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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE RD. SUITE 210 LISLE, IL  60532-4352  June 20, 2014   
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE RD. SUITE 210 LISLE, IL  60532-4352  
  June 20, 2014  
    
Mr. Anthony Vitale  
Mr. Anthony Vitale  
Vice President, Operations Entergy Nuclear Operations, Inc. Palisades Nuclear Plant  
Vice President, Operations Entergy Nuclear Operations, Inc. Palisades Nuclear Plant  
27780 Blue Star Memorial Highway  
27780 Blue Star Memorial Highway  
Covert, MI  49043-9530  
Covert, MI  49043-9530  
SUBJECT:  PALISADES NUCLEAR PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000255/2014007
   
   
SUBJECT:  PALISADES NUCLEAR PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000255/2014007 
Dear Mr. Vitale:  
Dear Mr. Vitale:  
   
   
On June 11, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution Inspection at your Palisades Nuclear Plant.  The enclosed inspection report documents the inspection results, which were discussed at an interim exit meeting on May 23, 2014, and a final exit meeting on June 11, 2014, with you and other  
On June 11, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution Inspection at your Palisades Nuclear Plant.  The enclosed inspection report documents the inspection results, which were discussed at an interim exit meeting on May 23, 2014, and a final exit meeting on June 11, 2014, with you and other  
members of your staff.  The inspection examined activities conducted under your license as they related to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.   
members of your staff.  The inspection examined activities conducted under your license as they related to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.   
   
   
On the basis of the samples selected for review, the inspectors concluded that the Corrective  
On the basis of the samples selected for review, the inspectors concluded that the Corrective  
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significance of the issues was screened using risk insights and the significance drove the  
significance of the issues was screened using risk insights and the significance drove the  
prioritization of issue evaluation and resolution.  Evaluations were adequate, overall, in  
prioritization of issue evaluation and resolution.  Evaluations were adequate, overall, in  
determining the underlying cause of the issues and corrective actions were generally implemented in a timely manner, commensurate with their safety significance.  Operating experience was evaluated and entered into the Corrective Action Program, if applicable.  The use of operating experience was integrated into daily activities and found to be effective in  
determining the underlying cause of the issues and corrective actions were generally implemented in a timely manner, commensurate wi
th their safety significance.  Operating experience was evaluated and entered into the Corrective Action Program, if applicable.  The use of operating experience was integrated into daily activities and found to be effective in  
preventing similar issues at the plant.  In addition, self-assessments, audits, and effectiveness reviews were found to be conducted at a sufficient depth for all departments.  The assessments  
preventing similar issues at the plant.  In addition, self-assessments, audits, and effectiveness reviews were found to be conducted at a sufficient depth for all departments.  The assessments  
reviewed were thorough and effective in identifying site performance deficiencies, programmatic concerns, and improvement opportunities.  Based on the results of the interviews conducted, the inspectors did not identify any impediment to the establishment of a safety conscious work environment (SCWE) at Palisades Nuclear Plant with the exception of the Security Department.  Licensee staff was aware of and generally familiar with the Corrective Action Program and other station processes, including the Employee Concerns Program, through which concerns could be raised.  The staff was also comfortable raising concerns without fear of retaliation.   
reviewed were thorough and effective in identifying site performance deficiencies, programmatic concerns, and improvement opportunities.  Based on the results of the interviews conducted, the inspectors did not identify any impediment to the establishment of a safety conscious work environment (SCWE) at Palisades Nuclear Plant with the exception of the Security Department.  Licensee staff was aware of and generally familiar with the Corrective Action Program and other station processes, including the Employee Concerns Program, through which concerns could be raised.  The staff was also comfortable raising concerns without fear of retaliation.  
   A. Vitale -2-   
    
As discussed in NRC Inspection Report 05000255/2014009, dated March 6, 2014, the NRC performed a limited scope Problem Identification and Resolution inspection that identified a chilled work environment within the Security Department.  In particular, the NRC concluded that staff within the Security Department perceived that:  (1) recent actions to terminate the  
   A. Vitale -2-  
   
As discussed in NRC Inspection Report 05000255/2014009, dated March 6, 2014, the NRC performed a limited scope Problem Identification and Resolution inspection that identified a chilled work environment within the Security D
epartment.  In particular, the NRC concluded that staff within the Security Department perceived that:  (1) recent actions to terminate the  
employment of two supervisors was in retaliation for their raised concerns; (2) the Corrective Action Program was ineffective at addressing equipment and other concerns raised by the  
employment of two supervisors was in retaliation for their raised concerns; (2) the Corrective Action Program was ineffective at addressing equipment and other concerns raised by the  
Security staff; (3) Security management was unresponsive to employees' concerns; and (4) the Employee Concerns Program could not be relied upon to maintain employee confidentiality.   
Security staff; (3) Security management was unresponsive to employees' concerns; and (4) the Employee Concerns Program could not be relied upon to maintain employee confidentiality.  
   
In response to our identification of a chilled work environment within the Security Department,  
In response to our identification of a chilled work environment within the Security Department,  
you developed the Palisades Security SCWE Action Plan and the NRC planned to review the effectiveness of actions taken to implement the Action Plan.  During this inspection, we reviewed your implementation of the Palisades Security SCWE  
you developed the Palisades Security SCWE Action Plan and the NRC planned to review the effectiveness of actions taken to implement the Action Plan.  
  During this inspection, we reviewed your implementation of the Palisades Security SCWE  
Action Plan and verified that, to date, you have completed all of the actions as committed to in  
Action Plan and verified that, to date, you have completed all of the actions as committed to in  
the Action Plan.  However, we concluded that the quality of the actions implemented have been  
the Action Plan.  However, we concluded that the quality of the actions implemented have been  
insufficient to assess and understand the cause of the chilled work environment within the Security Department and did not demonstrate a strong commitment to effectively improve the safety conscious work environment in the Security Department.  Specifically, significant gaps were found to exist in the security officers' knowledge of the actions being taken to address the  
insufficient to assess and understand the cause of the chilled work environment within the Security Department and did not demonstrate a strong commitment to effectively improve the safety conscious work environment in the Security Department.  Specif
ically, significant gaps were found to exist in the security officers' knowledge of the actions being taken to address the  
chilled safety conscious work environment and management's commitment to improving the overall safety conscious work environment.   
chilled safety conscious work environment and management's commitment to improving the overall safety conscious work environment.   
  For example, security officers had a limited recollection of any discussion of the results of the NRC's limited scope Problem Identification and Resolution inspection, and security officers  
  For example, security officers had a limited recollection of any discussion of the results of the NRC's limited scope Problem Identification and Resolution inspection, and security officers  
stated that they were not informed of the site's development and implementation of a Security  
stated that they were not informed of the site's development and implementation of a Security  
SCWE Action Plan or the specific actions required by the Action Plan.  Also, the security officers were unaware of the establishment of the site's Security Ombudsman Program as directed in the Action Plan; the intent of the program; or their shift representatives for the Program, despite the selection and assignment of personnel to these positions at the end of March 2014.  Lastly,  
SCWE Action Plan or the specific actions required by the Action Plan.  Also, the security officers were unaware of the establishment of the site's Security Ombudsman Program as directed in the Action Plan; the intent of the program; or their shift representatives for the Program, despite the selection and assignment of personnel to these positions at the end of March 2014.  Lastly,  
the security officers were unaware of a significant organizational change that added the  
the security officers were unaware of a significant organizational change that added the  
Regulatory and Performance Improvement Director to the Security Department chain of  
Regulatory and Performance Improvement Director to the Security Department chain of  
command.  
command.  
  Therefore, we are requesting that you provide a response to us, within 30 days of your receipt of this letter, that outlines actions that you have taken or plan to take to further enhance your  
  Therefore, we are requesting that you provide a response to us, within 30 days of your receipt of this letter, that outlines actions that you have taken or plan to take to further enhance your  
Palisades Security SCWE Action Plan to improve the safety conscious work environment in the Security Department at Palisades.  The NRC will continue to closely monitor Security Department safety conscious work environment and any supplemental actions that you may choose to take with a follow-up inspection.   
Palisades Security SCWE Action Plan to improve  
the safety conscious work environment in the Security Department at Palisades.  The NRC will  
continue to closely monitor Security Department safety conscious work environment and any supplemental actions that you may choose to take with a follow-up inspection.  
   
We plan to discuss with you the results of our safety conscious work environment inspections  
We plan to discuss with you the results of our safety conscious work environment inspections  
during the upcoming End-of-Cycle assessment public meeting.  The NRC requests that you be prepared to discuss:  (1) the root cause of the chilled work environment within the Security  
 
Department; (2) your progress in addressing the safety conscious work environment concerns within the Security Department; and (3) any additional actions planned and/or implemented to address the safety conscious work environment at Palisades, including actions as a result of our  
during the upcoming End-of-Cycle assessment  
public meeting.  The NRC requests that you be prepared to discuss:  (1) the root cause of the chilled work environment within the Security  
Department; (2) your progress in addressing the safety conscious work environment concerns  
within the Security Department; and (3) any additional actions planned and/or implemented to address the safety conscious work environment at Palisades, including actions as a result of our  
observations during this Problem Identification and Resolution inspection.  
observations during this Problem Identification and Resolution inspection.  
    
    
   A. Vitale -3-   
   A. Vitale -3-  
   
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the  
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the  
NRC's Agencywide Documents Access and Management System (ADAMS).  ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).   
NRC's Agencywide Documents Access and Managem
   Sincerely,  /RA/  Eric Duncan, Chief Branch 3 Division of Reactor Projects Docket No. 50-255 License No. DPR-20  
ent System (ADAMS).  ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html
(the Public Electronic Reading Room).   
 
   Sincerely,  
   /RA/  Eric Duncan, Chief  
Branch 3  
Division of Reactor Projects  
Docket No. 50-255 License No. DPR-20  
 
  Enclosure:  Inspection Report No. 05000255/2014007  
  Enclosure:  Inspection Report No. 05000255/2014007  
   w/Attachment:  Supplemental Information cc w/encl:  Distribution via LISTSERV  
   w/Attachment:  Supplemental Information cc w/encl:  Distribution via LISTSERV
 
  Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION III Docket No: 50-255 License No: DPR-20 Report No: 05000255/2014007  
  Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION III Docket No: 50-255 License No: DPR-20 Report No: 05000255/2014007  
Licensee: Entergy Nuclear Operations, Inc.  
Licensee: Entergy Nuclear Operations, Inc.  
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Dates: May 5, 2014, through June 11, 2014 Team Leader: R. Ng, Project Engineer Inspectors: A. Scarbeary, Resident Inspector  C. Zoia, License Examiner  
Dates: May 5, 2014, through June 11, 2014 Team Leader: R. Ng, Project Engineer Inspectors: A. Scarbeary, Resident Inspector  C. Zoia, License Examiner  
  E. Sanchez-Santiago, Reactor Inspector   
  E. Sanchez-Santiago, Reactor Inspector   
  G. Hansen, Physical Security Inspector     
  G. Hansen, Physical Security Inspector  
Approved by: E. Duncan, Chief Branch 3  
    
Division of Reactor Projects     
Approved by: E. Duncan, Chief  
Branch 3  
 
Division of Reactor Projects  
    
      
      
  2  SUMMARY OF FINDINGS Inspection Report 05000255/2014007; 05/05/2014 - 06/11/2014; Palisades Nuclear Plant; Problem Identification and Resolution.  This inspection was performed by four region-based inspectors and the Palisades Resident  
  2  SUMMARY OF FINDINGS Inspection Report 05000255/2014007; 05/05/2014 - 06/11/2014; Palisades Nuclear Plant; Problem Identification and Resolution.  
Inspector.  The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006. Problem Identification and Resolution On the basis of the samples selected for review, the inspectors concluded that the Corrective Action Program at Palisades Nuclear Plant was adequate in the areas of identifying, evaluating  
  This inspection was performed by four region-based inspectors and the Palisades Resident  
 
Inspector.  The NRC's program for overseeing t
he safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reac
tor Oversight Process," Revision 4, dated December 2006. Problem Identification and Resolution
On the basis of the samples selected for review, the inspectors concluded that the Corrective Action Program at Palisades Nuclear Plant was adequate in the areas of identifying, evaluating  
and correcting issues with some identified opportunities for improvement.  The licensee had a  
and correcting issues with some identified opportunities for improvement.  The licensee had a  
low threshold for identifying issues and entering them into the Corrective Action Program.  The  
low threshold for identifying issues and entering them into the Corrective Action Program.  The  
significance of the issues was screened using risk insights and the significance drove the prioritization of issue evaluation and resolution.  Evaluations were adequate, overall, in determining the underlying cause of the issues and corrective actions were generally  
significance of the issues was screened using risk insights and the significance drove the prioritization of issue evaluation and resolution.  Evaluations were adequate, overall, in determining the underlying cause of the issues and corrective actions were generally  
implemented in a timely manner, commensurate with their safety significance.  Operating experience was evaluated and entered into the Corrective Action Program, if applicable.  The  
implemented in a timely manner, commensurate wi
th their safety significance.  Operating experience was evaluated and entered into the Corrective Action Program, if applicable.  The  
use of operating experience was integrated into daily activities and found to be effective in preventing similar issues at the plant.  In addition, self-assessments, audits, and effectiveness reviews were found to be conducted at a sufficient depth for all departments.  The assessments  
use of operating experience was integrated into daily activities and found to be effective in preventing similar issues at the plant.  In addition, self-assessments, audits, and effectiveness reviews were found to be conducted at a sufficient depth for all departments.  The assessments  
reviewed were thorough and effective in identifying site performance deficiencies, programmatic  
reviewed were thorough and effective in identifying site performance deficiencies, programmatic  
concerns, and improvement opportunities.  Based on the results of the interviews conducted,  
concerns, and improvement opportunities.  Based on the results of the interviews conducted,  
the inspectors did not identify any impediment to the establishment of a safety conscious work environment (SCWE) at Palisades Nuclear Plant with the exception of the Security Department.  Licensee staff was aware of and generally familiar with the Corrective Action Program and other station processes, including the Employee Concerns Program, through which concerns could be raised.  The staff was also comfortable raising concerns without fear of retaliation.  
the inspectors did not identify any impediment to  
the establishment of a safety conscious work environment (SCWE) at Palisades Nuclear Plant with the exception of the Security Department.  Licensee staff was aware of and generally familiar with the Corrective Action Program and other station processes, including the Employee Concerns Program, through which concerns could be raised.  The staff was also comfortable raising concerns without fear of retaliation.  
 
   
   
Although implementation of the Corrective Action Program was determined to be adequate, the inspectors identified several issues that were either minor in nature and/or represented a potential weakness in the program.  
Although implementation of the Corrective Action Program was determined to be adequate, the inspectors identified several issues that were either minor in nature and/or represented a potential weakness in the program.  
   
   
The inspectors concluded that, to date, the site had completed all the actions as committed to in  
The inspectors concluded that, to date, the site had completed all the actions as committed to in  
the Security SCWE Action Plan.  However, the inspectors concluded that the quality of the  
the Security SCWE Action Plan.  However, the inspectors concluded that the quality of the  
actions implemented have been insufficient to assess and understand the cause of the chilled work environment within the Security Department and did not demonstrate a strong commitment to effectively improve the safety conscious work environment in the Security Department.  Specifically, significant gaps were found to exist in the security officers' knowledge of the actions being taken to address the chilled safety conscious work environment and  
actions implemented have been insufficient to assess and understand the cause of the chilled  
management's commitment to improving the overall safety conscious work environment.  Based on the information reviewed during this inspection, the inspectors concluded that the  
work environment within the Security Department and did not demonstrate a strong commitment to effectively improve the safety conscious work environment in the Security Department.  Specifically, significant gaps were found to exist in the security officers' knowledge of the actions being taken to address the chilled safety conscious work environment and  
management's commitment to improving the overall safety conscious work environment.  
  Based on the information reviewed during this inspection, the inspectors concluded that the  
control room structure continues to perform its intended safety function, and the installed  
control room structure continues to perform its intended safety function, and the installed  
modifications, if maintained, are adequate to prevent water intrusion into the control room.   
modifications, if maintained, are adequate to prevent water intrusion into the control room.   
Therefore, the inspectors determined that the licensee had fulfilled the Confirmatory Action  
Therefore, the inspectors determined that the licensee had fulfilled the Confirmatory Action  
Letter commitments to address the Safety Injection Refueling Water Tank (SIRWT) and Control Room concrete support structure leakage.     
Letter commitments to address the Safety Injection Refueling Water Tank (SIRWT) and Control Room concrete support structure leakage.     
  3  A. NRC-Identified and Self-Revealed Findings None.  B. Licensee-Identified Violations None.     
  3  A. NRC-Identified and Self-Revealed Findings
  4  REPORT DETAILS   4. OTHER ACTIVITIES  4OA2 Problem Identification and Resolution (71152B) This inspection constituted one biennial sample of Problem Identification and Resolution as defined by Inspection Procedure 71152, "Problem Identification and Resolution."   
  None.  B. Licensee-Identified Violations
Documents reviewed are listed in the Attachment to this report. .1 Assessment of the Corrective Action Program Effectiveness Inspection Scope The inspectors reviewed the procedures and processes that described the Corrective Action Program at Palisades Nuclear Plant to ensure, in part, that the requirements of  
None.     
  4  REPORT DETAILS
  4. OTHER ACTIVITIES  4OA2 Problem Identification and Resolution
(71152B) This inspection constituted one biennial sample of Problem Identification and Resolution as defined by Inspection Procedure 71152, "Problem Identification and Resolution."   
Documents reviewed are listed in the Attachment to this report. .1 Assessment of the Corrective Action Program Effectiveness
  Inspection Scope
The inspectors reviewed the procedures and processes that described the Corrective Action Program at Palisades Nuclear Plant to ensure, in part, that the requirements of  
10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," were met.  The inspectors  
10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," were met.  The inspectors  
observed and evaluated the effectiveness of meetings related to the Corrective Action Program, such as the Condition Report Prescreening meeting, the Condition Review Group meeting, and the Corrective Action Review Board meeting.  Selected licensee  
observed and evaluated the effectiveness of meetings related to the Corrective Action Program, such as the Condition Report Prescreening meeting, the Condition Review Group meeting, and the Corrective Action Review Board meeting.  Selected licensee  
personnel were interviewed to assess their understanding of and their involvement in the  
personnel were interviewed to assess their understanding of and their involvement in the  
Corrective Action Program. The inspectors reviewed selected condition reports across all seven Reactor Oversight Process cornerstones to determine if problems were being properly identified and entered into the licensee's Corrective Action Program.  The majority of the risk-informed samples of condition reports reviewed were issued since the last NRC biennial Problem Identification and Resolution inspection completed in February 2012.  The inspectors  
Corrective Action Program. The inspectors reviewed selected condition reports across all seven Reactor Oversight Process cornerstones to determine if problems were being properly identified and entered into the licensee's Corrective Action Program.  The majority of the risk-informed samples of condition reports reviewed were  
issued since the last NRC biennial Problem Identification and Resolution inspection completed in February 2012.  The inspectors  
also reviewed selected issues that were more than 5 years old. The inspectors assessed the licensee's characterization and evaluation of the issues and examined the assigned corrective actions.  This review encompassed the full range of safety significance and evaluation classes, including root cause evaluations, apparent  
also reviewed selected issues that were more than 5 years old. The inspectors assessed the licensee's characterization and evaluation of the issues and examined the assigned corrective actions.  This review encompassed the full range of safety significance and evaluation classes, including root cause evaluations, apparent  
cause evaluations, common cause evaluations, condition report responses, and human  
cause evaluations, common cause evaluations, condition report responses, and human  
performance error reviews.  The inspectors assessed the scope and depth of the  
performance error reviews.  The inspectors assessed the scope and depth of the  
licensee's evaluations.  For significant conditions adverse to quality, the inspectors evaluated the licensee's corrective actions to prevent recurrence and for less significant issues, the inspectors reviewed the corrective actions to determine if they were  
licensee's evaluations.  For significant conditions adverse to quality, the inspectors evaluated the licensee's corrective actions to prevent recurrence and for less significant issues, the inspectors reviewed the corrective actions to determine if they were  
implemented in a timely manner commensurate with their safety significance. The inspectors selected the Auxiliary Feedwater Actuation System and Reactor Protection System power supply components to review in detail over a 5 year period.  Both systems were safety-related and risk-significant Maintenance Rule (a)(1) systems with previously identified power supply component problems.  At the time of the inspection, the Reactor Protection System was in a Maintenance Rule (a)(1) status, and  
implemented in a timely manner commensurate with their safety significance. The inspectors selected the Auxiliary Feedwater Actuation System and Reactor Protection System power supply components to re
the Auxiliary Feedwater Actuation System had recently returned from a Maintenance Rule (a)(1) status to a Maintenance Rule (a)(2) status.  The primary purpose of this  
view in detail over a 5 year period.  Both systems were safety-related and risk-significant Maintenance Rule (a)(1) systems with previously identified power supply component problems.  At the time of the inspection, the Reactor Protection System was in a Maintenance Rule (a)(1) status, and  
 
the Auxiliary Feedwater Actuation System  
had recently returned from a Maintenance Rule (a)(1) status to a Maintenance Rule (a)(2) status.  The primary purpose of this  
review was to determine whether the licensee was properly monitoring and evaluating the performance of risk-significant systems.  The inspectors also assessed the licensee's implementation of various system monitoring programs and performed   
review was to determine whether the licensee was properly monitoring and evaluating the performance of risk-significant systems.  The inspectors also assessed the licensee's implementation of various system monitoring programs and performed   
  5  walkdowns, as needed, to verify the resolution of issues.  As part of this review, the inspectors interviewed the current and previous system engineers, reviewed a sample of system health reports, condition reports, operating experience, apparent cause evaluations, and root cause evaluations.  The inspectors also attended the Plant Health Committee Meeting to observe the process the licensee used for identifying, prioritizing, and resolving issues that challenged unit reliability.  The inspectors reviewed Corrective  
  5  walkdowns, as needed, to verify the resolution of issues.  As part of this review, the inspectors interviewed the current and prev
ious system engineers, reviewed a sample of system health reports, condition reports, operating experience, apparent cause evaluations, and root cause evaluations.  The inspectors also attended the Plant Health  
Committee Meeting to observe the process the licensee used for identifying, prioritizing, and resolving issues that challenged unit reliability.  The inspectors reviewed Corrective  
 
Action Program and work management system procedures that provided guidance for trending.  In addition, the inspectors walked down the Auxiliary Feedwater Actuation  
Action Program and work management system procedures that provided guidance for trending.  In addition, the inspectors walked down the Auxiliary Feedwater Actuation  
System panel area to visually inspect recent power supply-related maintenance and to verify that identified concerns were entered into the Corrective Action Program.  The inspectors examined the results of self-assessments of the Corrective Action Program completed during the review period.  The results of the self-assessments were  
System panel area to visually inspect recent power supply-related maintenance and to verify that identified concerns were entered into the Corrective Action Program.  The inspectors examined the results of self-assessments of the Corrective Action Program completed during the review period.  The results of the self-assessments were  
compared to self-revealed and NRC-identified findings.  The inspectors also reviewed  
compared to self-revealed and NRC-identified findings.  The inspectors also reviewed  
the corrective actions associated with previously identified non-cited violations and findings to determine whether the station properly evaluated and resolved those issues.  The inspectors performed walkdowns, as necessary, to verify the resolution of the  
the corrective actions associated with previously identified non-cited violations and findings to determine whether the station  
issues.  Assessment (1) Identification of Issues Based on the results of the inspection, the inspectors concluded that, overall, the station was effective in identifying issues at a low threshold and properly entering them into the Corrective Action Program.  The inspectors determined that problems were usually  
properly evaluated and resolved those issues.  The inspectors performed walkdowns, as necessary, to verify the resolution of the  
issues.  Assessment
(1) Identification of Issues
Based on the results of the inspection, the inspectors concluded that, overall, the station was effective in identifying issues at a low threshold and properly entering them into the Corrective Action Program.  The inspectors determined that problems were usually  
identified and captured in a complete and accurate manner in the Corrective Action  
identified and captured in a complete and accurate manner in the Corrective Action  
Program.  The station was appropriately screening issues from both NRC and industry operating experience at an appropriate level and entering them into the Corrective Action Program when the issues were applicable to the station.  The inspectors also noted that deficiencies were identified by external organizations, including the NRC, that had not been previously identified by licensee personnel.  These deficiencies were  
Program.  The station was appropriately screening issues from both NRC and industry operating experience at an appropriate level and entering them into the Corrective Action Program when the issues were applicable to the station.  The inspectors also noted that deficiencies were identified by external organizations, including the NRC, that had not been previously identified by licensee personnel.  These deficiencies were  
subsequently entered into the Corrective Action Program for resolution. The inspectors determined that the station was generally effective at trending low level issues to prevent more significant issues from developing.  The licensee also used the Corrective Action Program to document instances where previous corrective actions  
subsequently entered into the Corrective Action Program for resolution. The inspectors determined that the station was generally effective at trending low level issues to prevent more significant issues from developing.  The licensee also used the Corrective Action Program to document instances where previous corrective actions  
were ineffective or were inappropriately closed.  
were ineffective or were inappropriately closed.  
   
   
The inspectors concluded that power supply-related concerns were identified and  
The inspectors concluded that power supply-related concerns were identified and  
entered into the Corrective Action Program at a low threshold, and concerns were resolved in a timely manner commensurate with their safety significance.   (2) Prioritization and Evaluation of Issues
entered into the Corrective Action Program at a low threshold, and concerns were resolved in a timely manner commensurate with their safety significance.  
(2) Prioritization and Evaluation of Issues
 
Based on the results of the inspection, the inspectors concluded that the station was adequately prioritizing and evaluating issues commensurate with the safety significance of the identified issue, which included a consideration of risk.   
Based on the results of the inspection, the inspectors concluded that the station was adequately prioritizing and evaluating issues commensurate with the safety significance of the identified issue, which included a consideration of risk.   
   
   
The inspectors determined that the Condition Report Prescreening meeting, the  
The inspectors determined that the Condition Report Prescreening meeting, the  
Condition Review Group meeting, and the Corrective Action Review Board meeting were   
Condition Review Group meeting, and the Corrective Action Review Board meeting were   
  6  all generally thorough and maintained a high standard for evaluation quality.  Members of the Condition Review Group discussed selected issues in sufficient detail and  
  6  all generally thorough and maintained a high standard for evaluation quality.  Members of the Condition Review Group discussed selected issues in sufficient detail and  
challenged the responsible department representatives regarding their conclusions and recommendations.  
challenged the responsible department representatives regarding their conclusions and recommendations.  
The inspectors performed a detailed review of issues related to the Reactor Protection  
The inspectors performed a detailed review of issues related to the Reactor Protection  
System and Auxiliary Feedwater Actuation System power supplies over roughly the  past 5 years.  The inspectors concluded that the evaluation of design issues, along with  
System and Auxiliary Feedwater Actuation System power supplies over roughly the  past 5 years.  The inspectors concluded that the evaluation of design issues, along with  
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implemented in a timely manner commensurate with the safety significance of the issues.  The inspectors noted that the licensee generally exhibited no reluctance in  
implemented in a timely manner commensurate with the safety significance of the issues.  The inspectors noted that the licensee generally exhibited no reluctance in  
placing structures, systems, and components into a Maintenance Rule (a)(1) status.  Appropriate corrective actions to address identified maintenance deficiencies were prescribed and completed.  A detailed review of the structures, systems, and  
placing structures, systems, and components into a Maintenance Rule (a)(1) status.  Appropriate corrective actions to address identified maintenance deficiencies were prescribed and completed.  A detailed review of the structures, systems, and  
components performance generally occurred before returning such structures, systems, and components to a Maintenance Rule (a)(2) status.    The inspectors determined that the licensee typically evaluated equipment functionality requirements adequately after a degraded or non-conforming condition was identified.   
components performance generally occurred before returning such structures, systems, and components to a Maintenance Rule (a)(2) status.    The inspectors determined that the licensee  
Overall, appropriate actions were assigned to correct the degraded or non-conforming condition.   
typically evaluated equipment functionality requirements adequately after a degraded or non-conforming condition was identified.   
Vulnerabilities in Condition Evaluations
Overall, appropriate actions were assigned to correct the degraded or non-conforming condition.  
   
