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| issue date = 10/01/1987
| issue date = 10/01/1987
| title = Responds to Violations Noted in Insp Rept 50-244/87-19. Corrective Actions:Procedure CP-224 Changed on 870731 to Incorporate Steps Required to Document Radiation Source Check Steps
| title = Responds to Violations Noted in Insp Rept 50-244/87-19. Corrective Actions:Procedure CP-224 Changed on 870731 to Incorporate Steps Required to Document Radiation Source Check Steps
| author name = KOBER R W
| author name = Kober R
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name = RUSSELL W T
| addressee name = Russell W
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| docket = 05000244
| docket = 05000244
Line 15: Line 15:
| page count = 8
| page count = 8
}}
}}
See also: [[followed by::IR 05000244/1987019]]


=Text=
=Text=
{{#Wiki_filter:i REGULATORY
{{#Wiki_filter:REGULATORY INFORMATION DISTRIBUTION SYSTEM           (BIDS) i ACCESSION NBR: 8710130224           DOC. DATE: 87/10/01
INFORMATION
                                              ~              NOTARIZED: NO           DOCKET FACIL: 50-244 Robert Emmet Ginna Nuclear Planti Unit             i. Rochester   Q 05000244 AUTH. NAME           AUTHOR AFFILIATION OBER R. N.           Rochester Qas 5 Electric Corp.
DISTRIBUTION
                                                  ~
SYSTEM (BIDS)ACCESSION NBR: 8710130224
                                                            ~
DOC.DATE: 87/10/01 NOTARIZED:
REC IP. NAME         RECIPIENT AFFILIATION RUSSELL   W. T.       Region   1 Office of Director
NO DOCKET FACIL: 50-244 Robert Emmet Ginna Nuclear Planti Unit i.Rochester Q 05000244 AUTH.NAME~~~AUTHOR AFFILIATION
 
OBER R.N.Rochester Qas 5 Electric Corp.REC IP.NAME RECIPIENT AFFILIATION
==SUBJECT:==
RUSSELL W.T.Region 1 Office of Director SUBJECT: Responds to violations
Responds to violations noted in Insp Rept 50-244/87-19.
noted in Insp Rept 50-244/87-19.
Corrective actions: Procedure CP-224 changed on 870731 to incorporate steps required to document radiation source chec k steps.
Corrective
DISTRIBUTION CODE:       IE01D   COPIES RECEIVED: LTR     ~
actions: Procedure CP-224 changed on 870731 to incorporate
ENCL   ~ SIZE:
steps required to document radiation source chec k steps.DISTRIBUTION
TITLE: General     (50 Dkt)-Insp Rept/Notice of       Violation   Response NOTES:   License Exp date in accordance       eith   10CFR2i 2. 109(9/19/72).       05000244 RECIPIENT           COPIES            RECIPIENT            COP IES ID CODE/NAME        LTTR ENCL        ID CODE/NAME         LTTR ENCL PDi-3   PD                           STAHLEi C INTERNAL: AEOD                                   DEDRO NRR MOR ISSEAU) D                   NRR/DOEA DIR NRR/DREP/EPB                         NRR/DREP/RPB NRR/DRIS DIR                         NRR/P MAS/ ILRB OE~EBERMANi J                        OQC/HDS2 REG FILEE)                          RES DEPY QI RQNC    FTl E  Oi ERNAL: LPDR                                  NRC PDR NSIC TOTAL NUMBER OF COPIES REQUIRED: LTTR             20   ENCL
CODE: IE01D COPIES RECEIVED: LTR~ENCL~SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice
 
of Violation Response NOTES: License Exp date in accordance
N[1
eith 10CFR2i 2.109(9/19/72).
                                                                                                    ~ ~ v ~ ~
05000244 RECIPIENT ID CODE/NAME PDi-3 PD RQNC ERNAL: LPDR NSIC INTERNAL: AEOD NRR MOR ISSEAU)D NRR/DREP/EPB
C'y',
NRR/DRIS DIR OE~EBERMANi
so~~
J REG FILEE)FTl E Oi COPIES LTTR ENCL RECIPIENT ID CODE/NAME STAHLEi C DEDRO NRR/DOEA DIR NRR/DREP/RPB
                                                                                                                  > 51AIC ROCHESTER >As               .'. e ',t .,I~hi <'.iRi-ORATION 89 EAST AVENUE, ROCHESTER, N.Y. 74649-OP07 ROGER Vd 't(OQEf, TOLD @+Oh(
NRR/P MAS/ILRB OQC/HDS2 RES DEPY QI NRC PDR COP IES LTTR ENCLTOTAL NUMBER OF COPIES REQUIRED: LTTR 20 ENCL  
YKC PflCSl CRT f<L'C ~ RK'. PROD@, T,c ARE< conc ale 546 2700 Ginna     Station October 01, 1987 Mr. Vi lliam T. Russell, Regional Administrator U.S. Nuclear Regulatory Commission Region 631 Park Avenue I
King of Prussia, PA 19406 Subj       ect:         Inspection Report 50-244/87-19 Notice of'iolation R.E. Ginna Nuclear Power Plant Docket No. 50-244
N[1~~v~~C'y', so~~>51AIC ROCHESTER>As.'.e',t.,I~hi<'.iRi-ORATION
 
