IR 05000317/2005007: Difference between revisions

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{{IR-Nav| site = 05000317 | year = 2005 | report number = 007 | url = https://www.nrc.gov/reactors/operating/oversight/reports/calv_2005007.pdf }}
{{Adams
| number = ML053570380
| issue date = 12/22/2005
| title = IR 05000317-05-007, IR 05000318-05-007; 10/31/05 - 11/18/05; Calvert Cliffs Nuclear Plant, Units 1 and 2; Biennial Baseline Inspection of the Identification and Resolution of Problems
| author name = Trapp J
| author affiliation = NRC/RGN-I/DRP/PB1
| addressee name = Vanderheyden G
| addressee affiliation = Constellation Generation Group
| docket = 05000317, 05000318
| license number = DPR-053, DPR-069
| contact person = Barber G  S, RGN-I/DRP/610-337-5232
| document report number = IR-05-007
| document type = Inspection Report, Letter
| page count = 22
}}
 
{{IR-Nav| site = 05000317 | year = 2005 | report number = 007 }}
 
=Text=
{{#Wiki_filter:ber 22, 2005
 
==SUBJECT:==
CALVERT CLIFFS NUCLEAR GENERATING STATION - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT NO.
 
05000317/2005007, and 05000318/2005007
 
==Dear Mr. Vanderheyden:==
On November 18, 2005, the NRC completed a team inspection at the Calvert Cliffs Unit 1 and Unit 2 reactor facilities. The enclosed report documents the inspection findings, which were discussed on November 18, 2005, with you and other members of your staff.
 
This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, compliance with the Commissions rules and regulations, and with the conditions of your license. Within these areas, the inspection involved examination of selected procedures and representative records, observation of activities, and interviews with personnel.
 
On the basis of the sample selected for review, the team concluded that in general, problems were properly identified, evaluated, and corrected. Relatively few deficiencies were identified by external organizations that had not been previously identified by your organization. Audits and assessments appeared thorough.
 
This report documents one NRC-identified finding of very low safety significance (Green). This finding was determined to be a violation of NRC requirements. However, because of its very low safety significance and because it was entered into your corrective action program, the NRC is treating this finding as a non-cited violation, in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you deny this non-cited violation, you should provide a response with the basis for your denial within 30 days of the date of this inspection report, to the U. S.
 
Nuclear Regulatory Commission, ATTN. Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U. S. Nuclear Regulator Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Calvert Cliffs Facility.
 
Mr. George Vanderheyden  2 In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Sincerely,
/RA/
James Trapp, Chief Projects Branch 1 Division of Reactor Projects Docket Nos. 50-317, 50-318 License Nos. DPR-53, DPR-69
 
===Enclosure:===
Inspection Report No. 05000317/2005007, 05000318/2005007 w/Attachment: Supplemental Information
 
REGION I==
Docket Nos: 50-317, 50-318 License Nos: DPR-53, DPR-69 Report Nos: 05000317/2005007, 05000318/2005007 Licensee: Calvert Cliffs Nuclear Power Plant, Inc.
 
Facility: Calvert Cliffs Nuclear Power Plant Location: 1650 Calvert Cliffs Parkway Lusby, MD 20657-4702 Dates: October 31 - November 4, 2005 and November 14 - 18, 2005 Inspectors: G. Scott Barber, Senior Project Engineer, (Team Leader)
Donald Jackson, Senior Project Engineer John Richmond, Reactor Inspector Ryan Treadway, Acting Resident Inspector Dana Caron, Security Inspector Observer: Nicole Sieller, Nuclear Safety Professional Development Program (NSPDP) Engineer Approved by: James Trapp, Chief Projects Branch 1 Division of Reactor Projects i  Enclosure
 
SUMMARY OF FINDINGS IR 05000317/2005-007, IR 05000318/2005-007; 10/31/05 - 11/18/05; Calvert Cliffs Nuclear Plant, Units 1 and 2; biennial baseline inspection of the identification and resolution of problems. One violation was identified in the area of maintenance procedure adequacy.
 
This inspection was conducted by four regional inspectors and a resident inspector. One finding of very low safety significance (Green) was identified during this inspection and was classified as a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
 
Identification and Resolution of Problems The team determined that Constellations Calvert Cliffs (CC) Units 1 and 2 Nuclear Power Plants were effective at identifying problems and entering them into the corrective action program (CAP). Relatively few deficiencies were identified by external organizations (including NRC) that had not been previously identified by the licensee. Audits and self-assessments were generally thorough. Once entered into the CAP, issues were screened and prioritized in a timely manner using established criteria. Items entered into the CAP were also properly evaluated commensurate with their safety significance. The causal evaluations for equipment and performance issues were complete, and proposed corrective actions that addressed the identified causes. Corrective actions were generally effective and typically implemented in a timely manner. On the basis of interviews conducted during the inspection, workers at the station felt free to raise safety issues and were willing to enter them into the corrective action program. However, an ineffective maintenance procedure adversely impacted the availability of an auxiliary feedwater pump.
 
A. NRC Identified and Self-Revealing Findings Cornerstone: Mitigating Systems Green. The NRC identified a Green non-cited violation (NCV) of Technical Specification (TS) 5.4.1 due to an inadequate procedure for installation and adjustment of packing for the 22 turbine-driven auxiliary feedwater (TDAFW) pump, which led to premature pump shutdown during a quarterly surveillance test. During the test, operators secured the pump when they noticed a burning smell and observed smoke coming from the pumps inboard packing gland. Investigation found the inboard packing gland had lost adequate leak off flow along its inner diameter. The licensee entered the deficiency with the pump overhaul procedure into their corrective action (CA) program for resolution.
 
ii  Enclosure
 
This finding was greater than minor because it adversely affected the availability of a safety-related TDAFW pump which affected the equipment performance attribute of the Mitigating Systems Cornerstone because the pump was unavailable until the degraded packing had been replaced and the pump was satisfactorily retested. The finding was determined to be of very low safety significance (Green) in accordance with IMC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, because an engineering analysis determined that the pump would have remained operable, and was capable of performing its intended safety function.
 
(Section 4OA2.2)
B. Licensee-Identified Violations None iii  Enclosure
 
Report Details 4.OTHER ACTIVITIES (OA)
4OA2 Problem Identification and Resolution (Biennial - 71152B)
1. Effectiveness of Problem Identification a. Inspection Scope The inspection team reviewed the procedures, listed in the Attachment to this report, describing the corrective action program (CAP) at Constellations Calvert Cliffs Units 1 and 2 Nuclear Power Plants. Constellation identifies problems by initiating Condition Reports (CRs) for conditions adverse to quality, human performance problems, equipment nonconformances, industrial or radiological safety concerns, and other significant issues. The CRs are subsequently screened for operability, categorized by priority and significance (1 through 4), and assigned for evaluation and resolution.
 
The team considered risk insights from the NRCs and Constellations risk analyses to focus the sample selection and plant tours on risk-significant systems and components.
 
The team reviewed CRs selected across the seven cornerstones of safety in the NRCs Reactor Oversight Process (ROP) to determine if problems were being properly identified, characterized, and entered into the CAP for evaluation and resolution. The team selected items from the maintenance, operations, engineering, emergency planning, security, radiological protection, and oversight programs to ensure that the licensee was appropriately considering problems identified in each functional area. The team used this information to select a risk-informed sample of CRs that had been issued since the last NRC Problem Identification and Resolution (PI&R) inspection, which was completed in November 2003.
 
In addition to CRs, the team conducted plant tours and selected items from other processes at Calvert Cliffs to verify that problems identified in these areas were entered into the corrective action program when appropriate. Specifically, the team reviewed a sample of work requests, engineering documents, operator log entries, control room deficiency logs, operator work-arounds, operability determinations, system health reports, and temporary modifications. The documents were reviewed to ensure that underlying problems associated with each issue were appropriately considered for resolution via the corrective action process. In addition, the team interviewed plant staff and management to determine their understanding of and involvement with CAP. The CRs and other documents reviewed, and a list of key personnel contacted, are listed in the Attachment to this report.
 
The team reviewed a sample of the licensees Quality and Performance Assessment (Q&PA) audits and surveillances, including the most recent audit of the CAP, quarterly assessment reports, and departmental self-assessments. This review was performed to Enclosure
 
determine if problems identified through these assessments were entered into CAP, and whether the identified issues were dispositioned appropriately commensurate with the safety significance of the issue. The effectiveness of the audits and self-assessments was evaluated by comparing audit and self-assessment results against self-revealing and NRC-identified findings, and current observations during the inspection.
 
b. Findings and Assessments No findings of significance were identified.
 
The team concluded that Constellation was generally effective at problem identification at Calvert Cliffs. The CRs that are written are classified by their significance as category (I, II, III and IV) CRs, with Category I CRs usually requiring a root cause analysis (RCA)
and Category II CRs usually requiring an apparent cause evaluation (ACE). Level III and IV CRs do not typically require detailed reviews. The team noted station staff demonstrated appropriate knowledge of the corrective action program, and entered identified problems into the program at an appropriate threshold. There were approximately 3780 CRs assigned in 2004 and approximately 2877 assigned in 2005 as of the beginning of this inspection. The team did not identify any significant conditions adverse to quality in the maintenance, engineering, or operations tracking systems which did not have a CR associated with them.
 
