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| {{#Wiki_filter:Jeffrey B. Archie Vice President, Nuclear Operations 803.345.4214 A-SCANL A COMPAN December 11, 2009 A SCANA COMPANY Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555 | | {{#Wiki_filter:Jeffrey B. Archie Vice President,Nuclear Operations 803.345.4214 A-SCANLA COMPAN A SCANA COMPANY December 11, 2009 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555 |
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| ==Dear Sir / Madam:== | | ==Dear Sir / Madam:== |
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| ==Subject:== | | ==Subject:== |
| VIRGIL C. SUMMER NUCLEAR STATION (VCSNS) UNIT 1 DOCKET NO. 50/395 OPERATING LICENSE NO. NPF-12 SPECIAL REPORT (SPR) 2009-003 South Carolina Electric & Gas Company (SCE&G) is submitting this report pursuant to the requirements of Technical Specifications 6.9.2 and Fire Protection Procedure (FPP)-024, Enclosure 6.1.1. This report addresses the Electric Driven Fire Service Pump (XPP0134A) being out of service for greater than 7 days due to a loss of power.On November 22, 2009 while the plant was shut down for a refueling outage, a loss of Balance of Plant (BOP) power occurred. | | VIRGIL C. SUMMER NUCLEAR STATION (VCSNS) UNIT 1 DOCKET NO. 50/395 OPERATING LICENSE NO. NPF-12 SPECIAL REPORT (SPR) 2009-003 South Carolina Electric & Gas Company (SCE&G) is submitting this report pursuant to the requirements of Technical Specifications 6.9.2 and Fire Protection Procedure (FPP)-024, .1.1. This report addresses the Electric Driven Fire Service Pump (XPP0134A) being out of service for greater than 7 days due to a loss of power. |
| BOP power includes electrical bus XSW1C2 which supplies power to XPP0134A. | | On November 22, 2009 while the plant was shut down for a refueling outage, a loss of Balance of Plant (BOP) power occurred. BOP power includes electrical bus XSW1C2 which supplies power to XPP0134A. After power was restored to the bus, XPP0134A was returned to service on November 30, 2009 at 2141 hours. The pump remained out of service for a total of 8 days and 6 hours, and therefore exceeded the 7 day administrative limit established within the VCSNS Fire Protection Program. During the loss of power to XPP01 34A, the Fire Service System was maintained operable by the Diesel Driven Fire Service Pump (XPP0134B). |
| After power was restored to the bus, XPP0134A was returned to service on November 30, 2009 at 2141 hours. The pump remained out of service for a total of 8 days and 6 hours, and therefore exceeded the 7 day administrative limit established within the VCSNS Fire Protection Program. During the loss of power to XPP01 34A, the Fire Service System was maintained operable by the Diesel Driven Fire Service Pump (XPP0134B). | |
| The loss of BOP power and loss of power to XPP01 34A have been entered into the VCSNS corrective action program. Should you have any questions, please call Bruce Thompson at (803) 931-5042 at your convenience. | | The loss of BOP power and loss of power to XPP01 34A have been entered into the VCSNS corrective action program. Should you have any questions, please call Bruce Thompson at (803) 931-5042 at your convenience. |
| Very truly yours, GAR/JBA/jg c: K. B. Marsh S. A. Byrne N. S. Carns J. H. Hamilton R. J. White W. M. Cherry L. A. Reyes R. E. Martin K. M. Sutton NRC Resident Inspector INPO Records Center NSRC RTS (CR-09-05193) | | Very truly yours, GAR/JBA/jg c: K. B. Marsh S. A. Byrne K. M. Sutton N. S. Carns NRC Resident Inspector J. H. Hamilton INPO Records Center R. J. White NSRC W. M. Cherry RTS (CR-09-05193) |
