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                                                    w
                                            APPENDIX B
                                US NUCLEAR REGULATORY COMMISSION
        NRC Inspection Report:    50-482/85-19                LP:  NPF-32
        Docket:  50-482
        Licensee:  Kansas Gas and Electric Company (KG&E)
                    Post Office Box 208
                    Wichita, Kansas 67201
        Facility Name:    Wolf Creek Generating Station (WCGS)
        Inspection At:    Wolf Creek Site, Coffey County, Burlington, Kansas
        Inspection Conducted:    April 1 to 30,1985
        Inspectors:    f~
                      J. Ef Cummins, S' for~1sactor Inspector,
                                                    -                        f/f/f4
                                                                            /Dpfe
                      Operations,-
                      (pars. 2 and
                                                                            Yf $
                  gBFL< Bartlett,'R(s        e'nt' Reactor Inspector,
                                                                          [DAe
                      Operations,
                      (pars 2, 3,  4,  , 6, and 7)
                                                                          /'-26~ W
                      H. F. Bundy, Resident Reactor InTpector,                Date
                      Operations,
                      (pars. 2, 4, 5, 6, 7, and 8)
        Approved:            ,
                                                                            7    fc5
                      . ET MarTiri, Chid ,' Project Section A            /Dge
                      Reactor Project anch 2
,
    8508080762 850726
    PDR  ADOCK 05000482
    O                PDR
 
E        '
                                                                                          7
      .
  -
    +'
                                                    -2-
            .
          inspection Summary
            Inspection Conducted April 1-to 30, 1985 (Report 50-482/85-19)
            Areas Inspected: Routine, unannounced inspection including licensee actions on
            previous inspection: findings; compliance with Technical Specifications; event
            followup; startup test witnessing.and observation; plant tours; precritical
            testing data review; and document control.
            The inspection involved 342 inspector-hours onsite by three NRC inspectors
            including 56 inspector-hours onsite during offshifts.
            Results: Within the seven areas inspected, two violations were identified
            (failure to properly ~ update procedure manuals, paragraph 8 and failure to
            respond to control room annunciator, paragraph 4). One open item is
            identified in paragraph 7).                                                      ;
                                                                                            1
 
r.
        .
  .
                                                      -3-
                                                    DETAILS
          - 1.  Persons Contacted
                Principal Licensee Personnel
                *R.  M. Grant, Director-Quality
                *F. T. Rhodes, Plant Manager
                *C. C. Mason, Director-Nuclear Operations
                *M.  G. Williams, Superintendent of Regulatory, Quality, and
                    Administrative Services
                *K. Peterson, Licensing
                *C. E. Parry, Superintendent of Quality Systems Engineer
                *C. J. Hoch, QA Technologist
                V. MacTaggart, Results Engineering Supervisor
                J. Johnson, Chief of Security
                D. Smith, Plant Support Supervisor
                J. Zell, Operations Superintendent
l
'
                T. Gardner, Startup
                O. Maynard, Licensing Manager
                K. Ellison, Assistant to the Superintendent of Regulatory, Quality, and
                    Administrative Services
l              * Denotes those attending the exit interview on April 30, 1985,
t
          2.    Licensee Actions on Previous Inspection Findings
                (0 pen) Open Item (482/8515-01):      Ruskin Fire Dampers: The licensee's
                testing and rework of the Ruskin fire dampers has not been completed. By
g                letter dated May 1, 1985, the licensee made a 10 CFR Part 21 Report to the
                NRC Region IV office concerning the installation of some of the fire
'
i                dampers with less than the designed clearance between the fire damper
'                frame and the penetration sleeve. This insufficient clearance could cause
                the fire damper to warp and become inoperative during a fire. This item
                will remain open.
i                (Closed) Open Item (482/8511-08): This item involved Preoperational Test
                Deficiency Deferral (RO) #40 concerning retesting of a condensate
'
i.              demineralizer outlet sample throttling valve following rework.                  The NRC
l                inspector reviewed appropriate test documentation including Work Request
                (WR) 14140-84 and found test data for the reworked valve acceptable.
                (Closed) Open Item (482/8511-13):        This item involved RD #61 concerning an
                inability to perform Section 7.8 of Test SU3-HA01 due to equipment
                problems with the hydrogen and oxygen analyzers in the purge line from the
,
    e-      --                      n    ,,.. ,, ,          -    ----,-w-,- - - - _ . - , - - -      . - - - -
                                                                                                                e- n- e ,
 
