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=Text=
=Text=
{{#Wiki_filter:UNITED NUCLEAR REGULATORY WASHINGTON, D.C. 20555-0001 January 27, 2012 Mr. Mano Nazar Executive Vice President and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, Florida 33408-0420 TURKEY POINT UNIT 3 -
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 January 27, 2012 Mr. Mano Nazar Executive Vice President and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, Florida 33408-0420
 
==SUBJECT:==
TURKEY POINT UNIT 3 -  


==SUMMARY==
==SUMMARY==
OF THE STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 (TAC NO. ME6351)  
OF THE STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 (TAC NO. ME6351)


==Dear Mr. Nazar:==
==Dear Mr. Nazar:==
By letters dated April 19 and November 23,2011 (Agencywide Documents Access and Management Systems (ADAMS) Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. These reports were submitted in accordance with Turkey Point Unit 3 Technical Specifications (TSs) Sections 4.4.5.1, 4.4.5.2 and 6.9.1.8. A summary of the NRC staff's evaluation of the Turkey Point Unit 3 Fall 2010 Refueling Outage 25 SG tube inspection results is enclosed.
 
Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005).
By letters dated April 19 and November 23,2011 (Agencywide Documents Access and Management Systems (ADAMS) Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. These reports were submitted in accordance with Turkey Point Unit 3 Technical Specifications (TSs) Sections 4.4.5.1, 4.4.5.2 and 6.9.1.8.
The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no addition ollow-up is required at this time. Since ely, // ( ///7 /t'son c.
A summary of the NRC staff's evaluation of the Turkey Point Unit 3 Fall 2010 Refueling Outage 25 SG tube inspection results is enclosed. Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005). The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no addition ollow-up is required at this time.
L/PPlant Licensing Branch 11-2 Division of Operating Reactor licensing Office of Nuclear Reactor Regulation Docket No. 50-250  
Since ely,     ~.          //
(       I  ///7
                                          /t'son pa;ge,'pJ:/;.:::-
c.
L/PPlant Licensing Branch 11-2 Division of Operating Reactor licensing Office of Nuclear Reactor Regulation Docket No. 50-250


==Enclosure:==
==Enclosure:==
As stated cc w/encl: Distribution via Listserv


As stated cc w/encl: Distribution via Listserv UNITED NUCLEAR REGULATORY WASHINGTON, D.C. 20555-0001  
UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001


==SUMMARY==
==SUMMARY==
OF THE U.S. NUCLEAR REGULATORY COMMISSION STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 FLORIDA POWER AND LIGHT COMPANY TURKEY POINT UNIT 3 DOCKET NO. 50-250 By letters dated April 19 and November 23, 2011 (Agencywide Documents Access and Management Systems Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL, the licensee) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005).
OF THE U.S. NUCLEAR REGULATORY COMMISSION STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 FLORIDA POWER AND LIGHT COMPANY TURKEY POINT UNIT 3 DOCKET NO. 50-250 By letters dated April 19 and November 23, 2011 (Agencywide Documents Access and Management Systems Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL, the licensee) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005).
Turkey Point Unit 3 has three Westinghouse Model 44F SGs. The SGs have tubes that were hydraulically expanded into the tubesheet and are supported by Type 405 stainless steel tube support plates with broached quatrefoil holes. The Unit 3 SGs were placed into operation in 1982, and have thermally treated Alloy 600 tubing. The licensee provided the scope, extent, methods, and results of their SG tube inspections in the documents referenced above. In addition, the licensee described corrective actions (e.g., tube plugging) taken in response to the inspection findings.
Turkey Point Unit 3 has three Westinghouse Model 44F SGs. The SGs have tubes that were hydraulically expanded into the tubesheet and are supported by Type 405 stainless steel tube support plates with broached quatrefoil holes. The Unit 3 SGs were placed into operation in 1982, and have thermally treated Alloy 600 tubing.
As a result of its review of the above documents, the NRC staff has the following comments/observations: No crack-like indications were detected during the outage. Tubes R6 C45 and R7 C45 in SG B were plugged, but not stabilized.
The licensee provided the scope, extent, methods, and results of their SG tube inspections in the documents referenced above. In addition, the licensee described corrective actions (e.g.,
Both of these tubes had shallow wear indications attributed to a suspected foreign object near the upper edge of the 2 nd tube support plate on the cold leg side (02C). The tubes were plugged but not stabilized since the expected wear rate is low. The tubes surrounding R6 C45 and R7 C45A at the 02C location will be examined during the refueling outage for Cycle 27 in 2013 and during future inspections to monitor for degradation and for migration of the suspected foreign object. This required action has been documented in the plant's corrective action program. Enclosure
tube plugging) taken in response to the inspection findings.
-2 The licensee summarized the scope of inspections (primary and secondary side) as required by Technical Specification 6.9.1.8, "Steam Generator Tube Inspection Report." Based on a review of the information provided, the staff concludes that the licensee provided the information required by their technical specifications.
As a result of its review of the above documents, the NRC staff has the following comments/observations:
In addition, the staff concludes that there are no technical issues that warrant follow-up action at this time since the inspections appear to be consistent with the objective of detecting potential tube degradation and the inspection results appear to be consistent with industry operating experience at similarly designed and operated units.
: 1. No crack-like indications were detected during the outage.
January 27,2012 Mr. Mano Nazar Executive Vice President and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, Florida 33408-0420 TURKEY POINT UNIT 3 -
: 2. Tubes R6 C45 and R7 C45 in SG B were plugged, but not stabilized. Both of these tubes had shallow wear indications attributed to a suspected foreign object near the upper edge of the 2nd tube support plate on the cold leg side (02C). The tubes were plugged but not stabilized since the expected wear rate is low. The tubes surrounding R6 C45 and R7 C45A at the 02C location will be examined during the refueling outage for Cycle 27 in 2013 and during future inspections to monitor for degradation and for migration of the suspected foreign object. This required action has been documented in the plant's corrective action program.
Enclosure