| File (818.08)PRSF (RC-09-0155) | | L. A. Reyes File (818.08) |
| SCE&G I Virgil C. Summer Nuclear Station | | R. E. Martin PRSF (RC-09-0155) |
| * P. O. Box 88 | | SCE&G I Virgil C.Summer Nuclear Station |
| | * P.O.Box 88 |
| * Jenkinsville, South Carolina 29065 .T (803) 345.5209 | | * Jenkinsville, South Carolina 29065 .T (803) 345.5209 |
| * www.sceg.com JJ7~KI~}} | | * www.sceg.com JJ7~ |
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Category:Letter
MONTHYEARML24038A0322024-02-0707 February 2024 (Vcsns), Unit 1, 10 CFR 21 Report - Emergency Diesel Generator Flash Contactor Relay IR 05000395/20230042024-01-31031 January 2024 Integrated Inspection Report 05000395/2023004 ML24022A1582024-01-22022 January 2024 (Vcsns), Unit 1 - Reply to a Notice of Violation: EA-23-093 ML24022A1202024-01-22022 January 2024 Notification of Target Set Inspection and Request for Information (NRC Inspection Report 05000395/2024403) ML24018A0112024-01-18018 January 2024 CFR 21 Report Emergency Diesel Generator Fuel Oil Piping IR 05000395/20240112024-01-17017 January 2024 Notification of VC Summer Station Comprehensive Engineering Team Inspection - U.S. Nuclear Regulatory Commission Inspection Report 05000395/2024011 ML23361A1042023-12-21021 December 2023 Inservice Testing Program for Pumps and Valves Fifth Interval Update and Associated Relief and Alternative Requests IR 05000395/20230912023-12-21021 December 2023 Final Significance Determination of a White Finding and Notice of Violation and Assessment Followup Letternrc Inspection Report 05000395/2023091 ML23354A1802023-12-20020 December 2023 301 Examination Report with Cover Letter ML23347A0492023-12-12012 December 2023 Technical Specification Bases Changes Updated Through November 2023 ML23334A2462023-11-30030 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23334A2372023-11-30030 November 2023 (Vvsns), Unit 1 - Annual Commitment Change Summary Report ML23332A1942023-11-28028 November 2023 (Vcsns), Unit 1, Correction of Typographical Error in License Amendment Request - Inverter Allowed Outage Time (AOT) Extension ML23317A2242023-11-0909 November 2023 (Vcsns), Unit 1 - License Amendment Request - Inverter Allowed Outage Time (AOT) Extension ML23289A1172023-11-0303 November 2023 Tribal Request for Scoping Comments Concerning the Environmental Review of the V.C. Summer SLRA ML23289A1152023-11-0303 November 2023 Ltr to R. Nelson - Request for Scoping Comments Concerning the Environmental Review of the V.C. Summer SLRA ML23289A1162023-11-0303 November 2023 Ltr to W. Emerson - Request for Scoping Comments Concerning the Environmental Review of the V.C. Summer SLRA IR 05000395/20234032023-11-0101 November 2023 Material Control and Accounting Program Inspection Report 05000395/2023403 Cover IR 05000395/20230032023-11-0101 November 2023 Integrated Inspection Report 05000395/2023003 ML23284A1792023-10-16016 October 2023 Subsequent License Renewal Application Online Reference Portal ML23275A0142023-10-11011 October 2023 SLRA - Acceptance and Opportunity for Hearing - Letter ML23284A1662023-10-10010 October 2023 (Vcsns), Unit 1 - Request for Regulatory Conference; (EA-23-093) IR 05000395/20230902023-10-0404 October 2023 NRC Inspection Report 05000395/2023090 and Preliminary Yellow Finding and Apparent Violation IR 05000395/20230112023-09-27027 September 2023 Focused Engineering Inspection Report 05000395/2023011 ML23250A3112023-09-20020 September 2023 Request to Revise Reactor Vessel Material Surveillance Capsule Withdrawal Schedules ML23244A2352023-09-18018 September 2023 Request to Use a Subsequent Edition of the ASME Code, Section XI ML23230A0012023-09-15015 