ML19305A971: Difference between revisions

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om 4sa-sooo fu7'                                                            DUQUESNE LIGHT COMPANY Beaver Valley Power Station Post Office Box 4 Shippingport, PA 15077
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                                                                           %rch 12,1980 t' 'S: JAW:811 Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 LER 80-12/0lT Mr. B. H. Grier, Director of Regulation United States Nuclear Regulatory Commission Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406
                                                                           %rch 12,1980 t' 'S: JAW:811 Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 LER 80-12/0lT Mr. B. H. Grier, Director of Regulation United States Nuclear Regulatory Commission Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406


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Contrary to the above, this channel check has not been performed since July, 1976. This requirement was deleted because the meters always read zero during normal operation. Auxiliary feedwater system flow instrumentation was shown to be accurate and in calibration on October 18, 1979. Since the shutdown panel did not have to be manned for any reason, there are no safety implications associated with this incident.
Contrary to the above, this channel check has not been performed since July, 1976. This requirement was deleted because the meters always read zero during normal operation. Auxiliary feedwater system flow instrumentation was shown to be accurate and in calibration on October 18, 1979. Since the shutdown panel did not have to be manned for any reason, there are no safety implications associated with this incident.
Surveillance has been re-initiated and further checks will be made during startup when the auxiliary feedwater system is operating in order to provide positive verification of surveillance requirements.
Surveillance has been re-initiated and further checks will be made during startup when the auxiliary feedwater system is operating in order to provide positive verification of surveillance requirements.
Very truly yours,      g
Very truly yours,      g J. A. Werling        <
      -
J. A. Werling        <
Superintendent 8003180652-
Superintendent 8003180652-


     -                                                                              a 4gP
     -                                                                              a 4gP
   ..    \
   ..    \
Mr. B. H. Crier March 12, 1980 BVPS: JAW:811 Page 2
Mr. B. H. Crier March 12, 1980 BVPS: JAW:811 Page 2 cc:  Director Of Management & Program Analysis b/
                                                            .
United States Nuclear Regulatory Commission Washington, D. C. 20555 D. L. Wigginton, BVPS Licensing Project Manager United States Nuclear Regulatory Commission Washington, D. C. 20555 D. A. Beckman, Nuclear Regulatory Commission, King of Prussia, PA G. A. Olson, Secretary, Prime Movers Committee - EEI C. J. Six, PA Public Utilities Commission, Harrisburg l
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United States Nuclear Regulatory Commission Washington, D. C. 20555 D. L. Wigginton, BVPS Licensing Project Manager United States Nuclear Regulatory Commission Washington, D. C. 20555 D. A. Beckman, Nuclear Regulatory Commission, King of Prussia, PA G. A. Olson, Secretary, Prime Movers Committee - EEI C. J. Six, PA Public Utilities Commission, Harrisburg
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Latest revision as of 13:59, 1 February 2020

RO 80-12/01T:on 800312,during Operations Audit,Tech Spec Surveillance 4.3.3.5 Found to Be Violated.Required Channel Check Not Performed Since Jul 1976.Requirement Deleted Due to Meter Reading of Zero During Normal Operation
ML19305A971
Person / Time
Site: Beaver Valley
Issue date: 03/12/1980
From: Werling J
DUQUESNE LIGHT CO.
To:
References
BVPS:JAW:811, NUDOCS 8003180632
Download: ML19305A971 (2)


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om 4sa-sooo fu7' DUQUESNE LIGHT COMPANY Beaver Valley Power Station Post Office Box 4 Shippingport, PA 15077

%rch 12,1980 t' 'S: JAW:811 Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 LER 80-12/0lT Mr. B. H. Grier, Director of Regulation United States Nuclear Regulatory Commission Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

In accordance with Technical Specification 3.3.3.5, the following occurrence is reported. This incident was discussed with our Resident Inspector D. A. Beckman at 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> this date.

On March 12, 1980, BVPS was informed of a noncompliance item discovered during an operations audit. Technical Specification Surveillance 4.3.3.5 states that "each remote shutdown monitoring instrumentation channel shall be demonstrated operable by performance of a Channel Check and Channel Calibration.at the frequencies shown in Table 4.3-6". Table 4.3-6, Item 12, states that a Channel Check of the Remote Shutdown Panel Auxiliary Feedwater Flow Rate shall be checked monthly.

Contrary to the above, this channel check has not been performed since July, 1976. This requirement was deleted because the meters always read zero during normal operation. Auxiliary feedwater system flow instrumentation was shown to be accurate and in calibration on October 18, 1979. Since the shutdown panel did not have to be manned for any reason, there are no safety implications associated with this incident.

Surveillance has been re-initiated and further checks will be made during startup when the auxiliary feedwater system is operating in order to provide positive verification of surveillance requirements.

Very truly yours, g J. A. Werling <

Superintendent 8003180652-

- a 4gP

.. \

Mr. B. H. Crier March 12, 1980 BVPS: JAW:811 Page 2 cc: Director Of Management & Program Analysis b/

United States Nuclear Regulatory Commission Washington, D. C. 20555 D. L. Wigginton, BVPS Licensing Project Manager United States Nuclear Regulatory Commission Washington, D. C. 20555 D. A. Beckman, Nuclear Regulatory Commission, King of Prussia, PA G. A. Olson, Secretary, Prime Movers Committee - EEI C. J. Six, PA Public Utilities Commission, Harrisburg l

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