==SUMMARY==
                                                -2
OF THE STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 (TAC NO. ME6351)
: 3. The licensee summarized the scope of inspections (primary and secondary side) as required by Technical Specification 6.9.1.8, "Steam Generator Tube Inspection Report."
Based on a review of the information provided, the staff concludes that the licensee provided the information required by their technical specifications. In addition, the staff concludes that there are no technical issues that warrant follow-up action at this time since the inspections appear to be consistent with the objective of detecting potential tube degradation and the inspection results appear to be consistent with industry operating experience at similarly designed and operated units.


==Dear Mr. Nazar:==
ML110030005). The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no additional follow-up is required at this time.
By letters dated April 19 and November 23, 2011 (Agencywide Documents Access and Management Systems (ADAMS) Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. These reports were submitted in accordance with Turkey Point Unit 3 Technical Specifications (TSs) Sections 4.4.5.1, 4.4.5.2 and 6.9.1.8. A summary of the NRC staff's evaluation of the Turkey Point Unit 3 Fall 2010 Refueling Outage 25 SG tube inspection results is enclosed.
Sincerely, IRA!
Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005).
Jason C. Paige, Project Manager Plant Licensing Branch 11-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-250
The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no additional follow-up is required at this time. Sincerely, IRA! Jason C. Paige, Project Manager Plant Licensing Branch 11-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-250  


==Enclosure:==
==Enclosure:==
As stated cc w/encl: Distribution via Listserv Distribution:
As stated cc w/encl: Distribution via Listserv Distribution:
PUBLIC LPL2-2 RtF RidsNrrDorlLpl2-2 RidsN rrLABClayton RidsOgcRp RidsAcrsAcnwMailCenter RidsNrrDorlDpr RidsRgn2MailCenter CHunt, NRR KKarwoski.
PUBLIC                   LPL2-2 RtF                         RidsNrrDorlLpl2-2             RidsN rrLABClayton RidsOgcRp               RidsAcrsAcnwMailCenter             RidsNrrDorlDpr               RidsRgn2MailCenter CHunt, NRR               KKarwoski. NRR                     RidsNrrPMTurkeyPoint         RidsNrrDeEsgb ADAMSAccession NO.:ML11361A381                                                                     *8~ymemo OFFICE           LPL2-2/PM           LPL2-2/LA         ESGB/BC (A)         LPL2-2/BC             LPL2-2/PM NAME             JPaige             BClayton           VCusumano*           DBroaddus             JPaige (FSaba for)
NRR RidsNrrPMTurkeyPoint RidsNrrDeEsgb ADA MSA ccession NO.:ML11361A381  
DATE             12/28/11           12/28/11           12112111             1127112               1127/12}}
*8 OFFICE LPL2-2/PM LPL2-2/LA ESGB/BC (A) LPL2-2/BC LPL2-2/PM NAME JPaige BClayton VCusumano*
DBroaddus JPaige (FSaba for) DATE 12/28/11 12/28/11 12112111 1127112 1127/12 OFFICIAL RECORD COPY}}

Latest revision as of 19:16, 6 February 2020

Summary of the Staff'S Review of the Steam Generator Tube Inservice Inspection Refueling Outage 25
ML11361A381
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 01/27/2012
From: Jason Paige
Plant Licensing Branch II
To: Nazar M
Florida Power & Light Co
Paige J
References
TAC ME6351
Download: ML11361A381 (4)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 January 27, 2012 Mr. Mano Nazar Executive Vice President and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, Florida 33408-0420

SUBJECT:

TURKEY POINT UNIT 3 -

SUMMARY

OF THE STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 (TAC NO. ME6351)

Dear Mr. Nazar:

By letters dated April 19 and November 23,2011 (Agencywide Documents Access and Management Systems (ADAMS) Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. These reports were submitted in accordance with Turkey Point Unit 3 Technical Specifications (TSs) Sections 4.4.5.1, 4.4.5.2 and 6.9.1.8.

