IR 05000369/2017004: Difference between revisions

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| issue date = 01/26/2018
| issue date = 01/26/2018
| title = NRC Integrated Inspection Report 05000369/2017004 and 05000370/2017004
| title = NRC Integrated Inspection Report 05000369/2017004 and 05000370/2017004
| author name = Ehrhardt F J
| author name = Ehrhardt F
| author affiliation = NRC/RGN-II
| author affiliation = NRC/RGN-II
| addressee name = Ray T D
| addressee name = Ray T
| addressee affiliation = Duke Energy Carolinas, LLC
| addressee affiliation = Duke Energy Carolinas, LLC
| docket = 05000369, 05000370
| docket = 05000369, 05000370
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=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 January 26, 2018 Mr. Thomas Site Vice President
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION ary 26, 2018


Duke Energy Carolinas, LLC McGuire Nuclear Station MG01VP/12700 Hagers Ferry Road Huntersville, NC 28078
==SUBJECT:==
 
MCGUIRE NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000369/2017004 AND 05000370/2017004
SUBJECT: MCGUIRE NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000369/2017004 AND 05000370/2017004


==Dear Mr. Ray:==
==Dear Mr. Ray:==
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The NRC inspectors did not identify any finding or violation of more than minor significance.
The NRC inspectors did not identify any finding or violation of more than minor significance.


This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.


Sincerely,
Sincerely,
/RA/
/RA/
Frank Ehrhardt, Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos.: 50-369, 50-370 License Nos.: NPF-9, NPF-17 Enclosure: IR 05000369/2017004 and 05000370/2017004 w/Attachment: Supplemental Information cc Distribution via ListServ
Frank Ehrhardt, Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos.: 50-369, 50-370 License Nos.: NPF-9, NPF-17
 
ML18026A783 OFFICE RII:DRP RII:DRP RII:DRSRII:DRSRII:DRS RII:DRPNAME AHutto RCureton MMeeks PCooper RWilliams MToth DATE 1/23/2018 1/25/2018 1/24/2018 1/24/2018 1/24/2018 1/25/2018 OFFICE RII:DRP RII:DRP NAME JWorosilo FEhrhardt DATE 1/25/2018 1/26/2018 Enclosure U.S. NUCLEAR REGULATORY COMMISSION
 
==REGION II==


Docket Nos.: 50-369, 50-370
===Enclosure:===
IR 05000369/2017004 and 05000370/2017004 w/Attachment: Supplemental Information


License Nos.: NPF-9, NPF-17  
REGION II==
 
Docket Nos.: 50-369, 50-370 License Nos.: NPF-9, NPF-17 Report No.: 05000369/2017004; and 05000370/2017004 Licensee: Duke Energy Carolinas, LLC Facility: McGuire Nuclear Station, Units 1 and 2 Location: Huntersville, NC 28078 Dates: October 1, 2017 through December 31, 2017 Inspectors: A. Hutto, Senior Resident Inspector R. Cureton, Resident Inspector M. Meeks, Senior Operations Engineer (Section 1R11)
Report No.: 05000369/2017004; and 05000370/2017004  
R. Williams, Senior Reactor Inspector (Section 1R08)
 
P. Cooper, Reactor Inspector (Section 1R08)
Licensee: Duke Energy Carolinas, LLC  
Approved by: Frank Ehrhardt, Chief Reactor Projects Branch 1 Division of Reactor Projects Enclosure
 
Facility: McGuire Nuclear Station, Units 1 and 2  
 
Location: Huntersville, NC 28078  
 
Dates: October 1, 2017 through December 31, 2017  
 
Inspectors: A. Hutto, Senior Resident Inspector R. Cureton, Resident Inspector M. Meeks, Senior Operations Engineer (Section 1R11) R. Williams, Senior Reactor Inspector (Section 1R08)
P. Cooper, Reactor Inspector (Section 1R08)  
 
Approved by: Frank Ehrhardt, Chief Reactor Projects Branch 1 Division of Reactor Projects  


=SUMMARY=
=SUMMARY=
IR 05000369/2017004, and 05000370/2017004; October 1, 2017, through December 31, 2017; McGuire Nuclear Station, Units 1 and 2; Integrated Inspection Report
IR 05000369/2017004, and 05000370/2017004; October 1, 2017, through December 31, 2017;


The report covered a 3-month period of inspection by resident inspectors and regional inspectors. No findings were identified during this inspection period. The NRC's program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 6.
McGuire Nuclear Station, Units 1 and 2; Integrated Inspection Report The report covered a 3-month period of inspection by resident inspectors and regional inspectors. No findings were identified during this inspection period. The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 6.


=REPORT DETAILS=
=REPORT DETAILS=
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===Summary of Plant Status===
===Summary of Plant Status===


Unit 1: Began the inspection period shutdown for a scheduled refueling outage. The unit was placed online October 16, 2017, and was returned to 100 percent rated thermal power (RTP) on October 18. The unit was operated at essentially full power for the remainder of the inspection period.
Unit 1: Began the inspection period shutdown for a scheduled refueling outage. The unit was placed online October 16, 2017, and was returned to 100 percent rated thermal power (RTP) on October 18. The unit was operated at essentially full power for the remainder of the inspection period.


Unit 2: Operated at approximately 100 percent RTP for the entire inspection period.
Unit 2: Operated at approximately 100 percent RTP for the entire inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R01}}
{{a|1R01}}
==1R01 Adverse Weather Protection==
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01}}
{{IP sample|IP=IP 71111.01}}
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===.1 Seasonal Extreme Weather Conditions===
===.1 Seasonal Extreme Weather Conditions===


The inspectors conducted a detailed review of the station's adverse weather procedures written for extreme low temperatures. The inspectors verified that weather-related equipment deficiencies identified during the previous year had been placed into the work control process and/or corrected before the onset of seasonal extremes. The inspectors evaluated the licensee's implementation of adverse weather preparation procedures and compensatory measures before the onset of seasonal extreme (cold) weather conditions. Documents reviewed are listed in the attachment.
The inspectors conducted a detailed review of the stations adverse weather procedures written for extreme low temperatures. The inspectors verified that weather-related equipment deficiencies identified during the previous year had been placed into the work control process and/or corrected before the onset of seasonal extremes. The inspectors evaluated the licensees implementation of adverse weather preparation procedures and compensatory measures before the onset of seasonal extreme (cold) weather conditions. Documents reviewed are listed in the attachment.


The inspectors evaluated the following risk-significant systems:
The inspectors evaluated the following risk-significant systems:
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===.2 Readiness to Cope with External Flooding===
===.2 Readiness to Cope with External Flooding===


The inspectors evaluated the licensee's implementation of flood protection procedures and compensatory measures during impending conditions of flooding or heavy rains.
The inspectors evaluated the licensees implementation of flood protection procedures and compensatory measures during impending conditions of flooding or heavy rains.
 
The inspectors reviewed the updated final safety analysis report and related flood analysis documents to identify those areas containing safety-related equipment that could be affected by external flooding and their design flood levels. The inspectors walked down flood protection barriers, reviewed procedures for coping with external flooding, and reviewed corrective actions for past flooding events. The inspectors verified that the procedures for coping with flooding could reasonably be used to achieve the desired results. For those areas where operator actions are credited, the inspectors assessed whether the flooding event could limit or prevent the required actions.


The inspectors reviewed the updated final safety analysis report and related flood analysis documents to identify those areas containing safety-related equipment that could be affected by external flooding and their design flood levels. The inspectors walked down flood protection barriers, reviewed procedures for coping with external flooding, and reviewed corrective actions for past flooding events. The inspectors verified that the procedures for coping with flooding could reasonably be used to achieve the desired results. For those areas where operator actions are credited, the inspectors assessed whether the flooding event could limit or prevent the required actions. Documents reviewed are listed in the attachment.
Documents reviewed are listed in the attachment.


The inspectors conducted walkdowns of the following plant areas containing risk-significant structures, systems, and components that are below flood levels or otherwise susceptible to flooding:
The inspectors conducted walkdowns of the following plant areas containing risk-significant structures, systems, and components that are below flood levels or otherwise susceptible to flooding:
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====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R04}}
{{a|1R04}}
==1R04 Equipment Alignment==
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
{{IP sample|IP=IP 71111.04}}
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The inspectors selected the following three systems or trains to inspect:
The inspectors selected the following three systems or trains to inspect:
* Unit 1, "B" train safety injection (NI) system while the "A" NI pump was out of service (OOS) for breaker maintenance
* Unit 1, B train safety injection (NI) system while the A NI pump was out of service (OOS) for breaker maintenance
* Unit 1, "B" train component cooling water (KC) system while the "A" train was OOS for planned maintenance
* Unit 1, B train component cooling water (KC) system while the A train was OOS for planned maintenance
* Unit 1, "A" train KC system while the "B" train was OOS for planned maintenance
* Unit 1, A train KC system while the B train was OOS for planned maintenance


===.2 Complete Walkdown===
===.2 Complete Walkdown===


The inspectors verified the alignment of the Unit 2 emergency diesel generator. The inspectors selected this system for assessment because it is a risk-significant mitigating system. The inspectors determined the correct system lineup by reviewing plant procedures, drawings, the updated final safety analysis report, and other documents. The inspectors reviewed records related to the system design, maintenance work requests, and deficiencies. The inspectors verified that the selected system was
The inspectors verified the alignment of the Unit 2 emergency diesel generator.


correctly aligned by performing a complete walkdown of accessible components.
The inspectors selected this system for assessment because it is a risk-significant mitigating system. The inspectors determined the correct system lineup by reviewing plant procedures, drawings, the updated final safety analysis report, and other documents. The inspectors reviewed records related to the system design, maintenance work requests, and deficiencies. The inspectors verified that the selected system was correctly aligned by performing a complete walkdown of accessible components.


