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{{#Wiki_filter:REGULATORY
{{#Wiki_filter:REGULATORY     ]FORMATION DISTRIBUTION SY         EM <R IDS)
]FORMATION DISTRIBUTION SY EM<R IDS).;ACCESSION NBR: 8704210080 DQC.DATE: 87/03/30 NOTARIZED:
.;ACCESSION NBR:       8704210080         DQC. DATE: 87/03/30       NOTARIZED: NQ             DOCKET j FACIL: STN-50-528 Pal o Verde Nucl eav Station> Uni t 1> Av i zona Pub AUTH. NAME               AUTHOR AFFILIATION li  05000528 HAYNES, J. G.             Av'i zona Nucleav'owev'roJect (formerly Ari zona               Public Serv RECIP. NAME               RECIPIENT AFF IL IATlQN MAR T I N> J. B.         Region 5> Office of Div ector
NQ DOCKET j FACIL: STN-50-528 Pal o Verde Nucl eav Station>Uni t 1>Av i zona Pub li 05000528 AUTH.NAME AUTHOR AFFILIATION HAYNES, J.G.Av'i zona Nucleav'owev'roJect (formerly Ari zona Public Serv RECIP.NAME RECIPIENT AFF IL IATlQN MAR T I N>J.B.Region 5>Office of Div ector  


==SUBJECT:==
==SUBJECT:==
Special Rept 1-SR-87-010:
Special Rept 1-SR-87-010: on 870224> condenser evacuation sos high v'ange v adiation monitors declav'ed inoperable when continuous low flow alarms veceived. Caused bg water in sample tube. Boav ds v eplaced 5 monitors v etested.
on 870224>condenser evacuation sos high v'ange v adiation monitors declav'ed inoperable when continuous low flow alarms veceived.Caused bg water in sample tube.Boav ds v eplaced 5 monitors v etested.DISTRIBUTION CODE: IE01D COPIES RECEIVED: LTR+ENCL+SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES: Standardized plant.M.Davis>NRR: 1Cg.05000528 RECIPIENT ID CODE/NAME PD5 LA LICITRA, E , COPIES LTTR, ENCL 1 0)1 , RECIPIENT ID.,CODE/NAME PD5 PD DAVIS>M C QP IES LTTR ENCL 1 1 1 1 INTERNAL: ACRS DEDRO NRR RQE>M.L NRR/DOEA DIR NRR/DREP/RPB
DISTRIBUTION CODE: IE01D TITLE: General COPIES RECEIVED: LTR (50 Dkt)-Insp Rept/Notice of
>A ILRB REG FI 5 FILE Oi EXTERNAL: LPDR NSIC 1 2 2 1 1 1 LEOD ENF L IEBERMAN NRR/ADT NRR/QREP/EP B h!RR/DR IS DIR QGC/HDSi RES SPEIS>T N!RC PDR 1 1 1 1 1 1 1 1 NOTES: 1 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 24 I J/a ,i t/t Arizona Nuclear Power Project P.o.BOX 52034~PHOENIX.ARIZONA 85072-2034 192-00183-JGH/TRB/MJC March 30, 1987 Mr.John B.Martin, Regional Administrator Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission Region V 1450 Maria Lane, Suite 210 Walnut Creek, CA 94596-5368
                                                                    + ENCL +
Violation SIZE:
 
===Response===
NOTES:   Standardized       plant. M. Davis> NRR: 1Cg.                                     05000528 RECIPIENT           , COPIES          ,  RECIPIENT          C QP IES ID CODE/NAME           LTTR, ENCL         ID.,CODE/NAME       LTTR ENCL PD5 LA                      1    0      PD5 PD                     1      1 LICITRA, E                  )    1      DAVIS> M                   1     1 INTERNAL: ACRS                                   2      LEOD                      1      1 DEDRO                       1          ENF L IEBERMAN            1 NRR RQE> M. L                   1      NRR/ADT                    1 NRR/DOEA DIR                     1      NRR   /QREP /EP B          1     1 NRR/DREP/RPB                2          h!RR/DR IS DIR             1
                        >A  ILRB                1      QGC/HDSi                         1 REG  FI                                RES SPEIS> T 5      FILE    Oi EXTERNAL: LPDR                                          N!RC PDR NSIC NOTES:                                       1   1 TOTAL NUMBER OF COPIES REQUIRED: LTTR                   25     ENCL     24
 
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Arizona Nuclear Power Project P.o. BOX 52034 ~ PHOENIX. ARIZONA85072-2034 192-00183-JGH/TRB/MJC March 30, 1987 Mr. John B. Martin, Regional Administrator Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Region V 1450 Maria Lane, Suite 210 Walnut Creek, CA 94596-5368