Relatively few deficiencies were identified by external organizations, including the NRC, that had not been previously identified by the licensee. Audits and self-assessments were generally thorough. Each department was responsible for reviewing identified issues to look for trends. This program has generally been effective in identifying trends relating to conditions adverse to quality.
 
The use of the CAP by the security organization was also inspected and the results of this inspection are contained in NRC Inspection Report 05000317/2005008 and 05000318/2005008.
 
2. Prioritization and Evaluation of Issues a. Inspection Scope The team reviewed the CRs listed in the attachment to this report to assess whether the licensee adequately prioritized and evaluated problems. These reviews evaluated the causal assessment of each issue (i.e., root cause analysis or apparent cause evaluation); and for significant conditions adverse to quality, the extent of condition, and determination of corrective actions to preclude recurrence. Throughout the inspection, the team attended periodic meetings to observe the CR review process and to understand the basis for assigned significance and root cause levels.
 
The team also considered risk insights from the Calvert Cliffs probabilistic risk assessment to help focus the inspection sample. The team selected the auxiliary Enclosure
 
feedwater (AFW) system for an expanded review of five years. This system was selected because it is a significant contributor to plant risk.
 
The team selected a sample of CRs associated with previous NRC non-cited violations (NCVs) and findings to determine whether the licensee evaluated and resolved problems associated with compliance to applicable regulatory requirements and standards. The team reviewed the licensees approach to operating experience (OE),
which included an assessment of multiple examples of how effectively OE is used.
 
Operability and reportability determinations associated with CRs were also reviewed.
 
b. Assessments The team determined that Constellation adequately prioritized and evaluated the issues and concerns entered into the CAP. The team concluded that prioritized CRs were based on the safety significance of the issue. Operability determinations and reportability assessments were made promptly when issues were entered into the CAP.
 
The team noted that licensee management was thoroughly prepared during CR screening meetings as evidenced by their probing questions of presenters. Evaluations were generally completed in a timely manner, particularly after the CAP process was revised to establish a standard 30 day deadline for all CR evaluations. Clear guidance has been developed for performing cause evaluations, and multi-level review of completed evaluations has resulted in generally high quality evaluations with proposed corrective actions that addressed the identified causes.
 
The team developed specific insights regarding the five year review of the AFW system and of Constellations OE program. These assessments are described below. The team also identified that the evaluation of a maintenance activity did not fully address all potential causal factors because a key underlying procedural inadequacy remained unaddressed. Thus, the team identified one finding of low safety significance (Green)
that was a violation of NRC requirements which is described in section c. below.
 
Auxiliary Feedwater System Five Year Review The team selected the auxiliary feedwater (AFW) system for the five year inspection and review, which is the most risk significant system at Calvert Cliffs. A complete system walkdown was conducted and no significant conditions adverse to quality were identified. The team interviewed operators and the system engineer and determined that they had a basic understanding of the system and previous issues documented in CRs and IRs.
 
The team reviewed the last five years of logs, data and trends for the AFW system including condition reports, apparent cause evaluations, root cause evaluations, AFW system procedures, operator logs, and tagouts to assess AFW system performance from a corrective action standpoint. The team generated a table for AFW system components conditions that were adverse to quality and categorized the information by significance to assess performance. The team determined that there were several failed surveillances that involved the TDAFW control valves and questioned the licensee Enclosure
 
to determine if a previously undetected adverse trend existed. The inspectors noted several failed surveillances for the TDAFW control valves related to American Society of Mechanical Engineers code compliance issues, repetitive use of inadequate maintenance procedures which resulted in failed surveillances, and several condition reports related to improper use of vendor recommendations. Detailed followup by the team later determined that the licensees actions to evaluate these issues were adequate and that corrective action taken was commensurate with the issues safety significance.
 
Operating Experience The process that Constellation used to collect, screen, review OE appeared to be very effective. Operating experience is gathered from multiple sources, and is screened daily for general applicability and an update is e-mailed to an extensive list of licensee personnel for their information. In cases where the operating experience is screened to be applicable to the licensee, an action item is generated to perform a barrier analysis to determine if further corrective action is needed. If action is required, a condition report is generated to address the underlying OE. The program used a simple database that plant staff can easily access. Licensee staff charged with administering the operating experience program were proactive at screening OE which was clearly valued by line management as evidenced by the timely responses OE screening requests and actions generated by these reviews. The team reviewed several operating experience items that were in various stages of resolution. The team determined that the licensee had an effective program and management displayed strong support of the operating experience program.
 
c. Findings Introduction. The NRC identified a Green non-cited violation (NCV) of Technical Specification (TS) 5.4.1 due to inadequate procedures for installation and adjustment of packing for the 22 turbine driven auxiliary feedwater (TDAFW) pump, which led to premature pump shutdown during a quarterly surveillance test. The team determined that appropriate procedural guidance would have precluded the pump unavailability that occurred until the repairs were accomplished and the pump was satisfactorily retested.
 
Description. On December 8, 2004, during a quarterly surveillance test, the 22 TDAFW pump was shutdown due to a lack of adequate packing gland leakage, and the observation and smell of smoke coming from the pump inboard packing gland. After the pump shutdown, the licensee replaced the packing, performed a successful surveillance and declared the pump operable on December 9, 2004.
 
The apparent cause evaluation (ACE) (IR200400582) for this condition stated that the pressure applied to the bottom three rings of packing reduced the clearance needed for sufficient packing leak off. The licensee postulated that this raised the temperature of the water and caused flashing which virtually eliminated packing leak off flow. Thus, the packing began to deform and fuse together until all leak off was subsequently stopped.
 
Enclosure
 
The licensees operability assessment determined that the TDAFW pump was operable in the as-found condition, with the packing degraded.
 
Based on interviews, the team determined that operators would have taken action to secure the TDAFW pump and place the standby pump in-service if the packing had degraded during an actual plant event (e.g., a loss of off-site power) based on procedural guidance in OI-32A, AFW system. The team also determined that appropriate procedural guidance for repacking the pump would have precluded the pump unavailability that occurred until the repairs and a satisfactory retest were accomplished on December 9, 2004.
 
The licensee identified the apparent cause for the TDAFW pump unavailability as improper pump packing installation and adjustment. The licensee proposed changes to the AFW operating instruction and the surveillance test procedure but did not propose change the pump overhaul procedure. The team discussed the reasons for this approach with the licensee and pointed out that the pump overhaul procedure only included one step for repacking the pump and it did not reference the vendor technical manual (VTM). The Byron-Jackson VTM-B580-1032 listed several key steps that are necessary to ensure adequate packing installation and adjustment. Plant staff acknowledged that a change to the overhaul procedure was needed. Consequently, a Request for a Procedure Addendum (RPA) to make the appropriate changes to the pump overhaul procedure was implemented to ensure that appropriate vendor technical manual guidance for repacking of the pump was included.
 
Analysis. The packing failure was a performance deficiency because the existing maintenance procedure was not adequate to ensure that TDAFW pump repack was successfully performed. This finding was more then minor because it affected the procedure quality attribute of the Mitigating Systems Cornerstone and affected the cornerstone objective of ensuring the availability of systems that respond to initiating events to prevent undesirable consequences. The team conducted a significance determination process (SDP) Phase 1 screening in accordance with IMC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations. The finding was determined to be Green because the inadequate procedure and subsequent packing degradation did not result in a loss of function per Generic Letter 91-18, did not represent loss of a safety system function for longer than the TS limiting condition for operation (LCO) allowed outage time, and did not involve an external event.
 
Enforcement. Technical Specification 5.4.1 requires the licensee to establish, implement, and maintain procedures for the auxiliary feedwater system as referenced in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Contrary to these requirements, the licensee did not implement adequate procedures for the TDAFW pump packing installation and adjustment. Because this deficiency was of very low safety significance and has been entered into the corrective action program as IRE-001-860, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000318/2005007-01 AND 05000318/2005007-01, Inadequate Procedure for Installation and Adjustment of TDAFW Pump Packing.
 
Enclosure
 
3. Effectiveness of Corrective Actions a. Inspection Scope The team reviewed the corrective actions associated with selected CRs to determine whether they addressed the identified causes of the problems. The licensees timeliness in implementing corrective actions and their effectiveness in precluding recurrence for significant conditions adverse to quality was also reviewed. Furthermore, the team assessed the backlog of outstanding corrective actions to determine if they, individually or collectively, represented an increased risk to the plant. The team also reviewed NCVs and findings issued since the last inspection of the licensees CAP to determine if issues placed in the program had been properly evaluated and corrected.
 
b. Findings and Assessments Overall, the team concluded that Constellations corrective actions for identified deficiencies were typically timely and adequately implemented. Administrative controls have been put in place to ensure that corrective actions are completed as scheduled and reviews are performed to ensure the actions were implemented as intended.
 
Constellation also conducted in-depth effectiveness reviews for significant issues to determine if the corrective actions were effective in resolving the issue. In some cases, the licensee appropriately self-identified ineffective or improper closeout of corrective actions and reentered the issue into the CAP for further action. However, the team noted a long-standing issue in which corrective actions were not totally effective in addressing conditions adverse to quality.
 
