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| | STEAM GENERATOR REPAIR PROGRAM FOR THE SURRY POWER STATION UNIT NOS. 1 AND 2 Docket Nos. 50-280 I Z 50-281 License Nos. DPR-32 DPR-37 Is,ued August 17, 1977 R~vised December 2, 1977 R&vised I |
| * STEAM GENERATOR REPAIR PROGRAM FOR THE SURRY POWER STATION UNIT NOS. 1 AND 2 Docket Nos. 50-280 I Z 50-281 License Nos. DPR-32 DPR-37 Is,ued August 17, 1977 R~vised December 2, 1977 R&vised I
| | April 21, 1978 Revised June 2, 1978 Revised June 13, 1978 Revised June 30, 1978 Revised September 1, 1978 |
| April | |
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| 21, 1978 Revised June 2, 1978 Revised June 13, 1978 Revised June 30, 1978 Revised September 1, 1978 | |
| / | | / |
| VIRGINIA ELECTRIC AND POWER COMPANY | | VIRGINIA ELECTRIC AND POWER COMPANY |
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| 6 e | | 6 e |
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| **
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| SSGP 9.A.5-3 REV. 6 TABLE:A.5-1 e . 'ESTIMATED'QUANTITIES'AND'SPECIFIC'ACTIVITIES | | SSGP 9.A.5-3 REV. 6 TABLE:A.5-1 e . 'ESTIMATED'QUANTITIES'AND'SPECIFIC'ACTIVITIES |
| .. OF 'LAUNDRY. WASTE. WATER Specific Activity(l) Tota1(2) | | .. OF 'LAUNDRY. WASTE. WATER Specific Activity(l) Tota1(2) |
Line 67: |
Line 63: |
| Co-58 | | Co-58 |
| * 3. 2 X 10-6 2. 66 X l o-*2 Co-60 2.5 X ,a- 6 2.085 X 10-2 Cs-137 7.79 X 10-7 6.65 X 10~3 Cs-134 3.65 X 10- 7 | | * 3. 2 X 10-6 2. 66 X l o-*2 Co-60 2.5 X ,a- 6 2.085 X 10-2 Cs-137 7.79 X 10-7 6.65 X 10~3 Cs-134 3.65 X 10- 7 |
| * 3.04 X 10-3 6 Mn-54 2.28 X lQ-7 1.9 X 10-3 1.., 131 2.2 X ,a-7 1.84 X 10-3 Cr-51 1.4 X 10-6 | | * 3.04 X 10-3 6 Mn-54 2.28 X lQ-7 1.9 X 10-3 1.., 131 2.2 X ,a-7 1.84 X 10-3 Cr-51 1.4 X 10-6 1.16 X l o-2 TOTAL 7.25 X 10-2 e (1) Based on Surry Power Station data (2) 2,203,200 gallons of laundry water based ~n 12,240 gallons/day |
| . .
| |
| 1.16 X | |
| . . . . . . .
| |
| l o-2 TOTAL 7.25 X 10-2 e (1) Based on Surry Power Station data (2) 2,203,200 gallons of laundry water based ~n 12,240 gallons/day | |
| * for 6 mon.ths * | | * for 6 mon.ths * |
| (3) All numbers are "per unit 11 e | | (3) All numbers are "per unit 11 e |
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| * TABLE A.5-3 TOTAL ESTIMATED LIQUID EFFLUENTS Total Volume Total Activity Source (Gallons) (Ci) | | * TABLE A.5-3 TOTAL ESTIMATED LIQUID EFFLUENTS Total Volume Total Activity Source (Gallons) (Ci) |
| Laundry Wastes 2,203,200 6. 131 Steam Generator Secondary '.L side water 80,400 0.22 Local Decontamination Solutions 18,000 0.051 TOTAL 2.3 x 106 gallons 6.402 Ci Total 1977 liquid Wastes 1.4 x 108 gallons 67.67 Ci | | Laundry Wastes 2,203,200 6. 131 Steam Generator Secondary '.L side water 80,400 0.22 Local Decontamination Solutions 18,000 0.051 TOTAL 2.3 x 106 gallons 6.402 Ci Total 1977 liquid Wastes 1.4 x 108 gallons 67.67 Ci |
| *
| |
|
| |
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| **- SSGP 9.A.8-3 REV. 3 | | **- SSGP 9.A.8-3 REV. 3 |
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| (2) Biological shield wall e | | (2) Biological shield wall e |
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| ** **
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| ' . REV. 6 SSGP C\,C:,'3- \ | | ' . REV. 6 SSGP C\,C:,'3- \ |