89 EAST AVENUE, ROCHESTER, N.Y.74649-OP07
==Dear Mr. Russell:==
ROGER Vd't(OQEf, YKC PflCSl CRT f<L'C~RK'.PROD@, T,c TOLD@+Oh(ARE<conc ale 546 2700 Ginna Station October 01, 1987 Mr.Vi lliam T.Russell, Regional Administrator
 
U.S.Nuclear Regulatory
Rou tine unannounced occupati onal radiation protection Inspection Report 50-244/87-19 states in part:
Commission
As a result of the inspection conducted on July 27-31, 1987, and in accordance with the "General Statement of Poli cy and Procedure for NRC Enforcement Actions", 10 CFR Part 2, Appendix C (Enforcement Policy) (1986), the following violation was identified:
-Region I 631 Park Avenue King of Prussia, PA 19406 Subj ect: Inspection
Techni cal Speci f'i cati on 6. 8. 1 (a) requires, in part, that written procedures be established, implemented and maintained covering the activities referenced in Appendix A of Regul atory Guide 1. 33, November 1972.
Report 50-244/87-19
One of those activities, procedures for control of measuring and test equipment, in Section H of Appendix Regulatory Guide 1.33, requires that specific iinspection mpl ementi ng procedures for each survei llance test, or calibration listed in Technical Specifica-ti ons be provided               to assure that... instruments... are properly controlled, calibrated and adjusted at specified periods to maintain accuracy. Table 4.1-3, Accident Moni tori ng Instrumentation Survei l lance Requi rements, of the     li censee s Technical Specifications requires
Notice of'iolation
                                            ~
R.E.Ginna Nuclear Power Plant Docket No.50-244 Dear Mr.Russell: Rou tine unannounced
that a channel calibration of the Containment Area High Range Radiation Monitors (R-29 and R-30) be performed at each refueling in accordance with criteria for calibration provided in Table II.F.1-3 of NUREG-0737.
occupati onal radiation protection
87~0>30m<               BVX0OS PDR             ADOCK   05000244 8                             PDR g~ml
Inspection
 
Report 50-244/87-19
Page 2 Inspection Report 87-19 October 01, 1987 Contrary to the above, as of July 30, 1987, a procedure was   not established and implemented which incorporated all criteria for calibration specified in Table     II.F.1,-3 of NUREG-0737. Speci fically, procedures di d not provide for channel calibration of monitors R-29 and R-30 with a source at one point below 10R/hr.
states in part: As a result of the inspection
Rochester Gas and Electric Corporation (RG&E) agrees wi th the violation identified in that Maintenance Calibration Procedure CP-224 "Calibration and/or Maintenance of Containment High Range Area Monitors" was not properly maintained to cover the complete calibration of these instruments in accordance with Table II.F.2.-3 of NUREG-0737. Specifi cally, the steps which require channel calibration using an approved radiation source below 10 R/hr were i             tl nad ver ten y deleted when a Procedure Change Notice (PCN) was submitted to change the Procedure from Revision 3 to Revision 4.
conducted on July 27-31, 1987, and in accordance
The following is=- RG&E's explanation and reply to this statement    of'iolation:
with the"General Statement of Poli cy and Procedure for NRC Enforcement
1~  Corrective steps which have been taken and the results achieved:
Actions", 10 CFR Part 2, Appendix C (Enforcement
a~     Procedure   CP-224 was changed   on July 31, 1987 to incorporate the steps required to         document   the radiation source check steps.
Policy)(1986), the following violation was identified:
Revised copy of CP-224 was used and completed for both containment high range radiation monitors on August 12, 1987, with satisfactory results.
Techni cal Speci f'i cati on 6.8.1 (a)requires, in part, that written procedures
20  Corrective steps which wi 1 l     be taken   to avoid further violati ons:
be established, implemented
The change to incorporate the performance radiation source check was a permanent changeof toa a~
and maintained
CP-224 and, therefore, will continue to ensure that these steps are performed and documented.
covering the activities
: b. A letter has been issued to all plant personnel to stress the importance of a step by step review of all procedure changes to insure that all changes are incorporated properly, and to all Procedure Specialists to stress the importance of routing all permanent procedure changes (other than typographical error corrections) for a step by step review for complete-ness.
referenced
 
