IR 05000369/2023010

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Age Related Degradation Inspection Report 05000369/2023010 and 05000370/2023010
ML23286A076
Person / Time
Site: Mcguire, McGuire  Duke Energy icon.png
Issue date: 10/13/2023
From: James Baptist
Division of Reactor Safety II
To: Pigott E
Duke Energy Carolinas
References
IR 2023010
Download: ML23286A076 (1)


Text

October 13, 2023

SUBJECT:

MCGUIRE NUCLEAR STATION - AGE RELATED DEGRADATION INSPECTION REPORT 05000369/2023010 AND 05000370/2023010

Dear Edward Pigott:

On September 14, 2023, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at McGuire Nuclear Station and discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at McGuire Nuclear Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Signed by Baptist, James on 10/13/23 James B. Baptist, Chief Engineering Branch 1 Division of Reactor Safety Docket Nos. 05000369 and 05000370 License Nos. NPF-9 and NPF-17

Enclosure:

As stated

Inspection Report

Docket Numbers: 05000369 and 05000370 License Numbers: NPF-9 and NPF-17 Report Numbers: 05000369/2023010 and 05000370/2023010 Enterprise Identifier: I-2023-010-0050 Licensee: Duke Energy Carolinas, LLC Facility: McGuire Nuclear Station Location: Huntersville, NC Inspection Dates: August 28, 2023, to September 14, 2023 Inspectors: S. Campbell, Senior Reactor Systems Engineer J. Lizardi-Barreto, Reactor Inspector G. Ottenberg, Senior Reactor Inspector Approved By: James B. Baptist, Chief Engineering Branch 1 Division of Reactor Safety Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an Age Related Degradation Inspection at McGuire Nuclear Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Emergency Diesel Generator Fuel Oil and Lube Oil Hoses Installed With Less Than the Required Bend Radius Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green None (NPP) 71111.21N.

Systems NCV 05000370,05000369/2023010-01 04 Open/Closed The NRC identified a Green Finding and associated Non-cited Violation (NCV) of 10 CFR 50,

Appendix B, Criterion XI, Test Control, for the licensee's failure to incorporate the hose bend radius acceptance limits as provided by the hose vendor into the test procedure used to verify the correct installation of the fuel oil and lube oil hoses on Emergency Diesel Generators (EDGs) 1A, 2A, 1B, and 2B.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.21N.04 - Age-Related Degradation Age-Related Focused Engineering Inspection (section 03.01)

For each sample listed below, inspectors reviewed licensee activities credited to address age-related degradation to assess whether they were being performed using appropriate standards and procedures, assessed against appropriate acceptance criteria, and that maintenance was being performed at an appropriate interval. Inspectors assessed whether issues identified during licensee activities were being appropriately entered into and addressed by the station corrective action program, and whether periodic assessments of maintenance effectiveness and operating experience were being completed.

(1) Emergency Diesel Generator (EDG) Fuel Oil Flexible Hoses
(2) 1B and 2B EDG Jacket Water Cooling (KD) Piping Flexible Coupling
(3) Unit 2 VQ-1A and VQ-2B, Containment Air Release Diaphragm Valves
(4) Westinghouse Contactor for 1EMXAF01E, Vital AC-DC System Charger No EVCA
(5) 1EPCBKETB12, Circuit Breaker for 1B Nuclear Service Water (RN) pump
(6) 1VP-7A and 1VP-6B, Lower Compartment Purge Inlet Valves
(7) Unit 1 Hydrogen Igniters
(8) Unit 2 MNS-EM-5390 Relay K2, Containment Spray Containment Pressure Control Alarm Module Relay
(9) 1NSPY5540, Power Supply for 1NSLP5540/ 1VELP5110/ 1VELP5450
(10) Unit 2 Control Rod Drive Mechanism (CRDM) Thermal Sleeves
(11) 2A RN Pump Suction Piping (piping from 2A nuclear service water pond to RN pump suction)
(12) Unit Auxiliary Transformer 2ATA