p
                                                                                                    -
    .
  *
  .
                                                  -4-
l
                                                                                                      l
                                                                                                      l
                                                                                                      1
      volume control tank (VCT) to the gaseous radwaste system. The licensee
t
        requested and the NRC granted an extension of the completion of this item
        from prior to Mode 4 entry to prior to Mode 2 entry. The analyzers as
      presently installed meet Technical Specifications (TS) requirements due to
        their ability to be operated in manual; however, due to equipment procure-
      ment problems they are not presently able to be run in automatic which
      would be required in order to clear the test deficiencies. This section
      of the test can be deferred until prior to entry into Mode 2 for the
      reasons stated above.            This will be tracked as an open item.        (482/8519-03)
      (Closed) Open Item (482/8511-04):                  This item involved installation of the
      essential service water chlorination system prior to Mode 4. The NRC
      ' inspector walked down parts of the installed chlorination system,
      questioned plant operators on the operability of the chlorination system,
      reviewed Interim Design Change Package (IDCP) M-142KT, reviewed Field
      Change Work Plan 1-FJ-108-034, reviewed Field Change Request
      (FCR) 1-0303-H, and reviewed WRs on the installation and testing of the
      chlorination system.
      (Closed) Open Item (482/8511-21): This item involved RD #65 concerning
      computer calculation problems of. determining leakage rates into the
      auxiliary building and residual heat removal pump room (RHR) sumps. The
      NRC inspector reviewed the documentation of the retest to SU3-88158, Test
      Deficiency Reports (TDR) 01 and 02 and found it acceptable.
      (Closed) Open Item (482/8511-14): This item involved RD #66 concerning-
      computer calculation problems of determining leakage rates into the
      containment normal sumps.              The NRC inspector reviewed the documentation of
      the retest to 503-B8158, TDR-04 to the Test Deficiencies (TD) 010 and 017
      and found it acceptable.
      (Closed) Open Item (482/8511-07):                  This item involved completion of the
      reapplication of the concrete coatings removed on the 2000' elevations of
      containment as a result of 10 CFR 50.55(e) Report TE53564-K159. After the
      NRC inspector was informed by the licensee, the reapplication was
      complete, he toured the 2000' elevation of containment and reviewed
      appropriate WRs and found them acceptable.
      (Closed) Open Item (842/8427-06): This item tracked licensee evaluation
      of excess reactor coolant pump (RCP) seal leakage on the Number 1 seals of
      C and D RCPs          This evaluation was performed. It concluded that the seal
      surfaces had rubbed, but no cause could be definitely established.
      Foreign material contamination was ruled out. The seals were replaced and
      performed satisfactorily. This item was incorrectly referenced as
      482/8427-01 in Inspection Report 50-482/85-04.
;
l
l
                    - . . -      . . - -          - _ _ -              - --  -      --    - _. _-
 
{
!
      -
  '
    .
                                                  -5-
        3.    Compliance With TS
            .Through in plant inspections of system lineups, control room valve and
            breaker indications, review of control room logs, calibration data, and
            plant records,.the NRC. inspectors verified compliance with the following
            TS:
            -
                    3.1.1.1 - Boration Control-Shutdown Margin
            -
                    3.1.1.2 - Boration Control-Shutdown Margin
            -
                    3.1.2.1 - Boration Control-Shutdown Flow Path
            -
                    3.1.2.3 - Boration Control-Charging Pump
                    3.1.2.5 - Boration Control-Borated Water Source
            -
                -
                    3.4.1.2 - Reactor Coolant System-Hot Standby
            -
                  ~3.4.1.3 - Reactor Coolant System-Hot Shutdown
          ' - -
                    3.4.1.4.1 - Reactor Coolant System-Cold Shutdown
            -
                    3.4.4 - Reactor Coolant System-Relief Valves
            -
            -
                    3.4.9.3 - Reactor Coolant System-Overpressure Protection Systems
                    3.5.4 - Emergency Core Cooling Systems-ECCS Subsystem
                    3.5.5 - Emergency Core Cooling Systems-Refueling Water Storage Tank
            -
            No violations or deviations were identified.
        4.  Event Followup
            a.    The NRC inspector reviewed selected Wolf Creek events to determine:
                    -
                          Adequacy of response
                    -
                          Adequacy of analysis to determine cause
                    -
                          Adequacy of corrective action to prevent recurrence
                    The following Wolf Creek Event Reports were reviewed:
                    -
                          85-15 - Manual Aux. Transformer Deluge With Failure Of
                                  Electric Fire Pump To Start
                  -
                          85-16 - Inadvertent Closing Of EJ HV8701B While RHR Pump B Was
                                  Running
                    -
                          85-25 - Procedural Noncompliance
                    -
                          85-31'--Failure of GK RE-4
                    -
                          85-34 - Administrative Error Per ADM 01-070
                    -
                          85-40 - Timely PSRC Approval Not Obtained For Temporary
                                  Procedure Changes
                  -
                          85-41 - Start of STS-901 Without Shift Supervisor Approval
                  -
                          85-42 - Excessive Pressurizer Heatup Rate
                  -
                          85-44 - Control Room A/C Inlet Damper Blocked Closed
                  -
                          85-45 - Rod Speed Indicator Found Inoperative
                  -
                          85-48 - Reactor Trip Breaker Failed To Open Due To Switch Not
                                  Actuated Hard Enough
                  --
                          85-49 - STS MT-024 and STS MT-025 Used Beyond One Time Issue
                                  Date
_.
 
y              -
    .
  .
                                          -6-
            -
                    85-51 - Off Loading Of NA0H
            -
                    85-52 - Loss Of Paperwork (Containment Purge Permit CPP
                            No. 001)
            -
                    85-53 - Clearance Of Temporary Modification Prior To Issuance
                            Of PMR
            -
                    85-54 - Two Year Maintenance On Air Operated 3" Globe Valve
                            BMFV054
        b.  The following defect / deficiency reports were reviewed:
            -
                  85-10 - Excessive Vibration On EJ FO-3
            --
                  85-12 - Inadvertent Control Room Ventilation Isolation Signal
                            (CRVIS)
            -
                  85-19 - Containment Sump Screens
            -
                  85-20 - Ruskin Horizontal Dampers-Stitch Welds
            -
                  85-21 - Conduit Fire Barriers / Gas Seals
            -
                  85-22 - Inadvertent Reset Of Steam Line SI-Causing SI Train B
            -
                  85-23 - Failure Of Valve Operator EFHV-60 Caused By Broken Lug
            -
                  85-24 - CRVIS Due To Chlorine Monitor GK AI-2 Running Out
                            Of Paper
        c.  The following licensee event reports (LERs) were reviewed:
            -
                  50-482/85-001-00 - Engineered safety feature actuation
            -
                  50-482/85-002-00 - Technical Specifications violation
            -
                  50-482/85-003-00 - Engineered safety feature actuation
            -
                  50-482/85-004-00 - Technical Specifications violation
            -
                  50-482/85-005-00 - Technical Specifications violation
        Unless otherwise noted below, the NRC inspector had no comments,
        d.  During April, the licensee had three safety injections (SI).    All
            were inadvertent and due to low steam line pressure signals.    The
            following is a list of the dates, times, and modes in which they
            occurred:
            1.    April 19, 1985        16:19 CST      Mode 4
            2.    April 28, 1985        15:50 CDT      Mode 3
            3.    April 30, 1985        11:43 CDT      Mode 3
            The resident inspector was onsite during the three sis and responded
            to the control room as soon as he was notified. The NRC inspector
            verified the licensee had responded in accordance with procedures and
            notified the necessary agencies and personnel in a timely fashion.
            The plant operators responded to the sis in a calm, deliberate, and
            knowledgeable manner. During tne' April 28, 1985 SI, approximately 2
            hours after the event, the NRC inspector was performing a detailed
            review of all control room panels when he observed Annunciator F-79,
            " Loose Parts Monitor" energized. Upon questioning the supervising
            operator, the NRC inspector learned that the annunciator had been
            acknowledged without any control room personnel being aware it had
            "come in". An operator was sent to the loose parts monitor panel and
      .
.
 
