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Category:Licensee 30-Day Written Event Report
MONTHYEARML19010A2872019-01-10010 January 2019 (Vcsns), Unit 1 - Special Report 2019-001 for Meteorological Monitoring Channels Inoperable ML17349A6572017-12-15015 December 2017 Special Report (Spr) 2017-011 RC-17-0112, Special Report (Spr) 2017-007 Regarding Waste Gas Holdup System Explosive Gas Monitoring System Being Inoperable for Greater than Thirty Days2017-09-0101 September 2017 Special Report (Spr) 2017-007 Regarding Waste Gas Holdup System Explosive Gas Monitoring System Being Inoperable for Greater than Thirty Days RC-17-0116, Special Report (Spr) 2017-009 Regarding Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability2017-08-24024 August 2017 Special Report (Spr) 2017-009 Regarding Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability RC-17-0085, Special Report (Spr) 2017-0052017-06-13013 June 2017 Special Report (Spr) 2017-005 RC-17-0072, Special Report (Spr) 2017-003 Regarding Electrical Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability2017-06-0101 June 2017 Special Report (Spr) 2017-003 Regarding Electrical Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability RC-17-0062, Special Report (Spr) 2017-001 Regarding a Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability2017-05-0505 May 2017 Special Report (Spr) 2017-001 Regarding a Fire Barrier Assembly Not Being Restored to Operability within Seven Days After Declaration of Inoperability ML16319A1032016-11-0808 November 2016 Submittal of Special Report 2016-004 ML14209A8472014-07-24024 July 2014 Special Written Report of Theft or Loss of Licensed Material on 05/30/2014 ML0934804922009-12-11011 December 2009 Special Report (Spr) 2009-003 Re Electric Driven Fire Service Pump Being Out of Service for Greater than 7 Days Due to Loss of Power ML0909302862009-04-0101 April 2009 Special Report (Spr) 2008-005-01 for Virgil C. Summer Inoperability of the Main Steam Line Radiation Monitor RM-G19C for Greater than 72 Hours ML0821004482008-07-24024 July 2008 LER, Virgil C. Summer, Special Report 2008-004 on Inoperability of the Plant Vent High Range Radiation Monitor RMA00131 for Greater than 72 Hours ML0614402922006-05-22022 May 2006 Special Report (Spr) 2006-003 Re Inoperability of the Main Plant Vent & Reactor Building Purge Supply & Exhaust System Radiation Monitors for Greater than 72 Hours RC-05-0116, Special Report (Spr) 2005-032005-07-29029 July 2005 Special Report (Spr) 2005-03 RC-05-0099, Special Report 2005-0012005-07-0707 July 2005 Special Report 2005-001 RC-04-0171, Special Report 2004-0022004-10-13013 October 2004 Special Report 2004-002 ML0218602052002-07-0202 July 2002 Special Report 2002-001. Digital Metal Impact Monitor System Has One Channel Which Has Been Inoperable in Excess of 30 Days 2019-01-10
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Jeffrey B. Archie Vice President, Nuclear Operations
__ 803.345.4214 A SCANA COMPANY May 22, 2006 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555
Dear Sir or Madam:
Subject:
VIRGIL C. SUMMER NUCLEAR STATION DOCKET NO. 50/395 OPERATING LICENSE NO. NPF-12 SPECIAL REPORT (SPR) 2006-003 South Carolina Electric & Gas Company (SCE&G) is submitting this report pursuant to the requirements of Technical Specification 3.3.3.1.b. This report addresses the inoperability of the Main Plant Vent and Reactor Building Purge Supply and Exhaust System radiation monitors (RMA-1 3 and RMA-1 4) for greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. V. C. Summer Nuclear Station (VCSNS) implemented a preplanned alternate monitoring in accordance with the requirement of Action 30 of the Technical Specification following the declaration of inoperability for these monitors on May 5, 2006.
The Victoreen Model 945A series radiation monitors were recently installed in February 2006.
As ambient temperatures increased, VCSNS personnel have observed these monitors exhibiting erratic behavior. The erratic behavior is believed to be caused by a possible temperature compensation problem; therefore, VCSNS is returning the monitors to the vendor for a failure analysis and repair. The alternate monitoring for these release paths will continue until operability for the permanent monitors is re-established. A schedule for corrective action implementation could not be finalized at this time. SCE&G will work with the vendor to determine the cause and the appropriate schedule for replacement and return to operability.
Should you have any questions, please call Mr. Robert Sweet at (803) 345-4080 at your convenience.
Ve yours, y B. Archi CJM/JBA/cm c: K. B. Marsh K. M. Sutton S. A. Byrne NRC Resident Inspector N. S. Cams INPO Records Center J. H. Hamilton NSRC R. J. White CER (C-06-1363 & C-06-1530)
W. D. Travers File (818.08)
R. E. Martin DMS (RC-06-0098)
SCE&G I Virgil C.Summer Nuclear Station
- P.0. Box 88. Jenkinsville, South Carolina 29065 .T (803) 345.5209 *www.scana.com