To verify the licensee was identifying and resolving equipment alignment discrepancies, the inspectors reviewed corrective action documents, including condition reports and outstanding work orders. The inspectors also reviewed periodic reports containing information on the status of risk-significant systems, including maintenance rule reports and system health reports. Documents reviewed are listed in the attachment.
To verify the licensee was identifying and resolving equipment alignment discrepancies, the inspectors reviewed corrective action documents, including condition reports and outstanding work orders. The inspectors also reviewed periodic reports containing information on the status of risk-significant systems, including maintenance rule reports and system health reports. Documents reviewed are listed in the attachment.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R05}}
{{a|1R05}}
==1R05 Fire Protection==
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05AQ}}
{{IP sample|IP=IP 71111.05AQ}}
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* passive fire protection features
* passive fire protection features
* compensatory measures and fire watches
* compensatory measures and fire watches
* issues related to fire protection contained in the licensee's corrective action program The inspectors toured the following four fire areas to assess material condition and operational status of fire protection equipment. Documents reviewed are listed in the attachment.
* issues related to fire protection contained in the licensees corrective action program The inspectors toured the following four fire areas to assess material condition and operational status of fire protection equipment. Documents reviewed are listed in the attachment.
* Unit 1, motor generator (MG) set room 767' elevation, fire area 22
* Unit 1, motor generator (MG) set room 767 elevation, fire area 22
* Unit 2, MG set room 767' elevation, fire area 23
* Unit 2, MG set room 767 elevation, fire area 23
* Unit 1/2, service building basement, fire area SRV
* Unit 1/2, service building basement, fire area SRV
* Unit 2, turbine building basement, fire area 44
* Unit 2, turbine building basement, fire area 44


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R06}}
{{a|1R06}}
==1R06 Flood Protection Measures==
==1R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06}}
{{IP sample|IP=IP 71111.06}}
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====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R08}}
{{a|1R08}}
==1R08 Inservice Inspection Activities==
==1R08 Inservice Inspection Activities==
{{IP sample|IP=IP 71111.08}}
{{IP sample|IP=IP 71111.08}}


====a. Inspection Scope====
====a. Inspection Scope====
Non-Destructive Examination Acti vities and Welding Activities From October 2, 2017, through October 6, 2017, the inspectors conducted an onsite review of the implementation of the licensee's inservice inspection (ISI) program for Unit 1. The ISI program is designed to monitor degradation of pressure retaining components in vital system boundaries. The scope of this program includes components within the reactor coolant system boundary, risk-significant piping boundaries, and containment system boundaries.
Non-Destructive Examination Activities and Welding Activities From October 2, 2017, through October 6, 2017, the inspectors conducted an onsite review of the implementation of the licensees inservice inspection (ISI) program for Unit 1. The ISI program is designed to monitor degradation of pressure retaining components in vital system boundaries. The scope of this program includes components within the reactor coolant system boundary, risk-significant piping boundaries, and containment system boundaries.


The inspectors either directly observed or reviewed the following non-destructive examination (NDE) activities. These activities were mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record:
The inspectors either directly observed or reviewed the following non-destructive examination (NDE) activities. These activities were mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record:
2008 Edition with 2000 Addenda). The inspectors evaluated the NDE activities for compliance with the requirements in Section XI and Section V of the ASME Code. The inspectors also evaluated if any identified indications or defects were dispositioned in accordance with either the ASME Code or an NRC-approved alternative requirement. Additionally, the inspectors reviewed the qualifications of the NDE technicians performing the examinations to determine if they were in compliance with ASME Code
2008 Edition with 2000 Addenda). The inspectors evaluated the NDE activities for compliance with the requirements in Section XI and Section V of the ASME Code. The inspectors also evaluated if any identified indications or defects were dispositioned in accordance with either the ASME Code or an NRC-approved alternative requirement.


requirements.
Additionally, the inspectors reviewed the qualifications of the NDE technicians performing the examinations to determine if they were in compliance with ASME Code requirements.
* ultrasonic examination (UT) of weld 1RPV3-445E-SE, safe-end-to-nozzle weld, ASME Class 1 (observed)
* ultrasonic examination (UT) of weld 1RPV3-445E-SE, safe-end-to-nozzle weld, ASME Class 1 (observed)
* UT of weld 1NC1F-1-1, pipe-to-safe-end weld, ASME Class 1 (observed)
* UT of weld 1NC1F-1-1, pipe-to-safe-end weld, ASME Class 1 (observed)
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* reviewed the Effective Degradation Years and Reinspection Years calculations to determine if a volumetric examination or bare metal visual examination of the penetration nozzles was required during the current outage
* reviewed the Effective Degradation Years and Reinspection Years calculations to determine if a volumetric examination or bare metal visual examination of the penetration nozzles was required during the current outage
* reviewed the final examination report for the bare metal visual examination of ten upper head penetrations
* reviewed the final examination report for the bare metal visual examination of ten upper head penetrations
* verified that the examinations were performed in accordance with the requirements of the ASME Code and that the frequency was consistent with ASME Code Case N-729-4  
* verified that the examinations were performed in accordance with the requirements of the ASME Code and that the frequency was consistent with ASME Code Case N-729-4 The inspectors verified that the licensee did not identify any indications that were accepted for continued service. Additionally, the inspectors verified that the licensee did not perform any welding repairs to the upper head penetrations since the last Unit 1 refueling outage.
 
The inspectors verified that the licensee did not identify any indications that were accepted for continued service. Additionally, the inspectors verified that the licensee did not perform any welding repairs to the upper head penetrations since the last Unit 1 refueling outage.


Boric Acid Corrosion Control Inspection Activities  
Boric Acid Corrosion Control Inspection Activities The inspectors reviewed the licensees boric acid corrosion control program (BACCP)activities to determine if they were implemented in accordance with program requirements, applicable regulatory requirements, and industry guidance. Specifically, the inspectors performed the following activities:
 
* reviewed applicable procedures and the results of the licensees most recent containment walkdown inspection
The inspectors reviewed the licensee's boric acid corrosion control program (BACCP) activities to determine if they were implemented in accordance with program requirements, applicable regulatory requirements, and industry guidance. Specifically, the inspectors performed the following activities:
* reviewed applicable procedures and the results of the licensee's most recent containment walkdown inspection
* interviewed the BACCP owner
* interviewed the BACCP owner
* conducted an independent walkdown of accessible areas of the Unit 1 reactor building containment pipe chase
* conducted an independent walkdown of accessible areas of the Unit 1 reactor building containment pipe chase
* verified that degraded or non-conforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensee's BACCP and the CAP
* verified that degraded or non-conforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensees BACCP and the CAP
* reviewed engineering evaluations of components with boric acid leakage which verified that minimum wall thickness of those components was maintained Steam Generator Tube Inspection Activities The inspectors reviewed the Unit 1 steam generator maintenance program. This inspection schedule was verified with the requirements of the ASME Code, the licensee's technical specifications, and applicable industry guidance. For steam generators A, B, C and D, the inspectors performed the following activities to verify compliance with program requirements, regulatory requirements, and industry guidance:
* reviewed engineering evaluations of components with boric acid leakage which verified that minimum wall thickness of those components was maintained Steam Generator Tube Inspection Activities The inspectors reviewed the Unit 1 steam generator maintenance program. This inspection schedule was verified with the requirements of the ASME Code, the licensees technical specifications, and applicable industry guidance. For steam generators A, B, C and D, the inspectors performed the following activities to verify compliance with program requirements, regulatory requirements, and industry guidance:
* reviewed the scope of the eddy current (ET) examinations, and the implementation of scope expansion criteria
* reviewed the scope of the eddy current (ET) examinations, and the implementation of scope expansion criteria
* reviewed documentation for a sample of ET data analysts, probes, and testers to verify that personnel and equipment were qualified to detect the applicable degradation mechanisms
* reviewed documentation for a sample of ET data analysts, probes, and testers to verify that personnel and equipment were qualified to detect the applicable degradation mechanisms
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* reviewed a sample of ET data for four steam generator tubes with a qualified data analyst (AR96C75, BR97C72, CR85C60, and DR34C7)
* reviewed a sample of ET data for four steam generator tubes with a qualified data analyst (AR96C75, BR97C72, CR85C60, and DR34C7)
* verified that recordable indications were detected and sized in accordance with vendor procedures
* verified that recordable indications were detected and sized in accordance with vendor procedures
* compared the latest ET examination results with the last Condition Monitoring and Operational Assessment report to assess the licensee's prediction capability for maximum tube degradation
* compared the latest ET examination results with the last Condition Monitoring and Operational Assessment report to assess the licensees prediction capability for maximum tube degradation
* verified that that current examination results were bound by the operational assessment projections
* verified that that current examination results were bound by the operational assessment projections
* assessed the latest ET examination results to verify that new degradation mechanisms, if any, were identified and evaluated before plant startup
* assessed the latest ET examination results to verify that new degradation mechanisms, if any, were identified and evaluated before plant startup
* reviewed the licensee's secondary side steam generator foreign object search and retrieval activities
* reviewed the licensees secondary side steam generator foreign object search and retrieval activities
* verified that primary-to-secondary leakage for Unit 1 in each steam generator remained below the detection or action level threshold during the previous operating cycle Identification and Resolution of Problems The inspectors reviewed a sample of ISI-related issues entered into the CAP. The inspectors evaluated if the licensee had appropriately described the scope of the problem and had initiated corrective actions. The review also included the licensee's consideration and assessment of operating experience events applicable to the plant.
* verified that primary-to-secondary leakage for Unit 1 in each steam generator remained below the detection or action level threshold during the previous operating cycle Identification and Resolution of Problems The inspectors reviewed a sample of ISI-related issues entered into the CAP. The inspectors evaluated if the licensee had appropriately described the scope of the problem and had initiated corrective actions. The review also included the licensees consideration and assessment of operating experience events applicable to the plant.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R11}}
{{a|1R11}}
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
 