Vulnerabilities in Condition Evaluations
 
The inspectors identified several instances in which the licensee's evaluation lacked  
The inspectors identified several instances in which the licensee's evaluation lacked  
sufficient quality to address the condition such that a technically competent reviewer could understand how the corrective actions would correct the identified condition.  This lack of quality could potentially impact the licensee's ability to identify adequate  
sufficient quality to address the condition such that a technically competent reviewer could understand how the corrective actions would correct the identified condition.  This lack of quality could potentially impact the licensee's ability to identify adequate  
corrective actions.  The inspectors identified the following condition reports as examples where the licensee's evaluation lacked sufficient quality:   
corrective actions.  The inspectors identified the following condition reports as examples where the licensee's evaluation lacked sufficient quality:   
  * Foreign Material Intrusion Effectiveness Review   Condition Report CR-PLP-2012-05054, "Root Cause Evaluation Report for Foreign Material Intrusion P-74, SIRWT Recirculation Pump," evaluated a foreign material  
 
  * Foreign Material Intrusion Effectiveness Review
Condition Report CR-PLP-2012-05054, "Root Cause Evaluation Report for Foreign Material Intrusion P-74, SIRWT Recirculation Pump," evaluated a foreign material  
intrusion event in July 2012 that affected the Safety Injection Refueling Water Tank  
intrusion event in July 2012 that affected the Safety Injection Refueling Water Tank  
recirculation pump.  The effectiveness reviews performed by the licensee did not  
recirculation pump.  The effectiveness reviews performed by the licensee did not  
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threshold for the effectiveness review performed was a failure to follow procedures  
threshold for the effectiveness review performed was a failure to follow procedures  
that resulted in foreign material intrusion.  During the effectiveness review, the  
that resulted in foreign material intrusion.  During the effectiveness review, the  
licensee identified failures to follow the foreign material excursion procedure.  However, the licensee concluded in the effectiveness review that the corrective actions were effective because no foreign material intrusion event actually occurred.    
licensee identified failures to follow the foreign material excursion procedure.  However, the licensee concluded in the effectiveness review that the corrective actions were effective because no foreign material intrusion event actually occurred.
   
  7  The inspectors reasoned that the absence of a foreign material intrusion given a failure to follow the foreign material excursion procedure may have been fortuitous,  
  7  The inspectors reasoned that the absence of a foreign material intrusion given a failure to follow the foreign material excursion procedure may have been fortuitous,  
rather than deliberate.  Subsequently, an actual foreign material intrusion event occurred, which further demonstrated that the corrective actions might not have been effective.  Specifically, when installing an inflatable bladder inside the Service Water system, on two occasions these bladders were inadvertently entrained into the return  
rather than deliberate.  Subsequently, an actual foreign material intrusion event occurred, which further demonstrated that the corrective actions might not have been effective.  Specifically, when installing an inflatable bladder inside the Service Water system, on two occasions these bladders were inadvertently entrained into the return  
header of the Service Water system by the relative vacuum created by the system flow.  It was determined that this was a result of the failure to establish adequate  
header of the Service Water system by the relative vacuum created by the system flow.  It was determined that this was a result of the failure to establish adequate  
controls as required by the foreign material excursion procedure.  This issue was documented as a non-cited violation in NRC Inspection Report 05000255/2014002.  * Vital Area Doors Alarm Evaluation  While reviewing the common cause analysis for Condition Report CR-PLP-2013-
controls as required by the foreign material excursion procedure.  This issue was documented as a non-cited violation in NRC Inspection Report 05000255/2014002.  
  * Vital Area Doors Alarm Evaluation  
  While reviewing the common cause analysis for Condition Report CR-PLP-2013-
4391, "Trend in Vital Area Doors Found Unsecured," the inspectors identified issues  
4391, "Trend in Vital Area Doors Found Unsecured," the inspectors identified issues  
with the thoroughness of the initial evaluation for the identified trend and the methodology used for the effectiveness review of the corrective actions implemented.  The common cause analysis reviewed 40 instances of unsecured vital  
with the thoroughness of the initial evaluation for the identified trend and the  
methodology used for the effectiveness review of the corrective actions implemented.  The common cause analysis reviewed 40 instances of unsecured vital  
area doors that occurred between January and October 2013.  The analysis  
area doors that occurred between January and October 2013.  The analysis  
identified the departments that were responsible for the doors being found unsecured  
identified the departments that were responsible for the doors being found unsecured  
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proper human performance tools to use when traversing through security doors and  
proper human performance tools to use when traversing through security doors and  
actions to take if a door did not properly close.  This common cause analysis did not  
actions to take if a door did not properly close.  This common cause analysis did not  
evaluate potential mechanical issues with the doors that would not allow them to close properly.   The effectiveness review for this trend reviewed 20 instances of unsecured vital area  
evaluate potential mechanical issues with the doors that would not allow them to close properly.  
The effectiveness review for this trend reviewed 20 instances of unsecured vital area  
doors that occurred between January 15 and March 16, 2014.  This review  
doors that occurred between January 15 and March 16, 2014.  This review  
compared the number of times the door was used to how many times the door was found unsecured.  The effectiveness review determined that a low percentage of errors occurred during this timeframe, and therefore the issue was resolved with no  
compared the number of times the door was used to how many times the door was found unsecured.  The effectiveness review determined that a low percentage of errors occurred during this timeframe, and therefore the issue was resolved with no  
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security door violations that occurred and planned to re-evaluate both the human  
security door violations that occurred and planned to re-evaluate both the human  
performance and the mechanical door operation components of this issue and  
performance and the mechanical door operation components of this issue and  
initiate follow-on corrective actions to address them.  The inspectors concluded that a lack of quality in some evaluations existed and that this  
initiate follow-on corrective actions to address them.  
was similar to what was documented in the previous biennial Problem Identification and Resolution inspection.    
  The inspectors concluded that a lack of quality in some evaluations existed and that this  
was similar to what was documented in the previous biennial Problem Identification and Resolution inspection.  
 
  8  During this inspection, although the inspectors did not identify any findings related to the lack of quality in evaluations, a minor violation related to a Part 21 evaluation is  
  8  During this inspection, although the inspectors did not identify any findings related to the lack of quality in evaluations, a minor violation related to a Part 21 evaluation is  
documented in Section 4OA2.2.b of this report.  Therefore, based on the samples reviewed during this inspection, the quality of evaluations, overall, appeared to be improving.   
documented in Section 4OA2.2.b of this report.  Therefore, based on the samples reviewed during this inspection, the quality of evaluations, overall, appeared to be improving.   
  (3) Effectiveness of Corrective Actions Based on the results of the inspection, the inspectors concluded that the licensee was generally effective in addressing identified issues and that the assigned corrective actions were generally appropriate.  The licensee implemented corrective actions in a timely manner, commensurate with their safety significance, including an appropriate  
 
  (3) Effectiveness of Corrective Actions
Based on the results of the inspection, the inspectors concluded that the licensee was generally effective in addressing identified issues and that the assigned corrective actions were generally appropriate.  The licensee implemented corrective actions in a timely manner, commensurate with their safety significance, including an appropriate  
consideration of risk.  Problems identified using root or apparent cause methodologies  
consideration of risk.  Problems identified using root or apparent cause methodologies  
were resolved in accordance with the Corrective Action Program procedural and  
were resolved in accordance with the Corrective Action Program procedural and  
regulatory requirements.  Corrective actions designed to prevent recurrence were generally comprehensive, thorough, and timely.  The inspectors sampled corrective action assignments for selected NRC documented violations and determined that  
regulatory requirements.  Corrective actions designed to prevent recurrence were generally comprehensive, thorough, and timely.  The inspectors sampled corrective  
action assignments for selected NRC documented violations and determined that  
actions assigned were generally effective and timely.  
actions assigned were generally effective and timely.  
   
   
For example, the licensee received a non-cited violation in 2002 for the failure to operate the primary coolant pumps in accordance with their design operating criteria.  The inspectors verified that the licensee's evaluations for the issue were comprehensive and  
For example, the licensee received a non-cited violation in 2002 for the failure to operate the primary coolant pumps in accordance with their design operating criteria.  The inspectors verified that the licensee's evaluations for the issue were comprehensive and  
the corrective actions completed and planned were appropriate and timely,  
the corrective actions completed and planned were appropriate and timely,  
commensurate with their safety significance.  
commensurate with their safety significance.  
   
   
The licensee's pre-inspection review identified several instances where corrective actions were closed inappropriately and that additional actions were needed to complete the closeout of the corrective actions.  The inspectors determined these discrepancies  
The licensee's pre-inspection review identified several instances where corrective actions were closed inappropriately and that additional actions were needed to complete the closeout of the corrective actions.  The inspectors determined these discrepancies  
were minor compliance issues with the licensee's Corrective Action Program procedures and the licensee had taken appropriate actions to address these issues.   
were minor compliance issues with the licensee's Corrective Action Program procedures and the licensee had taken appropriate actions to address these issues.   
  The inspectors also identified that there were approximately 260 open corrective action items at the time of the inspection.  However, only 20 of these open corrective action  
  The inspectors also identified that there were approximately 260 open corrective action items at the time of the inspection.  However, only 20 of these open corrective action  
items were more than 2 years old.  The inspectors reviewed a sample of these corrective  
items were more than 2 years old.  The inspectors reviewed a sample of these corrective  
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safety significant, the inspectors verified that the due dates were reasonable and the  
safety significant, the inspectors verified that the due dates were reasonable and the  
licensee had appropriate compensatory actions in place.   
licensee had appropriate compensatory actions in place.   
  Through interviews with the licensee staff and a review of the trend of the total outstanding corrective actions over the last 5 years, the inspectors determined that the  
  Through interviews with the licensee staff and a review of the trend of the total outstanding corrective actions over the last 5 years, the inspectors determined that the  
licensee had been reducing the corrective action backlog.  
licensee had been reducing the corrective action backlog.  
  c. Findings No findings were identified.   
 
  9  .2 Implementation of Corrective Actions Generated Following NRC Inspection Procedure  (IP) 95002 Supplemental Inspection a. Inspection Scope The inspectors reviewed the IP 95002 supplemental inspection action items that  were implemented since the completion of an IP 95002 supplemental inspection on  
  c. Findings
No findings were identified.   
  9  .2 Implementation of Corrective Actions Generated Following NRC Inspection Procedure  
  (IP) 95002 Supplemental Inspection
a. Inspection Scope
The inspectors reviewed the IP 95002 supplemental inspection action items that  were implemented since the completion of an IP 95002 supplemental inspection on  
November 9, 2012.  This supplemental inspection was related to a Yellow finding  
November 9, 2012.  This supplemental inspection was related to a Yellow finding  
documented in NRC Inspection Report 05000255/2011019 and 0500025/2011020.   
documented in NRC Inspection Report 05000255/2011019 and 0500025/2011020.   
The Yellow finding was associated with the loss of the Left train of direct current (DC)  
The Yellow finding was associated with the loss of the Left train of direct current (DC)  
power due to the failure to ensure that the work instructions on a safety-related  125-Volt DC distribution panel were adequate for the scheduled work.  The results of this supplemental inspection were documented in NRC Inspection Report  
power due to the failure to ensure that the work instructions on a safety-related  125-Volt DC distribution panel were adequate for the scheduled work.  The results of this  
05000255/2012011.  b. Assessment The inspectors reviewed Condition Report CR-PLP-2011-04822, which was the overarching condition report for the issue that resulted in the Yellow finding, and found  
supplemental inspection were documented in NRC Inspection Report  
 
05000255/2012011.  
  b. Assessment
The inspectors reviewed Condition Report CR-PLP-2011-04822, which was the overarching condition report for the issue that resulted in the Yellow finding, and found  
that the associated corrective actions had been planned and implemented.  There were  
that the associated corrective actions had been planned and implemented.  There were  
various tasks associated with this condition report that were completed subsequent to  
various tasks associated with this condition report that were completed subsequent to  
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ensure any additional issues and/or concerns identified had already been addressed and  
ensure any additional issues and/or concerns identified had already been addressed and  
did not invalidate the actions taken.  The inspectors reviewed the completed corrective  
did not invalidate the actions taken.  The inspectors reviewed the completed corrective  
actions and found them to be adequate.   c. Findings No findings were identified. .3 Implementation of Corrective Actions Generated Following NRC IP 95001 Supplemental Inspection a. Inspection Scope The inspectors reviewed the corrective actions that were implemented and the effectiveness reviews of those corrective actions that had been conducted since the  
actions and found them to be adequate.  
c. Findings
No findings were identified. .3 Implementation of Corrective Actions Generated Following NRC IP 95001 Supplemental  
Inspection
a. Inspection Scope
The inspectors reviewed the corrective actions that were implemented and the effectiveness reviews of those corrective actions that had been conducted since the  
completion of an IP 95001 supplemental inspection on June 29, 2012.  This  
completion of an IP 95001 supplemental inspection on June 29, 2012.  This  
supplemental inspection was related to a White finding associated with the Turbine-
supplemental inspection was related to a White finding associated with the Turbine-
Driven Auxiliary Feedwater pump that was documented in NRC Inspection Report 05000255/2011013 and 05000255/2011017.  The results of this supplemental inspection were documented in NRC Inspection Report 05000255/2012010. b. Assessment The inspectors reviewed Condition Report CR-PLP-2011-5723 and the associated root cause evaluation report, "Auxiliary Feedwater Pump P-8B Overspeed Trip Actuation," and found that all of the associated corrective actions had been implemented.  Two effectiveness reviews had also been completed to evaluate the adequacy of the   
Driven Auxiliary Feedwater pump that  
was documented in NRC Inspection Report 05000255/2011013 and 05000255/2011017.  The results of this supplemental inspection  
were documented in NRC Inspection Report 05000255/2012010. b. Assessment
The inspectors reviewed Condition Report CR-PLP-2011-5723 and the associated root cause evaluation report, "Auxiliary Feedwater Pump P-8B Overspeed Trip Actuation," and found that all of the associated corrective actions had been implemented.  Two effectiveness reviews had also been completed to evaluate the adequacy of the   
  10  corrective actions implemented.  The first effectiveness review conducted in April 2012 examined the revisions to the maintenance procedure for the Auxiliary Feedwater Pump,  
  10  corrective actions implemented.  The first effectiveness review conducted in April 2012 examined the revisions to the maintenance procedure for the Auxiliary Feedwater Pump,  
and identified some enhancements to be included in the procedure based on information in the root cause evaluation.  The inspectors reviewed the most current revision of this maintenance procedure and found that all of those enhancements had been included in  
and identified some enhancements to be included in the procedure based on information in the root cause evaluation.  The inspectors reviewed the most current revision of this maintenance procedure and found that all of those enhancements had been included in  
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finding initially), and concluded that there were no maintenance-induced problems  
finding initially), and concluded that there were no maintenance-induced problems  
related to this pump.  All corrective actions associated with the aforementioned condition  
related to this pump.  All corrective actions associated with the aforementioned condition  
report and root cause evaluation, and all effectiveness reviews had been completed for this White finding.  The inspectors reviewed all of this information and determined that the actions implemented were adequate.  c. Findings No findings were identified. .4 Assessment of the Use of Operating Experience a. Inspection Scope The inspectors reviewed the licensee's implementation of the facility's Operating Experience Program.  Specifically, the inspectors reviewed the Operating Experience Program implementing procedures and licensee evaluations of operating experience issues and events.  The inspectors also observed meetings and daily activities for the  
report and root cause evaluation, and all effectiveness reviews had been completed for this White finding.  The inspectors reviewed all of this information and determined that the actions implemented were adequate.  c. Findings
No findings were identified. .4 Assessment of the Use of Operating Experience
a. Inspection Scope
The inspectors reviewed the licensee's implementation of the facility's Operating Experience Program.  Specifically, the inspectors reviewed the Operating Experience Program implementing procedures and licensee evaluations of operating experience issues and events.  The inspectors also observed meetings and daily activities for the  
use of operating experience information to determine whether the licensee was effectively integrating operating experience into the performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel,  
use of operating experience information to determine whether the licensee was effectively integrating operating experience into the performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel,  
whether the licensee's Operating Experience Program was sufficient to prevent future  
whether the licensee's Operating Experience Program was sufficient to prevent future  
occurrences of previous industry events, and whether the licensee effectively used operating experience information in the planning and performance of departmental assessments and facility audits.  The inspectors also assessed if corrective actions, as a result of operating experience, were identified and implemented effectively and in a timely manner.  In addition, the inspectors interviewed the Operating Experience Program owner to obtain insights on its use.  b. Assessment Based on the results of the inspection, the inspectors concluded that, overall, operating experience was effectively utilized at the station.  The inspectors observed that representatives from different sites held periodic meetings to discuss recently published  
 
occurrences of previous industry events, and whether the licensee effectively used operating experience information in the planning and performance of departmental assessments and facility audits.  The inspectors also assessed if corrective actions, as a result of operating experience, were identified and implemented effectively and in a timely manner.  In addition, the inspectors interviewed the Operating Experience Program owner to obtain insights on its use.  b. Assessment
Based on the results of the inspection, the inspectors concluded that, overall, operating experience was effectively utilized at the station.  The inspectors observed that representatives from different sites held periodic meetings to discuss recently published  
operating experience.  Issues that were applicable to the Palisades Nuclear Plant were  
operating experience.  Issues that were applicable to the Palisades Nuclear Plant were  
entered into the Corrective Action Program for resolution.  Industry operating experience  
entered into the Corrective Action Program for resolution.  Industry operating experience  
was effectively disseminated across plant departments through daily and pre-job briefings.     
was effectively disseminated across plant departments through daily and pre-job briefings.     
  11  Nonetheless, the inspectors noted the following licensee identified minor violation of  10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," related to a   
  11  Nonetheless, the inspectors noted the following licensee identified minor violation of  10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," related to a   
10 CFR Part 21 evaluation.  Deficiencies in Part 21 Evaluation
10 CFR Part 21 evaluation.  Deficiencies in Part 21 Evaluation
 
On November 8, 2012, Fisher Control International submitted a Part 21 report that  
On November 8, 2012, Fisher Control International submitted a Part 21 report that  
described certain butterfly valve parts that did not receive proper commercial grade  
described certain butterfly valve parts that did not receive proper commercial grade  
dedication.  These parts were considered essential-to-function and were required for the  
dedication.  These parts were considered essential-to-function and were required for the  
butterfly valve assembly to perform its safety-related function.  Fisher Control International requested the recipients of the Part 21 report to review this information for applicability to their equipment and facilities and take appropriate actions, if required.  
butterfly valve assembly to perform its safety-related function.  Fisher Control International requested the recipients of the Part 21 report to review this information for applicability to their equipment and facilities and take appropriate actions, if required.  
   
   
The licensee entered this issue in the Corrective Action Program on November 20, 2012.   
The licensee entered this issue in the Corrective Action Program on November 20, 2012.   
The licensee contacted Fisher Control International and identified that two installed safety-related Component Cooling Heat Exchanger temperature control valves were affected.  The licensee concluded that the valves would perform their design function,  
The licensee contacted Fisher Control International and identified that two installed safety-related Component Cooling Heat Ex
changer temperature control valves were affected.  The licensee concluded that the valves would perform their design function,  
but did not clearly document the basis of that conclusion.  In addition, Fisher Control  
but did not clearly document the basis of that conclusion.  In addition, Fisher Control  
International also communicated to the licensee that they had identified and notified the  
International also communicated to the licensee that they had identified and notified the  
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Subsequently, an operability evaluation was performed, which concluded that all of the equipment impacted remained operable, but were non-conforming.  The inspectors determined that this was a licensee-identified minor violation of 10 CFR 50, Appendix B, Criteria XVI, "Corrective Action."  This failure to comply with the  
Subsequently, an operability evaluation was performed, which concluded that all of the equipment impacted remained operable, but were non-conforming.  The inspectors determined that this was a licensee-identified minor violation of 10 CFR 50, Appendix B, Criteria XVI, "Corrective Action."  This failure to comply with the  
Appendix B requirement constituted a minor violation that is not subject to enforcement  
Appendix B requirement constituted a minor violation that is not subject to enforcement  
action in accordance with the NRC's Enforcement Policy.  A replacement of the affected equipment was scheduled for the next refueling outage.  c. Findings No findings were identified. .5 Assessment of Self-Assessments and Audits a. Inspection Scope The inspectors reviewed selected self-assessments, bench markings, "Snap-shot" self-assessments, and Nuclear Oversight audits, as well as the schedule of past and future assessments.  The inspectors evaluated whether these audits and self-assessments  
 
action in accordance with the NRC's Enforcement Policy.  A replacement of the affected equipment was scheduled for the next refueling outage.  c. Findings
No findings were identified. .5 Assessment of Self-Assessments and Audits
a. Inspection Scope
The inspectors reviewed selected self-assessments, bench markings, "Snap-shot" self-assessments, and Nuclear Oversight audits, as well as the schedule of past and future assessments.  The inspectors evaluated whether these audits and self-assessments  
were effectively managed, adequately covered the subject areas, and properly captured  
were effectively managed, adequately covered the subject areas, and properly captured  
identified issues in the Corrective Action Program.  In addition, the inspectors  
identified issues in the Corrective Action Program.  In addition, the inspectors  
interviewed licensee personnel regarding the implementation of the audit and self-assessment programs.     
interviewed licensee personnel regarding the implementation of the audit and self-assessment programs.     
  12  b. Assessment Based on the results of the inspection, the inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying issues and enhancement opportunities at an appropriate threshold.  The inspectors concluded that these audits and self-assessments were completed by personnel knowledgeable in the  
  12  b. Assessment
Based on the results of the inspection, the inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying issues and enhancement opportunities at an appropriate threshold.  The inspectors concluded that these audits and self-assessments were completed by personnel knowledgeable in the  
subject area.  In many cases, these self-assessments and audits had identified  
subject area.  In many cases, these self-assessments and audits had identified  
numerous issues that were not previously recognized by the station.  These issues were  
numerous issues that were not previously recognized by the station.  These issues were  
entered into condition reports as required by Corrective Action Program procedures.  c. Findings No findings were identified. .6 Assessment of Safety Conscious Work Environment a. Inspection Scope The inspectors interviewed 19 Palisades Nuclear Plant personnel to determine if there were any indications that licensee personnel were reluctant to raise safety concerns to either their management or the NRC due to fear of retaliation.  These individuals represented various departments onsite including Engineering, Maintenance,  
entered into condition reports as required by Corrective Action Program procedures.  c. Findings
No findings were identified. .6 Assessment of Safety Conscious Work Environment
  a. Inspection Scope
The inspectors interviewed 19 Palisades Nuclear Plant personnel to determine if there were any indications that licensee personnel were reluctant to raise safety concerns to either their management or the NRC due to fear of retaliation.  These individuals represented various departments onsite including Engineering, Maintenance,  
Operations, Radiation Protection, and Security.  The inspectors also assessed the  
Operations, Radiation Protection, and Security.  The inspectors also assessed the  
licensee's safety conscious work environment through a review of Employee Concerns Program implementing procedures, discussions with the Employee Concerns Program Manager, and reviews of condition reports.  The inspectors reviewed selected Employee Concerns Program activities to identify any emergent issues or potential trends.  The  
licensee's safety conscious work environment through a review of Employee Concerns Program implementing procedures, discussions with the Employee Concerns Program Manager, and reviews of condition reports.  The inspectors reviewed selected Employee Concerns Program activities to identify any emergent issues or potential trends.  The  
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Program were also reviewed.  The review was performed to ensure there was a free flow  
Program were also reviewed.  The review was performed to ensure there was a free flow  
of information and to determine if individuals were willing to raise nuclear safety  
of information and to determine if individuals were willing to raise nuclear safety  
concerns without fear of retaliation.  b. Assessment As discussed in NRC Inspection Report 05000255/2014009, dated March 6, 2014, the NRC performed a limited scope Problem Identification and Resolution inspection that  
concerns without fear of retaliation.  b. Assessment
focused on an assessment of the safety conscious work environment in the Chemistry Department, Security Department, and Mechanical Maintenance working group.  This inspection was performed as a result of the NRC's receipt of several safety conscious work environment or safety culture-related concerns that prompted questions into the progress made in implementing the licensee's Recovery Plan regarding safety culture deficiencies that, in part, contributed to two Greater-than-Green findings identified in  
As discussed in NRC Inspection Report 05000255/2014009, dated March 6, 2014, the NRC performed a limited scope Problem Identification and Resolution inspection that  
focused on an assessment of the safety conscious work environment in the Chemistry Department, Security Department, and Mechanical Maintenance working group.  This  
inspection was performed as a result of the NRC's receipt of several safety conscious  
work environment or safety culture-related concerns that prompted questions into the progress made in implementing the licensee's Recovery Plan regarding safety culture deficiencies that, in part, contributed to two Greater-than-Green findings identified in  
 
2011.   
2011.   
  The NRC identified a chilled work environment in the Security Department as documented in NRC Inspection Report 05000255/2014009.  The licensee implemented  
  The NRC identified a chilled work environment in the Security Department as documented in NRC Inspection Report 05000255/2014009.  The licensee implemented  
a number of corrective actions to address the chilled environment in the Security Department.     
a number of corrective actions to address the chilled environment in the Security Department.  
  13  During this inspection, the inspectors determined that the safety conscious work environment and overall performance related to identifying, evaluating, and resolving problems was acceptable for the site in general.  However, the assessment below was not characteristic of the safety conscious work environment in the Security Department.  A detailed review of the licensee's Security SCWE Action Plan is discussed in   
    
  13  During this inspection, the inspectors determined that the safety conscious work environment and overall performance related to
identifying, evaluating, and resolving problems was acceptable for the site in general.  However, the assessment below was not characteristic of the safety conscious work environment in the Security Department.  A detailed review of the licensee's Security SCWE Action Plan is discussed in   
Section 4OA5.2 of this report.  
Section 4OA5.2 of this report.  
   
   
With the exception of the Security Department, the inspectors did not identify any issues that suggested conditions were not conducive to the establishment and existence of a safety conscious work environment at Palisades Nuclear Plant.  Licensee staff was aware of and familiar with the Corrective Action Program and other station processes,  
With the exception of the Security Department, the inspectors did not identify any issues that suggested conditions were not conducive to the establishment and existence of a safety conscious work environment at Palisades Nuclear Plant.  Licensee staff was aware of and familiar with the Corrective Action Program and other station processes,  
including the Employee Concerns Program, through which concerns could be raised.   
including the Employee Concerns Program, through which concerns could be raised.   
   
