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| | issue date = 09/12/1997 | | | issue date = 09/12/1997 |
| | title = LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr | | | title = LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr |
| | author name = DONAHUE J W, VERRILLI M | | | author name = Donahue J, Verrilli M |
| | author affiliation = CAROLINA POWER & LIGHT CO. | | | author affiliation = CAROLINA POWER & LIGHT CO. |
| | addressee name = | | | addressee name = |
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| {{#Wiki_filter:CATEGORY I REGUIATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9709180097 DOC.DATE: 97/09/12 NOTARIZED: | | {{#Wiki_filter:CATEGORY I REGUIATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) |
| NO FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina AUTH.NAME.AUTHOR AFFILIATION VERRILLI I M.Carolina Power 6 Light Co.DONAHUE,J.W. | | ACCESSION NBR:9709180097 DOC.DATE: 97/09/12 NOTARIZED: NO DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH. NAME . AUTHOR AFFILIATION VERRILLII M. Carolina Power 6 Light Co. |
| Carolina Power a Light Co.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000400 A E 05000400 NOTES:Application for permit renewal filed. | | DONAHUE,J.W. Carolina Power a Light Co. |
| | RECIP.NAME RECIPIENT AFFILIATION |
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| |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER 97-020-00:on 970814,inadequate fire protection provided for safety-related EDG fuel oil transfer pump cables caused operation outside design basis,was identified. | | LER 97-020-00:on 970814,inadequate fire protection provided for safety-related EDG fuel oil transfer pump cables caused operation outside design basis,was identified. Caused by engineering oversight. Established fire watches.W/970912 ltr. A DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: |
| Caused by engineering oversight. | | TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc. |
| Established fire watches.W/970912 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.RECIPIENT ID CODE/NAME PD2-1 PD INTERNAL: ACRS AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DET/EIB EXTERNAL: L ST LOBBY WARD NOAC POOREgW.NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME ROONEYiV CE NRR/DE/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN2 FILE 01 LITCO BRYCEiJ H NOAC QUEENER,DS NUDOCS FULL TXT COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 0 D 0 C N NOTE TO ALL"RIDS" RECIPIENTS: | | E NOTES:Application for permit renewal filed. 05000400 RECIPIENT COPIES RECIPIENT COPIES 0 ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-1 PD 1 1 ROONEYiV 1 1 INTERNAL: ACRS 1 1 2 2 AEOD/SPD/RRAB 1 1 CE 1 1 NRR/DE/ECGB 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DET/EIB 1 1 RGN2 FILE 01 1 1 D EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCEiJ H 1 1 0 NOAC POOREgW. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 C N |
| PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25 O.l 4~t t t h S I ,l F~s'f 1 I l I r 1 t 4 Carolina Power&Light Company Harris Nuclear Plant PO Box 165 New Hill NC 27562 SEP 12 1997 U.S.Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 Serial: HNP-97-174 10CFR50.73 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO.50-400 LICENSE NO.NPF-63 LICENSEE EVENT REPORT 97-020-00 Sir or Madam: In accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted.
| | NOTE TO ALL "RIDS" RECIPIENTS: |
| This report describes a design deficiency related to inadequate fire protection for safety-related cables.Sincerely, MV J.W.Donahue Director of Site Operations Harris Plant Enclosure c: Mr.J.B, Brady (HNP Senior NRC Resident)Mr.L.A.Reyes (NRC Regional Administrator, Region II)Mr.V.L.Rooney (NRC-NRR Project Manager)9709180097 970912 PDR ADGCK 05000400 8 PDR State Road 1134 New Hill NC lllllilI5lllllllElllllllllllllllllll NRC FORM 366 (495)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)(See reverse for required number of digits/characters for each block)APPROVED BY OMB No.3160-0104 EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THS MANDATORY D(FORMATION COLLECTION REOUESR QN HRS.REPORTED LESSONS LEARNED ARE BICORPORATEO UITO THE UCENQNG PROCESS ANO FEO BACK TO INDUSTRY.FORWARD COMMENTS REGARDB(G BURDEN ESTIMATE TO THE INFORMATION ANO RECORDS MANAGEMENT BRANCH IT4 F33l, US.NUCLEAR REGULATORY COMMISIOH, WASHINGTOIL OC 20555000), ANO TO THE PAPERWORK REDUCTION PROJECT (3)50.OIO(L OFF)CE OF MANAGEMEHT AND BUDGET, WASHBIGTOH, OC 20503.FACIUTY NAME Ill Harris Nuclear Plant Unit-1 DOCKET NUMBER (2)50-400 PAOE (3)1 OF3 TITLE (4)Inadequate fire protection provided for safety-related EDG Fuel Oil Transfer Pump cables resulting in operation outside design basis.EVENT DATE (5)LER NUMBER (6)REPORT DATE (7)OTHER FACILITIES INVOLVED (8)MONTH DAY YEAR 14 97 YEAR SEQUENTIAl NUMBER REVIIDN NUMBER 97-020-00 MONTH DAY 97 FACIUTY NAME FACIUTY NAME OOCKET NUMBER DOCKET NUMBER 05000 OPERATING MODE (9)POWER LEVEL (10)kAME 1005G 50.73(a)(2)(i) 20.2203(a)
| | PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25 |
| (2)(v)20.2201(b) 50.73(a)(2)(viii)50.73(a)(2)(x) 50.73(a)(2)(ii)50.73(a)(2)(iii)20.2203(a)(3)(i)20.2203(a)(3)(ii) 20.2203(a)(l | | |
| )20.2203(a)(2)(i) 73.71 20.2203(a)
| | l O. |
| (2)(ii)20.2203(a)(2)(iii) 20.2203(a) | | |
| (2)(iv)50.73(a)(2)(iv) 50.73(a)(2)(v)50.73(a)(2)(vii)20.2203(a) | | 4 ~ |
| (4)50.36(c)(1) 50.36(c)(2)LICENSEE CONTACT FOR THIS LER (12)TELEP)(ONE NUMBER Urcrude Ares Code)OTHER W Specify In Abstract belo or in NRC Form 306A THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR B: (Check one or morel (11)Michael Verrilli Sr.Analyst-Licensing (919)362-2303'COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABIE TD NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (lf yes, complete EXPECTED SUBMISSION DATE).X NO EXPECTED SUBMISSION DATE (16)MONTH DAY YEAR ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single.spaced typewritten lines)(16)On August 14, 1997, with the plant at approximately 100%power in mode 1, design discrepancies were identified during an Engineering review of the Safe Shutdown Analysis in Case of Fire.These discrepancies pertain to safety-related Emergency Diesel Generator Fuel Oil Transfer pump electrical cables.These cables are required for safe shutdown in case of a fire, but were not adequately protected. | | t t |
| Specifically, section 9.5.1 of the Harris Plant Final Safety Analysis Report (FSAR)provides separation requirements for redundant safe shutdown divisions to maintain safe shutdown capability. | | t h |
| During the Engineering review, Cables 12549E-SA and 12550A-SB, located in the 261'levation of the Reactor Auxiliary Building were found to not meet the specific design requirements. | | S I ,l F |
| The first cable (12549E-SA) was in an area that had automatic fire detection/suppression systems, but was not separated by a 3-hour fire barrier or 20 feet of horizontal distance and was not enclosed in a 1-hr rated barrier.The second cable (12550A-SA) was separated by 20 feet horizontally, but no suppression/detection system was provided in its location, nor was a 3-hour barrier provided.These design deficiencies were caused by engineering oversight and inadequate design verification during initial plant construction. | | ~s ' |
| Immediate corrective actions included establishing fire watches for the areas with unprotected cables.A plant modification will be developed and installed to provide the required protection. | | f 1 |
| NRC FORM 3SSA I4.85l LICENSEE EVENT REPORT (LER)TEXT CONTINUATION US.NUCEEAR RECUIATORZ COMMISSION FACIUTZ NAME (I)Shearon Harris Nuclear Plant~Unit rII1 TEXT pl sssdr sptssis sssisisd.dss sdStknd soidss ol A'RC Fam 3SQI ill)OOCKET 50400 IER NUMBER ISI SEOUENTIAl. | | I l |
| REZISION NUMBER NUMBER 07-020-00 PACE Ql 2 OF 3 EVENT DESCRIPTION:
| | I r |
| On August 14, 1997, with the plant at approximately 100%power in mode 1, design discrepancies were identified during an Engineering review of the Safe Shutdown Analysis in Case of Fire performed per Engineering Service Request (ESR9500433). | | 1 t |
| These discrepancies pertain to safety-related"A" and"B" Emergency Diesel Generator Fuel Oil Transfer pump electrical cables.These electrical cables are required for safe shutdown in case of a fire, but were not adequately protected. | | 4 |
| Specifically, section 9.5.1 of the Harris Plant Final Safety Analysis Report (FSAR)provides separation requirements for redundant safe shutdown divisions to maintain safe shutdown capability. | | |
| FSAR section 9.5.1 requires protection of cables outside containment by one of the following methods such that at least one division of redundant safe shutdown cables located within the same fire area are protected from fire damage: (1)Separation of cables and equipment and associated circuits of redundant safe shutdown divisions by a fire barrier having a 3-hour rating or equivalent. | | Carolina Power & Light Company Harris Nuclear Plant PO Box 165 New Hill NC 27562 SEP 12 1997 U.S. Nuclear Regulatory Commission Serial: HNP-97-174 ATTN: NRC Document Control Desk 10CFR50.73 Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 97-020-00 Sir or Madam: |