in Appendix A of Regul atory Guide 1.33, November 1972.One of those activities, procedures
Cl Page 3 Inspection Report 87-19 October 01, 1987 3 ~   Date when full compliance will be achieved:
for control of measuring and test equipment, in Section H of Appendix Regulatory
Documentation of the source check of the high range containment radiation monitors was achieved upon completion of the revised CP-224 procedure on August 12, 1987.
Guide 1.33, requires that specific i mpl ementi ng procedures
                                      ~a W~
for each survei llance test, inspection
Very Roper truly yours, PT. Kober Vice President Electric Production xc:     Document Control Clerk RVK: ss
or calibration
 
listed in Technical Specifica-
49 CS}}
ti ons be provided to assure that...instruments...
are properly controlled, calibrated
and adjusted at specified periods to maintain accuracy.Table 4.1-3, Accident Moni tori ng Instrumentation
Survei l lance Requi rements, of the li censee~s Technical Specifications
requires that a channel calibration
of the Containment
Area High Range Radiation Monitors (R-29 and R-30)be performed at each refueling in accordance
with criteria for calibration
provided in Table II.F.1-3 of NUREG-0737.
87~0>30m<BVX0OS PDR ADOCK 05000244 8 PDR g~ml  
'
Page 2 Inspection
Report 87-19 October 01, 1987 Contrary to the above, as of July 30, 1987, a procedure was not established
and implemented
which incorporated
all criteria for calibration
specified in Table II.F.1,-3 of NUREG-0737.
Speci fi cally, procedures
di d not provide for channel calibration
of monitors R-29 and R-30 with a source at one point below 10R/hr.The following is=-RG&E's explanation
and reply to this statement of'iolation:
1~Corrective
steps which have been taken and the results achieved: Rochester Gas and Electric Corporation (RG&E)agrees wi th the violation identified
in that Maintenance
Calibration
Procedure CP-224"Calibration
and/or Maintenance
of Containment
High Range Area Monitors" was not properly maintained
to cover the complete calibration
of these instruments
in accordance
with Table II.F.2.-3 of NUREG-0737.
Specifi cally, the steps which require channel calibration
using an approved radiation source below 10 R/hr were i nad ver ten tl y deleted when a Procedure Change Notice (PCN)was submitted to change the Procedure from Revision 3 to Revision 4.a~Procedure CP-224 was changed on July 31, 1987 to incorporate
the steps required to document the radiation source check steps.Revised copy of CP-224 was used and completed for both containment
high range radiation monitors on August 12, 1987, with satisfactory
results.2 0 Corrective
steps which wi 1 l be taken to avoid further viol ati ons: a~b.The change to incorporate
the performance
of a radiation source check was a permanent change to CP-224 and, therefore, will continue to ensure that these steps are performed and documented.
A letter has been issued to all plant personnel to stress the importance
of a step by step review of all procedure changes to insure that all changes are incorporated
properly, and to all Procedure Specialists
to stress the importance
of routing all permanent procedure changes (other than typographical
error corrections)
for a step by step review for complete-ness.  
Cl  
Page 3 Inspection
Report 87-19 October 01, 1987 3~Date when full compliance
will be achieved: Documentation
of the source check of the high range containment
radiation monitors was achieved upon completion
of the revised CP-224 procedure on August 12, 1987.Very truly yours,~a W~Roper PT.Kober Vice President Electric Production
xc: Document Control Clerk RVK: ss  
49 CS
}}

Latest revision as of 10:58, 4 February 2020

Responds to Violations Noted in Insp Rept 50-244/87-19. Corrective Actions:Procedure CP-224 Changed on 870731 to Incorporate Steps Required to Document Radiation Source Check Steps
ML17261A626
Person / Time
Site: Ginna Constellation icon.png
Issue date: 10/01/1987
From: Kober R
ROCHESTER GAS & ELECTRIC CORP.
To: Russell W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-2.F.1, TASK-TM NUDOCS 8710130224
Download: ML17261A626 (8)


Text

REGULATORY INFORMATION DISTRIBUTION SYSTEM (BIDS) i ACCESSION NBR: 8710130224 DOC. DATE: 87/10/01

~ NOTARIZED: NO DOCKET FACIL: 50-244 Robert Emmet Ginna Nuclear Planti Unit i. Rochester Q 05000244 AUTH. NAME AUTHOR AFFILIATION OBER R. N. Rochester Qas 5 Electric Corp.

~

~

REC IP. NAME RECIPIENT AFFILIATION RUSSELL W. T. Region 1 Office of Director

SUBJECT:

Responds to violations noted in Insp Rept 50-244/87-19.

Corrective actions: Procedure CP-224 changed on 870731 to incorporate steps required to document radiation source chec k steps.

