inspection will be issued within 45 days following the final exitmeeting for the inspection.Before the end of the first day onsite, the Team Manager shall provide a recommendation to theRegional Administrator as to whether the]]
the Memorandum
SIT should continue or be upgraded to an AugmentedInspection Team response.This Charter may be modified should the Team develop significant new information thatwarrants review.Attachment 2
of Understanding
A,3-1DETAILED
between the NRC and the State of Massachusetts
: [[SEQUEN]] [[CE]]
to offer observation
of the inspection
by representatives
of the state. A report documenting
the results of the inspection
will be issued within 45 days following
the final exit meeting for the inspection.
Before the end of the first day onsite, the Team Manager shall provide a recommendation
to the Regional Administrator
as to whether the SIT should continue or be upgraded to an Augmented Inspection
Team response.This Charter may be modified should the Team develop significant
new information
that warrants review.Attachment  
 
A,3-1
: [[DETAIL]] [[ED SEQUENCE]]
: [[OF]] [[]]
: [[OF]] [[]]
: [[EVENTS]] [[May 10,2011, Reactor Scram EventThe team constructed the sequence of events from a review of control room narrative logs, plantprocess computer (PPC) data (alarm printout, sequence of event printout, plant parametergraphs) and plant personnel interviews.TimeEvent05/09/11TwoSessionsJust In Time Training (JITT) was conducted for the reactor startup. Certain keymembers of the operating crew that were directly involved with this event were notpresent for the training including the Shift Manager (SM), the Assistant ControlRoom Supervisor (ACRS) who temporarily relieved the Control Room Supervisor(CRS) prior to the scram, and the Reactor Operator who was at the controls (RO-ATC)when the scram occurred.05/10/1 10626The reactor mode switch was moved to the startup position.-0630The oncoming day shift operators received a reactor maneuvering plan briefing.The Reactor Engineers (REs) led the brief.0641Operators commenced control rod withdrawal.0700The day shift operating crew assumed the shift, and control rod withdraw continues.1212The reactor became critical.1227The point of adding heat was reached.-1231The]]
EVENTS May 10,2011, Reactor Scram Event The team constructed
the sequence of events from a review of control room narrative
logs, plant process computer (PPC) data (alarm printout, sequence of event printout, plant parameter graphs) and plant personnel
interviews.
Time Event 05/09/11 Two Sessions Just In Time Training (JITT) was conducted
for the reactor startup. Certain key members of the operating
crew that were directly involved with this event were not present for the training including
the Shift Manager (SM), the Assistant
Control Room Supervisor (ACRS) who temporarily
relieved the Control Room Supervisor (CRS) prior to the scram, and the Reactor Operator who was at the controls (RO-ATC)when the scram occurred.05/10/1 1 0626 The reactor mode switch was moved to the startup position.-0630 The oncoming day shift operators
received a reactor maneuvering
plan briefing.The Reactor Engineers (REs) led the brief.0641 Operators
commenced
control rod withdrawal.
0700 The day shift operating
crew assumed the shift, and control rod withdraw continues.
212 The reactor became critical.1227 The point of adding heat was reached.-1231 The
: [[CRS]] [[was relieved for lunch by the]]
: [[CRS]] [[was relieved for lunch by the]]
: [[ACRS.]] [[The oncoming]]
ACRS. The oncoming CRS providing
: [[CRS]] [[providing therelief did not receive Just In Time Training (]]
the relief did not receive Just In Time Training (JITT), nor did he participate
: [[JITT]] [[), nor did he participate in thereactor maneuvering plan briefing.-1231The RO-ATC was relieved for lunch by the Licensed Operator previously assignedas the]]
in the reactor maneuvering
: [[ATC]] [[verifier. The oncoming]]
plan briefing.-1231 The RO-ATC was relieved for lunch by the Licensed Operator previously
: [[RO]] [[-ATC providing the relief did not receive JustIn Time Training (JITT), but he did participate in the reactor maneuvering planbriefing.-1231A Licensed Operator previously assigned to other startup activities was reassignedto fill the role of]]
assigned as the ATC verifier.
: [[ATC]] [[verifier. This individual received]]
The oncoming RO-ATC providing
: [[JITT]] [[training, and he alsoreceived a separate reactor maneuvering plan briefing from a]]
the relief did not receive Just In Time Training (JITT), but he did participate
: [[RE]] [[upon arriving towork at approximately 1 100.1246The]]
in the reactor maneuvering
RO-ATC withdrew 5 rods 2 notches to establish a heat-up rate.Attachment 3
plan briefing.-1231 A Licensed Operator previously
A-3-2DETAILED
assigned to other startup activities
: [[SEQUEN]] [[CE]]
was reassigned
to fill the role of ATC verifier.
This individual
received JITT training, and he also received a separate reactor maneuvering
plan briefing from a RE upon arriving to work at approximately
100.1246 The RO-ATC withdrew 5 rods 2 notches to establish
a heat-up rate.Attachment  
 
A-3-2
: [[DETAIL]] [[ED SEQUENCE]]
: [[OF]] [[]]
: [[OF]] [[]]
: [[EVENTS]] [[TimeEvent1255The RO-ATC attempts to withdraw control rod 30-11 from position 08 to position 10using single notch control, but the control rod does not move, The RO-ATC raiseddrive water pressure and attempted several notch withdraw commands, but thecontrol rod failed to move.1257The RO-ATC attempts to withdraw control rod 30-1 1 from position 08 to position 10using a "double clutch" maneuver, but the control rod incorrectly inserted one notchto position 06. The RO-ATC does not discuss the control rod mispositioning errorwith the crew.1257The]]
EVENTS Time Event 1255 The RO-ATC attempts to withdraw control rod 30-11 from position 08 to position 10 using single notch control, but the control rod does not move, The RO-ATC raised drive water pressure and attempted
several notch withdraw commands, but the control rod failed to move.1257 The RO-ATC attempts to withdraw control rod 30-1 1 from position 08 to position 10 using a "double clutch" maneuver, but the control rod incorrectly
inserted one notch to position 06. The RO-ATC does not discuss the control rod mispositioning
error with the crew.1257 The
: [[ATC]] [[verifier and]]
: [[ATC]] [[verifier and]]
: [[CRS]] [[also saw control rod 30-11 move incorrectly to position06, but the control rod mispositioning error is not discussed.1302The RO-ATC then withdraws control rod 30-11 from position 06 to position 12.-1 305The crew observes that the 5 minute average reactor coolant heat-up rate is 18"Fover the 5 minute period, and the crew determines that this corresponded to a216'Flhour heat-up rate. In actuality, the 5 minute average heat-up rate reflectedthe instantaneous heat-up rate. The actual hourly heat-up rate was 50'F/hour.The crew informs the]]
CRS also saw control rod 30-11 move incorrectly
: [[SM]] [[of the perceived heat-up rate.-1 306The]]
to position 06, but the control rod mispositioning
: [[SM]] [[directed the RO-ATC to insert control rods to reduce the heat-up rate, butthe]]
error is not discussed.
: [[SM]] [[did not specify the number of control rods or notches to insert.1307The]]
1302 The RO-ATC then withdraws
: [[RO]] [[-ATC begins to drive 5 rods 2 notches into the core to the reduce heatuprate.-1 308The]]
control rod 30-11 from position 06 to position 12.-1 305 The crew observes that the 5 minute average reactor coolant heat-up rate is 18"F over the 5 minute period, and the crew determines
that this corresponded
to a 216'Flhour
heat-up rate. In actuality, the 5 minute average heat-up rate reflected the instantaneous
heat-up rate. The actual hourly heat-up rate was 50'F/hour.
The crew informs the SM of the perceived
heat-up rate.-1 306 The
: [[SM]] [[directed the]]
: [[RO]] [[-ATC to insert control rods to reduce the heat-up rate, but the]]
: [[SM]] [[did not specify the number of control rods or notches to insert.1307 The]]
: [[RO]] [[-ATC begins to drive 5 rods 2 notches into the core to the reduce heatup rate.-1 308 The]]
: [[RE]] [[question the]]
: [[RE]] [[question the]]
: [[SM]] [[regarding the decision to insert control rods, and the SMtold the]]
SM regarding
: [[RE]] [[that the insertion was needed to control the heat-up rate. There wasno further discussion.-1 309The Assistant Operations Manager (]]
the decision to insert control rods, and the
: [[AOM]] [[-Shift) cautioned the]]
: [[SM]] [[told the]]
: [[SM]] [[that there wasthe potential to drive the reactor sub-critical by inserting control rods and that theyneeded to be careful. The]]
REs that the insertion
: [[SM]] [[also recalled being concerned about the potential todrive the reactor sub-critical. The operating crew at the controls was not madeaware of these concerns.1310Control rod insertion is stopped. The control rods are now at the same position aswhen the reactor initially became critical; however, moderator temperature is now40"F higher than it was at initial criticality. The higher moderator temperature inconjunction with the control rod insertion rendered the reactor sub-critical, but theoperators were not aware of this.-1310The]]
was needed to control the heat-up rate. There was no further discussion.
-1 309 The Assistant
Operations
Manager (AOM-Shift)
cautioned
the SM that there was the potential
to drive the reactor sub-critical
by inserting
control rods and that they needed to be careful. The SM also recalled being concerned
about the potential
to drive the reactor sub-critical.
The operating
crew at the controls was not made aware of these concerns.1310 Control rod insertion
is stopped. The control rods are now at the same position as when the reactor initially
became critical;
however, moderator
temperature
is now 40"F higher than it was at initial criticality.
The higher moderator
temperature
in conjunction
with the control rod insertion
rendered the reactor sub-critical, but the operators
were not aware of this.-1310 The
: [[SM]] [[left the control room to take a break, and the]]
: [[SM]] [[left the control room to take a break, and the]]
AOM-Shift left the controlsarea to get his lunch in the control room kitchen.Attachment 3
AOM-Shift
A-3-3DETAILED
left the controls area to get his lunch in the control room kitchen.Attachment  
: [[SEQUEN]] [[CE]]
 
A-3-3
: [[DETAIL]] [[ED SEQUENCE]]
: [[OF]] [[]]
: [[OF]] [[]]
: [[EVENTS]] [[TimeEvent-1311The operators range down the Intermediate Range Monitors (lRMs)two decadesfrom Range 8 to Range 6 in response to the lowering neutron flux.-1312The original]]
EVENTS Time Event-1311 The operators
range down the Intermediate
Range Monitors (lRMs)two
decades from Range 8 to Range 6 in response to the lowering neutron flux.-1312 The original
: [[CRS]] [[returns from break and resumes duties as]]
: [[CRS]] [[returns from break and resumes duties as]]
: [[CRS]] [[as well asresponsibility for the reactivity maneuver as the Reactivity SRO.1313After observing a O"F/hour heat-up rate, the]]
CRS as well as responsibility
for the reactivity
maneuver as the Reactivity
SRO.1313 After observing
a O"F/hour heat-up rate, the
: [[CRS]] [[directs the]]
: [[CRS]] [[directs the]]
: [[RO]] [[-ATC to resumecontrol rod withdrawalto establish a positive heat-up rate. The RO-ATC begins towithdraw 5 rods 2 notches each to restore the heat-up rate.1315While notch withdrawing control rod 14-19 from position 08 to position 12, IRMreadings begin to rise again requiring the operators to range up on the lRMs inresponse to the rising neutron flux. The reactor has returned to a critical condition,but the operators are not aware of the change in reactor status with regards tocriticality.1316The RO-ATC notch withdraws control rod 22-43 from position 08 to position 12resulting in a more rapid rise in]]
RO-ATC to resume control rod withdrawalto
: [[IRM]] [[readings, The reactor period was calculated tobe 40 seconds during the post trip review.-1318The]]
establish
: [[RO]] [[-ATC attempts to notch withdraw control rod 30-11 from position 08 toposition 10 resulting in a sharp rise in]]
a positive heat-up rate. The RO-ATC begins to withdraw 5 rods 2 notches each to restore the heat-up rate.1315 While notch withdrawing
: [[IRM]] [[readings.1318The reactor automatically scrammed on]]
control rod 14-19 from position 08 to position 12, IRM readings begin to rise again requiring
: [[IRM]] [[high-high flux level prior to completingthe withdrawal of rod 30-1 1 to position 10. Post event analysis determined that thereactor period was approximately 20 seconds, and that the scram occurred atapproximately 1.7o/o equivalent Average Power Range Monitor (APRM) power.-1320The]]
the operators
: [[RE]] [[stated that he recognized that the operators had caused the reactor scramby withdrawing rods to criticality.1 345The crew debriefed the events leading up to the reactor scram.-1400The]]
to range up on the lRMs in response to the rising neutron flux. The reactor has returned to a critical condition, but the operators
: [[RE]] [[participated in a conference call with the fuels group in Jackson (corporatereactor engineering staff) to discuss the event. The]]
are not aware of the change in reactor status with regards to criticality.
: [[RE]] [[informed the conferencecall participants that the reactor scram had been caused by human error.-1 600The]]
1316 The RO-ATC notch withdraws
: [[RE]] [[participated in a conference callwith General Electric (GE) to discuss theevent.-1 630The]]
control rod 22-43 from position 08 to position 12 resulting
: [[RE]] [[informed the Director of Engineering that the reactor scram was caused byhuman error.-1 700The]]
in a more rapid rise in IRM readings, The reactor period was calculated
: [[RE]] [[informed the General Manager Plant Operations (GMPO) that the reactorscram was caused by human error. The]]
to be 40 seconds during the post trip review.-1318 The RO-ATC attempts to notch withdraw control rod 30-11 from position 08 to position 10 resulting
in a sharp rise in IRM readings.1318 The reactor automatically
scrammed on IRM high-high
flux level prior to completing
the withdrawal
of rod 30-1 1 to position 10. Post event analysis determined
that the reactor period was approximately
seconds, and that the scram occurred at approximately
1.7o/o equivalent
Average Power Range Monitor (APRM) power.-1320 The RE stated that he recognized
that the operators
had caused the reactor scram by withdrawing
rods to criticality.
345 The crew debriefed
the events leading up to the reactor scram.-1400 The RE participated
in a conference
call with the fuels group in Jackson (corporate
reactor engineering
staff) to discuss the event. The RE informed the conference
call participants
that the reactor scram had been caused by human error.-1 600 The RE participated
in a conference
callwith General Electric (GE) to discuss the event.-1 630 The RE informed the Director of Engineering
that the reactor scram was caused by human error.-1 700 The
: [[RE]] [[informed the General Manager Plant Operations (]]
: [[GMPO]] [[) that the reactor scram was caused by human error. The]]
: [[GMPO]] [[asked the]]
: [[GMPO]] [[asked the]]
RE to draft a memodescribing what happened and send it to him.Attachment 3
RE to draft a memo describing
A-3-4TimeEvent1730The
what happened and send it to him.Attachment  
: [[GMPO]] [[met with the Operations Manager (]]
 