September 2023 Request to Use a Provision of a Previous Edition of the ASME Boiler and Pressure Vessel Code, Section XI, for Non-Destructive Examinations ML23235A0432023-09-0505 September 2023 Receipt and Availability of the Subsequent License Renewal Application IR 05000395/20234012023-08-30030 August 2023 Security Baseline Inspection Report 05000395/2023401 ML23242A1192023-08-29029 August 2023 (Vcsns), Unit 1 - Inservice Inspection (ISI) Owner'S Activity Report (OAR) for Refueling Outage 27 ML23243B0362023-08-25025 August 2023 Request for FEMA Consultation on the Dominion Energy Proposal to Consolidate the Emergency Operations Facility for the Virgil C. Summer Nuclear Station Unit 1 IR 05000395/20230052023-08-23023 August 2023 Updated Inspection Plan for Virgil C. Summer Nuclear Station (Report 05000395 2023005) ML23233A1752023-08-17017 August 2023 Application for Subsequent Renewed Operating License IR 05000395/20230022023-08-14014 August 2023 Integrated Inspection Report - Integrated Inspection Report 05000395/2023002 and Apparent Violation IR 05000395/20230102023-08-12012 August 2023 Biennial Problem Identification and Resolution Inspection Report 05000395/2023010 ML23207A1102023-07-26026 July 2023 NRC Regulatory Issues Summary 2023-01 Preparation and Scheduling of Operator Licensing Examinations IR 05000395/20234412023-07-17017 July 2023 95001 Supplemental Inspection Report 05000395/2023441 and Follow Up Assessment Letter ML23190A0012023-07-0909 July 2023 Special Report 2023-003 Inoperable Radiation Monitoring Instrumentation Channel ML23187A5092023-07-0606 July 2023 Request for Federal Emergency Management Agency Consultation on the Dominion Energy Proposal to Consolidate the Emergency Operations Facility for the Virgil C. Summer Nuclear Station Unit 1 ML23178A1682023-06-26026 June 2023 2022 Annual Report of Emergency Core Cooling System (ECCS) Model Changes Pursuant to the Requirements of 10 CFR 50.46 ML23173A1052023-06-22022 June 2023 Special Report 2023-002 Inoperable Loose-Part Monitoring System Channel ML23163A2352023-06-12012 June 2023 Request to Use a Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI, for the SPS Sixth Inservice Inspection (Isi) Intervals and VCSNS Fifth ISI Interval ML23159A2332023-06-0808 June 2023 License Amendment Request - Emergency Response Organization Augmentation Time Change, Emergency Operations Facility Relocation and Other Emergency Plan Changes ML23156A3092023-06-0505 June 2023 Requalification Program Inspection Virgil C. Summer Nuclear Station Unit 1 - 05000395/2023003 2024-02-07
[Table view] Category:Licensee 30-Day Written Event Report
MONTHYEARML19010A2872019-01-10010 January 2019 (Vcsns), Unit 1 - Special Report 2019-001 for Meteorological Monitoring Channels Inoperable ML17349A6572017-12-15015 December 2017 Special Report (Spr) 2017-011 RC-17-0112, Special Report (Spr) 2017-007 Regarding Waste Gas Holdup System Explosive Gas Monitoring System Being Inoperable for Greater than Thirty Days2017-09-0101 September 2017 Special Report (Spr) 2017-007 Regarding Waste Gas Holdup System Explosive Gas Monitoring System Being Inoperable for Greater than Thirty Days RC-17-0116, Special Report (Spr) 2017-009 Regarding Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability2017-08-24024 August 2017 Special Report (Spr) 2017-009 Regarding Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability RC-17-0085, Special Report (Spr) 2017-0052017-06-13013 June 2017 Special Report (Spr) 2017-005 RC-17-0072, Special Report (Spr) 2017-003 Regarding Electrical Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability2017-06-0101 June 2017 