INSPECTION RESULTS

Emergency Diesel Generator Fuel Oil and Lube Oil Hoses Installed With Less Than the Required Bend Radius Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green None (NPP) 71111.21N.0 Systems NCV 05000370,05000369/2023010-01 4 Open/Closed The NRC identified a Green Finding and associated Non-cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion XI, Test Control, for the licensee's failure to incorporate the hose bend radius acceptance limits as provided by the hose vendor into the test procedure used to verify the correct installation of the fuel oil and lube oil hoses on Emergency Diesel Generators (EDGs) 1A, 2A, 1B, and 2B.

Description:

During a walkdown of the EDGs, the inspectors identified that the flexible hoses installed on EDGs 1A, 2A, 1B and 2B used to deliver fuel oil and lube oil to the engines had bend radii smaller than the minimum bend radius published by the hose manufacturer, Eaton Aeroquip. The fuel oil injection pump suction/supply hoses (Catalog ID 864263 and Nordberg P/N 4425 3884) on the emergency diesel generators are Aeroquip FC300-10 material.

Aeroquip literature specifies a minimum bend radius of 5.5 inches for this hose material and diameter. The lube oil supply to the link shaft actuator is through a flexible hose (Catalog ID 864234 and Nordberg P/N 4425 4051) made from Aeroquip FC300-12 material. Aeroquip literature specifies a minimum bend radius of 6.5 inches for this hose material and diameter.

In response to the observation, the licensee initiated NCR 02486130, conducted an operability determination, and determined the EDGs remained operable. This determination was based, in part, on the licensee's prior evaluation to extend the hose replacement interval from six to 12 years. For this evaluation, the licensee removed a set of used hoses from the 1A diesel generator in 2020 and sent them for testing. The vendor lab tested new and used hoses to quantify the changes in mechanical properties of hoses that had been installed on 1A diesel for 5.6 years. While the hoses were not tested with the bend radius as installed on 1A EDG, the licensee determined the vendor testing supported the conclusion that current and near-term operability was not impacted by the configuration.

During the extent of condition review, the licensee determined 56 fuel oil hoses had a bend radius smaller than the manufacturer's acceptance limits, including 16 fuel oil hoses on EDGs 1A, 2A, and 2B and 8 fuel oil hoses on the left bank cylinders of EDG 1B. The licensee also determined that the lube oil hoses on EDGs 1A, 1B, and 2A had a smaller bend radius than specified by the hose manufacturer. There were no signs of leakage or damage to the fuel and lube oil hoses at the time of discovery, however, hoses with tighter bends may potentially experience abnormal wear and fatigue resulting in possible premature failure and downstream fluid pressures and/or flows inside the hose to be outside acceptable parameters.

In 2006, as part of the stations change in hose suppliers from original parts supplier, NAK Engineering, to the commercial hose manufacturer, Aeroquip, the licensee conducted a reverse engineering evaluation documented in Duke Energy Company Reverse Engineering Technical Document No. REDI 2020.00-00-0005, Aeroquip Fuel and Oil Hoses for MNS Diesels." The inspectors reviewed REDI 2020.00-00-0005 and test procedure PT/0/A/4350/030, "Nordberg Diesel Engine 6 Year Periodic Maintenance," Revisions 023, 027 and 029, which the licensee used to replace the hoses and accept the installation and determined that bend radius acceptance limits provided in REDI 2020.00-00-0005 were not translated into applicable sections of the procedure. The licensee previously installed the hoses under Work Orders -20378334-13, -20257780-02, -02102410-02, -20464037-01, 20464038-07, and 20464038-02, on the 1A EDG (June 2020 internal and external hose replacement), the 1B EDG (April 2019 internal and external hose replacement), the 2A EDG (April 2014 external hose replacement), the 2A EDG (July 2021 internal hose replacement),the 2B EDG (July 2022 external hose replacement), and the 2B EDG (March 2023 internal hose replacement), respectively.

