|
---|
Category:Letter
MONTHYEARML24038A0322024-02-0707 February 2024 (Vcsns), Unit 1, 10 CFR 21 Report - Emergency Diesel Generator Flash Contactor Relay IR 05000395/20230042024-01-31031 January 2024 Integrated Inspection Report 05000395/2023004 ML24022A1582024-01-22022 January 2024 (Vcsns), Unit 1 - Reply to a Notice of Violation: EA-23-093 ML24022A1202024-01-22022 January 2024 Notification of Target Set Inspection and Request for Information (NRC Inspection Report 05000395/2024403) ML24018A0112024-01-18018 January 2024 CFR 21 Report Emergency Diesel Generator Fuel Oil Piping IR 05000395/20240112024-01-17017 January 2024 Notification of VC Summer Station Comprehensive Engineering Team Inspection - U.S. Nuclear Regulatory Commission Inspection Report 05000395/2024011 ML23361A1042023-12-21021 December 2023 Inservice Testing Program for Pumps and Valves Fifth Interval Update and Associated Relief and Alternative Requests IR 05000395/20230912023-12-21021 December 2023 Final Significance Determination of a White Finding and Notice of Violation and Assessment Followup Letternrc Inspection Report 05000395/2023091 ML23354A1802023-12-20020 December 2023 301 Examination Report with Cover Letter ML23347A0492023-12-12012 December 2023 Technical Specification Bases Changes Updated Through November 2023 ML23334A2462023-11-30030 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23334A2372023-11-30030 November 2023 (Vvsns), Unit 1 - Annual Commitment Change Summary Report ML23332A1942023-11-28028 November 2023 (Vcsns), Unit 1, Correction of Typographical Error in License Amendment Request - Inverter Allowed Outage Time (AOT) Extension ML23317A2242023-11-0909 November 2023 (Vcsns), Unit 1 - License Amendment Request - Inverter Allowed Outage Time (AOT) Extension ML23289A1172023-11-0303 November 2023 Tribal Request for Scoping Comments Concerning the Environmental Review of the V.C. Summer SLRA ML23289A1152023-11-0303 November 2023 Ltr to R. Nelson - Request for Scoping Comments Concerning the Environmental Review of the V.C. Summer SLRA ML23289A1162023-11-0303 November 2023 Ltr to W. Emerson - Request for Scoping Comments Concerning the Environmental Review of the V.C. Summer SLRA IR 05000395/20234032023-11-0101 November 2023 Material Control and Accounting Program Inspection Report 05000395/2023403 Cover IR 05000395/20230032023-11-0101 November 2023 Integrated Inspection Report 05000395/2023003 ML23284A1792023-10-16016 October 2023 Subsequent License Renewal Application Online Reference Portal ML23275A0142023-10-11011 October 2023 SLRA - Acceptance and Opportunity for Hearing - Letter ML23284A1662023-10-10010 October 2023 (Vcsns), Unit 1 - Request for Regulatory Conference; (EA-23-093) IR 05000395/20230902023-10-0404 October 2023 NRC Inspection Report 05000395/2023090 and Preliminary Yellow Finding and Apparent Violation IR 05000395/20230112023-09-27027 September 2023 Focused Engineering Inspection Report 05000395/2023011 ML23250A3112023-09-20020 September 2023 Request to Revise Reactor Vessel Material Surveillance Capsule Withdrawal Schedules ML23244A2352023-09-18018 September 2023 Request to Use a Subsequent Edition of the ASME Code, Section XI ML23230A0012023-09-15015 September 2023 Request to Use a Provision of a Previous Edition of the ASME Boiler and Pressure Vessel Code, Section XI, for Non-Destructive Examinations ML23235A0432023-09-0505 September 2023 Receipt and Availability of the Subsequent License Renewal Application IR 05000395/20234012023-08-30030 August 2023 Security Baseline Inspection Report 05000395/2023401 ML23242A1192023-08-29029 August 2023 (Vcsns), Unit 1 - Inservice Inspection (ISI) Owner'S Activity Report (OAR) for Refueling Outage 27 ML23243B0362023-08-25025 August 2023 Request for FEMA Consultation on the Dominion Energy Proposal to Consolidate the Emergency Operations Facility for the Virgil C. Summer Nuclear Station Unit 1 IR 05000395/20230052023-08-23023 August 2023 Updated Inspection Plan for Virgil C. Summer Nuclear Station (Report 05000395 2023005) ML23233A1752023-08-17017 August 2023 Application for Subsequent Renewed Operating License IR 05000395/20230022023-08-14014 August 2023 Integrated Inspection Report - Integrated Inspection Report 05000395/2023002 and Apparent Violation IR 05000395/20230102023-08-12012 August 2023 Biennial Problem Identification and Resolution Inspection Report 05000395/2023010 ML23207A1102023-07-26026 July 2023 NRC Regulatory Issues Summary 2023-01 Preparation and Scheduling of Operator Licensing Examinations IR 05000395/20234412023-07-17017 July 2023 95001 Supplemental Inspection Report 05000395/2023441 and Follow Up Assessment Letter ML23190A0012023-07-0909 July 2023 Special Report 2023-003 Inoperable Radiation Monitoring Instrumentation Channel ML23187A5092023-07-0606 July 2023 Request for Federal Emergency Management Agency Consultation on the Dominion Energy Proposal to Consolidate the Emergency Operations Facility for the Virgil C. Summer Nuclear Station Unit 1 ML23178A1682023-06-26026 June 2023 2022 Annual Report of Emergency Core Cooling System (ECCS) Model Changes Pursuant to the Requirements of 10 CFR 50.46 ML23173A1052023-06-22022 June 2023 Special Report 2023-002 Inoperable Loose-Part Monitoring System Channel ML23163A2352023-06-12012 June 2023 Request to Use a Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI, for the SPS Sixth Inservice Inspection (Isi) Intervals and VCSNS Fifth ISI Interval ML23159A2332023-06-0808 June 2023 License Amendment Request - Emergency Response Organization Augmentation Time Change, Emergency Operations Facility Relocation and Other Emergency Plan Changes ML23156A3092023-06-0505 June 2023 Requalification Program Inspection Virgil C. Summer Nuclear Station Unit 1 - 05000395/2023003 2024-02-07