Component Mispositioning The team reviewed the effectiveness of corrective actions taken to resolve a long-standing issue associated with component mispositioning events. In December 2003, a Category 1 Root Cause Analysis (RCA) was generated to resolve a continuing series of component mispositioning problems. Corrective actions for this issue included raising personnel accountability, providing additional personnel training, pre-job briefing improvements, general employee training improvements, and work load controls. These corrective actions had little effect in lowering the number or significance of component mispositionings. As a result, in May 2004, a Category 2 Apparent Cause Analysis (ACE) was conducted to further address this problem. The actions generated in response to this ACE were numerous and significant and included the initiation of a comprehensive human performance improvement program (HPIP). The HPIP program action plan has become a living document where changes to the original action plan have been made based on need and the scope of improvements was widened beyond those in response to the original December 2003 RCA on this issue. This program has been generally effective at lowering the significance of component mispositionings, however, the number of component mispositionings have not significantly decreased.
 
Enclosure
 
The licensee has generated an effective performance indicator to track progress in the mispositioning area. The performance indicator accounts for both the number and significance of component mispositionings. In May and June 2005, the performance indicator indicated that expectations were not being met in the area of component mispositionings as a result of 8 component mispositionings in early 2005, including one mis-positioning that had a negative consequence as determined by the licensees program. As a result of the performance indicator degradation, the licensee initiated another Category 2 Apparent/ Common Cause Analysis to correct the negative trend.
 
This analysis determined that the cause of the mis-positionings was due to a lack or misuse of error prevention tools that had been established by their HPIP. The team observed a number of planned activities that had the potential to result in component mis-positionings. During these observations, the team noted that station personnel were very consistent in their use of the error prevention tools that had been established by their HPIP and that the number and nature of the tools being used was commensurate with the potential significance of any mis-positioning that could occur.
 
Although the corrective actions for a previous significant condition adverse to quality have not been totally effective at curtailing the frequency of component mispositionings, the significance of component mispositionings has lowered to a level where the mitigating systems cornerstone attribute has not been negatively impacted. Thus, the team determined that this was a minor issue because Constellation had improved the frequency of use of error prevention tools to limit the actual significance of component mispositionings.
 
4. Assessment of Safety Conscious Work Environment a. Inspection Scope The team members interviewed plant staff, observed various activities throughout the plant, and attended a cross section of meetings to determine if conditions existed that would result in personnel being hesitant to raise safety concerns to their management and/or the NRC. The team also reviewed a sample of investigations performed to address employee and contractor concerns to assess the effectiveness of the employee concerns program (ECP).
 
b. Findings and Assessments No findings of significance were identified.
 
Employee Concerns Program The team determined that the investigations performed for employee concerns appeared prompt and thorough. The program administrator willingly accepted not only safety concerns, but work place concerns. The threshold for entering concerns in the program appeared appropriately low. Although the reviews did appear thorough, there was a great deal of variability in the level of documentation for some investigations. In some instances, the status of open investigations was not available in the written record although it was available on the computer. In other instance, the basis for the closeout Enclosure
 
of certain workplace concerns was not succinctly provided. The specific details of these and other similar issues were discussed with the program administrator and the quality assurance manager.
 
4OA6 Meetings, Including the Exit Meeting The team presented the inspection results to Mr. George Vanderheyden and other members of licensee management on November 18, 2005. Licensee management acknowledged the results presented. No proprietary information was identified during the inspection.
 
4OA7 Licensee-Identified Violations None ATTACHMENT: Supplemental Information In addition to the documentation that the inspectors reviewed (listed in the attachment), copies of information requests given to the licensee are in ADAMS, under accession number ML053460412.
 
Enclosure
 
A-1 SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT Licensee Personnel J. Pollack , Plant General Manager D. Bauder, Operations Manager J. Sickle, Manager, Nuclear Training M. Gahan III, Principal Engineer, Equipment Reliability Unit W. Rummel, Senior Operational Safety Analyst A. Simpson, Senior Engineer, Calvert Cliffs Regulatory Matters P. Suter, Operations Maintenance Coordinator E. Dean, Assistant Operations Manager M. Seckens, Supervisor of Nuclear Safety Services K. Crissman, Supervisor E&C, and Human Performance Improvement Lead T. Huber, Shift Manager J. Grooms, Shift Manager J. Gioffre, Control Room Supervisor G. Getz, Control Room Supervisor D. Woods, Nuclear Plant Operator L. Vandersnick, Nuclear Plant Operator R. Ciabattoni, Nuclear Plant Operator B. Shobert, Nuclear Plant Operator W. Tippett, Operating Experience Lead J. Wynn, Senior Engineer, Primary Systems Engineering M. Lewis, Senior Engineer, Primary Systems Engineering M. Dorn, Associate Engineer, Systems Engineering LIST OF DOCUMENTS REVIEWED Opened and Closed 05000317, 05000318/2005007-01 NCV Failure to identify and correct unavailability problems for the turbine drive AFW pump.
 
(Section 4OA2.c.2).
 
Procedures NO-1-106  Functional Evaluation/Operability Determination, Rev. 10 NS-1-100  Use of Operating Experience, Rev. 7 NS-1-101  Employee Concerns Program, Rev. 0 QL-2-100  Corrective Action Program, Rev 0 EN-1-100  Engineering Services Process Overview MN-1-101  Control of Maintenance Activities
 
A-2 MN-1-123  Integrated Work Planning CNG-CA-1.01-1001 Management Review Committee, Rev. 0 CNG-CA-1.01-1002 Corrective Action Review Board, Rev. 0 CNG-CA-1.01-1004 Root Cause Analysis, Rev. 0 CNG-CA-1.01-1005 Apparent Cause Evaluation, Rev. 0 CNG-CA-1.01-1006 Common Cause Analysis, Rev. 0 CNG-HU-1.01-1001, Rev. 1 Human Performance Tools and Verification Practices CNG-HU-1.01-1002, Rev. 2 Pre-Job Briefings and Post-Job Critiques CNG-HU-1.01-1003, Rev. 0 Human Performance Tools For Non-Field Technical Activities TR-1-101, Rev 18 Conduct of Training NO-1-106  Functional Evaluation/Operability Determination, Rev. 10 NS-1-100  Use of Operating Experience, Rev. 5 QL-2-104  Self-Assessment, Rev. 3 QL-2-105  Conduct of the Corrective Action Review Board, Rev. 4 QL-2-106  Site Key Performance Indicators, Rev. 0 OI-29  Saltwater System, Rev. 57 OI-32A  Auxiliary Feedwater System, Rev.16 STP-O5A-1  Auxiliary Feedwater System Quarterly Surveillance Test, Rev. 19 STP-O5A-2  Auxiliary Feedwater System Quarterly Surveillance Test, Rev. 18 Pump-12  Turbine Driven Auxiliary Feedwater Pump Overhaul, Rev. 7 Audits and Self-Assessments RPP-04-01-C  Radiation Protection and Radioactive Materials Management SPT-04-01-C  Special Processes / Section XI / Testing ISF-04-01-C  Independent Spent Fuel Storage Installation (ISFSI)
MAP-05-01-C  Maintenance Program SA200300050-  Operations Department Self Assessment SA200400042-  Operations Department Self Assessment SA200400168-  Calvert Cliffs Nuclear Safety Self Assessment\
Audit OPS-04-01-C Nuclear Plant Operations- QA Audit Operating Experience Documents Reviewed OE 18634  Small Fire Under Reactor Feed Pump Turbine OE 18895  Mihama- Death of a Worker Due To Condensate Rupture OE 19803  High Initial License Class Failure Rate OE 19810  Error In Plant Monitoring System Software OE 20688  Tin Whiskers Found On SSPS Circuit Cards Miscellaneous Items Reviewed Operations Work-Around List- Dated October 6, 2005 Control Room Deficiencies List- Dated October 6, 2005 Active Operability Determinations List- Dated September 29, 2005 Training Lesson Plan- Corrective Action Program Basic Overview Operations Component Mis-positioning Action Plan Attachment
 
A-3 Non-Cited Violations (NCV) and Findings (FIN)
NRC NCV 2003-006-01 IR4-027-075 [IR200300457]
NRC NCV 2004-002-02 IR4-008-006 [IR200400065]
NRC NCV 2004-002-03 IR4-008-997 [IR200400073]
NRC NCV 2004-004-01 IR4-023-638 [IR200400310]
NRC NCV 2004-005-02 IR4-030-055 [IR200400254]
NRC NCV 2004-008-04 IR4-030-176 [IR200400276] special inspection Condition Reports IR4-019-491  3R200402451 3R200500940 IR4-019-404  3R200402486 3R200500956 IR4-001-097  3R200500094 3R200501421 IRE-002-678  3R200500529 3R200501440 IRE-003-544  3R200500794 3R200501871 IRE-003-998  IR3-077-073 3R200501951 IRE-004-359  IR3-062-103 IR200300307 IRE-007-196  IRE-001-860 IR200300402 IR200300402  IR4-028-800 IR200400047 IR200400056  IR4-025-059 IR200400198 IR200400066  IR4-028-786 IR200400254 IR200400106  IR4-007-136 IR200400198 IR200400546  IR4-007-137 IR200400053 IR200400564  IR4-002-245 IR200400254 IR200500004  IR4-026-577 IR200400047 IR200500071  IR4-007-138 IR200400053 IR200500151  IR4-034-668 IR200400254 IR200300410  IR4-028-774 IR200300458 IR200400036  IR4-023-561 IR3-072-603 IR200400051  IR4-035-828 IRE-008-095 IR200400089  IR4-028-183 IRE-008-859 IR200400126  IR3-031-076 IRE-008-318 IR200400162  IR3-042-570 IRE-008-142 IR200400186  IR3-054-115 IRE-008-058 IR200400211  IR3-062-103 IRE-006-910 IR200400248  IR3-063-687 IR4-003-606 IR200400251  IR3-075-298 IR4-031-243 IR200400299  IR3-076-835 IRE-006-286 IR200400342  IR3-076-860 IR4-031-267 IR200400402  IR3-077-073 IRE-003-501 IR200400454  IR3-077-124 IR200300409 IR200400458  IR3-084-380 IR200300458 IR200400589  IR3-084-400 IR200400033 IR200500125  IR4-010-076 IR200400111 IR200500185  IR4-010-875 IR200400198 Attachment
 