   
The inspectors did not review the site Safety Culture and SCWE surveys and assessments during this inspection because these documents were recently reviewed as part of the limited scope Problem Identification and Resolution inspection and the  
The inspectors did not review the site Safety Culture and SCWE surveys and assessments during this inspection because these documents were recently reviewed as part of the limited scope Problem Identification and Resolution inspection and the  
conclusions from that inspection remained valid.  The results indicated that there were  
conclusions from that inspection remained valid.  The results indicated that there were  
no impediments to the identification of nuclear safety issues.   
no impediments to the identification of nuclear safety issues.   
  The staff also indicated that management had been focused on promoting an environment that encourages raising issues and concerns without fear of retaliation.   
  The staff also indicated that management had been focused on promoting an environment that encourages raising issues and concerns without fear of retaliation.   
The formal policy was communicated at all hands meetings, shift turnover meetings, and  
The formal policy was communicated at all hands meetings, shift turnover meetings, and  
through other communication venues, such as newsletters and emails.  Department  
through other communication venues, such as newsletters and emails.  Department  
managers and supervisors promoted a safety conscious work environment and reinforced senior management's policy.  Individuals were comfortable raising issues and concerns without fear of retaliation.   
 
managers and supervisors promoted a safe
ty conscious work environment and  
reinforced senior management's policy.  
  Individuals were comfortable raising issues and concerns without fear of retaliation.   
Overall, they felt that condition reports were given the appropriate priority and actions  
Overall, they felt that condition reports were given the appropriate priority and actions  
taken to close condition reports were effective in addressing the identified issues.   c. Findings No findings were identified.   
taken to close condition reports were effective in addressing the identified issues.  
4OA5 Other Activities .1 Confirmatory Action Letter (CAL) - Palisades Nuclear Plant Commitments to Address SIRWT and Control Room Concrete Support Structure Leakage As documented in NRC Letter EA-12-155, "Confirmatory Action Letter (CAL) Revision 1 - Palisades Nuclear Plant Commitments to Address Safety Injection Refueling Water  
c. Findings
  No findings were identified.  
   
4OA5 Other Activities
  .1 Confirmatory Action Letter (CAL) - Palisades Nuclear Plant Commitments to Address  
SIRWT and Control Room Concrete Support Structure Leakage
As documented in NRC Letter EA-12-155, "Confirmatory Action Letter (CAL) Revision 1 - Palisades Nuclear Plant Commitments to Address Safety Injection Refueling Water  
Tank (SIRWT) and Control Room Concrete Support Structure Leakage," (ADAMS  
Tank (SIRWT) and Control Room Concrete Support Structure Leakage," (ADAMS  
ML13177A280) the NRC concluded that the structural integrity of the Safety Injection Refueling Water Tank was sufficient to meet its intended safety function, which addressed three of the five CAL items.  The remaining two CAL items associated with  
ML13177A280) the NRC concluded that the structural integrity of the Safety Injection Refueling Water Tank was sufficient to meet its intended safety function, which addressed three of the five CAL items.  The remaining two CAL items associated with  
the control room support structure were as follows:  
the control room support structure were as follows:  
  1. Entergy Nuclear Operations, Inc., (ENO) will continue inspections of the concrete support structure above the control room, control room hallway, and the concrete support structure ceiling as prescribed in the approved Operations Standing Order.  These inspections are to ensure that the   
  1. Entergy Nuclear Operations, Inc., (ENO) will continue inspections of the concrete support structure above the control room, control room hallway, and the concrete support structure ceiling as prescribed in the approved Operations Standing Order.  These inspections are to ensure that the   
  14  temporary modifications installed to prevent impact to safety-related structures, systems and components are performing their intended functions.  2. ENO will correct the adverse condition related to cracking of the concrete support structure around the ceiling of the control room, which could lead to  
  14  temporary modifications installed to prevent impact to safety-related structures, systems and components are performing their intended functions.  
water intrusion, prior to restart from the next refueling outage.   
  2. ENO will correct the adverse condition related to cracking of the concrete support structure around the ceiling of the control room, which could lead to  
water intrusion, prior to restart from the next refueling outage.  
   
To address these items, the licensee performed a modification in the catacombs area  
To address these items, the licensee performed a modification in the catacombs area  
above the control room.  This modification included the installation of a waterproof membrane and a design feature to divert water away from the control room, in the event of a leak into the catacombs area.  The licensee also performed inspections of the areas  
above the control room.  This modification included the installation of a waterproof membrane and a design feature to divert water away from the control room, in the event of a leak into the catacombs area.  The licensee also performed inspections of the areas  
where SIRWT leakage could occur, including the catacombs area, until all modification  
where SIRWT leakage could occur, including the catacombs area, until all modification  
activities were complete.  
activities were complete.  
  The inspectors performed a review of the engineering change package that documented the details of the modification and the analyses performed to determine acceptability.   
  The inspectors performed a review of the engineering change package that documented the details of the modification and the analyses performed to determine acceptability.   
The inspectors ensured that the licensee addressed the capability of this system as well  
The inspectors ensured that the licensee addressed the capability of this system as well  
Line 290: Line 436:
that were performed to ensure these inspections were adequate to identify any water  
that were performed to ensure these inspections were adequate to identify any water  
intrusion and were performed in accordance with the CAL commitment.  
intrusion and were performed in accordance with the CAL commitment.  
   
   
Based on the information reviewed during this inspection, the inspectors concluded that the control room structure continues to perform its intended safety function, and the installed modifications, if maintained, are adequate to prevent water intrusion into the  
Based on the information reviewed during this inspection, the inspectors concluded that the control room structure continues to perform its intended safety function, and the installed modifications, if maintained, are adequate to prevent water intrusion into the  
control room.  Therefore, the inspectors determined that the licensee had fulfilled its  
control room.  Therefore, the inspectors determined that the licensee had fulfilled its  
commitments to address the Safety Injection Refueling Water Tank and control room  
commitments to address the Safety Injection Refueling Water Tank and control room  
concrete support structure leakage.   Separate correspondence will be issued to formally close Confirmatory Action Letter EA-12-155.   
concrete support structure leakage.  
  .2 Security Safety Conscious Work Environment Action Plan The inspectors performed an independent evaluation of the site's implementation of the Security Safety Conscious Work Environment (SCWE) Action Plan.  The plan was developed by the site and was being implemented in response to the NRC's identification of a chilled work environment within the Security Department during the December 2013 limited scope Problem Identification and Resolution inspection, which was documented in NRC Inspection Report 05000255/2014009 (ADAMS ML14064A569).  The inspectors performed an independent review of the licensee's implementation of the Security SCWE Action Plan.  The inspection included a review of  
Separate correspondence will be issued to formally close Confirmatory Action  
Letter EA-12-155.   
 
  .2 Security Safety Conscious Work Environment Action Plan
The inspectors performed an independent evaluation of the site's implementation of the Security Safety Conscious Work Environment (SCWE) Action Plan.  The plan was  
developed by the site and was being implemented in response to the NRC's identification of a chilled work environment within the Security Department during the December 2013 limited scope Problem Identif
ication and Resolution inspection, which  
was documented in NRC Inspection Report 05000255/2014009 (ADAMS ML14064A569).  The inspectors performed an independent review of the licensee's implementation of the Security SCWE Action Plan.  The inspection included a review of  
the licensee's implementation and completion of SCWE Action Plan actions; two focus  
the licensee's implementation and completion of SCWE Action Plan actions; two focus  
group meetings with 19 non-supervisory level security officers; and interviews with the  
group meetings with 19 non-supervisory level security officers; and interviews with the  
Regulatory and Performance Improvement Director, Security Manager, and the  
Regulatory and Performance Improvement Director, Security Manager, and the  
Employee Concerns Program Manager.     
Employee Concerns Program Manager.  
  15  Specific observations included the following: * Security officers had a limited recollection of discussing the results of the NRC's limited scope Problem Identification and Resolution inspection that was completed in February 2014.  Security officers recalled being told that the NRC stated there "appears to be a potential chilled work environment in Security."   
    
  15  Specific observations included the following:  
* Security officers had a limited recollection of discussing the results of the NRC's limited scope Problem Identification and Resolution inspection that was completed in February 2014.  Security officers recalled being told that the NRC stated there "appears to be a potential chilled work environment in Security."   
The security officers stated that they believed the site did not feel there was a  
The security officers stated that they believed the site did not feel there was a  
chilled work environment, but was only taking actions in response to the NRC's conclusions.  During an interview with the Security Manager, additional details on the dissemination of the inspection results were obtained.  Specifically, security officers were provided the inspection report as an email attachment in advance of the Security Manager meeting with each of the security shifts.  At the meetings,  
chilled work environment, but was only taking actions in response to the NRC's conclusions.  During an interview with the Security Manager, additional details on the dissemination of the inspection results were obtained.  Specifically, security officers were provided the inspection report as an email attachment in advance of the Security Manager meeting with each of the security shifts.  At the meetings,  
hard copies of the report were available for the security officers to reference and  
hard copies of the report were available for the security officers to reference and  
retain, as desired.  The Security Manager acknowledged discussing the NRC's  
retain, as desired.  The Security Manager acknowledged discussing the NRC's  
conclusions, but validated the fact that security officers were told the NRC stated there "appears to be a potential chilled work environment in Security."  * Security officers stated they were never informed of the site's development and implementation of a Security SCWE Action Plan and were unaware of the specific actions required by the existing plan.  * Security officers perceived site management to be simply "putting checks in the block" to credit completion of action items and were not committed to changing  
conclusions, but validated the fact that security officers were told the NRC stated there "appears to be a potential chilled work environment in Security."   
the existing safety conscious work environment issues in the Security Department.  * Security officers identified a lack of interaction with supervisory and management personnel above the Security Shift Supervisor level within the Security  
* Security officers stated they were never informed of the site's development and implementation of a Security SCWE Action Plan and were unaware of the specific actions required by the existing plan.  
Department and site senior management personnel external to the Security Department.  Security officers did acknowledge an increase in the attendance of Security Operations Superintendents at shift turnover meetings.   * Security officers were unaware of the establishment of the site's Security Ombudsman Program and the intent of the program.  Additionally, the security  
  * Security officers perceived site management to be simply "putting checks in the block" to credit completion of action items and were not committed to changing  
officers were unaware of who the security ombudsman was for their respective shift despite the selection and assignment of staff to these positions at the end of March 2014.  * Security officers were not aware of a change in the site security chain of command.  Specifically, the fact that the Palisades Security Manager no longer reported to the Entergy Corporate Security Director, but reported to the Site Vice President through the Regulatory and Performance Improvement Director was  
the existing safety conscious work environment issues in the Security Department.  
  * Security officers identified a lack of interaction with supervisory and management personnel above the Security Shift Supervisor level within the Security  
Department and site senior management per
sonnel external to the Security Department.  Security officers did acknowledge an increase in the attendance of Security Operations Superintendents at shift turnover meetings.
* Security officers were unaware of the establishment of the site's Security Ombudsman Program and the intent of the program.  Additionally, the security  
officers were unaware of who the security ombudsman was for their respective shift despite the selection and assignment of staff to these positions at the end of  
March 2014.  
  * Security officers were not aware of a change in the site security chain of command.  Specifically, the fact that the Palisades Security Manager no longer reported to the Entergy Corporate Security Director, but reported to the Site Vice President through the Regulatory and Performance Improvement Director was  
not communicated.  In addition, security officers were not introduced to the  
not communicated.  In addition, security officers were not introduced to the  
Regulatory and Performance Improvement Director.  * Since November 2013, the site's Aggregate Performance Review rated the Security Department as Green in the area of Nuclear Safety.  At an Aggregate Performance Review Meeting conducted on May 19, 2014, this rating was  
 
Regulatory and Performance Improvement Director.  
  * Since November 2013, the site's Aggregate Performance Review rated the Security Department as Green in the area of Nuclear Safety.  At an Aggregate Performance Review Meeting conducted on May 19, 2014, this rating was  
challenged by a manager outside the Security Department and, as a result of this   
challenged by a manager outside the Security Department and, as a result of this   
  16  challenge, the participants agreed the Security Department should be rated Red in this area due to the chilled work environment identified in the department.   
  16  challenge, the participants agreed the Security Department should be rated Red in this area due to the chilled work environment identified in the department.   
Since November 2013, the Security Department had been rating this area as Green in the Department Performance Review and this rating was unchallenged by senior management until the May 2014 Aggregate Performance Review  
Since November 2013, the Security Department had been rating this area as Green in the Department Performance Review and this rating was unchallenged by senior management until the May 2014 Aggregate Performance Review  
Meeting.  
 
Meeting.
The inspectors concluded that, to date, the site had completed all the actions as  
The inspectors concluded that, to date, the site had completed all the actions as  
committed to in the Security SCWE Action Plan.  However, the inspectors concluded that the quality of the actions implemented have been insufficient to assess and understand the cause of the chilled work environment within the Security Department  
committed to in the Security SCWE Action Plan.  However, the inspectors concluded that the quality of the actions implemented have been insufficient to assess and understand the cause of the chilled work environment within the Security Department  
and did not demonstrate a strong commitment to effectively improve the safety  
and did not demonstrate a strong commitment to effectively improve the safety  
conscious work environment in the Security Department.  Specifically, significant gaps were found to exist in the security officers' knowledge of the actions being taken to address the chilled safety conscious work environment and management's commitment to improving the overall safety conscious work environment.  
conscious work environment in the Security Department.  Specifically, significant gaps were found to exist in the security officers' knowledge of the actions being taken to address the chilled safety conscious work environment and management's commitment to improving the overall safety conscious work environment.  
  4OA6  Management Meetings a. Interim Exit Meeting On May 23, 2014, the inspectors presented the preliminary inspection results to  Mr. A. Vitale, Site Vice President, and other members of the licensee staff.  b. Exit Meeting On June 11, 2014, the inspectors presented the final inspection results to Mr. A. Vitale, Site Vice President and other members of the licensee staff.  The licensee  
 
  4OA6  Management Meetings
a. Interim Exit Meeting
On May 23, 2014, the inspectors presented the preliminary inspection results to  Mr. A. Vitale, Site Vice President, and other members of the licensee staff.  b. Exit Meeting
On June 11, 2014, the inspectors presented the final inspection results to Mr. A. Vitale, Site Vice President and other members of the licensee staff.  The licensee  
acknowledged the issues presented.  The inspectors confirmed that none of the potential report input discussed was considered proprietary. ATTACHMENT:  SUPPLEMENTAL INFORMATION  
acknowledged the issues presented.  The inspectors confirmed that none of the potential report input discussed was considered proprietary. ATTACHMENT:  SUPPLEMENTAL INFORMATION  
  Attached  SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT Licensee A. Vitale, Site Vice President W. Nelson, Training Manager  
  Attached  
  SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT  
Licensee A. Vitale, Site Vice President W. Nelson, Training Manager  
 
G. Heisterman, Maintenance Manager  
G. Heisterman, Maintenance Manager  
A. Notbohm, CA&A Manager  
A. Notbohm, CA&A Manager  
O. Gustafson, Regulatory and Performance Improvement Director  
O. Gustafson, Regulatory and Performance Improvement Director  
D. Corbin, Operations Manager M. Seleski, Chemistry Supervisor C. Plachta, Nuclear Oversight Manager  
D. Corbin, Operations Manager M. Seleski, Chemistry Supervisor C. Plachta, Nuclear Oversight Manager  
B. Davis, Engineering Director  
B. Davis, Engineering Director  
E. Chetfield, Employee Concern Program Manager  
E. Chetfield, Employee Concern Program Manager  
D. Lucy, Planning, Scheduling and Outage Manager J. Wright, Radwaste Supervisor J. Ridley, Emergency Preparedness Coordinator  
D. Lucy, Planning, Scheduling and Outage Manager J. Wright, Radwaste Supervisor  
J. Ridley, Emergency Preparedness Coordinator  
J. Haverly, Security Supervisor  
J. Haverly, Security Supervisor  
   
   
  NRC   
  NRC   
Line 335: Line 514:
E. Duncan, Branch Chief, Division of Reactor Projects  
E. Duncan, Branch Chief, Division of Reactor Projects  
A. Garmoe, Senior Resident Inspector  
A. Garmoe, Senior Resident Inspector  
A. Scarbeary, Resident inspector  LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED Opened  None   
A. Scarbeary, Resident inspector  
   LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
Opened  None   
   
   
Closed   
Closed   
None   
None   
Discussed
Discussed
 
None   
None   
  2  LIST OF DOCUMENTS REVIEWED The following is a list of documents reviewed during the inspection.  Inclusion on this list does not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections or portions of the documents were evaluated as part of the overall inspection effort.  Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.   Condition Reports CR-PLP-2007-05898 Greater than Green Security Finding Identified November 6, 2007 CR-PLP-2008-04279 Adverse Trend in Power Supply Failures October 16, 2008 CR-PLP-2009-04028 Increasing Trend in Number of Maintenance Rule a(1) Issues and Repeat Equipment Failures at Palisades August 21, 2009 CR-PLP-2009-04831 Four New Capacitors for P/S-0110A Have Different Size Case than the Installed Ones October 16, 2009 CR-PLP-2009-05002 Declining Trend in RPS Voltage Converter +15 Vdc Output October 29, 2009 CR-PLP-2010-00315 Potential Adverse Trend with Scaffold Periodic Inspection January 22, 2010 CR-PLP-2010-00551 Additional Operability and/or Mitigating Action Guidance is Needed Regarding the Effect of  
  2  LIST OF DOCUMENTS REVIEWED The following is a list of documents reviewed during the inspection.  Inclusion on this list does  
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections or portions of the documents were evaluated as part of the overall inspection effort.  Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.
Condition Reports
  CR-PLP-2007-05898 Greater than Green Security Finding Identified November 6, 2007 CR-PLP-2008-04279 Adverse Trend in Power Supply Failures October 16, 2008 CR-PLP-2009-04028 Increasing Trend in Number of Maintenance Rule a(1) Issues and Repeat Equipment Failures at Palisades August 21, 2009 CR-PLP-2009-04831 Four New Capacitors for P/S-0110A Have Different Size Case than the Installed Ones  
October 16, 2009 CR-PLP-2009-05002 Declining Trend in RPS Voltage Converter +15  
Vdc Output  
October 29, 2009 CR-PLP-2010-00315 Potential Adverse Trend with Scaffold Periodic Inspection  
January 22, 2010 CR-PLP-2010-00551 Additional Operability and/or Mitigating Action Guidance is Needed Regarding the Effect of  
Unfiltered Air In-Leakage into the Control Room  
Unfiltered Air In-Leakage into the Control Room  
Envelope February 8, 2010 CR-PLP-2010-02351 Received Alarm EK-0601A, Variable High Power Level Channel Trip June 13, 2010 CR-PLP-2010-02551 Received Unexpected AFAS Alarms in the Control Room June 27, 2010 CR-PLP-2010-03292 P-55C, 'C' Charging Pump, Declared Maintenance Rule Unavailable August 6, 2010 CR-PLP-2010-03809 Functional Failure Determination Performed for CR-PLP-2010-2551 Determined the Issue was a Functional Failure and Should be Re-classified September 7, 2010 CR-PLP-2010-06100 Increase in Spent Fuel Pool Liner Leakage November 14, 2010 CR-PLP-2011-02144 Received Alarms EK-0602A and EK-0606A April 28, 2011 CR-PLP-2011-03902 Indications of a Sheared Shaft on Service Water Pump P-7C August 9, 2011 CR-PLP-2011-04620 Primary Coolant System Unidentified Leakage Greater Than the Technical Specification  
 
Envelope  
February 8, 2010 CR-PLP-2010-02351 Received Alarm EK-0601A, Variable High Power Level Channel Trip June 13, 2010 CR-PLP-2010-02551 Received Unexpected AFAS Alarms in the  
Control Room June 27, 2010 CR-PLP-2010-03292 P-55C, 'C' Charging Pump, Declared Maintenance Rule Unavailable August 6, 2010 CR-PLP-2010-03809 Functional Failure Determination Performed for CR-PLP-2010-2551 Determined the Issue was a Functional Failure and Should be Re-classified September 7, 2010 CR-PLP-2010-06100 Increase in Spent Fuel Pool Liner Leakage November 14, 2010 CR-PLP-2011-02144 Received Alarms EK-0602A and EK-0606A April 28, 2011 CR-PLP-2011-03902 Indications of a Sheared Shaft on Service Water Pump P-7C August 9, 2011 CR-PLP-2011-04620 Primary Coolant System Unidentified Leakage  
Greater Than the Technical Specification  
 
Limiting Condition for Operation September 16, 2011 CR-PLP-2011-04822 Post 95002 Corrective Actions March 7, 2013 CR-PLP-2011-04822 Unplanned, Automatic Reactor Trip Occurred During Maintenance on a DC Supply Panel September 25, 2011   
Limiting Condition for Operation September 16, 2011 CR-PLP-2011-04822 Post 95002 Corrective Actions March 7, 2013 CR-PLP-2011-04822 Unplanned, Automatic Reactor Trip Occurred During Maintenance on a DC Supply Panel September 25, 2011   
  3  CR-PLP-2011-05125 ERO Staff Augmentation Test - TSC Operations Support Communicator had Not Arranged for an  
  3  CR-PLP-2011-05125 ERO Staff Augmentation Test - TSC Operations Support Communicator had Not Arranged for an  
Alternate to Fill His Position October 6, 2011 CR-PLP-2011-05127 ERO Staff Augmentation Test - CR Operations Support did Not Satisfactorily Respond to the  
Alternate to Fill His Position  
Test Notification October 6, 2011 CR-PLP-2011-05128 ERO Staff Augmentation Test - On Call I&C Electrical Engineer Determined to be on Medical  
October 6, 2011 CR-PLP-2011-05127 ERO Staff Augmentation Test - CR Operations  
Leave October 6, 2011 CR-PLP-2011-05723 Perform Root Cause Evaluation for P-8B, Steam Driven Auxiliary Feedwater Pump, Tripping on Overspeed October 28, 2011 CR-PLP-2011-06845 Manual Reactor Trip Due to Lowering Feedwater Suction Pressure Caused by CV-
Support did Not Satisfactorily Respond to the  
0711, Feed Pump P-1A Recirculation Valve December 14, 2011 CR-PLP-2012-00165 PCS Leak Identified by Operating Crew January 7, 2012 CR-PLP-2012-00188 Control Room Requested Electrical Maintenance to Investigate Reduced Amps on Group 2 Pressurizer Heaters January 7, 2012 CR-PLP-2012-00361 Maintenance Rule Performance Criteria Exceeded for Main Feedwater System January 16, 2012 CR-PLP-2012-00455 No Maintenance Rule Evaluation Performed for Potential Failure of ELU-175 January 19, 2012 CR-PLP-2012-00499 Personnel Contamination Event While Working in the Spent Fuel Pool Area for Dry Fuel Storage  
Test Notification  
Activities January 20, 2012 CR-PLP-2012-00665 Placekeeping Not Performed During Monthly Communications Checks January 26, 2012 CR-PLP-2012-00728 Personnel Contamination Event While Working in the RCA to Issue M&TE January 31, 2012 CR-PLP-2012-00774 Missed Delivery of Replacement Power Supply Boards February 1, 2012 CR-PLP-2012-00860 Personnel Contamination Event While Performing a Peer Check for Chemistry  
October 6, 2011 CR-PLP-2011-05128 ERO Staff Augmentation Test - On Call I&C Electrical Engineer Determined to be on Medical  
Verifying Valve Positions During PCS Sampling February 6, 2012 CR-PLP-2012-00861 Personnel Contamination Event While Performing Sampling PCS and SIRWT February 6, 2012 CR-PLP-2012-00873 Fire Tours on Certain Doors Not Documented on the Fire Tour Checklist February 6, 2012 CR-PLP-2012-00895 Trend in Personnel Contamination Events. February 7, 2012 CR-PLP-2012-01073 During Annual Performance Exam Crew Failed to Accurately Classify the Event February 15, 2012 CR-PLP-2012-01775 PI-1490, K-6B Starting Air Pressure Indicator for EDG 1-2 was Reading Abnormally High March 17, 2012 CR-PLP-2012-01778 Unsatisfactory Failure Rate of New Style Diesel Generator Air Start Pressure Control Valves March 17, 2012   
 
Leave October 6, 2011 CR-PLP-2011-05723 Perform Root Cause Evaluation for P-8B, Steam Driven Auxiliary Feedwater Pump, Tripping on Overspeed  
October 28, 2011 CR-PLP-2011-06845 Manual Reactor Trip Due to Lowering  
Feedwater Suction Pressure Caused by CV-
0711, Feed Pump P-1A Recirculation Valve December 14, 2011 CR-PLP-2012-00165 PCS Leak Identified by Operating Crew January 7, 2012 CR-PLP-2012-00188 Control Room Requested Electrical  
Maintenance to Investigate Reduced Amps on Group 2 Pressurizer Heaters  
January 7, 2012 CR-PLP-2012-00361 Maintenance Rule Performance Criteria Exceeded for Main Feedwater System  
January 16, 2012 CR-PLP-2012-00455 No Maintenance Rule Evaluation Performed for  
Potential Failure of ELU-175  
January 19, 2012 CR-PLP-2012-00499 Personnel Contamination Event While Working in the Spent Fuel Pool Area for Dry Fuel Storage  
 
Activities  
January 20, 2012 CR-PLP-2012-00665 Placekeeping Not Performed During Monthly  
Communications Checks  
January 26, 2012 CR-PLP-2012-00728 Personnel Contamination Event While Working  
in the RCA to Issue M&TE  
January 31, 2012 CR-PLP-2012-00774 Missed Delivery of Replacement Power Supply  
Boards February 1, 2012 CR-PLP-2012-00860 Personnel Contamination Event While Performing a Peer Check for Chemistry  
Verifying Valve Positions During PCS Sampling  
February 6, 2012 CR-PLP-2012-00861 Personnel Contamination Event While Performing Sampling PCS and SIRWT  
February 6, 2012 CR-PLP-2012-00873 Fire Tours on Certain Doors Not Documented on the Fire Tour Checklist  
February 6, 2012 CR-PLP-2012-00895 Trend in Personnel Contamination Events. February 7, 2012 CR-PLP-2012-01073 During Annual Performance Exam Crew Failed to Accurately Classify the Event  
February 15, 2012 CR-PLP-2012-01775 PI-1490, K-6B Starting Air Pressure Indicator for EDG 1-2 was Reading Abnormally High  
March 17, 2012 CR-PLP-2012-01778 Unsatisfactory Failure Rate of New Style Diesel  
Generator Air Start Pressure Control Valves  
March 17, 2012   
  4  CR-PLP-2012-01828 Plant Drawings in Error Concerning Breakers Operated During Temporary Modification  
  4  CR-PLP-2012-01828 Plant Drawings in Error Concerning Breakers Operated During Temporary Modification  
Installation March 20, 2012 CR-PLP-2012-02044 Operation of Primary Coolant Pumps with  Inadequate Net Positive Suction Head  April 2, 2012 CR-PLP-2012-02107 Tracking CR for Correcting Configuration Errors April 2, 2012 CR-PLP-2012-02384 Inappropriate Response to a Dose Rate Alarm April 10, 2012 CR-PLP-2012-02725 Review of Turbine Driven AFW Maintenance that was Performed in October 2011 Revealed Discrepancies with the Work Order and Procedures April 16, 2012 CR-PLP-2012-02730 Review of Turbine Driven AFW Maintenance that was Performed in October 2011 Revealed  
Installation  
March 20, 2012 CR-PLP-2012-02044 Operation of Primary Coolant Pumps with  Inadequate Net Positive Suction Head  April 2, 2012 CR-PLP-2012-02107 Tracking CR for Correcting Configuration Errors April 2, 2012 CR-PLP-2012-02384 Inappropriate Response to a Dose Rate Alarm April 10, 2012 CR-PLP-2012-02725 Review of Turbine Driven AFW Maintenance that was Performed in October 2011 Revealed Discrepancies with the Work Order and  
Procedures April 16, 2012 CR-PLP-2012-02730 Review of Turbine Driven AFW Maintenance that was Performed in October 2011 Revealed  
 