{{IP sample|IP=IP 71111.11}}
(71111.11)


====a. Inspection Scope====
====a. Inspection Scope====
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* simulator performance Documents reviewed are listed in the attachment.
* simulator performance Documents reviewed are listed in the attachment.


===.2 Resident Inspector Quarterly Review of Licensed Operator Performance in the Actual Plant/Main Control Room===
===.2 Resident Inspector Quarterly Review of Licensed Operator Performance in the Actual===


On October 16, 2017, the inspectors observed licensed operator performance in the main control room during Unit 1 reactor startup activities following a refueling outage.
Plant/Main Control Room On October 16, 2017, the inspectors observed licensed operator performance in the main control room during Unit 1 reactor startup activities following a refueling outage.


The inspectors assessed the following:
The inspectors assessed the following:
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===.3 Annual Review of Licensee Requalification Examination Results:===
===.3 Annual Review of Licensee Requalification Examination Results:===


On July 20, 2017, the licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2), "Requalification Requirements," of the NRC's "Operator's Licenses.During the week of December 25, 2017, the inspectors performed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance with Inspection Procedure (IP) 71111.11, "Licensed Operator Requalification Program."
On July 20, 2017, the licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2), Requalification Requirements, of the NRCs Operators Licenses. During the week of December 25, 2017, the inspectors performed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance with Inspection Procedure (IP) 71111.11, Licensed Operator Requalification Program.


These results were compared to the thresholds established in Section 3.02, "Requalification Examination Results," of IP 71111.11.
These results were compared to the thresholds established in Section 3.02, Requalification Examination Results, of IP 71111.11.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R12}}
{{a|1R12}}
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12}}
{{IP sample|IP=IP 71111.12}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors assessed the licensee's treatment of the two issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants"). The inspectors reviewed procedures and records to evaluate the licensee's identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. Documents reviewed are listed in the attachment.
The inspectors assessed the licensees treatment of the two issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. Documents reviewed are listed in the attachment.
* Unit 1, hydrogen skimmer fan, green off light dark on HVAC board
* Unit 1, hydrogen skimmer fan, green off light dark on HVAC board
* Unit 1, 1ELXC-5C did not close during 1A ESF testing
* Unit 1, 1ELXC-5C did not close during 1A ESF testing


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R13}}
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
{{IP sample|IP=IP 71111.13}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the three maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensee's risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the corrective action program. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensee's planning and control of emergent work activities. Documents reviewed are listed in the attachment.
The inspectors reviewed the three maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the corrective action program. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities.
 
Documents reviewed are listed in the attachment.
* Unit 1, October 30, 2017, equipment protection plan for B train spent fuel cooling during high decay heat
* Unit 1, October 30, 2017, equipment protection plan for B train spent fuel cooling during high decay heat
* Unit 1, December 12, 2017, equipment protection plan for the B train of KC being OOS for planned maintenance
* Unit 1, December 12, 2017, equipment protection plan for the B train of KC being OOS for planned maintenance
* Unit 1, December 14, 2017, risk management actions associated with replacing 1CF-106AB (1C steam generator feed reg. bypass valve) distributed control system control room board control module
* Unit 1, December 14, 2017, risk management actions associated with replacing 1CF-106AB (1C steam generator feed reg. bypass valve) distributed control system control room board control module


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R15}}
{{a|1R15}}
==1R15 Operability Determinations and Functionality Assessments==
==1R15 Operability Determinations and Functionality Assessments==
{{IP sample|IP=IP 71111.15}}
{{IP sample|IP=IP 71111.15}}


====a. Inspection Scope====
====a. Inspection Scope====
Operability and Functionality Review The inspectors selected the five operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the technical specification and updated final safety analysis report to the licensee's evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations.
Operability and Functionality Review The inspectors selected the five operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the technical specification and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations.


Documents reviewed are listed in the attachment.
Documents reviewed are listed in the attachment.
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* Unit 1, Equipment hatch leak rate test exceeded acceptance criteria, NCR 2158011
* Unit 1, Equipment hatch leak rate test exceeded acceptance criteria, NCR 2158011
* Unit 1, Nylon rope found in exhaust tailpipe of 1SV-19AB, NCR 02162954
* Unit 1, Nylon rope found in exhaust tailpipe of 1SV-19AB, NCR 02162954
* Unit 2, "B" motor driven auxiliary feedwater pump local control panel door handle broken off, affecting the panel's flood barrier, NCR 02170999
* Unit 2, B motor driven auxiliary feedwater pump local control panel door handle broken off, affecting the panels flood barrier, NCR 02170999
* Unit 2, 2A strainer is overflowing the top catch containment, NCR 2158735
* Unit 2, 2A strainer is overflowing the top catch containment, NCR 2158735


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R18}}
{{a|1R18}}
==1R18 Plant Modifications==
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18}}
{{IP sample|IP=IP 71111.18}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors verified that the temporary plant modification listed below did not affect the safety functions of important safety systems. The inspectors confirmed the modification did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components. The inspectors also verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition. Additionally, the inspectors evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator  
The inspectors verified that the temporary plant modification listed below did not affect the safety functions of important safety systems. The inspectors confirmed the modification did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components. The inspectors also verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition. Additionally, the inspectors evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements. Documents reviewed are listed in the attachment.
 
* Engineering Change (EC) 409880, Jumper Sliding Links B-17 and B-18 in 2AFP2B Panel
training materials, complied with licensee standards and NRC requirements. Documents reviewed are listed in the attachment.
* Engineering Change (EC) 409880, "Jumper Sliding Links B-17 and B-18 in 2AFP2B Panel"


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R19}}
{{a|1R19}}
==1R19 Post-Maintenance Testing==
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19}}
{{IP sample|IP=IP 71111.19}}
Line 305: Line 276:
* Unit 1 outage activity 11132, core reload (physics acceptance testing),
* Unit 1 outage activity 11132, core reload (physics acceptance testing),
October 15, 2017
October 15, 2017
* Work Order (WO) 20164744, PM-2EQADE0001: MISC.2A diesel generator (DG) Work Downday, October 24, 2017
* Work Order (WO) 20164744, PM-2EQADE0001: MISC.2A diesel generator (DG)
Work Downday, October 24, 2017
* WO 20201574, PM-2NVGX0016: Inspect 2B oil pump pins, November 7, 2017
* WO 20201574, PM-2NVGX0016: Inspect 2B oil pump pins, November 7, 2017
* WO 20218497, 1CFSS6060: Investigate and Repair 1CF-160AB Controls,   December 14, 2017
* WO 20218497, 1CFSS6060: Investigate and Repair 1CF-160AB Controls, December 14, 2017
* WO 20201904, PM-2EQADE0001: 2A DG fluid check, December 19, 2017 The inspectors evaluated these activities for the following:
* WO 20201904, PM-2EQADE0001: 2A DG fluid check, December 19, 2017 The inspectors evaluated these activities for the following:
* acceptance criteria were clear and demonstrated operational readiness
* acceptance criteria were clear and demonstrated operational readiness
Line 314: Line 286:
* tests were performed in accordance with approved procedures
* tests were performed in accordance with approved procedures
* equipment was returned to its operational status following testing
* equipment was returned to its operational status following testing
* test documentation was properly evaluated Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing. Documents reviewed are listed in the attachment.
* test documentation was properly evaluated Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing. Documents reviewed are listed in the attachment.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R20}}
{{a|1R20}}
==1R20 Refueling and Other Outage Activities==
==1R20 Refueling and Other Outage Activities==
{{IP sample|IP=IP 71111.20}}
{{IP sample|IP=IP 71111.20}}
Line 335: Line 306:


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R22}}
{{a|1R22}}
==1R22 Surveillance Testing==
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22}}
{{IP sample|IP=IP 71111.22}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the four surveillance tests listed below and either observed the test or reviewed test results to verify testing adequately demonstrated equipment operability and met technical specification and current licensing basis. The inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance. Additionally, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with surveillance testing. Documents reviewed are listed in the attachment.
The inspectors reviewed the four surveillance tests listed below and either observed the test or reviewed test results to verify testing adequately demonstrated equipment operability and met technical specification and current licensing basis. The inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance.
 