: [[OPS]] [[MGR) and the operatorsinvolved in the re-criticality to discuss the events.-1 900After shift turnover, the Assistant Operations Manager (AOM) recognized thathuman error was the cause of the scram. Equipment issues had been ruled out.-1 930To*2200The]]
A-3-4 Time Event 1730 The GMPO met with the Operations
Manager (OPS MGR) and the operators involved in the re-criticality
to discuss the events.-1 900 After shift turnover, the Assistant
Operations
Manager (AOM) recognized
that human error was the cause of the scram. Equipment
issues had been ruled out.-1 930 To*2200 The
: [[GMPO]] [[recalls meeting with the]]
: [[GMPO]] [[recalls meeting with the]]
: [[OPS]] [[MGR,]]
OPS MGR, RE and corporate
: [[RE]] [[and corporate core designgroup to discuss issues associated with the scram. The]]
core design group to discuss issues associated
: [[GMPO]] [[indicated that histeam was certain that the scram was caused by a human performance / knowledgedeficiency problem.-2330The Operations Manager (OPS MGR) prepared a written briefing for the crew onthe event.5t111110030An On-site Safety Review Committee (OSRC) conference callwas convened toreview the event and evaluate a recommendation to restart the reactor.01 30The]]
with the scram. The GMPO indicated
: [[OSRC]] [[recommended restarting the reactor. The]]
that his team was certain that the scram was caused by a human performance  
: [[GMPO]] [[was briefed regardingthe]]
/ knowledge deficiency
: [[OSRC]] [[recommendations.0200The]]
problem.-2330 The Operations
: [[GMPO]] [[approved restarting the reactor. He directed the]]
Manager (OPS MGR) prepared a written briefing for the crew on the event.5t11111 0030 An On-site Safety Review Committee (OSRC) conference
callwas convened to review the event and evaluate a recommendation
to restart the reactor.01 30 The OSRC recommended
restarting
the reactor. The
: [[GMPO]] [[was briefed regarding the]]
OSRC recommendations.
200 The GMPO approved restarting
the reactor. He directed the
: [[OPS]] [[]]
: [[OPS]] [[]]
: [[MGR]] [[to call theNRC Senior Resident lnspector (SRl).0200The]]
: [[MGR]] [[to call the]]
: [[NRC]] [[Senior Resident lnspector (]]
: [[SR]] [[l).0200 The]]
: [[OPS]] [[]]
: [[OPS]] [[]]
: [[MGR]] [[called the]]
: [[MGR]] [[called the]]
Line 243: Line 964:
: [[OPS]] [[]]
: [[OPS]] [[]]
: [[MGR]] [[informed the]]
: [[MGR]] [[informed the]]
: [[SRI]] [[that the cause of the scram was due to human error.0215The]]
: [[SRI]] [[that the cause of the scram was due to human error.0215 The]]
: [[SRI]] [[called the]]
: [[SRI]] [[called the]]
: [[NRC]] [[Region I Division of Reactor Projects (DRP) Branch Chiefto inform him of the decision to restart the plant. The]]
NRC Region I Division of Reactor Projects (DRP) Branch Chief to inform him of the decision to restart the plant. The SRI then responded
: [[SRI]] [[then responded to thesite to observe the startup.-0300The reactor mode switch was placed in the startup position.-0300The]]
to the site to observe the startup.-0300 The reactor mode switch was placed in the startup position.-0300 The
: [[SRI]] [[arrives onsite.*0300The]]
: [[SRI]] [[arrives onsite.*0300 The]]
: [[DRP]] [[Branch Chief called the]]
: [[DRP]] [[Branch Chief called the]]
: [[GMPO]] [[to discuss the decision to restart thereactor.DETAILED SEQUENCE]]
: [[GMPO]] [[to discuss the decision to restart the reactor.]]
: [[DETAIL]] [[ED SEQUENCE]]
: [[OF]] [[]]
: [[OF]] [[]]
EVENTSAttachment 3
EVENTS Attachment
A-4-1IMC 0609,
 
: [[APPEND]] [[IX M,Qualitative Decision-Making Attributes forTABLE 4.1NRC Management ReviewDecision AttributeApplicabletoDecision?Basis for Input to Decision - Provide qualitativeand/or quantitative information for managementreview and decision making.Finding can be boundedusing qualitative and/orquantitative information?NoIMC 0609 Appendix G is not appropriate since theconditions for reactor shutdown operations were notmet. The at-power safety Significance DeterminationProcess,]]
A-4-1
: [[IMC]] [[0609 Appendix A, quantitative analysismethodology is not adequate to provide reasonableestimates of the finding's significance. Furthermore, the]]
: [[SDP]] [[does not model errors of commission and doesnot provide a method of accurately estimating changesto the human error probabilities caused for errors ofomission. As a result, no quantitative risk evaluationcan be performed for this finding.lmproper use and execution of procedures coupled withweak work control practices has the potential toincrease the human error probability (HEP) for creditedoperator actions. The probabilistic risk assessmentmodels are highly sensitive to small variations in HEPchanges. The existing]]
: [[PRA]] [[research does not currentlysupport a method for varying the performance shapingfactors in response to defined error forcing contexts. ltis not possible to calculate a valid single point riskestimate. Human performance is a very largecontributor to]]
: [[PRA]] [[uncertainty.Defense-in-Depthaffected?YesThe term "defense in depth" is commonly associatedwith the maintenance of the integrity and independenceof the three fission product barriers as well asemergency response actions. In addition, redundantand diverse safety systems, including trained licensedoperators conducting operations in accordance withapproved station procedures that were developedunder an approved quality control program are integralto maintaining a "defense in depth." While an automaticreactor scram was initiated as designed to protect thecore during this event, the fuel barrier was not actuallycompromised by the crew's actions since the automaticprotective action was successful.However, this performance deficiency revealedorganizational and human performance weaknesseswhich eroded defense in depth. The operating crewAttachment 4]]
: [[IMC]] [[0609,]]
: [[IMC]] [[0609,]]
: [[APPEND]] [[IX M,]]
APPENDIX M, Qualitative
: [[TABLE]] [[4.1plays a vital role in the maintenance of "defense indepth" from the perspective that they directly operatestation controls. Human errors can lead toconsequences that have the potential to compromisethe three fission product barriers. The commission ofmultiple unforeseen human errors in a short period oftime during the reactor startup degraded the operator'sperformance as an important "defense in depth" barrier.These operator human performance errors resulted in achallenge to the automatic Reactor Protection Systemwhich successfully terminated the event in thisparticular case.Performance Deficiencyeffect on the SafetyMargin maintained?YesThis performance deficiency had the potential toadversely affect the margin of safety. In this particularevent, the failure to implement conduct of operationsand reactivity control standards and procedures led to areactor protection set-point being exceeded, causing areactor scram. In fact, non-conservative operatoractions led to an unrecognized subcriticality followed byan unrecognized return to criticality. These operatoractions caused a rapid rise in neutron flux and reactorpower such that the]]
Decision-Making
: [[IRM]] [[Hl-Hl neutron flux reactor tripset point was exceeded resulting in an automaticreactor scram,In this case, the]]
Attributes
for
: [[TABLE]] [[4.1]]
NRC Management
Review Decision Attribute Applicable
to Decision?Basis for Input to Decision - Provide qualitative
and/or quantitative
information
for management
review and decision making.Finding can be bounded using qualitative
and/or quantitative
information?
No IMC 0609 Appendix G is not appropriate
since the conditions
for reactor shutdown operations
were not met. The at-power safety Significance
Determination
Process, IMC 0609 Appendix A, quantitative
analysis methodology
is not adequate to provide reasonable
estimates
of the finding's
significance.
Furthermore, the SDP does not model errors of commission
and does not provide a method of accurately
estimating
changes to the human error probabilities
caused for errors of omission.
As a result, no quantitative
risk evaluation
can be performed
for this finding.lmproper use and execution
of procedures
coupled with weak work control practices
has the potential
to increase the human error probability (HEP) for credited operator actions. The probabilistic
risk assessment
models are highly sensitive
to small variations
in
: [[HEP]] [[changes. The existing]]
PRA research does not currently support a method for varying the performance
shaping factors in response to defined error forcing contexts.
lt is not possible to calculate
a valid single point risk estimate.
Human performance
is a very large contributor
to PRA uncertainty.
Defense-in-Depth
affected?Yes The term "defense in depth" is commonly associated
with the maintenance
of the integrity
and independence
of the three fission product barriers as well as emergency
response actions. In addition, redundant and diverse safety systems, including
trained licensed operators
conducting
operations
in accordance
with approved station procedures
that were developed under an approved quality control program are integral to maintaining
a "defense in depth." While an automatic reactor scram was initiated
as designed to protect the core during this event, the fuel barrier was not actually compromised
by the crew's actions since the automatic protective
action was successful.
However, this performance
deficiency
revealed organizational
and human performance
weaknesses
which eroded defense in depth. The operating
crew Attachment
: [[IMC]] [[0609,]]
APPENDIX M, TABLE 4.1 plays a vital role in the maintenance
of "defense in depth" from the perspective
that they directly operate station controls.
Human errors can lead to consequences
that have the potential
to compromise
the three fission product barriers.
The commission
of multiple unforeseen
human errors in a short period of time during the reactor startup degraded the operator's
performance
as an important "defense in depth" barrier.These operator human performance
errors resulted in a challenge
to the automatic
Reactor Protection
System which successfully
terminated
the event in this particular
case.Performance
Deficiency
effect on the Safety Margin maintained?
Yes This performance
deficiency
had the potential
to adversely
affect the margin of safety. In this particular
event, the failure to implement
conduct of operations
and reactivity
control standards
and procedures
led to a reactor protection
set-point
being exceeded, causing a reactor scram. In fact, non-conservative
operator actions led to an unrecognized
subcriticality
followed by an unrecognized
return to criticality.
These operator actions caused a rapid rise in neutron flux and reactor power such that the IRM Hl-Hl neutron flux reactor trip set point was exceeded resulting
in an automatic reactor scram, In this case, the
: [[IRM]] [[Hl-Hl neutron flux]]
: [[IRM]] [[Hl-Hl neutron flux]]
: [[RPS]] [[protectivefunction successfully terminated the event andprevented exceeding fuel barrier design safety marginand the potential for subsequent fuel barrier damage. ltshould also be noted that the Average Power RangeMonitor (APRM) Low Power]]
RPS protective
: [[RPS]] [[set point wasavailable as a backup to the]]
function successfully
: [[IRM]] [[trip function. TheAPRM Low Power set point will initiate a reactor scramat less than or equal to 15% power whenever the modeswitch is]]
terminated
: [[NOT]] [[in "]]
the event and prevented
RUN".While there was no reduction in the quantitative designmargin, there was a qualitative reduction in the safetymargin as there is an expectation that the operators willmaintain an understanding of the status of the reactorand approach criticality in a deliberate and carefullycontrolled manner. ln this case, the operators lostsituational awareness regarding the status of thereactor and subsequently initiated incorrect actions thatled to an unrecognized subcriticality followed by anAttachment 4
exceeding
A-4-3unrecognized return to criticality resulting in anautomatic reactor scram.The extent theperformance deficiencyaffects other eq uipment.YesThe inspectors reviewed the Entergy root causeevaluation team report and determined that theunderlying causes of this performance deficiency existacross the Operations organization, This includesweaknesses in oversight, human performancebehaviors, as well as operator knowledge, skills, andabilities deficiencies associated with low power reactorphysics and operations in the
fuel barrier design safety margin and the potential
: [[IRM]] [[range. lt should benoted that the performance deficiency did not degradephysical plant equipment; however, the requirementthat licensed operators conduct licensed activities inaccordance with station approved procedures is integralto maintaining plant safety. Faulty operatorperformance has the potential to adversely affect plantequipment.Degree of degradation offailed or unavailablecomponent(s).N/]]
for subsequent
: [[AN]] [[/APeriod of time (exposuretime) effect on theperformance deficiency.YesWith respect to the issues underlying this performancedeficiency, the exposure time is indeterminate, butclearly developed over an extended period of time.The Entergy root cause evaluation team determinedthat the causal factors for the event had existed for aconsiderable period of time, but they did not quantifythe exposure time, A number of condition reports werewritten over the last year, including a Fleet Assessmentperformed in February 2011, which identified shortfallsin oversight and adherence to conduct of operationshuman performance standards.This assessment is complicated by the fact that therewere not any apparent significant licensed operatorperformance issues at Pilgrim before this event. ln theHuman Performance cross-cutting area, none of theaspects currently has a theme, nor has there been atheme in the recent past. The behaviors outlined by theperformance deficiency have not been observed by theresident inspector staff prior to this event.IMC 0609, APPENDIX M,]]
fuel barrier damage. lt should also be noted that the Average Power Range Monitor (APRM) Low Power RPS set point was available
: [[TABLE]] [[4.1Attachment 4]]
as a backup to the IRM trip function.
IMC 0609, APPENDIX M, TABLE 4.1The likelihood that thelicensee's recoveryactions wouldsuccessfully mitigate theperformance deficiency.YesAlthough "recovery actions" do not equate to "correctiveactions," this section lends itself to a discussion oflicensee corrective action in that completion of theseactions would mitigate the performance deficiency.The licensee's root cause analysis was thorough andappeared to identify all underlying causal factors. Theassociated proposed corrective actions appear toadequately address the undedying causal factors.Short term corrective actions have been completed tocorrect the specific issues associated with this event.Longer term corrective actions are in progress toaddress programmatic weakness in training and humanperformance behaviors.Additional qualitativecircumstancesassociated with thefinding that regionalmanagement shouldconsider in theevaluation process.YesIn this event, there were a significant number of lapsesin operator human performance fundamentals asdescribed in the conduct of operations and reactivitycontrol standards and procedures. These lapses inhuman performance fundamentals degraded individualoperator performance, crew performance, as well asmanagement oversight performance. The lack ofenforcement of, and adherence to, the conduct ofoperations and reactivity control standards andprocedures were identified as the root cause of thereactor scram event.The inspectors, as well as the Entergy root causeevaluation team, determined that the extent of conditionexisted across multiple crews of the Operationsdepartment and has the potential to exist across allPilgrim Nuclear Power Station departments.It should be noted that overall licensee operationalperformance has been acceptable. The plant runs well,and there are few bhallenges to the licensed operatorssince the plant tends to run reliably through theoperating cycle.The inspectors noted that licensee corrective actions tocorrect this performance deficiency prior to this eventwere ineffective, and that this pattern continued tomanifest itself immediately before the reactor scramand in the days immediately following the reactorscram. For example, the Entergy root cause teamidentified a number of condition reports that wereAttachment 4
The
A-4-5IMC 0609,
: [[APRM]] [[Low Power set point will initiate a reactor scram at less than or equal to 15% power whenever the mode switch is]]
NOT in "RUN".While there was no reduction
in the quantitative
design margin, there was a qualitative
reduction
in the safety margin as there is an expectation
that the operators
will maintain an understanding
of the status of the reactor and approach criticality
in a deliberate
and carefully controlled
manner. ln this case, the operators
lost situational
awareness
regarding
the status of the reactor and subsequently
initiated
incorrect
actions that led to an unrecognized
subcriticality
followed by an Attachment
 