| Structural steel forming a part of or supporting such fire barriers is protected to provide resistance equivalent to that required of the barrier.(2)Separation of cables and equipment and associated circuits of redundant safe shutdown divisions by a horizontal distance of more than 20 feet with no intervening combustible or fire hazards.In addition, fire detectors and an automatic suppression system is installed in the area.(3)Enclosure of cable and equipment and associated circuits of one redundant train in a fire barrier having a 1-hour rating.In addition, fire detectors and an automatic fire suppression system are installed in the fire area.During the ESR-9500433 Engineering review, Cables 12549E-SA and 12550A-SB, located in the 261'levation of the Reactor Auxiliary Building were found to not meet the above requirements. | | In accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted. This report describes a design deficiency related to inadequate fire protection for safety-related cables. |
| The first cable (12549E-SA), which provides control power for the"A" EDG Fuel Oil Transfer Pump, was in an area that had automatic fire detection/suppression systems, but was not separated by a 3-hour'fire barrier or 20 feet of horizontal distance and was not enclosed in a 1-hr rated barrier.Approximately 50 feet of conduit for this cable will require additional protection. | | Sincerely, J. W. Donahue Director of Site Operations Harris Plant MV Enclosure c: Mr. J. B, Brady (HNP Senior NRC Resident) |
| This will involve installation of a one hour fire wrap and a penetration seal.The second cable (12550A-SA), which provides the supply power for the"B" EDG Fuel Oil Transfer Pump, was separated by 20 feet horizontally, but no suppression/detection system was provided in its location, nor was a 3-hour barrier provided.Approximately 80 feet of conduit for this cable will require additional protection. | | Mr. L. A. Reyes (NRC Regional Administrator, Region II) |
| This will be accomplished by sealing a wall to provide a 3 hour barrier.CAUSE: These design deficiencies were caused by engineering oversight and inadequate design verification during initial plant construction.
| | Mr. V. L. Rooney (NRC - NRR Project Manager) 9709180097 970912 lllllilI5lllllllElllllllllllllllllll PDR ADGCK 05000400 8 PDR State Road 1134 New Hill NC |
| | |
| | NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB No. 3160-0104 (495) EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THS MANDATORY D(FORMATION COLLECTION REOUESR QN HRS. REPORTED LESSONS LEARNED ARE LICENSEE EVENT REPORT (LER) BICORPORATEO UITO THE UCENQNG PROCESS ANO FEO BACK TO INDUSTRY. |
| | FORWARD COMMENTS REGARDB(G BURDEN ESTIMATE TO THE INFORMATION ANO RECORDS MANAGEMENT BRANCH IT4 F33l, US. NUCLEAR REGULATORY COMMISIOH, (See reverse for required number of WASHINGTOIL OC 20555000), ANO TO THE PAPERWORK REDUCTION PROJECT (3)50. |
| | digits/characters for each block) OIO(L OFF)CE OF MANAGEMEHT AND BUDGET, WASHBIGTOH, OC 20503. |
| | FACIUTY NAME Ill DOCKET NUMBER (2) PAOE (3) |
| | Harris Nuclear Plant Unit-1 50-400 1 OF3 TITLE (4) |
| | Inadequate fire protection provided for safety-related EDG Fuel Oil Transfer Pump cables resulting in operation outside design basis. |
| | EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8) |
| | FACIUTY NAME OOCKET NUMBER SEQUENTIAl REVIIDN MONTH DAY YEAR YEAR MONTH DAY NUMBER NUMBER FACIUTY NAME DOCKET NUMBER 14 97 97 020 00 97 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR B: (Check one or morel (11) |
| | MODE (9) 20.2201(b) 20.2203(a) (2) (v) 50.73(a)(2)(i) 50.73(a)(2) (viii) |
| | POWER 20.2203(a)(l ) 20.2203(a)(3) (i) 50.73(a) (2) (ii) 50.73(a)(2)(x) |
| | LEVEL (10) 1005G 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a) (2)(iii) 73.71 20.2203(a) (2)(ii) 20.2203(a) (4) 50.73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50.73(a)(2) (v) Specify In Abstract belo W or in NRC Form 306A 20.2203(a) (2) (iv) 50.36(c) (2) 50.73(a)(2) (vii) |
| | LICENSEE CONTACT FOR THIS LER (12) kAME TELEP)(ONE NUMBER Urcrude Ares Code) |
| | Michael Verrilli Sr. Analyst - Licensing (919) 362-2303 |
| | 'COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| | REPORTABLE REPORTABIE CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER TO NPRDS TD NPRDS SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED YES SUBMISSION (lf yes, complete EXPECTED SUBMISSION DATE). X NO DATE (16) |
| | ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single. spaced typewritten lines) (16) |
| | On August 14, 1997, with the plant at approximately 100% power in mode 1, design discrepancies were identified during an Engineering review of the Safe Shutdown Analysis in Case of Fire. These discrepancies pertain to safety-related Emergency Diesel Generator Fuel Oil Transfer pump electrical cables. These cables are required for safe shutdown in case of a fire, but were not adequately protected. Specifically, section 9.5.1 of the Harris Plant Final Safety Analysis Report (FSAR) provides separation requirements for redundant safe shutdown divisions to maintain safe shutdown capability. |