Corrective Actions: The licensee initiated a condition report, conducted an operability determination, and determined the EDGs remained operable. Additionally, the licensee initiated Work Requests to replace the existing lube and fuel oil hoses on all four EDGs so the minimum bend radii is not exceeded.

Corrective Action References: NCR 02486130

Performance Assessment:

Performance Deficiency: The installation procedure for the EDG fuel oil and lube oil hoses (PT/0/A/4350/030) did not contain acceptance limits in document (Duke Energy Company Reverse Engineering Technical Document REDI Number 2020.00-00-0005, Aeroquip Fuel and Oil Hoses for MNS Diesels) for bend radius as provided by the hose vendor. The Duke Quality Assurance Program Document for Catawba, McGuire and Oconee, section D17.3.2.8, Test Control, required that:

Test procedures contain the following information or require this information be documented: 1) Requirements and acceptance limits contained in applicable design and vendor documents.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the inspectors determined the assurance of the reliability of the hose was impacted by the smaller than specified bend radius.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Exhibit 2 - Mitigating Systems Screening Questions, Item A. Mitigating SSCs and PRA Functionality (except Reactivity Control Systems), which specified that if the finding affected the design or qualification of a mitigating SSC, but it maintained its operability or PRA functionality then it screens to GREEN.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance.

Enforcement:

Violation: 10 CFR 50, Appendix B, Criterion XI, Test Control, requires, in part, that A test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents.

Contrary to the above, the test program for the EDG, which included PT/0/A/4350/030, did not incorporate requirements and acceptance limits contained in applicable design documents. Specifically, limits on the fuel oil and lube oil hose bend radius contained in applicable vendor documents contained in REDI Number 2020.00-00-0005 were not incorporated into PT/0/A/4350/030.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On September 14, 2023, the inspectors presented the Age Related Degradation Inspection results to Edward Pigott and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.21N.04 Calculations MCS-1240.03-00- McGuire Nuclear Station Plant Environmental Revision 16

0001 Qualification and Parameters

Corrective Action Action Requests 2314076, 2321224, 2351242, 2397076, 2449174, various

Documents (AR) 2456604, 2486659, 2486660, 00916710, 01580026,

01699714, 01710737, 01903878, 02236247, 02236288,

247546, 02463772, 01582835, 01614118

Corrective Action EAR 02486324 Remove legacy NOTE on MCEE-165.00-07 09/11/2023

Documents NCR 02481429 Dresser Style 38 couplings on 1B and 2B EDG do not 08/01/2023