A summary of the NRC staff's evaluation of the Turkey Point Unit 3 Fall 2010 Refueling Outage 25 SG tube inspection results is enclosed. Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005). The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no addition ollow-up is required at this time.

Since ely, ~. //

( I ///7

/t'son pa;ge,'pJ:/;.:::-

c.

L/PPlant Licensing Branch 11-2 Division of Operating Reactor licensing Office of Nuclear Reactor Regulation Docket No. 50-250

Enclosure:

As stated cc w/encl: Distribution via Listserv

UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001

SUMMARY

OF THE U.S. NUCLEAR REGULATORY COMMISSION STAFF'S REVIEW OF THE STEAM GENERATOR TUBE INSERVICE INSPECTION REPORT FOR REFUELING OUTAGE 25 FLORIDA POWER AND LIGHT COMPANY TURKEY POINT UNIT 3 DOCKET NO. 50-250 By letters dated April 19 and November 23, 2011 (Agencywide Documents Access and Management Systems Accession Nos. ML11119A006 and ML11340A074), Florida Power and Light Co. (FPL, the licensee) submitted information summarizing the results of the steam generator (SG) tube inspections performed at Turkey Point Unit 3, during the Fall 2010 Refueling Outage 25. Additionally, the U.S. Nuclear Regulatory Commission (NRC) staff summarized information provided in a conference call about the results of the fall 2010 outage in a letter dated January 19, 2011 (ADAMS Accession No. ML110030005).

Turkey Point Unit 3 has three Westinghouse Model 44F SGs. The SGs have tubes that were hydraulically expanded into the tubesheet and are supported by Type 405 stainless steel tube support plates with broached quatrefoil holes. The Unit 3 SGs were placed into operation in 1982, and have thermally treated Alloy 600 tubing.

The licensee provided the scope, extent, methods, and results of their SG tube inspections in the documents referenced above. In addition, the licensee described corrective actions (e.g.,

tube plugging) taken in response to the inspection findings.

As a result of its review of the above documents, the NRC staff has the following comments/observations:

1. No crack-like indications were detected during the outage.
2. Tubes R6 C45 and R7 C45 in SG B were plugged, but not stabilized. Both of these tubes had shallow wear indications attributed to a suspected foreign object near the upper edge of the 2nd tube support plate on the cold leg side (02C). The tubes were plugged but not stabilized since the expected wear rate is low. The tubes surrounding R6 C45 and R7 C45A at the 02C location will be examined during the refueling outage for Cycle 27 in 2013 and during future inspections to monitor for degradation and for migration of the suspected foreign object. This required action has been documented in the plant's corrective action program.

Enclosure

-2

3. The licensee summarized the scope of inspections (primary and secondary side) as required by Technical Specification 6.9.1.8, "Steam Generator Tube Inspection Report."

Based on a review of the information provided, the staff concludes that the licensee provided the information required by their technical specifications. In addition, the staff concludes that there are no technical issues that warrant follow-up action at this time since the inspections appear to be consistent with the objective of detecting potential tube degradation and the inspection results appear to be consistent with industry operating experience at similarly designed and operated units.

ML110030005). The NRC staff concluded that FPL provided the information required by the Turkey Point Unit 3 TSs and that no additional follow-up is required at this time.

Sincerely, IRA!

Jason C. Paige, Project Manager Plant Licensing Branch 11-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-250

Enclosure:

As stated cc w/encl: Distribution via Listserv Distribution:

PUBLIC LPL2-2 RtF RidsNrrDorlLpl2-2 RidsN rrLABClayton RidsOgcRp RidsAcrsAcnwMailCenter RidsNrrDorlDpr RidsRgn2MailCenter CHunt, NRR KKarwoski. NRR RidsNrrPMTurkeyPoint RidsNrrDeEsgb ADAMSAccession NO.:ML11361A381 *8~ymemo OFFICE LPL2-2/PM LPL2-2/LA ESGB/BC (A) LPL2-2/BC LPL2-2/PM NAME JPaige BClayton VCusumano* DBroaddus JPaige (FSaba for)

DATE 12/28/11 12/28/11 12112111 1127112 1127/12