| C.3. If decontamination is necessary, demonstrate that the methods and the decontamination solutions will not degrade or adversely affect the reactor coolant piping or components which are part of the primary system pressure boundary. Further show that the decontami-nation solutions will not have deleterious latent effects in subse-quent plant operations. | | C.3. If decontamination is necessary, demonstrate that the methods and the decontamination solutions will not degrade or adversely affect the reactor coolant piping or components which are part of the primary system pressure boundary. Further show that the decontami-nation solutions will not have deleterious latent effects in subse-quent plant operations. |
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[Table view] Category:TEXT-SAFETY REPORT
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[Table view] |
Text
- STEAM GENERATOR REPAIR PROGRAM FOR THE SURRY POWER STATION UNIT NOS. 1 AND 2
{
REVISION 7 I REMOVE INSERT Title Page/ I THle P a g e ~
Page 9.A.4-:l ~ Page 9.A;4-1 ~
Page 9.A.4-2 ~ .~
Page 9.A.5-3\./ Page 9.A.5-3 ..___....-1 Page 9.A.5-5 ~ Page 9.A.5-5~
Page 9.A.8-3 V Page 9.A.8-3 ~
Page, 9 .A. 9-2 / ' Page 9.A.9-2 ~
Page 9.C.3-1 V Page 9.A.3-1"'
P°c3e.. C\, C, '3~2
__J
STEAM GENERATOR REPAIR PROGRAM FOR THE SURRY POWER STATION UNIT NOS. 1 AND 2 Docket Nos. 50-280 I Z 50-281 License Nos. DPR-32 DPR-37 Is,ued August 17, 1977 R~vised December 2, 1977 R&vised I
April 21, 1978 Revised June 2, 1978 Revised June 13, 1978 Revised June 30, 1978 Revised September 1, 1978
/
VIRGINIA ELECTRIC AND POWER COMPANY
- ------.;;IVUI J .n.-Y I
- REV. 6 ~'1,A,,~\
A.4. ** -*
Estimate the quantity of laundry and general decontamination wastes that will be generated during the repair program. Describe the sampling program for this waste. and identify which isotopes will be specifically assayed. If beta emitters such as Fe~55 and Ni-63 are not measured, provide justification for not analyzing for these and other beta emitters which could be present.
RESPONSE
An estimate of the quantity .of laundry waste water and other potential sources of contaminated 1 i quid waste is provided in the response to qu*estion A.5.
The sampling program for this waste will be that which is required to implement the requirements of the Technical Specifications and 10 CFR 20.
Regulatory Guide 1.21, 11 Measuring, Evaluating, and Reporting Radioactivity in Solid Wastes and Releases of Radioactive Materials in Liquid and Gaseous Effluents from Light Water Cooled Nuclear Power Plants 11 serves as a basic
. guide for establishi_ng specific isotopes to be reported. The sampling pro-
. gram will be the same as that which is presently in use at the stations.
This program and identification of the specific isotopes reported has been submitted in the Arinual Reports.
It is presently not planned to measure such beta emitters as Fe-55 andl 6 Ni-63. The basis for not measuring these isotopes is that:
.1. The gross beta activity is reported. A breakdown by iso-tope only further qualifies the data required .
.2. The techniques required to determine isotope composition beta emitters is complex and its benefit is not commensurate with its cost.
- 3. Existi_ng regulations can be satisfied by current practice.
SSGP 9.A.4-2
- REV. 6 Sampling for Fe-55 has been addressed in the Standard Technical Specifications
- For the Implementation of Appendix I, NUREG 0472, May 1978. The Surry Standard Technical Specifications For the Implementation of Appendix I, are scheduled to be submitted on November 11, 1978.