Resulting from match parts manual

Inspection NCR 02482332 Correct Degraded Voltage Relay EDB Records 08/09/2023

NCR 02486130 Emergency diesel generator flexible hose bend radius 09/08/2023

challenges

NCR 02486869 ARD NRC Inspection Observation on NDE-NE-ALL-6401 09/14/2023

Drawings 54541862 Jacket Cooling Water Inlet Pipe 09/11/1967

91720162 Turbo Cooling Water Piping Assembly 05/05/1997

DW-26950014 3" Coupling 02/23/1961

MCM 1201.04- Diesel Fuel Oil Storage Tank Revision 15

0099.001

MCM 1205.02- 24 Type 9220 Valve 150# A.N.S.I. - Class "2" W Bettis Revision 1

0095 #732C-SR Actuator

MCM 1205.02- Cross Sectional Drawing 24" Type 9220 Valve W/ Bettis Revision 1

0098 732C-SR Actuator

MCM 1205.04- O/L 6" GRINNELL NUC. DIAPHRAGM VALVE W/#32101 10/04/2017

0133.001 AMO, ITEM 05B-219

MCM 1314.01- 600V MCC 1EMXA B/M & O/L 12/15/2016

0098.001

MCM 1314.01- Wiring Diagram SZ4 CFVNR Contactor with CPT 600V Revision 03

24.001 Non Penetration, Essential Circuit

Engineering 0000422389 REACTOR VESSEL HEAD CRDM THERMAL Revision 1

Changes SLEEVE/FUNNEL REPAIR

EC 110260 Replace H2 Glow Plugs Revision 2

EC410758 M/CN, CGI, PQL2, Various, Hose, Aeroquip, JAS/MTB 12/13/2017

Inspection Type Designation Description or Title Revision or

Procedure Date

EC421723 EDG Hose Replacement Evaluation 03/27/2023

EC71722 Evaluation of Biobor JF as a Lubricity Enhancing 11/13/2006

Supplemental Additive in Ultra Low Sulfur Diesel

MD101156 Upgrade Engine Mounted FD Duplex Filters 06/12/2008

Engineering CGI010048 Commercial Grade Item Evaluation Revision 1

Evaluations MCM-1312.03- Evaluation and Testing of ABB Circuit Breakers with Revision 0

213.001 MOBIL Grease 28

PP12 Galvanic Susceptibility Inspection Package Revision 0

PP13 Selective Leaching Inspection Package Revision 1

PP20B Buried Piping Integrity (NEI 09-14) Program Package Revision 2

PP21 Service Water Piping Corrosion Program Package Revision 5

REDI No. Aerogui:g Fuel and Oil Hoses for MNS Diesels 01/17/2007

20.00-00-0005

Miscellaneous Justification for Using PRI-D Stability Additives

Fleet PM Template for Metal Clad Breakers Revision 5

AOV PM Template 03/02/2015

00082160 PURCHASE ORDER FOR DIAPHRAGM, VALVE, 6", 08/29/2023

EPDM, M-1

00133063 Purchase Order for CAT ID 201632, contactor 07/07/2010

2007856 PM-2EQADE0001 : Perform 2-Year Inspection 10/20/2022

03037883 Purchase Order for Breaker, Circuit, Power, 4.16k, 1.2K, 12/21/2016

N CAT ID: 0000445275

03053480 Duke Energy Carolinas, LLC contract 08/16/2017

03094988 Duke Energy Carolinas, LLC contract 08/28/2023

2694 Laboratory Analysis Report 08/23/2022

203391 QC Inspection Report for HOSE, LUBE OIL PIPING, 10/26/2021

DIESEL ENGINE, 33"

3116927 Purchase Order for CAT ID 201632, contactor 09/08/2020

AR02429929 PMCH - Add EDG 2R PM scope to 6Y PM 06/02/2022

CGI010111 Commercial Grade Item Dedication for ExxonMobil Oil, Revision 0

Mobil Oil

EHM.1 Maintenance Rule Function Scoping: Provides two trains 05/27/2015

of H2 igniters to protect the containment structure from a

Inspection Type Designation Description or Title Revision or

Procedure Date

sudden overpressure due to a hydrogen reaction by

igniting and burning off low concentrations of hydrogen

gas.

EPB-E-0 Basis Document for EP/1-2/A/5000/E-0 (Reactor Trip Or Revision 3

Safety Injection)

EPRI NP-6406 _Technical Evaluation of Replacement Items (NCIG-11) December

1989

EVAL-2021-MC- (a)(1) Action Plan Approved, Actions in Progress 09/30/2020

EHM-00002181

MC, OS - 204.07 Emergency and SSF Diesel Fuel Oil Treatment 09/04/1987

MC-SFL Surveillance Frequency List (SFL) Revision 12

MCC -1535.00- McGuire PRA - Hydrogen Mitigation System Revision 6

00-0033

MCM 1205.02- Instruction Manual Type 9200 T-Ring Butterfly Valve 02/29/1984

0161 Bodies

MCM 1301.00- Diesel Gen Engine Parts Manual 03/23/2023

0077.001

MCM 1341.00- Tayco Hydrogen Igniter Equipment Test Reports Revision

0007.001 D01

MCM 1341.00- Tayco Hydrogen Igniters Similarity Test Report Revision

0007.002 D02

MCS-0165.EHM- Design Basis Specification for the Hydrogen Mitigation Revision 3

00-0001 System (EHM)