A-4 IR200500188  IR4-041-139 IR200400254 IR200500204  IR3-043-669 IRE-004-220 3R200400010  IR3-044-531 IRE-019-658 3R200400310  IR3-048-589 IRE-014-006 3R200400406  IR3-048-642 3R200400733  IR3-053-642 3R200400771  IR3-076-976 3R200400868  IR3-081-274 3R200401135  IR3-084-379 3R200401253  IR4-015-857 3R200401292  IR3-032-391 3R200401453  IR3-059-054 3R200401647  IR3-082-917 3R200401713  IR4-002-760 3R200401771  IR4-015-052 3R200401839  IR4-018-247 3R200402077  IR4-001-896 3R200402119  IR4-011-627 3R200402199  IR3-041-489 3R200402351  IR3-059-099 3R200402449 3R200402448 3R200402450 Action Item Tracking - Responses AIT 4B200200042 AIT 4B200200073 AIT 4B200300070 AIT 4B200300125 AIT 4B200300139 AIT 4B200300179 AIT 4B200300184 AIT 4B200300381 AIT IR200400582 AIT IR200500209 Maintenance Orders 0200102212  1200102971 1200204878 0200202140  1200201224 2000101865 1200100846  1200203328 2199501219 Attachment
 
A-5 2199601549 2200404545 2199700837 2200200685 2200003755 2200101441 2200100609 2200302891 2200100610 2200400612 2200101305 2200400728 2200102726 2200400310 2200102951 1200401033 2200103805 1200400448 2200103815 2200304932 2200203698 2200102181 2200203963 1200401980 2200302231 1200303236 2910542001 1200402911 2910542101 2200400444 2200401217 2204016770 2200403496 1200501254 2200304260 2200401216 2200401173 2200303845 1200401591 2200302811 Drawings 62708SH0002 Circulating Water Cooling System, Rev. 95 62708SH0003 Circulating Water Cooling System, Rev. 7 62706SH0002 Service Water Cooling System Auxiliary Building/Containment, Rev. 64 60730SH0001 Chemical and Volume Control System 60730SH0002 Chemical and Volume Control System 60730SH0003 Chemical and Volume Control System 62731SH0003 Safety Injection and Containment Spray Systems, Rev. 39 63024 Single Line Diagram 125 DC Vital System Bus 21 61025 Single Line Diagram 125 DC Vital System Bus 12 and 22 61024 Single Line Diagram 125 DC Vital System Bus 11 60583SH0002 Auxiliary Feedwater System (Steam), Rev. 60 60583SH0002 Auxiliary Feedwater System (Condensate), Rev.0 60727SH0002 Diesel Generator Cooling Water, Starting Air, fuel, & Lube Oil Diesel No. 1B, Rev. 62 60727SH0003 Diesel Generator Cooling Water, Starting Air, fuel, & Lube Oil Diesel No. 2B, Rev. 50 60727SH0001 Diesel Generator Cooling Water, Starting Air, fuel, & Lube Oil Attachment
 
A-6 Diesel No. 2A, Rev. 59 60738SH0001  Area and Process Radiation Monitoring System, Rev. 66 60738SH0002  Area and Process Radiation Monitoring System, Rev. 21 Operating Experience Review Information Notice 94-03 Deficiencies identified during SW operational inspections Information Notice 03-02 Recent Experience with Reactor Coolant System Leakage and Boric Acid Corrosion Information Notice 02-36 Incomplete or Inaccurate Information Provided to the License and/or By Any Contractor or Subcontractor Employee Information Notice 03-08 NRC Potential Flooding Through Unsealed Concrete Floor Cracks Information Notice 02-27 Recent Fires at Commercial Nuclear Power Plants in the United States Information Notice 02-18 Effect of Adding Gas Into Water Storage Tanks on the Net Positive Suction Head for Pumps Information Notice 03-15 Importance Of Followup Activities In Resolving Maintenance Issues Miscellaneous Letter: Response to Inspection Report Nos. 50-317/89-200; 50-318/89-200 (Special Team Inspection), June 21, 1989 Letter: Implementation of Computerized Trending of Surveillance Data, dated April 4, 1990 Letter: Response and Supplemental Responses to NRC Bulletin 88-04, Potential Safety-Related Pump Loss, dated July 5, 1988, December 21, 1988, and August 22, 1989 Letter: Nuclear Logistics Inc to Mr. G. Dare CCNPS , 10/31/03, documenting safety function of 125 VDC post seal components Letter: Calvert Cliff Response to 10 CFR 21 Notification (ABB Breakers), dated May 13, 2002 Memorandum:February 10, 2000 Maintenance Rule Expert Panel Meeting Minutes, 2/17/00 Memorandum:Designation of Surveillance Test Coordinator and Functional Surveillance Test Coordinators per EN-4-104, Surveillance Testing, 4/10/02 CARB Meeting Minutes of 10/23/03 and 10/28/03 Maintenance Indicators for October 2003 Maintenance Rule Scoping Document - System 015 - Rev. 21 Corrective Action Program Performance Indicator Index July and August, 2003 System Health Report- Salt Water System Health Report- Component Cooling Water System Health Report- Service Water System Health Report - 125 Vdc System Health Report - 120 Vac System Health Report - Reactor Coolant System Calvert Cliffs Industrial Safety Manual, Rev. 4, Component Manipulation Form CM-03-186, Unit 1 Component Manipulation Form CM-03-153, Unit 2 Operability Determination OD No. 03-004, Intake Structure Fire Detection Equipment Reliability Improvement Project (ERIP) Plan Attachment
 
A-7 ERIP Plant Health Committee Charter, September 17, 2002 ERIP Steering Committee Charter, March 15, 2003 Plant Health Committee - Outstanding Equipment Reliability Issues, 11/7/03 Plant Health Committee Meeting Minutes: 6/5/03, 7/22/03, 7/24/03 8/7/03, 8/28/03, 9/5/03 ES200200752, Request for Alternate Mounting of Trico Oiler (9/10/02), Rev. 0 Final Response to NRC Generic Letter 89-13, Service Water system problems affecting safety-related equipment, dated June 30, 1994 UFSAR Section 9.5, Cooling Water Systems CARB Meeting Minutes of 10/31/05 and 11/02/05 Maintenance Rule Scoping Document - System 036A - Rev. 24 Maintenance Rule Scoping Document - System 064B - Rev. 24 Plant Health Committee Issues List Plant Health Committee Issues List Coming Due Plant Health Committee Meeting- 11/01/2005 System Health Report-Process Rad Monitor RCS Leak Detection Inside Containment System Health Report- Process Rad Monitor Gaseous Effluent Radiation Monitor System Health Report- Process Rad Fuel Handling Accident Monitors System Health Report- Auxiliary Feedwater System Unit 1 System Health Report- Auxiliary Feedwater System Unit 2 System Health Report - Reactor Coolant Pump Unit 1 System Health Report - Reactor Coolant Pump Unit 2 Equipment Reliability Improvement Project (ERIP) Plan PM Deferral Request #0200501199/10010020 - Overhaul 500Kv Disconnect Switch 0DISC589-42B PM Deferral Request #1200501833/10030059 - Replace / Test the P-13000-1 Fault Press Device PM Deferral Request #1200501831/10030068 - Wire Chack from XFMR CNTRL Cabinets Final Response to NRC Generic Letter 89-13, Service Water system problems affecting safety-related equipment, dated June 30, 1994 UFSAR Section 6.9, Auxiliary Feedwater Pump Room Emergency Cooling UFSAR Section 7.10, Auxiliary Feedwater Actuation System UFSAR Section 10.3, Auxiliary Feedwater System Vendor Technical Manual #15002-027 - Automatic Recirculation Control Valve Field Engineering Change #87-115-26 - AFW Enhancements Engineering Service Package #ES200100390 - 22 TDAFW pump sealant repairs Byron Jackson Technical Manual #VTD-B580-1032 - DVMX six-stage pump Calvert Cliffs Top Ten Material Condition List ler 012991-001-000022891 - Design Error in EGD Air Start System Parker V-Series Needle Valve Technical Manual for Model #4Z-V4LK-SS Vendor Information ITE Technical Manual - 125 Volt DC Distribution Panel Valtek Technical Manual Maintenance Bulletin Number 10, Rev. 5/87/5M/P Maintenance Bulletin Number 10, Valdisk Control Valves Rotary Actuators, Beta Positioners Specifications Attachment
 
A-8 LIST OF ACRONYMS AFW Auxiliary Feedwater CAP Corrective Action Program CARB Corrective Action Review Board CCNPS Calvert Cliffs Nuclear Power Station CCW Component Cooling Water CEA Control Element Assembly CFR Code of Federal Regulations EAL Emergency Action Level EDG Emergency Diesel Generator FIN Finding gpm gallons per minute HX Heat Exchanger IMC Inspection Manual Chapter IR Issue Report kV kiloVolt LCO Limiting Condition for Operation LOCA Loss of Coolant Accident NCV Non-Cited Violation NRC Nuclear Regulatory Commission PM Preventive Maintenance POSRC Plant Operations and Safety Review Committee Q&PA Quality and Performance Assessment ROP Reactor Oversight Process SDP Significant Determination Process STDT Surveillance Test Data Trending SW Service Water TSP Thimble Support Plate UFSAR Updated Final Safety Analysis Report VAC Volts - Alternating Current VDC Volts - Direct Current Attachment
}}

Latest revision as of 22:33, 7 December 2019

IR 05000317-05-007, IR 05000318-05-007; 10/31/05 - 11/18/05; Calvert Cliffs Nuclear Plant, Units 1 and 2; Biennial Baseline Inspection of the Identification and Resolution of Problems
ML053570380
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 12/22/2005
From: James Trapp
Reactor Projects Branch 1
To: Vanderheyden G
Constellation Generation Group
Barber G S, RGN-I/DRP/610-337-5232
References
IR-05-007
Download: ML053570380 (22)


Text

ber 22, 2005

SUBJECT:

CALVERT CLIFFS NUCLEAR GENERATING STATION - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT NO.