m
                                                                                _.        -___ -
                                                                                                  -
          ..
  "
..
            .
          -
                                                  -7-
    .
                    reported a signal on Channel'2. ' Operations requested reactor
                    engineering personnel to investigate, and.it was verified that the
                  -noise was being heard on Channels.1, 2, and 4.      At this time, the
                    noise ~is a high frequency, low amplitude type which is indicative of
                    an object with a small mass or one which is restrained. The failure
                        -
                    to follow Alarm Procedure ALR 00-0079F is a violation.
                    (50-482/8519-02)
              e. .During this inspection the NRC inspector also followed up on the
                    following engineered safety features actuation events:
                    1.    ; April 7, 1985 10:38 CST Mode 5    Control Room Ventilation
                                                              Isolation (CRVIS) and Fuel
                                                              Building Isolation (FBIS)
                    2.      April 8, 1985 08:47 CST Mode 5    CRVIS
                    3. .    April 9, 1985 14:06 CST Mode 5    Containment Purge Isolation
                                                              (CPIS) and CRVIS
                    4.      April 12, 1985 22:15 CST Mode 5    CRVIS
                    5.      April 12,~ 1985 11:14 CST Mode 5  FBIS, CPIS, and CRVIS
                    6.-    April 21, 1985 19:22 CST Mode 4    CRVIS
;                  7.      April 26, 1985 18:54 CST Mode 3    Feedwater Isolation (FWIS)
                                                              and Auxiliary Feedwater
                                                              Actuation (AFAS)
              f.  On April 10, 1985, at approximately 1555 hours CST the central alarm
                    station (CAS) operator identified a problem with Door 31042-(access
                    from health physics area to auxiliary building) and dispatched an
,                  officer to.that location. Upon arrival, the officer found 10 to 15
                    individuals waiting for. access through the door. Apparently, no one
                    had identified an access problem to security. A number of
                    individuals had apparently entered the auxiliary building when other
                    individuals exited as the card reader had not been operating
                  -properly. The_CAS operator dispatched an officer to the scene after
                    several individuals had requested computer overrides to allow then to
                    exit the auxiliary building.
                    The CAS operator incorrectly assumed the locking mechanism was not
                    operating properly, when the dispatched officer could not' gain access
                    through the door, and placed it in access.. He directed the officer
                    to ensure everyone was'using the card reader. Approximately 20
                    minutes later, a second CAS operator decided the card reader was
                    inoperable and directed the officer at the scene to initiate a manual
                                        ~
                    access log. All personnel who had entered the auxiliary building
i                  during this incident were identified and found to have access
;                  authorization.
                    The NRC inspector discussed with the plant superintendent the
,                  apparent slow response in discovering the problem and lack of
:                  training and/or concern for security. The plant superintendent                  I
{                  stated that he would have al1~ individuals involved in the incident
[.                  interviewed to determine why they had not contacted security when
l                  they were having access problems.
l                                                                                                    \
                                                                                                    l
E      ._                                                                                          ;
 