Procedure Quality Issues April 16, 2012 CR-PLP-2012-02780 QA Functional Area Rating for EP is Yellow for Trimester Report Covering November 2011  
Procedure Quality Issues April 16, 2012 CR-PLP-2012-02780 QA Functional Area Rating for EP is Yellow for Trimester Report Covering November 2011  
through February 2012 April 17, 2012 CR-PLP-2012-02905 Thirteen Condition Reports Generated On-Site for Losing Control of Assigned Photo Badges in  
through February 2012 April 17, 2012 CR-PLP-2012-02905 Thirteen Condition Reports Generated On-Site for Losing Control of Assigned Photo Badges in  
the Protected Area April 19, 2012 CR-PLP-2012-03012 RPS Matrix Ladder Power Indicating Light Extinguished on Channel C RPS Cabinet July 11, 2013 CR-PLP-2012-03229 Inappropriate Response to a Dose Rate Alarm April 25, 2012 CR-PLP-2012-03313 Inappropriate Response to a Dose Rate Alarm April 27, 2012 CR-PLP-2012-03761 Fatigue Assessment Not Sent to Access Authorization for Post-Event Tests May 9, 2012 CR-PLP-2012-03782 MO-3068, Redundant HPSI Injection Valve, Would Not Move In Closed Direction May 9, 2012 CR-PLP-2012-03873 Received Control Room Alarms for SPI Trouble, 125V DC Bus Ground, and CCW Heat  
 
Exchanger Hi-Lo Temperature Unexpectedly May 14, 2012 CR-PLP-2012-03948 Could Not Locate Fatigue Assessment Paperwork May 17, 2012 CR-PLP-2012-03948 Fatigue Assessments Not Performed as Required May 17, 2012 CR-PLP-2012-04292 Two Key System Health Work Orders Moved Inside the Scope Freeze Milestone Per  
the Protected Area April 19, 2012 CR-PLP-2012-03012 RPS Matrix Ladder Power Indicating Light Extinguished on Channel C RPS Cabinet  
Engineering's Request June 5, 2012 CR-PLP-2012-04457 Radiation Protection Technician Response to Off-hours Mobilization Drill June 6, 2012 CR-PLP-2012-04690 Stop Work for Effluents for SIRW Tank Not  Recognized June 25, 2012 CR-PLP-2012-04885 SIRW Tank Observed Dripping in Main Control Room July 5, 2012 CR-PLP-2012-04921 Failure of PMT of SIRWT July 7, 2012   
July 11, 2013 CR-PLP-2012-03229 Inappropriate Response to a Dose Rate Alarm April 25, 2012 CR-PLP-2012-03313 Inappropriate Response to a Dose Rate Alarm April 27, 2012 CR-PLP-2012-03761 Fatigue Assessment Not Sent to Access Authorization for Post-Event Tests May 9, 2012 CR-PLP-2012-03782 MO-3068, Redundant HPSI Injection Valve, Would Not Move In Closed Direction May 9, 2012 CR-PLP-2012-03873 Received Control Room Alarms for SPI Trouble, 125V DC Bus Ground, and CCW Heat  
  5  CR-PLP-2012-05512 CR for MO-3068, Redundant HPSI Injection Valve, Failed to Close Not Appropriately  
Exchanger Hi-Lo Temperature Unexpectedly May 14, 2012 CR-PLP-2012-03948 Could Not Locate Fatigue Assessment  
Classified August 6, 2012 CR-PLP-2012-05832 Usable Parts Not Currently on Material Readiness List August 22, 2012 CR-PLP-2012-05849 LPIR-0101B Pressurizer Level Pressure Channel 2 Input Channel 4 Did Not Read  
Paperwork May 17, 2012 CR-PLP-2012-03948 Fatigue Assessments Not Performed as  
Correctly After Modification August 23, 2012 CR-PLP-2012-05854 Emergency Planning CFAM Performance Indicator for Defense-in Depth Turned Red as of July PI Data August 23, 2012 CR-PLP-2012-05893 After Replacement of New Power Supplies, "A" Channel of RPS Failed to Pass PMT August 25, 2012 CR-PLP-2012-05894 New Power Supplies Would Not Pass PMT August 25, 2012 CR-PLP-2012-06069 An Existing Degraded Fire Barrier is Only Marginally Acceptable September, 2012 CR-PLP-2012-06382 Junction Box J91 Not Protected Against External Flooding September 25, 2012 CR-PLP-2012-06404 Potential Release of Low Level Radioactive Material September 26, 2012 CR-PLP-2012-06899 Palisades May Not Be Out of Industry Norm for Containment Work Performed Online October 25, 2012 CR-PLP-2012-07003 Shift Managers Inaccurate EP Classifications November 1, 2012 CR-PLP-2012-07010 RP Fundamental Techniques Not Followed November 1, 2012 CR-PLP-2012-07047 Steam/Water Pin Hole Leak on Inlet Socket Weld Side of MV-MS526, E-50B ASDV CV-0779  
Required May 17, 2012 CR-PLP-2012-04292 Two Key System Health Work Orders Moved Inside the Scope Freeze Milestone Per  
Inlet Drain Valve November 4, 2012 CR-PLP-2012-07140 Leaks That Impacted Plant Operations By Causing Shutdowns or Forced Outages November 8, 2012 CR-PLP-2012-07348 Limited Repair of Underground Pipe Leak and Incomplete Risk Assessment of Underground  
Engineering's Request June 5, 2012 CR-PLP-2012-04457 Radiation Protection Technician Response to Off-hours Mobilization Drill June 6, 2012 CR-PLP-2012-04690 Stop Work for Effluents for SIRW Tank Not  Recognized June 25, 2012 CR-PLP-2012-04885 SIRW Tank Observed Dripping in Main Control  
Room July 5, 2012 CR-PLP-2012-04921 Failure of PMT of SIRWT July 7, 2012   
  5  CR-PLP-2012-05512 CR for MO-3068, Redundant HPSI Injection  
Valve, Failed to Close Not Appropriately  
Classified August 6, 2012 CR-PLP-2012-05832 Usable Parts Not Currently on Material Readiness List August 22, 2012 CR-PLP-2012-05849 LPIR-0101B Pressurizer Level Pressure  
Channel 2 Input Channel 4 Did Not Read  
 
Correctly After Modification August 23, 2012 CR-PLP-2012-05854 Emergency Planning CFAM Performance Indicator for Defense-in Depth Turned Red as of  
July PI Data August 23, 2012 CR-PLP-2012-05893 After Replacement of New Power Supplies, "A"  
Channel of RPS Failed to Pass PMT August 25, 2012 CR-PLP-2012-05894 New Power Supplies Would Not Pass PMT August 25, 2012 CR-PLP-2012-06069 An Existing Degraded Fire Barrier is Only Marginally Acceptable  
September, 2012 CR-PLP-2012-06382 Junction Box J91 Not Protected Against  
External Flooding September 25, 2012 CR-PLP-2012-06404 Potential Release of Low Level Radioactive  
Material September 26, 2012 CR-PLP-2012-06899 Palisades May Not Be Out of Industry Norm for Containment Work Performed Online  
October 25, 2012 CR-PLP-2012-07003 Shift Managers Inaccurate EP Classifications November 1, 2012 CR-PLP-2012-07010 RP Fundamental Techniques Not Followed November 1, 2012 CR-PLP-2012-07047 Steam/Water Pin Hole Leak on Inlet Socket Weld Side of MV-MS526, E-50B ASDV CV-0779  
 
Inlet Drain Valve November 4, 2012 CR-PLP-2012-07140 Leaks That Impacted Plant Operations By  
Causing Shutdowns or Forced Outages November 8, 2012 CR-PLP-2012-07348 Limited Repair of Underground Pipe Leak and Incomplete Risk Assessment of Underground  
Piping and Tanks November 21, 2012 CR-PLP-2012-07351 Reductions in Source Term and CRE Ineffective November 21, 2012 CR-PLP-2012-07430 One Member of On Duty ERO Team (TSC Security Coordinator) Did Not Respond During  
Piping and Tanks November 21, 2012 CR-PLP-2012-07351 Reductions in Source Term and CRE Ineffective November 21, 2012 CR-PLP-2012-07430 One Member of On Duty ERO Team (TSC Security Coordinator) Did Not Respond During  
Quarterly Augmentation Test November 28, 2012 CR-PLP-2012-07617 Replacement Impellers for the Primary Coolant Pump Oversized December 7, 2012 CR-PLP-2012-07685 The Ratio of Oil Drained to Oil Added was Outside of Acceptance Criteria December 12, 2012 CR-PLP-2013-00158 Timeliness of the Immediate Operability for the  Small Steam Leak Discovered Near MV-MS526,  
Quarterly Augmentation Test November 28, 2012 CR-PLP-2012-07617 Replacement Impellers for the Primary Coolant Pump Oversized December 7, 2012 CR-PLP-2012-07685 The Ratio of Oil Drained to Oil Added was Outside of Acceptance Criteria December 12, 2012 CR-PLP-2013-00158 Timeliness of the Immediate Operability for the  Small Steam Leak Discovered Near MV-MS526,  
'B" S/G Atmospheric Steam Dump Drain Isolation January 14, 2013   
'B" S/G Atmospheric Steam Dump Drain Isolation  
January 14, 2013   
  6  CR-PLP-2013-00422 Work Orders in "Finish" Greater Than 30 Days are Not Being Routed Back to the Technical  
  6  CR-PLP-2013-00422 Work Orders in "Finish" Greater Than 30 Days are Not Being Routed Back to the Technical  
Specification Surveillance Coordinator in a  
Specification Surveillance Coordinator in a  
Timely Fashion January 30, 2013 CR-PLP-2013-00460 Critical Group Re-Investigation Expired February 1, 2013 CR-PLP-2013-00656 Entered LCO for Component Cooling Water Systems Due to Indications of a CCW Leak on  
 
Timely Fashion  
January 30, 2013 CR-PLP-2013-00460 Critical Group Re-Investigation Expired February 1, 2013 CR-PLP-2013-00656 Entered LCO for Component Cooling Water Systems Due to Indications of a CCW Leak on  
 
E-54A, Component Cooling Water Heat  
E-54A, Component Cooling Water Heat  
Exchanger February 14, 2013 CR-PLP-2013-01017 Changing System Software on Security Computer System Impacted the Ability to Receive Alarms March 6, 2013 CR-PLP-2013-01023 During 2013 First ERO Staff Augmentation Test the JIC Inquiry Responder Did Not Satisfactorily Respond to the Test March 7, 2013 CR-PLP-2013-01025 During 2013 First ERO Staff Augmentation Test the OSC Mechanical Coordinator Did Not  
 
Satisfactorily Respond to the Test March 7, 2013 CR-PLP-2013-01026 During 2013 First ERO Staff Augmentation Test the EOF Security Coordinator Did Not  
Exchanger  
Satisfactorily Respond to the Test March 7, 2013 CR-PLP-2013-01213 Administrative Issues Identified in EC 20082 and EC 37737 March 20, 2013 CR-PLP-2013-01446 Track CR for Correcting Configuration Errors April 1, 2013 CR-PLP-2013-01882 Preventive Maintenance Work Will Be Performed Late for CK-DMW400 April 26, 2013 CR-PLP-2013-02095 New +12 Vdc Test Power Supply Found to Adversely Affect the Alpha Channel Bistable  
February 14, 2013 CR-PLP-2013-01017 Changing System Software on Security Computer System Impacted the Ability to  
Receive Alarms  
March 6, 2013 CR-PLP-2013-01023 During 2013 First ERO Staff Augmentation Test  
the JIC Inquiry Responder Did Not Satisfactorily Respond to the Test  
March 7, 2013 CR-PLP-2013-01025 During 2013 First ERO Staff Augmentation Test the OSC Mechanical Coordinator Did Not  
Satisfactorily Respond to the Test  
March 7, 2013 CR-PLP-2013-01026 During 2013 First ERO Staff Augmentation Test the EOF Security Coordinator Did Not  
Satisfactorily Respond to the Test  
March 7, 2013 CR-PLP-2013-01213 Administrative Issues Identified in EC 20082 and  
EC 37737  
March 20, 2013 CR-PLP-2013-01446 Track CR for Correcting Configuration Errors April 1, 2013 CR-PLP-2013-01882 Preventive Maintenance Work Will Be Performed Late for CK-DMW400 April 26, 2013 CR-PLP-2013-02095 New +12 Vdc Test Power Supply Found to Adversely Affect the Alpha Channel Bistable  
 
Setpoints May 9, 2013 CR-PLP-2013-02158 Part 21 Evaluation Not Rigorous Enough to Support Conclusions and Not Addressing All  
Setpoints May 9, 2013 CR-PLP-2013-02158 Part 21 Evaluation Not Rigorous Enough to Support Conclusions and Not Addressing All  
Issues Raised May 13, 2013 CR-PLP-2013-02644 Overspeed Testing of P-8B was Not Successful with Newly Installed Parts June 15, 2013 CR-PLP-2013-02802 Fuel Oil Transfer System Delay in Discharge Pressure Increase June 25, 2013 CR-PLP-2013-02831 Quality Assurance Escalation on the Timeliness/Effectiveness of Correcting QA Identified Issues June 7, 2013 CR-PLP-2013-02959 During Quarterly ERO Staff Augmentation Test a Member of the ERO Team (OSC RAD/Chem Coordinator) Did Not Respond  July 9, 2013 CR-PLP-2013-02982 Aux Feedwater AFAS-FOFF Subsystem Trip Unexpectedly July 9, 2013 CR-PLP-2013-02982 Received Alarm EK-0137, Aux Feedwater AFAS-FOGG Subsystem Trip, Unexpectedly  July 9, 2013 CR-PLP-2013-03001 Power Supply P/S-0704 was Removed Following Failure  July 10, 2013   
 
Issues Raised May 13, 2013 CR-PLP-2013-02644 Overspeed Testing of P-8B was Not Successful with Newly Installed Parts June 15, 2013 CR-PLP-2013-02802 Fuel Oil Transfer System Delay in Discharge Pressure Increase June 25, 2013 CR-PLP-2013-02831 Quality Assurance Escalation on the Timeliness/Effectiveness of Correcting QA  
Identified Issues June 7, 2013 CR-PLP-2013-02959 During Quarterly ERO Staff Augmentation Test a Member of the ERO Team (OSC RAD/Chem Coordinator) Did Not Respond   
July 9, 2013 CR-PLP-2013-02982 Aux Feedwater AFAS-FOFF Subsystem Trip  
Unexpectedly  
July 9, 2013 CR-PLP-2013-02982 Received Alarm EK-0137, Aux Feedwater AFAS-FOGG Subsystem Trip, Unexpectedly   
July 9, 2013 CR-PLP-2013-03001 Power Supply P/S-0704 was Removed Following Failure   
July 10, 2013   
  7  CR-PLP-2013-03002 FIN TEAM Electrician Did Not Complete Required Computer Based Training by Due  
  7  CR-PLP-2013-03002 FIN TEAM Electrician Did Not Complete Required Computer Based Training by Due  
Date July 10, 2013 CR-PLP-2013-03025 RPS Matrix "CD" Power Indication Light Extinguished on C-06 July 11, 2013 CR-PLP-2013-03026 Power Supply P/S-CW8-15 was Removed From the RPS Following a Failure July 11, 2013 CR-PLP-2013-03063 Received Alarm for AFAS-FOGG Subsystem Trip Unexpectedly July 15, 2013 CR-PLP-2013-03103 Security Force Member Failed to Shoot Qualifying Score July 17, 2013 CR-PLP-2013-03136 NRC Identified Issue - ALARA Planning for SFP Rerack Failed to Identify Alpha Level 3  
 
Contamination  July 18, 2013 CR-PLP-2013-03137 NRC Identified Issue - Individual Working on the SFP Rerack Not Wearing a Lapel July 18, 2013 CR-PLP-2013-03155 Missing Rifle Magazine Rounds July 19, 2013 CR-PLP-2013-03298 Received Unexpected AFAS-FOGG Alarms July 31, 2013 CR-PLP-2013-03523 Door 15, Equipment Room Missile Shield/Radiation Door, Was Unable to Be  
Date July 10, 2013 CR-PLP-2013-03025 RPS Matrix "CD" Power Indication Light  
Closed August 13, 2013 CR-PLP-2013-03683 Exceeded Maintenance Rule Criteria for Auxiliary Feedwater Actuation System (AFAS) August 21, 2013 CR-PLP-2013-03838 During Third Quarter ERO Staff Augmentation Test the Designated EOF Van Buren County  
Extinguished on C-06  
July 11, 2013 CR-PLP-2013-03026 Power Supply P/S-CW8-15 was Removed From  
the RPS Following a Failure  
July 11, 2013 CR-PLP-2013-03063 Received Alarm for AFAS-FOGG Subsystem Trip Unexpectedly  
July 15, 2013 CR-PLP-2013-03103 Security Force Member Failed to Shoot  
Qualifying Score  
July 17, 2013 CR-PLP-2013-03136 NRC Identified Issue - ALARA Planning for SFP Rerack Failed to Identify Alpha Level 3  
 
Contamination   
July 18, 2013 CR-PLP-2013-03137 NRC Identified Issue - Individual Working on the  
SFP Rerack Not Wearing a Lapel  
July 18, 2013 CR-PLP-2013-03155 Missing Rifle Magazine Rounds July 19, 2013 CR-PLP-2013-03298 Received Unexpected AFAS-FOGG Alarms July 31, 2013 CR-PLP-2013-03523 Door 15, Equipment Room Missile  
Shield/Radiation Door, Was Unable to Be  
 
Closed August 13, 2013 CR-PLP-2013-03683 Exceeded Maintenance Rule Criteria for  
Auxiliary Feedwater Actuation System (AFAS) August 21, 2013 CR-PLP-2013-03838 During Third Quarter ERO Staff Augmentation  
Test the Designated EOF Van Buren County  
 
Liaison Failed to Respond  August 29, 2013 CR-PLP-2013-03839 During Third Quarter ERO Staff Augmentation Test the Designated TSC Reactor Engineer  
Liaison Failed to Respond  August 29, 2013 CR-PLP-2013-03839 During Third Quarter ERO Staff Augmentation Test the Designated TSC Reactor Engineer  
Provided a 45 Minute Response  August 29, 2013 CR-PLP-2013-03840 During Third Quarter ERO Staff Augmentation Test One Designated Non-traditional Radiation Protection Technic Failed to Respond to the Test  August 29, 2013 CR-PLP-2013-04246 Power Supplies Received from Vendor Had a Damaged Component September 27, 2013 CR-PLP-2013-04391 Potential Trend in Vital Area Doors Found Unsecured October 8, 2013 CR-PLP-2013-04405 Key System Health Work Order was Not Completed per the Schedule October 9, 2013 CR-PLP-2013-04462 71 Licensed Operator Requalification Tasks Selected for Continuing Training Have Not Been  
Provided a 45 Minute Response  August 29, 2013 CR-PLP-2013-03840 During Third Quarter ERO Staff Augmentation Test One Designated Non-traditional Radiation Protection Technic Failed to Respond to the  
Trained on Within Their Prescribed Frequencies October 15, 2013 CR-PLP-2013-04802 Crack in a Turbocharger Support Weld for Emergency Diesel Generator 1-1 November 6, 2013 CR-PLP-2013-04817 Operating Experience Review Revealed Possible Secondary Fire Could Be Caused in  
Test  August 29, 2013 CR-PLP-2013-04246 Power Supplies Received from Vendor Had a  
Damaged Component September 27, 2013 CR-PLP-2013-04391 Potential Trend in Vital Area Doors Found  
Unsecured  
October 8, 2013 CR-PLP-2013-04405 Key System Health Work Order was Not  
Completed per the Schedule  
October 9, 2013 CR-PLP-2013-04462 71 Licensed Operator Requalification Tasks Selected for Continuing Training Have Not Been  
Trained on Within Their Prescribed Frequencies  
October 15, 2013 CR-PLP-2013-04802 Crack in a Turbocharger Support Weld for Emergency Diesel Generator 1-1 November 6, 2013 CR-PLP-2013-04817 Operating Experience Review Revealed Possible Secondary Fire Could Be Caused in  
the Cable Spreading Room By a Short in the Station Battery Room November 7, 2013   
the Cable Spreading Room By a Short in the Station Battery Room November 7, 2013   
  8  CR-PLP-2013-05166 ALARA Planning and Controls Green Finding December 6, 2013 CR-PLP-2013-05176 NRC Debriefed Three Green NCVs December 8, 2013 CR-PLP-2013-05278 Potential Multiple Leak Locations Originating from the Irrigation Header Isolation Line in the  
  8  CR-PLP-2013-05166 ALARA Planning and Controls Green Finding December 6, 2013 CR-PLP-2013-05176 NRC Debriefed Three Green NCVs December 8, 2013 CR-PLP-2013-05278 Potential Multiple Leak Locations Originating from the Irrigation Header Isolation Line in the  
Screen House December 14, 2013 CR-PLP-2014-00022 Palisades Security SCWE Action Plan January 1, 2014 CR-PLP-2014-00687 Electronic Dosimeter Issue January 26, 2014 CR-PLP-2014-01193 Substantial Accumulation of Ooze, Sludge, and Bioslimes were Discovered Inside of Piping February 8, 2014 CR-PLP-2014-01195 Missed Inspection of Opportunity February 8, 2014 CR-PLP-2014-01359 No Materials Ordered Resulting in Delay to Perform Work Order February 14, 2013 CR-PLP-2014-02656 Violations of EN-OM-123 Fatigue Management Program April 19, 2014 CR-PLP-2014-02856 Installed Flexitallic Style R Gasket Had Significantly Deteriorated May 1, 2014 CR-PLP-2014-02863 Gasket Supplied for Work was Incorrect May 2, 2014 CR-PLP-2014-02864 Slight Over Crush of the B/B Gasket May 2, 2014 LR-LAR-2012-00211 SIRW Tank CAL Items August 1, 2012 WT-WTPLP-2012-00425 Ensure Electrical and I&C Supervision Periodically Discuss the Importance of 30 Min Responder Responsibilities December 21, 2012 WT-WTPLP-2014-00022 Security SCWE Action Plan January 15, 2014  Apparent Cause Evaluation CR-PLP 2012-04457 HT-ACE Insufficient Radiation Protection Technician 30 Minute Response for the Off-Hours Mobilization  
 
Screen House December 14, 2013 CR-PLP-2014-00022 Palisades Security SCWE Action Plan January 1, 2014 CR-PLP-2014-00687 Electronic Dosimeter Issue January 26, 2014 CR-PLP-2014-01193 Substantial Accumulation of Ooze, Sludge, and Bioslimes were Discovered Inside of Piping  
February 8, 2014 CR-PLP-2014-01195 Missed Inspection of Opportunity February 8, 2014 CR-PLP-2014-01359 No Materials Ordered Resulting in Delay to Perform Work Order  
February 14, 2013 CR-PLP-2014-02656 Violations of EN-OM-123 Fatigue Management  
Program April 19, 2014 CR-PLP-2014-02856 Installed Flexitallic Style R Gasket Had Significantly Deteriorated May 1, 2014 CR-PLP-2014-02863 Gasket Supplied for Work was Incorrect May 2, 2014 CR-PLP-2014-02864 Slight Over Crush of the B/B Gasket May 2, 2014 LR-LAR-2012-00211 SIRW Tank CAL Items August 1, 2012  
WT-WTPLP-2012-
00425 Ensure Electrical and I&C Supervision Periodically Discuss the Importance of 30 Min  
Responder Responsibilities December 21, 2012  
WT-WTPLP-2014-
00022 Security SCWE Action Plan January 15, 2014  
  Apparent Cause Evaluation
CR-PLP 2012-04457 HT-ACE Insufficient Radiation Protection Technician 30 Minute Response for the Off-Hours Mobilization  
 
Drill July 12, 2012 CR-PLP-2011-06130 Operations Human Performance Standards December 7, 2011 CR-PLP-2012-00362 NRC Unplanned Scrams per 7,000 Critical Hours Indicator is White as a Result of Four  
Drill July 12, 2012 CR-PLP-2011-06130 Operations Human Performance Standards December 7, 2011 CR-PLP-2012-00362 NRC Unplanned Scrams per 7,000 Critical Hours Indicator is White as a Result of Four  
Reactor Trips February 14, 2012 CR-PLP-2012-01073 Annual Operator Licensing Exam EAL Classification Failures February 15, 2012 CR-PLP-2012-01073  HT-ACE Annual Operator Licensing Exam EAL Classification Failures March 12, 2012 CR-PLP-2012-01482 HT Apparent Cause Evaluation Report for Chemical Control Program Cause/Corrective  
 