Additionally, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with surveillance testing. Documents reviewed are listed in the attachment.


Routine Surveillance Tests
Routine Surveillance Tests
* PT/1/A/4200/001 C "Isolation Valve Leak Rate Test, Enclosure 13.14 Test Sheet for Penetration M-302 (NI)"
* PT/1/A/4200/001 C Isolation Valve Leak Rate Test, Enclosure 13.14 Test Sheet for Penetration M-302 (NI)
* PT/0/A/4200/032, "Periodic Inspection of Ice Condenser Lower Inlet Doors"
* PT/0/A/4200/032, Periodic Inspection of Ice Condenser Lower Inlet Doors
* PT/2/A/4350/002 A, "2A Diesel Generator Operability Test" In-Service Tests (IST)
* PT/2/A/4350/002 A, 2A Diesel Generator Operability Test In-Service Tests (IST)
* PT/2/A/4252/001 A, "2A CA pump Performance Test"
* PT/2/A/4252/001 A, 2A CA pump Performance Test


====b. Findings====
====b. Findings====
Line 358: Line 330:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between October 2016 and September 2017 to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, "Regulatory Assessment Performance Indicator Guideline," and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI.
The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between October 2016 and September 2017 to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI.


In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data. Documents reviewed are listed in the attachment.
In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data. Documents reviewed are listed in the attachment.


===Cornerstone: Barrier Integrity===
===Cornerstone: Barrier Integrity===
* reactor coolant system leak rate
* reactor coolant system leak rate
* reactor coolant system specific activity
* reactor coolant system specific activity


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|4OA2}}
{{a|4OA2}}
==4OA2 Problem Identification and Resolution==
==4OA2 Problem Identification and Resolution==
{{IP sample|IP=IP 71152}}
{{IP sample|IP=IP 71152}}
===.1 Routine Review===
===.1 Routine Review===


The inspectors screened items entered into the licensee's CAP to identify repetitive equipment failures or specific human performance issues for follow-up. The inspectors reviewed nuclear condition reports, attended screening meetings, or accessed the licensee's computerized corrective action database.
The inspectors screened items entered into the licensees CAP to identify repetitive equipment failures or specific human performance issues for follow-up. The inspectors reviewed nuclear condition reports, attended screening meetings, or accessed the licensees computerized corrective action database.


===.2 Semi-Annual Trend Review===
===.2 Semi-Annual Trend Review===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed issues entered in the licensee's CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on repetitive equipment issues and human performance trends, but also considered the results of inspector daily nuclear condition report screenings, licensee trending efforts, and licensee human performance results. The review nominally considered the 6-month period of July 2017 through December 2017 although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensee's analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensee's trend reports. The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions. Documents reviewed are listed in the attachment.
The inspectors reviewed issues entered in the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on repetitive equipment issues and human performance trends, but also considered the results of inspector daily nuclear condition report screenings, licensee trending efforts, and licensee human performance results.
 
The review nominally considered the 6-month period of July 2017 through December 2017 although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensees analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensees trend reports. The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions. Documents reviewed are listed in the attachment.


====b. Findings and Observations====
====b. Findings and Observations====
No findings of significance were identified. In general, the licensee has identified trends and has appropriately addressed the trends with their CAP. However, the inspectors identified a trend associated with nuclear service water system (RN) health related to corrosion and external leakage. Prior to the 6-month review period, leakage was noted near 1RN-884 which was determined to be attributed to galvanic corrosion and an extent of condition identified wall thinning near 1RN-883 (NCR 2032731). These conditions were repaired during refueling outage M1R25. During M1R25 (October 2017), two instances of RN system corrosion were identified by the licensee (NCRs 2156395, 2156405). The first was through-wall leakage in RN test loop piping welds 1RNWEFW-12/15 and was a result of microbial induced corrosion. The second was significant wall thinning on a vent line on the 1A RN/KC heat exchanger (1RN-188) that was attributed to general corrosion. In November 2017, the inspectors identified leakage coming from the 2B RN strainer backwash piping (NCR 2169010) that was determined to be a result of a leaking mechanical coupling. None of the issues discussed challenged operability. Although the above examples are attributed to different causes, collectively they represent a degradation of RN system health.
No findings of significance were identified. In general, the licensee has identified trends and has appropriately addressed the trends with their CAP. However, the inspectors identified a trend associated with nuclear service water system (RN) health related to corrosion and external leakage. Prior to the 6-month review period, leakage was noted near 1RN-884 which was determined to be attributed to galvanic corrosion and an extent of condition identified wall thinning near 1RN-883 (NCR 2032731). These conditions were repaired during refueling outage M1R25. During M1R25 (October 2017), two instances of RN system corrosion were identified by the licensee (NCRs 2156395, 2156405). The first was through-wall leakage in RN test loop piping welds 1RNWEFW-12/15 and was a result of microbial induced corrosion. The second was significant wall thinning on a vent line on the 1A RN/KC heat exchanger (1RN-188) that was attributed to general corrosion. In November 2017, the inspectors identified leakage coming from the 2B RN strainer backwash piping (NCR 2169010) that was determined to be a result of a leaking mechanical coupling. None of the issues discussed challenged operability.


The licensee's corrective actions included extent of condition visual inspections and non-destructive testing at similar RN piping locations, and additional flushes of stagnant sections of RN piping. The inspectors will continue to monitor and assess the long term effectiveness of corrective actions. The documents reviewed and used as the basis for this trend statement are listed in the attachment to this report.
Although the above examples are attributed to different causes, collectively they represent a degradation of RN system health.
 
The licensees corrective actions included extent of condition visual inspections and non-destructive testing at similar RN piping locations, and additional flushes of stagnant sections of RN piping. The inspectors will continue to monitor and assess the long term effectiveness of corrective actions. The documents reviewed and used as the basis for this trend statement are listed in the attachment to this report.


===.3 Annual Followup of Selected Issues===
===.3 Annual Followup of Selected Issues===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted a detailed review of NCR 02115752, "2ND-14B/2ND-29A operating opposite of label."
The inspectors conducted a detailed review of NCR 02115752, 2ND-14B/2ND-29A operating opposite of label.


The inspectors evaluated the following attributes of the licensee's actions:
The inspectors evaluated the following attributes of the licensees actions:
* complete and accurate identification of the problem in a timely manner
* complete and accurate identification of the problem in a timely manner
* evaluation and disposition of operability and reportability issues
* evaluation and disposition of operability and reportability issues
Line 401: Line 376:
====b. Findings and Observations====
====b. Findings and Observations====
No findings were identified.
No findings were identified.
 
{{a|4OA5}}
{{a|4OA5}}
==4OA5 Other Activities==
==4OA5 Other Activities==


Line 408: Line 382:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a walkdown of the onsite independent spent fuel storage installation (ISFSI). The inspectors reviewed changes made to the ISFSI programs and procedures, including associated 10 CFR 72.48, "Changes, Tests, and Experiments,"
The inspectors performed a walkdown of the onsite independent spent fuel storage installation (ISFSI). The inspectors reviewed changes made to the ISFSI programs and procedures, including associated 10 CFR 72.48, Changes, Tests, and Experiments, screens and evaluations to verify that changes made were consistent with the license or certificate of compliance. The inspectors reviewed records to verify that the licensee recorded and maintained the location of each fuel assembly placed in the ISFSI. The inspectors also reviewed surveillance records to verify that daily surveillance requirements were performed as required by technical specifications. Documents reviewed are listed in the attachment.
screens and evaluations to verify that changes made were consistent with the license or certificate of compliance. The inspectors reviewed records to verify that the licensee recorded and maintained the location of each fuel assembly placed in the ISFSI. The inspectors also reviewed surveillance reco rds to verify that daily surveillance requirements were performed as required by technical specifications. Documents reviewed are listed in the attachment.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|4OA6}}
{{a|4OA6}}
==4OA6 Meetings, Including Exit==
==4OA6 Meetings, Including Exit==


On January 11, 2018, the resident inspectors presented the inspection results to Mr.
On January 11, 2018, the resident inspectors presented the inspection results to Mr.


Tom Ray and other members of the licensee's staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.
Tom Ray and other members of the licensees staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.