A-4-3 unrecognized
return to criticality
resulting
in an automatic
reactor scram.The extent the performance
deficiency
affects other eq uipment.Yes The inspectors
reviewed the Entergy root cause evaluation
team report and determined
that the underlying
causes of this performance
deficiency
exist across the Operations
organization, This includes weaknesses
in oversight, human performance
behaviors, as well as operator knowledge, skills, and abilities
deficiencies
associated
with low power reactor physics and operations
in the IRM range. lt should be noted that the performance
deficiency
did not degrade physical plant equipment;
however, the requirement
that licensed operators
conduct licensed activities
in accordance
with station approved procedures
is integral to maintaining
plant safety. Faulty operator performance
has the potential
to adversely
affect plant equipment.
Degree of degradation
of failed or unavailable
component(s).
N/A N/A Period of time (exposure time) effect on the performance
deficiency.
Yes With respect to the issues underlying
this performance
deficiency, the exposure time is indeterminate, but clearly developed
over an extended period of time.The Entergy root cause evaluation
team determined
that the causal factors for the event had existed for a considerable
period of time, but they did not quantify the exposure time, A number of condition
reports were written over the last year, including
a Fleet Assessment
performed
in February 2011, which identified
shortfalls
in oversight
and adherence
to conduct of operations
human performance
standards.
This assessment
is complicated
by the fact that there were not any apparent significant
licensed operator performance
issues at Pilgrim before this event. ln the Human Performance
cross-cutting
area, none of the aspects currently
has a theme, nor has there been a theme in the recent past. The behaviors
outlined by the performance
deficiency
have not been observed by the resident inspector
staff prior to this event.IMC 0609,
: [[APPEND]] [[IX M,]]
: [[APPEND]] [[IX M,]]
: [[TABLE]] [[4.1written over the past year that identified shortfalls inoversight and adherence to conduct of operationshuman performance standards, Corrective actionswere narrowly focused and failed to arrest thedegrading trend. Inspectors also noted that, during thestartup leading to the reactor scram, there werenumerous lapses in human performance fundamentalsand missed opportunities to correct those behavioraldeficiencies. lmmediately following the reactor scram,the licensee's post trip reviews and]]
: [[TABLE]] [[4.1 Attachment]]
: [[OSRC]] [[reviewsfailed to fully evaluate the extent and scope of thehuman performance and knowledge deficiencies priorto authorizing the restart of the reactor. For instance,NRC inspectors identified that a control rod had beenmispositioned during the startup and that anlnfrequently Performed Test or Evolution (IPTE) briefinghad not been conducted during the initial andsubsequent startups. The control rod mispositioningand failure to perform the]]
IMC 0609, APPENDIX M, TABLE 4.1 The likelihood
: [[IPTE]] [[briefing were notidentified by the licensee. In addition, in the daysimmediately following the event, inspectors continued toobserve a lack of formality in operator communications,a lack of apparent peer checking, and a number ofcontrol room distractions,While it will clearly take time to fully change thebehaviors associated with this performance deficiency,the inspectors did observe progress being made duringthe inspection. The licensee's Significant Event ReviewTeam (]]
that the licensee's
: [[SERT]] [[) and root cause analysis team performedthorough reviews of the event, and the licensee hasidentified a number of appropriate corrective actionsthat should correct the performance deficiency. Inaddition, licensee line personnel up through senior plantmanagement were interviewed extensively by theinspectors in the days and weeks following the event,and it appears as though the licensee has fullyinternalized the significance of this event.However, while progress is being made to correct theperformance deficiency, add itiona I follow-u pinspection(s) may be warranted to confirm the futureeffectiveness of the licensee's corrective actions.Attachment 4]]
recovery actions would successfully
mitigate the performance
deficiency.
Yes Although "recovery
actions" do not equate to "corrective
actions," this section lends itself to a discussion
of licensee corrective
action in that completion
of these actions would mitigate the performance
deficiency.
The licensee's
root cause analysis was thorough and appeared to identify all underlying
causal factors. The associated
proposed corrective
actions appear to adequately
address the undedying
causal factors.Short term corrective
actions have been completed
to correct the specific issues associated
with this event.Longer term corrective
actions are in progress to address programmatic
weakness in training and human performance
behaviors.
Additional
qualitative
circumstances
associated
with the finding that regional management
should consider in the evaluation
process.Yes In this event, there were a significant
number of lapses in operator human performance
fundamentals
as described
in the conduct of operations
and reactivity
control standards
and procedures.
These lapses in human performance
fundamentals
degraded individual
operator performance, crew performance, as well as management
oversight
performance.
The lack of enforcement
of, and adherence
to, the conduct of operations
and reactivity
control standards
and procedures
were identified
as the root cause of the reactor scram event.The inspectors, as well as the Entergy root cause evaluation
team, determined
that the extent of condition existed across multiple crews of the Operations
department
and has the potential
to exist across all Pilgrim Nuclear Power Station departments.
It should be noted that overall licensee operational
performance
has been acceptable.
The plant runs well, and there are few bhallenges
to the licensed operators since the plant tends to run reliably through the operating
cycle.The inspectors
noted that licensee corrective
actions to correct this performance
deficiency
prior to this event were ineffective, and that this pattern continued
to manifest itself immediately
before the reactor scram and in the days immediately
following
the reactor scram. For example, the Entergy root cause team identified
a number of condition
reports that were Attachment
 
A-4-5
: [[IMC]] [[0609,]]
APPENDIX M, TABLE 4.1 written over the past year that identified
shortfalls
in oversight
and adherence
to conduct of operations
human performance
standards, Corrective
actions were narrowly focused and failed to arrest the degrading
trend. Inspectors
also noted that, during the startup leading to the reactor scram, there were numerous lapses in human performance
fundamentals
and missed opportunities
to correct those behavioral
deficiencies.
lmmediately
following
the reactor scram, the licensee's
post trip reviews and OSRC reviews failed to fully evaluate the extent and scope of the human performance
and knowledge
deficiencies
prior to authorizing
the restart of the reactor. For instance, NRC inspectors
identified
that a control rod had been mispositioned
during the startup and that an lnfrequently
Performed
Test or Evolution (IPTE) briefing had not been conducted
during the initial and subsequent
startups.
The control rod mispositioning
and failure to perform the IPTE briefing were not identified
by the licensee.
In addition, in the days immediately
following
the event, inspectors
continued
to observe a lack of formality
in operator communications, a lack of apparent peer checking, and a number of control room distractions, While it will clearly take time to fully change the behaviors
associated
with this performance
deficiency, the inspectors
did observe progress being made during the inspection.
The licensee's
Significant
Event Review Team (SERT) and root cause analysis team performed thorough reviews of the event, and the licensee has identified
a number of appropriate
corrective
actions that should correct the performance
deficiency.
In addition, licensee line personnel
up through senior plant management
were interviewed
extensively
by the inspectors
in the days and weeks following
the event, and it appears as though the licensee has fully internalized
the significance
of this event.However, while progress is being made to correct the performance
deficiency, add itiona I follow-u p inspection(s)
may be warranted
to confirm the future effectiveness
of the licensee's
corrective
actions.Attachment
4
}}
}}

Revision as of 08:10, 3 August 2018

IR 05000293-11-012, on 05/16/2011 - 07/20/2011, Pilgrim Nuclear Power Station, Inspection Procedure 93812, Special Inspection
ML112440100
Person / Time
Site: Pilgrim
Issue date: 09/01/2011
From: Christopher Miller
Division of Reactor Safety I
To: Smith R G
Entergy Nuclear Operations
References
EA-11-174 IR-11-012
Download: ML112440100 (37)


Text

,2+**ti UNITED STATES N UCLEAR REGU LATORY COMM ISSION REGION I 475 ALLENDALE ROAD KING OF PRUSSIA. PENNSYLVANIA 19406-1415 September 1, 2011 EA-11-174 Mr. Robert Site Vice President Entergy Nuclear Operations, Inc.Pilgrim Nuclear Power Station 600 Rocky Hill Road Plymouth, MA 02360-5508 PILGRIM NUCLEAR POWER STATION . NRC SPECIAL INSPECTION REPORT 05000293/2011012:

PRELIMINARY WHITE FINDING

Dear Mr. Smith:

On July 2Q,2011, the U.S. Nuclear Regulatory Commission (NRC) completed a Special Inspection at your Pilgrim Nuclear Power Station (PNPS). The inspection was conducted in response to the May 10,2011, reactor scram event that occurred due to an unrecognized subcriticality and subsequent unrecognized return to criticality.

The NRC's initial evaluation of this event satisfied the criteria in NRC Inspection Manual Chapter (lMC) 0309, "Reactive lnspection Decision Basis for Reactors," for conducting a Special Inspection.

The Special Inspection Team (SlT) Charter (Attachment 2 of the enclosed report) provides the basis and additional details concerning the scope of the inspection.

The enclosed inspection report documents the inspection results, which were discussed at the exit meeting on July 20,2011, with you and other members of your staff.The inspection team examined activities conducted under your license as they relate to safety and compliance with Commission rules and regulations and with the conditions of your license.The inspection team reviewed selected procedures and records, observed activities, and interviewed personnel.

In particular, the inspection team reviewed event evaluations, causal investigations, relevant performance history, and extent of condition to assess the significance and potential consequences of issues related to the May 10 event.The inspection team concluded that the plant operated within acceptable power limits, and no equipment malfunctioned during the power transient and subsequent reactor scram.Nonetheless, the inspection team identified several issues related to human performance and compliance with conduct of operations and reactivity control standards and procedures that contributed to the event. The enclosed chronology (Attachment 3 of the enclosed report)provides additional details regarding the sequence of events.

R, Smith 2 This report documents one finding that, using the reactor safety Significance Determination Process (SDP), has preliminarily been determined to be White, or of low to moderate safety significance.

The finding involves the failure of Pilgrim personnel to implement conduct of operations and reactivity control standards and procedures during a reactor startup, which contributed to an unrecognized subcriticality followed by an unrecognized return to criticality and subseq uent reactor scram.This finding was assessed using NRC IMC 0609, Appendix M, "Significance Determination Process Using Qualitative Criteria," because probabilistic risk assessment tools were not well suited to evaluate the multiple human performance errors associated with this issue.Preliminarily, the NRC has determined this finding to be of low to moderate safety significance based on a qualitative assessment.

