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See also: [[followed by::IR 05000272/1989017]]


=Text=
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{{#Wiki_filter:' ' * Public Service Electric and Gas Company Stanley LaBruna Public Service Electric and Gas Company P.O. Box 236. Hancocks Bridge, NJ 08038 609-339-4800  
{{#Wiki_filter:' '
Vice President  
* Public Service Electric and Gas Company Stanley LaBruna Public Service Electric and Gas Company P.O. Box 236. Hancocks Bridge, NJ 08038 609-339-4800 Vice President  
-Nuclear Operations  
-Nuclear Operations
* AUG 0 2 1989 NLR-N89149  
* AUG 0 2 1989 NLR-N89149 United States Nuclear Regulatory Commission Document Control Desk Washington DC 20555 Gentlemen:
United States Nuclear Regulatory  
RESPONSE TO NOTICE OF VIOLATION NRC INSPECTION NO. 50-272/89-17 SALEM GENERATING STATION UNIT NO. 1 DOCKET NOS. 50-272 Public Service Electric and Gas Company (PSE&G) has received the subject inspection report dated July 3, 1989, which included a Notice of Violation concerning failure to notify the NRC within four hours and failure to have SORC review a procedure that contained an SSI. Pursuant to the requirements of 10 CFR 2.201, our response to this Notice of Violation is provided in the attachment to this letter. Should you have any questions in regards to this transmittal, do not hesitate to call. Attachment Sincerely, s. LaBruna Vice President  
Commission  
Document Control Desk Washington  
DC 20555 Gentlemen:  
RESPONSE TO NOTICE OF VIOLATION  
NRC INSPECTION  
NO. 50-272/89-17  
SALEM GENERATING  
STATION UNIT NO. 1 DOCKET NOS. 50-272 Public Service Electric and Gas Company (PSE&G) has received the subject inspection  
report dated July 3, 1989, which included a Notice of Violation  
concerning  
failure to notify the NRC within four hours and failure to have SORC review a procedure  
that contained  
an SSI. Pursuant to the requirements  
of 10 CFR 2.201, our response to this Notice of Violation  
is provided in the attachment  
to this letter. Should you have any questions  
in regards to this transmittal, do not hesitate to call. Attachment  
Sincerely, s. LaBruna Vice President  
-Nuclear Operations   
-Nuclear Operations   
.. * * * Document Control Desk NLR-N89149  
.. * *
C Mr. J. c. Stone Licensing  
* Document Control Desk NLR-N89149 C Mr. J. c. Stone Licensing Project Manager Ms. K. Halvey Gibson Senior Resident Inspector 2 Mr. w. T. Russell, Administrator Region I Mr. Kent Tosch, Chief New Jersey Department of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625 AUG 0 2 1989 J .. * *
Project Manager Ms. K. Halvey Gibson Senior Resident Inspector  
* ATTACHMENT 1   
2 Mr. w. T. Russell, Administrator  
Region I Mr. Kent Tosch, Chief New Jersey Department  
of Environmental  
Protection  
Division of Environmental  
Quality Bureau of Nuclear Engineering  
CN 415 Trenton, NJ 08625 AUG 0 2 1989
J .. * * * ATTACHMENT  
1   