05000317/2005007, and 05000318/2005007

Dear Mr. Vanderheyden:

On November 18, 2005, the NRC completed a team inspection at the Calvert Cliffs Unit 1 and Unit 2 reactor facilities. The enclosed report documents the inspection findings, which were discussed on November 18, 2005, with you and other members of your staff.

This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, compliance with the Commissions rules and regulations, and with the conditions of your license. Within these areas, the inspection involved examination of selected procedures and representative records, observation of activities, and interviews with personnel.

On the basis of the sample selected for review, the team concluded that in general, problems were properly identified, evaluated, and corrected. Relatively few deficiencies were identified by external organizations that had not been previously identified by your organization. Audits and assessments appeared thorough.

This report documents one NRC-identified finding of very low safety significance (Green). This finding was determined to be a violation of NRC requirements. However, because of its very low safety significance and because it was entered into your corrective action program, the NRC is treating this finding as a non-cited violation, in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you deny this non-cited violation, you should provide a response with the basis for your denial within 30 days of the date of this inspection report, to the U. S.

Nuclear Regulatory Commission, ATTN. Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U. S. Nuclear Regulator Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Calvert Cliffs Facility.

Mr. George Vanderheyden 2 In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

James Trapp, Chief Projects Branch 1 Division of Reactor Projects Docket Nos. 50-317, 50-318 License Nos. DPR-53, DPR-69

Enclosure:

Inspection Report No. 05000317/2005007, 05000318/2005007 w/Attachment: Supplemental Information

REGION I==

Docket Nos: 50-317, 50-318 License Nos: DPR-53, DPR-69 Report Nos: 05000317/2005007, 05000318/2005007 Licensee: Calvert Cliffs Nuclear Power Plant, Inc.

Facility: Calvert Cliffs Nuclear Power Plant Location: 1650 Calvert Cliffs Parkway Lusby, MD 20657-4702 Dates: October 31 - November 4, 2005 and November 14 - 18, 2005 Inspectors: G. Scott Barber, Senior Project Engineer, (Team Leader)

Donald Jackson, Senior Project Engineer John Richmond, Reactor Inspector Ryan Treadway, Acting Resident Inspector Dana Caron, Security Inspector Observer: Nicole Sieller, Nuclear Safety Professional Development Program (NSPDP) Engineer Approved by: James Trapp, Chief Projects Branch 1 Division of Reactor Projects i Enclosure

SUMMARY OF FINDINGS IR 05000317/2005-007, IR 05000318/2005-007; 10/31/05 - 11/18/05; Calvert Cliffs Nuclear Plant, Units 1 and 2; biennial baseline inspection of the identification and resolution of problems. One violation was identified in the area of maintenance procedure adequacy.

This inspection was conducted by four regional inspectors and a resident inspector. One finding of very low safety significance (Green) was identified during this inspection and was classified as a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

Identification and Resolution of Problems The team determined that Constellations Calvert Cliffs (CC) Units 1 and 2 Nuclear Power Plants were effective at identifying problems and entering them into the corrective action program (CAP). Relatively few deficiencies were identified by external organizations (including NRC) that had not been previously identified by the licensee. Audits and self-assessments were generally thorough. Once entered into the CAP, issues were screened and prioritized in a timely manner using established criteria. Items entered into the CAP were also properly evaluated commensurate with their safety significance. The causal evaluations for equipment and performance issues were complete, and proposed corrective actions that addressed the identified causes. Corrective actions were generally effective and typically implemented in a timely manner. On the basis of interviews conducted during the inspection, workers at the station felt free to raise safety issues and were willing to enter them into the corrective action program. However, an ineffective maintenance procedure adversely impacted the availability of an auxiliary feedwater pump.

A. NRC Identified and Self-Revealing Findings Cornerstone: Mitigating Systems Green. The NRC identified a Green non-cited violation (NCV) of Technical Specification (TS) 5.4.1 due to an inadequate procedure for installation and adjustment of packing for the 22 turbine-driven auxiliary feedwater (TDAFW) pump, which led to premature pump shutdown during a quarterly surveillance test. During the test, operators secured the pump when they noticed a burning smell and observed smoke coming from the pumps inboard packing gland. Investigation found the inboard packing gland had lost adequate leak off flow along its inner diameter. The licensee entered the deficiency with the pump overhaul procedure into their corrective action (CA) program for resolution.

ii Enclosure

This finding was greater than minor because it adversely affected the availability of a safety-related TDAFW pump which affected the equipment performance attribute of the Mitigating Systems Cornerstone because the pump was unavailable until the degraded packing had been replaced and the pump was satisfactorily retested. The finding was determined to be of very low safety significance (Green) in accordance with IMC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, because an engineering analysis determined that the pump would have remained operable, and was capable of performing its intended safety function.

(Section 4OA2.2)

B. Licensee-Identified Violations None iii Enclosure

Report Details 4.OTHER ACTIVITIES (OA)

4OA2 Problem Identification and Resolution (Biennial - 71152B)

1. Effectiveness of Problem Identification a. Inspection Scope The inspection team reviewed the procedures, listed in the Attachment to this report, describing the corrective action program (CAP) at Constellations Calvert Cliffs Units 1 and 2 Nuclear Power Plants. Constellation identifies problems by initiating Condition Reports (CRs) for conditions adverse to quality, human performance problems, equipment nonconformances, industrial or radiological safety concerns, and other significant issues. The CRs are subsequently screened for operability, categorized by priority and significance (1 through 4), and assigned for evaluation and resolution.

The team considered risk insights from the NRCs and Constellations risk analyses to focus the sample selection and plant tours on risk-significant systems and components.

The team reviewed CRs selected across the seven cornerstones of safety in the NRCs Reactor Oversight Process (ROP) to determine if problems were being properly identified, characterized, and entered into the CAP for evaluation and resolution. The team selected items from the maintenance, operations, engineering, emergency planning, security, radiological protection, and oversight programs to ensure that the licensee was appropriately considering problems identified in each functional area. The team used this information to select a risk-informed sample of CRs that had been issued since the last NRC Problem Identification and Resolution (PI&R) inspection, which was completed in November 2003.

In addition to CRs, the team conducted plant tours and selected items from other processes at Calvert Cliffs to verify that problems identified in these areas were entered into the corrective action program when appropriate. Specifically, the team reviewed a sample of work requests, engineering documents, operator log entries, control room deficiency logs, operator work-arounds, operability determinations, system health reports, and temporary modifications. The documents were reviewed to ensure that underlying problems associated with each issue were appropriately considered for resolution via the corrective action process. In addition, the team interviewed plant staff and management to determine their understanding of and involvement with CAP. The CRs and other documents reviewed, and a list of key personnel contacted, are listed in the Attachment to this report.

The team reviewed a sample of the licensees Quality and Performance Assessment (Q&PA) audits and surveillances, including the most recent audit of the CAP, quarterly assessment reports, and departmental self-assessments. This review was performed to Enclosure

determine if problems identified through these assessments were entered into CAP, and whether the identified issues were dispositioned appropriately commensurate with the safety significance of the issue. The effectiveness of the audits and self-assessments was evaluated by comparing audit and self-assessment results against self-revealing and NRC-identified findings, and current observations during the inspection.

b. Findings and Assessments No findings of significance were identified.

The team concluded that Constellation was generally effective at problem identification at Calvert Cliffs. The CRs that are written are classified by their significance as category (I, II, III and IV) CRs, with Category I CRs usually requiring a root cause analysis (RCA)

and Category II CRs usually requiring an apparent cause evaluation (ACE). Level III and IV CRs do not typically require detailed reviews. The team noted station staff demonstrated appropriate knowledge of the corrective action program, and entered identified problems into the program at an appropriate threshold. There were approximately 3780 CRs assigned in 2004 and approximately 2877 assigned in 2005 as of the beginning of this inspection. The team did not identify any significant conditions adverse to quality in the maintenance, engineering, or operations tracking systems which did not have a CR associated with them.

Relatively few deficiencies were identified by external organizations, including the NRC, that had not been previously identified by the licensee. Audits and self-assessments were generally thorough. Each department was responsible for reviewing identified issues to look for trends. This program has generally been effective in identifying trends relating to conditions adverse to quality.

The use of the CAP by the security organization was also inspected and the results of this inspection are contained in NRC Inspection Report 05000317/2005008 and 05000318/2005008.