.c_                                                                                  _
      .
    b
                                            -8-
        5. Startup Test Witnessing and Observation
          The NRC inspectors observed portions of the following startup tests:
          -
          -
                SU7-SF03.1 - Cold No Flow Control Rod System Testing
          -
                SU7-SF03.2 - Cold Full Flow Control Rod System Testing
                SU7-SR03 - Incore Movable Detector Test
          -
                SU7-0015 - Power Ascension Thermal and Dynamic Test
          -
          -
                SU8-BB13 - Pressurizer Relief Valve Test
                STS-PE19 - Reactor Coolant System Isolation Valve Leakage
          The NRC inspectors verified conformance by the licensee to procedural and
          license requirements, observed the performance of the plant operating
          staff and verified the adequacy of test program records, including
          preliminary evaluation of the test results.
          No violations or deviations were identified.
        6. Precritical Testing Data Review
          The NRC inspectors reviewed the following completed test procedures to
          ascertain compliance with administrative and test procedures and
          conformance to Final Safety Analysis Report (FSAR) and Technical
          Specifications requirements:
          -
          -
                SU7-0001 - Initial Core Loading
                SU7-0002 - Inverse Count Rate Ratio Monitoring For Core Loading
          -
                5U7-5009 - Initial Core Loading
          -
                SU7-SE02.1 - Operational Alignment Of Nuclear Instrumentation
          -
                SU7-SC01 - Core Loading Instrumentation and Neutron Source
                            Requirements
          -
                SU7-SR03 - Incore Movable Detector Test
          Selected NRC inspector comments are noted below:
          During the review of SU7-5009, the inspector noted that steps 4.1, " Core
          loading operations shall be suspended, pending evaluation by the senior
          reactor operator (SRO) in charge of refueling, who has no concurrent
          responsibilities, and reactor engineering personnel, if any of the
          following conditions occur during core loading" and 4.1.8 "Less than two
  ,
  '        of the nuclear channels being used for inverse count rate ratio ICRR
          monitoring have counting rates greater than or equal to 2 counts per
          second (af ter both primary source-bearing assemblies are loaded in the
          vessel and completion of core loading step 10)" were written so as to be
          vague enough to allow test and operations personnel to exceed the
i          limitations desired by the plant safety review committee (PSRC) and the
          Plant Manager. Although this did not occur during the performance of this
          test, the inspectors concern was that it could happen during a future
          refueling operation. The licensee stated that this statement was not in
l
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                                          -9-
        the procedure to be used for the refueling operation and they committed
        that if they wanted to place it in that procedure, appropriate limitations
        and precautions would be taken.    All NRC inspector concerns with this
        procedure have been resolved.
        No violations or deviations were identified.
      7. Plant Tours
        Control room activities were observed on a regular basis including several
        shift turnovers. Special emphasis was placed on verifying implementation
        of administrative controls for fire protection, temporary modifications,
        and out of-service equipment.    Compliance with TS and limiting conditions
        for operations were verified as appropriate.
        The NRC inspector observed that although WCGS Administrative Procedure ADM
        13-102, Rev. 4, requires an expiration date for combustible materials
        permits in step 5.2.1, the form in use does not have a block for this          i
        date. The Superintendent of Plant Support committed to making the              '
        procedure and form compatible. This will be tracked as an open item.
        (482/8519-03)
        On April 2, 1985, the NRC inspector noted the following unusual
        indications which he discussed with the supervising operator:
        -
              345 Kv west bus indicating light was blinking
        -
              No status lights were illuminated for Breaker 69-16
        The supervising operator stated that these conditions would be promptly
        corrected or work requests would be issued and the indicating lights
        status tagged.    The NRC inspector verified that this had been
        accomplished.
        No violations or deviations were identified.
      8. Document Control
        The NRC inspector conducted an audit of WCGS Procedure Manuals and
        Drawings located in the TSC and EOF on April 10 and 11, 1985, in response
        to expressed concerns. Documents surveyed were randomly selected from the
        KG&E master drawing file index and the computer based master procedure
        index. Sixteen drawings were selected and the correct revision levels
        were found at either location. Of 46 procedures selected, the NRC
        inspector identified problems with nine at the TSC and fifteen at the EOF
        as follows:
        a.    TSC
              1.  Temporary Change Notice (TCN) MI 85-162 was not filed with
                    Procedure CHM 01-004, Rev. 1.
!
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    ,
                                              -10-
                          >
<
                  2.    Rev. O with a'TCN was also filed with Rev. 1 of Procedure
l                    . CHM 01-007, Rev. 1.
                3.    TCN MI.85-224 was not~ filed with Procedure CHM 02-480, Rev. 4.
                .4.    TCN MI 85-115 was not filed with Procedure SYS A8-120, Rev. 4.
                5.    TCNs MA 85-594 and MA 85-611 were not filed with Procedure SYS
                        88-201, Rev. 4.
                  6.    TCNs MA 85-486 and MA 85-669 were not filed with Procedure SYS
      -
                        EF-200, Rev. 5,
                7.    Expired TCN 84-277 was filed with Procedure SYS GT-121, Rev. 3.
                8.    .TCN MA 85-422 was not filed with and expired TCN 84-307 was
                        filed with Procedure SYS NB-201, Rev. 3.
                9.    Expired TCN 84-361 was filed with Procedure SYS NG-131, Rev.-3.
            b.  EOF
,                1.    Two expired TCNs were filed with Procedure GEN 00-005, Rev. 2.
;
'
                2.    Two expired TCNs were filed with Procedure GEN 00-006, Rev. 4.
                3.    TCN MA 85-220 was not filed with, Procedure EMG FR-C1, Rev. O.
l                4.    TCN MA 85-084 was not filed with Procedure EMG C-31, Rev. O.
i                5.    TCNs MA 85-087, 217, and 439 were not filed with Procedure
                        EMG E-0, Rev. O.
                6.    TCNs MA 85-088 and 218 were not filed with Procedure EMG E-1,
;.                      Rev. O.
                            .
I
                7.    TCNs MA 85-089 and 219 were not filed with Procedure'EMG E-3,      l
                        Rev. O.
                8.    TCN MI 85-162 was not filed with Procedure CHM 01-004, Rev. 1.
                9.    An expired TCN was filed with Procedure CHM 01-007, Rev. 1.
!                10.    TCN MI 85-224 was not filed with Procedure CHM 02-480,.Rev. 4.
!    p          11.    Procedure SYS AB-120 should have been Rev. 4 with TCN MI
l0                      85-115.                                                        <
l                12.  TCNs MA 85-486 and 669 were not filed with Procedure SYS EF-200,
!                      Rev. 5.
,                13. Procedure SYS EP-200 should have been Rev. I with TCN MA 85-539.
'
                      Only Rev. O was found.
                14. An expired TCN was found with SYS NG-131. Rev. 3.
                15. - Procedure HPH 01-017 should have been Rev. 1. Only Rev. O was
l                      found.
,
l                The above findings were discussed with the licensee site emergency
l                planning coordinator, who accompanied the NRC inspector during the
;                audit, and the Superintendent of Regulatory, Quality, and
l              -Administrative Services committed to the following corrective
!                actions:
                -
                      The licensee will perform a 100 percent review of WCGS
                      procedures located at the EOF and TSC and correct any
                      . discrepancies found prior to April 30, 1985.
le
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~
                                                                                            l
      .
    .
                                              -11-
                  -
                        KG&E Document Control will assign an individual to be
                        responsible for drawings and procedures in the EOF and TSC.
                  -
                        Periodic surveillances will be performed in accordance with WCGS
                        Administrative Procedure ADM 07-100 for WCGS procedures located
                        at the E0F and TSC and any deficiencies found will be corrected.
            The above findings constitute a violation of NRC regulations.
            (482/8519-01)
        9.  Open Items _
            Open items are matters which have been discussed with the licensee, which
            will be reviewed further by the inspector. and which involve some action
            on the part of the NRC or licensee or bot..        An open item disclosed during
            the inspections is discussed in paragraph i.
        10. Exit Meeting
  s
            The NRC inspectors met with licensee personnel to discuss the scope and
            findings of this inspection on April 30, 1985.
}}
}}