Reactor Trips  
February 14, 2012 CR-PLP-2012-01073 Annual Operator Licensing Exam EAL Classification Failures  
February 15, 2012 CR-PLP-2012-01073  HT-ACE Annual Operator Licensing Exam EAL Classification Failures  
March 12, 2012 CR-PLP-2012-01482 HT Apparent Cause Evaluation Report for  
Chemical Control Program Cause/Corrective  
Action and Chemistry Department ACE Quality  
Action and Chemistry Department ACE Quality  
Issues August 25, 2012   
Issues August 25, 2012   
  9  CR-PLP-2012-01775 Higher Tier Apparent Cause Evaluation:  PI-1490, K-6B Starting Air Pressure Indicator for  
  9  CR-PLP-2012-01775 Higher Tier Apparent Cause Evaluation:  PI-1490, K-6B Starting Air Pressure Indicator for  
Line 393: Line 696:
Reading Abnormally High June 18, 2012 CR-PLP-2012-03873 Level 1 Human Performance Evaluation Review:  CCW Surge Tank Fill CV Doesn't Turn On Red  
Reading Abnormally High June 18, 2012 CR-PLP-2012-03873 Level 1 Human Performance Evaluation Review:  CCW Surge Tank Fill CV Doesn't Turn On Red  
Light When Open (WR #271959) May 16, 2012 CR-PLP-2012-03948 Level 2 Human Performance Error Review:  Fatigue Assessment Not Performed in Post-Event Response May 24, 2012 CR-PLP-2012-04457 Insufficient Radiation Protection Technician 30 Minute Response for the Off-Hours Mobilization  
Light When Open (WR #271959) May 16, 2012 CR-PLP-2012-03948 Level 2 Human Performance Error Review:  Fatigue Assessment Not Performed in Post-Event Response May 24, 2012 CR-PLP-2012-04457 Insufficient Radiation Protection Technician 30 Minute Response for the Off-Hours Mobilization  
Drill July 12, 2012 CR-PLP-2012-06454 HT-Apparent Cause Evaluation Report for Maintenance Department Procedure Use and  
Drill July 12, 2012 CR-PLP-2012-06454 HT-Apparent Cause Evaluation Report for Maintenance Department Procedure Use and  
Adherence December 5, 2012 CR-PLP-2012-07348 Lower Tier Apparent Cause Evaluation:  Limited Repair of Underground Pipe Leak and  
Adherence December 5, 2012 CR-PLP-2012-07348 Lower Tier Apparent Cause Evaluation:  Limited Repair of Underground Pipe Leak and  
Incomplete Risk Assessment of Underground Piping and Tanks January 16, 2013 CR-PLP-2013-00460 Lower Tier Apparent Cause Evaluation:  Critical Group Re-Investigation Expired February 20, 2013 CR-PLP-2013-02982 Lower Tier Apparent Cause Evaluation:  P/S-0704 Failure April 15, 2014 CR-PLP-2013-03063 Lower Tier Apparent Cause Evaluation:  Failure of AFAS Optical Isolator August 13, 2013 CR-PLP-2013-03650 Operations OJT/TPE Practice Issues October 15, 2013 CR-PLP-2014-00589 Level 1 Human Performance Evaluation: Security Compensatory Measures Not in Place  
Incomplete Risk Assessment of Underground Piping and Tanks  
as Required January 26, 2014 CR-PLP-2014-02461 Equipment Apparent Cause Evaluation:  E-22B; Unexpected Discovery of ID Pitting on Recently Replaced Jacket Water Heat Exchanger May 7, 2014  Common Cause Evaluation CR-PLP-2012-02905 Negative Trend Relating to the Control of Security Keycards in Controlled Areas May 5, 2012 CR-PLP-2012-05861 Common Cause Analysis for Possible Emerging Trend for Procedural Compliance in Respiratory  
January 16, 2013 CR-PLP-2013-00460 Lower Tier Apparent Cause Evaluation:  Critical Group Re-Investigation Expired  
February 20, 2013 CR-PLP-2013-02982 Lower Tier Apparent Cause Evaluation:  P/S-0704 Failure April 15, 2014 CR-PLP-2013-03063 Lower Tier Apparent Cause Evaluation:  Failure of AFAS Optical Isolator August 13, 2013 CR-PLP-2013-03650 Operations OJT/TPE Practice Issues October 15, 2013 CR-PLP-2014-00589 Level 1 Human Performance Evaluation: Security Compensatory Measures Not in Place  
 
as Required  
January 26, 2014 CR-PLP-2014-02461 Equipment Apparent Cause Evaluation:  E-22B; Unexpected Discovery of ID Pitting on Recently Replaced Jacket Water Heat Exchanger May 7, 2014  
  Common Cause Evaluation
CR-PLP-2012-02905 Negative Trend Relating to the Control of Security  
Keycards in Controlled Areas May 5, 2012 CR-PLP-2012-05861 Common Cause Analysis for Possible Emerging Trend for Procedural Compliance in Respiratory  
Protection. September 17, 2012 CR-PLP-2012-07140 Palisades Leaks That Resulted In or Extended Forced Outages in June 2012 Through November  
Protection. September 17, 2012 CR-PLP-2012-07140 Palisades Leaks That Resulted In or Extended Forced Outages in June 2012 Through November  
2012 December 6, 2012 CR-PLP-2013-03457 Common Cause Analysis for Cross-Cutting Aspect H.2.c, Human Performance, NRC Findings July 28, 2013 CR-PLP-2013-03533 Unplanned Entries into TS LCO Action Statements August 13, 2013   
 
  10  CR-PLP-2013-04391 Trend in Vital Area Doors Found Unsecured December 17, 2013  Audit, Assessment, and Self-Assessments LO-PLPLO-2011-0101 Effectiveness Reviews of RCE CR-PLP-2011-5723 November 10, 2011 LO-PLPLO-2012-00037 Snapshot Assessment of DPRMs and Coaching Quality in Radiation Protection March 29, 2012 LO-PLPLO-2012-00051 Snapshot Assessment of  Use of EAL Basis Document, and Causes of Untimely or  
2012 December 6, 2012 CR-PLP-2013-03457 Common Cause Analysis for Cross-Cutting Aspect H.2.c, Human Performance, NRC Findings  
Inaccurate EAL Classifications May 8, 2012 LO-PLPLO-2012-00084 Effectiveness Review of CR-PLP-2012-3873 (1 Year Snapshot) March 17, 2014 LO-PLPLO-2012-00084 Effectiveness Reviews for Root Cause Evaluation Completed Under CR-PLP-2012-
July 28, 2013 CR-PLP-2013-03533 Unplanned Entries into TS LCO Action  
3873 June 12, 2012 LO-PLPLO-2012-00106 Snapshot Assessment of Power Air Purifying Respirator Issues September 10, 2012 LO-PLPLO-2012-00117 Snapshot Assessment - Plant Status and Configuration Control November 3, 2012 LO-PLPLO-2012-00121 IST Program Focused Self-Assessment May 20, 2013 LO-PLPLO-2012-00122 Electrical Work Practices May 17, 2013 LO-PLPLO-2012-00125 Snapshot Assessment on OBJ 5 (OJT-TPE) November 3, 2012 LO-PLPLO-2012-00169-00003 Chemistry Trending Program January 19, 2013 LO-PLPLO-2012-00176 Perform Crew Assessment, in Accordance with EN-OP-117, Operations Assessments, of  
Statements August 13, 2013   
  10  CR-PLP-2013-04391 Trend in Vital Area Doors Found Unsecured December 17, 2013  
   Audit, Assessment, and Self-Assessments
LO-PLPLO-2011-0101 Effectiveness Reviews of RCE CR-PLP-2011-
5723 November 10, 2011 LO-PLPLO-2012-00037 Snapshot Assessment of DPRMs and  
Coaching Quality in Radiation Protection  
March 29, 2012 LO-PLPLO-2012-00051 Snapshot Assessment of  Use of EAL Basis Document, and Causes of Untimely or  
Inaccurate EAL Classifications May 8, 2012 LO-PLPLO-2012-00084 Effectiveness Review of CR-PLP-2012-3873  
(1 Year Snapshot)  
March 17, 2014 LO-PLPLO-2012-00084 Effectiveness Reviews for Root Cause  
Evaluation Completed Under CR-PLP-2012-
 
3873 June 12, 2012 LO-PLPLO-2012-00106 Snapshot Assessment of Power Air Purifying  
Respirator Issues September 10, 2012 LO-PLPLO-2012-00117 Snapshot Assessment - Plant Status and  
Configuration Control November 3, 2012 LO-PLPLO-2012-00121 IST Program Focused Self-Assessment May 20, 2013 LO-PLPLO-2012-00122 Electrical Work Practices May 17, 2013 LO-PLPLO-2012-00125 Snapshot Assessment on OBJ 5 (OJT-TPE) November 3, 2012 LO-PLPLO-2012-00169-
00003 Chemistry Trending Program January 19, 2013 LO-PLPLO-2012-00176 Perform Crew Assessment, in Accordance  
with EN-OP-117, Operations Assessments, of  
 
Shift 5 November 15, 2012 LO-PLPLO-2013-00015 Snapshot Self-Assessment:  Fatigue Assessments Due to Post Event/For-Cause  
Shift 5 November 15, 2012 LO-PLPLO-2013-00015 Snapshot Self-Assessment:  Fatigue Assessments Due to Post Event/For-Cause  
Testing March 26, 2013 LO-PLPLO-2013-00028 Rework Program Snapshot Assessment July 10, 2013 LO-PLPLO-2013-00042 Tendon Selection Criteria Benchmark July 29, 2013 LO-PLPLO-2013-00069 Follow-up Snapshot Assessment for CR-PLP-2013-4462 - Some Licensed Operator Tasks Selected for Continuing Training Were not  
Testing March 26, 2013 LO-PLPLO-2013-00028 Rework Program Snapshot Assessment July 10, 2013 LO-PLPLO-2013-00042 Tendon Selection Criteria Benchmark July 29, 2013 LO-PLPLO-2013-00069 Follow-up Snapshot Assessment for CR-PLP-
Presented Within Required Periodicity December 12, 2013 LO-PLPPLO-2012-00003 Operations Training January 5, 2012 LO-PLPPLO-2012-00048 Snapshot Assessment Critical Steps in Operations Procedures May 5, 2012 LO-PLPPLO-2014-00076 Snapshot Assessment of Accredited Training March 5, 2014   
2013-4462 - Some Licensed Operator Tasks Selected for Continuing Training Were not  
  11  PL-PLPLO-2012-00083 5 Year Periodic Self-Assessment November 2, 2013 QA-2012-PLP-013 Quality Assurance Surveillance Report May 4, 2012 QA-3-2013-PLP-01 Corrective Action Program August 1, 2013 QA-7-2013-PLP-01 Emergency Plan July 1, 2013  Miscellaneous 10CFR50.54(q) Evaluation for Relocation of One of the Two Emergency Van to the EOF July 26, 2012 Backshift Mobilization Drill Results Overall Response Report June 15, 2009 CCW, DG 1-1 & 1-2 and Fire Water System Report Various Dates Maintenance, Operations, and Radiation Protection Safety Culture Survey April 2014 NRC Exit Notes for RP Radiation Monitoring/Radiological Hazard Assessment/ ALARA Planning Inspection. December 6, 2013 Palisades Condition Prescreening Meeting Package Various Dates Palisades Condition Review Group Meeting Package Various Dates Palisades Correction Action Review Board Meeting Package May 8, 2014 Palisades ECP Informal Benchmark Report April 2014 Palisades Maintenance Rule Periodic Assessment October 20, 2011 Palisades Maintenance Rule Periodic Assessment June 4, 2013 Palisades Nuclear Plant Quarterly Trend Reports  1Q2012 through 4Q2013 Palisades Security SCWE Action Plan May 9, 2014 Palisades Self-Assessment Review Board Meeting Package May 6, 2014 Palisades Spent Fuel Pool Leakage Trend April 2012 - Present Plant Health Committee Meeting Package May 19, 2014 PLP CRG Summary Agenda Report Prescreen May 9, 2014 Quarterly Augmentation Tests of the NRO Notification System  
 
(Everbridge) Various Security Work Hour Violation/Waiver Report April 1, 2013 -  May 21, 2014 BOP-UT-14-012 UT Erosion/Corrosion Examination for HB-23-4-P1836 February 19, 2014 BOP-UT-14-012 UT Erosion/Corrosion Examination for HB-23-116-P1827 February 19, 2014   
Presented Within Required Periodicity December 12, 2013 LO-PLPPLO-2012-00003 Operations Training January 5, 2012 LO-PLPPLO-2012-00048 Snapshot Assessment Critical Steps in  
Operations Procedures May 5, 2012 LO-PLPPLO-2014-00076 Snapshot Assessment of Accredited Training March 5, 2014   
  11  PL-PLPLO-2012-00083 5 Year Periodic Self-Assessment November 2, 2013 QA-2012-PLP-013 Quality Assurance Surveillance Report May 4, 2012 QA-3-2013-PLP-01 Corrective Action Program August 1, 2013 QA-7-2013-PLP-01 Emergency Plan July 1, 2013  
   Miscellaneous
10CFR50.54(q) Evaluation for Relocation of One of the Two Emergency Van to the EOF  
July 26, 2012 Backshift Mobilization Drill Results Overall Response Report June 15, 2009 CCW, DG 1-1 & 1-2 and Fire Water System Report Various Dates Maintenance, Operations, and Radiation Protection Safety Culture Survey April 2014 NRC Exit Notes for RP Radiation Monitoring/Radiological Hazard Assessment/ ALARA Planning Inspection. December 6, 2013 Palisades Condition Prescreening Meeting Package Various Dates Palisades Condition Review Group Meeting Package Various Dates Palisades Correction Action Review Board Meeting Package May 8, 2014 Palisades ECP Informal Benchmark Report April 2014 Palisades Maintenance Rule Periodic Assessment October 20, 2011 Palisades Maintenance Rule Periodic Assessment June 4, 2013 Palisades Nuclear Plant Quarterly Trend Reports  1Q2012 through  
4Q2013 Palisades Security SCWE Action Plan May 9, 2014 Palisades Self-Assessment Review Board Meeting Package May 6, 2014 Palisades Spent Fuel Pool Leakage Trend April 2012 - Present Plant Health Committee Meeting Package May 19, 2014 PLP CRG Summary Agenda Report Prescreen May 9, 2014 Quarterly Augmentation Tests of the NRO Notification System  
 
(Everbridge)  
Various Security Work Hour Violation/Waiver Report April 1, 2013 -  May 21, 2014 BOP-UT-14-012 UT Erosion/Corrosion Examination for HB-23-4-
P1836 February 19, 2014 BOP-UT-14-012 UT Erosion/Corrosion Examination for HB-23-116-
P1827 February 19, 2014   
  12  BOP-UT-14-013 UT Erosion/Corrosion Examination for KB-1-P176 February 19, 2014 CR-PLP-2013-04677 HUE Human Performance Evaluation - Supplemental RP Tech Left a Suspended Empty Fuel Rack in the SFP Unattended, Creating a Potential Locked  
  12  BOP-UT-14-013 UT Erosion/Corrosion Examination for KB-1-P176 February 19, 2014 CR-PLP-2013-04677 HUE Human Performance Evaluation - Supplemental RP Tech Left a Suspended Empty Fuel Rack in the SFP Unattended, Creating a Potential Locked  
High Radiation Area Condition October 29, 2013 Drawing C-38 Field Erected Tanks, Sheet 2 Revision 9 Drawing C-539 Cellular Slab Repair Plan of Control Room Roof EL 643'-0"  Revision C Drawing E-44 Lighting Panel Schedule L-35, Sheet 115A Revision 5 EC 27632 Perform an Evaluation of Inspection Opportunities Prior to License Renewal Per Commitment LO-
High Radiation Area Condition  
LAR-2009-244-38 March 17, 2011 EC 38728 Raw Water Corrosion Program Report - Operational Cycle 22 and 2012 Refueling Outage January 14, 2014 LER 2011-004-01 Turbine-Driven Auxiliary Feedwater Pump Inoperable in Excess of Technical Specification Requirements Due to Unexpected Trip January 31, 2012 LER 2011-005-00 Service Water Pump Shaft Coupling Failure October 3, 2011 LER 2011-006 Valve Packing Failure Resulted in Reactor Trip and Auxiliary Feedwater System Actuation November 10, 2011 LER 2011-007 Direct Current Electrical System Fault Causes Reactor Trip and Multiple Safety System Actuations November 21, 2011 LER 2011-008 Reactor Protection System and Auxiliary Feedwater System Actuation February 3, 2012 LER 2012-002-00 Technical Specification Required Shutdown Due to Un-isolable Secondary Side Drain Valve Leak December 20, 2012 LER 2013-001 Technical Specification Required Shutdown Due to a Component Cooling Water System Leak April 15, 2013 LER 2013-003-01 Both Control Room Ventilation Filtration Trains Declared Inoperable October 11, 2013 LER 2013-004-00 Discovery of Latent Design Deficiency Results in Non-Compliance with 10CFR50 Appendix R  January 6, 2014 PL-ERO-NTRP010 Lesson Plan - RPT ERO Duties  Revision 0 PLLP-LOR-12B-03 Emergency Event Classification Revision 0 PNP 2013-044 License Amendment Request to Revise Emergency Response Organization Staff  
October 29, 2013 Drawing C-38 Field Erected Tanks, Sheet 2 Revision 9 Drawing C-539 Cellular Slab Repair Plan of Control Room Roof  
Augmentation Response Times June 25, 2013 RWP 2012-0319 Repair of CRD-24 Housing Various Revisions Work Order 177025 P-52C, Remove/Inspection Inboard Pump Bearing Outer Flinger June 3, 2014 Work Order 318169 PI-1489 Indicated 238 psig August 8, 2012 Work Order 342442 Perform Exterior Inspection of the MV-FP707, FPS Header Isolation Piping July 13, 2013   
EL 643'-0"   
  13  Work Order 347562 J-91, Install Flood Barrier Within Conduits March 27, 2014 Work Order 355289 P-18A, Troubleshoot and Correct Air In-Leakage May 1, 2014 Work Order 356432 P/S-0704 Power Supply Failure July 11, 2013 Work Order 362248 MV-CVC2157 Exhibiting Leak-By June 4, 2014 Work Order 367426 K-6A, Cracked Turbo Charger Support May 19, 2014 Work Order 51623737 P/S-0110A Aux Hot Shutdown Panel Capacitor Replacement April 15, 2010 Work Order 52357830 CK-DMW400 Non-Intrusive Check Test April 26, 2013 Work Order 52432007 CK-DMW400 Non-Intrusive Check Test June 10, 2013  Operating Experience CR-ANO-C-2007-01862 All Positions Required by Table B-1 of the ANO Emergency Plan Not Filled During an Annual ERO Staffing Drill Dated 2007 CRG OPEX Report Database of CRG Reviews of Operating Experience January 2012 -  May 6, 2014 CR-PLP-2007-06343 Potential Staffing Problem for the RP Department to Meet Site Emergency Plan ERO Obligations. December 20, 2007 CR-PLP-2009-04527 Internal OE - Improper Classification of the Event During an Emergency Preparedness Drill  September 29, 2009 CR-PLP-2012-01245 IER-L2-12-14 - Automatic Reactor Scram Resulting From a Design Vulnerability in the  
Revision C Drawing E-44 Lighting Panel Schedule L-35, Sheet 115A Revision 5 EC 27632 Perform an Evaluation of Inspection Opportunities Prior to License Renewal Per Commitment LO-
4.16-kV Bus Undervoltage Protection Scheme February 23, 2012 CR-PLP-2012-01827 NRC-IN-2012-03 - Design Vulnerability in Electric Power System March 20, 2012 CR-PLP-2012-05719 NRC-IN-2012-14 - Motor Operated Valve Inoperable Due to Stem-Disc Separation August 16, 2012 CR-PLP-2012-05721 NRC-IN-2012-11 - Age Related Capacitor Degradation August 6, 2012 CR-PLP-2012-07334 NRC-21-2012-48-00 - Commercial Grade Dedication Not Properly Applied to Type 9200  
LAR-2009-244-38  
Butterfly Valves November 20, 2012 CR-PLP-2013-02674 NRC-RIS-2013-05 - NRC Position on the Relationship Between General Design Criteria and Technical Specification Operability June 17, 2013 CR-PLP-2023-01678 NRC-IN-2013-06 - Corrosion in Fire Protection Piping Due to Air and Water Interaction April 15, 2013 eB OPEX Report Completed OE Reviews Assigned Through eB January 2012 -  May 5, 2014 LO-PLP-2011-00338 MOV Program WT September 15, 2011   
March 17, 2011 EC 38728 Raw Water Corrosion Program Report -  
Operational Cycle 22 and 2012 Refueling Outage  
January 14, 2014 LER 2011-004-01 Turbine-Driven Auxiliary Feedwater Pump Inoperable in Excess of Technical Specification Requirements Due to Unexpected Trip  
January 31, 2012 LER 2011-005-00 Service Water Pump Shaft Coupling Failure October 3, 2011 LER 2011-006 Valve Packing Failure Resulted in Reactor Trip and Auxiliary Feedwater System Actuation November 10, 2011 LER 2011-007 Direct Current Electrical System Fault Causes  
Reactor Trip and Multiple Safety System  
Actuations November 21, 2011 LER 2011-008 Reactor Protection System and Auxiliary Feedwater System Actuation  
February 3, 2012 LER 2012-002-00 Technical Specification Required Shutdown Due to Un-isolable Secondary Side Drain Valve Leak December 20, 2012 LER 2013-001 Technical Specification Required Shutdown Due to a Component Cooling Water System Leak April 15, 2013 LER 2013-003-01 Both Control Room Ventilation Filtration Trains Declared Inoperable  
October 11, 2013 LER 2013-004-00 Discovery of Latent Design Deficiency Results in Non-Compliance with 10CFR50 Appendix R   
January 6, 2014 PL-ERO-NTRP010 Lesson Plan - RPT ERO Duties  Revision 0 PLLP-LOR-12B-03 Emergency Event Classification Revision 0 PNP 2013-044 License Amendment Request to Revise Emergency Response Organization Staff  
 
Augmentation Response Times June 25, 2013 RWP 2012-0319 Repair of CRD-24 Housing Various Revisions Work Order 177025 P-52C, Remove/Inspection Inboard Pump Bearing  
Outer Flinger June 3, 2014 Work Order 318169 PI-1489 Indicated 238 psig August 8, 2012 Work Order 342442 Perform Exterior Inspection of the MV-FP707,  
FPS Header Isolation Piping  
July 13, 2013   
  13  Work Order 347562 J-91, Install Flood Barrier Within Conduits March 27, 2014 Work Order 355289 P-18A, Troubleshoot and Correct Air In-Leakage May 1, 2014 Work Order 356432 P/S-0704 Power Supply Failure July 11, 2013 Work Order 362248 MV-CVC2157 Exhibiting Leak-By June 4, 2014 Work Order 367426 K-6A, Cracked Turbo Charger Support May 19, 2014  
Work Order  
51623737 P/S-0110A Aux Hot Shutdown Panel Capacitor  
Replacement April 15, 2010  
Work Order  
52357830 CK-DMW400 Non-Intrusive Check Test April 26, 2013  
Work Order  
52432007 CK-DMW400 Non-Intrusive Check Test June 10, 2013  
  Operating Experience
  CR-ANO-C-2007-
01862 All Positions Required by Table B-1 of the ANO Emergency Plan Not Filled During an Annual ERO  
Staffing Drill  
Dated 2007 CRG OPEX Report Database of CRG Reviews of Operating  
Experience  
January 2012 -  May 6, 2014 CR-PLP-2007-06343 Potential Staffing Problem for the RP Department to Meet Site Emergency Plan ERO Obligations. December 20, 2007 CR-PLP-2009-04527 Internal OE - Improper Classification of the Event During an Emergency Preparedness Drill  September 29, 2009 CR-PLP-2012-01245 IER-L2-12-14 - Automatic Reactor Scram Resulting From a Design Vulnerability in the  
4.16-kV Bus Undervoltage Protection Scheme  
February 23, 2012 CR-PLP-2012-01827 NRC-IN-2012-03 - Design Vulnerability in Electric Power System  
March 20, 2012 CR-PLP-2012-05719 NRC-IN-2012-14 - Motor Operated Valve Inoperable Due to Stem-Disc Separation August 16, 2012 CR-PLP-2012-05721 NRC-IN-2012-11 - Age Related Capacitor  
Degradation August 6, 2012 CR-PLP-2012-07334 NRC-21-2012-48-00 - Commercial Grade Dedication Not Properly Applied to Type 9200  
 
Butterfly Valves November 20, 2012 CR-PLP-2013-02674 NRC-RIS-2013-05 - NRC Position on the Relationship Between General Design Criteria and Technical Specification Operability June 17, 2013 CR-PLP-2023-01678 NRC-IN-2013-06 - Corrosion in Fire Protection  
Piping Due to Air and Water Interaction April 15, 2013 eB OPEX Report Completed OE Reviews Assigned Through eB January 2012 -  May 5, 2014 LO-PLP-2011-00338 MOV Program WT September 15, 2011   
  14  OE-31777 External OE - Human Performance Errors Contributed to Less than Expected Emergency  
  14  OE-31777 External OE - Human Performance Errors Contributed to Less than Expected Emergency  
Response Organization Team Performance May 26, 2010 OE-2013-000026 NRC-21-2012-55-00 - Adequacy of Design Change in AM Magne-Blast Circuitry Breakers January 8, 2013 OE-2013-000144 NRC-IN-2013-01 - Emergency Action Level Thresholds Outside the Range of Radiation  
Response Organization Team Performance May 26, 2010 OE-2013-000026 NRC-21-2012-55-00 - Adequacy of Design  
Monitors February 26, 2013 OE-2013-000388 NRC-21-2012-55-01 - Update Report - Adequacy of Design Change in AM Magne-Blast Circuitry Breakers June 12, 2013 OE-2013-000533 NRC-RIS-2013-09 - Guidelines for Effective Prevention and Management of System Gas Accumulation August 23, 2013 OE-2013-000651 NRC-21-2013-50-00 - Rosemount Model 710DU Trip Units May Not Meet Established Post-
Change in AM Magne-Blast Circuitry Breakers  
January 8, 2013 OE-2013-000144 NRC-IN-2013-01 - Emergency Action Level Thresholds Outside the Range of Radiation  
 
Monitors  
February 26, 2013 OE-2013-000388 NRC-21-2012-55-01 - Update Report - Adequacy  
of Design Change in AM Magne-Blast Circuitry  
Breakers June 12, 2013 OE-2013-000533 NRC-RIS-2013-09 - Guidelines for Effective Prevention and Management of System Gas Accumulation August 23, 2013 OE-2013-000651 NRC-21-2013-50-00 - Rosemount Model 710DU Trip Units May Not Meet Established Post-
Exposure Radiation Performance Criteria September 20, 2013 OE-2013-000711 NRC-21-2013-68-00 - Interim Report - Inability to Complete 10CFR Part 21 Evaluation Regarding  
Exposure Radiation Performance Criteria September 20, 2013 OE-2013-000711 NRC-21-2013-68-00 - Interim Report - Inability to Complete 10CFR Part 21 Evaluation Regarding  
Cracking in KCR-13 Standby Battery Jars December 20, 2013 OE-2014-000061 NRC-IN-2014-03 - Turbine-Driven Auxiliary Feedwater Pump Overspeed Trip Mechanism  
Cracking in KCR-13 Standby Battery Jars December 20, 2013 OE-2014-000061 NRC-IN-2014-03 - Turbine-Driven Auxiliary Feedwater Pump Overspeed Trip Mechanism  
Issues February 25, 2014  Procedures Administrative Procedure No 4.00 Operations Organization, Responsibilities and Conduct Revision 53 EI-16.1 Maintenance of Emergency Equipment Revision 30 EN-DC-336 Plant Health Committee Revision 7 EN-EC-100 Guidelines for Implementation of the Employee Concerns Program Revision 7 Revision 8 EN-EP-305 Emergency Planning 10CFR50.54(q) Review Program Revision 3 EN-EP-306 Drills and Exercises Revision 5 EN-EP-310 Emergency Response Organization Notification System Revision 2 EN-FAP-LI-001 Condition Review Group (CRG) Revision 4 EN-FAP-LI-003 Corrective Action Review Board (CARB) Process Revision 13 EN-HU-102 Human Performance Traps &Tools Revision 13 EN-HU-103 Human Performance Error Reviews Revision 7 EN-LI-100 Process Applicability Determination Revision 15 EN-LI-102 Corrective Action Process Revision 23   
 