ATTACHMENT:
ATTACHMENT:  


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=
Line 428: Line 400:


===Licensee Personnel===
===Licensee Personnel===
: [[contact::S. Cloninger]], Weld Planning  
: [[contact::S. Cloninger]], Weld Planning
: [[contact::S. Gibby]], Maintenance Manager  
: [[contact::S. Gibby]], Maintenance Manager
: [[contact::J. Glenn]], Organizational Effectiveness Manager  
: [[contact::J. Glenn]], Organizational Effectiveness Manager
: [[contact::L. Grass]], ISI Planning  
: [[contact::L. Grass]], ISI Planning
: [[contact::M. Hatley]], SG Inspection Program  
: [[contact::M. Hatley]], SG Inspection Program
: [[contact::J. Hussey]], Licensing Engineer  
: [[contact::J. Hussey]], Licensing Engineer
: [[contact::M. Kelly]], Training Manager  
: [[contact::M. Kelly]], Training Manager
: [[contact::K. Kinard]], Security Manager  
: [[contact::K. Kinard]], Security Manager
: [[contact::N. Kunkel]], Engineering Manager  
: [[contact::N. Kunkel]], Engineering Manager
: [[contact::S. Mooneyhan]], Radiation Protection Manager  
: [[contact::S. Mooneyhan]], Radiation Protection Manager
: [[contact::T. Paglia]], Work Control Manager  
: [[contact::T. Paglia]], Work Control Manager
: [[contact::E. Pigott]], Operations Manager  
: [[contact::E. Pigott]], Operations Manager
: [[contact::T. Ray]], Vice President, McGuire Nuclear  
: [[contact::T. Ray]], Vice President, McGuire Nuclear
: [[contact::J. Smith]], Boric Acid Corrosion Control Program Owner  
: [[contact::J. Smith]], Boric Acid Corrosion Control Program Owner
: [[contact::S. Snider]], Plant Manager  
: [[contact::S. Snider]], Plant Manager
: [[contact::J. Thomas]], Regulatory Affairs Manager  
: [[contact::J. Thomas]], Regulatory Affairs Manager
: [[contact::P.T. Vu]], Regulatory Affairs  
: [[contact::P.T. Vu]], Regulatory Affairs


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==


None  
None


==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
==Section 1R01: Adverse Weather Protection==
: AD-WC-ALL-0230, Seasonal Readiness PT/0/B/4700/038, Cold Weather Protection
: PT/0/B/4700/070, On Demand Freeze Protection Verification Checklist McGuire Winter Readiness Details Report (of freeze protection program from September - December 2017) UFSAR Section 2.4, Hydrology
: MCS-1465.00-00-0012, Design Basis Specification for Flooding from External Sources
: MCC-1100.00-00-0002, McGuire Probable Maximum Precipitation Flood Analysis Drawing No.
: MC-1022-01.00, Grading Plan, Plant Area
: AP/0/A/5500/044, Plant Flooding
==Section 1R04: Equipment Alignment==
: OP/2/A/6350/002, "Diesel Generator"
: MCFD-2573-01.00, "Flow Diagram of Component Cooling System (Unit 2)"
: MCFD-1573-01.00, "Flow Diagram of Component Cooling System (Unit 1)"
: OP/1/A/6400/005 A, "Component Cooling Water System Valve and Power Supply Checklists"
==Section 1R05: Fire Protection==
: MCS-1465.00-00-0008, Design Basis Specification for Fire Protection
: MCS-1465.00-00-0022, Appendix R Safe Shutdown Analysis
: MCC-1435.00-00-0059, NFPA 805 - Appendix R Safe Shutdown Deterministic Analysis
: AD-EG-ALL-1520, Transient Combustible Control FS/1/B/9000/022, Unit 1 MG set room 767' elevation, Fire Strategy 22
: FS/2/B/9000/023, Unit 2 MG set room 767' elevation, Fire Strategy 23
: FS/2/B/9000/044, Unit 2 turbine building basement Fire Strategy #44
: MFSD-044, Unit 2 turbine building basement
: MFSD-022, Unit 1 MG set room 767' elevation
: MFSD-023, Unit 2 MG set room 767' elevation Pre-fire Plan,
: CSD-MNS-PFP-SRV-0739-001, Unit 1&2 Service Building Elevation 739
==Section 1R08: Inservice Inspection Activities==
===Procedures===
: 03-6016219, Areva Field Procedure for In-Situ Pressure Testing RSG Tubes using the Triplex Pump, Rev. 11 54-ISI-400-022, Multi-Frequency Eddy Current Examination of Tubing, Rev. 22
: 54-ISI-24-036, Written Practice for Personnel Qualification in Eddy Current Examination, Rev.
: AD-EG-PWR-1611, Boric Acid Corrosion Control Program - Implementation, Rev. 2
: AD-MN-ALL-0006, Fluid Leak Management, Rev. 0
: MP/0/A/7700/080, Inspection, Assessment, and Cleanup of Boric Acid on Plant Materials, Rev.
: NDE-NE-ALL-7202, Visual Examination of PW
: R Reactor Pressure Vessel Upper Head Penetrations, Rev. 2
: NDE-NE-ALL-7203, Visual Examination of PWR Reactor Pressure Vessel Bottom Mounted Instrument Penetrations, Rev. 2
: NDE-NE-CFR-0101, Eddy Current Guidelines for Duke Energy CFR80 Steam Generators, Rev.
: PD-EG-PWR-1801, Steam Generator Management Program, Rev. 4
: PDI-ISI-254-SE-NB, Remote Inservice Examination of Reactor Vessel Nozzle to Safe End, Nozzle to Pipe, and Safe End to Pipe Welds Using the Nozzle Scanner, Rev. 3 SM/0/A/8140/001, Welding of QA and Non-QA Piping, Valves, and Components, Rev. 42
===Calculations===
: MCC -1201.01-00-0064, EDY & RIY Calculation to Determine Reactor Vessel Head Inspection Requirements, Rev. 9 
===Drawings===
: 10019718, EXP/FAN Bar ASME Standard, 02/11/05
: 10019722, ID/OD AX/C IRC SPIRAL/EDM Combo Standard Assy, 02/08/05 8372D12, Swing Check Valve Mod 06000CS8800000, Rev. A
: MC-1414-03.20-00, ISO
: MCFI-1NC52, Rev. 4
: MC-1414-09.42-00, ISO
: MCFI-1NI53, Rev. 7
: MC-1414-22.42-02, ISO
: MCFI-1NV77, Rev. 15
: MCFD-1554-02.00, Flow Diagram of Chemical and Volume Control System (NV), Rev. 19
: MCFD-1562-03.00, Flow Diagram of Safety Injection System (NI), Rev. 17 
===Other Documents===
: 51-9272188-000, Areva McGuire Unit 1EOC25 SG ECT Inspection Plan, Rev. 0 0224-AST-101483, Condition Monitoring and Operational Assessment for McGuire Unit 1 M1R25 Outage, Rev. 1 2017-Reactor Vessel Outlet Nozzle Safe-End Weld Examination - Examination Program Plan (Scan Plan), Rev. 1 Certificate of Compliance for Calibration Block SN:
: 175808,
: 260009
: Certificate of Compliance for Transducer SN: 13A00D8N, 01Y1MM, 01R158, 01R154, 01PWPW, 01PJJ6, 01PJJ4, 01PBK8, 01P8MC, 01P8MB, 01CX0M, 15B000NA, 14I01RC0, 13E02N45, 13D01U6L, 13D01U6E Certificate of Calibration
: MIZ-80iD: 51680, 51679, 52049, 52048, 52050, 51831, 52051, 51674, 51672, 50222, 52052, 51833, 52053, 51671, 52054 Certification Records for Areva and MoreTech NDE Examiners: A2421, B1055, B2860, B3720, B4052, B4165, B5128, C1250, C5542, D9573, F3162, F3453, F6623, G1931, G2573, G3910, G7112,
: H0282, J6276, K0727, K2118, K6437, K6975, L2157, M2655, M4757, M8048,
: P2472, P4776, S5527
: Certification Records for NDE Examiners:
: MLH-3126
: Certification Records for WesDyne International NDE Examiners: 33476, 35871
: CFR80 Steam Generator Site Technique Validation for Catawba Nuclear Station Unit 1 McGuire Nuclear Station Units 1 & 2, Rev 1
: EC 405119, Alternate Repair Option for 3" RN Line at Valve 1RN-884, Rev. 1
: EC 405140, Install Non-ASME Code Encapsulation Sleeves On 1RN883 & 1RN884, Rev. 0
: EC 405141, Alternate Repair Option for 3" RN Line at Valve 1RN-883, Rev. 1
: Eddy Current Examination Technique Specification Sheet: 27091.2, 96004.3
: Linearity Record Sheets for Pulser/Receiver SAP#:
: 30024835 M-ISISG-0169.030.0040, Fourth Interval Steam Generator Tubing Inservice Inspection Plan McGuire Nuclear Station Unit 1, Rev 2
: MCC 1201.37000074, Steam Generator Management Program, McGuire Unit 1, 3/29/12
: McGuire Unit 1EOC25 Steam Generator Degradation Assessment, Rev 0 McGuire Units 1 and 2 Model
: CFR 80 Tri-Pitch Steam Generators Secondary Side Integrity Plan, Rev. 3
: MISI-1462.10-0040, Fourth Interval Inservice Inspection Plan McGuire Nuclear Station, Rev. 1
: MISI-1462.10-0040AUGISI-U1&U2, McGuire Nuclear Station - Fourth Interval Augmented Inservice Inspection Plan and Schedule Units 1 And 2, Rev. 1
: PD-EG-PWR-1611, Boric Acid Corrosion Control Program, Rev. 1
: Ultrasonic Analysis Log #:
: DM-22-01,
: DM-338-01
: VT-16-1166, Visual Examination for Boric Acid Detection - 1RPV-Head
: VT-17-099, Visual Examination for Boric Acid Detection - 1RPV-BMI-Nozzles
: VT-17-100, Visual Examination for Boric Acid Detection - 1RPV-Head Weld Document No.
: 160222,
: 171466 Weld Material Certificate of Compliance UTC No.:
: 1950757,
: 2017771,
: 2043088,
: 2044618,
: 2053345,
: 30030588,
: 30031855,
: 30047742,
: 30050920,
: 30080135 Welder Procedure Qualification Records for Welders: R. Carbonel, S. Kelly, J. Murison, C.
: Prevette, T. Surrett, W. Vause, M. Panter, R. Peoples Welding Procedure Specification: GTOO0808-04 Welding Program Procedure Qualification Record for PQR: L-110D, L-148C, L-138 
===Condition Reports===
: AR 01985576, Focused Self-Assessment Report, Boric Acid Corrosion Control Program - Implementation Procedure Effectiveness
: AR 02047008, Increased corrosion rate at 1RN-884
: AR 02055701, 1KF-134: Tighten and Clean Boron from Pipe Cap
: AR 02058427, 1-KF-VA-0134 Excessive Boron Accumulation at Pipe Cap
: AR 02074869, MNS Welding Program Self-Assessment
: AR 02086711, 1-NS-FT-5030 Excessive/Moist Boron Accumulation
: AR 02093500, 1-KF-PG-5170 Active/Excessive Boron from Threaded Connection
: AR 02094612, 1-NV-PU-0016 1B Pump Head Flange Minor Leakage/Boron
: AR 02125620, 1-KF-VA-0020 Excessive Boron accumulation and moist boron
: AR 02125711, 1-FW-FT-5250 Active & Excessive boron on Transmitter 
===Work Orders===
(WO)/Work Requests (WR)
: WO 20202500, 1NV Piping Weld Cap (Weld NV1F4316)
: WO 2178270, 1NI-126 I/R Seat Leakage
==Section 1R11: ==
: Licensed Operator Requa lification Program and Licensed Operator Performance Quarterly Resident Inspector LOR Activity Review
: NSD-509, Site Standards in Support of Operational Focus SOMP 01-07, Control Room Oversight Active Simulator Examination
: ASE-17
: EP/1/A/5000/E-0, Reactor Trip or Safety injection
: EP/1/A/500/E-1, Loss of Reactor or Secondary Coolant Resident Inspector Quarterly Review of Licensed Operator Performance in the Actual Plant/Main Control Room
: AD-OP-ALL-1000, Conduct of Operations
: SOMP 01-07, Control Room Oversight OP/1/A/6100/003, Controlling Procedure for Unit Operation OP/1/A/6100/SU-19, Heatup to 557 Degrees F
: OP/1A/6100/SU-20, Modes 1 and 2 Checklist
: PT/0/A/4150/028, Initial Criticality and Zero Power Physics Testing
==Section 1R12: Maintenance Effectiveness==
: AD-EG-ALL-1204, Single Point Vulnerability Identification, Elimination and Mitigation
: AD-EG-ALL-1206, Equipment Reliability Classification
: AD-EG-ALL-1209, System, Component, and Program Health Reports and Notebooks
: AD-EG-ALL-1210, Maintenance Rule Program
: AD-EG-ALL-1211, System Performance Monitoring and Trending Duke Equipment Reliability Maintenance Rule Database
: NCR 2152989, 1ELXC-5C did not close during 1A ESF testing
==Section 1R13: Maintenance Risk Assessments and Emergent Work Control==
: NSD-213, "Risk Management Process"
: NSD-415, "Operational Risk Management (Modes 1-3) per 10
: CFR 50.65(a)(4)"
: SOMP 02-02, "Operations Roles in the Risk Management Process"
: OMP 13-7, "Operational Control of Protected Equipment"
: AD-OP-ALL-0201, "Protected Equipment"
==Section 1R15: Operability Determinations and Functionality Assessments==
: AD-OP-ALL-0102, "Operability Decision Making"
: AD-OP-ALL-0105, "Operability Determinations and Functionality Assessment"
==Section 1R18: Plant Modifications==
: EC 409880, "Jumper Sliding Links B-17 and B-18 in 2AFP2B Panel" Applicability Determination
: AR2151825 for
: EC 409880
: AD-EG-ALL-1137, "Engineering Change Product Selection"
==Section 1R19: Post-Maintenance Testing==
: AD-EG-ALL-1155, Post Modification Testing PT/2/A/4350/002 A, "Diesel Generator 2A Operability Test"
: PT/0/A/4150/028, "Initial Criticality and Zero Power Physics Testing"
: OP/2/A/6200/001 B, "Chemical and Volume Control System Charging"
==Section 1R20: Refueling and Other Outage Activities McGuire 2EOC24 Refueling Outage Schedule==
: OP/2/A/6100/SD-16, "Preparing for NC System Drain"
: OP/2/A/6100/SD-20, "Draining the NC System"
: OP/2/A/6100/SO-1, "Maintaining NC System Level"
: OP/1/A/6100/003, Controlling Procedure for Unit Operation OP/1/A/6100/SO-1, Maintaining NC System Level OP/1/A/6100/SO-10, Controlling Procedure for LTOP Operation
: OP/1/A/6100/SU-2, Refueling and Replacing Reactor Vessel Head
: OP/1/A/6100/SU-5, Filling the NC System
: OP/1/A/6100/SU-6, Venting the NC System
: OP/1/A/6100/SU-8, Heatup to 200 Degrees F OP/1/A/6100/SU-9, Mode 4 Checklist OP/1/A/6100/SU-13, Heatup to 350 Degrees F
: OP/1/A/6100/SU-14, Removing ND from Service
: OP/1/A/6100/SU-15, Mode 3 Checklist
: OP/1/A/6100/SU-19, Heatup to 557 Degrees F OP/1A/6100/SU-20, Modes 1 and 2 Checklist PT/0/A/4150/033, Total Core Reloading
: PT/1/A/4600/003F, Containment Cleanliness and ECCS Operability Inspection
: PT/0/A/4150/028, Initial Criticality and Zero Power Physics Testing
: PT/0/A/4150/047, 1/M Monitoring During Startup
==Section 1R22: Surveillance Testing==
: AD-EG-ALL-1202, "Preventive Maintenance and Surveillance Testing Administration"
: AD-WC-ALL-0250, "Work Implementation and Completion"
: AD-EG-ALL-1720, "In-service Testing (IST) Program Implementation"
==Section 4OA1: Performance Indicator (PI) Verification==
: AD-LS-ALL-0004, "NRC Performance Indicators and Monthly Operating Report"
: AD-PI-ALL-0100, "Corrective Action Program"
==Section 4OA2: Problem Identification and Resolution==
: AD-PI-ALL-0100, "Corrective Action Program"
: AD-PI-ALL-0101, "Root Cause Evaluation"
: AD-PI-ALL-0102, "Apparent Cause Evaluation"
: AD-PI-ALL-0103, "Quick Cause Evaluation"
: AD-PI-ALL-0104, "Prompt Investigation Response Team"
: AD-PI-ALL-0105, "Effectiveness Reviews"
: AD-LS-ALL-0006, "Notification/Reportability Evaluation"