Latest revision as of 01:41, 23 July 2020

Insp Rept 50-482/85-19 on 850401-30.Violation Noted: Failure to Properly Update Procedure Manuals & to Respond to Control Room Annunciator
ML20133G592
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 07/08/1985
From: Bruce Bartlett, Bundy H, Cummins J, Martin L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20133G582 List:
References
50-482-85-19, NUDOCS 8508080762
Download: ML20133G592 (11)


See also: IR 05000482/1985019

Text

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APPENDIX B

US NUCLEAR REGULATORY COMMISSION

NRC Inspection Report: 50-482/85-19 LP: NPF-32

Docket: 50-482

Licensee: Kansas Gas and Electric Company (KG&E)

Post Office Box 208

Wichita, Kansas 67201

Facility Name: Wolf Creek Generating Station (WCGS)

Inspection At: Wolf Creek Site, Coffey County, Burlington, Kansas

Inspection Conducted: April 1 to 30,1985

Inspectors: f~

J. Ef Cummins, S' for~1sactor Inspector,

- f/f/f4

/Dpfe

Operations,-

(pars. 2 and

Yf $

gBFL< Bartlett,'R(s e'nt' Reactor Inspector,

[DAe

Operations,

(pars 2, 3, 4, , 6, and 7)

/'-26~ W

H. F. Bundy, Resident Reactor InTpector, Date

Operations,

(pars. 2, 4, 5, 6, 7, and 8)

Approved: ,

7 fc5

. ET MarTiri, Chid ,' Project Section A /Dge

Reactor Project anch 2

,

8508080762 850726

PDR ADOCK 05000482

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inspection Summary

Inspection Conducted April 1-to 30, 1985 (Report 50-482/85-19)

Areas Inspected: Routine, unannounced inspection including licensee actions on

previous inspection: findings; compliance with Technical Specifications; event

followup; startup test witnessing.and observation; plant tours; precritical

testing data review; and document control.

The inspection involved 342 inspector-hours onsite by three NRC inspectors

including 56 inspector-hours onsite during offshifts.

Results: Within the seven areas inspected, two violations were identified

(failure to properly ~ update procedure manuals, paragraph 8 and failure to

respond to control room annunciator, paragraph 4). One open item is

identified in paragraph 7).  ;

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DETAILS

- 1. Persons Contacted

Principal Licensee Personnel

  • R. M. Grant, Director-Quality
  • F. T. Rhodes, Plant Manager
  • C. C. Mason, Director-Nuclear Operations
  • M. G. Williams, Superintendent of Regulatory, Quality, and

Administrative Services

  • K. Peterson, Licensing
  • C. E. Parry, Superintendent of Quality Systems Engineer
  • C. J. Hoch, QA Technologist

V. MacTaggart, Results Engineering Supervisor

J. Johnson, Chief of Security

D. Smith, Plant Support Supervisor

J. Zell, Operations Superintendent

l

'

T. Gardner, Startup

O. Maynard, Licensing Manager

K. Ellison, Assistant to the Superintendent of Regulatory, Quality, and

Administrative Services

l * Denotes those attending the exit interview on April 30, 1985,

t

2. Licensee Actions on Previous Inspection Findings

(0 pen) Open Item (482/8515-01): Ruskin Fire Dampers: The licensee's

testing and rework of the Ruskin fire dampers has not been completed. By

g letter dated May 1, 1985, the licensee made a 10 CFR Part 21 Report to the

NRC Region IV office concerning the installation of some of the fire

'

i dampers with less than the designed clearance between the fire damper

' frame and the penetration sleeve. This insufficient clearance could cause

the fire damper to warp and become inoperative during a fire. This item

will remain open.

i (Closed) Open Item (482/8511-08): This item involved Preoperational Test

Deficiency Deferral (RO) #40 concerning retesting of a condensate

'

i. demineralizer outlet sample throttling valve following rework. The NRC

l inspector reviewed appropriate test documentation including Work Request

(WR) 14140-84 and found test data for the reworked valve acceptable.