2. Prioritization and Evaluation of Issues a. Inspection Scope The team reviewed the CRs listed in the attachment to this report to assess whether the licensee adequately prioritized and evaluated problems. These reviews evaluated the causal assessment of each issue (i.e., root cause analysis or apparent cause evaluation); and for significant conditions adverse to quality, the extent of condition, and determination of corrective actions to preclude recurrence. Throughout the inspection, the team attended periodic meetings to observe the CR review process and to understand the basis for assigned significance and root cause levels.

The team also considered risk insights from the Calvert Cliffs probabilistic risk assessment to help focus the inspection sample. The team selected the auxiliary Enclosure

feedwater (AFW) system for an expanded review of five years. This system was selected because it is a significant contributor to plant risk.

The team selected a sample of CRs associated with previous NRC non-cited violations (NCVs) and findings to determine whether the licensee evaluated and resolved problems associated with compliance to applicable regulatory requirements and standards. The team reviewed the licensees approach to operating experience (OE),

which included an assessment of multiple examples of how effectively OE is used.

Operability and reportability determinations associated with CRs were also reviewed.

b. Assessments The team determined that Constellation adequately prioritized and evaluated the issues and concerns entered into the CAP. The team concluded that prioritized CRs were based on the safety significance of the issue. Operability determinations and reportability assessments were made promptly when issues were entered into the CAP.

The team noted that licensee management was thoroughly prepared during CR screening meetings as evidenced by their probing questions of presenters. Evaluations were generally completed in a timely manner, particularly after the CAP process was revised to establish a standard 30 day deadline for all CR evaluations. Clear guidance has been developed for performing cause evaluations, and multi-level review of completed evaluations has resulted in generally high quality evaluations with proposed corrective actions that addressed the identified causes.

The team developed specific insights regarding the five year review of the AFW system and of Constellations OE program. These assessments are described below. The team also identified that the evaluation of a maintenance activity did not fully address all potential causal factors because a key underlying procedural inadequacy remained unaddressed. Thus, the team identified one finding of low safety significance (Green)

that was a violation of NRC requirements which is described in section c. below.

Auxiliary Feedwater System Five Year Review The team selected the auxiliary feedwater (AFW) system for the five year inspection and review, which is the most risk significant system at Calvert Cliffs. A complete system walkdown was conducted and no significant conditions adverse to quality were identified. The team interviewed operators and the system engineer and determined that they had a basic understanding of the system and previous issues documented in CRs and IRs.

The team reviewed the last five years of logs, data and trends for the AFW system including condition reports, apparent cause evaluations, root cause evaluations, AFW system procedures, operator logs, and tagouts to assess AFW system performance from a corrective action standpoint. The team generated a table for AFW system components conditions that were adverse to quality and categorized the information by significance to assess performance. The team determined that there were several failed surveillances that involved the TDAFW control valves and questioned the licensee Enclosure

to determine if a previously undetected adverse trend existed. The inspectors noted several failed surveillances for the TDAFW control valves related to American Society of Mechanical Engineers code compliance issues, repetitive use of inadequate maintenance procedures which resulted in failed surveillances, and several condition reports related to improper use of vendor recommendations. Detailed followup by the team later determined that the licensees actions to evaluate these issues were adequate and that corrective action taken was commensurate with the issues safety significance.

Operating Experience The process that Constellation used to collect, screen, review OE appeared to be very effective. Operating experience is gathered from multiple sources, and is screened daily for general applicability and an update is e-mailed to an extensive list of licensee personnel for their information. In cases where the operating experience is screened to be applicable to the licensee, an action item is generated to perform a barrier analysis to determine if further corrective action is needed. If action is required, a condition report is generated to address the underlying OE. The program used a simple database that plant staff can easily access. Licensee staff charged with administering the operating experience program were proactive at screening OE which was clearly valued by line management as evidenced by the timely responses OE screening requests and actions generated by these reviews. The team reviewed several operating experience items that were in various stages of resolution. The team determined that the licensee had an effective program and management displayed strong support of the operating experience program.

c. Findings Introduction. The NRC identified a Green non-cited violation (NCV) of Technical Specification (TS) 5.4.1 due to inadequate procedures for installation and adjustment of packing for the 22 turbine driven auxiliary feedwater (TDAFW) pump, which led to premature pump shutdown during a quarterly surveillance test. The team determined that appropriate procedural guidance would have precluded the pump unavailability that occurred until the repairs were accomplished and the pump was satisfactorily retested.

Description. On December 8, 2004, during a quarterly surveillance test, the 22 TDAFW pump was shutdown due to a lack of adequate packing gland leakage, and the observation and smell of smoke coming from the pump inboard packing gland. After the pump shutdown, the licensee replaced the packing, performed a successful surveillance and declared the pump operable on December 9, 2004.

The apparent cause evaluation (ACE) (IR200400582) for this condition stated that the pressure applied to the bottom three rings of packing reduced the clearance needed for sufficient packing leak off. The licensee postulated that this raised the temperature of the water and caused flashing which virtually eliminated packing leak off flow. Thus, the packing began to deform and fuse together until all leak off was subsequently stopped.

Enclosure

The licensees operability assessment determined that the TDAFW pump was operable in the as-found condition, with the packing degraded.

Based on interviews, the team determined that operators would have taken action to secure the TDAFW pump and place the standby pump in-service if the packing had degraded during an actual plant event (e.g., a loss of off-site power) based on procedural guidance in OI-32A, AFW system. The team also determined that appropriate procedural guidance for repacking the pump would have precluded the pump unavailability that occurred until the repairs and a satisfactory retest were accomplished on December 9, 2004.

The licensee identified the apparent cause for the TDAFW pump unavailability as improper pump packing installation and adjustment. The licensee proposed changes to the AFW operating instruction and the surveillance test procedure but did not propose change the pump overhaul procedure. The team discussed the reasons for this approach with the licensee and pointed out that the pump overhaul procedure only included one step for repacking the pump and it did not reference the vendor technical manual (VTM). The Byron-Jackson VTM-B580-1032 listed several key steps that are necessary to ensure adequate packing installation and adjustment. Plant staff acknowledged that a change to the overhaul procedure was needed. Consequently, a Request for a Procedure Addendum (RPA) to make the appropriate changes to the pump overhaul procedure was implemented to ensure that appropriate vendor technical manual guidance for repacking of the pump was included.

Analysis. The packing failure was a performance deficiency because the existing maintenance procedure was not adequate to ensure that TDAFW pump repack was successfully performed. This finding was more then minor because it affected the procedure quality attribute of the Mitigating Systems Cornerstone and affected the cornerstone objective of ensuring the availability of systems that respond to initiating events to prevent undesirable consequences. The team conducted a significance determination process (SDP) Phase 1 screening in accordance with IMC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations. The finding was determined to be Green because the inadequate procedure and subsequent packing degradation did not result in a loss of function per Generic Letter 91-18, did not represent loss of a safety system function for longer than the TS limiting condition for operation (LCO) allowed outage time, and did not involve an external event.

Enforcement. Technical Specification 5.4.1 requires the licensee to establish, implement, and maintain procedures for the auxiliary feedwater system as referenced in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Contrary to these requirements, the licensee did not implement adequate procedures for the TDAFW pump packing installation and adjustment. Because this deficiency was of very low safety significance and has been entered into the corrective action program as IRE-001-860, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000318/2005007-01 AND 05000318/2005007-01, Inadequate Procedure for Installation and Adjustment of TDAFW Pump Packing.

Enclosure

3. Effectiveness of Corrective Actions a. Inspection Scope The team reviewed the corrective actions associated with selected CRs to determine whether they addressed the identified causes of the problems. The licensees timeliness in implementing corrective actions and their effectiveness in precluding recurrence for significant conditions adverse to quality was also reviewed. Furthermore, the team assessed the backlog of outstanding corrective actions to determine if they, individually or collectively, represented an increased risk to the plant. The team also reviewed NCVs and findings issued since the last inspection of the licensees CAP to determine if issues placed in the program had been properly evaluated and corrected.

b. Findings and Assessments Overall, the team concluded that Constellations corrective actions for identified deficiencies were typically timely and adequately implemented. Administrative controls have been put in place to ensure that corrective actions are completed as scheduled and reviews are performed to ensure the actions were implemented as intended.

Constellation also conducted in-depth effectiveness reviews for significant issues to determine if the corrective actions were effective in resolving the issue. In some cases, the licensee appropriately self-identified ineffective or improper closeout of corrective actions and reentered the issue into the CAP for further action. However, the team noted a long-standing issue in which corrective actions were not totally effective in addressing conditions adverse to quality.

Component Mispositioning The team reviewed the effectiveness of corrective actions taken to resolve a long-standing issue associated with component mispositioning events. In December 2003, a Category 1 Root Cause Analysis (RCA) was generated to resolve a continuing series of component mispositioning problems. Corrective actions for this issue included raising personnel accountability, providing additional personnel training, pre-job briefing improvements, general employee training improvements, and work load controls. These corrective actions had little effect in lowering the number or significance of component mispositionings. As a result, in May 2004, a Category 2 Apparent Cause Analysis (ACE) was conducted to further address this problem. The actions generated in response to this ACE were numerous and significant and included the initiation of a comprehensive human performance improvement program (HPIP). The HPIP program action plan has become a living document where changes to the original action plan have been made based on need and the scope of improvements was widened beyond those in response to the original December 2003 RCA on this issue. This program has been generally effective at lowering the significance of component mispositionings, however, the number of component mispositionings have not significantly decreased.