There was no significant impact on the plant following the transient because the event itself did not result in power exceeding license limits or fuel damage. Additionally, interim corrective actions were taken, which included removing the Pilgrim control room personnel involved in the event from operational duties pending remediation, providing additional training for operators not involved with the event, and providing increased management oversight presence in the Pilgrim control room while long term corrective actions were developed.

The finding involved one apparent violation (AV) of NRC requirements regarding Technical Specification 5.4, "Procedures," that is being considered for escalated enforcement action in accordance with the NRC's Enforcement Policy, which can be found on NRC's website at http://www.

nrc.qov/read inq-rom/doc-col lections/enforcemenU.

ln accordance with NRC IMC 0609, we will complete our evaluation using the best available information and issue our final determination of safety significance within 90 days of the date of this letter. The SDP encourages an open dialogue between the NRC staff and the licensee;however, the dialogue should not impact the timeliness of the staff's final determination.

Before we make a final decision on this matter, we are providing you with an opportunity to (1) attend a Regulatory Conference where you can present to the NRC your perspective on the facts and assumptions the NRC used to arrive at the finding and assess its significance, or (2) submit your position on the finding to the NRC in writing. lf you request a Regulatory Conference, it should be held within 30 days of your response to this letter, and we encourage you to submit supporting documentation at least one week prior to the conference in an effort to make the conference more efficient and effective.

lf a Regulatory Conference is held, it will be open for public observation.

lf you decide to submit only a written response, such submittal should be sent to the NRC within 30 days of your receipt of this letter. lf you decline to request a Regulatory Conference or submit a written response, you relinquish your right to appeal the final SDP determination, in that by not doing either, you fail to meet the appeal requirements stated in the Prerequisite and Limitation Sections of Attachment 2 of IMC 0609.Please contact Mr. Donald E. Jackson by telephone at (610) 337-5306 within 10 days from the issue date of this letter to notify the NRC of your intentions.

lf we have not heard from you within 10 days, we will continue with our significance determination and enforcement decision.The final resolution of this matter will be conveyed in separate correspondence. Because the NRC has not made a final determination in this matter, no Notice of Violation is being issued for this inspection finding at this time. Please be advised that the number and characterization of the apparent violation described in the enclosed inspection report may change as a result of further NRC review.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room and from the Publicly Available Records (PARS) component of NRC's document system, Agencywide Documents Access and Management System (ADAMS), ADAMS is accessible from the NRC Website at http://www.nrc.qov/readinq-rm/adams.html (the Public Electronic Reading Room).Division of Reactor Safety Docket No. 50-293 License No. DPR-35

Enclosure:

Inspection Report 05000293/201 1012

w/Attachments:

Supplemental Information (Attachment 1 )Special Inspection Team Charter (Attachment 2)Detailed Sequence of Events (Attachment 3)Appendix M Table 4.1 (Attachment 4)cc w/encl: Distribution via ListServ

Sincerely,&

R, Smith Because the NRC has not made a final determination in this matter, no Notice of Violation is being issued for this inspection finding at this time. Please be advised that the number and characterization of the apparent violation described in the enclosed inspection report may change as a result of further NRC review.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room and from the Publicly Available Records (PARS) component of NRC's document system, Agencywide Documents Access and Management System (ADAMS).ADAMS is accessible from the NRC Website at http://www.nrc.qov/readinq-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/Christopher G. Miller, Director Division of Reactor Safety Docket No. 50-293 License No. DPR-35

Enclosure:

lnspection Report 05000293/201 1012

w/Attachments:

Supplemental Information (Attachment 1 )Special Inspection Team Charter (Attachment 2)Detailed Sequence of Events (Attachment 3)Appendix M Table 4.1 (Attachment 4)cc w/encl: Distribution via ListServ Distribution:

See next page SUNSI Review Complete:

rrm* (Reviewer's Initials)DOCUMENT NAME: G:\DRS\Operations Branch\M0KINLE\lPilgrim SIT June 20'11\lnspection Report Drafts\Pilgrim SIT Concurrence\Pilgrim 2011 SIT Report Final.docx After declaring this document "An Official Agency Record" it will be released to the Public.MLI12440't00 To teceivs a coov of this documGnt.

indicate in the box: "C" = CoDy without attachmenvenclosure "E" = Copy with attachmenvenclosure

'N" = No OFFICE RIiDRS RI/DRS RI/ORA RI/DRP RI/DRP NAME RMcKinley/rrm*

Prior concurrence DJackson/dej*

Prior concurrence DHolody/aed for*Prior concurrence RBellamy/tcs for*Prior concurrence DRoberts/djr-

Prior concurrence DATE 08t19t11 08t19t11 08t19t11 08/ t11 08/30/1 1 OFFICE RI/DRS NAME CMiller/cgm DATE 08131111 OFFICIAL RECORD COPY Docket No.: License No.: Report No,: Licensee: Facility: Location: Dates: Team Leader: Team: Approved By: U. S. NUCLEAR REGULATORY COMMISSION REGION I 50-293 DPR-35 05000293/2011012 Entergy Nuclear Operations, Inc Pilgrim Nuclear Power Station (PNPS)600 Rocky Hill Road Plymouth, MA 02360 May 16 through July 20,2011 R. McKinley, Senior Emergency Response Coordinator Division of Reactor Safety B. Haagensen, Resident Inspector, Division of Reactor Projects D. Molteni, Operations Engineer, Division of Reactor Safety Donald E. Jackson, Chief Operations Branch Division of Reactor Safety Enclosure

SUMMARY OF FINDINGS

lR 0500029312011012; 0511612011 - 071201201 1; Pilgrim Nuclear Power Station (PNPS);lnspection Procedure 93812, Special Inspection.

A three-person NRC team, comprised of two regional inspectors and one resident inspector, conducted this Special lnspection.

One finding with potentialfor greater than Green safety significance was identified.

The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using lnspection Manual Chapter (lMC) 0609, "Significance Determination Process" (SDP). The cross-cutting aspect was determined using IMC 0310,"Components Within the Cross-Cutting Areas." Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.NRC ldentified and Self Revealing Findings

Cornerstone: Initiating

Events. Preliminary White: A self-revealing finding was identified involving the failure of Pilgrim personnel to implement conduct of operations and reactivity control standards and procedures during a reactor startup, which contributed to an unrecognized subcriticality followed by an unrecognized return to criticality and subsequent reactor scram.The significance of the finding has preliminarily been determined to be White, or of low to moderate safety significance.

The finding is also associated with one apparent violation of NRC requirements specified by Technical Specification 5.4, "Procedures." There was no significant impact on the plant following the transient because the event itself did not result in power exceeding license limits or fuel damage. Additionally, interim corrective actions were taken, which included removing the Pilgrim control room personnel involved in the event from operational duties pending remediation, providing additional training for operators not involved with the event, and providing increased management oversight presence in the Pilgrim control room while long term corrective actions were developed.

Entergy staff entered this issue, including the evaluation of extent of condition, into its corrective action program (CR-PNP-2011-2475)and performed a Root Cause Evaluation (RcE).The finding is more than minor because it was associated with the Human Performance attribute of the Initiating Events cornerstone and affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during power operations.

Specifically, the failure of Pilgrim personnel to effectively implement conduct of operations and reactivity control standards and procedures during a reactor startup caused an unrecognized subcriticality followed by an unrecognized return to criticality and subsequent reactor scram. Because the finding primarily involved multiple human performance errors, probabilistic risk assessment tools were not well suited for evaluating its significance.

The inspection team determined that the criteria for using IMC 0609, Appendix.M, "Significance Determination Process Using lll

Qualitative Criteria," were met, and the finding was evaluated using this guidance, as described in Attachment to this report. Based on the qualitative review of this finding, the NRC has preliminarily concluded that the finding was of low to moderate safety significance (preliminary White).The inspection team determined that multiple factors contributed to this performance deficiency, including:

inadequate enforcement of operating standards, failure to follow procedures, and ineffective operator training.

The Entergy RCE determined that the primary cause was a failure to adhere to established Entergy standards and expectations due to a lack of consistent supervisory and management enforcement.

The inspection team concluded that the finding had a cross-cutting aspect in the Human Performance cross-cutting area, Work Practices component, because Entergy did not adequately enforce human error prevention techniques, such as procedural adherence, holding pre-job briefs, self and peer checking, and proper documentation of activities during a reactor startup, which is a risk significant evolution.

Additionally, licensed personnel did not effectively implement the human performance prevention techniques mentioned above, and they proceeded when they encountered unceftainty and unexpected circumstances during the reactor startup H.4(a). (Section 2)iv

1.

REPORT DETAILS

Backoround and Description of Event In accordance with the Special Inspection Team (SlT) Charter (Attachment 2), the inspection team conducted a detailed review of the May 10, 2011, reactor scram event at Pilgrim Nuclear Power Station, including a review of the Pilgrim operators' response to the event. The inspection team gathered information from the plant process computer (PPC) alarm printouts and parameter trends, interviewed station personnel, observed on-going control room activities, and reviewed procedures, logs, and various technical documents to develop a detailed timeline of the event (Attachment 3).On May 10,2011, following a refueling outage, the reactor mode switch was taken to startup at 0626, and control rod withdrawal commenced at 0641. The control room crew consisted of the following personnel (additional licensed operators were present in the control room conducting various startup related activities):

o Assistant Operations Manager (AOM-Shift) - Senior Line Management oversight r Shift Manager (SM)- management oversight. Reactivity Senior Reactor Operator (SRO/Control Room Supervisor (CRS) -command and control o Assistant Control Room Supervisor (ACRS). Reactor Operator At-The-Controls (RO-ATC)o Reactor Operator (Verifier)

  • ATC verifier r Reactor Engineer (RE). RE in Training At 1212, the reactor was made critical when control rod 38-19 was moved to position 12.Power continued to rise to the point of adding heat (POAH), and the POAH was achieved at 1227. Once the POAH was achieved, the RO-ATC operator inserted rod 38-19 to position 10 to obtain lntermediate Range Monitor (lRM) overlap correlation data. Following the data collection, the RO-ATC operator withdrew rod 38-19 back to position 12.At approximately 1231, the Reactivity SRO/CRS and the RO-ATC operator were relieved by other licensed operators who continued with plant startup. The crew withdrew control rods to establish a moderator heat-up rate. The RO-ATC operator withdrew control rods 14-35, 38-35 , 14-19 and 22-43 from position 08 to 12 without incident.The RO-ATC operator continued with the rod withdrawal sequence and tried to withdraw control rod 30-11 from position 08 to 12, but the control rod would not move using normal notch withdraw commands.

The RO-ATC then attempted to withdraw control rod 30-11 using a "double-clutch" maneuver in accordance with procedures; however, the control rod inadvertently inserted and settled at position 06. As stated during interviews with the NRC inspectors, the RO-ATC operator, the ATC verifier, and the Reactivity SRO/CRS all saw the control rod in the incorrect position.

However, the operators did not enter and follow Pilgrim Nuclear Power Station (PNPS) Procedure 2.4.11, "Control Rod Positioning Malfunctions" as required.

This procedure required the operators to assess the amount of the mispositioning to determine the appropriate course of remedial 2 action before proceeding, and it also required the issue to be documented in a condition report. The operators did not perform an assessment, and they moved the control rod back to position 08 and ultimately to position 12, which was the correct final position in accordance with reactor engineering maneuvering instructions.

During interviews with the NRC inspectors, the three operators each indicated that there was confusion in their mind regarding whether or not the control rod met the definition of a mispositioned control rod because the control rod was only out of position by one notch from the initial position, but none of the operators referred to the procedure, and there was no discussion or challenge regarding the proper course of action among the operators.

The condition was not logged, and a condition report was not generated until the issue was identified by NRC inspectors.

In addition, the problem of the mispositioned control rod was not discovered by the licensee during the post trip review.Following withdrawal of the five control rods (ten control rod notches), the RO-ATC observed the process computer displaying a high short{erm (five minute average)moderator heat-up rate reading of 18'F per 5 minutes that he mistakenly believed corresponded to an hourly heat-up rate of 216"Flhr (the actual hourly heatup rate was 50"F/hr).

The heat-up rate concern was discussed among the SM, Reactivity SRO/CRS, RO-ATC operator, Verifier and AOM-Shift.

After the discussion, the SM directed the crew at the controls to insert control rods to reduce the heat-up rate. This direction did not include specific guidance or limitations regarding the number of control rod notches to insert, At this point, the AOM-Shift and SM left the front panels area of the control room.The RE and RE-in-training were working at their computer terminals in the control room performing procedurally required calculations related to the startup. The REs had been occupied with these tasks from the time criticality had been achieved and had not been consulted on the plan to insert control rods to reduce the heatup rate. The RE-in-training overheard the operator conversation about inserting control rods. He informed the RE, who in turn, questioned the SM about the decision to insert rods. The SM responded that the actions were necessary to control heat-up rate. No further discussion occurred between the SM and the RE regarding the number of control rods/notches to be used to control the heat-up rate or if there was a need to modify the reactor maneuvering plan. During interviews with the NRC inspectors, the SM and the AOM-Shift stated that they both discussed that there was a need to be careful to avoid taking the reactor subcritical and that the action of inserting control rods had the potential to cause the reactor to become subcritical.