1 VIOLATION  
1 VIOLATION A Technical Specification 6.8.2 requires that surveillance and test activity procedures shall be independently reviewed to make a determination as to whether the procedure contains a significant safety issue (SSI). Additionally, Technical Specification 6.5.1.6 requires that the Station Operations Review Committee (SORC) shall review procedures that involve an SSI. Contrary to the above, on May 20, 1989, Surveillance Procedure No. SP(0)4.0.5-V-SJ-6, "Inservice Testing -Valves -Safety Injection," which involved an SSI, injection of nitrogen into the reactor coolant system, was not reviewed by SORC. RESPONSE The test methodolbgy for the Accumulator discharge check valves was developed in 1982 to provide full stroke testing. This test method was developed to comply with an IST program submittal for NRC approval.
A Technical  
Inspection Report 50-272/82-23, issued on October 5, 1982, documents the inspectors review of the status of the Salem IST program in regards to the submittal.
Specification  
A major portion of the review was to finalize an NRC Staff evaluation of the submittal.
6.8.2 requires that surveillance  
The inspector reviewed the procedures and indicated that the minimum design flow rates were not identified in the test procedures and were needed to demonstrate the minimum safety analysis design flowrate criteria through the valves. Surveillance procedure SP(O) 4.0.5-V-REFUEL was developed for Units 1 and 2 to meet this requirement.
and test activity procedures  
The Safety Evaluation Report for the IST Program submittal was issued on April 12, 1983. In the evaluation section of the SER the NRC indicated that Salem should investigate a means to satisfy the NRC full-stroke exercise criteria (demonstrate safety analysis design flowrate through the check valves). SP(O) 4.0.5-V-REFUEL procedure provided the means to full flow test the check valves.for the IST Program. This procedure was reviewed by SORC in 1982 and again in 1984. When the SP(O) 4.0.5-V-REFUEL procedure was broken down into separate procedures as a procedural enhancement, during the two year review process, SP(O) 4.0.5-V-SJ-6 was developed.
shall be independently  
This procedure specifies the same testing methodology as the previous procedure and was reviewed by a Station Qualified Reviewer.
reviewed to make a determination  
The SQR determined that the procedure did not contain a SSI. The SQR was performing a two year review; therefore, he was reviewing the changes and comments with respect to the technical review. However, since he was aware that* the procedure was performed satisfactorily using the steps specified by the procedure and that the procedure had been   
as to whether the procedure  
*
contains a significant  
* SORC approved, he did not perform a full technical basis review of the old procedural steps. It did, however, receive the required two year review specified by procedure.
safety issue (SSI). Additionally, Technical  
When it was decided that the procedure should be separated to reduce the confusion involved with multiple tests covered by one procedure, it was felt that the steps were the same and thus the review performed was adequate.
Specification  
The procedures do not provide specific guidance on the exact review steps to perform if the two year review results in new procedures being developed to seperate an old procedure.
6.5.1.6 requires that the Station Operations  
In reviewing the guidance of AP-32, Implementing Procedures Program, the guidance provided would indicate that an SSI was not involved as the examples provided discuss revising the procedure for specific purposes.
Review Committee (SORC) shall review procedures  
In this case of the SP(O) 4.0.5-V-SJ6 procedure the revision was made to make the procedure more usable not to change order of steps or step method. Therefore, by the SS! criteria an SS! was not involved.
that involve an SSI. Contrary to the above, on May 20, 1989, Surveillance  
However, review of the incident did reveal that the original procedure (SP(0)4.0.5-REFUEL) should have required a 50.59 safety evaluation in that it did involve a change to the a test described in the FSAR. Corrective Actions Taken Use of the accumulator discharge procedure SP(0)4.0.5-V-SJ-6 was immediately discontinued.
Procedure  
The weaknesses with the SP(0)4.0.5-V-SJ-6 and AOP-RHR-1 procedures were reviewed with the Operations Procedure Writers. Corrective Actions to Prevent Recurrence PSE&G will evaluate the !ST Program to determine the appropriate method for testing the accumulator check valves. This will be determined by October 24, 1989. PSE&G will revise appropriate procedures for accumulator check valve test after method is determined, and ensure SORC review. To be completed by December 31, 1989. A training plan will be developed and procedures revised to incorporate the information and improvements provided by the Engineering and OSR evaluations of the event. This will be completed by September 29, 1989. PSE&G is currently developing an extensive procedure upgrade program that will ensure that high risk procedures are identified and that adequate precaution and human factor considerations are included .   
No. SP(0)4.0.5-V-SJ-6, "Inservice  
,\ To assist the procedure upgrade effort, PSE&G will establish an independent review group to perform SQR review to ensure that all commitments and 10CFR50.59 requirements are being met and maintained.
Testing -Valves -Safety Injection," which involved an SSI, injection  