==Section 4OA5: Other Activities Operation of an Independent Spent Fuel Storage Installation (60855.1)==
: PT/1/A/4600/003B, "Daily Surveillance Items" PT/0/A/4150/034, "Fuel Assembly - Component Verification"
}}
}}

Latest revision as of 04:41, 19 December 2019

NRC Integrated Inspection Report 05000369/2017004 and 05000370/2017004
ML18026A783
Person / Time
Site: McGuire, Mcguire  Duke Energy icon.png
Issue date: 01/26/2018
From: Frank Ehrhardt
NRC/RGN-II
To: Teresa Ray
Duke Energy Carolinas
References
IR 2017004
Download: ML18026A783 (23)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION ary 26, 2018

SUBJECT:

MCGUIRE NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000369/2017004 AND 05000370/2017004

Dear Mr. Ray:

On December 31, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your McGuire Nuclear Station Units 1 and 2. On January 11, 2018, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspectors did not identify any finding or violation of more than minor significance.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Frank Ehrhardt, Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos.: 50-369, 50-370 License Nos.: NPF-9, NPF-17

Enclosure:

IR 05000369/2017004 and 05000370/2017004 w/Attachment: Supplemental Information

REGION II==

Docket Nos.: 50-369, 50-370 License Nos.: NPF-9, NPF-17 Report No.: 05000369/2017004; and 05000370/2017004 Licensee: Duke Energy Carolinas, LLC Facility: McGuire Nuclear Station, Units 1 and 2 Location: Huntersville, NC 28078 Dates: October 1, 2017 through December 31, 2017 Inspectors: A. Hutto, Senior Resident Inspector R. Cureton, Resident Inspector M. Meeks, Senior Operations Engineer (Section 1R11)

R. Williams, Senior Reactor Inspector (Section 1R08)

P. Cooper, Reactor Inspector (Section 1R08)

Approved by: Frank Ehrhardt, Chief Reactor Projects Branch 1 Division of Reactor Projects Enclosure

SUMMARY

IR 05000369/2017004, and 05000370/2017004; October 1, 2017, through December 31, 2017;

McGuire Nuclear Station, Units 1 and 2; Integrated Inspection Report The report covered a 3-month period of inspection by resident inspectors and regional inspectors. No findings were identified during this inspection period. The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 6.

REPORT DETAILS

Summary of Plant Status

Unit 1: Began the inspection period shutdown for a scheduled refueling outage. The unit was placed online October 16, 2017, and was returned to 100 percent rated thermal power (RTP) on October 18. The unit was operated at essentially full power for the remainder of the inspection period.