| | During the Engineering review, Cables 12549E-SA and 12550A-SB, located in the 261'levation of the Reactor Auxiliary Building were found to not meet the specific design requirements. The first cable (12549E-SA) was in an area that had automatic fire detection/suppression systems, but was not separated by a 3-hour fire barrier or 20 feet of horizontal distance and was not enclosed in a 1-hr rated barrier. The second cable (12550A-SA) was separated by 20 feet horizontally, but no suppression/detection system was provided in its location, nor was a 3-hour barrier provided. |
| | These design deficiencies were caused by engineering oversight and inadequate design verification during initial plant construction. |
| | Immediate corrective actions included establishing fire watches for the areas with unprotected cables. A plant modification will be developed and installed to provide the required protection. |
| | |
| | US. NUCEEAR RECUIATORZ COMMISSION NRC FORM 3SSA I4.85l LICENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION FACIUTZ NAME (I) OOCKET IER NUMBER ISI PACE Ql SEOUENTIAl. REZISION NUMBER NUMBER Shearon Harris Nuclear Plant ~ Unit rII1 50400 2 OF 3 07 - 020 - 00 TEXT pl sssdr sptssis sssisisd. dss sdStknd soidss ol A'RC Fam 3SQI ill) |
| | EVENT DESCRIPTION: |
| | On August 14, 1997, with the plant at approximately 100% power in mode 1, design discrepancies were identified during an Engineering review of the Safe Shutdown Analysis in Case of Fire performed per Engineering Service Request (ESR9500433). These discrepancies pertain to safety-related "A" and "B" Emergency Diesel Generator Fuel Oil Transfer pump electrical cables. These electrical cables are required for safe shutdown in case of a fire, but were not adequately protected. Specifically, section 9.5.1 of the Harris Plant Final Safety Analysis Report (FSAR) provides separation requirements for redundant safe shutdown divisions to maintain safe shutdown capability. FSAR section 9.5.1 requires protection of cables outside containment by one of the following methods such that at least one division of redundant safe shutdown cables located within the same fire area are protected from fire damage: |
| | (1) Separation of cables and equipment and associated circuits of redundant safe shutdown divisions by a fire barrier having a 3-hour rating or equivalent. Structural steel forming a part of or supporting such fire barriers is protected to provide resistance equivalent to that required of the barrier. |
| | (2) Separation of cables and equipment and associated circuits of redundant safe shutdown divisions by a horizontal distance of more than 20 feet with no intervening combustible or fire hazards. In addition, fire detectors and an automatic suppression system is installed in the area. |
| | (3) Enclosure of cable and equipment and associated circuits of one redundant train in a fire barrier having a 1-hour rating. In addition, fire detectors and an automatic fire suppression system are installed in the fire area. |
| | During the ESR-9500433 Engineering review, Cables 12549E-SA and 12550A-SB, located in the 261'levation of the Reactor Auxiliary Building were found to not meet the above requirements. The first cable (12549E-SA), which provides control power for the "A" EDG Fuel Oil Transfer Pump, was in an area that had automatic fire detection/suppression systems, but was not separated by a 3-hour'fire barrier or 20 feet of horizontal distance and was not enclosed in a 1-hr rated barrier. Approximately 50 feet of conduit for this cable will require additional protection. |
| | This will involve installation of a one hour fire wrap and a penetration seal. The second cable (12550A-SA), which provides the supply power for the "B" EDG Fuel Oil Transfer Pump, was separated by 20 feet horizontally, but no suppression/detection system was provided in its location, nor was a 3-hour barrier provided. Approximately 80 feet of conduit for this cable will require additional protection. This will be accomplished by sealing a wall to provide a 3 hour barrier. |
| | CAUSE: |
| | These design deficiencies were caused by engineering oversight and inadequate design verification during initial plant construction. |
| SAFETY SIGNIFICANCE: | | SAFETY SIGNIFICANCE: |
| There were no actual safety consequences resulting from these deficiencies. | | There were no actual safety consequences resulting from these deficiencies. Had a fire occurred in either of the plant locations containing the unprotected cables, it is conceivable that the Fuel Oil Transfer pump and opposite train EDG could be rendered inoperable and when the day tank on the remaining EDG emptied in approximately 6 hours, both EDGs would be unavailable. This could impair the ability to maintain hot standby and negate the capability to reach cold shutdown. This scenario would only be of consequence if off-site power was also lost during the fire event, thereby requiring operation of the EDGs. The above scenario also takes no credit for the actions of the fire brigade or the fire suppression system to mitigate the extent of fire damage. Considering the defense-in-depth approach to fire protection at the Harris Plant (prevention, detection, suppression, spatial separation, fire fighting capability etc.) the |