[Table view] Category:Licensee 30-Day Written Event Report
MONTHYEARML19010A2872019-01-10010 January 2019 (Vcsns), Unit 1 - Special Report 2019-001 for Meteorological Monitoring Channels Inoperable ML17349A6572017-12-15015 December 2017 Special Report (Spr) 2017-011 RC-17-0112, Special Report (Spr) 2017-007 Regarding Waste Gas Holdup System Explosive Gas Monitoring System Being Inoperable for Greater than Thirty Days2017-09-0101 September 2017 Special Report (Spr) 2017-007 Regarding Waste Gas Holdup System Explosive Gas Monitoring System Being Inoperable for Greater than Thirty Days RC-17-0116, Special Report (Spr) 2017-009 Regarding Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability2017-08-24024 August 2017 Special Report (Spr) 2017-009 Regarding Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability RC-17-0085, Special Report (Spr) 2017-0052017-06-13013 June 2017 Special Report (Spr) 2017-005 RC-17-0072, Special Report (Spr) 2017-003 Regarding Electrical Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability2017-06-0101 June 2017 Special Report (Spr) 2017-003 Regarding Electrical Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability RC-17-0062, Special Report (Spr) 2017-001 Regarding a Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability2017-05-0505 May 2017 Special Report (Spr) 2017-001 Regarding a Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability ML16319A1032016-11-0808 November 2016 Submittal of Special Report 2016-004 ML14209A8472014-07-24024 July 2014 Special Written Report of Theft or Loss of Licensed Material on 05/30/2014 ML0934804922009-12-11011 December 2009 Special Report (Spr) 2009-003 Re Electric Driven Fire Service Pump Being Out of Service for Greater than 7 Days Due to Loss of Power ML0909302862009-04-0101 April 2009 Special Report (Spr) 2008-005-01 for Virgil C. Summer Inoperability of the Main Steam Line Radiation Monitor RM-G19C for Greater than 72 Hours ML0821004482008-07-24024 July 2008 LER, Virgil C. Summer, Special Report 2008-004 on Inoperability of the Plant Vent High Range Radiation Monitor RMA00131 for Greater than 72 Hours ML0614402922006-05-22022 May 2006 Special Report (Spr) 2006-003 Re Inoperability of the Main Plant Vent & Reactor Building Purge Supply & Exhaust System Radiation Monitors for Greater than 72 Hours RC-05-0116, Special Report (Spr) 2005-032005-07-29029 July 2005 Special Report (Spr) 2005-03 RC-05-0099, Special Report 2005-0012005-07-0707 July 2005 Special Report 2005-001 RC-04-0171, Special Report 2004-0022004-10-13013 October 2004 Special Report 2004-002 ML0218602052002-07-0202 July 2002 Special Report 2002-001. Digital Metal Impact Monitor System Has One Channel Which Has Been Inoperable in Excess of 30 Days 2019-01-10
[Table view] |
Text
Jeffrey B. Archie Vice President,Nuclear Operations 803.345.4214 A SCANA COMPANY July 24, 2008 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555
Dear Sir / Madam:
Subject:
VIRGIL C. SUMMER NUCLEAR STATION DOCKET NO. 50/395 OPERATING LICENSE NO. NPF-12 SPECIAL REPORT (SPR) 2008-004 South Carolina Electric & Gas Company (SCE&G) is submitting this report pursuant to the requirements of Technical Specification 3.3.3.1 b., Table 3.3-6, Action 30. This report addresses the inoperability of the Plant Vent High Range radiation monitor RMA001 3 for greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. During the inoperable period, V. C. Summer Nuclear Station (VCSNS) implemented a preplanned alternate method of monitoring in accordance with the requirements of Action 30 of Technical Specification 3.3.3.1 b.
RMA0013 was declared inoperable July 3, 2008, at 0430 hours0.00498 days <br />0.119 hours <br />7.109788e-4 weeks <br />1.63615e-4 months <br /> due to spurious alarms. Further investigation determined that a Universal Digital Ratemeter (UDR) had failed. The UDR was replaced, and the radiation monitor was returned to operable status on July 7, 2008, at 1025 hours0.0119 days <br />0.285 hours <br />0.00169 weeks <br />3.900125e-4 months <br />.
Due to an administrative error, this report exceeded the 14 day submittal requirements specified in Technical Specification 3.3.3.1.b, Table 3.3-6, Action 30. The failure to submit the report in a timely manner has been entered into the VCSNS corrective action program.
Should you have any questions, please call Mr. Bruce Thompson at (803) 931-5042 at your convenience.
yours, truly
/Very ey B. Archi JIG/JBA/cm c: K. B. Marsh NRC Resident Inspector S. A. Byrne K. M Sutton N. S. Cams INPO Records Center J. H. Hamilton NSRC R. J. White RTS (CR-08-02936; CR-08-03160)
L. A. Reyes File (818.08)
R. E. Martin PRSF (RC-08-0094)
SCE&G I Virgil C.Summer Nuclear Station