Unit 2: Operated at approximately 100 percent RTP for the entire inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

.1 Seasonal Extreme Weather Conditions

The inspectors conducted a detailed review of the stations adverse weather procedures written for extreme low temperatures. The inspectors verified that weather-related equipment deficiencies identified during the previous year had been placed into the work control process and/or corrected before the onset of seasonal extremes. The inspectors evaluated the licensees implementation of adverse weather preparation procedures and compensatory measures before the onset of seasonal extreme (cold) weather conditions. Documents reviewed are listed in the attachment.

The inspectors evaluated the following risk-significant systems:

  • Unit 1 and 2 freeze protection for refueling water storage tank level instrumentation
  • Unit 1 and 2 main feedwater flow transmitter compartments
  • Unit 1 and 2 freeze protection for interior and exterior doghouse equipment

.2 Readiness to Cope with External Flooding

The inspectors evaluated the licensees implementation of flood protection procedures and compensatory measures during impending conditions of flooding or heavy rains.

The inspectors reviewed the updated final safety analysis report and related flood analysis documents to identify those areas containing safety-related equipment that could be affected by external flooding and their design flood levels. The inspectors walked down flood protection barriers, reviewed procedures for coping with external flooding, and reviewed corrective actions for past flooding events. The inspectors verified that the procedures for coping with flooding could reasonably be used to achieve the desired results. For those areas where operator actions are credited, the inspectors assessed whether the flooding event could limit or prevent the required actions.

Documents reviewed are listed in the attachment.

The inspectors conducted walkdowns of the following plant areas containing risk-significant structures, systems, and components that are below flood levels or otherwise susceptible to flooding:

  • Unit 1 and 2 yard drains inside the protected area
  • Unit 1 and 2 auxiliary building, service building, and fuel handling building rooftop drainage systems

b. Findings

No findings were identified.

1R04 Equipment Alignment

a. Inspection Scope

.1 Partial Walkdown

The inspectors verified that critical portions of the selected systems were correctly aligned by performing partial walkdowns. The inspectors selected systems for assessment because they were a redundant or backup system or train, were important for mitigating risk for the current plant conditions, had been recently realigned, or were a single-train system. The inspectors determined the correct system lineup by reviewing plant procedures and drawings. Documents reviewed are listed in the attachment.

The inspectors selected the following three systems or trains to inspect:

  • Unit 1, B train safety injection (NI) system while the A NI pump was out of service (OOS) for breaker maintenance
  • Unit 1, B train component cooling water (KC) system while the A train was OOS for planned maintenance
  • Unit 1, A train KC system while the B train was OOS for planned maintenance

.2 Complete Walkdown

The inspectors verified the alignment of the Unit 2 emergency diesel generator.

The inspectors selected this system for assessment because it is a risk-significant mitigating system. The inspectors determined the correct system lineup by reviewing plant procedures, drawings, the updated final safety analysis report, and other documents. The inspectors reviewed records related to the system design, maintenance work requests, and deficiencies. The inspectors verified that the selected system was correctly aligned by performing a complete walkdown of accessible components.

To verify the licensee was identifying and resolving equipment alignment discrepancies, the inspectors reviewed corrective action documents, including condition reports and outstanding work orders. The inspectors also reviewed periodic reports containing information on the status of risk-significant systems, including maintenance rule reports and system health reports. Documents reviewed are listed in the attachment.

b. Findings

No findings were identified.

1R05 Fire Protection

a. Inspection Scope

Quarterly Inspection The inspectors evaluated the adequacy of selected fire plans by comparing the fire plans to the defined hazards and defense-in-depth features specified in the fire protection program. In evaluating the fire plans, the inspectors assessed the following items:

  • control of transient combustibles and ignition sources
  • fire detection systems
  • fire suppression systems
  • manual firefighting equipment and capability
  • passive fire protection features
  • compensatory measures and fire watches
  • issues related to fire protection contained in the licensees corrective action program The inspectors toured the following four fire areas to assess material condition and operational status of fire protection equipment. Documents reviewed are listed in the attachment.
  • Unit 1, motor generator (MG) set room 767 elevation, fire area 22
  • Unit 2, MG set room 767 elevation, fire area 23
  • Unit 1/2, service building basement, fire area SRV
  • Unit 2, turbine building basement, fire area 44

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

Internal Flooding The inspectors reviewed related flood analysis documents and walked down the areas listed below containing risk-significant structures, systems, and components susceptible to flooding. The inspectors verified that plant design features and plant procedures for flood mitigation were consistent with design requirements and internal flooding analysis assumptions. The inspectors also assessed the condition of flood protection barriers and drain systems. In addition, the inspectors verified the licensee was identifying and properly addressing issues using the corrective action program (CAP). Documents reviewed are listed in the attachment.

  • Unit 1 and 2 turbine building/auxiliary building interface flood mitigation features

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities

a. Inspection Scope

Non-Destructive Examination Activities and Welding Activities From October 2, 2017, through October 6, 2017, the inspectors conducted an onsite review of the implementation of the licensees inservice inspection (ISI) program for Unit 1. The ISI program is designed to monitor degradation of pressure retaining components in vital system boundaries. The scope of this program includes components within the reactor coolant system boundary, risk-significant piping boundaries, and containment system boundaries.

The inspectors either directly observed or reviewed the following non-destructive examination (NDE) activities. These activities were mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record:

2008 Edition with 2000 Addenda). The inspectors evaluated the NDE activities for compliance with the requirements in Section XI and Section V of the ASME Code. The inspectors also evaluated if any identified indications or defects were dispositioned in accordance with either the ASME Code or an NRC-approved alternative requirement.

Additionally, the inspectors reviewed the qualifications of the NDE technicians performing the examinations to determine if they were in compliance with ASME Code requirements.

The inspectors either directly observed or reviewed the following welding activities. The inspectors evaluated these activities for compliance with site procedures and the requirements in Section IX and Section XI of the ASME Code. Specifically, the inspectors reviewed the work orders, repair or replacement plans, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports.

The inspectors reviewed the listing of non-destructive surface and volumetric examinations performed during the previous refueling outage. The inspectors verified that the licensee did not identify any relevant indications that were analytically evaluated and accepted for continued service.

PWR Vessel Upper Head Penetration Inspection Activities The inspectors performed the following activities to verify that the requirements of the ASME Code and applicable licensee procedures were being met for the Unit 1 reactor vessel upper head:

  • reviewed the Effective Degradation Years and Reinspection Years calculations to determine if a volumetric examination or bare metal visual examination of the penetration nozzles was required during the current outage
  • reviewed the final examination report for the bare metal visual examination of ten upper head penetrations
  • verified that the examinations were performed in accordance with the requirements of the ASME Code and that the frequency was consistent with ASME Code Case N-729-4 The inspectors verified that the licensee did not identify any indications that were accepted for continued service. Additionally, the inspectors verified that the licensee did not perform any welding repairs to the upper head penetrations since the last Unit 1 refueling outage.

Boric Acid Corrosion Control Inspection Activities The inspectors reviewed the licensees boric acid corrosion control program (BACCP)activities to determine if they were implemented in accordance with program requirements, applicable regulatory requirements, and industry guidance. Specifically, the inspectors performed the following activities:

  • reviewed applicable procedures and the results of the licensees most recent containment walkdown inspection
  • interviewed the BACCP owner
  • conducted an independent walkdown of accessible areas of the Unit 1 reactor building containment pipe chase
  • verified that degraded or non-conforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensees BACCP and the CAP
  • reviewed engineering evaluations of components with boric acid leakage which verified that minimum wall thickness of those components was maintained Steam Generator Tube Inspection Activities The inspectors reviewed the Unit 1 steam generator maintenance program. This inspection schedule was verified with the requirements of the ASME Code, the licensees technical specifications, and applicable industry guidance. For steam generators A, B, C and D, the inspectors performed the following activities to verify compliance with program requirements, regulatory requirements, and industry guidance:
  • reviewed the scope of the eddy current (ET) examinations, and the implementation of scope expansion criteria
  • reviewed documentation for a sample of ET data analysts, probes, and testers to verify that personnel and equipment were qualified to detect the applicable degradation mechanisms
  • reviewed a sample of site-specific examination technique specification sheets (ETSS)
  • reviewed the in-situ steam generator tube pressure testing screening criteria; the inspectors verified that the assumed NDE flaw sizing accuracy was consistent with data from the ETSS or other applicable performance demonstrations
  • reviewed a sample of ET data for four steam generator tubes with a qualified data analyst (AR96C75, BR97C72, CR85C60, and DR34C7)
  • verified that recordable indications were detected and sized in accordance with vendor procedures
  • compared the latest ET examination results with the last Condition Monitoring and Operational Assessment report to assess the licensees prediction capability for maximum tube degradation
  • verified that that current examination results were bound by the operational assessment projections
  • assessed the latest ET examination results to verify that new degradation mechanisms, if any, were identified and evaluated before plant startup
  • reviewed the licensees secondary side steam generator foreign object search and retrieval activities
  • verified that primary-to-secondary leakage for Unit 1 in each steam generator remained below the detection or action level threshold during the previous operating cycle Identification and Resolution of Problems The inspectors reviewed a sample of ISI-related issues entered into the CAP. The inspectors evaluated if the licensee had appropriately described the scope of the problem and had initiated corrective actions. The review also included the licensees consideration and assessment of operating experience events applicable to the plant.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

a. Inspection Scope

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification

On December 13, 2017, the inspectors observed a simulator scenario conducted as part of an emergency response organization drill. The scenario consisted of a loss of coolant accident with a failure of the 1B emergency diesel generator and 1A NI pump.