However, this important information was never communicated to any of the operators at the controls, including at the time when the SM directed the at-the-controls crew to insert control rods to reduce the heat-up rate.As a result of the previous control rod withdrawal, moderator temperature was 40"F higher than it was at initial criticality resulting in slightly increased control rod worth.The crew did not factor this increased control rod worth into their decision regarding the number of control rod notches to insert.Over the next three minutes, the RO-ATC operator proceeded to re-insert the following control rods from positions 12 to 8 (10 notches total) that had been previously withdrawn Enclosure 2.3 to establish the heat-up: 30-1 1 , 22-43, 14-19,38-35 and 14-35. At the end of the rod insertion evolution, the SM directed the Reactivity SRO/CRS and the RO-ATC operator to keep reactor power on IRM range 7. This communication was not acknowledged by the RO-ATC operator.

During interviews with the NRC inspectors, none of the operators recalled receiving such instructions.

The SM then left the control room to take a break.The AOM-Shift left the controls area to get lunch in the control room kitchen.As a result of the control rod insertions, reactor power lowered, thus requiring the RO-ATC operator to range the lRMs down to range 7 and then to range 6. The reactor had become subcritical, but the crew did not recognize the change in reactor status.Approximately four minutes after the control rods were inserted to reduce the heat-up rate, the RO-ATC operator observed the process computer displaying a 0'F/hr heat-up rate. At this time, the SRO who had previously been relieved, returned and re-assumed his role as Reactivity SRO/CRS. The Reactivity SRO/CRS and the RO-ATC operator decided to once again withdraw control rods to re-establish the desired heat-up rate.Three of the same control rods (14-35, 38-35, and 14-19) were withdrawn from positions 8-12 resulting in a rising IRM count rate that was observed by the operators.

However, the crew did not recognize that the reactor status had changed from subcritical to critical.At this point, the AOM-Shift returned to the reactor panel area. The RO-ATC operator continued rod withdrawal with control rod 22-43 from position 08 to 10. The RO-ATC operator and the Verifier ranged the lRMs up as reactor power increased.

The RO-ATC operator then withdrew control rod 22-43 from position 10 to 12. The operators did not recognize the increasing rate of change in IRM power.Finally, the RO-ATC operator selected and withdrew control rod 30-11 from position 8 to 10. At 1318, IRM readings rose sharply and an IRM Hi-Hi flux condition was experienced on both Reactor Protection System (RPS) channels resulting in an automatic reactor scram at approximately 1

.7 o/o reactor power.Operator Human Performance

Inspection Scope The inspection team interviewed the Pilgrim control room personnel that responded to the May 10,2011, event including the SM, AOM-Shift, CRS, ACRS, RO-ATC, RO verifier, and the REs to determine whether these personnel performed their duties in accordance with plant procedures and training.

The inspection team also reviewed narrative logs, sequence of events and alarm printouts, condition reports, PPC trend data, procedures implemented by the crew, and procedures regarding the conduct of operations.

a.Enclosure 4 b. Findinqs/Observations Failure to lmplement Procedures durinq Reactor Startup

Introduction:

A self-revealing finding was identified involving the failure of Pilgrim personnel to implement conduct of operations and reactivity control standards and procedures during a reactor startup, which contributed to an unrecognized subcriticality followed by an unrecognized return to criticality and subsequent reactor scram. The significance of the finding has preliminarily been determined to be White, or of low to moderate safety significance.

The finding is also associated with one apparent violation of NRC requirements specified by Technical Specification 5.4, "Procedures."

Description:

On May 10,2011, following a refueling outage, operators were in the process of conducting a reactor startup. During the course of the startup, multiple licensed operators failed to implement written procedures as described below:. Entergy procedure EN-OP-1 15, "Conduct of Operations," Revision 10, Section 4.0, states that the SM is to "provide oversight of activities supporting complex and infrequently performed plant evolutions such as plant heat-up [and] startup." Additionally, the SM is responsible for ensuring "conservative actions are taken during unusual conditions

... when dealing with reactivity control," However, the SM did not oversee the activities in progress during reactor heatup and left the control room when the heat-up rate was being adjusted with control rod insertion, The SM did not ensure the actions taken to reestablish or adjust the reactor heatup rate were conservative nor did he reinforce those actions with the operating crew.r Entergy procedure EN-OP-1 15, "Conduct of Operations," Revision 10, Section 4.0, states that the CRS is required to "Ensure Pre-Evolution Briefings are held [and]plant operations are conducted in compliance with administrative and regulatory requirements." PNPS procedure 1.3.34, "Operations Administrative Policies and Procedures," Revision 1 17, Section 6.10.1

.1 states, "All complex or infrequently

performed activities warrant a pre-evolution briefing." Section 6,10.1.1[8]

lists an Infrequently Performed Tests or Evolutions Briefing as one type of pre-evolution briefing, and Section 6.10.1

.1 [4] states, "lnfrequently

Performed Tests or Evolutions Briefings for the performance of Procedures classified as "lnfrequently Performed Tests or Evolutions" (IPTE) should be performed with Senior Line Manager oversight as specified in EN-OP-116, "lnfrequently Performed Tests or Evolutions." Entergy Procedure EN-OP-116, Revision 7, Attachment 9.1 identifies "Reactor Startup" as an IPTE. However, in this case, the licensee conducted a reactor startup without performing an IPTE briefing or any other type of pre-evolution briefing as defined in PNPS procedure 1.3.34. lt is noteworthy to point out that an IPTE briefing package was previously prepared, approved, and scheduled; however, the IPTE briefing was never performed as required by the procedures described above. In addition, an IPTE briefing was also not performed for the startup following this event. Finally, the CRSs did not ensure the administrative requirements of the conduct of operations procedures or the regulatory requirement to implement the control rod mispositioning procedure were met. This issue was identified by the NRC inspectors.

5 Entergy procedure EN-OP-115, "Conduct of Operations," Revision 10, Section 5.2, states control room operators are required to "develop and implement a plan that includes contingencies and compensatory measures" and when implementing those plans the "crew ... continuously evaluates the plan for changing conditions" and"Human Performance (HU) tools (..., peer/cross-checking, oversight, questioning attitude, etc.) are utilized ..." In addition, "When the control room team is faced with a time critical decision:

Use all available resources...do not proceed in the face of uncertainty..." However, the control room operators failed to develop contingency plans or compensatory measures for adjusting reactor heat-up rate or addressing higher than expected reactor heat-up rates. The crew also failed to develop or implement contingencies for control rods which were difficult to maneuver when they were at low reactor power. Additionally, the use of human performance tools was ineffective in addressing the actions or conditions that led to the unexpected reactor heatup rate and the mispositioning of control rod 30-11. Specifically, failures in the use of peer checking and questioning the conditions that led to the unexpected reactor heat-up rate directly contributed to the mispositioned control rod and the subsequent reactor scram. Lastly, the control room team did not use all available resources by involving Reactor Engineering staff in its decision-making, and proceeded in the face of uncertainty by failing to consider the consequences of the reactivity changes.Entergy procedure EN-OP-115, "Conduct of Operations," Revision 10, Section 5.4 states that reactor operators are expected to perform reactivity manipulations "in a deliberate, carefully controlled manner while the reactor is monitored to ensure the desired result is obtained." However, the reactor operators did not adequately monitor the conditions of the reactor while attempting to establish and adjust the reactor heat-up rate. Although the reactor operators were watching the response of both the lRMs and the computer point displaying a five minute average reactor heatup, they were moving control rods faster than the plant temperature could respond and therefore taking actions to continue control rod movement before the desired result of their manipulations could be assessed.

Additionally, after inserting control rods to adjust the reactor heat-up rate, the operators had sufficient indications that the reactor was significantly subcritical as evidenced by the required ranging down of lRMs, the drop in Source Range Monitor (SRM) count rates, and establishing a negative reactor period. The operator's failure to adequately monitor the status of the reactor led to an unrecognized subcritical condition and subsequent return to criticality resulting in an eventual reactor scram.PNPS procedure 1.3.34, "Operations Administrative Policies and Procedures," Revision 1 17, Section 6.7.5 states, "Any relief occurring during the shift (either short-term or for the remainder of the shift) will be recorded in the CRS log." lt further states, "...a verbal discussion of plant status and off-normal conditions must be conducted." However, several people in watch standing positions changed from the start of the shift, but none of those changes were entered into the control room log. In addition, when the ACRS was turning over to the CRS, there was no discussion of the mispositioning of control rod 30-11.Enclosure

6. PNPS Procedure

2.4.11, "Control Rod Positioning Malfunctions," Revision 35, Section 5.4 defines a mispositioned control rod as "a control rod found to be left in a position other than the intended position $ a control rod that moves more than one notch beyond its intended position." Attachment 4 Step [3] and Step [a] of the same procedure requires the operators to assess the degree of mispositioning and take the appropriate remedial action depending on the degree of mispositioning.

4 Step [5] also states, "lf the control rod is determined to be mispositioned, then record the event as a condition report." In this case, the RO-ATC attempted to withdraw control rod 30-11 from position 08 to position 10 (intended position), but the rod inadvertently insertbd to position 06. Upon recognizing the error, the operators did not enter the procedure when control rod 30-11 was found to be left in a position other than the intended position and which was more than one notch from the intended position.

The operators did not assess the amount of the control rod mispositioning in accordance with the procedure, nor was there any discussion about the mispositioning on the crew. Furthermore, the event was not logged, nor was a condition report generated.

Instead, the operators did not enter and follow the procedure, and they continued on with the startup in the face of uncertainty.

This issue was not detected during the licensee posttrip review. lt was identified by the NRC inspectors.

o PNPS Procedure 2.1.1, "Startup from Shutdown," Revision 173, Page 53, Caution 2 states, "ln the event the reactor goes subcritical after achieving initial criticality, then return to step [53] and re-perform the steps to restore the Reactor to a critical condition." In addition, PNPS Procedure 2.1.4, "Approach to Critical," Revision 26, Section 5.0 states, "ln the event the reactor goes subcritical after achieving initial criticality, then with Reactor Engineering guidance, re-perform Section 7.0 Steps [6]and [7] to restore the Reactor to a critical condition." However, the operators did not recognize that the reactor had become subcritical and did not re-perform the procedural steps mentioned above to restore the reactor to a critical condition in a controlled manner under the guidance of Reactor Engineering.

There was sufficient information available to the operators to identify that the reactor had become subcritical.

In addition, REs were available in the control room, but they were not consulted by the operators.

Analvsis:

The inspection team determined that the failure of Pilgrim personnel to implement conduct of operations and reactivity control standards and procedures during a reactor startup was a performance deficiency that was reasonably within Entergy's ability to foresee and prevent. The finding is more than minor because it was associated with the Human Performance attribute of the Initiating Events cornerstone and affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during power operations.

Specifically, the failure of Pilgrim personnel to effectively implement conduct of operations and reactivity control standards and procedures during a reactor startup caused an unrecognized subcriticality followed by an unrecognized return to criticality and subsequent reactor scram.Enclosure 7 The inspection team determined that multiple factors contributed to this performance deficiency including:

inadequate enforcement of operating standards, failure to follow procedures, and ineffective operator training.

The Entergy RCE documented that the primary cause was a failure to adhere to established Entergy standards and expectations due to a lack of consistent supervisory and management enforcement.

In addition, the Entergy RCE specified a number of condition reports and self assessment reports written in the months preceding this event that demonstrated that the performance deficiency existed over an extended period of time and affected all operating crews. While the performance deficiency manifested itself during this particular low power event, there was the potential for the performance deficiency to result in a more consequential event under different circumstances.

Because the finding primarily involved multiple human performance errors, probabilistic risk assessment tools were not well suited for evaluating its significance.

The inspection team determined that the criteria for using IMC 0609, Appendix M, "Significance Determination Process Using Qualitative Criteria," were met, and the finding was evaluated using this guidance as described in Attachment 4 to this report. Based on the qualitative review of this finding, the NRC concluded that the finding was preliminarily of low to moderate safety significance (preliminary White). The completed Appendix M table is attached to this report (Attachment 4). There was no significant impact on the plant following the transient because the event itself did not result in power exceeding license limits or fuel damage. Additionally, interim corrective actions were taken, which included removing the Pilgrim control room personnel involved in the event from operational duties pending remediation, providing additional training for operators not involved with the event, and providing increased management oversight presence in the Pilgrim control room while long term corrective actions were developed.

This finding had a cross-cutting aspect in the Human Performance cross-cutting area, Work Practices component, because Entergy management and supervision did not adequately enforce human error prevention techniques, such as procedural adherence, holding pre-job briefs, self and peer checking, and proper documentation of activities during a reactor startup, which is a risk significant evolution.

Additionally, licensed personnel did not effectively implement the human performance prevention techniques mentioned above, and they proceeded when they encountered uncertainty and unexpected circumstances during the reactor startup [H.a(a)].Enforcement:

Technical Specification 5.4, "Procedures," states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix "A" of Regulatory Guide (RG) 1.33, February, 1978. RG 1.33, Appendix "A," requires that typical safety-related activities listed therein be covered by written procedures.

Contrary to the above, on May 10,2011, as reflected in the examples listed in the description section of this finding, the licensee failed to implement safety-related procedures related to RG 1.33, Appendix "A," Paragraph 1,"Administrative Procedures;" Paragraph 2, "General Plant Operating Procedures;" and, Paragraph 4, "Procedures for Startup, Operation, and Shutdown of Safety-Related BWR Systems." Enclosure 3.I Following a review of the event, the licensee documented the condition in the corrective action program (CR-PNP-2011-2475).

There was no significant impact on the plant following the transient because the event itself did not result in power exceeding license limits or fuel damage. Additionally, interim corrective actions were taken, which included removing the Pilgrim control room personnel involved in the event from operational duties pending remediation, providing additional training for operators not involved with the event, and providing increased management oversight presence in the Pilgrim control room while long term corrective actions were developed.