The procedure upgrade effort is scheduled for completion by December, 1991. PSE&G will also provide additional training to the present SQR reviewers, by October, 1989, to ensure that they remain fully astute of the SSI requirement and the appropriate procedural requirements resulting from current revisions to the Administrative Procedures.
of nitrogen into the reactor coolant system, was not reviewed by SORC. RESPONSE The test methodolbgy  
PSE&G will revise the existing guidance on two year reviews to ensure that specific guidance is provided for instances where the revision process leads to the development of new procedures.
for the Accumulator  
This will be completed by December, 1989. PSE&G IS IN FULL COMPLIANCE.
discharge  
VIOLATION B 10CFRS0.72(b)
check valves was developed  
(2) "Four-hour reports," requires that the licensee shall notify the NRC within four hours of the occurrence of any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat. Contrary to the above, on May 20, 1989, when the residual heat removal capability was lost for about fifty minutes, the licensee did not notify the NRC within four hours. RESPONSE PSE&G DOES NOT CONTEST THE VIOLATION Corrective Actions Although the four hour report was not made in accordance with the Event Classification Guide (ECG) PSE&G recognized that the seriousness of the incident warranted NRC attention, and contacted the NRC on Saturday, May 20, 1989, to provide the NRC with the significant information associated with the event. When PSE&G management recognized that a four hour report should have been made. PSE&G promptly made the report on Monday, May 22, 1989. --
in 1982 to provide full stroke testing. This test method was developed  
I Prior to the loss of RHR event, an effort to review and upgrade the ECG was undertaken by the Emergency Preparedness Group. The ECG was reviewed against 10CFR50.72 and 50.73, NUREG-1022 and NUREG-0654 to insure consistency with the regulations.
to comply with an IST program submittal  
Cross references to the applicable reporting requirements were added to the ECG subsections.
for NRC approval.  
Additionally, the sections were revised to facilitate usage. The revised ECG has several advantages over the version in use at the time of the event. The revised sections are tied directly to plant conditions (i.e. , "Loss of Decay Heat Removal" is more explicit than coupling the "Safeguards" and "Technical Specifications" sections for a single event). All of the applicable emergency and non-emergency events are addressed in the "Loss of Decay Heat Removal" section. Cross references to the applicable regulatory requirements help assure that the ECG addresses the reporting criteria, and also facilitates update of the ECG in light of changes in regulations.
Inspection  
This revision will correct the ECG deficiency relative to the loss of RHR and assure that events are properly reported in accordance with regulations.
Report 50-272/82-23, issued on October 5, 1982, documents  
The revised ECG was issued on May 26, 1989. CORRECTIVE ACTIONS TO PREVENT RECURRENCE The new ECG was reviewed against the regulations by the Licensing Department to insure compliance with the regulations.
the inspectors  
During the next requal cycle (scheduled to begin in September, 1989) the licensed operators will be provided with additional ECG and 10CFR50 training to strengthen their understanding and usage of the ECG with regard to the appropriate regulatory requirements.
review of the status of the Salem IST program in regards to the submittal.  
PSE&G IS IN FULL COMPLIANCE}}
A major portion of the review was to finalize an NRC Staff evaluation  
of the submittal.  
The inspector  
reviewed the procedures  
and indicated  
that the minimum design flow rates were not identified  
in the test procedures  
and were needed to demonstrate  
the minimum safety analysis design flowrate criteria through the valves. Surveillance  
procedure  
SP(O) 4.0.5-V-REFUEL  
was developed  
for Units 1 and 2 to meet this requirement.  
The Safety Evaluation  
Report for the IST Program submittal  
was issued on April 12, 1983. In the evaluation  
section of the SER the NRC indicated  
that Salem should investigate  
a means to satisfy the NRC full-stroke  
exercise criteria (demonstrate  
safety analysis design flowrate through the check valves). SP(O) 4.0.5-V-REFUEL  
procedure  
provided the means to full flow test the check valves.for  
the IST Program. This procedure  
was reviewed by SORC in 1982 and again in 1984. When the SP(O) 4.0.5-V-REFUEL  
procedure  
was broken down into separate procedures  
as a procedural  
enhancement, during the two year review process, SP(O) 4.0.5-V-SJ-6  
was developed.  
This procedure  
specifies  
the same testing methodology  
as the previous procedure  
and was reviewed by a Station Qualified  
Reviewer.  
The SQR determined  
that the procedure  
did not contain a SSI. The SQR was performing  
a two year review; therefore, he was reviewing  
the changes and comments with respect to the technical  
review. However, since he was aware that* the procedure  
was performed  
satisfactorily  
using the steps specified  
by the procedure  
and that the procedure  
had been   
* * SORC approved, he did not perform a full technical  
basis review of the old procedural  
steps. It did, however, receive the required two year review specified  
by procedure.  
When it was decided that the procedure  
should be separated  
to reduce the confusion  
involved with multiple tests covered by one procedure, it was felt that the steps were the same and thus the review performed  