| Had a fire occurred in either of the plant locations containing the unprotected cables, it is conceivable that the Fuel Oil Transfer pump and opposite train EDG could be rendered inoperable and when the day tank on the remaining EDG emptied in approximately 6 hours, both EDGs would be unavailable. | | |
| This could impair the ability to maintain hot standby and negate the capability to reach cold shutdown.This scenario would only be of consequence if off-site power was also lost during the fire event, thereby requiring operation of the EDGs.The above scenario also takes no credit for the actions of the fire brigade or the fire suppression system to mitigate the extent of fire damage.Considering the defense-in-depth approach to fire protection at the Harris Plant (prevention, detection, suppression, spatial separation, fire fighting capability etc.)the NRC FORM 366A H.BQ LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U rr.NUCLEAR REGULATORT COMMISSION FACILITT NAME II)Shearon Harris Nuclear Plant~Unit 41 TENT RY rrrvrv srsvsv N rcpvhd, vsv vrsrrir'orrvl sssrrBs oMRc Form SrrarU i1 Tl DOCKET 50100 LER NUMBER I6I TEAR SEGUENTIAL REVISION NUMBER NUMBER 97-020-00 PAGE gr 3 OF 3 SAFETY SIGNIFICANCE: (continued) probability of the assumed worst case fire occurring and simultaneously losing off-site power is extremely low.This condition is being reported per 10CFR50.73.a.2.ii as a condition outside the design basis of the plant.PREVIOUS SIMILAR EVENTS: LER f97-06 was submitted on April, 17, 1997 and reported deficiencies in a Thermo-Lag fire barrier wall which resulted in the plant operating outside the design basis.However, the scope and corrective actions for LER f97-06 were specific to the Thermo-Lag barriers within the plant and would not be expected to identify or prevent the deficiencies identified in this LER.CORRECTIVE ACTIONS COMPLETED: | | NRC FORM 366A U rr. NUCLEAR REGULATORT COMMISSION H.BQ LICENSEE EVENT REPORT (LER) |
| Immediate corrective actions included establishing fire watches for the areas with unprotected cables.This was completed on the day the deficiencies were identified, August 14, 1997.CORRECTIVE ACTIONS PLANNED: A plant modification will be developed and installed to provide the required protection for the cited cables.This will be completed by November 15, 1997.}} | | TEXT CONTINUATION FACILITT NAME II) DOCKET LER NUMBER I6I PAGE gr SEGUENTIAL REVISION TEAR NUMBER NUMBER Shearon Harris Nuclear Plant ~ |
| | Unit 41 50100 3 OF 3 97 - 020 - 00 TENT RY rrrvrv srsvsv N rcpvhd, vsv vrsrrir'orrvl sssrrBs oMRc Form SrrarU i1 Tl SAFETY SIGNIFICANCE: (continued) probability of the assumed worst case fire occurring and simultaneously losing off-site power is extremely low. |
| | This condition is being reported per 10CFR50.73.a.2.ii as a condition outside the design basis of the plant. |
| | PREVIOUS SIMILAREVENTS: |
| | LER f97-06 was submitted on April, 17, 1997 and reported deficiencies in a Thermo-Lag fire barrier wall which resulted in the plant operating outside the design basis. However, the scope and corrective actions for LER f97-06 were specific to the Thermo-Lag barriers within the plant and would not be expected to identify or prevent the deficiencies identified in this LER. |
| | CORRECTIVE ACTIONS COMPLETED: |
| | Immediate corrective actions included establishing fire watches for the areas with unprotected cables. This was completed on the day the deficiencies were identified, August 14, 1997. |
| | CORRECTIVE ACTIONS PLANNED: |
| | A plant modification will be developed and installed to provide the required protection for the cited cables. This will be completed by November 15, 1997.}} |
|
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:RO)
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A9151999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Shearon Harris Npp. with 991012 Ltr ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18017A8621999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Harris Nuclear Plant.With 990908 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18017A8361999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Shearon Harris Nuclear Power Plant.With 990811 Ltr ML18016B0151999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Shearon Harris Npp. with 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990614 Ltr ML18017A8981999-05-12012 May 1999 Technical Rept Entitled, Harris Nuclear Plant-Bacteria Detection in Water from C&D Spent Fuel Pool Cooling Lines. ML18016A9581999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990513 Ltr ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8941999-04-0505 April 1999 Revised Pages 20-25 to App 4A of non-proprietary Version of Rev 3 to HI-971760 ML18016A9101999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Shearon Harris Nuclear Power Plant.With 990413 Ltr ML18016A8661999-03-31031 March 1999 Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept. ML18017A8931999-02-28028 February 1999 Risks & Alternative Options Associated with Spent Fuel Storage at Shearon Harris Nuclear Power Plant. ML18016A8551999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Shearon Harris Npp. with 990312 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8531999-02-18018 February 1999 Non-proprietary Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFP 'C' & 'D'. ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18022B0631999-02-0404 February 1999 Rev 0 to Nuclear NDE Manual. with 28 Oversize Uncodable Drawings of Alternative Plan Scope & 4 Oversize Codable Drawings ML20202J1161999-02-0101 February 1999 SER Accepting Relief Requests Associated with Second 10-year Interval Inservice Testing Program ML18016A8041999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Shearon Harris Nuclear Power Plant.With 990211 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7801998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Shearon Harris Npp. with 990113 Ltr ML18016A7671998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Shnpp,Unit 1.With 981215 Ltr ML18016A9731998-11-28028 November 1998 Changes,Tests & Experiments, for Harris Nuclear Plant.Rept Provides Brief Description of Changes to Facility & Summary & of SE for Each Item That Was Implemented Under 10CFR50.59 Between 970608-981128.With 990527 Ltr ML18016A8351998-11-28028 November 1998 ISI Summary 8th Refueling Outage for Shearon Harris Power Plant,Unit 1. ML18016A7411998-11-25025 November 1998 Rev 1 to Shnpp Cycle 9 Colr. ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A7071998-11-0303 November 1998 Rev 0 to Harris Unit 1 Cycle 9 Colr. ML18016A7201998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Shearon Harris Nuclear Power Plant.With 981113 Ltr ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves ML18016A6201998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Harris Nuclear Power Plant.With 981012 Ltr ML18016A5971998-09-21021 September 1998 Rev 1 to Harris Unit 1 Cycle 8 Colr. ML18016A5881998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Shnpp,Unit 1.With 980914 Ltr ML18016A5071998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Shearon Harris Nuclear Plant.W/980811 Ltr ML18016A9431998-07-0707 July 1998 Rev 1 to QAP Manual. ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A9371998-06-30030 June 1998 Technical Rept on Matl Identification of Spent Fuel Piping Welds at Hnp. ML18016A4861998-06-30030 June 1998 Monthly Operating Rept for June 1998 for SHNPP.W/980715 Ltr ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18016A4521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Shearon Harris Nuclear Power Plant.W/980612 Ltr ML18016A7711998-05-26026 May 1998 Non-proprietary Rev 2 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris Spent Fuel Pools 'C' & 'D'. 1999-09-30
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CATEGORY I REGUIATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9709180097 DOC.DATE: 97/09/12 NOTARIZED: NO DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH. NAME . AUTHOR AFFILIATION VERRILLII M. Carolina Power 6 Light Co.
DONAHUE,J.W. Carolina Power a Light Co.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 97-020-00:on 970814,inadequate fire protection provided for safety-related EDG fuel oil transfer pump cables caused operation outside design basis,was identified. Caused by engineering oversight. Established fire watches.W/970912 ltr. A DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
E NOTES:Application for permit renewal filed. 05000400 RECIPIENT COPIES RECIPIENT COPIES 0 ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-1 PD 1 1 ROONEYiV 1 1 INTERNAL: ACRS 1 1 2 2 AEOD/SPD/RRAB 1 1 CE 1 1 NRR/DE/ECGB 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DET/EIB 1 1 RGN2 FILE 01 1 1 D EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCEiJ H 1 1 0 NOAC POOREgW. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 C N
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25
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Carolina Power & Light Company Harris Nuclear Plant PO Box 165 New Hill NC 27562 SEP 12 1997 U.S. Nuclear Regulatory Commission Serial: HNP-97-174 ATTN: NRC Document Control Desk 10CFR50.73 Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 97-020-00 Sir or Madam:
In accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted. This report describes a design deficiency related to inadequate fire protection for safety-related cables.