Pending determination of final safety significance, this finding with the associated apparent violation will be tracked as AV 05000293/2011012-01, Failure to lmplement Gonduct of Operations and Reactivity Gontrol Procedures during Reactor Startup.Fitness for Dutv Inspection Scope The inspection team interviewed the control room personnel that were directly involved with the May 10,2011, reactor scram event as well as management personnel involved with the immediate post event investigation.

The inspection team also reviewed Entergy Fitness for Duty (FFD) program requirements contained in the corporate and site procedures.

Fi nd i nos/Observations No findings were identified.

Traininq Inspection Scope The inspection team interviewed personnel, reviewed simulator modeling and performance, and reviewed training material related to Just in Time Training (JITT)material for the initial and subsequent startups, remedial training for the operators involved with the event, and training plans for startups and reactivity maneuvers.

Fi nd i nqs/Observations No findings were identified.

The inspection team observed that the JITT training that was provided prior to the initial startup was very limited in scope in that it only covered the approach to criticality up to the POAH. lt did not cover the full range of reactor heat-up, and it covered very little Operating Experience.

In addition, several operators that were directly involved with this event did not attend the JITT training including the SM, the ACRS who temporarily relieved the CRS prior to the scram, and the RO who was at the controls when the scram occurred.a.h 4.a.b.Enclosure 5.I Orqanizational Response lmmediate Response Inspection Scope The inspection team interviewed personnel, reviewed various procedures and records, and observed control room operations to assess immediate response of station personnel to the reactor scram event.Fi nd i nqs/Observations No findings were identified.

The inspection team observed that Entergy's initial response to the event was not appropriately thorough and was narrowly focused. lmmediately foilowing the event, operators were debriefed in an attempt to ascertain the cause of the event. Initially, Entergy personnel focused on a potential IRM malfunction as the potential cause of the event despite the fact that multiple IRM channels accurately tracked reactor power along with operator reactivity inputs. lmmediate post event interviews with the crew did not probe human error as a potential cause even though the SM, the AOM-Shift, and the REs had expressed concerns just prior to the scram regarding the insertion of control rods so near the point of criticality.

Operators involved with the event were dismissed for the day as the investigation continued to incorrectly focus on equipment malfunction as the most likely cause of the event. Several hours passed before it became clear to site management that human error was the cause of the event. As a result, the operators involved with the event were not thoroughly interviewed to ensure that all of the human performance aspects were fully understood prior to proceeding with the next startup. In addition, the inspection team identified that the posttrip review failed to identify that a control rod had been mispositioned just prior to the scram and that an IPTE briefing had not been conducted for the startup. Consequently, additional human performance issues were not evaluated, and the licensee again failed to perform an IPTE briefing prior to the subsequent startup as required by Entergy procedures.

Post-Event Root Cause Evaluation and Actions Inspection Scope The inspection team reviewed Entergy's Root Cause Evaluation (RCE) report for the event to determine whether the causes and associated human performance issues were properly identified.

Additionally, the inspection team assessed whether interim and planned long term corrective actions were appropriate to address the cause(s).61 a.b.5.2 a.Enclosure b.10 Find inqs/Observations No findings were identified.

The RCE was thorough and appeared to identify the underlying causal factors. The associated proposed corrective actions appeared to adequately address the underlying causal factors. Entergy identified the root cause as a lack of consistent supervisory and management enforcement of administrative procedure requirements and management expectations for command and control, roles and responsibilities, reactivity manipulations, clear communications, proper briefings, and proper turnovers.

The RCE also identified contributing causes including weaknesses in monitoring plant status and parameters as well as weaknesses in operator proficiency with regards to low power operations.

Meetinqs.

Includinq Exit Exit Meetino Summarv On July 20,2011, the inspection team discussed the inspection results with Mr. R. Smith, Site Vice President, and members of his staff. The inspection team confirmed that proprietary information reviewed during the inspection period was returned to Entergy.40A6 Enclosure Enterov Personnel R. Smith J. Dreyfuss D. Noyes J. Macdonald R. Probasco J. Couto S. Anderson T. Tomon J. Byron J. Hayhurst S. Bethay J. Lynch T. White F. McGinnis R. Byrne V. Fallacara S. Reininghaus J. House V. Magnatta R. Paranjape A,1-1

=SUPPLEMENTAL

INFORMATION=

KEY POINTS OF CONTACT

Site Vice President General Manager Plant Operations

Manager, Operations

Assistant

Manager, Operations

Shift Manager, Operations

Shift Supervisor, Operations

Shift Supervisor, Operations

Reactor Operator, Operations

Reactor Operator, Operations

Reactor Operator, Operations

Director, Nuclear Safety Assurance Manager, Licensing Manager, Quality Assurance Engineer, Licensing Senior Engineer, Licensing Director, Engineering

Manager, Training Supervisor, Operations

Training Lead lnstructor, Operations

Training Reactor Engineer

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Ooened

05000293/2011012-01

AV Failure to lmplement

Conduct of Operations

and Reactivity

Control Procedures

during Reactor Startup (Section 2)

LIST OF DOCUMENTS

REVIEWED Procedures:

1.3.34, "Operations Administrative policies and Procedures," Revision 1 19 1 .3.37 , "Post-Trip Reviews," Revision 27 1.3,63, "Conduct of Event Review Meetings," Revision 25 1.3.109, "lssue Management," Revision 8 2.1.1, "Startup from Shutdown," Revision 173 2.1.4, "Approach to Critical," Revision 26 2.1.7, "Vessel Heat-up and Cool Down," Revision 54 2.4.11, "Control Rod Positioning Malfunctions," Revision 35 2.4.11.1, "CRD System Malfunctions," Revision 21 Attachment
A-1-2 SUPPLEMENTAL
INFORMATION
NOP96A3, "Reactivity Management Peer Panel," Revision 10
EN-FAP-AD-OO1, "Fleet Administrative

Procedure

(FAP) Process," Revision 0

EN-FAP-OM-006, "Working Hour Limits for Non-Covered Workers," Revision 2
EN-FAP-OP-008, "Reactivity Management Performance Indicator Program," Revision 0
EN-FAP-OP-01
1, "Operator Human Performance Indicator Program," Revision 0
EN-HU-102, "Human Performance Tools," Revision 5
EN-HU-103, "Human Performance Error Reviews," Revision 4
EN-NS-102, "Fitness for Duty Program," Revision 9
EN-OM-119, "On-Site Safety Review Committee," Revision 7
EN-OM-123, "Fatigue Management Program," Revision 3
EN-OP-103, "Reactivity Management Program," Revision 5
EN-OP-1 15, "Conduct of Operations," Revision 10
EN-OP-1 16, "lnfrequently Performed Tests of Evolutions," Revision 7
EN-RE-214, "Conduct of Reactor Engineering," Revision 0
EN-RE-215, "Reactivity Maneuver Plan," Revision 1
EN-RE-219, "Startup sequence Criticality Controls (BWR)," Revision 0 Condition Reports:
CR-PNP-2011-02475

and associated Root Cause Evaluation Report, Revision 1

CR-PNP-201
1-02488 cR-PNP-2011-02493

cR-PNP-2011-02504

CR-PNP-201
1-02506 CR-PNP-2011-02546
CR-PNP-201
1-02568 CR-PNP-2011-02572

cR-PNP-2011-02577

CR-PNP-201
1-03598 Self Assessments:
LO-PNPLO-2009-00071, "Focused Assessment on Reactivity Management"
LO-PNPLO-2010-00106, "Snapshot Assessment on Reactivity Management

Procedure

Revision lmplementation"
LO-PNPLO-2010-00106, "Snapshot Assessment on SOER 07-01 Recommendation Reactivity Management Operations Training" Technical Specifications:
3.5.C, "HPCI System" 3.5.D,'RCIC
System" 5.4.1, "PROCEDURES" Traininq Material: lnstructional Module, Reactor Startup and Criticality

(& Main Turbine Overspeed)

Just in Time Training used for
0511012011

and

0511112011
Startup JITT Instructional Module, Reactor Startup and Criticality May 2011 Just in Time Training used for 051
1812011 Startup JITT Attachment
A-1-3 SUPPLEMENTAL
INFORMATION
Just in Time Training PowerPoint used for 05/1812011
Startup JITT lnstructor Lesson Plan JITT
RFO 18 Hydro 2.1 .8.5 Simulator
JITT Reactor Shutdown 2.1.5 and Vessel Cooldown 2.1.7 , Revised 0410112011
Simulator
JITT Reactor Shutdown 2.1.5 and Vessel Cooldown 2.1 .7 , Revised 0211912011
Training Schedules for Outage Training Cycle
0311412011

-0410712011

Training Schedules for Training Cycle 020211312011

-0211712011

Training Schedules for Training Cycle 01
1112212010 - 0112212011
Training Records and Remediation Training for Current Licensed Operators lnitial License Class 2009-2011
Class Schedule O-RO-03-02, "Reactor Plant Startup Certification Unit Guide," Revision 10 O-RO-03-01-19, "Reactivity Management and Control Instructor/Student Guide," Revision 2 O-RO-03-01

-20, "Simulator Scenario, Operations Standards," Revision 0 O-RO-03-02-01, "lnstructional Module - Day One Cold Reactor Startup," Revision 7 O-RO-03-02-02, "lnstructional Module - Day Two Hot Reactor Startup," Revision 7 O-RO-03-02-03, "lnstructional Module * Day Three Cold Reactor Startup," Revision 3 O-RO-03-02-04, "lnstructional Module - Day Four Hot Reactor Startup," Revision 3 O*RO-03-02-05, "lnstructional Module - Day Five Cold Reactor Startup," Revision 3 O-RO-03-02-06, "lnstructional Module - Day Six Cold Reactor Startup," Revision 3 O-RO-03-02-07, "lnstructional Module - Day Seven 905 Certification Practice," Revision 3 O-RO-03-02-08, "lnstructional Module * Day Eight 905 Certification Practice," Revision 2 O-RO-03-02-09, "lnstructional Module - Day Nine Reactor Power Operations," Revision 1 O-RO-03-02-51, "lnstructional Module - SOER 90-3 Nuclear Instrument Miscalibration," Revision 3 Miscellaneous:

Crew Briefing Sheet from May 10,2011 SCRAM Operations Section Standing Order 11-03 OSRC Meeting 2011-008 Meeting Minutes Post-Trip Review Package from May 10,2011 SCRAM with Attachments and Supporting Data"EN-OP-116
9,3 ITPE Supplemental Controls," developed for Post-Refueling Outage Startup Reactor Engineer's calculations pertaining to criticality prior to the reactor SCRAM eSOMS Control Room Logs from
0510912011

through 0511112011

SRM and Moderator Temperature Traces with Calculated
SRM Period 0511012011
Control Room Personnel Chart Dayshift 0511012011
Control Rod Notch History from Reactor Critical to Reactor SCRAM 0511012011
Control Rod Notch Worth Calculations for 05/1012011
Reactor Startup Power Maneuver Plan Cycle 19-01 Attachment
A-1-4 SUPPLEMENTAL
INFORMATION

LIST OF ACRONYMS

ACRS Assistant

Control Room Supervisor

ADAMS Agency-wide

Documents

Access and Management

System AOM Assistant

Operations

Manager

ATC At the Controls
AV Apparent Violation
BOP Balance of Plant

CCDP Conditional

Core Damage Probability

CFR Code of Federal Regulations

CR Condition

Report

CRD Control Rod Drive
CRS Control Room Supervisor
DRP Division of Reactor Projects
DRS Division of Reactor Safety
FFD Fitness for Duty
HEP Human Error Probability
HPCI High Pressure Coolant Injection

HUR Heatup Rate IMC lnspection

Manual Chapter IPTE Infrequently

Performed

Tests or Evolutions

IRM Intermediate

Range Monitor

JITT Just in Time Training

NRC Nuclear Regulatory

Commission

OPS [[]]

MGR Operations

Manager PARS Publicly Available

Records PD Performance

Deficiency

PNPS Pilgrim Nuclear Power Station
POAH Point of Adding Heat
PPC Plant Process Computer

PRA Probabilistic

Risk Assessment

RCE Root Cause Evaluation

RCIC Reactor Core lsolation

Cooling

RE Reactor Engineer

RG Regulatory

Guide

RO Reactor Operator

RO-ATC Reactor Operator at the Controls RPS Reactor Protection

System SDP Significance

Determination

Process

SM Shift Manager
SRI Senior Resident Inspector
SRM Source Range Monitor

SRO Senior Reactor Operator SIT Special Inspection

Team STA Shift Technical

Advisor TS Technical

Specification

A-2-1

SPECIA L INSPECTION
TEAM [[]]
CHARTE R
UNITED [[]]
STATES N
UCLEAR [[]]

REGULATORY

COMMIS SION
REGION I 475
ALLEND ALE
ROAD [[]]
KING [[]]
OF [[]]
PRUSSI A.
PA 19406-1415

MEMORANDUM

TO SPECIAL INSPECTION
TEAM [[]]

CHARTER May 13, 2011 Samuel L. Hansell Jr., Manager Special Inspection

Team Raymond R. McKinley, Leader Special Inspection

Team Christopher

G. Miller, Director /
RA /Division of Reactor Safety Darrell
J. Roberts, Director /
RA by Paul Krohn Acting For/Division of Reactor Projects SPECIAL INSPECTION
TEAM [[]]
CHARTE R -PILGRIM NUCLEAR
POWER [[]]
STATIO N OPERATOR PERFORMANCE
DURING [[]]
REACTO R STARTUP
ON [[]]

MAY 1Q.2011 FROM: SUBJECT: In accordance

with lnspection

Manual Chapter (lMC) 0309, "Reactive

Inspection

Decision Basis for Reactors," a Special Inspection

Team (SlT) is being chartered

to evaluate operator performance

and organizational

decision-making

associated

with a reactor scram that occurred during a startup on May 10,2011, The decision to conduct this special inspection

was based on meeting the deterministic

criteria (the event involved questions

or concerns pertaining

to licensee operational

performance)

and risk criteria specified

in Enclosure

of IMC 0309. The calculable

increase in conditional

core damage probability (CCDP), which was in the low E-6 range, was based on application

of an Initiating

Event Analysis in Sapphire 8 due to the reactor scram, which was then modified for the conditions

of the reactor when the transient

occurred, The SIT will expand on the event follow-up

inspection

activities

started by the resident inspectors

and augmented

by a Division of Reactor Projects (DRP) inspector

who was dispatched

to the site soon after the event. The Team will review the causes of the event, and Entergy's

organizational

and operator response during and after the event, The Team will Attachment

t rt *.r. i

A-2-2

SPECIA L INSPECTION
TEAM [[]]

CHARTER perform interviews, as necessary, to understand

the scope of operator actions performed

during the event. The Team will also assess whether the SIT should be upgraded to an Augmented Inspection

Team in accordance

with IMC 0309.The inspection

will be conducted

in accordance

with the guidance contained

in NRC Inspection

Procedure

93812, "Special Inspection," and an inspection

report will be issued within 45 days following

the final exit meeting for the inspection.