(Closed) Open Item (482/8511-13): This item involved RD #61 concerning an

inability to perform Section 7.8 of Test SU3-HA01 due to equipment

problems with the hydrogen and oxygen analyzers in the purge line from the

,

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volume control tank (VCT) to the gaseous radwaste system. The licensee

t

requested and the NRC granted an extension of the completion of this item

from prior to Mode 4 entry to prior to Mode 2 entry. The analyzers as

presently installed meet Technical Specifications (TS) requirements due to

their ability to be operated in manual; however, due to equipment procure-

ment problems they are not presently able to be run in automatic which

would be required in order to clear the test deficiencies. This section

of the test can be deferred until prior to entry into Mode 2 for the

reasons stated above. This will be tracked as an open item. (482/8519-03)

(Closed) Open Item (482/8511-04): This item involved installation of the

essential service water chlorination system prior to Mode 4. The NRC

' inspector walked down parts of the installed chlorination system,

questioned plant operators on the operability of the chlorination system,

reviewed Interim Design Change Package (IDCP) M-142KT, reviewed Field

Change Work Plan 1-FJ-108-034, reviewed Field Change Request

(FCR) 1-0303-H, and reviewed WRs on the installation and testing of the

chlorination system.

(Closed) Open Item (482/8511-21): This item involved RD #65 concerning

computer calculation problems of. determining leakage rates into the

auxiliary building and residual heat removal pump room (RHR) sumps. The

NRC inspector reviewed the documentation of the retest to SU3-88158, Test

Deficiency Reports (TDR) 01 and 02 and found it acceptable.

(Closed) Open Item (482/8511-14): This item involved RD #66 concerning-

computer calculation problems of determining leakage rates into the

containment normal sumps. The NRC inspector reviewed the documentation of

the retest to 503-B8158, TDR-04 to the Test Deficiencies (TD) 010 and 017

and found it acceptable.

(Closed) Open Item (482/8511-07): This item involved completion of the

reapplication of the concrete coatings removed on the 2000' elevations of

containment as a result of 10 CFR 50.55(e) Report TE53564-K159. After the

NRC inspector was informed by the licensee, the reapplication was

complete, he toured the 2000' elevation of containment and reviewed

appropriate WRs and found them acceptable.

(Closed) Open Item (842/8427-06): This item tracked licensee evaluation

of excess reactor coolant pump (RCP) seal leakage on the Number 1 seals of

C and D RCPs This evaluation was performed. It concluded that the seal

surfaces had rubbed, but no cause could be definitely established.

Foreign material contamination was ruled out. The seals were replaced and

performed satisfactorily. This item was incorrectly referenced as

482/8427-01 in Inspection Report 50-482/85-04.

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- . . - . . - - - _ _ - - -- - -- - _. _-

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3. Compliance With TS

.Through in plant inspections of system lineups, control room valve and

breaker indications, review of control room logs, calibration data, and

plant records,.the NRC. inspectors verified compliance with the following

TS:

-

3.1.1.1 - Boration Control-Shutdown Margin

-

3.1.1.2 - Boration Control-Shutdown Margin

-

3.1.2.1 - Boration Control-Shutdown Flow Path

-

3.1.2.3 - Boration Control-Charging Pump

3.1.2.5 - Boration Control-Borated Water Source

-

-

3.4.1.2 - Reactor Coolant System-Hot Standby

-

~3.4.1.3 - Reactor Coolant System-Hot Shutdown

' - -

3.4.1.4.1 - Reactor Coolant System-Cold Shutdown

-

3.4.4 - Reactor Coolant System-Relief Valves

-

-

3.4.9.3 - Reactor Coolant System-Overpressure Protection Systems

3.5.4 - Emergency Core Cooling Systems-ECCS Subsystem

3.5.5 - Emergency Core Cooling Systems-Refueling Water Storage Tank

-

No violations or deviations were identified.

4. Event Followup

a. The NRC inspector reviewed selected Wolf Creek events to determine:

-

Adequacy of response

-

Adequacy of analysis to determine cause

-

Adequacy of corrective action to prevent recurrence

The following Wolf Creek Event Reports were reviewed:

-

85-15 - Manual Aux. Transformer Deluge With Failure Of

Electric Fire Pump To Start

-

85-16 - Inadvertent Closing Of EJ HV8701B While RHR Pump B Was

Running

-

85-25 - Procedural Noncompliance

-

85-31'--Failure of GK RE-4

-

85-34 - Administrative Error Per ADM 01-070

-

85-40 - Timely PSRC Approval Not Obtained For Temporary

Procedure Changes

-

85-41 - Start of STS-901 Without Shift Supervisor Approval

-

85-42 - Excessive Pressurizer Heatup Rate

-

85-44 - Control Room A/C Inlet Damper Blocked Closed

-

85-45 - Rod Speed Indicator Found Inoperative

-

85-48 - Reactor Trip Breaker Failed To Open Due To Switch Not

Actuated Hard Enough

--

85-49 - STS MT-024 and STS MT-025 Used Beyond One Time Issue

Date

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85-51 - Off Loading Of NA0H

-

85-52 - Loss Of Paperwork (Containment Purge Permit CPP

No. 001)

-

85-53 - Clearance Of Temporary Modification Prior To Issuance

Of PMR

-

85-54 - Two Year Maintenance On Air Operated 3" Globe Valve

BMFV054

b. The following defect / deficiency reports were reviewed:

-

85-10 - Excessive Vibration On EJ FO-3

--

85-12 - Inadvertent Control Room Ventilation Isolation Signal

(CRVIS)

-

85-19 - Containment Sump Screens

-

85-20 - Ruskin Horizontal Dampers-Stitch Welds

-

85-21 - Conduit Fire Barriers / Gas Seals

-

85-22 - Inadvertent Reset Of Steam Line SI-Causing SI Train B

-

85-23 - Failure Of Valve Operator EFHV-60 Caused By Broken Lug

-

85-24 - CRVIS Due To Chlorine Monitor GK AI-2 Running Out

Of Paper

c. The following licensee event reports (LERs) were reviewed:

-

50-482/85-001-00 - Engineered safety feature actuation

-

50-482/85-002-00 - Technical Specifications violation

-

50-482/85-003-00 - Engineered safety feature actuation

-

50-482/85-004-00 - Technical Specifications violation

-

50-482/85-005-00 - Technical Specifications violation

Unless otherwise noted below, the NRC inspector had no comments,

d. During April, the licensee had three safety injections (SI). All

were inadvertent and due to low steam line pressure signals. The

following is a list of the dates, times, and modes in which they

occurred:

1. April 19, 1985 16:19 CST Mode 4

2. April 28, 1985 15:50 CDT Mode 3

3. April 30, 1985 11:43 CDT Mode 3

The resident inspector was onsite during the three sis and responded

to the control room as soon as he was notified. The NRC inspector

verified the licensee had responded in accordance with procedures and

notified the necessary agencies and personnel in a timely fashion.

The plant operators responded to the sis in a calm, deliberate, and

knowledgeable manner. During tne' April 28, 1985 SI, approximately 2

hours after the event, the NRC inspector was performing a detailed

review of all control room panels when he observed Annunciator F-79,

" Loose Parts Monitor" energized. Upon questioning the supervising

operator, the NRC inspector learned that the annunciator had been

acknowledged without any control room personnel being aware it had

"come in". An operator was sent to the loose parts monitor panel and

.

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reported a signal on Channel'2. ' Operations requested reactor

engineering personnel to investigate, and.it was verified that the

-noise was being heard on Channels.1, 2, and 4. At this time, the

noise ~is a high frequency, low amplitude type which is indicative of

an object with a small mass or one which is restrained. The failure

-

to follow Alarm Procedure ALR 00-0079F is a violation.

(50-482/8519-02)

e. .During this inspection the NRC inspector also followed up on the

following engineered safety features actuation events:

1.  ; April 7, 1985 10:38 CST Mode 5 Control Room Ventilation

Isolation (CRVIS) and Fuel

Building Isolation (FBIS)

2. April 8, 1985 08:47 CST Mode 5 CRVIS

3. . April 9, 1985 14:06 CST Mode 5 Containment Purge Isolation

(CPIS) and CRVIS

4. April 12, 1985 22:15 CST Mode 5 CRVIS

5. April 12,~ 1985 11:14 CST Mode 5 FBIS, CPIS, and CRVIS

6.- April 21, 1985 19:22 CST Mode 4 CRVIS

7. April 26, 1985 18
54 CST Mode 3 Feedwater Isolation (FWIS)

and Auxiliary Feedwater

Actuation (AFAS)

f. On April 10, 1985, at approximately 1555 hours0.018 days <br />0.432 hours <br />0.00257 weeks <br />5.916775e-4 months <br /> CST the central alarm

station (CAS) operator identified a problem with Door 31042-(access

from health physics area to auxiliary building) and dispatched an

, officer to.that location. Upon arrival, the officer found 10 to 15

individuals waiting for. access through the door. Apparently, no one

had identified an access problem to security. A number of

individuals had apparently entered the auxiliary building when other

individuals exited as the card reader had not been operating

-properly. The_CAS operator dispatched an officer to the scene after

several individuals had requested computer overrides to allow then to

exit the auxiliary building.

The CAS operator incorrectly assumed the locking mechanism was not

operating properly, when the dispatched officer could not' gain access

through the door, and placed it in access.. He directed the officer

to ensure everyone was'using the card reader. Approximately 20

minutes later, a second CAS operator decided the card reader was

inoperable and directed the officer at the scene to initiate a manual

~

access log. All personnel who had entered the auxiliary building

i during this incident were identified and found to have access

authorization.

The NRC inspector discussed with the plant superintendent the

, apparent slow response in discovering the problem and lack of

training and/or concern for security. The plant superintendent I

{ stated that he would have al1~ individuals involved in the incident

[. interviewed to determine why they had not contacted security when

l they were having access problems.

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5. Startup Test Witnessing and Observation

The NRC inspectors observed portions of the following startup tests:

-

-

SU7-SF03.1 - Cold No Flow Control Rod System Testing

-

SU7-SF03.2 - Cold Full Flow Control Rod System Testing

SU7-SR03 - Incore Movable Detector Test

-

SU7-0015 - Power Ascension Thermal and Dynamic Test

-

-

SU8-BB13 - Pressurizer Relief Valve Test

STS-PE19 - Reactor Coolant System Isolation Valve Leakage

The NRC inspectors verified conformance by the licensee to procedural and

license requirements, observed the performance of the plant operating

staff and verified the adequacy of test program records, including

preliminary evaluation of the test results.

No violations or deviations were identified.

6. Precritical Testing Data Review

The NRC inspectors reviewed the following completed test procedures to

ascertain compliance with administrative and test procedures and

conformance to Final Safety Analysis Report (FSAR) and Technical

Specifications requirements:

-

-

SU7-0001 - Initial Core Loading

SU7-0002 - Inverse Count Rate Ratio Monitoring For Core Loading

-

5U7-5009 - Initial Core Loading

-

SU7-SE02.1 - Operational Alignment Of Nuclear Instrumentation

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SU7-SC01 - Core Loading Instrumentation and Neutron Source

Requirements

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SU7-SR03 - Incore Movable Detector Test

Selected NRC inspector comments are noted below:

During the review of SU7-5009, the inspector noted that steps 4.1, " Core

loading operations shall be suspended, pending evaluation by the senior

reactor operator (SRO) in charge of refueling, who has no concurrent

responsibilities, and reactor engineering personnel, if any of the

following conditions occur during core loading" and 4.1.8 "Less than two

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' of the nuclear channels being used for inverse count rate ratio ICRR

monitoring have counting rates greater than or equal to 2 counts per

second (af ter both primary source-bearing assemblies are loaded in the

vessel and completion of core loading step 10)" were written so as to be

vague enough to allow test and operations personnel to exceed the

i limitations desired by the plant safety review committee (PSRC) and the

Plant Manager. Although this did not occur during the performance of this

test, the inspectors concern was that it could happen during a future

refueling operation. The licensee stated that this statement was not in

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the procedure to be used for the refueling operation and they committed

that if they wanted to place it in that procedure, appropriate limitations

and precautions would be taken. All NRC inspector concerns with this

procedure have been resolved.