The inspectors assessed the following:

  • licensed operator performance
  • the ability of the licensee to administer the scenario and evaluate the operators
  • the quality of the post-scenario critique
  • simulator performance Documents reviewed are listed in the attachment.

.2 Resident Inspector Quarterly Review of Licensed Operator Performance in the Actual

Plant/Main Control Room On October 16, 2017, the inspectors observed licensed operator performance in the main control room during Unit 1 reactor startup activities following a refueling outage.

The inspectors assessed the following:

  • use of plant procedures
  • control board manipulations
  • communications between crew members
  • use and interpretation of instruments, indications, and alarms
  • use of human error prevention techniques
  • documentation of activities
  • management and supervision Documents reviewed are listed in the attachment.

.3 Annual Review of Licensee Requalification Examination Results:

On July 20, 2017, the licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2), Requalification Requirements, of the NRCs Operators Licenses. During the week of December 25, 2017, the inspectors performed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance with Inspection Procedure (IP) 71111.11, Licensed Operator Requalification Program.

These results were compared to the thresholds established in Section 3.02, Requalification Examination Results, of IP 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors assessed the licensees treatment of the two issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. Documents reviewed are listed in the attachment.

  • Unit 1, hydrogen skimmer fan, green off light dark on HVAC board

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the three maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the corrective action program. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities.

Documents reviewed are listed in the attachment.

  • Unit 1, October 30, 2017, equipment protection plan for B train spent fuel cooling during high decay heat
  • Unit 1, December 12, 2017, equipment protection plan for the B train of KC being OOS for planned maintenance
  • Unit 1, December 14, 2017, risk management actions associated with replacing 1CF-106AB (1C steam generator feed reg. bypass valve) distributed control system control room board control module

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

Operability and Functionality Review The inspectors selected the five operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the technical specification and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations.

Documents reviewed are listed in the attachment.

  • Unit 1, 1RN-188 broken pipe, nuclear condition report (NCR) 2156405
  • Unit 1, Equipment hatch leak rate test exceeded acceptance criteria, NCR 2158011
  • Unit 2, 2A strainer is overflowing the top catch containment, NCR 2158735

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

The inspectors verified that the temporary plant modification listed below did not affect the safety functions of important safety systems. The inspectors confirmed the modification did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components. The inspectors also verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition. Additionally, the inspectors evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements. Documents reviewed are listed in the attachment.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors either observed post-maintenance testing or reviewed the test results for the maintenance activities listed below to verify the work performed was completed correctly and the test activities were adequate to verify system operability and functional capability.

  • Unit 1 outage activity 11132, core reload (physics acceptance testing),

October 15, 2017

  • Work Order (WO) 20164744, PM-2EQADE0001: MISC.2A diesel generator (DG)

Work Downday, October 24, 2017

  • WO 20201574, PM-2NVGX0016: Inspect 2B oil pump pins, November 7, 2017
  • WO 20201904, PM-2EQADE0001: 2A DG fluid check, December 19, 2017 The inspectors evaluated these activities for the following:
  • acceptance criteria were clear and demonstrated operational readiness
  • effects of testing on the plant were adequately addressed
  • test instrumentation was appropriate
  • tests were performed in accordance with approved procedures
  • equipment was returned to its operational status following testing
  • test documentation was properly evaluated Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing. Documents reviewed are listed in the attachment.

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

For the Unit 1 refueling outage from October 1, 2017, through October 16, 2017, the inspectors evaluated the following outage activities:

  • refueling, heatup, and startup
  • reactivity and inventory control
  • containment closure The inspectors verified that the licensee:
  • controlled plant configuration per administrative risk reduction methodologies
  • developed work schedules to manage fatigue
  • developed mitigation strategies for loss of key safety functions
  • adhered to operating license and technical specification requirements The inspectors verified that safety-related and risk-significant structures, systems, and components not accessible during power operations were maintained in an operable condition. The inspectors also reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with outage activities. Documents reviewed are listed in the attachment.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the four surveillance tests listed below and either observed the test or reviewed test results to verify testing adequately demonstrated equipment operability and met technical specification and current licensing basis. The inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance.

Additionally, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with surveillance testing. Documents reviewed are listed in the attachment.

Routine Surveillance Tests

  • PT/1/A/4200/001 C Isolation Valve Leak Rate Test, Enclosure 13.14 Test Sheet for Penetration M-302 (NI)
  • PT/0/A/4200/032, Periodic Inspection of Ice Condenser Lower Inlet Doors
  • PT/2/A/4350/002 A, 2A Diesel Generator Operability Test In-Service Tests (IST)
  • PT/2/A/4252/001 A, 2A CA pump Performance Test

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between October 2016 and September 2017 to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI.

In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data. Documents reviewed are listed in the attachment.

Cornerstone: Barrier Integrity

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

The inspectors screened items entered into the licensees CAP to identify repetitive equipment failures or specific human performance issues for follow-up. The inspectors reviewed nuclear condition reports, attended screening meetings, or accessed the licensees computerized corrective action database.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors reviewed issues entered in the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on repetitive equipment issues and human performance trends, but also considered the results of inspector daily nuclear condition report screenings, licensee trending efforts, and licensee human performance results.

The review nominally considered the 6-month period of July 2017 through December 2017 although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensees analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensees trend reports. The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions. Documents reviewed are listed in the attachment.

b. Findings and Observations

No findings of significance were identified. In general, the licensee has identified trends and has appropriately addressed the trends with their CAP. However, the inspectors identified a trend associated with nuclear service water system (RN) health related to corrosion and external leakage. Prior to the 6-month review period, leakage was noted near 1RN-884 which was determined to be attributed to galvanic corrosion and an extent of condition identified wall thinning near 1RN-883 (NCR 2032731). These conditions were repaired during refueling outage M1R25. During M1R25 (October 2017), two instances of RN system corrosion were identified by the licensee (NCRs 2156395, 2156405). The first was through-wall leakage in RN test loop piping welds 1RNWEFW-12/15 and was a result of microbial induced corrosion. The second was significant wall thinning on a vent line on the 1A RN/KC heat exchanger (1RN-188) that was attributed to general corrosion. In November 2017, the inspectors identified leakage coming from the 2B RN strainer backwash piping (NCR 2169010) that was determined to be a result of a leaking mechanical coupling. None of the issues discussed challenged operability.

Although the above examples are attributed to different causes, collectively they represent a degradation of RN system health.

The licensees corrective actions included extent of condition visual inspections and non-destructive testing at similar RN piping locations, and additional flushes of stagnant sections of RN piping. The inspectors will continue to monitor and assess the long term effectiveness of corrective actions. The documents reviewed and used as the basis for this trend statement are listed in the attachment to this report.

.3 Annual Followup of Selected Issues

a. Inspection Scope

The inspectors conducted a detailed review of NCR 02115752, 2ND-14B/2ND-29A operating opposite of label.

The inspectors evaluated the following attributes of the licensees actions:

  • complete and accurate identification of the problem in a timely manner
  • evaluation and disposition of operability and reportability issues
  • consideration of extent of condition, generic implications, common cause, and previous occurrences
  • classification and prioritization of the problem
  • identification of root and contributing causes of the problem
  • identification of any additional condition reports
  • completion of corrective actions in a timely manner Documents reviewed are listed in the attachment.

b. Findings and Observations

No findings were identified.

4OA5 Other Activities

Operation of an Independent Spent Fuel Storage Installation (60855.1)

a. Inspection Scope

The inspectors performed a walkdown of the onsite independent spent fuel storage installation (ISFSI). The inspectors reviewed changes made to the ISFSI programs and procedures, including associated 10 CFR 72.48, Changes, Tests, and Experiments, screens and evaluations to verify that changes made were consistent with the license or certificate of compliance. The inspectors reviewed records to verify that the licensee recorded and maintained the location of each fuel assembly placed in the ISFSI. The inspectors also reviewed surveillance records to verify that daily surveillance requirements were performed as required by technical specifications. Documents reviewed are listed in the attachment.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

On January 11, 2018, the resident inspectors presented the inspection results to Mr.

Tom Ray and other members of the licensees staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

S. Cloninger, Weld Planning
S. Gibby, Maintenance Manager
J. Glenn, Organizational Effectiveness Manager
L. Grass, ISI Planning
M. Hatley, SG Inspection Program
J. Hussey, Licensing Engineer
M. Kelly, Training Manager
K. Kinard, Security Manager
N. Kunkel, Engineering Manager
S. Mooneyhan, Radiation Protection Manager
T. Paglia, Work Control Manager
E. Pigott, Operations Manager
T. Ray, Vice President, McGuire Nuclear
J. Smith, Boric Acid Corrosion Control Program Owner
S. Snider, Plant Manager
J. Thomas, Regulatory Affairs Manager
P.T. Vu, Regulatory Affairs

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

None

LIST OF DOCUMENTS REVIEWED