Enclosure

The licensee has generated an effective performance indicator to track progress in the mispositioning area. The performance indicator accounts for both the number and significance of component mispositionings. In May and June 2005, the performance indicator indicated that expectations were not being met in the area of component mispositionings as a result of 8 component mispositionings in early 2005, including one mis-positioning that had a negative consequence as determined by the licensees program. As a result of the performance indicator degradation, the licensee initiated another Category 2 Apparent/ Common Cause Analysis to correct the negative trend.

This analysis determined that the cause of the mis-positionings was due to a lack or misuse of error prevention tools that had been established by their HPIP. The team observed a number of planned activities that had the potential to result in component mis-positionings. During these observations, the team noted that station personnel were very consistent in their use of the error prevention tools that had been established by their HPIP and that the number and nature of the tools being used was commensurate with the potential significance of any mis-positioning that could occur.

Although the corrective actions for a previous significant condition adverse to quality have not been totally effective at curtailing the frequency of component mispositionings, the significance of component mispositionings has lowered to a level where the mitigating systems cornerstone attribute has not been negatively impacted. Thus, the team determined that this was a minor issue because Constellation had improved the frequency of use of error prevention tools to limit the actual significance of component mispositionings.

4. Assessment of Safety Conscious Work Environment a. Inspection Scope The team members interviewed plant staff, observed various activities throughout the plant, and attended a cross section of meetings to determine if conditions existed that would result in personnel being hesitant to raise safety concerns to their management and/or the NRC. The team also reviewed a sample of investigations performed to address employee and contractor concerns to assess the effectiveness of the employee concerns program (ECP).

b. Findings and Assessments No findings of significance were identified.

Employee Concerns Program The team determined that the investigations performed for employee concerns appeared prompt and thorough. The program administrator willingly accepted not only safety concerns, but work place concerns. The threshold for entering concerns in the program appeared appropriately low. Although the reviews did appear thorough, there was a great deal of variability in the level of documentation for some investigations. In some instances, the status of open investigations was not available in the written record although it was available on the computer. In other instance, the basis for the closeout Enclosure

of certain workplace concerns was not succinctly provided. The specific details of these and other similar issues were discussed with the program administrator and the quality assurance manager.

4OA6 Meetings, Including the Exit Meeting The team presented the inspection results to Mr. George Vanderheyden and other members of licensee management on November 18, 2005. Licensee management acknowledged the results presented. No proprietary information was identified during the inspection.

4OA7 Licensee-Identified Violations None ATTACHMENT: Supplemental Information In addition to the documentation that the inspectors reviewed (listed in the attachment), copies of information requests given to the licensee are in ADAMS, under accession number ML053460412.

Enclosure

A-1 SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT Licensee Personnel J. Pollack , Plant General Manager D. Bauder, Operations Manager J. Sickle, Manager, Nuclear Training M. Gahan III, Principal Engineer, Equipment Reliability Unit W. Rummel, Senior Operational Safety Analyst A. Simpson, Senior Engineer, Calvert Cliffs Regulatory Matters P. Suter, Operations Maintenance Coordinator E. Dean, Assistant Operations Manager M. Seckens, Supervisor of Nuclear Safety Services K. Crissman, Supervisor E&C, and Human Performance Improvement Lead T. Huber, Shift Manager J. Grooms, Shift Manager J. Gioffre, Control Room Supervisor G. Getz, Control Room Supervisor D. Woods, Nuclear Plant Operator L. Vandersnick, Nuclear Plant Operator R. Ciabattoni, Nuclear Plant Operator B. Shobert, Nuclear Plant Operator W. Tippett, Operating Experience Lead J. Wynn, Senior Engineer, Primary Systems Engineering M. Lewis, Senior Engineer, Primary Systems Engineering M. Dorn, Associate Engineer, Systems Engineering LIST OF DOCUMENTS REVIEWED Opened and Closed 05000317,05000318/2005007-01 NCV Failure to identify and correct unavailability problems for the turbine drive AFW pump.

(Section 4OA2.c.2).

Procedures NO-1-106 Functional Evaluation/Operability Determination, Rev. 10 NS-1-100 Use of Operating Experience, Rev. 7 NS-1-101 Employee Concerns Program, Rev. 0 QL-2-100 Corrective Action Program, Rev 0 EN-1-100 Engineering Services Process Overview MN-1-101 Control of Maintenance Activities

A-2 MN-1-123 Integrated Work Planning CNG-CA-1.01-1001 Management Review Committee, Rev. 0 CNG-CA-1.01-1002 Corrective Action Review Board, Rev. 0 CNG-CA-1.01-1004 Root Cause Analysis, Rev. 0 CNG-CA-1.01-1005 Apparent Cause Evaluation, Rev. 0 CNG-CA-1.01-1006 Common Cause Analysis, Rev. 0 CNG-HU-1.01-1001, Rev. 1 Human Performance Tools and Verification Practices CNG-HU-1.01-1002, Rev. 2 Pre-Job Briefings and Post-Job Critiques CNG-HU-1.01-1003, Rev. 0 Human Performance Tools For Non-Field Technical Activities TR-1-101, Rev 18 Conduct of Training NO-1-106 Functional Evaluation/Operability Determination, Rev. 10 NS-1-100 Use of Operating Experience, Rev. 5 QL-2-104 Self-Assessment, Rev. 3 QL-2-105 Conduct of the Corrective Action Review Board, Rev. 4 QL-2-106 Site Key Performance Indicators, Rev. 0 OI-29 Saltwater System, Rev. 57 OI-32A Auxiliary Feedwater System, Rev.16 STP-O5A-1 Auxiliary Feedwater System Quarterly Surveillance Test, Rev. 19 STP-O5A-2 Auxiliary Feedwater System Quarterly Surveillance Test, Rev. 18 Pump-12 Turbine Driven Auxiliary Feedwater Pump Overhaul, Rev. 7 Audits and Self-Assessments RPP-04-01-C Radiation Protection and Radioactive Materials Management SPT-04-01-C Special Processes / Section XI / Testing ISF-04-01-C Independent Spent Fuel Storage Installation (ISFSI)

MAP-05-01-C Maintenance Program SA200300050- Operations Department Self Assessment SA200400042- Operations Department Self Assessment SA200400168- Calvert Cliffs Nuclear Safety Self Assessment\

Audit OPS-04-01-C Nuclear Plant Operations- QA Audit Operating Experience Documents Reviewed OE 18634 Small Fire Under Reactor Feed Pump Turbine OE 18895 Mihama- Death of a Worker Due To Condensate Rupture OE 19803 High Initial License Class Failure Rate OE 19810 Error In Plant Monitoring System Software OE 20688 Tin Whiskers Found On SSPS Circuit Cards Miscellaneous Items Reviewed Operations Work-Around List- Dated October 6, 2005 Control Room Deficiencies List- Dated October 6, 2005 Active Operability Determinations List- Dated September 29, 2005 Training Lesson Plan- Corrective Action Program Basic Overview Operations Component Mis-positioning Action Plan Attachment

A-3 Non-Cited Violations (NCV) and Findings (FIN)

NRC NCV 2003-006-01 IR4-027-075 [IR200300457]

NRC NCV 2004-002-02 IR4-008-006 [IR200400065]

NRC NCV 2004-002-03 IR4-008-997 [IR200400073]

NRC NCV 2004-004-01 IR4-023-638 [IR200400310]

NRC NCV 2004-005-02 IR4-030-055 [IR200400254]

NRC NCV 2004-008-04 IR4-030-176 [IR200400276] special inspection Condition Reports IR4-019-491 3R200402451 3R200500940 IR4-019-404 3R200402486 3R200500956 IR4-001-097 3R200500094 3R200501421 IRE-002-678 3R200500529 3R200501440 IRE-003-544 3R200500794 3R200501871 IRE-003-998 IR3-077-073 3R200501951 IRE-004-359 IR3-062-103 IR200300307 IRE-007-196 IRE-001-860 IR200300402 IR200300402 IR4-028-800 IR200400047 IR200400056 IR4-025-059 IR200400198 IR200400066 IR4-028-786 IR200400254 IR200400106 IR4-007-136 IR200400198 IR200400546 IR4-007-137 IR200400053 IR200400564 IR4-002-245 IR200400254 IR200500004 IR4-026-577 IR200400047 IR200500071 IR4-007-138 IR200400053 IR200500151 IR4-034-668 IR200400254 IR200300410 IR4-028-774 IR200300458 IR200400036 IR4-023-561 IR3-072-603 IR200400051 IR4-035-828 IRE-008-095 IR200400089 IR4-028-183 IRE-008-859 IR200400126 IR3-031-076 IRE-008-318 IR200400162 IR3-042-570 IRE-008-142 IR200400186 IR3-054-115 IRE-008-058 IR200400211 IR3-062-103 IRE-006-910 IR200400248 IR3-063-687 IR4-003-606 IR200400251 IR3-075-298 IR4-031-243 IR200400299 IR3-076-835 IRE-006-286 IR200400342 IR3-076-860 IR4-031-267 IR200400402 IR3-077-073 IRE-003-501 IR200400454 IR3-077-124 IR200300409 IR200400458 IR3-084-380 IR200300458 IR200400589 IR3-084-400 IR200400033 IR200500125 IR4-010-076 IR200400111 IR200500185 IR4-010-875 IR200400198 Attachment