==Subject:==
==Subject:==
Palo Verde Nuclear Generating Station Unit 1 Docket No.STN 50-528 (License NPF-41)Special Report 1-SR-87-010 File: 87-020-404
Palo Verde Nuclear Generating Station Unit 1 Docket No. STN 50-528 (License NPF-41)
Special Report 1-SR-87-010 File: 87-020-404
 
==Dear Mr. Martin:==
 
Attached please find a Special Report 1-SR-87-010 prepared and submitted pursuant to Technical Specifications 3.3.3.9 and 6.9.2. This report d3.scusses a radiation monitor that was inoperable for greater than 72 hours.
If you  have any questions, please      contact  Tom    Bradish, Compliance Supervisor at (602) 932-5300, Ext. 6936.
Very    truly yours, J. G. Haynes Vice President Nuclear Production JGH/TRB/MJC/cld Attachment cc:  0. M. DeMichele      (all    w/a)
E. E. Van Brunt,  Jr.
R. P. Zimmerman R. C. Sorenson E. A. Licitra A. C. Gehr INPO Records Center 870w210080 870330 PDR    ADOCK 050005>8 8                  PDR


==Dear Mr.Martin:==
t PALO VERDE NUCLEAR GENERATING STATION UNIT         1 Condenser Evacuation System Radiation Monitor Inoperable for Greater Than           72 Hours Docket No. STN 50-528 License No.     NPF-41 Special Report     No. 1-SR-87-010 This Special Report is being submitted pursuant to Technical Specification (T.S.)
Attached please find a Special Report 1-SR-87-010 prepared and submitted pursuant to Technical Specifications 3.3.3.9 and 6.9.2.This report d3.scusses a radiation monitor that was inoperable for greater than 72 hours.If you have any questions, please contact Tom Bradish, Compliance Supervisor at (602)932-5300, Ext.6936.Very truly yours, J.G.Haynes Vice President Nuclear Production JGH/TRB/MJC/cld Attachment cc: 0.M.DeMichele E.E.Van Brunt, Jr.R.P.Zimmerman R.C.Sorenson E.A.Licitra A.C.Gehr INPO Records Center (all w/a)870w210080 870330 PDR ADOCK 050005>8 8 PDR t
3.3.3.9 ACTION 42b and T.S. 6.9.2 to report an event in which a Condenser Evacuation System high range radiation monitor (RU-142) was inoperable for greater than 72 hours following entry into Mode 4 (HOT SHUTDOWN). The 72 hour limit for operability was exceeded at approximately 1604 MST on March 4, 1987. Pursuant to T.S. 3.3.3.9 ACTION 42a the Preplanned Alternate Sampling Program was initiated to monitor the Condenser Evacuation System.
PALO VERDE NUCLEAR GENERATING STATION UNIT 1 Condenser Evacuation System Radiation Monitor Inoperable for Greater Than 72 Hours Docket No.STN 50-528 License No.NPF-41 Special Report No.1-SR-87-010 This Special Report is being submitted pursuant to Technical Specification (T.S.)3.3.3.9 ACTION 42b and T.S.6.9.2 to report an event in which a Condenser Evacuation System high range radiation monitor (RU-142)was inoperable for greater than 72 hours following entry into Mode 4 (HOT SHUTDOWN).
Monitors RU-141   and RU-142 monitor the Condenser Evacuation System for gaseous activity resulting from primary   to secondary   system leakage.     These monitors work as a pair with   RU-141 being the low range monitor   and RU-142   being   the high range monitor. Normal configuration   consists of RU-141 operating   and RU-142   in standby. When RU-141 reaches it's maximum range, RU-142 starts and RU-141 goes to standby. RU-141 and RU-142 are required to be operable in Modes 1, 2, 3 and 4. The, provisions of T.S. 3.0.3 and T.S. 3.0.4 are not applicable.
The 72 hour limit for operability was exceeded at approximately 1604 MST on March 4, 1987.Pursuant to T.S.3.3.3.9 ACTION 42a the Preplanned Alternate Sampling Program was initiated to monitor the Condenser Evacuation System.Monitors RU-141 and RU-142 monitor the Condenser Evacuation System for gaseous activity resulting from primary to secondary system leakage.These monitors work as a pair with RU-141 being the low range monitor and RU-142 being the high range monitor.Normal configuration consists of RU-141 operating and RU-142 in standby.When RU-141 reaches it's maximum range, RU-142 starts and RU-141 goes to standby.RU-141 and RU-142 are required to be operable in Modes 1, 2, 3 and 4.The, provisions of T.S.3.0.3 and T.S.3.0.4 are not applicable.
At approximately 2300 on February 24, 1987, Palo Verde Unit 1 was in Mode 5 (COLD SHUTDOWN) for a maintenance outage wh .. continuous low flow alarms were received on RU-141'. Since RU-141 and RU-142 work as a pair, both monitors were declared inoperable to allow corrective maint'enance to be performed on RU-141.
At approximately 2300 on February 24, 1987, Palo Verde Unit 1 was in Mode 5 (COLD SHUTDOWN)for a maintenance outage wh..continuous low flow alarms were received on RU-141'.Since RU-141 and RU-142 work as a pair, both monitors were declared inoperable to allow corrective maint'enance to be performed on RU-141.Troubleshooting transmitter and water was found transmitter and were replaced.conducted under an authorized work document revealed that the flow the flow indicator boards had malfunctioned.
Troubleshooting conducted under an authorized work document revealed that the flow transmitter and the flow indicator boards had malfunctioned. During troubleshooting, water was found in the RU-141 s,"-.;;,>l t'!'o and is believed to be the cause of the flow transmitter and flow indicator board malfunction. As corrective action the boards were replaced.
During troubleshooting, in the RU-141 s,"-.;;,>l t'!'o and is believed to be the cause of the flow flow indicator board malfunction.
Prior to this event the condenser evacuation system         was   in operation. As a conservative measure   the condenser was being evacuated through the normal exhaust to pass potentially contaminated air through the charcoal filters and RU-141. This resulted in water accumulating in the RU-141 sample line. This is not the usual exhaust path in Mode 5 since RU-141 is not required.
As corrective action the boards Prior to this event the condenser evacuation system was in operation.
At approximately 1604 MST on March 1, 1987 T.S. ACTION 42 was entered when Palo Verde Unit 1 entered Mode 4 (HOZ SHUTDOWN) with RU-142 inoperable. RU-141 and RU-142 were declared operable at approximately 1430 MST on March 5, 1987 following the successful performance of 36ST-9SQ04 (Radiation Monitoring Quarterly Functional Test). The Unit was in ACTION 42 for 4 days and 26 minutes.}}
As a conservative measure the condenser was being evacuated through the normal exhaust to pass potentially contaminated air through the charcoal filters and RU-141.This resulted in water accumulating in the RU-141 sample line.This is not the usual exhaust path in Mode 5 since RU-141 is not required.At approximately 1604 MST on March 1, 1987 T.S.ACTION 42 was entered when Palo Verde Unit 1 entered Mode 4 (HOZ SHUTDOWN)with RU-142 inoperable.
RU-141 and RU-142 were declared operable at approximately 1430 MST on March 5, 1987 following the successful performance of 36ST-9SQ04 (Radiation Monitoring Quarterly Functional Test).The Unit was in ACTION 42 for 4 days and 26 minutes.}}