was adequate.  
The procedures  
do not provide specific guidance on the exact review steps to perform if the two year review results in new procedures  
being developed  
to seperate an old procedure.  
In reviewing  
the guidance of AP-32, Implementing  
Procedures  
Program, the guidance provided would indicate that an SSI was not involved as the examples provided discuss revising the procedure  
for specific purposes.  
In this case of the SP(O) 4.0.5-V-SJ6  
procedure  
the revision was made to make the procedure  
more usable not to change order of steps or step method. Therefore, by the SS! criteria an SS! was not involved.  
However, review of the incident did reveal that the original procedure (SP(0)4.0.5-REFUEL)  
should have required a 50.59 safety evaluation  
in that it did involve a change to the a test described  
in the FSAR. Corrective  
Actions Taken Use of the accumulator  
discharge  
procedure  
SP(0)4.0.5-V-SJ-6  
was immediately  
discontinued.  
The weaknesses  
with the SP(0)4.0.5-V-SJ-6  
and AOP-RHR-1  
procedures  
were reviewed with the Operations  
Procedure  
Writers. Corrective  
Actions to Prevent Recurrence  
PSE&G will evaluate the !ST Program to determine  
the appropriate  
method for testing the accumulator  
check valves. This will be determined  
by October 24, 1989. PSE&G will revise appropriate  
procedures  
for accumulator  
check valve test after method is determined, and ensure SORC review. To be completed  
by December 31, 1989. A training plan will be developed  
and procedures  
revised to incorporate  
the information  
and improvements  
provided by the Engineering  
and OSR evaluations  
of the event. This will be completed  
by September  
29, 1989. PSE&G is currently  
developing  
an extensive  
procedure  
upgrade program that will ensure that high risk procedures  
are identified  
and that adequate precaution  
and human factor considerations  
are included .   
,\ To assist the procedure  
upgrade effort, PSE&G will establish  
an independent  
review group to perform SQR review to ensure that all commitments  
and 10CFR50.59  
requirements  
are being met and maintained.  
The procedure  
upgrade effort is scheduled  
for completion  
by December, 1991. PSE&G will also provide additional  
training to the present SQR reviewers, by October, 1989, to ensure that they remain fully astute of the SSI requirement  
and the appropriate  
procedural  
requirements  
resulting  
from current revisions  
to the Administrative  
Procedures.  
PSE&G will revise the existing guidance on two year reviews to ensure that specific guidance is provided for instances  
where the revision process leads to the development  
of new procedures.  
This will be completed  
by December, 1989. PSE&G IS IN FULL COMPLIANCE.  
VIOLATION  
B 10CFRS0.72(b)  
(2) "Four-hour  
reports," requires that the licensee shall notify the NRC within four hours of the occurrence  
of any event or condition  
that alone could have prevented  
the fulfillment  
of the safety function of structures  
or systems that are needed to remove residual heat. Contrary to the above, on May 20, 1989, when the residual heat removal capability  
was lost for about fifty minutes, the licensee did not notify the NRC within four hours. RESPONSE PSE&G DOES NOT CONTEST THE VIOLATION  
Corrective  
Actions Although the four hour report was not made in accordance  
with the Event Classification  
Guide (ECG) PSE&G recognized  
that the seriousness  
of the incident warranted  
NRC attention, and contacted  
the NRC on Saturday, May 20, 1989, to provide the NRC with the significant  
information  
associated  
with the event. When PSE&G management  
recognized  
that a four hour report should have been made. PSE&G promptly made the report on Monday, May 22, 1989. --  
I Prior to the loss of RHR event, an effort to review and upgrade the ECG was undertaken  
by the Emergency  
Preparedness  
Group. The ECG was reviewed against 10CFR50.72  
and 50.73, NUREG-1022  
and NUREG-0654  
to insure consistency  
with the regulations.  
Cross references  
to the applicable  
reporting  
requirements  
were added to the ECG subsections.  
Additionally, the sections were revised to facilitate  
usage. The revised ECG has several advantages  
over the version in use at the time of the event. The revised sections are tied directly to plant conditions (i.e. , "Loss of Decay Heat Removal" is more explicit than coupling the "Safeguards" and "Technical  
Specifications" sections for a single event). All of the applicable  
emergency  
and non-emergency  
events are addressed  
in the "Loss of Decay Heat Removal" section. Cross references  
to the applicable  
regulatory  
requirements  
help assure that the ECG addresses  
the reporting  
criteria, and also facilitates  
update of the ECG in light of changes in regulations.  
This revision will correct the ECG deficiency  
relative to the loss of RHR and assure that events are properly reported in accordance  
with regulations.  
The revised ECG was issued on May 26, 1989. CORRECTIVE  
ACTIONS TO PREVENT RECURRENCE  
The new ECG was reviewed against the regulations  
by the Licensing  
Department  
to insure compliance  
with the regulations.  
During the next requal cycle (scheduled  
to begin in September, 1989) the licensed operators  
will be provided with additional  
ECG and 10CFR50 training to strengthen  
their understanding  
and usage of the ECG with regard to the appropriate  
regulatory  
requirements.  
PSE&G IS IN FULL COMPLIANCE
}}