A-4 IR200500188 IR4-041-139 IR200400254 IR200500204 IR3-043-669 IRE-004-220 3R200400010 IR3-044-531 IRE-019-658 3R200400310 IR3-048-589 IRE-014-006 3R200400406 IR3-048-642 3R200400733 IR3-053-642 3R200400771 IR3-076-976 3R200400868 IR3-081-274 3R200401135 IR3-084-379 3R200401253 IR4-015-857 3R200401292 IR3-032-391 3R200401453 IR3-059-054 3R200401647 IR3-082-917 3R200401713 IR4-002-760 3R200401771 IR4-015-052 3R200401839 IR4-018-247 3R200402077 IR4-001-896 3R200402119 IR4-011-627 3R200402199 IR3-041-489 3R200402351 IR3-059-099 3R200402449 3R200402448 3R200402450 Action Item Tracking - Responses AIT 4B200200042 AIT 4B200200073 AIT 4B200300070 AIT 4B200300125 AIT 4B200300139 AIT 4B200300179 AIT 4B200300184 AIT 4B200300381 AIT IR200400582 AIT IR200500209 Maintenance Orders 0200102212 1200102971 1200204878 0200202140 1200201224 2000101865 1200100846 1200203328 2199501219 Attachment

A-5 2199601549 2200404545 2199700837 2200200685 2200003755 2200101441 2200100609 2200302891 2200100610 2200400612 2200101305 2200400728 2200102726 2200400310 2200102951 1200401033 2200103805 1200400448 2200103815 2200304932 2200203698 2200102181 2200203963 1200401980 2200302231 1200303236 2910542001 1200402911 2910542101 2200400444 2200401217 2204016770 2200403496 1200501254 2200304260 2200401216 2200401173 2200303845 1200401591 2200302811 Drawings 62708SH0002 Circulating Water Cooling System, Rev. 95 62708SH0003 Circulating Water Cooling System, Rev. 7 62706SH0002 Service Water Cooling System Auxiliary Building/Containment, Rev. 64 60730SH0001 Chemical and Volume Control System 60730SH0002 Chemical and Volume Control System 60730SH0003 Chemical and Volume Control System 62731SH0003 Safety Injection and Containment Spray Systems, Rev. 39 63024 Single Line Diagram 125 DC Vital System Bus 21 61025 Single Line Diagram 125 DC Vital System Bus 12 and 22 61024 Single Line Diagram 125 DC Vital System Bus 11 60583SH0002 Auxiliary Feedwater System (Steam), Rev. 60 60583SH0002 Auxiliary Feedwater System (Condensate), Rev.0 60727SH0002 Diesel Generator Cooling Water, Starting Air, fuel, & Lube Oil Diesel No. 1B, Rev. 62 60727SH0003 Diesel Generator Cooling Water, Starting Air, fuel, & Lube Oil Diesel No. 2B, Rev. 50 60727SH0001 Diesel Generator Cooling Water, Starting Air, fuel, & Lube Oil Attachment

A-6 Diesel No. 2A, Rev. 59 60738SH0001 Area and Process Radiation Monitoring System, Rev. 66 60738SH0002 Area and Process Radiation Monitoring System, Rev. 21 Operating Experience Review Information Notice 94-03 Deficiencies identified during SW operational inspections Information Notice 03-02 Recent Experience with Reactor Coolant System Leakage and Boric Acid Corrosion Information Notice 02-36 Incomplete or Inaccurate Information Provided to the License and/or By Any Contractor or Subcontractor Employee Information Notice 03-08 NRC Potential Flooding Through Unsealed Concrete Floor Cracks Information Notice 02-27 Recent Fires at Commercial Nuclear Power Plants in the United States Information Notice 02-18 Effect of Adding Gas Into Water Storage Tanks on the Net Positive Suction Head for Pumps Information Notice 03-15 Importance Of Followup Activities In Resolving Maintenance Issues Miscellaneous Letter: Response to Inspection Report Nos. 50-317/89-200; 50-318/89-200 (Special Team Inspection), June 21, 1989 Letter: Implementation of Computerized Trending of Surveillance Data, dated April 4, 1990 Letter: Response and Supplemental Responses to NRC Bulletin 88-04, Potential Safety-Related Pump Loss, dated July 5, 1988, December 21, 1988, and August 22, 1989 Letter: Nuclear Logistics Inc to Mr. G. Dare CCNPS , 10/31/03, documenting safety function of 125 VDC post seal components Letter: Calvert Cliff Response to 10 CFR 21 Notification (ABB Breakers), dated May 13, 2002 Memorandum:February 10, 2000 Maintenance Rule Expert Panel Meeting Minutes, 2/17/00 Memorandum:Designation of Surveillance Test Coordinator and Functional Surveillance Test Coordinators per EN-4-104, Surveillance Testing, 4/10/02 CARB Meeting Minutes of 10/23/03 and 10/28/03 Maintenance Indicators for October 2003 Maintenance Rule Scoping Document - System 015 - Rev. 21 Corrective Action Program Performance Indicator Index July and August, 2003 System Health Report- Salt Water System Health Report- Component Cooling Water System Health Report- Service Water System Health Report - 125 Vdc System Health Report - 120 Vac System Health Report - Reactor Coolant System Calvert Cliffs Industrial Safety Manual, Rev. 4, Component Manipulation Form CM-03-186, Unit 1 Component Manipulation Form CM-03-153, Unit 2 Operability Determination OD No.03-004, Intake Structure Fire Detection Equipment Reliability Improvement Project (ERIP) Plan Attachment

A-7 ERIP Plant Health Committee Charter, September 17, 2002 ERIP Steering Committee Charter, March 15, 2003 Plant Health Committee - Outstanding Equipment Reliability Issues, 11/7/03 Plant Health Committee Meeting Minutes: 6/5/03, 7/22/03, 7/24/03 8/7/03, 8/28/03, 9/5/03 ES200200752, Request for Alternate Mounting of Trico Oiler (9/10/02), Rev. 0 Final Response to NRC Generic Letter 89-13, Service Water system problems affecting safety-related equipment, dated June 30, 1994 UFSAR Section 9.5, Cooling Water Systems CARB Meeting Minutes of 10/31/05 and 11/02/05 Maintenance Rule Scoping Document - System 036A - Rev. 24 Maintenance Rule Scoping Document - System 064B - Rev. 24 Plant Health Committee Issues List Plant Health Committee Issues List Coming Due Plant Health Committee Meeting- 11/01/2005 System Health Report-Process Rad Monitor RCS Leak Detection Inside Containment System Health Report- Process Rad Monitor Gaseous Effluent Radiation Monitor System Health Report- Process Rad Fuel Handling Accident Monitors System Health Report- Auxiliary Feedwater System Unit 1 System Health Report- Auxiliary Feedwater System Unit 2 System Health Report - Reactor Coolant Pump Unit 1 System Health Report - Reactor Coolant Pump Unit 2 Equipment Reliability Improvement Project (ERIP) Plan PM Deferral Request #0200501199/10010020 - Overhaul 500Kv Disconnect Switch 0DISC589-42B PM Deferral Request #1200501833/10030059 - Replace / Test the P-13000-1 Fault Press Device PM Deferral Request #1200501831/10030068 - Wire Chack from XFMR CNTRL Cabinets Final Response to NRC Generic Letter 89-13, Service Water system problems affecting safety-related equipment, dated June 30, 1994 UFSAR Section 6.9, Auxiliary Feedwater Pump Room Emergency Cooling UFSAR Section 7.10, Auxiliary Feedwater Actuation System UFSAR Section 10.3, Auxiliary Feedwater System Vendor Technical Manual #15002-027 - Automatic Recirculation Control Valve Field Engineering Change #87-115-26 - AFW Enhancements Engineering Service Package #ES200100390 - 22 TDAFW pump sealant repairs Byron Jackson Technical Manual #VTD-B580-1032 - DVMX six-stage pump Calvert Cliffs Top Ten Material Condition List ler 012991-001-000022891 - Design Error in EGD Air Start System Parker V-Series Needle Valve Technical Manual for Model #4Z-V4LK-SS Vendor Information ITE Technical Manual - 125 Volt DC Distribution Panel Valtek Technical Manual Maintenance Bulletin Number 10, Rev. 5/87/5M/P Maintenance Bulletin Number 10, Valdisk Control Valves Rotary Actuators, Beta Positioners Specifications Attachment

A-8 LIST OF ACRONYMS AFW Auxiliary Feedwater CAP Corrective Action Program CARB Corrective Action Review Board CCNPS Calvert Cliffs Nuclear Power Station CCW Component Cooling Water CEA Control Element Assembly CFR Code of Federal Regulations EAL Emergency Action Level EDG Emergency Diesel Generator FIN Finding gpm gallons per minute HX Heat Exchanger IMC Inspection Manual Chapter IR Issue Report kV kiloVolt LCO Limiting Condition for Operation LOCA Loss of Coolant Accident NCV Non-Cited Violation NRC Nuclear Regulatory Commission PM Preventive Maintenance POSRC Plant Operations and Safety Review Committee Q&PA Quality and Performance Assessment ROP Reactor Oversight Process SDP Significant Determination Process STDT Surveillance Test Data Trending SW Service Water TSP Thimble Support Plate UFSAR Updated Final Safety Analysis Report VAC Volts - Alternating Current VDC Volts - Direct Current Attachment