DISTRIBUTION CODE: IE01D COPIES RECEIVED: LTR ~

ENCL ~ SIZE:

TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES: License Exp date in accordance eith 10CFR2i 2. 109(9/19/72). 05000244 RECIPIENT COPIES RECIPIENT COP IES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PDi-3 PD STAHLEi C INTERNAL: AEOD DEDRO NRR MOR ISSEAU) D NRR/DOEA DIR NRR/DREP/EPB NRR/DREP/RPB NRR/DRIS DIR NRR/P MAS/ ILRB OE~EBERMANi J OQC/HDS2 REG FILEE) RES DEPY QI RQNC FTl E Oi ERNAL: LPDR NRC PDR NSIC TOTAL NUMBER OF COPIES REQUIRED: LTTR 20 ENCL

N[1

~ ~ v ~ ~

C'y',

so~~

> 51AIC ROCHESTER >As .'. e ',t .,I~hi <'.iRi-ORATION 89 EAST AVENUE, ROCHESTER, N.Y. 74649-OP07 ROGER Vd 't(OQEf, TOLD @+Oh(

YKC PflCSl CRT f<L'C ~ RK'. PROD@, T,c ARE< conc ale 546 2700 Ginna Station October 01, 1987 Mr. Vi lliam T. Russell, Regional Administrator U.S. Nuclear Regulatory Commission Region 631 Park Avenue I

King of Prussia, PA 19406 Subj ect: Inspection Report 50-244/87-19 Notice of'iolation R.E. Ginna Nuclear Power Plant Docket No. 50-244

Dear Mr. Russell:

Rou tine unannounced occupati onal radiation protection Inspection Report 50-244/87-19 states in part:

As a result of the inspection conducted on July 27-31, 1987, and in accordance with the "General Statement of Poli cy and Procedure for NRC Enforcement Actions", 10 CFR Part 2, Appendix C (Enforcement Policy) (1986), the following violation was identified:

Techni cal Speci f'i cati on 6. 8. 1 (a) requires, in part, that written procedures be established, implemented and maintained covering the activities referenced in Appendix A of Regul atory Guide 1. 33, November 1972.

One of those activities, procedures for control of measuring and test equipment, in Section H of Appendix Regulatory Guide 1.33, requires that specific iinspection mpl ementi ng procedures for each survei llance test, or calibration listed in Technical Specifica-ti ons be provided to assure that... instruments... are properly controlled, calibrated and adjusted at specified periods to maintain accuracy. Table 4.1-3, Accident Moni tori ng Instrumentation Survei l lance Requi rements, of the li censee s Technical Specifications requires

~

that a channel calibration of the Containment Area High Range Radiation Monitors (R-29 and R-30) be performed at each refueling in accordance with criteria for calibration provided in Table II.F.1-3 of NUREG-0737.

87~0>30m< BVX0OS PDR ADOCK 05000244 8 PDR g~ml

Page 2 Inspection Report 87-19 October 01, 1987 Contrary to the above, as of July 30, 1987, a procedure was not established and implemented which incorporated all criteria for calibration specified in Table II.F.1,-3 of NUREG-0737. Speci fically, procedures di d not provide for channel calibration of monitors R-29 and R-30 with a source at one point below 10R/hr.

Rochester Gas and Electric Corporation (RG&E) agrees wi th the violation identified in that Maintenance Calibration Procedure CP-224 "Calibration and/or Maintenance of Containment High Range Area Monitors" was not properly maintained to cover the complete calibration of these instruments in accordance with Table II.F.2.-3 of NUREG-0737. Specifi cally, the steps which require channel calibration using an approved radiation source below 10 R/hr were i tl nad ver ten y deleted when a Procedure Change Notice (PCN) was submitted to change the Procedure from Revision 3 to Revision 4.

The following is=- RG&E's explanation and reply to this statement of'iolation:

1~ Corrective steps which have been taken and the results achieved:

a~ Procedure CP-224 was changed on July 31, 1987 to incorporate the steps required to document the radiation source check steps.

Revised copy of CP-224 was used and completed for both containment high range radiation monitors on August 12, 1987, with satisfactory results.

20 Corrective steps which wi 1 l be taken to avoid further violati ons:

The change to incorporate the performance radiation source check was a permanent changeof toa a~

CP-224 and, therefore, will continue to ensure that these steps are performed and documented.

b. A letter has been issued to all plant personnel to stress the importance of a step by step review of all procedure changes to insure that all changes are incorporated properly, and to all Procedure Specialists to stress the importance of routing all permanent procedure changes (other than typographical error corrections) for a step by step review for complete-ness.

Cl Page 3 Inspection Report 87-19 October 01, 1987 3 ~ Date when full compliance will be achieved:

Documentation of the source check of the high range containment radiation monitors was achieved upon completion of the revised CP-224 procedure on August 12, 1987.

~a W~

Very Roper truly yours, PT. Kober Vice President Electric Production xc: Document Control Clerk RVK: ss

49 CS