Revision as of 19:56, 31 July 2019

Responds to NRC 890703 Ltr Re Violations Noted in Insp Rept 50-272/89-17.Corrective Actions:Inservice Testing Program Will Be Evaluated to Determine Appropriate Method for Testing Accumulator Check Valves & Training Plan Developed
ML18094A597
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/02/1989
From: Labruna S
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NLR-N89149, NUDOCS 8908080330
Download: ML18094A597 (7)


Text

' '

  • Public Service Electric and Gas Company Stanley LaBruna Public Service Electric and Gas Company P.O. Box 236. Hancocks Bridge, NJ 08038 609-339-4800 Vice President

-Nuclear Operations

  • AUG 0 2 1989 NLR-N89149 United States Nuclear Regulatory Commission Document Control Desk Washington DC 20555 Gentlemen:

RESPONSE TO NOTICE OF VIOLATION NRC INSPECTION NO. 50-272/89-17 SALEM GENERATING STATION UNIT NO. 1 DOCKET NOS. 50-272 Public Service Electric and Gas Company (PSE&G) has received the subject inspection report dated July 3, 1989, which included a Notice of Violation concerning failure to notify the NRC within four hours and failure to have SORC review a procedure that contained an SSI. Pursuant to the requirements of 10 CFR 2.201, our response to this Notice of Violation is provided in the attachment to this letter. Should you have any questions in regards to this transmittal, do not hesitate to call. Attachment Sincerely, s. LaBruna Vice President

-Nuclear Operations

.. * *

  • Document Control Desk NLR-N89149 C Mr. J. c. Stone Licensing Project Manager Ms. K. Halvey Gibson Senior Resident Inspector 2 Mr. w. T. Russell, Administrator Region I Mr. Kent Tosch, Chief New Jersey Department of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625 AUG 0 2 1989 J .. * *
  • ATTACHMENT 1

1 VIOLATION A Technical Specification 6.8.2 requires that surveillance and test activity procedures shall be independently reviewed to make a determination as to whether the procedure contains a significant safety issue (SSI). Additionally, Technical Specification 6.5.1.6 requires that the Station Operations Review Committee (SORC) shall review procedures that involve an SSI. Contrary to the above, on May 20, 1989, Surveillance Procedure No. SP(0)4.0.5-V-SJ-6, "Inservice Testing -Valves -Safety Injection," which involved an SSI, injection of nitrogen into the reactor coolant system, was not reviewed by SORC. RESPONSE The test methodolbgy for the Accumulator discharge check valves was developed in 1982 to provide full stroke testing. This test method was developed to comply with an IST program submittal for NRC approval.

Inspection Report 50-272/82-23, issued on October 5, 1982, documents the inspectors review of the status of the Salem IST program in regards to the submittal.

A major portion of the review was to finalize an NRC Staff evaluation of the submittal.

The inspector reviewed the procedures and indicated that the minimum design flow rates were not identified in the test procedures and were needed to demonstrate the minimum safety analysis design flowrate criteria through the valves. Surveillance procedure SP(O) 4.0.5-V-REFUEL was developed for Units 1 and 2 to meet this requirement.

The Safety Evaluation Report for the IST Program submittal was issued on April 12, 1983. In the evaluation section of the SER the NRC indicated that Salem should investigate a means to satisfy the NRC full-stroke exercise criteria (demonstrate safety analysis design flowrate through the check valves). SP(O) 4.0.5-V-REFUEL procedure provided the means to full flow test the check valves.for the IST Program. This procedure was reviewed by SORC in 1982 and again in 1984. When the SP(O) 4.0.5-V-REFUEL procedure was broken down into separate procedures as a procedural enhancement, during the two year review process, SP(O) 4.0.5-V-SJ-6 was developed.

This procedure specifies the same testing methodology as the previous procedure and was reviewed by a Station Qualified Reviewer.

The SQR determined that the procedure did not contain a SSI. The SQR was performing a two year review; therefore, he was reviewing the changes and comments with respect to the technical review. However, since he was aware that* the procedure was performed satisfactorily using the steps specified by the procedure and that the procedure had been

  • SORC approved, he did not perform a full technical basis review of the old procedural steps. It did, however, receive the required two year review specified by procedure.