Sincerely, J. W. Donahue Director of Site Operations Harris Plant MV Enclosure c: Mr. J. B, Brady (HNP Senior NRC Resident)
Mr. L. A. Reyes (NRC Regional Administrator, Region II)
Mr. V. L. Rooney (NRC - NRR Project Manager) 9709180097 970912 lllllilI5lllllllElllllllllllllllllll PDR ADGCK 05000400 8 PDR State Road 1134 New Hill NC
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB No. 3160-0104 (495) EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THS MANDATORY D(FORMATION COLLECTION REOUESR QN HRS. REPORTED LESSONS LEARNED ARE LICENSEE EVENT REPORT (LER) BICORPORATEO UITO THE UCENQNG PROCESS ANO FEO BACK TO INDUSTRY.
FORWARD COMMENTS REGARDB(G BURDEN ESTIMATE TO THE INFORMATION ANO RECORDS MANAGEMENT BRANCH IT4 F33l, US. NUCLEAR REGULATORY COMMISIOH, (See reverse for required number of WASHINGTOIL OC 20555000), ANO TO THE PAPERWORK REDUCTION PROJECT (3)50.
digits/characters for each block) OIO(L OFF)CE OF MANAGEMEHT AND BUDGET, WASHBIGTOH, OC 20503.
FACIUTY NAME Ill DOCKET NUMBER (2) PAOE (3)
Harris Nuclear Plant Unit-1 50-400 1 OF3 TITLE (4)
Inadequate fire protection provided for safety-related EDG Fuel Oil Transfer Pump cables resulting in operation outside design basis.
EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
FACIUTY NAME OOCKET NUMBER SEQUENTIAl REVIIDN MONTH DAY YEAR YEAR MONTH DAY NUMBER NUMBER FACIUTY NAME DOCKET NUMBER 14 97 97 020 00 97 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR B: (Check one or morel (11)
MODE (9) 20.2201(b) 20.2203(a) (2) (v) 50.73(a)(2)(i) 50.73(a)(2) (viii)
POWER 20.2203(a)(l ) 20.2203(a)(3) (i) 50.73(a) (2) (ii) 50.73(a)(2)(x)
LEVEL (10) 1005G 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a) (2)(iii) 73.71 20.2203(a) (2)(ii) 20.2203(a) (4) 50.73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) 50.73(a)(2) (v) Specify In Abstract belo W or in NRC Form 306A 20.2203(a) (2) (iv) 50.36(c) (2) 50.73(a)(2) (vii)
LICENSEE CONTACT FOR THIS LER (12) kAME TELEP)(ONE NUMBER Urcrude Ares Code)
Michael Verrilli Sr. Analyst - Licensing (919) 362-2303
'COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
REPORTABLE REPORTABIE CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER TO NPRDS TD NPRDS SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED YES SUBMISSION (lf yes, complete EXPECTED SUBMISSION DATE). X NO DATE (16)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single. spaced typewritten lines) (16)
On August 14, 1997, with the plant at approximately 100% power in mode 1, design discrepancies were identified during an Engineering review of the Safe Shutdown Analysis in Case of Fire. These discrepancies pertain to safety-related Emergency Diesel Generator Fuel Oil Transfer pump electrical cables. These cables are required for safe shutdown in case of a fire, but were not adequately protected. Specifically, section 9.5.1 of the Harris Plant Final Safety Analysis Report (FSAR) provides separation requirements for redundant safe shutdown divisions to maintain safe shutdown capability.
During the Engineering review, Cables 12549E-SA and 12550A-SB, located in the 261'levation of the Reactor Auxiliary Building were found to not meet the specific design requirements. The first cable (12549E-SA) was in an area that had automatic fire detection/suppression systems, but was not separated by a 3-hour fire barrier or 20 feet of horizontal distance and was not enclosed in a 1-hr rated barrier. The second cable (12550A-SA) was separated by 20 feet horizontally, but no suppression/detection system was provided in its location, nor was a 3-hour barrier provided.
These design deficiencies were caused by engineering oversight and inadequate design verification during initial plant construction.
Immediate corrective actions included establishing fire watches for the areas with unprotected cables. A plant modification will be developed and installed to provide the required protection.