  15  EN-LI-104 Self-Assessment and Benchmark Process Revision 10 EN-LI-115 Apparent Cause Evaluation (ACE) Process Revision 15 EN-LI-118 Cause Evaluation Process Revision 17, 18, 19 and 20 EN-LI-118-06 Common Cause Analysis Evaluation Revision 4 EN-LI-121 Trending and Performance Review Process Revision 15 EN-MA-118 Foreign Material Exclusion Revision 8 EN-MA-125 Troubleshooting Control of Maintenance Activities  Revision 4 EN-MA-125 Troubleshooting Control of Maintenance Activities Revision 17 EN-NS-221 Security Department Standards and Expectations Revision 5 EN-OE-100 Operating Experience Program Revision 20 EN-OP-117 Operations Assessments Revision 6 EN-RP-115 BRAC/SRMP Survey Program Revision 0 EN-WM-107 Post-Maintenance Testing Revision 4 FPIP-1 Fire Protection Plan, Organization and Responsibilities Revision 22 FPSP-SO-3 Fire Suppression Water System Fire Hydrant Flush Revision 8 FWS-M-6 Auxiliary Feedwater Turbine Maintenance Revision 28 SEP-SW-PLP-002 Service Water and Fire Protection Inspection Program Revision 3  Root Cause Evaluations CR-PLP-2011-05723 Root Cause Evaluation:  Auxiliary Feedwater Pump P-8B Overspeed Trip Actuation April 23, 2012 CR-PLP-2012-03873 Root Cause Evaluation:  Ground Connected to DC Circuit on CCW Tank Level Switch August 15, 2012 CR-PLP-2012-05054 Root Cause Evaluation Report for Foreign Material Intrusion P-74, SIRWT Recirculation  
Issues February 25, 2014  
Pump July 12, 2012 CR-PLP-2012-07047 Steam Leak in MV-MS526 Upstream Weld Results in Plant Shutdown November 27, 2012 CR-PLP-2013-00885 Root Cause Evaluation Report:  Main Generator Disconnect MOD 26H5 Hotspot March 28, 2103 CR-PLP-2014-00738 Root Cause Evaluation:  Unattended Pathway Leads to One Hour Reportable Safeguards Event  
  Procedures
to the NRC February 24, 2014   
Administrative  
  16  LIST OF ACRONYMS  CAL  Confirmatory Action Letter CFR  Code of Federal Regulations DC  Direct Current  
Procedure No 4.00 Operations Organization, Responsibilities and Conduct Revision 53 EI-16.1 Maintenance of Emergency Equipment Revision 30 EN-DC-336 Plant Health Committee Revision 7 EN-EC-100 Guidelines for Implementation of the Employee  
Concerns Program  
Revision 7  
Revision 8 EN-EP-305 Emergency Planning 10CFR50.54(q) Review Program Revision 3 EN-EP-306 Drills and Exercises Revision 5 EN-EP-310 Emergency Response Organization Notification System Revision 2 EN-FAP-LI-001 Condition Review Group (CRG) Revision 4 EN-FAP-LI-003 Corrective Action Review Board (CARB) Process Revision 13 EN-HU-102 Human Performance Traps &Tools Revision 13 EN-HU-103 Human Performance Error Reviews Revision 7 EN-LI-100 Process Applicability Determination Revision 15 EN-LI-102 Corrective Action Process Revision 23   
  15  EN-LI-104 Self-Assessment and Benchmark Process Revision 10 EN-LI-115 Apparent Cause Evaluation (ACE) Process Revision 15 EN-LI-118 Cause Evaluation Process Revision 17, 18, 19 and 20 EN-LI-118-06 Common Cause Analysis Evaluation Revision 4 EN-LI-121 Trending and Performance Review Process Revision 15 EN-MA-118 Foreign Material Exclusion Revision 8 EN-MA-125 Troubleshooting Control of Maintenance Activities  Revision 4 EN-MA-125 Troubleshooting Control of Maintenance Activities Revision 17 EN-NS-221 Security Department Standards and Expectations Revision 5 EN-OE-100 Operating Experience Program Revision 20 EN-OP-117 Operations Assessments Revision 6 EN-RP-115 BRAC/SRMP Survey Program Revision 0 EN-WM-107 Post-Maintenance Testing Revision 4 FPIP-1 Fire Protection Plan, Organization and Responsibilities Revision 22 FPSP-SO-3 Fire Suppression Water System Fire Hydrant Flush Revision 8 FWS-M-6 Auxiliary Feedwater Turbine Maintenance Revision 28 SEP-SW-PLP-002 Service Water and Fire Protection Inspection Program Revision 3  
   Root Cause Evaluations
  CR-PLP-2011-05723 Root Cause Evaluation:  Auxiliary Feedwater Pump P-8B Overspeed Trip Actuation April 23, 2012 CR-PLP-2012-03873 Root Cause Evaluation:  Ground Connected to DC Circuit on CCW Tank Level Switch August 15, 2012 CR-PLP-2012-05054 Root Cause Evaluation Report for Foreign Material Intrusion P-74, SIRWT Recirculation  
Pump July 12, 2012 CR-PLP-2012-07047 Steam Leak in MV-MS526 Upstream Weld  
Results in Plant Shutdown November 27, 2012 CR-PLP-2013-00885 Root Cause Evaluation Report:  Main Generator Disconnect MOD 26H5 Hotspot  
March 28, 2103 CR-PLP-2014-00738 Root Cause Evaluation:  Unattended Pathway  
Leads to One Hour Reportable Safeguards Event  
 
to the NRC  
February 24, 2014   
  16  LIST OF ACRONYMS  
  CAL  Confirmatory Action Letter CFR  Code of Federal Regulations DC  Direct Current  
ENO  Entergy Nuclear Operation  
ENO  Entergy Nuclear Operation  
IP  Inspection Procedure  
IP  Inspection Procedure  
NRC  Nuclear Regulatory Commission  
NRC  Nuclear Regulatory Commission  
SCWE  Safety Conscious Work Environment  
SCWE  Safety Conscious Work Environment  
   A. Vitale -3-   
   A. Vitale -3-  
   
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the  
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the  
NRC's Agencywide Documents Access and Management System (ADAMS).  ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).   
NRC's Agencywide Documents Access and Managem
   Sincerely,  /RA/  Eric Duncan, Chief  
ent System (ADAMS).  ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html
Branch 3 Division of Reactor Projects Docket No. 50-255 License No. DPR-20  
(the Public Electronic Reading Room).   
 
   Sincerely,  
   /RA/  Eric Duncan, Chief  
 
Branch 3  
Division of Reactor Projects  
Docket No. 50-255 License No. DPR-20  
 
  Enclosure:  Inspection Report No. 05000255/2014007  
  Enclosure:  Inspection Report No. 05000255/2014007  
   w/Attachment:  Supplemental Information cc w/encl:  Distribution via LISTSERV DISTRIBUTION: See next page   
   w/Attachment:  Supplemental Information cc w/encl:  Distribution via LISTSERV
  DISTRIBUTION
: See next page  
   
   
   
   
   
Line 441: Line 849:
   
   
   
   
   DOCUMENT NAME:  Palisades PI&R 2014007  Publicly Available  Non-Publicly Available   Sensitive  Non-Sensitive To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy OFFICE RIII      NAME RNg:rj EDuncan  DATE 06/20/14 06/20/14  OFFICIAL RECORD COPY   
   DOCUMENT NAME:  Palisades PI&R 2014007  Publicly Available  Non-Publicly Available
Sensitive  Non-Sensitive To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE RIII      NAME RNg:rj EDuncan  DATE 06/20/14 06/20/14  OFFICIAL RECORD COPY  
   
    
    
   Letter to Anthony Vitale from Eric Duncan dated June 20, 2014 SUBJECT: PALISADES NUCLEAR PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000255/2014007   
   Letter to Anthony Vitale from Eric Duncan dated June 20, 2014
DISTRIBUTION w/encl: Joseph Nick  
  SUBJECT: PALISADES NUCLEAR PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000255/2014007  
   
DISTRIBUTION w/encl
: Joseph Nick  
RidsNrrPMPalisades Resource  
RidsNrrPMPalisades Resource  
RidsNrrDorlLpl3-1 Resource  RidsNrrDirsIrib Resource Cynthia Pederson  
 
RidsNrrDorlLpl3-1 Resource   
RidsNrrDirsIrib Resource Cynthia Pederson  
 
Darrell Roberts  
Darrell Roberts  
Steven Orth  
Steven Orth  
Allan Barker Carole Ariano Linda Linn  
 
Allan Barker  
Carole Ariano Linda Linn  
DRPIII  
DRPIII  
DRSIII  
DRSIII  
Patricia Buckley Carmen Olteanu ROPassessment.Resource@nrc.gov
Patricia Buckley  
Carmen Olteanu ROPassessment.Resource@nrc.gov
}}
}}

Revision as of 13:25, 1 July 2018

IR 05000255-14-007; 05/05/2014-06/11/2014; Palisades Nuclear Plant; Problem Identification and Resolution
ML14171A394
Person / Time
Site: Palisades Entergy icon.png
Issue date: 06/20/2014
From: Duncan E R
Region 3 Branch 3
To: Vitale A
Entergy Nuclear Operations
References
IR-14-007
Download: ML14171A394 (37)


See also: IR 05000255/2014007

Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE RD. SUITE 210 LISLE, IL 60532-4352

June 20, 2014

Mr. Anthony Vitale

Vice President, Operations Entergy Nuclear Operations, Inc. Palisades Nuclear Plant

27780 Blue Star Memorial Highway

Covert, MI 49043-9530

SUBJECT: PALISADES NUCLEAR PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000255/2014007

Dear Mr. Vitale:

On June 11, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution Inspection at your Palisades Nuclear Plant. The enclosed inspection report documents the inspection results, which were discussed at an interim exit meeting on May 23, 2014, and a final exit meeting on June 11, 2014, with you and other

members of your staff. The inspection examined activities conducted under your license as they related to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

On the basis of the samples selected for review, the inspectors concluded that the Corrective

Action Program at Palisades Nuclear Plant was adequate in the areas of identifying, evaluating and correcting issues with some identified opportunities for improvement. There was a low threshold for identifying issues and entering them into the Corrective Action Program. The

significance of the issues was screened using risk insights and the significance drove the

prioritization of issue evaluation and resolution. Evaluations were adequate, overall, in

determining the underlying cause of the issues and corrective actions were generally implemented in a timely manner, commensurate wi

th their safety significance. Operating experience was evaluated and entered into the Corrective Action Program, if applicable. The use of operating experience was integrated into daily activities and found to be effective in

preventing similar issues at the plant. In addition, self-assessments, audits, and effectiveness reviews were found to be conducted at a sufficient depth for all departments. The assessments

reviewed were thorough and effective in identifying site performance deficiencies, programmatic concerns, and improvement opportunities. Based on the results of the interviews conducted, the inspectors did not identify any impediment to the establishment of a safety conscious work environment (SCWE) at Palisades Nuclear Plant with the exception of the Security Department. Licensee staff was aware of and generally familiar with the Corrective Action Program and other station processes, including the Employee Concerns Program, through which concerns could be raised. The staff was also comfortable raising concerns without fear of retaliation.

A. Vitale -2-

As discussed in NRC Inspection Report 05000255/2014009, dated March 6, 2014, the NRC performed a limited scope Problem Identification and Resolution inspection that identified a chilled work environment within the Security D

epartment. In particular, the NRC concluded that staff within the Security Department perceived that: (1) recent actions to terminate the

employment of two supervisors was in retaliation for their raised concerns; (2) the Corrective Action Program was ineffective at addressing equipment and other concerns raised by the

Security staff; (3) Security management was unresponsive to employees' concerns; and (4) the Employee Concerns Program could not be relied upon to maintain employee confidentiality.

In response to our identification of a chilled work environment within the Security Department,

you developed the Palisades Security SCWE Action Plan and the NRC planned to review the effectiveness of actions taken to implement the Action Plan.

During this inspection, we reviewed your implementation of the Palisades Security SCWE

Action Plan and verified that, to date, you have completed all of the actions as committed to in

the Action Plan. However, we concluded that the quality of the actions implemented have been

insufficient to assess and understand the cause of the chilled work environment within the Security Department and did not demonstrate a strong commitment to effectively improve the safety conscious work environment in the Security Department. Specif

ically, significant gaps were found to exist in the security officers' knowledge of the actions being taken to address the

chilled safety conscious work environment and management's commitment to improving the overall safety conscious work environment.

For example, security officers had a limited recollection of any discussion of the results of the NRC's limited scope Problem Identification and Resolution inspection, and security officers

stated that they were not informed of the site's development and implementation of a Security

SCWE Action Plan or the specific actions required by the Action Plan. Also, the security officers were unaware of the establishment of the site's Security Ombudsman Program as directed in the Action Plan; the intent of the program; or their shift representatives for the Program, despite the selection and assignment of personnel to these positions at the end of March 2014. Lastly,

the security officers were unaware of a significant organizational change that added the

Regulatory and Performance Improvement Director to the Security Department chain of

command.

Therefore, we are requesting that you provide a response to us, within 30 days of your receipt of this letter, that outlines actions that you have taken or plan to take to further enhance your

Palisades Security SCWE Action Plan to improve

the safety conscious work environment in the Security Department at Palisades. The NRC will

continue to closely monitor Security Department safety conscious work environment and any supplemental actions that you may choose to take with a follow-up inspection.

We plan to discuss with you the results of our safety conscious work environment inspections

during the upcoming End-of-Cycle assessment

public meeting. The NRC requests that you be prepared to discuss: (1) the root cause of the chilled work environment within the Security

Department; (2) your progress in addressing the safety conscious work environment concerns

within the Security Department; and (3) any additional actions planned and/or implemented to address the safety conscious work environment at Palisades, including actions as a result of our

observations during this Problem Identification and Resolution inspection.

A. Vitale -3-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRC's Agencywide Documents Access and Managem

ent System (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/ Eric Duncan, Chief

Branch 3

Division of Reactor Projects

Docket No. 50-255 License No. DPR-20

Enclosure: Inspection Report No. 05000255/2014007

w/Attachment: Supplemental Information cc w/encl: Distribution via LISTSERV

Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION III Docket No: 50-255 License No: DPR-20 Report No: 05000255/2014007

Licensee: Entergy Nuclear Operations, Inc.

Facility: Palisades Nuclear Plant

Location: Covert, MI

Dates: May 5, 2014, through June 11, 2014 Team Leader: R. Ng, Project Engineer Inspectors: A. Scarbeary, Resident Inspector C. Zoia, License Examiner

E. Sanchez-Santiago, Reactor Inspector

G. Hansen, Physical Security Inspector

Approved by: E. Duncan, Chief

Branch 3

Division of Reactor Projects

2 SUMMARY OF FINDINGS Inspection Report 05000255/2014007; 05/05/2014 - 06/11/2014; Palisades Nuclear Plant; Problem Identification and Resolution.

This inspection was performed by four region-based inspectors and the Palisades Resident

Inspector. The NRC's program for overseeing t

he safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reac

tor Oversight Process," Revision 4, dated December 2006. Problem Identification and Resolution

On the basis of the samples selected for review, the inspectors concluded that the Corrective Action Program at Palisades Nuclear Plant was adequate in the areas of identifying, evaluating

and correcting issues with some identified opportunities for improvement. The licensee had a

low threshold for identifying issues and entering them into the Corrective Action Program. The

significance of the issues was screened using risk insights and the significance drove the prioritization of issue evaluation and resolution. Evaluations were adequate, overall, in determining the underlying cause of the issues and corrective actions were generally

implemented in a timely manner, commensurate wi

th their safety significance. Operating experience was evaluated and entered into the Corrective Action Program, if applicable. The

use of operating experience was integrated into daily activities and found to be effective in preventing similar issues at the plant. In addition, self-assessments, audits, and effectiveness reviews were found to be conducted at a sufficient depth for all departments. The assessments

reviewed were thorough and effective in identifying site performance deficiencies, programmatic

concerns, and improvement opportunities. Based on the results of the interviews conducted,

the inspectors did not identify any impediment to

the establishment of a safety conscious work environment (SCWE) at Palisades Nuclear Plant with the exception of the Security Department. Licensee staff was aware of and generally familiar with the Corrective Action Program and other station processes, including the Employee Concerns Program, through which concerns could be raised. The staff was also comfortable raising concerns without fear of retaliation.

Although implementation of the Corrective Action Program was determined to be adequate, the inspectors identified several issues that were either minor in nature and/or represented a potential weakness in the program.

The inspectors concluded that, to date, the site had completed all the actions as committed to in

the Security SCWE Action Plan. However, the inspectors concluded that the quality of the

actions implemented have been insufficient to assess and understand the cause of the chilled

work environment within the Security Department and did not demonstrate a strong commitment to effectively improve the safety conscious work environment in the Security Department. Specifically, significant gaps were found to exist in the security officers' knowledge of the actions being taken to address the chilled safety conscious work environment and

management's commitment to improving the overall safety conscious work environment.

Based on the information reviewed during this inspection, the inspectors concluded that the

control room structure continues to perform its intended safety function, and the installed

modifications, if maintained, are adequate to prevent water intrusion into the control room.

Therefore, the inspectors determined that the licensee had fulfilled the Confirmatory Action

Letter commitments to address the Safety Injection Refueling Water Tank (SIRWT) and Control Room concrete support structure leakage.

3 A. NRC-Identified and Self-Revealed Findings

None. B. Licensee-Identified Violations

None.

4 REPORT DETAILS

4. OTHER ACTIVITIES 4OA2 Problem Identification and Resolution

(71152B) This inspection constituted one biennial sample of Problem Identification and Resolution as defined by Inspection Procedure 71152, "Problem Identification and Resolution."

Documents reviewed are listed in the Attachment to this report. .1 Assessment of the Corrective Action Program Effectiveness

Inspection Scope

The inspectors reviewed the procedures and processes that described the Corrective Action Program at Palisades Nuclear Plant to ensure, in part, that the requirements of

10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," were met. The inspectors

observed and evaluated the effectiveness of meetings related to the Corrective Action Program, such as the Condition Report Prescreening meeting, the Condition Review Group meeting, and the Corrective Action Review Board meeting. Selected licensee

personnel were interviewed to assess their understanding of and their involvement in the

Corrective Action Program. The inspectors reviewed selected condition reports across all seven Reactor Oversight Process cornerstones to determine if problems were being properly identified and entered into the licensee's Corrective Action Program. The majority of the risk-informed samples of condition reports reviewed were

issued since the last NRC biennial Problem Identification and Resolution inspection completed in February 2012. The inspectors

also reviewed selected issues that were more than 5 years old. The inspectors assessed the licensee's characterization and evaluation of the issues and examined the assigned corrective actions. This review encompassed the full range of safety significance and evaluation classes, including root cause evaluations, apparent

cause evaluations, common cause evaluations, condition report responses, and human

performance error reviews. The inspectors assessed the scope and depth of the

licensee's evaluations. For significant conditions adverse to quality, the inspectors evaluated the licensee's corrective actions to prevent recurrence and for less significant issues, the inspectors reviewed the corrective actions to determine if they were

implemented in a timely manner commensurate with their safety significance. The inspectors selected the Auxiliary Feedwater Actuation System and Reactor Protection System power supply components to re

view in detail over a 5 year period. Both systems were safety-related and risk-significant Maintenance Rule (a)(1) systems with previously identified power supply component problems. At the time of the inspection, the Reactor Protection System was in a Maintenance Rule (a)(1) status, and

the Auxiliary Feedwater Actuation System

had recently returned from a Maintenance Rule (a)(1) status to a Maintenance Rule (a)(2) status. The primary purpose of this

review was to determine whether the licensee was properly monitoring and evaluating the performance of risk-significant systems. The inspectors also assessed the licensee's implementation of various system monitoring programs and performed

5 walkdowns, as needed, to verify the resolution of issues. As part of this review, the inspectors interviewed the current and prev

ious system engineers, reviewed a sample of system health reports, condition reports, operating experience, apparent cause evaluations, and root cause evaluations. The inspectors also attended the Plant Health

Committee Meeting to observe the process the licensee used for identifying, prioritizing, and resolving issues that challenged unit reliability. The inspectors reviewed Corrective

Action Program and work management system procedures that provided guidance for trending. In addition, the inspectors walked down the Auxiliary Feedwater Actuation

System panel area to visually inspect recent power supply-related maintenance and to verify that identified concerns were entered into the Corrective Action Program. The inspectors examined the results of self-assessments of the Corrective Action Program completed during the review period. The results of the self-assessments were

compared to self-revealed and NRC-identified findings. The inspectors also reviewed

the corrective actions associated with previously identified non-cited violations and findings to determine whether the station

properly evaluated and resolved those issues. The inspectors performed walkdowns, as necessary, to verify the resolution of the

issues. Assessment

(1) Identification of Issues

Based on the results of the inspection, the inspectors concluded that, overall, the station was effective in identifying issues at a low threshold and properly entering them into the Corrective Action Program. The inspectors determined that problems were usually

identified and captured in a complete and accurate manner in the Corrective Action

Program. The station was appropriately screening issues from both NRC and industry operating experience at an appropriate level and entering them into the Corrective Action Program when the issues were applicable to the station. The inspectors also noted that deficiencies were identified by external organizations, including the NRC, that had not been previously identified by licensee personnel. These deficiencies were

subsequently entered into the Corrective Action Program for resolution. The inspectors determined that the station was generally effective at trending low level issues to prevent more significant issues from developing. The licensee also used the Corrective Action Program to document instances where previous corrective actions

were ineffective or were inappropriately closed.

The inspectors concluded that power supply-related concerns were identified and

entered into the Corrective Action Program at a low threshold, and concerns were resolved in a timely manner commensurate with their safety significance.

(2) Prioritization and Evaluation of Issues

Based on the results of the inspection, the inspectors concluded that the station was adequately prioritizing and evaluating issues commensurate with the safety significance of the identified issue, which included a consideration of risk.

The inspectors determined that the Condition Report Prescreening meeting, the

Condition Review Group meeting, and the Corrective Action Review Board meeting were

6 all generally thorough and maintained a high standard for evaluation quality. Members of the Condition Review Group discussed selected issues in sufficient detail and

challenged the responsible department representatives regarding their conclusions and recommendations.

The inspectors performed a detailed review of issues related to the Reactor Protection

System and Auxiliary Feedwater Actuation System power supplies over roughly the past 5 years. The inspectors concluded that the evaluation of design issues, along with

failure analyses, provided for a thorough review of potential causes of issues. The corrective actions already implemented to evaluate the extent of condition of an issue and those being completed to revise the design of the power supplies were being

implemented in a timely manner commensurate with the safety significance of the issues. The inspectors noted that the licensee generally exhibited no reluctance in

placing structures, systems, and components into a Maintenance Rule (a)(1) status. Appropriate corrective actions to address identified maintenance deficiencies were prescribed and completed. A detailed review of the structures, systems, and

components performance generally occurred before returning such structures, systems, and components to a Maintenance Rule (a)(2) status. The inspectors determined that the licensee

typically evaluated equipment functionality requirements adequately after a degraded or non-conforming condition was identified.

Overall, appropriate actions were assigned to correct the degraded or non-conforming condition.

Vulnerabilities in Condition Evaluations

The inspectors identified several instances in which the licensee's evaluation lacked

sufficient quality to address the condition such that a technically competent reviewer could understand how the corrective actions would correct the identified condition. This lack of quality could potentially impact the licensee's ability to identify adequate

corrective actions. The inspectors identified the following condition reports as examples where the licensee's evaluation lacked sufficient quality:

  • Foreign Material Intrusion Effectiveness Review

Condition Report CR-PLP-2012-05054, "Root Cause Evaluation Report for Foreign Material Intrusion P-74, SIRWT Recirculation Pump," evaluated a foreign material

intrusion event in July 2012 that affected the Safety Injection Refueling Water Tank

recirculation pump. The effectiveness reviews performed by the licensee did not

establish the proper threshold to identify issues at a level that could be addressed prior to the issue becoming a more significant concern. In the root cause evaluation report, the licensee documented that the foreign material intrusion event was caused

by a failure to follow the foreign material excursion procedure. However, the failure

threshold for the effectiveness review performed was a failure to follow procedures

that resulted in foreign material intrusion. During the effectiveness review, the

licensee identified failures to follow the foreign material excursion procedure. However, the licensee concluded in the effectiveness review that the corrective actions were effective because no foreign material intrusion event actually occurred.

7 The inspectors reasoned that the absence of a foreign material intrusion given a failure to follow the foreign material excursion procedure may have been fortuitous,

rather than deliberate. Subsequently, an actual foreign material intrusion event occurred, which further demonstrated that the corrective actions might not have been effective. Specifically, when installing an inflatable bladder inside the Service Water system, on two occasions these bladders were inadvertently entrained into the return

header of the Service Water system by the relative vacuum created by the system flow. It was determined that this was a result of the failure to establish adequate

controls as required by the foreign material excursion procedure. This issue was documented as a non-cited violation in NRC Inspection Report 05000255/2014002.

  • Vital Area Doors Alarm Evaluation

While reviewing the common cause analysis for Condition Report CR-PLP-2013-

4391, "Trend in Vital Area Doors Found Unsecured," the inspectors identified issues

with the thoroughness of the initial evaluation for the identified trend and the

methodology used for the effectiveness review of the corrective actions implemented. The common cause analysis reviewed 40 instances of unsecured vital

area doors that occurred between January and October 2013. The analysis

identified the departments that were responsible for the doors being found unsecured

and the month the issue occurred. The evaluation identified a lack of use of appropriate human performance tools associated with verifying that security doors were properly latched and closed after use. The corrective actions resulting from this

trend analysis were to reinforce with site personnel and supplemental employees the

proper human performance tools to use when traversing through security doors and

actions to take if a door did not properly close. This common cause analysis did not

evaluate potential mechanical issues with the doors that would not allow them to close properly.

The effectiveness review for this trend reviewed 20 instances of unsecured vital area

doors that occurred between January 15 and March 16, 2014. This review

compared the number of times the door was used to how many times the door was found unsecured. The effectiveness review determined that a low percentage of errors occurred during this timeframe, and therefore the issue was resolved with no

additional actions needed. This was a different methodology with a different

acceptance standard than the initial common cause analysis used since in the

identification of security door violations originally identified, the number of violations

was focused on, and in the follow-up review, the failure rate was focused on. These observations were discussed with the licensee. Subsequent to the effectiveness review, the licensee identified an adverse trend station-wide for the number of

security door violations that occurred and planned to re-evaluate both the human

performance and the mechanical door operation components of this issue and

initiate follow-on corrective actions to address them.

The inspectors concluded that a lack of quality in some evaluations existed and that this

was similar to what was documented in the previous biennial Problem Identification and Resolution inspection.

8 During this inspection, although the inspectors did not identify any findings related to the lack of quality in evaluations, a minor violation related to a Part 21 evaluation is

documented in Section 4OA2.2.b of this report. Therefore, based on the samples reviewed during this inspection, the quality of evaluations, overall, appeared to be improving.

(3) Effectiveness of Corrective Actions

Based on the results of the inspection, the inspectors concluded that the licensee was generally effective in addressing identified issues and that the assigned corrective actions were generally appropriate. The licensee implemented corrective actions in a timely manner, commensurate with their safety significance, including an appropriate

consideration of risk. Problems identified using root or apparent cause methodologies

were resolved in accordance with the Corrective Action Program procedural and

regulatory requirements. Corrective actions designed to prevent recurrence were generally comprehensive, thorough, and timely. The inspectors sampled corrective

action assignments for selected NRC documented violations and determined that

actions assigned were generally effective and timely.