The Special Inspection

willcommence

on May 16, 2411. The following

personnel

have been assigned to this effort: Manager: Samuel L. Hansell, Jr., Branch Chief Operations

Branch, DRS, Region I Team Leader: Team Members: Enclosure:

Special Inspection

Team Charter Raymond R. McKinley, Senior Emergency

Response Coordinator

Plant Support Branch, DRS, Region I Brian C. Haagensen, Millstone

Power Station Resident Inspector Division of Reactor Projects, DRP, Region I David L. Molteni, Operations

Engineer Operations

Branch, DRS, Region I Attachment

A-2-3

SPECIA L INSPECTION
TEAM [[]]

CHARTER Special Inspection

Team Charter Pilgrim Nuclear Power Station Operator Performance

During Reactor Startup May 10,2011 Backqround:

During startup from a refueling

outage, Entergy operators

withdrew rods to criticality

the afternoon

of May 10,2011 and continued

to withdraw control rods to the point of adding heat (approximately

1o/o power). While continuing

to increase power, operators

identified

a higher than expected heat-up rate (HUR) with a five minute average HUR that, if allowed to continue, would have resulted in exceeding

the technical

specification

limit. Operators

made the Control Room Supervisor (CRS) and Shift Manager (SM) aware of the condition

and proceeded

to insert five control rods (two notches each) to lower the HUR to approximately

65"F/hr. At the time, it was not identified

by the operators, reactor engineers

or management

oversight

in the control room that the control rod insertions

brought the reactor to a subcritical

state (approximately

0.35% subcritical

by later calculations).

After reducing the HUR, the operators (without recognition

of the subcritical

reactor condition), proceeded

to withdraw the five control rods back to their previous position.

While withdrawing

the fifth control rod back to its original position, the reactor experienced

a full SCRAM on Intermediate

Range Monitor (lRM) Hl-Hl flux signals. All rods inserted and equipment

responded

as expected.Pilgrim initially

investigated

potential

equipment

related causes for the automatic scram as communicated

to the NRC on the afternoon

of May 10,2011. Subsequent

analysis revealed that human performance

errors made by the operators

were the cause of the scram. NRC was informed of this in the early morning hours of May 11,2011. Entergy is continuing

its investigation

of the operator actions taken during this event. Entergy suspended

the qualifications

of the operators

and the Shift Manager directly involved with the event while the investigation

continues.

Additional

actions have been taken by Entergy that include more restrictive

controls on reactivity

additions

following

a negative reactivity

insertion

of any kind, briefing to other operating

crews regarding

the event, and initiation

of a root cause evaluation.

The Pilgrim resident inspectors

and a resident inspector

from a different

site provided follow-up to this event under the Reactor Oversight

Process (ROP) baseline inspection

program, Basis for the Formation

of the SIT: The IMC 0309 review concluded

that one of the deterministic

criteria was met due to questions or concerns pertaining

to licensee operational

performance.

This criterion

was met based on human performance

errors that occurred and led to the unanticipated

automatic reactor scram.The human performance

errors included:. Reactor operators

were focused on monitoring

heatup rate (HUR)without

appropriate

focus on power level throughout

the startup event;. Reactor operators

and control room supervision

did not have proper sensitivity

for the impacts from negative reactivity

insertions

with the reactor at low power conditions;

A-2-4

SPECIA L INSPECTION
TEAM [[]]

CHARTER. The operators

did not identify or utilize available

plant indications

that indicated

the reactor was subcritical;. Reactor operators

did not follow shift manager instructions

to maintain reactor power within the current IRM power band while addressing

the elevated HUR;. Operators

and control room supervision

did not engage reactor engineering

staff with regard to planned rod movement after the reactor was made subcritical;

and o Prior to the identification

of the unexpected

HUR, reactor operators

did not implemenVenter

the required abnormal operating

procedure

for a mispositioned

control rod (Rod 30-1 1).In accordance

with IMC 0309, the event was evaluated

for risk significance

because one deterministic

criterion

was met, A Region I SRA evaluated

the transient (reactor scram)from

low reactor power using the Initiating

Event Assessment

feature of Saphire 8. The lE-Trans basic event probability

was set to 1.0 and all other initiating

events were set to zero. The resulting

dominant core damage sequences

were subsequently

evaluated

by the SRA to account for the low reactor power conditions

and alternating

current (AC) power being supplied by off-site sources at the time of the event. The resulting

conditional

core damage probability (CCDP)was

conservatively

estimated

in the low E-6 range, which is the overlap region between an SIT and No Additional

inspection

required.

The dominant core damage sequences

involve failure of direct current (DC) power sources and failure of residual heat removal. However, with the low decay heat load following

the refuel outage, these core damage sequences

represent

a conservative

estimate of risk.Additionally, this event involved multiple licensed operators

not recognizing

the reactivity

status of an operating

reactor during startup and demonstrating

a poor understanding

of reactor physics in a low power condition.

In light of the aforementioned

human performance

errors, and consistent

with the risk evaluation

and Section 4.04, Region I has decided to initiate an SlT.Obiectives

of the Special Inspection:

The Team will review the causes of the event, and Entergy's

organizational

and operator response during and following

the event. The Team will perform interviews, as necessary, to understand

the scope of operator actions performed

during the event.To accomplish

these objectives, the Team will: 1. Develop a complete sequence of events including

follow-up

actions taken by Entergy, and the sequence of communications

within Entergy and to the NRC subsequent

to the event;2. Review and assess crew operator performance

and crew decision making, including adherence

to expected roles and responsibilities, the use of the command and control elements associated

with reactivity

manipulations, the use of procedures, the use of diverse instrumentation

to assess plant conditions, response to alarms and overall implementation

of operations

department

and station standards;

A-2-5

SPECIA L INSPECTION
TEAM [[]]

CHARTER Evaluate the extent of condition

with respect to the other crews;Review the adequacy of operator requalification

training as it relates to this event, including

the integration

of newly licensed operators

into the operator requalification

training program;Review the adequacy of the preparation

by the operations

staff for the reactor startup including

training prior to the evolution

and briefings

by the operations

staff.Review the adequacy of the simulator

to model the behavior of the current reactor core during startup activities

and the current adequacy of the simulator

for use in reactor startup training ;Assess the decision making and actions taken by the operators

and station management

during the initial and subsequent

reactor startup to determine

if there are any implications

related to safety culture;Review and assess the effectiveness

of Entergy's

response to this event and corrective

actions taken to date. This includes overall organizational

response, and adequacy of immediate, interim and proposed longterm corrective

actions. This will also include evaluation

of the root cause analysis when developed

by the licensee;9. Review the adequacy of the Entergy and Site fitness for duty processes

and procedures

when a human performance

error has occurred;10. Evaluate Entergy's

application

of pertinent

industry operating

experience, including

INPO [[]]
SOER 10-2, "Engaged, Thinking Organizations,"
INPO [[]]

SOER 07-1, "Reactivity

Management," and other recent events involving

reactivity

management

errors to assess the effectiveness

of any actions taken in response to the operating experience;

and 11. Document the inspection

findings and conclusions

in a Special Inspection

Team final report within 45 days of inspection

completion.

Guidance: Inspection

Procedure

93812, "Special Inspection", provides additional

guidance to be used by the SlT. Team duties will be as described

in Inspection

Procedure

93812. The inspection

should emphasize

fact-finding

in its review of the circumstances

surrounding

the event. Safety concerns identified

that are not directly related to the event should be reported to the Region I office for appropriate

action.The Team will conduct an entrance meeting and begin the inspection

on May 16,2011. While on-site, the Team Leader will provide daily briefings

to Region I management, who will coordinate

with the Office of Nuclear Reactor Regulation

to ensure that all other pertinent parties are kept informed.

The Team will also coordinate

with the Region I State Liaison Officer Attachment

3.4.5.6.7.8.

A-2-6

SPECIA L INSPECTION
TEAM [[]]

CHARTER to implement

the Memorandum

of Understanding

between the NRC and the State of Massachusetts

to offer observation

of the inspection

by representatives

of the state. A report documenting

the results of the inspection

will be issued within 45 days following

the final exit meeting for the inspection.

Before the end of the first day onsite, the Team Manager shall provide a recommendation

to the Regional Administrator

as to whether the SIT should continue or be upgraded to an Augmented Inspection

Team response.This Charter may be modified should the Team develop significant

new information

that warrants review.Attachment

A,3-1

DETAIL ED SEQUENCE
OF [[]]

EVENTS May 10,2011, Reactor Scram Event The team constructed

the sequence of events from a review of control room narrative

logs, plant process computer (PPC) data (alarm printout, sequence of event printout, plant parameter graphs) and plant personnel

interviews.

Time Event 05/09/11 Two Sessions Just In Time Training (JITT) was conducted

for the reactor startup. Certain key members of the operating

crew that were directly involved with this event were not present for the training including

the Shift Manager (SM), the Assistant

Control Room Supervisor (ACRS) who temporarily

relieved the Control Room Supervisor (CRS) prior to the scram, and the Reactor Operator who was at the controls (RO-ATC)when the scram occurred.05/10/1 1 0626 The reactor mode switch was moved to the startup position.-0630 The oncoming day shift operators

received a reactor maneuvering

plan briefing.The Reactor Engineers (REs) led the brief.0641 Operators

commenced

control rod withdrawal.

0700 The day shift operating

crew assumed the shift, and control rod withdraw continues.

212 The reactor became critical.1227 The point of adding heat was reached.-1231 The

CRS was relieved for lunch by the

ACRS. The oncoming CRS providing

the relief did not receive Just In Time Training (JITT), nor did he participate

in the reactor maneuvering

plan briefing.-1231 The RO-ATC was relieved for lunch by the Licensed Operator previously

assigned as the ATC verifier.

The oncoming RO-ATC providing

the relief did not receive Just In Time Training (JITT), but he did participate

in the reactor maneuvering

plan briefing.-1231 A Licensed Operator previously

assigned to other startup activities

was reassigned

to fill the role of ATC verifier.

This individual

received JITT training, and he also received a separate reactor maneuvering

plan briefing from a RE upon arriving to work at approximately

100.1246 The RO-ATC withdrew 5 rods 2 notches to establish

a heat-up rate.Attachment

A-3-2

DETAIL ED SEQUENCE
OF [[]]

EVENTS Time Event 1255 The RO-ATC attempts to withdraw control rod 30-11 from position 08 to position 10 using single notch control, but the control rod does not move, The RO-ATC raised drive water pressure and attempted

several notch withdraw commands, but the control rod failed to move.1257 The RO-ATC attempts to withdraw control rod 30-1 1 from position 08 to position 10 using a "double clutch" maneuver, but the control rod incorrectly

inserted one notch to position 06. The RO-ATC does not discuss the control rod mispositioning

error with the crew.1257 The

ATC verifier and

CRS also saw control rod 30-11 move incorrectly

to position 06, but the control rod mispositioning

error is not discussed.

1302 The RO-ATC then withdraws

control rod 30-11 from position 06 to position 12.-1 305 The crew observes that the 5 minute average reactor coolant heat-up rate is 18"F over the 5 minute period, and the crew determines

that this corresponded

to a 216'Flhour

heat-up rate. In actuality, the 5 minute average heat-up rate reflected the instantaneous

heat-up rate. The actual hourly heat-up rate was 50'F/hour.

The crew informs the SM of the perceived

heat-up rate.-1 306 The

SM directed the
RO -ATC to insert control rods to reduce the heat-up rate, but the
SM did not specify the number of control rods or notches to insert.1307 The
RO -ATC begins to drive 5 rods 2 notches into the core to the reduce heatup rate.-1 308 The
RE question the

SM regarding

the decision to insert control rods, and the

SM told the

REs that the insertion

was needed to control the heat-up rate. There was no further discussion.