Latest revision as of 11:30, 29 October 2019

Special Rept 1-SR-87-010:on 870224,condenser Evacuation Sys high-range Radiation Monitors Declared Inoperable When Continuous Low Flow Alarms Received.Caused by Water in Sample Tube.Boards Replaced & Monitors Retested
ML17300A754
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 03/30/1987
From: Haynes J
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To: Martin J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
1-SR-87-010, 1-SR-87-10, 192-00183-JGH-T, 192-183-JGH-T, NUDOCS 8704210080
Download: ML17300A754 (5)


Text

REGULATORY ]FORMATION DISTRIBUTION SY EM <R IDS)

.;ACCESSION NBR: 8704210080 DQC. DATE: 87/03/30 NOTARIZED: NQ DOCKET j FACIL: STN-50-528 Pal o Verde Nucl eav Station> Uni t 1> Av i zona Pub AUTH. NAME AUTHOR AFFILIATION li 05000528 HAYNES, J. G. Av'i zona Nucleav'owev'roJect (formerly Ari zona Public Serv RECIP. NAME RECIPIENT AFF IL IATlQN MAR T I N> J. B. Region 5> Office of Div ector

SUBJECT:

Special Rept 1-SR-87-010: on 870224> condenser evacuation sos high v'ange v adiation monitors declav'ed inoperable when continuous low flow alarms veceived. Caused bg water in sample tube. Boav ds v eplaced 5 monitors v etested.