Special Report (Spr) 2017-003 Regarding Electrical Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability RC-17-0062, Special Report (Spr) 2017-001 Regarding a Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability2017-05-0505 May 2017 Special Report (Spr) 2017-001 Regarding a Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability ML16319A1032016-11-0808 November 2016 Submittal of Special Report 2016-004 ML14209A8472014-07-24024 July 2014 Special Written Report of Theft or Loss of Licensed Material on 05/30/2014 ML0934804922009-12-11011 December 2009 Special Report (Spr) 2009-003 Re Electric Driven Fire Service Pump Being Out of Service for Greater than 7 Days Due to Loss of Power ML0909302862009-04-0101 April 2009 Special Report (Spr) 2008-005-01 for Virgil C. Summer Inoperability of the Main Steam Line Radiation Monitor RM-G19C for Greater than 72 Hours ML0821004482008-07-24024 July 2008 LER, Virgil C. Summer, Special Report 2008-004 on Inoperability of the Plant Vent High Range Radiation Monitor RMA00131 for Greater than 72 Hours ML0614402922006-05-22022 May 2006 Special Report (Spr) 2006-003 Re Inoperability of the Main Plant Vent & Reactor Building Purge Supply & Exhaust System Radiation Monitors for Greater than 72 Hours RC-05-0116, Special Report (Spr) 2005-032005-07-29029 July 2005 Special Report (Spr) 2005-03 RC-05-0099, Special Report 2005-0012005-07-0707 July 2005 Special Report 2005-001 RC-04-0171, Special Report 2004-0022004-10-13013 October 2004 Special Report 2004-002 ML0218602052002-07-0202 July 2002 Special Report 2002-001. Digital Metal Impact Monitor System Has One Channel Which Has Been Inoperable in Excess of 30 Days 2019-01-10
[Table view] |
Text
Jeffrey B. Archie Vice President,Nuclear Operations 803.345.4214 A-SCANLA COMPAN A SCANA COMPANY December 11, 2009 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555
Dear Sir / Madam:
Subject:
VIRGIL C. SUMMER NUCLEAR STATION (VCSNS) UNIT 1 DOCKET NO. 50/395 OPERATING LICENSE NO. NPF-12 SPECIAL REPORT (SPR) 2009-003 South Carolina Electric & Gas Company (SCE&G) is submitting this report pursuant to the requirements of Technical Specifications 6.9.2 and Fire Protection Procedure (FPP)-024, .1.1. This report addresses the Electric Driven Fire Service Pump (XPP0134A) being out of service for greater than 7 days due to a loss of power.
On November 22, 2009 while the plant was shut down for a refueling outage, a loss of Balance of Plant (BOP) power occurred. BOP power includes electrical bus XSW1C2 which supplies power to XPP0134A. After power was restored to the bus, XPP0134A was returned to service on November 30, 2009 at 2141 hours0.0248 days <br />0.595 hours <br />0.00354 weeks <br />8.146505e-4 months <br />. The pump remained out of service for a total of 8 days and 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and therefore exceeded the 7 day administrative limit established within the VCSNS Fire Protection Program. During the loss of power to XPP01 34A, the Fire Service System was maintained operable by the Diesel Driven Fire Service Pump (XPP0134B).
The loss of BOP power and loss of power to XPP01 34A have been entered into the VCSNS corrective action program. Should you have any questions, please call Bruce Thompson at (803) 931-5042 at your convenience.
Very truly yours, GAR/JBA/jg c: K. B. Marsh S. A. Byrne K. M. Sutton N. S. Carns NRC Resident Inspector J. H. Hamilton INPO Records Center R. J. White NSRC W. M. Cherry RTS (CR-09-05193)
L. A. Reyes File (818.08)
R. E. Martin PRSF (RC-09-0155)
SCE&G I Virgil C.Summer Nuclear Station
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