US. NUCEEAR RECUIATORZ COMMISSION NRC FORM 3SSA I4.85l LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACIUTZ NAME (I) OOCKET IER NUMBER ISI PACE Ql SEOUENTIAl. REZISION NUMBER NUMBER Shearon Harris Nuclear Plant ~ Unit rII1 50400 2 OF 3 07 - 020 - 00 TEXT pl sssdr sptssis sssisisd. dss sdStknd soidss ol A'RC Fam 3SQI ill)
EVENT DESCRIPTION:
On August 14, 1997, with the plant at approximately 100% power in mode 1, design discrepancies were identified during an Engineering review of the Safe Shutdown Analysis in Case of Fire performed per Engineering Service Request (ESR9500433). These discrepancies pertain to safety-related "A" and "B" Emergency Diesel Generator Fuel Oil Transfer pump electrical cables. These electrical cables are required for safe shutdown in case of a fire, but were not adequately protected. Specifically, section 9.5.1 of the Harris Plant Final Safety Analysis Report (FSAR) provides separation requirements for redundant safe shutdown divisions to maintain safe shutdown capability. FSAR section 9.5.1 requires protection of cables outside containment by one of the following methods such that at least one division of redundant safe shutdown cables located within the same fire area are protected from fire damage:
(1) Separation of cables and equipment and associated circuits of redundant safe shutdown divisions by a fire barrier having a 3-hour rating or equivalent. Structural steel forming a part of or supporting such fire barriers is protected to provide resistance equivalent to that required of the barrier.
(2) Separation of cables and equipment and associated circuits of redundant safe shutdown divisions by a horizontal distance of more than 20 feet with no intervening combustible or fire hazards. In addition, fire detectors and an automatic suppression system is installed in the area.
(3) Enclosure of cable and equipment and associated circuits of one redundant train in a fire barrier having a 1-hour rating. In addition, fire detectors and an automatic fire suppression system are installed in the fire area.
During the ESR-9500433 Engineering review, Cables 12549E-SA and 12550A-SB, located in the 261'levation of the Reactor Auxiliary Building were found to not meet the above requirements. The first cable (12549E-SA), which provides control power for the "A" EDG Fuel Oil Transfer Pump, was in an area that had automatic fire detection/suppression systems, but was not separated by a 3-hour'fire barrier or 20 feet of horizontal distance and was not enclosed in a 1-hr rated barrier. Approximately 50 feet of conduit for this cable will require additional protection.
This will involve installation of a one hour fire wrap and a penetration seal. The second cable (12550A-SA), which provides the supply power for the "B" EDG Fuel Oil Transfer Pump, was separated by 20 feet horizontally, but no suppression/detection system was provided in its location, nor was a 3-hour barrier provided. Approximately 80 feet of conduit for this cable will require additional protection. This will be accomplished by sealing a wall to provide a 3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> barrier.
CAUSE:
These design deficiencies were caused by engineering oversight and inadequate design verification during initial plant construction.
SAFETY SIGNIFICANCE:
There were no actual safety consequences resulting from these deficiencies. Had a fire occurred in either of the plant locations containing the unprotected cables, it is conceivable that the Fuel Oil Transfer pump and opposite train EDG could be rendered inoperable and when the day tank on the remaining EDG emptied in approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, both EDGs would be unavailable. This could impair the ability to maintain hot standby and negate the capability to reach cold shutdown. This scenario would only be of consequence if off-site power was also lost during the fire event, thereby requiring operation of the EDGs. The above scenario also takes no credit for the actions of the fire brigade or the fire suppression system to mitigate the extent of fire damage. Considering the defense-in-depth approach to fire protection at the Harris Plant (prevention, detection, suppression, spatial separation, fire fighting capability etc.) the
NRC FORM 366A U rr. NUCLEAR REGULATORT COMMISSION H.BQ LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITT NAME II) DOCKET LER NUMBER I6I PAGE gr SEGUENTIAL REVISION TEAR NUMBER NUMBER Shearon Harris Nuclear Plant ~
Unit 41 50100 3 OF 3 97 - 020 - 00 TENT RY rrrvrv srsvsv N rcpvhd, vsv vrsrrir'orrvl sssrrBs oMRc Form SrrarU i1 Tl SAFETY SIGNIFICANCE: (continued) probability of the assumed worst case fire occurring and simultaneously losing off-site power is extremely low.
This condition is being reported per 10CFR50.73.a.2.ii as a condition outside the design basis of the plant.
PREVIOUS SIMILAREVENTS:
LER f97-06 was submitted on April, 17, 1997 and reported deficiencies in a Thermo-Lag fire barrier wall which resulted in the plant operating outside the design basis. However, the scope and corrective actions for LER f97-06 were specific to the Thermo-Lag barriers within the plant and would not be expected to identify or prevent the deficiencies identified in this LER.
CORRECTIVE ACTIONS COMPLETED:
Immediate corrective actions included establishing fire watches for the areas with unprotected cables. This was completed on the day the deficiencies were identified, August 14, 1997.
CORRECTIVE ACTIONS PLANNED:
A plant modification will be developed and installed to provide the required protection for the cited cables. This will be completed by November 15, 1997.