-1 309 The Assistant

Operations

Manager (AOM-Shift)

cautioned

the SM that there was the potential

to drive the reactor sub-critical

by inserting

control rods and that they needed to be careful. The SM also recalled being concerned

about the potential

to drive the reactor sub-critical.

The operating

crew at the controls was not made aware of these concerns.1310 Control rod insertion

is stopped. The control rods are now at the same position as when the reactor initially

became critical;

however, moderator

temperature

is now 40"F higher than it was at initial criticality.

The higher moderator

temperature

in conjunction

with the control rod insertion

rendered the reactor sub-critical, but the operators

were not aware of this.-1310 The

SM left the control room to take a break, and the

AOM-Shift

left the controls area to get his lunch in the control room kitchen.Attachment

A-3-3

DETAIL ED SEQUENCE
OF [[]]

EVENTS Time Event-1311 The operators

range down the Intermediate

Range Monitors (lRMs)two

decades from Range 8 to Range 6 in response to the lowering neutron flux.-1312 The original

CRS returns from break and resumes duties as

CRS as well as responsibility

for the reactivity

maneuver as the Reactivity

SRO.1313 After observing

a O"F/hour heat-up rate, the

CRS directs the

RO-ATC to resume control rod withdrawalto

establish

a positive heat-up rate. The RO-ATC begins to withdraw 5 rods 2 notches each to restore the heat-up rate.1315 While notch withdrawing

control rod 14-19 from position 08 to position 12, IRM readings begin to rise again requiring

the operators

to range up on the lRMs in response to the rising neutron flux. The reactor has returned to a critical condition, but the operators

are not aware of the change in reactor status with regards to criticality.

1316 The RO-ATC notch withdraws

control rod 22-43 from position 08 to position 12 resulting

in a more rapid rise in IRM readings, The reactor period was calculated

to be 40 seconds during the post trip review.-1318 The RO-ATC attempts to notch withdraw control rod 30-11 from position 08 to position 10 resulting

in a sharp rise in IRM readings.1318 The reactor automatically

scrammed on IRM high-high

flux level prior to completing

the withdrawal

of rod 30-1 1 to position 10. Post event analysis determined

that the reactor period was approximately

seconds, and that the scram occurred at approximately

1.7o/o equivalent

Average Power Range Monitor (APRM) power.-1320 The RE stated that he recognized

that the operators

had caused the reactor scram by withdrawing

rods to criticality.

345 The crew debriefed

the events leading up to the reactor scram.-1400 The RE participated

in a conference

call with the fuels group in Jackson (corporate

reactor engineering

staff) to discuss the event. The RE informed the conference

call participants

that the reactor scram had been caused by human error.-1 600 The RE participated

in a conference

callwith General Electric (GE) to discuss the event.-1 630 The RE informed the Director of Engineering

that the reactor scram was caused by human error.-1 700 The

RE informed the General Manager Plant Operations (
GMPO ) that the reactor scram was caused by human error. The
GMPO asked the

RE to draft a memo describing

what happened and send it to him.Attachment

A-3-4 Time Event 1730 The GMPO met with the Operations

Manager (OPS MGR) and the operators involved in the re-criticality

to discuss the events.-1 900 After shift turnover, the Assistant

Operations

Manager (AOM) recognized

that human error was the cause of the scram. Equipment

issues had been ruled out.-1 930 To*2200 The

GMPO recalls meeting with the

OPS MGR, RE and corporate

core design group to discuss issues associated

with the scram. The GMPO indicated

that his team was certain that the scram was caused by a human performance

/ knowledge deficiency

problem.-2330 The Operations

Manager (OPS MGR) prepared a written briefing for the crew on the event.5t11111 0030 An On-site Safety Review Committee (OSRC) conference

callwas convened to review the event and evaluate a recommendation

to restart the reactor.01 30 The OSRC recommended

restarting

the reactor. The

GMPO was briefed regarding the

OSRC recommendations.

200 The GMPO approved restarting

the reactor. He directed the

OPS [[]]
MGR to call the
NRC Senior Resident lnspector (
SR l).0200 The
OPS [[]]
MGR called the
SRI to inform him of the decision to restart the plant. The
OPS [[]]
MGR informed the
SRI that the cause of the scram was due to human error.0215 The
SRI called the

NRC Region I Division of Reactor Projects (DRP) Branch Chief to inform him of the decision to restart the plant. The SRI then responded

to the site to observe the startup.-0300 The reactor mode switch was placed in the startup position.-0300 The

SRI arrives onsite.*0300 The
DRP Branch Chief called the
GMPO to discuss the decision to restart the reactor.
DETAIL ED SEQUENCE
OF [[]]

EVENTS Attachment

A-4-1

IMC 0609,

APPENDIX M, Qualitative

Decision-Making

Attributes

for

TABLE 4.1

NRC Management

Review Decision Attribute Applicable

to Decision?Basis for Input to Decision - Provide qualitative

and/or quantitative

information

for management

review and decision making.Finding can be bounded using qualitative

and/or quantitative

information?

No IMC 0609 Appendix G is not appropriate

since the conditions

for reactor shutdown operations

were not met. The at-power safety Significance

Determination

Process, IMC 0609 Appendix A, quantitative

analysis methodology

is not adequate to provide reasonable

estimates

of the finding's

significance.

Furthermore, the SDP does not model errors of commission

and does not provide a method of accurately

estimating

changes to the human error probabilities

caused for errors of omission.

As a result, no quantitative

risk evaluation

can be performed

for this finding.lmproper use and execution

of procedures

coupled with weak work control practices

has the potential

to increase the human error probability (HEP) for credited operator actions. The probabilistic

risk assessment

models are highly sensitive

to small variations

in

HEP changes. The existing

PRA research does not currently support a method for varying the performance

shaping factors in response to defined error forcing contexts.

lt is not possible to calculate

a valid single point risk estimate.

Human performance

is a very large contributor

to PRA uncertainty.

Defense-in-Depth

affected?Yes The term "defense in depth" is commonly associated

with the maintenance

of the integrity

and independence

of the three fission product barriers as well as emergency

response actions. In addition, redundant and diverse safety systems, including

trained licensed operators

conducting

operations

in accordance

with approved station procedures

that were developed under an approved quality control program are integral to maintaining

a "defense in depth." While an automatic reactor scram was initiated

as designed to protect the core during this event, the fuel barrier was not actually compromised

by the crew's actions since the automatic protective

action was successful.

However, this performance

deficiency

revealed organizational

and human performance

weaknesses

which eroded defense in depth. The operating

crew Attachment

IMC 0609,

APPENDIX M, TABLE 4.1 plays a vital role in the maintenance

of "defense in depth" from the perspective

that they directly operate station controls.

Human errors can lead to consequences

that have the potential

to compromise

the three fission product barriers.

The commission

of multiple unforeseen

human errors in a short period of time during the reactor startup degraded the operator's

performance

as an important "defense in depth" barrier.These operator human performance

errors resulted in a challenge

to the automatic

Reactor Protection

System which successfully

terminated

the event in this particular

case.Performance

Deficiency

effect on the Safety Margin maintained?

Yes This performance

deficiency

had the potential

to adversely

affect the margin of safety. In this particular

event, the failure to implement

conduct of operations

and reactivity

control standards

and procedures

led to a reactor protection

set-point

being exceeded, causing a reactor scram. In fact, non-conservative

operator actions led to an unrecognized

subcriticality

followed by an unrecognized

return to criticality.

These operator actions caused a rapid rise in neutron flux and reactor power such that the IRM Hl-Hl neutron flux reactor trip set point was exceeded resulting

in an automatic reactor scram, In this case, the

IRM Hl-Hl neutron flux

RPS protective

function successfully

terminated

the event and prevented

exceeding

fuel barrier design safety margin and the potential

for subsequent

fuel barrier damage. lt should also be noted that the Average Power Range Monitor (APRM) Low Power RPS set point was available

as a backup to the IRM trip function.

The

APRM Low Power set point will initiate a reactor scram at less than or equal to 15% power whenever the mode switch is

NOT in "RUN".While there was no reduction

in the quantitative

design margin, there was a qualitative

reduction

in the safety margin as there is an expectation

that the operators

will maintain an understanding

of the status of the reactor and approach criticality

in a deliberate

and carefully controlled

manner. ln this case, the operators

lost situational

awareness

regarding

the status of the reactor and subsequently

initiated

incorrect

actions that led to an unrecognized

subcriticality

followed by an Attachment

A-4-3 unrecognized

return to criticality

resulting

in an automatic reactor scram.The extent the performance

deficiency

affects other eq uipment.Yes The inspectors

reviewed the Entergy root cause evaluation

team report and determined

that the underlying

causes of this performance

deficiency

exist across the Operations

organization, This includes weaknesses

in oversight, human performance

behaviors, as well as operator knowledge, skills, and abilities

deficiencies

associated

with low power reactor physics and operations

in the IRM range. lt should be noted that the performance

deficiency

did not degrade physical plant equipment;

however, the requirement

that licensed operators

conduct licensed activities

in accordance

with station approved procedures

is integral to maintaining

plant safety. Faulty operator performance

has the potential

to adversely

affect plant equipment.

Degree of degradation

of failed or unavailable

component(s).

N/A N/A Period of time (exposure time) effect on the performance

deficiency.

Yes With respect to the issues underlying

this performance

deficiency, the exposure time is indeterminate, but clearly developed

over an extended period of time.The Entergy root cause evaluation

team determined

that the causal factors for the event had existed for a considerable

period of time, but they did not quantify the exposure time, A number of condition

reports were written over the last year, including

a Fleet Assessment

performed

in February 2011, which identified

shortfalls

in oversight

and adherence

to conduct of operations

human performance

standards.

This assessment

is complicated

by the fact that there were not any apparent significant

licensed operator performance

issues at Pilgrim before this event. ln the Human Performance

cross-cutting

area, none of the aspects currently

has a theme, nor has there been a theme in the recent past. The behaviors

outlined by the performance

deficiency

have not been observed by the resident inspector

staff prior to this event.IMC 0609,

APPEND IX M,
TABLE 4.1 Attachment

IMC 0609, APPENDIX M, TABLE 4.1 The likelihood

that the licensee's

recovery actions would successfully

mitigate the performance

deficiency.

Yes Although "recovery

actions" do not equate to "corrective

actions," this section lends itself to a discussion

of licensee corrective

action in that completion

of these actions would mitigate the performance

deficiency.

The licensee's

root cause analysis was thorough and appeared to identify all underlying

causal factors. The associated

proposed corrective

actions appear to adequately

address the undedying

causal factors.Short term corrective

actions have been completed

to correct the specific issues associated

with this event.Longer term corrective

actions are in progress to address programmatic

weakness in training and human performance

behaviors.

Additional

qualitative

circumstances

associated

with the finding that regional management

should consider in the evaluation

process.Yes In this event, there were a significant

number of lapses in operator human performance

fundamentals

as described

in the conduct of operations

and reactivity

control standards

and procedures.

These lapses in human performance

fundamentals

degraded individual

operator performance, crew performance, as well as management

oversight

performance.

The lack of enforcement

of, and adherence

to, the conduct of operations

and reactivity

control standards

and procedures

were identified

as the root cause of the reactor scram event.The inspectors, as well as the Entergy root cause evaluation

team, determined

that the extent of condition existed across multiple crews of the Operations

department

and has the potential

to exist across all Pilgrim Nuclear Power Station departments.

It should be noted that overall licensee operational

performance

has been acceptable.

The plant runs well, and there are few bhallenges

to the licensed operators since the plant tends to run reliably through the operating

cycle.The inspectors

noted that licensee corrective

actions to correct this performance

deficiency

prior to this event were ineffective, and that this pattern continued

to manifest itself immediately

before the reactor scram and in the days immediately

following

the reactor scram. For example, the Entergy root cause team identified

a number of condition

reports that were Attachment

A-4-5

IMC 0609,

APPENDIX M, TABLE 4.1 written over the past year that identified

shortfalls

in oversight

and adherence

to conduct of operations

human performance

standards, Corrective

actions were narrowly focused and failed to arrest the degrading

trend. Inspectors

also noted that, during the startup leading to the reactor scram, there were numerous lapses in human performance

fundamentals

and missed opportunities

to correct those behavioral

deficiencies.

lmmediately

following

the reactor scram, the licensee's

post trip reviews and OSRC reviews failed to fully evaluate the extent and scope of the human performance

and knowledge

deficiencies

prior to authorizing

the restart of the reactor. For instance, NRC inspectors

identified

that a control rod had been mispositioned

during the startup and that an lnfrequently

Performed

Test or Evolution (IPTE) briefing had not been conducted

during the initial and subsequent

startups.

The control rod mispositioning

and failure to perform the IPTE briefing were not identified

by the licensee.

In addition, in the days immediately

following

the event, inspectors

continued

to observe a lack of formality

in operator communications, a lack of apparent peer checking, and a number of control room distractions, While it will clearly take time to fully change the behaviors

associated

with this performance

deficiency, the inspectors

did observe progress being made during the inspection.

The licensee's

Significant

Event Review Team (SERT) and root cause analysis team performed thorough reviews of the event, and the licensee has identified

a number of appropriate

corrective

actions that should correct the performance

deficiency.

In addition, licensee line personnel

up through senior plant management

were interviewed

extensively

by the inspectors

in the days and weeks following

the event, and it appears as though the licensee has fully internalized

the significance

of this event.However, while progress is being made to correct the performance

deficiency, add itiona I follow-u p inspection(s)

may be warranted

to confirm the future effectiveness

of the licensee's

corrective

actions.Attachment

4