For example, the licensee received a non-cited violation in 2002 for the failure to operate the primary coolant pumps in accordance with their design operating criteria. The inspectors verified that the licensee's evaluations for the issue were comprehensive and

the corrective actions completed and planned were appropriate and timely,

commensurate with their safety significance.

The licensee's pre-inspection review identified several instances where corrective actions were closed inappropriately and that additional actions were needed to complete the closeout of the corrective actions. The inspectors determined these discrepancies

were minor compliance issues with the licensee's Corrective Action Program procedures and the licensee had taken appropriate actions to address these issues.

The inspectors also identified that there were approximately 260 open corrective action items at the time of the inspection. However, only 20 of these open corrective action

items were more than 2 years old. The inspectors reviewed a sample of these corrective

action items and verified that the sampled condition reports were evaluated and actions

assigned appropriately. The inspectors determined that most of the remaining actions

were related to a fire protection license amendment request, which was in the NRC review process. Other corrective actions were related to minor non-conformances or enhancements with low safety significance. For those corrective actions that were

safety significant, the inspectors verified that the due dates were reasonable and the

licensee had appropriate compensatory actions in place.

Through interviews with the licensee staff and a review of the trend of the total outstanding corrective actions over the last 5 years, the inspectors determined that the

licensee had been reducing the corrective action backlog.

c. Findings

No findings were identified.

9 .2 Implementation of Corrective Actions Generated Following NRC Inspection Procedure

(IP) 95002 Supplemental Inspection

a. Inspection Scope

The inspectors reviewed the IP 95002 supplemental inspection action items that were implemented since the completion of an IP 95002 supplemental inspection on

November 9, 2012. This supplemental inspection was related to a Yellow finding

documented in NRC Inspection Report 05000255/2011019 and 0500025/2011020.

The Yellow finding was associated with the loss of the Left train of direct current (DC)

power due to the failure to ensure that the work instructions on a safety-related 125-Volt DC distribution panel were adequate for the scheduled work. The results of this

supplemental inspection were documented in NRC Inspection Report 05000255/2012011.

b. Assessment

The inspectors reviewed Condition Report CR-PLP-2011-04822, which was the overarching condition report for the issue that resulted in the Yellow finding, and found

that the associated corrective actions had been planned and implemented. There were

various tasks associated with this condition report that were completed subsequent to

the supplemental inspection. These actions included development and implementation of training to address the deficiencies identified as part of the root cause analysis, as well as actions to review the root cause report and completed corrective actions to

ensure any additional issues and/or concerns identified had already been addressed and

did not invalidate the actions taken. The inspectors reviewed the completed corrective

actions and found them to be adequate.

c. Findings

No findings were identified. .3 Implementation of Corrective Actions Generated Following NRC IP 95001 Supplemental

Inspection

a. Inspection Scope

The inspectors reviewed the corrective actions that were implemented and the effectiveness reviews of those corrective actions that had been conducted since the

completion of an IP 95001 supplemental inspection on June 29, 2012. This

supplemental inspection was related to a White finding associated with the Turbine-

Driven Auxiliary Feedwater pump that

was documented in NRC Inspection Report 05000255/2011013 and 05000255/2011017. The results of this supplemental inspection

were documented in NRC Inspection Report 05000255/2012010. b. Assessment

The inspectors reviewed Condition Report CR-PLP-2011-5723 and the associated root cause evaluation report, "Auxiliary Feedwater Pump P-8B Overspeed Trip Actuation," and found that all of the associated corrective actions had been implemented. Two effectiveness reviews had also been completed to evaluate the adequacy of the

10 corrective actions implemented. The first effectiveness review conducted in April 2012 examined the revisions to the maintenance procedure for the Auxiliary Feedwater Pump,

and identified some enhancements to be included in the procedure based on information in the root cause evaluation. The inspectors reviewed the most current revision of this maintenance procedure and found that all of those enhancements had been included in

the document. The second effectiveness review examined maintenance records,

condition reports generated, and operations' logs to determine if any unexpected

Limiting Condition for Operation entries were made, or Limiting Condition for Operation

time was extended, due to maintenance issues related to the Turbine-Driven Auxiliary Feedwater Pump. This review was conducted in April 2014 after the most recent refueling outage (refueling outage maintenance caused the issues the led to the White

finding initially), and concluded that there were no maintenance-induced problems

related to this pump. All corrective actions associated with the aforementioned condition

report and root cause evaluation, and all effectiveness reviews had been completed for this White finding. The inspectors reviewed all of this information and determined that the actions implemented were adequate. c. Findings

No findings were identified. .4 Assessment of the Use of Operating Experience

a. Inspection Scope

The inspectors reviewed the licensee's implementation of the facility's Operating Experience Program. Specifically, the inspectors reviewed the Operating Experience Program implementing procedures and licensee evaluations of operating experience issues and events. The inspectors also observed meetings and daily activities for the

use of operating experience information to determine whether the licensee was effectively integrating operating experience into the performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel,

whether the licensee's Operating Experience Program was sufficient to prevent future

occurrences of previous industry events, and whether the licensee effectively used operating experience information in the planning and performance of departmental assessments and facility audits. The inspectors also assessed if corrective actions, as a result of operating experience, were identified and implemented effectively and in a timely manner. In addition, the inspectors interviewed the Operating Experience Program owner to obtain insights on its use. b. Assessment

Based on the results of the inspection, the inspectors concluded that, overall, operating experience was effectively utilized at the station. The inspectors observed that representatives from different sites held periodic meetings to discuss recently published

operating experience. Issues that were applicable to the Palisades Nuclear Plant were

entered into the Corrective Action Program for resolution. Industry operating experience

was effectively disseminated across plant departments through daily and pre-job briefings.

11 Nonetheless, the inspectors noted the following licensee identified minor violation of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," related to a

10 CFR Part 21 evaluation. Deficiencies in Part 21 Evaluation

On November 8, 2012, Fisher Control International submitted a Part 21 report that

described certain butterfly valve parts that did not receive proper commercial grade

dedication. These parts were considered essential-to-function and were required for the

butterfly valve assembly to perform its safety-related function. Fisher Control International requested the recipients of the Part 21 report to review this information for applicability to their equipment and facilities and take appropriate actions, if required.

The licensee entered this issue in the Corrective Action Program on November 20, 2012.

The licensee contacted Fisher Control International and identified that two installed safety-related Component Cooling Heat Ex

changer temperature control valves were affected. The licensee concluded that the valves would perform their design function,

but did not clearly document the basis of that conclusion. In addition, Fisher Control

International also communicated to the licensee that they had identified and notified the

licensee of other components that might not have been commercially dedicated properly due to an ambiguity in the purchase orders. However, the licensee did not research this matter any further. In May 2013 during an audit, Nuclear Oversight identified that the Part 21 evaluation was inadequate to support the conclusion that it was acceptable to use the butterfly valve as-

is and did not address all the issues communicated by Fisher Control International.

Subsequently, an operability evaluation was performed, which concluded that all of the equipment impacted remained operable, but were non-conforming. The inspectors determined that this was a licensee-identified minor violation of 10 CFR 50, Appendix B, Criteria XVI, "Corrective Action." This failure to comply with the

Appendix B requirement constituted a minor violation that is not subject to enforcement

action in accordance with the NRC's Enforcement Policy. A replacement of the affected equipment was scheduled for the next refueling outage. c. Findings

No findings were identified. .5 Assessment of Self-Assessments and Audits

a. Inspection Scope

The inspectors reviewed selected self-assessments, bench markings, "Snap-shot" self-assessments, and Nuclear Oversight audits, as well as the schedule of past and future assessments. The inspectors evaluated whether these audits and self-assessments

were effectively managed, adequately covered the subject areas, and properly captured

identified issues in the Corrective Action Program. In addition, the inspectors

interviewed licensee personnel regarding the implementation of the audit and self-assessment programs.

12 b. Assessment

Based on the results of the inspection, the inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying issues and enhancement opportunities at an appropriate threshold. The inspectors concluded that these audits and self-assessments were completed by personnel knowledgeable in the

subject area. In many cases, these self-assessments and audits had identified

numerous issues that were not previously recognized by the station. These issues were

entered into condition reports as required by Corrective Action Program procedures. c. Findings

No findings were identified. .6 Assessment of Safety Conscious Work Environment

a. Inspection Scope

The inspectors interviewed 19 Palisades Nuclear Plant personnel to determine if there were any indications that licensee personnel were reluctant to raise safety concerns to either their management or the NRC due to fear of retaliation. These individuals represented various departments onsite including Engineering, Maintenance,

Operations, Radiation Protection, and Security. The inspectors also assessed the

licensee's safety conscious work environment through a review of Employee Concerns Program implementing procedures, discussions with the Employee Concerns Program Manager, and reviews of condition reports. The inspectors reviewed selected Employee Concerns Program activities to identify any emergent issues or potential trends. The

licensee's actions to publicize the Corrective Action Program and Employee Concerns

Program were also reviewed. The review was performed to ensure there was a free flow

of information and to determine if individuals were willing to raise nuclear safety

concerns without fear of retaliation. b. Assessment

As discussed in NRC Inspection Report 05000255/2014009, dated March 6, 2014, the NRC performed a limited scope Problem Identification and Resolution inspection that

focused on an assessment of the safety conscious work environment in the Chemistry Department, Security Department, and Mechanical Maintenance working group. This

inspection was performed as a result of the NRC's receipt of several safety conscious

work environment or safety culture-related concerns that prompted questions into the progress made in implementing the licensee's Recovery Plan regarding safety culture deficiencies that, in part, contributed to two Greater-than-Green findings identified in

2011.

The NRC identified a chilled work environment in the Security Department as documented in NRC Inspection Report 05000255/2014009. The licensee implemented

a number of corrective actions to address the chilled environment in the Security Department.

13 During this inspection, the inspectors determined that the safety conscious work environment and overall performance related to

identifying, evaluating, and resolving problems was acceptable for the site in general. However, the assessment below was not characteristic of the safety conscious work environment in the Security Department. A detailed review of the licensee's Security SCWE Action Plan is discussed in

Section 4OA5.2 of this report.

With the exception of the Security Department, the inspectors did not identify any issues that suggested conditions were not conducive to the establishment and existence of a safety conscious work environment at Palisades Nuclear Plant. Licensee staff was aware of and familiar with the Corrective Action Program and other station processes,

including the Employee Concerns Program, through which concerns could be raised.

The inspectors did not review the site Safety Culture and SCWE surveys and assessments during this inspection because these documents were recently reviewed as part of the limited scope Problem Identification and Resolution inspection and the

conclusions from that inspection remained valid. The results indicated that there were

no impediments to the identification of nuclear safety issues.

The staff also indicated that management had been focused on promoting an environment that encourages raising issues and concerns without fear of retaliation.

The formal policy was communicated at all hands meetings, shift turnover meetings, and

through other communication venues, such as newsletters and emails. Department

managers and supervisors promoted a safe

ty conscious work environment and

reinforced senior management's policy.

Individuals were comfortable raising issues and concerns without fear of retaliation.

Overall, they felt that condition reports were given the appropriate priority and actions

taken to close condition reports were effective in addressing the identified issues.

c. Findings

No findings were identified.

4OA5 Other Activities

.1 Confirmatory Action Letter (CAL) - Palisades Nuclear Plant Commitments to Address

SIRWT and Control Room Concrete Support Structure Leakage

As documented in NRC Letter EA-12-155, "Confirmatory Action Letter (CAL) Revision 1 - Palisades Nuclear Plant Commitments to Address Safety Injection Refueling Water

Tank (SIRWT) and Control Room Concrete Support Structure Leakage," (ADAMS

ML13177A280) the NRC concluded that the structural integrity of the Safety Injection Refueling Water Tank was sufficient to meet its intended safety function, which addressed three of the five CAL items. The remaining two CAL items associated with

the control room support structure were as follows:

1. Entergy Nuclear Operations, Inc., (ENO) will continue inspections of the concrete support structure above the control room, control room hallway, and the concrete support structure ceiling as prescribed in the approved Operations Standing Order. These inspections are to ensure that the

14 temporary modifications installed to prevent impact to safety-related structures, systems and components are performing their intended functions.

2. ENO will correct the adverse condition related to cracking of the concrete support structure around the ceiling of the control room, which could lead to

water intrusion, prior to restart from the next refueling outage.

To address these items, the licensee performed a modification in the catacombs area

above the control room. This modification included the installation of a waterproof membrane and a design feature to divert water away from the control room, in the event of a leak into the catacombs area. The licensee also performed inspections of the areas

where SIRWT leakage could occur, including the catacombs area, until all modification

activities were complete.

The inspectors performed a review of the engineering change package that documented the details of the modification and the analyses performed to determine acceptability.

The inspectors ensured that the licensee addressed the capability of this system as well

as other impacts that the addition of the waterproof membrane could have on other

equipment. The inspectors also performed a walkdown of the areas below the catacombs to ensure a water intrusion scenario would not impact other safety-related equipment. The inspectors reviewed the logs that described the licensee's inspections

that were performed to ensure these inspections were adequate to identify any water

intrusion and were performed in accordance with the CAL commitment.

Based on the information reviewed during this inspection, the inspectors concluded that the control room structure continues to perform its intended safety function, and the installed modifications, if maintained, are adequate to prevent water intrusion into the

control room. Therefore, the inspectors determined that the licensee had fulfilled its

commitments to address the Safety Injection Refueling Water Tank and control room

concrete support structure leakage.

Separate correspondence will be issued to formally close Confirmatory Action

Letter EA-12-155.

.2 Security Safety Conscious Work Environment Action Plan

The inspectors performed an independent evaluation of the site's implementation of the Security Safety Conscious Work Environment (SCWE) Action Plan. The plan was

developed by the site and was being implemented in response to the NRC's identification of a chilled work environment within the Security Department during the December 2013 limited scope Problem Identif

ication and Resolution inspection, which

was documented in NRC Inspection Report 05000255/2014009 (ADAMS ML14064A569). The inspectors performed an independent review of the licensee's implementation of the Security SCWE Action Plan. The inspection included a review of

the licensee's implementation and completion of SCWE Action Plan actions; two focus

group meetings with 19 non-supervisory level security officers; and interviews with the

Regulatory and Performance Improvement Director, Security Manager, and the

Employee Concerns Program Manager.

15 Specific observations included the following:

  • Security officers had a limited recollection of discussing the results of the NRC's limited scope Problem Identification and Resolution inspection that was completed in February 2014. Security officers recalled being told that the NRC stated there "appears to be a potential chilled work environment in Security."

The security officers stated that they believed the site did not feel there was a

chilled work environment, but was only taking actions in response to the NRC's conclusions. During an interview with the Security Manager, additional details on the dissemination of the inspection results were obtained. Specifically, security officers were provided the inspection report as an email attachment in advance of the Security Manager meeting with each of the security shifts. At the meetings,

hard copies of the report were available for the security officers to reference and

retain, as desired. The Security Manager acknowledged discussing the NRC's

conclusions, but validated the fact that security officers were told the NRC stated there "appears to be a potential chilled work environment in Security."

  • Security officers stated they were never informed of the site's development and implementation of a Security SCWE Action Plan and were unaware of the specific actions required by the existing plan.
  • Security officers perceived site management to be simply "putting checks in the block" to credit completion of action items and were not committed to changing

the existing safety conscious work environment issues in the Security Department.

  • Security officers identified a lack of interaction with supervisory and management personnel above the Security Shift Supervisor level within the Security

Department and site senior management per

sonnel external to the Security Department. Security officers did acknowledge an increase in the attendance of Security Operations Superintendents at shift turnover meetings.

  • Security officers were unaware of the establishment of the site's Security Ombudsman Program and the intent of the program. Additionally, the security

officers were unaware of who the security ombudsman was for their respective shift despite the selection and assignment of staff to these positions at the end of

March 2014.

  • Security officers were not aware of a change in the site security chain of command. Specifically, the fact that the Palisades Security Manager no longer reported to the Entergy Corporate Security Director, but reported to the Site Vice President through the Regulatory and Performance Improvement Director was

not communicated. In addition, security officers were not introduced to the

Regulatory and Performance Improvement Director.

  • Since November 2013, the site's Aggregate Performance Review rated the Security Department as Green in the area of Nuclear Safety. At an Aggregate Performance Review Meeting conducted on May 19, 2014, this rating was

challenged by a manager outside the Security Department and, as a result of this

16 challenge, the participants agreed the Security Department should be rated Red in this area due to the chilled work environment identified in the department.

Since November 2013, the Security Department had been rating this area as Green in the Department Performance Review and this rating was unchallenged by senior management until the May 2014 Aggregate Performance Review

Meeting.

The inspectors concluded that, to date, the site had completed all the actions as

committed to in the Security SCWE Action Plan. However, the inspectors concluded that the quality of the actions implemented have been insufficient to assess and understand the cause of the chilled work environment within the Security Department

and did not demonstrate a strong commitment to effectively improve the safety

conscious work environment in the Security Department. Specifically, significant gaps were found to exist in the security officers' knowledge of the actions being taken to address the chilled safety conscious work environment and management's commitment to improving the overall safety conscious work environment.

4OA6 Management Meetings

a. Interim Exit Meeting

On May 23, 2014, the inspectors presented the preliminary inspection results to Mr. A. Vitale, Site Vice President, and other members of the licensee staff. b. Exit Meeting

On June 11, 2014, the inspectors presented the final inspection results to Mr. A. Vitale, Site Vice President and other members of the licensee staff. The licensee

acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary. ATTACHMENT: SUPPLEMENTAL INFORMATION

Attached

SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT

Licensee A. Vitale, Site Vice President W. Nelson, Training Manager

G. Heisterman, Maintenance Manager

A. Notbohm, CA&A Manager

O. Gustafson, Regulatory and Performance Improvement Director

D. Corbin, Operations Manager M. Seleski, Chemistry Supervisor C. Plachta, Nuclear Oversight Manager

B. Davis, Engineering Director

E. Chetfield, Employee Concern Program Manager

D. Lucy, Planning, Scheduling and Outage Manager J. Wright, Radwaste Supervisor

J. Ridley, Emergency Preparedness Coordinator

J. Haverly, Security Supervisor

NRC

A. Boland, Director, Division of Reactor Projects

E. Duncan, Branch Chief, Division of Reactor Projects

A. Garmoe, Senior Resident Inspector

A. Scarbeary, Resident inspector

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened None

Closed

None

Discussed

None

2 LIST OF DOCUMENTS REVIEWED The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections or portions of the documents were evaluated as part of the overall inspection effort. Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.

Condition Reports

CR-PLP-2007-05898 Greater than Green Security Finding Identified November 6, 2007 CR-PLP-2008-04279 Adverse Trend in Power Supply Failures October 16, 2008 CR-PLP-2009-04028 Increasing Trend in Number of Maintenance Rule a(1) Issues and Repeat Equipment Failures at Palisades August 21, 2009 CR-PLP-2009-04831 Four New Capacitors for P/S-0110A Have Different Size Case than the Installed Ones

October 16, 2009 CR-PLP-2009-05002 Declining Trend in RPS Voltage Converter +15

Vdc Output

October 29, 2009 CR-PLP-2010-00315 Potential Adverse Trend with Scaffold Periodic Inspection

January 22, 2010 CR-PLP-2010-00551 Additional Operability and/or Mitigating Action Guidance is Needed Regarding the Effect of

Unfiltered Air In-Leakage into the Control Room

Envelope

February 8, 2010 CR-PLP-2010-02351 Received Alarm EK-0601A, Variable High Power Level Channel Trip June 13, 2010 CR-PLP-2010-02551 Received Unexpected AFAS Alarms in the

Control Room June 27, 2010 CR-PLP-2010-03292 P-55C, 'C' Charging Pump, Declared Maintenance Rule Unavailable August 6, 2010 CR-PLP-2010-03809 Functional Failure Determination Performed for CR-PLP-2010-2551 Determined the Issue was a Functional Failure and Should be Re-classified September 7, 2010 CR-PLP-2010-06100 Increase in Spent Fuel Pool Liner Leakage November 14, 2010 CR-PLP-2011-02144 Received Alarms EK-0602A and EK-0606A April 28, 2011 CR-PLP-2011-03902 Indications of a Sheared Shaft on Service Water Pump P-7C August 9, 2011 CR-PLP-2011-04620 Primary Coolant System Unidentified Leakage

Greater Than the Technical Specification

Limiting Condition for Operation September 16, 2011 CR-PLP-2011-04822 Post 95002 Corrective Actions March 7, 2013 CR-PLP-2011-04822 Unplanned, Automatic Reactor Trip Occurred During Maintenance on a DC Supply Panel September 25, 2011

3 CR-PLP-2011-05125 ERO Staff Augmentation Test - TSC Operations Support Communicator had Not Arranged for an

Alternate to Fill His Position

October 6, 2011 CR-PLP-2011-05127 ERO Staff Augmentation Test - CR Operations

Support did Not Satisfactorily Respond to the

Test Notification

October 6, 2011 CR-PLP-2011-05128 ERO Staff Augmentation Test - On Call I&C Electrical Engineer Determined to be on Medical

Leave October 6, 2011 CR-PLP-2011-05723 Perform Root Cause Evaluation for P-8B, Steam Driven Auxiliary Feedwater Pump, Tripping on Overspeed

October 28, 2011 CR-PLP-2011-06845 Manual Reactor Trip Due to Lowering

Feedwater Suction Pressure Caused by CV-

0711, Feed Pump P-1A Recirculation Valve December 14, 2011 CR-PLP-2012-00165 PCS Leak Identified by Operating Crew January 7, 2012 CR-PLP-2012-00188 Control Room Requested Electrical

Maintenance to Investigate Reduced Amps on Group 2 Pressurizer Heaters

January 7, 2012 CR-PLP-2012-00361 Maintenance Rule Performance Criteria Exceeded for Main Feedwater System

January 16, 2012 CR-PLP-2012-00455 No Maintenance Rule Evaluation Performed for

Potential Failure of ELU-175

January 19, 2012 CR-PLP-2012-00499 Personnel Contamination Event While Working in the Spent Fuel Pool Area for Dry Fuel Storage

Activities

January 20, 2012 CR-PLP-2012-00665 Placekeeping Not Performed During Monthly

Communications Checks

January 26, 2012 CR-PLP-2012-00728 Personnel Contamination Event While Working

in the RCA to Issue M&TE

January 31, 2012 CR-PLP-2012-00774 Missed Delivery of Replacement Power Supply

Boards February 1, 2012 CR-PLP-2012-00860 Personnel Contamination Event While Performing a Peer Check for Chemistry

Verifying Valve Positions During PCS Sampling

February 6, 2012 CR-PLP-2012-00861 Personnel Contamination Event While Performing Sampling PCS and SIRWT

February 6, 2012 CR-PLP-2012-00873 Fire Tours on Certain Doors Not Documented on the Fire Tour Checklist

February 6, 2012 CR-PLP-2012-00895 Trend in Personnel Contamination Events. February 7, 2012 CR-PLP-2012-01073 During Annual Performance Exam Crew Failed to Accurately Classify the Event

February 15, 2012 CR-PLP-2012-01775 PI-1490, K-6B Starting Air Pressure Indicator for EDG 1-2 was Reading Abnormally High

March 17, 2012 CR-PLP-2012-01778 Unsatisfactory Failure Rate of New Style Diesel

Generator Air Start Pressure Control Valves

March 17, 2012

4 CR-PLP-2012-01828 Plant Drawings in Error Concerning Breakers Operated During Temporary Modification

Installation

March 20, 2012 CR-PLP-2012-02044 Operation of Primary Coolant Pumps with Inadequate Net Positive Suction Head April 2, 2012 CR-PLP-2012-02107 Tracking CR for Correcting Configuration Errors April 2, 2012 CR-PLP-2012-02384 Inappropriate Response to a Dose Rate Alarm April 10, 2012 CR-PLP-2012-02725 Review of Turbine Driven AFW Maintenance that was Performed in October 2011 Revealed Discrepancies with the Work Order and

Procedures April 16, 2012 CR-PLP-2012-02730 Review of Turbine Driven AFW Maintenance that was Performed in October 2011 Revealed

Procedure Quality Issues April 16, 2012 CR-PLP-2012-02780 QA Functional Area Rating for EP is Yellow for Trimester Report Covering November 2011

through February 2012 April 17, 2012 CR-PLP-2012-02905 Thirteen Condition Reports Generated On-Site for Losing Control of Assigned Photo Badges in

the Protected Area April 19, 2012 CR-PLP-2012-03012 RPS Matrix Ladder Power Indicating Light Extinguished on Channel C RPS Cabinet

July 11, 2013 CR-PLP-2012-03229 Inappropriate Response to a Dose Rate Alarm April 25, 2012 CR-PLP-2012-03313 Inappropriate Response to a Dose Rate Alarm April 27, 2012 CR-PLP-2012-03761 Fatigue Assessment Not Sent to Access Authorization for Post-Event Tests May 9, 2012 CR-PLP-2012-03782 MO-3068, Redundant HPSI Injection Valve, Would Not Move In Closed Direction May 9, 2012 CR-PLP-2012-03873 Received Control Room Alarms for SPI Trouble, 125V DC Bus Ground, and CCW Heat

Exchanger Hi-Lo Temperature Unexpectedly May 14, 2012 CR-PLP-2012-03948 Could Not Locate Fatigue Assessment

Paperwork May 17, 2012 CR-PLP-2012-03948 Fatigue Assessments Not Performed as

Required May 17, 2012 CR-PLP-2012-04292 Two Key System Health Work Orders Moved Inside the Scope Freeze Milestone Per

Engineering's Request June 5, 2012 CR-PLP-2012-04457 Radiation Protection Technician Response to Off-hours Mobilization Drill June 6, 2012 CR-PLP-2012-04690 Stop Work for Effluents for SIRW Tank Not Recognized June 25, 2012 CR-PLP-2012-04885 SIRW Tank Observed Dripping in Main Control

Room July 5, 2012 CR-PLP-2012-04921 Failure of PMT of SIRWT July 7, 2012

5 CR-PLP-2012-05512 CR for MO-3068, Redundant HPSI Injection

Valve, Failed to Close Not Appropriately

Classified August 6, 2012 CR-PLP-2012-05832 Usable Parts Not Currently on Material Readiness List August 22, 2012 CR-PLP-2012-05849 LPIR-0101B Pressurizer Level Pressure

Channel 2 Input Channel 4 Did Not Read

Correctly After Modification August 23, 2012 CR-PLP-2012-05854 Emergency Planning CFAM Performance Indicator for Defense-in Depth Turned Red as of

July PI Data August 23, 2012 CR-PLP-2012-05893 After Replacement of New Power Supplies, "A"

Channel of RPS Failed to Pass PMT August 25, 2012 CR-PLP-2012-05894 New Power Supplies Would Not Pass PMT August 25, 2012 CR-PLP-2012-06069 An Existing Degraded Fire Barrier is Only Marginally Acceptable

September, 2012 CR-PLP-2012-06382 Junction Box J91 Not Protected Against

External Flooding September 25, 2012 CR-PLP-2012-06404 Potential Release of Low Level Radioactive

Material September 26, 2012 CR-PLP-2012-06899 Palisades May Not Be Out of Industry Norm for Containment Work Performed Online