When it was decided that the procedure should be separated to reduce the confusion involved with multiple tests covered by one procedure, it was felt that the steps were the same and thus the review performed was adequate.

The procedures do not provide specific guidance on the exact review steps to perform if the two year review results in new procedures being developed to seperate an old procedure.

In reviewing the guidance of AP-32, Implementing Procedures Program, the guidance provided would indicate that an SSI was not involved as the examples provided discuss revising the procedure for specific purposes.

In this case of the SP(O) 4.0.5-V-SJ6 procedure the revision was made to make the procedure more usable not to change order of steps or step method. Therefore, by the SS! criteria an SS! was not involved.

However, review of the incident did reveal that the original procedure (SP(0)4.0.5-REFUEL) should have required a 50.59 safety evaluation in that it did involve a change to the a test described in the FSAR. Corrective Actions Taken Use of the accumulator discharge procedure SP(0)4.0.5-V-SJ-6 was immediately discontinued.

The weaknesses with the SP(0)4.0.5-V-SJ-6 and AOP-RHR-1 procedures were reviewed with the Operations Procedure Writers. Corrective Actions to Prevent Recurrence PSE&G will evaluate the !ST Program to determine the appropriate method for testing the accumulator check valves. This will be determined by October 24, 1989. PSE&G will revise appropriate procedures for accumulator check valve test after method is determined, and ensure SORC review. To be completed by December 31, 1989. A training plan will be developed and procedures revised to incorporate the information and improvements provided by the Engineering and OSR evaluations of the event. This will be completed by September 29, 1989. PSE&G is currently developing an extensive procedure upgrade program that will ensure that high risk procedures are identified and that adequate precaution and human factor considerations are included .

,\ To assist the procedure upgrade effort, PSE&G will establish an independent review group to perform SQR review to ensure that all commitments and 10CFR50.59 requirements are being met and maintained.

The procedure upgrade effort is scheduled for completion by December, 1991. PSE&G will also provide additional training to the present SQR reviewers, by October, 1989, to ensure that they remain fully astute of the SSI requirement and the appropriate procedural requirements resulting from current revisions to the Administrative Procedures.

PSE&G will revise the existing guidance on two year reviews to ensure that specific guidance is provided for instances where the revision process leads to the development of new procedures.

This will be completed by December, 1989. PSE&G IS IN FULL COMPLIANCE.

VIOLATION B 10CFRS0.72(b)

(2) "Four-hour reports," requires that the licensee shall notify the NRC within four hours of the occurrence of any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat. Contrary to the above, on May 20, 1989, when the residual heat removal capability was lost for about fifty minutes, the licensee did not notify the NRC within four hours. RESPONSE PSE&G DOES NOT CONTEST THE VIOLATION Corrective Actions Although the four hour report was not made in accordance with the Event Classification Guide (ECG) PSE&G recognized that the seriousness of the incident warranted NRC attention, and contacted the NRC on Saturday, May 20, 1989, to provide the NRC with the significant information associated with the event. When PSE&G management recognized that a four hour report should have been made. PSE&G promptly made the report on Monday, May 22, 1989. --

I Prior to the loss of RHR event, an effort to review and upgrade the ECG was undertaken by the Emergency Preparedness Group. The ECG was reviewed against 10CFR50.72 and 50.73, NUREG-1022 and NUREG-0654 to insure consistency with the regulations.

Cross references to the applicable reporting requirements were added to the ECG subsections.

Additionally, the sections were revised to facilitate usage. The revised ECG has several advantages over the version in use at the time of the event. The revised sections are tied directly to plant conditions (i.e. , "Loss of Decay Heat Removal" is more explicit than coupling the "Safeguards" and "Technical Specifications" sections for a single event). All of the applicable emergency and non-emergency events are addressed in the "Loss of Decay Heat Removal" section. Cross references to the applicable regulatory requirements help assure that the ECG addresses the reporting criteria, and also facilitates update of the ECG in light of changes in regulations.

This revision will correct the ECG deficiency relative to the loss of RHR and assure that events are properly reported in accordance with regulations.

The revised ECG was issued on May 26, 1989. CORRECTIVE ACTIONS TO PREVENT RECURRENCE The new ECG was reviewed against the regulations by the Licensing Department to insure compliance with the regulations.

During the next requal cycle (scheduled to begin in September, 1989) the licensed operators will be provided with additional ECG and 10CFR50 training to strengthen their understanding and usage of the ECG with regard to the appropriate regulatory requirements.

PSE&G IS IN FULL COMPLIANCE