6 e
SSGP 9.A.5-3 REV. 6 TABLE:A.5-1 e . 'ESTIMATED'QUANTITIES'AND'SPECIFIC'ACTIVITIES
.. OF 'LAUNDRY. WASTE. WATER Specific Activity(l) Tota1(2)
- Isotope * (uCi/ct} * * * * *Activity (Ci)
Co-58
- 3. 2 X 10-6 2. 66 X l o-*2 Co-60 2.5 X ,a- 6 2.085 X 10-2 Cs-137 7.79 X 10-7 6.65 X 10~3 Cs-134 3.65 X 10- 7
- 3.04 X 10-3 6 Mn-54 2.28 X lQ-7 1.9 X 10-3 1.., 131 2.2 X ,a-7 1.84 X 10-3 Cr-51 1.4 X 10-6 1.16 X l o-2 TOTAL 7.25 X 10-2 e (1) Based on Surry Power Station data (2) 2,203,200 gallons of laundry water based ~n 12,240 gallons/day
(3) All numbers are "per unit 11 e
- TABLE A.5-3 TOTAL ESTIMATED LIQUID EFFLUENTS Total Volume Total Activity Source (Gallons) (Ci)
Laundry Wastes 2,203,200 6. 131 Steam Generator Secondary '.L side water 80,400 0.22 Local Decontamination Solutions 18,000 0.051 TOTAL 2.3 x 106 gallons 6.402 Ci Total 1977 liquid Wastes 1.4 x 108 gallons 67.67 Ci
- The contamination levels for the secondary system components should be less than 1 uCi/cm2 and would result in insignificant releases.
- b. The ~irborne levels in occupied areas of the containment during the replacement activities are expected to be similar to those normally experienced during a refueling outage. Following the movement of the fuel, airborne levels are expected to decrease significantly. Typical specific airborne activities for a refuel-ing outage are listed in Table A.8-1.
- c. The total effluents from a unit during the replacement activities are shown in table A.8-2. These effluents will be much less than that normally experienced during routine operation as can be seen in Table A.8-2. Therefore, the maximum individual doses are popu-
.e lation doses will be much less than those during routine operation.
The doses for routine operation have been presented in "Appendix I analysis, Surry Power Station Unit Nos. 1 and 211 , dated June 1977, submitted June 17, 1977.
- d. It is presently planned to install a temporary containment venti-lation system that will be equipped with a HEPA and charcoal fil-ter. The capacity of the ventilation system will be 30,000 CFM.
The efficiency of the filter has been conservatively assumed to be at least 95 percent for the purpose of these evaluations, al-though they will be purchased to a specification which requires them to be 99.97 percent efficient.
- - SSGP 9.A.9-2 Rev-. 2 TABLE.A.9-1 SOLID WASTE ESTIMATE
{all values per unit)
Description Volume Estimated Activitl
¥Ws¥s {ft3) {Ci)
Feedwater pipe 540 37. 71 <0.03
.. Main Steam Pipe 2,400 63.81 <0.03 Primary Moisture Separator 66,000 3,520.5 <0.03 Feedwater Ring 6,300 94.5 <0.03 Thermal Sleeve 600 8.4 <0.03 Telescoping Deck Plate 9,000 652.2 <0.03 Downcomer Guard Assem-bly 102,000 7, 182 <0.03 Feedwater Nozzle 2,100 19.2 <0.03 55.gal. drums (com~
pacted waste) 416,000 7,644 6.5 Steam Generator In-sulation
- 14,900 966 <0.03 Concrete B1ocks(2) 193,050 1,350 <0.03 Rebarred Concrete 14, 125 94.5 <0.01 Upper Steam Gene-rator Support rings 29,400 60 <0.03 Support Ring Keys 3,400 7.0 <0.03 TOTAL 878,165 26,236 6.9
( 1) 1040 drums of compacted waste, includes trash, disposable protective equipment, rags, etc.
(2) Biological shield wall e
' . REV. 6 SSGP C\,C:,'3- \
C.3. If decontamination is necessary, demonstrate that the methods and the decontamination solutions will not degrade or adversely affect the reactor coolant piping or components which are part of the primary system pressure boundary. Further show that the decontami-nation solutions will not have deleterious latent effects in subse-quent plant operations.
RESPONSE
At the present time it is only *planned to decontaminate the removed por-tions of reactor coolant pipe for reuse. The method of decontamination*to be used will be electropolishing.
Electropolishi_ng has been widely used in the chemical industry to clean and prefinish chemical piping and process systems. The techniques for electropolish- 6 ing are over JO yeais old and have been tried and proven to be technically sound.
The wastes created by this process consist of two (2) 55 gallon drums of solid wastes.and 300 gallons of water. The electrolyte or decontamination solution will be removed from the site by the decontamination contractor for reuse.