DISTRIBUTION CODE: IE01D TITLE: General COPIES RECEIVED: LTR (50 Dkt)-Insp Rept/Notice of

+ ENCL +

Violation SIZE:

Response

NOTES: Standardized plant. M. Davis> NRR: 1Cg. 05000528 RECIPIENT , COPIES , RECIPIENT C QP IES ID CODE/NAME LTTR, ENCL ID.,CODE/NAME LTTR ENCL PD5 LA 1 0 PD5 PD 1 1 LICITRA, E ) 1 DAVIS> M 1 1 INTERNAL: ACRS 2 LEOD 1 1 DEDRO 1 ENF L IEBERMAN 1 NRR RQE> M. L 1 NRR/ADT 1 NRR/DOEA DIR 1 NRR /QREP /EP B 1 1 NRR/DREP/RPB 2 h!RR/DR IS DIR 1

>A ILRB 1 QGC/HDSi 1 REG FI RES SPEIS> T 5 FILE Oi EXTERNAL: LPDR N!RC PDR NSIC NOTES: 1 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 24

I J

/a

,i t

/t

Arizona Nuclear Power Project P.o. BOX 52034 ~ PHOENIX. ARIZONA85072-2034 192-00183-JGH/TRB/MJC March 30, 1987 Mr. John B. Martin, Regional Administrator Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Region V 1450 Maria Lane, Suite 210 Walnut Creek, CA 94596-5368

Subject:

Palo Verde Nuclear Generating Station Unit 1 Docket No. STN 50-528 (License NPF-41)

Special Report 1-SR-87-010 File: 87-020-404

Dear Mr. Martin:

Attached please find a Special Report 1-SR-87-010 prepared and submitted pursuant to Technical Specifications 3.3.3.9 and 6.9.2. This report d3.scusses a radiation monitor that was inoperable for greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

If you have any questions, please contact Tom Bradish, Compliance Supervisor at (602) 932-5300, Ext. 6936.

Very truly yours, J. G. Haynes Vice President Nuclear Production JGH/TRB/MJC/cld Attachment cc: 0. M. DeMichele (all w/a)

E. E. Van Brunt, Jr.

R. P. Zimmerman R. C. Sorenson E. A. Licitra A. C. Gehr INPO Records Center 870w210080 870330 PDR ADOCK 050005>8 8 PDR

t PALO VERDE NUCLEAR GENERATING STATION UNIT 1 Condenser Evacuation System Radiation Monitor Inoperable for Greater Than 72 Hours Docket No. STN 50-528 License No. NPF-41 Special Report No. 1-SR-87-010 This Special Report is being submitted pursuant to Technical Specification (T.S.)

3.3.3.9 ACTION 42b and T.S. 6.9.2 to report an event in which a Condenser Evacuation System high range radiation monitor (RU-142) was inoperable for greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> following entry into Mode 4 (HOT SHUTDOWN). The 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> limit for operability was exceeded at approximately 1604 MST on March 4, 1987. Pursuant to T.S. 3.3.3.9 ACTION 42a the Preplanned Alternate Sampling Program was initiated to monitor the Condenser Evacuation System.

Monitors RU-141 and RU-142 monitor the Condenser Evacuation System for gaseous activity resulting from primary to secondary system leakage. These monitors work as a pair with RU-141 being the low range monitor and RU-142 being the high range monitor. Normal configuration consists of RU-141 operating and RU-142 in standby. When RU-141 reaches it's maximum range, RU-142 starts and RU-141 goes to standby. RU-141 and RU-142 are required to be operable in Modes 1, 2, 3 and 4. The, provisions of T.S. 3.0.3 and T.S. 3.0.4 are not applicable.

At approximately 2300 on February 24, 1987, Palo Verde Unit 1 was in Mode 5 (COLD SHUTDOWN) for a maintenance outage wh .. continuous low flow alarms were received on RU-141'. Since RU-141 and RU-142 work as a pair, both monitors were declared inoperable to allow corrective maint'enance to be performed on RU-141.

Troubleshooting conducted under an authorized work document revealed that the flow transmitter and the flow indicator boards had malfunctioned. During troubleshooting, water was found in the RU-141 s,"-.;;,>l t'!'o and is believed to be the cause of the flow transmitter and flow indicator board malfunction. As corrective action the boards were replaced.

Prior to this event the condenser evacuation system was in operation. As a conservative measure the condenser was being evacuated through the normal exhaust to pass potentially contaminated air through the charcoal filters and RU-141. This resulted in water accumulating in the RU-141 sample line. This is not the usual exhaust path in Mode 5 since RU-141 is not required.

At approximately 1604 MST on March 1, 1987 T.S. ACTION 42 was entered when Palo Verde Unit 1 entered Mode 4 (HOZ SHUTDOWN) with RU-142 inoperable. RU-141 and RU-142 were declared operable at approximately 1430 MST on March 5, 1987 following the successful performance of 36ST-9SQ04 (Radiation Monitoring Quarterly Functional Test). The Unit was in ACTION 42 for 4 days and 26 minutes.