No violations or deviations were identified.

7. Plant Tours

Control room activities were observed on a regular basis including several

shift turnovers. Special emphasis was placed on verifying implementation

of administrative controls for fire protection, temporary modifications,

and out of-service equipment. Compliance with TS and limiting conditions

for operations were verified as appropriate.

The NRC inspector observed that although WCGS Administrative Procedure ADM

13-102, Rev. 4, requires an expiration date for combustible materials

permits in step 5.2.1, the form in use does not have a block for this i

date. The Superintendent of Plant Support committed to making the '

procedure and form compatible. This will be tracked as an open item.

(482/8519-03)

On April 2, 1985, the NRC inspector noted the following unusual

indications which he discussed with the supervising operator:

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345 Kv west bus indicating light was blinking

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No status lights were illuminated for Breaker 69-16

The supervising operator stated that these conditions would be promptly

corrected or work requests would be issued and the indicating lights

status tagged. The NRC inspector verified that this had been

accomplished.

No violations or deviations were identified.

8. Document Control

The NRC inspector conducted an audit of WCGS Procedure Manuals and

Drawings located in the TSC and EOF on April 10 and 11, 1985, in response

to expressed concerns. Documents surveyed were randomly selected from the

KG&E master drawing file index and the computer based master procedure

index. Sixteen drawings were selected and the correct revision levels

were found at either location. Of 46 procedures selected, the NRC

inspector identified problems with nine at the TSC and fifteen at the EOF

as follows:

a. TSC

1. Temporary Change Notice (TCN) MI 85-162 was not filed with

Procedure CHM 01-004, Rev. 1.

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2. Rev. O with a'TCN was also filed with Rev. 1 of Procedure

l . CHM 01-007, Rev. 1.

3. TCN MI.85-224 was not~ filed with Procedure CHM 02-480, Rev. 4.

.4. TCN MI 85-115 was not filed with Procedure SYS A8-120, Rev. 4.

5. TCNs MA 85-594 and MA 85-611 were not filed with Procedure SYS88-201, Rev. 4.

6. TCNs MA 85-486 and MA 85-669 were not filed with Procedure SYS

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EF-200, Rev. 5,

7. Expired TCN 84-277 was filed with Procedure SYS GT-121, Rev. 3.

8. .TCN MA 85-422 was not filed with and expired TCN 84-307 was

filed with Procedure SYS NB-201, Rev. 3.

9. Expired TCN 84-361 was filed with Procedure SYS NG-131, Rev.-3.

b. EOF

, 1. Two expired TCNs were filed with Procedure GEN 00-005, Rev. 2.

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2. Two expired TCNs were filed with Procedure GEN 00-006, Rev. 4.

3. TCN MA 85-220 was not filed with, Procedure EMG FR-C1, Rev. O.

l 4. TCN MA 85-084 was not filed with Procedure EMG C-31, Rev. O.

i 5. TCNs MA 85-087, 217, and 439 were not filed with Procedure

EMG E-0, Rev. O.

6. TCNs MA 85-088 and 218 were not filed with Procedure EMG E-1,

. Rev. O.

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7. TCNs MA 85-089 and 219 were not filed with Procedure'EMG E-3, l

Rev. O.

8. TCN MI 85-162 was not filed with Procedure CHM 01-004, Rev. 1.

9. An expired TCN was filed with Procedure CHM 01-007, Rev. 1.

! 10. TCN MI 85-224 was not filed with Procedure CHM 02-480,.Rev. 4.

! p 11. Procedure SYS AB-120 should have been Rev. 4 with TCN MI

l0 85-115. <

l 12. TCNs MA 85-486 and 669 were not filed with Procedure SYS EF-200,

! Rev. 5.

, 13. Procedure SYS EP-200 should have been Rev. I with TCN MA 85-539.

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Only Rev. O was found.

14. An expired TCN was found with SYS NG-131. Rev. 3.

15. - Procedure HPH 01-017 should have been Rev. 1. Only Rev. O was

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l The above findings were discussed with the licensee site emergency

l planning coordinator, who accompanied the NRC inspector during the

audit, and the Superintendent of Regulatory, Quality, and

l -Administrative Services committed to the following corrective

! actions:

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The licensee will perform a 100 percent review of WCGS

procedures located at the EOF and TSC and correct any

. discrepancies found prior to April 30, 1985.

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KG&E Document Control will assign an individual to be

responsible for drawings and procedures in the EOF and TSC.

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Periodic surveillances will be performed in accordance with WCGS

Administrative Procedure ADM 07-100 for WCGS procedures located

at the E0F and TSC and any deficiencies found will be corrected.

The above findings constitute a violation of NRC regulations.

(482/8519-01)

9. Open Items _

Open items are matters which have been discussed with the licensee, which

will be reviewed further by the inspector. and which involve some action

on the part of the NRC or licensee or bot.. An open item disclosed during

the inspections is discussed in paragraph i.

10. Exit Meeting

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The NRC inspectors met with licensee personnel to discuss the scope and

findings of this inspection on April 30, 1985.