October 25, 2012 CR-PLP-2012-07003 Shift Managers Inaccurate EP Classifications November 1, 2012 CR-PLP-2012-07010 RP Fundamental Techniques Not Followed November 1, 2012 CR-PLP-2012-07047 Steam/Water Pin Hole Leak on Inlet Socket Weld Side of MV-MS526, E-50B ASDV CV-0779

Inlet Drain Valve November 4, 2012 CR-PLP-2012-07140 Leaks That Impacted Plant Operations By

Causing Shutdowns or Forced Outages November 8, 2012 CR-PLP-2012-07348 Limited Repair of Underground Pipe Leak and Incomplete Risk Assessment of Underground

Piping and Tanks November 21, 2012 CR-PLP-2012-07351 Reductions in Source Term and CRE Ineffective November 21, 2012 CR-PLP-2012-07430 One Member of On Duty ERO Team (TSC Security Coordinator) Did Not Respond During

Quarterly Augmentation Test November 28, 2012 CR-PLP-2012-07617 Replacement Impellers for the Primary Coolant Pump Oversized December 7, 2012 CR-PLP-2012-07685 The Ratio of Oil Drained to Oil Added was Outside of Acceptance Criteria December 12, 2012 CR-PLP-2013-00158 Timeliness of the Immediate Operability for the Small Steam Leak Discovered Near MV-MS526,

'B" S/G Atmospheric Steam Dump Drain Isolation

January 14, 2013

6 CR-PLP-2013-00422 Work Orders in "Finish" Greater Than 30 Days are Not Being Routed Back to the Technical

Specification Surveillance Coordinator in a

Timely Fashion

January 30, 2013 CR-PLP-2013-00460 Critical Group Re-Investigation Expired February 1, 2013 CR-PLP-2013-00656 Entered LCO for Component Cooling Water Systems Due to Indications of a CCW Leak on

E-54A, Component Cooling Water Heat

Exchanger

February 14, 2013 CR-PLP-2013-01017 Changing System Software on Security Computer System Impacted the Ability to

Receive Alarms

March 6, 2013 CR-PLP-2013-01023 During 2013 First ERO Staff Augmentation Test

the JIC Inquiry Responder Did Not Satisfactorily Respond to the Test

March 7, 2013 CR-PLP-2013-01025 During 2013 First ERO Staff Augmentation Test the OSC Mechanical Coordinator Did Not

Satisfactorily Respond to the Test

March 7, 2013 CR-PLP-2013-01026 During 2013 First ERO Staff Augmentation Test the EOF Security Coordinator Did Not

Satisfactorily Respond to the Test

March 7, 2013 CR-PLP-2013-01213 Administrative Issues Identified in EC 20082 and

EC 37737

March 20, 2013 CR-PLP-2013-01446 Track CR for Correcting Configuration Errors April 1, 2013 CR-PLP-2013-01882 Preventive Maintenance Work Will Be Performed Late for CK-DMW400 April 26, 2013 CR-PLP-2013-02095 New +12 Vdc Test Power Supply Found to Adversely Affect the Alpha Channel Bistable

Setpoints May 9, 2013 CR-PLP-2013-02158 Part 21 Evaluation Not Rigorous Enough to Support Conclusions and Not Addressing All

Issues Raised May 13, 2013 CR-PLP-2013-02644 Overspeed Testing of P-8B was Not Successful with Newly Installed Parts June 15, 2013 CR-PLP-2013-02802 Fuel Oil Transfer System Delay in Discharge Pressure Increase June 25, 2013 CR-PLP-2013-02831 Quality Assurance Escalation on the Timeliness/Effectiveness of Correcting QA

Identified Issues June 7, 2013 CR-PLP-2013-02959 During Quarterly ERO Staff Augmentation Test a Member of the ERO Team (OSC RAD/Chem Coordinator) Did Not Respond

July 9, 2013 CR-PLP-2013-02982 Aux Feedwater AFAS-FOFF Subsystem Trip

Unexpectedly

July 9, 2013 CR-PLP-2013-02982 Received Alarm EK-0137, Aux Feedwater AFAS-FOGG Subsystem Trip, Unexpectedly

July 9, 2013 CR-PLP-2013-03001 Power Supply P/S-0704 was Removed Following Failure

July 10, 2013

7 CR-PLP-2013-03002 FIN TEAM Electrician Did Not Complete Required Computer Based Training by Due

Date July 10, 2013 CR-PLP-2013-03025 RPS Matrix "CD" Power Indication Light

Extinguished on C-06

July 11, 2013 CR-PLP-2013-03026 Power Supply P/S-CW8-15 was Removed From

the RPS Following a Failure

July 11, 2013 CR-PLP-2013-03063 Received Alarm for AFAS-FOGG Subsystem Trip Unexpectedly

July 15, 2013 CR-PLP-2013-03103 Security Force Member Failed to Shoot

Qualifying Score

July 17, 2013 CR-PLP-2013-03136 NRC Identified Issue - ALARA Planning for SFP Rerack Failed to Identify Alpha Level 3

Contamination

July 18, 2013 CR-PLP-2013-03137 NRC Identified Issue - Individual Working on the

SFP Rerack Not Wearing a Lapel

July 18, 2013 CR-PLP-2013-03155 Missing Rifle Magazine Rounds July 19, 2013 CR-PLP-2013-03298 Received Unexpected AFAS-FOGG Alarms July 31, 2013 CR-PLP-2013-03523 Door 15, Equipment Room Missile

Shield/Radiation Door, Was Unable to Be

Closed August 13, 2013 CR-PLP-2013-03683 Exceeded Maintenance Rule Criteria for

Auxiliary Feedwater Actuation System (AFAS) August 21, 2013 CR-PLP-2013-03838 During Third Quarter ERO Staff Augmentation

Test the Designated EOF Van Buren County

Liaison Failed to Respond August 29, 2013 CR-PLP-2013-03839 During Third Quarter ERO Staff Augmentation Test the Designated TSC Reactor Engineer

Provided a 45 Minute Response August 29, 2013 CR-PLP-2013-03840 During Third Quarter ERO Staff Augmentation Test One Designated Non-traditional Radiation Protection Technic Failed to Respond to the

Test August 29, 2013 CR-PLP-2013-04246 Power Supplies Received from Vendor Had a

Damaged Component September 27, 2013 CR-PLP-2013-04391 Potential Trend in Vital Area Doors Found

Unsecured

October 8, 2013 CR-PLP-2013-04405 Key System Health Work Order was Not

Completed per the Schedule

October 9, 2013 CR-PLP-2013-04462 71 Licensed Operator Requalification Tasks Selected for Continuing Training Have Not Been

Trained on Within Their Prescribed Frequencies

October 15, 2013 CR-PLP-2013-04802 Crack in a Turbocharger Support Weld for Emergency Diesel Generator 1-1 November 6, 2013 CR-PLP-2013-04817 Operating Experience Review Revealed Possible Secondary Fire Could Be Caused in

the Cable Spreading Room By a Short in the Station Battery Room November 7, 2013

8 CR-PLP-2013-05166 ALARA Planning and Controls Green Finding December 6, 2013 CR-PLP-2013-05176 NRC Debriefed Three Green NCVs December 8, 2013 CR-PLP-2013-05278 Potential Multiple Leak Locations Originating from the Irrigation Header Isolation Line in the

Screen House December 14, 2013 CR-PLP-2014-00022 Palisades Security SCWE Action Plan January 1, 2014 CR-PLP-2014-00687 Electronic Dosimeter Issue January 26, 2014 CR-PLP-2014-01193 Substantial Accumulation of Ooze, Sludge, and Bioslimes were Discovered Inside of Piping

February 8, 2014 CR-PLP-2014-01195 Missed Inspection of Opportunity February 8, 2014 CR-PLP-2014-01359 No Materials Ordered Resulting in Delay to Perform Work Order

February 14, 2013 CR-PLP-2014-02656 Violations of EN-OM-123 Fatigue Management

Program April 19, 2014 CR-PLP-2014-02856 Installed Flexitallic Style R Gasket Had Significantly Deteriorated May 1, 2014 CR-PLP-2014-02863 Gasket Supplied for Work was Incorrect May 2, 2014 CR-PLP-2014-02864 Slight Over Crush of the B/B Gasket May 2, 2014 LR-LAR-2012-00211 SIRW Tank CAL Items August 1, 2012

WT-WTPLP-2012-

00425 Ensure Electrical and I&C Supervision Periodically Discuss the Importance of 30 Min

Responder Responsibilities December 21, 2012

WT-WTPLP-2014-

00022 Security SCWE Action Plan January 15, 2014

Apparent Cause Evaluation

CR-PLP 2012-04457 HT-ACE Insufficient Radiation Protection Technician 30 Minute Response for the Off-Hours Mobilization

Drill July 12, 2012 CR-PLP-2011-06130 Operations Human Performance Standards December 7, 2011 CR-PLP-2012-00362 NRC Unplanned Scrams per 7,000 Critical Hours Indicator is White as a Result of Four

Reactor Trips

February 14, 2012 CR-PLP-2012-01073 Annual Operator Licensing Exam EAL Classification Failures

February 15, 2012 CR-PLP-2012-01073 HT-ACE Annual Operator Licensing Exam EAL Classification Failures

March 12, 2012 CR-PLP-2012-01482 HT Apparent Cause Evaluation Report for

Chemical Control Program Cause/Corrective

Action and Chemistry Department ACE Quality

Issues August 25, 2012

9 CR-PLP-2012-01775 Higher Tier Apparent Cause Evaluation: PI-1490, K-6B Starting Air Pressure Indicator for

the Emergency Diesel Generator 1-2 was

Reading Abnormally High June 18, 2012 CR-PLP-2012-03873 Level 1 Human Performance Evaluation Review: CCW Surge Tank Fill CV Doesn't Turn On Red

Light When Open (WR #271959) May 16, 2012 CR-PLP-2012-03948 Level 2 Human Performance Error Review: Fatigue Assessment Not Performed in Post-Event Response May 24, 2012 CR-PLP-2012-04457 Insufficient Radiation Protection Technician 30 Minute Response for the Off-Hours Mobilization

Drill July 12, 2012 CR-PLP-2012-06454 HT-Apparent Cause Evaluation Report for Maintenance Department Procedure Use and

Adherence December 5, 2012 CR-PLP-2012-07348 Lower Tier Apparent Cause Evaluation: Limited Repair of Underground Pipe Leak and

Incomplete Risk Assessment of Underground Piping and Tanks

January 16, 2013 CR-PLP-2013-00460 Lower Tier Apparent Cause Evaluation: Critical Group Re-Investigation Expired

February 20, 2013 CR-PLP-2013-02982 Lower Tier Apparent Cause Evaluation: P/S-0704 Failure April 15, 2014 CR-PLP-2013-03063 Lower Tier Apparent Cause Evaluation: Failure of AFAS Optical Isolator August 13, 2013 CR-PLP-2013-03650 Operations OJT/TPE Practice Issues October 15, 2013 CR-PLP-2014-00589 Level 1 Human Performance Evaluation: Security Compensatory Measures Not in Place

as Required

January 26, 2014 CR-PLP-2014-02461 Equipment Apparent Cause Evaluation: E-22B; Unexpected Discovery of ID Pitting on Recently Replaced Jacket Water Heat Exchanger May 7, 2014

Common Cause Evaluation

CR-PLP-2012-02905 Negative Trend Relating to the Control of Security

Keycards in Controlled Areas May 5, 2012 CR-PLP-2012-05861 Common Cause Analysis for Possible Emerging Trend for Procedural Compliance in Respiratory

Protection. September 17, 2012 CR-PLP-2012-07140 Palisades Leaks That Resulted In or Extended Forced Outages in June 2012 Through November

2012 December 6, 2012 CR-PLP-2013-03457 Common Cause Analysis for Cross-Cutting Aspect H.2.c, Human Performance, NRC Findings

July 28, 2013 CR-PLP-2013-03533 Unplanned Entries into TS LCO Action

Statements August 13, 2013

10 CR-PLP-2013-04391 Trend in Vital Area Doors Found Unsecured December 17, 2013

Audit, Assessment, and Self-Assessments

LO-PLPLO-2011-0101 Effectiveness Reviews of RCE CR-PLP-2011-

5723 November 10, 2011 LO-PLPLO-2012-00037 Snapshot Assessment of DPRMs and

Coaching Quality in Radiation Protection

March 29, 2012 LO-PLPLO-2012-00051 Snapshot Assessment of Use of EAL Basis Document, and Causes of Untimely or

Inaccurate EAL Classifications May 8, 2012 LO-PLPLO-2012-00084 Effectiveness Review of CR-PLP-2012-3873

(1 Year Snapshot)

March 17, 2014 LO-PLPLO-2012-00084 Effectiveness Reviews for Root Cause

Evaluation Completed Under CR-PLP-2012-

3873 June 12, 2012 LO-PLPLO-2012-00106 Snapshot Assessment of Power Air Purifying

Respirator Issues September 10, 2012 LO-PLPLO-2012-00117 Snapshot Assessment - Plant Status and

Configuration Control November 3, 2012 LO-PLPLO-2012-00121 IST Program Focused Self-Assessment May 20, 2013 LO-PLPLO-2012-00122 Electrical Work Practices May 17, 2013 LO-PLPLO-2012-00125 Snapshot Assessment on OBJ 5 (OJT-TPE) November 3, 2012 LO-PLPLO-2012-00169-

00003 Chemistry Trending Program January 19, 2013 LO-PLPLO-2012-00176 Perform Crew Assessment, in Accordance

with EN-OP-117, Operations Assessments, of

Shift 5 November 15, 2012 LO-PLPLO-2013-00015 Snapshot Self-Assessment: Fatigue Assessments Due to Post Event/For-Cause

Testing March 26, 2013 LO-PLPLO-2013-00028 Rework Program Snapshot Assessment July 10, 2013 LO-PLPLO-2013-00042 Tendon Selection Criteria Benchmark July 29, 2013 LO-PLPLO-2013-00069 Follow-up Snapshot Assessment for CR-PLP-

2013-4462 - Some Licensed Operator Tasks Selected for Continuing Training Were not

Presented Within Required Periodicity December 12, 2013 LO-PLPPLO-2012-00003 Operations Training January 5, 2012 LO-PLPPLO-2012-00048 Snapshot Assessment Critical Steps in

Operations Procedures May 5, 2012 LO-PLPPLO-2014-00076 Snapshot Assessment of Accredited Training March 5, 2014

11 PL-PLPLO-2012-00083 5 Year Periodic Self-Assessment November 2, 2013 QA-2012-PLP-013 Quality Assurance Surveillance Report May 4, 2012 QA-3-2013-PLP-01 Corrective Action Program August 1, 2013 QA-7-2013-PLP-01 Emergency Plan July 1, 2013

Miscellaneous

10CFR50.54(q) Evaluation for Relocation of One of the Two Emergency Van to the EOF

July 26, 2012 Backshift Mobilization Drill Results Overall Response Report June 15, 2009 CCW, DG 1-1 & 1-2 and Fire Water System Report Various Dates Maintenance, Operations, and Radiation Protection Safety Culture Survey April 2014 NRC Exit Notes for RP Radiation Monitoring/Radiological Hazard Assessment/ ALARA Planning Inspection. December 6, 2013 Palisades Condition Prescreening Meeting Package Various Dates Palisades Condition Review Group Meeting Package Various Dates Palisades Correction Action Review Board Meeting Package May 8, 2014 Palisades ECP Informal Benchmark Report April 2014 Palisades Maintenance Rule Periodic Assessment October 20, 2011 Palisades Maintenance Rule Periodic Assessment June 4, 2013 Palisades Nuclear Plant Quarterly Trend Reports 1Q2012 through

4Q2013 Palisades Security SCWE Action Plan May 9, 2014 Palisades Self-Assessment Review Board Meeting Package May 6, 2014 Palisades Spent Fuel Pool Leakage Trend April 2012 - Present Plant Health Committee Meeting Package May 19, 2014 PLP CRG Summary Agenda Report Prescreen May 9, 2014 Quarterly Augmentation Tests of the NRO Notification System

(Everbridge)

Various Security Work Hour Violation/Waiver Report April 1, 2013 - May 21, 2014 BOP-UT-14-012 UT Erosion/Corrosion Examination for HB-23-4-

P1836 February 19, 2014 BOP-UT-14-012 UT Erosion/Corrosion Examination for HB-23-116-

P1827 February 19, 2014

12 BOP-UT-14-013 UT Erosion/Corrosion Examination for KB-1-P176 February 19, 2014 CR-PLP-2013-04677 HUE Human Performance Evaluation - Supplemental RP Tech Left a Suspended Empty Fuel Rack in the SFP Unattended, Creating a Potential Locked

High Radiation Area Condition

October 29, 2013 Drawing C-38 Field Erected Tanks, Sheet 2 Revision 9 Drawing C-539 Cellular Slab Repair Plan of Control Room Roof

EL 643'-0"

Revision C Drawing E-44 Lighting Panel Schedule L-35, Sheet 115A Revision 5 EC 27632 Perform an Evaluation of Inspection Opportunities Prior to License Renewal Per Commitment LO-

LAR-2009-244-38

March 17, 2011 EC 38728 Raw Water Corrosion Program Report -

Operational Cycle 22 and 2012 Refueling Outage

January 14, 2014 LER 2011-004-01 Turbine-Driven Auxiliary Feedwater Pump Inoperable in Excess of Technical Specification Requirements Due to Unexpected Trip

January 31, 2012 LER 2011-005-00 Service Water Pump Shaft Coupling Failure October 3, 2011 LER 2011-006 Valve Packing Failure Resulted in Reactor Trip and Auxiliary Feedwater System Actuation November 10, 2011 LER 2011-007 Direct Current Electrical System Fault Causes

Reactor Trip and Multiple Safety System

Actuations November 21, 2011 LER 2011-008 Reactor Protection System and Auxiliary Feedwater System Actuation

February 3, 2012 LER 2012-002-00 Technical Specification Required Shutdown Due to Un-isolable Secondary Side Drain Valve Leak December 20, 2012 LER 2013-001 Technical Specification Required Shutdown Due to a Component Cooling Water System Leak April 15, 2013 LER 2013-003-01 Both Control Room Ventilation Filtration Trains Declared Inoperable

October 11, 2013 LER 2013-004-00 Discovery of Latent Design Deficiency Results in Non-Compliance with 10CFR50 Appendix R

January 6, 2014 PL-ERO-NTRP010 Lesson Plan - RPT ERO Duties Revision 0 PLLP-LOR-12B-03 Emergency Event Classification Revision 0 PNP 2013-044 License Amendment Request to Revise Emergency Response Organization Staff

Augmentation Response Times June 25, 2013 RWP 2012-0319 Repair of CRD-24 Housing Various Revisions Work Order 177025 P-52C, Remove/Inspection Inboard Pump Bearing

Outer Flinger June 3, 2014 Work Order 318169 PI-1489 Indicated 238 psig August 8, 2012 Work Order 342442 Perform Exterior Inspection of the MV-FP707,

FPS Header Isolation Piping

July 13, 2013

13 Work Order 347562 J-91, Install Flood Barrier Within Conduits March 27, 2014 Work Order 355289 P-18A, Troubleshoot and Correct Air In-Leakage May 1, 2014 Work Order 356432 P/S-0704 Power Supply Failure July 11, 2013 Work Order 362248 MV-CVC2157 Exhibiting Leak-By June 4, 2014 Work Order 367426 K-6A, Cracked Turbo Charger Support May 19, 2014

Work Order 51623737 P/S-0110A Aux Hot Shutdown Panel Capacitor

Replacement April 15, 2010

Work Order 52357830 CK-DMW400 Non-Intrusive Check Test April 26, 2013

Work Order 52432007 CK-DMW400 Non-Intrusive Check Test June 10, 2013

Operating Experience

CR-ANO-C-2007-

01862 All Positions Required by Table B-1 of the ANO Emergency Plan Not Filled During an Annual ERO

Staffing Drill

Dated 2007 CRG OPEX Report Database of CRG Reviews of Operating

Experience

January 2012 - May 6, 2014 CR-PLP-2007-06343 Potential Staffing Problem for the RP Department to Meet Site Emergency Plan ERO Obligations. December 20, 2007 CR-PLP-2009-04527 Internal OE - Improper Classification of the Event During an Emergency Preparedness Drill September 29, 2009 CR-PLP-2012-01245 IER-L2-12-14 - Automatic Reactor Scram Resulting From a Design Vulnerability in the

4.16-kV Bus Undervoltage Protection Scheme

February 23, 2012 CR-PLP-2012-01827 NRC-IN-2012-03 - Design Vulnerability in Electric Power System

March 20, 2012 CR-PLP-2012-05719 NRC-IN-2012-14 - Motor Operated Valve Inoperable Due to Stem-Disc Separation August 16, 2012 CR-PLP-2012-05721 NRC-IN-2012-11 - Age Related Capacitor

Degradation August 6, 2012 CR-PLP-2012-07334 NRC-21-2012-48-00 - Commercial Grade Dedication Not Properly Applied to Type 9200

Butterfly Valves November 20, 2012 CR-PLP-2013-02674 NRC-RIS-2013-05 - NRC Position on the Relationship Between General Design Criteria and Technical Specification Operability June 17, 2013 CR-PLP-2023-01678 NRC-IN-2013-06 - Corrosion in Fire Protection

Piping Due to Air and Water Interaction April 15, 2013 eB OPEX Report Completed OE Reviews Assigned Through eB January 2012 - May 5, 2014 LO-PLP-2011-00338 MOV Program WT September 15, 2011

14 OE-31777 External OE - Human Performance Errors Contributed to Less than Expected Emergency

Response Organization Team Performance May 26, 2010 OE-2013-000026 NRC-21-2012-55-00 - Adequacy of Design

Change in AM Magne-Blast Circuitry Breakers

January 8, 2013 OE-2013-000144 NRC-IN-2013-01 - Emergency Action Level Thresholds Outside the Range of Radiation

Monitors

February 26, 2013 OE-2013-000388 NRC-21-2012-55-01 - Update Report - Adequacy

of Design Change in AM Magne-Blast Circuitry

Breakers June 12, 2013 OE-2013-000533 NRC-RIS-2013-09 - Guidelines for Effective Prevention and Management of System Gas Accumulation August 23, 2013 OE-2013-000651 NRC-21-2013-50-00 - Rosemount Model 710DU Trip Units May Not Meet Established Post-

Exposure Radiation Performance Criteria September 20, 2013 OE-2013-000711 NRC-21-2013-68-00 - Interim Report - Inability to Complete 10CFR Part 21 Evaluation Regarding

Cracking in KCR-13 Standby Battery Jars December 20, 2013 OE-2014-000061 NRC-IN-2014-03 - Turbine-Driven Auxiliary Feedwater Pump Overspeed Trip Mechanism

Issues February 25, 2014

Procedures

Administrative

Procedure No 4.00 Operations Organization, Responsibilities and Conduct Revision 53 EI-16.1 Maintenance of Emergency Equipment Revision 30 EN-DC-336 Plant Health Committee Revision 7 EN-EC-100 Guidelines for Implementation of the Employee

Concerns Program

Revision 7

Revision 8 EN-EP-305 Emergency Planning 10CFR50.54(q) Review Program Revision 3 EN-EP-306 Drills and Exercises Revision 5 EN-EP-310 Emergency Response Organization Notification System Revision 2 EN-FAP-LI-001 Condition Review Group (CRG) Revision 4 EN-FAP-LI-003 Corrective Action Review Board (CARB) Process Revision 13 EN-HU-102 Human Performance Traps &Tools Revision 13 EN-HU-103 Human Performance Error Reviews Revision 7 EN-LI-100 Process Applicability Determination Revision 15 EN-LI-102 Corrective Action Process Revision 23

15 EN-LI-104 Self-Assessment and Benchmark Process Revision 10 EN-LI-115 Apparent Cause Evaluation (ACE) Process Revision 15 EN-LI-118 Cause Evaluation Process Revision 17, 18, 19 and 20 EN-LI-118-06 Common Cause Analysis Evaluation Revision 4 EN-LI-121 Trending and Performance Review Process Revision 15 EN-MA-118 Foreign Material Exclusion Revision 8 EN-MA-125 Troubleshooting Control of Maintenance Activities Revision 4 EN-MA-125 Troubleshooting Control of Maintenance Activities Revision 17 EN-NS-221 Security Department Standards and Expectations Revision 5 EN-OE-100 Operating Experience Program Revision 20 EN-OP-117 Operations Assessments Revision 6 EN-RP-115 BRAC/SRMP Survey Program Revision 0 EN-WM-107 Post-Maintenance Testing Revision 4 FPIP-1 Fire Protection Plan, Organization and Responsibilities Revision 22 FPSP-SO-3 Fire Suppression Water System Fire Hydrant Flush Revision 8 FWS-M-6 Auxiliary Feedwater Turbine Maintenance Revision 28 SEP-SW-PLP-002 Service Water and Fire Protection Inspection Program Revision 3

Root Cause Evaluations

CR-PLP-2011-05723 Root Cause Evaluation: Auxiliary Feedwater Pump P-8B Overspeed Trip Actuation April 23, 2012 CR-PLP-2012-03873 Root Cause Evaluation: Ground Connected to DC Circuit on CCW Tank Level Switch August 15, 2012 CR-PLP-2012-05054 Root Cause Evaluation Report for Foreign Material Intrusion P-74, SIRWT Recirculation

Pump July 12, 2012 CR-PLP-2012-07047 Steam Leak in MV-MS526 Upstream Weld

Results in Plant Shutdown November 27, 2012 CR-PLP-2013-00885 Root Cause Evaluation Report: Main Generator Disconnect MOD 26H5 Hotspot

March 28, 2103 CR-PLP-2014-00738 Root Cause Evaluation: Unattended Pathway

Leads to One Hour Reportable Safeguards Event

to the NRC

February 24, 2014

16 LIST OF ACRONYMS

CAL Confirmatory Action Letter CFR Code of Federal Regulations DC Direct Current

ENO Entergy Nuclear Operation

IP Inspection Procedure

NRC Nuclear Regulatory Commission

SCWE Safety Conscious Work Environment

A. Vitale -3-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRC's Agencywide Documents Access and Managem

ent System (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/ Eric Duncan, Chief

Branch 3

Division of Reactor Projects

Docket No. 50-255 License No. DPR-20

Enclosure: Inspection Report No. 05000255/2014007

w/Attachment: Supplemental Information cc w/encl: Distribution via LISTSERV

DISTRIBUTION

See next page

DOCUMENT NAME: Palisades PI&R 2014007 Publicly Available Non-Publicly Available

Sensitive Non-Sensitive To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE RIII NAME RNg:rj EDuncan DATE 06/20/14 06/20/14 OFFICIAL RECORD COPY

Letter to Anthony Vitale from Eric Duncan dated June 20, 2014

SUBJECT: PALISADES NUCLEAR PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000255/2014007

DISTRIBUTION w/encl

Joseph Nick

RidsNrrPMPalisades Resource

RidsNrrDorlLpl3-1 Resource

RidsNrrDirsIrib Resource Cynthia Pederson

Darrell Roberts

Steven Orth

Allan Barker

Carole Ariano Linda Linn

DRPIII

DRSIII

Patricia Buckley

Carmen Olteanu ROPassessment.Resource@nrc.gov