MCS-1205.04-1 Diaphragm-Type Valves to ASME Boiler & Pressure 10/21/1991

Vessel Code Section III

MCS-1301-00-00- Original Purchase Order Specification for 3500 KW, 4160 06/16/1969

0001 Volt Emergency Diesel Electric generating units

MCS-1301.00-00- NORDBERG DIESEL REPLACEMENT PARTS Revision 30

0007

ML003751396, Assessment of Age-Related Degradation of Structures August 2000

NUREG/CR-6679 and Passive Components for U.S. Nuclear Power Plants

ML14128A117 NUCLEAR REGULATORY COMMISSION INSPECTION 05/15/2014

REPORT NO. 99901445/2014-201 AND NOTICE OF

NONCONFORMANCE

Inspection Type Designation Description or Title Revision or

Procedure Date

MP-0-A-7300-066 Infrared Thermography and Motor Current Data Revision 15

Acquisition

PO 03120292 Purchase Order for Flexible Hoses 11/20/2020

R-10730 Purchase Order Receiving Inspection Report for 3"

Dresser Coupling

VP.1 Maintenance Rule Function Scoping: Maintain two trains 05/27/2015

of containment integrity.

VP.4 Maintenance Rule Function Scoping: Maintain 05/27/2015

containment closure for shutdown.

VQ-Unit 2-LSS Maintenance Rule PMG Details: Containment Air Release 05/27/2015

& Addition-Unit 2-LSS-At Power

VQ.1 Maintenance Rule Function Scoping: Provide two trains 05/27/2015

of containment isolation

VQ.2 Maintenance Rule Function Scoping: Maintain 05/27/2015

containment pressure (-0.3 to +0.3) during normal

operation such that a plant level event per AD-EG-ALL-

210 cannot occur

VQ.3 Maintenance Rule Function Scoping: Maintain 05/27/2015

containment closure for shutdown.

Procedures 48-500-10H Power Transformer Maintenance May 29,

2003

AD-EG-ALL-1103 Procurement Engineering Products Revision 7

AD-EG-ALL-1132 Preparation and Control of Engineering Changes Revision 25

AD-EG-ALL-1216 SURVEILLANCE FREQUENCY CONTROL PROGRAM Revision 3

AD-EG-ALL-1650 License Renewal Aging Management Revision 5

AD-EG-ALL-1670 VENDOR TECHNICAL INFORMATION PROGRAM 02/04/2021

AD-EG-MNS- MNS License Renewal Implementation Revision 0

1650

CP/0/A/8600/027 Sampling Diesel Fuel Oil Tanks March 7,

2008

CSD-EG-MNS- MNS License Renewal Containment Inservice Inspection Revision 0

1650-16 Plan Basis Document

CSD-EG-MNS- MNS License Renewal Containment Leak Rate Testing Revision 0

1650-17 Program Basis Document

Inspection Type Designation Description or Title Revision or

Procedure Date

ET-1215 Rochester Instrument Systems, Dual Input Revision A

Voltage/Current Alarm with Fixed Deadband

MCC -1535.00- PRA RISK SIGNIFICANT SSCS FOR THE Revision 5

00-0006 MAINTENANCE RULE

MCM 1306.00- Transformer General Electric Instruction Manual 5-25-2010

0012.001

MCM 1314.01- Instructions for A200 Size 3 or 4, 3 Pole Motor Controller 01/31/2019

0166.001

MSS SP-100- Qualification Requirements for Elastomer Diaphragms for

2015 Nuclear Service Diaphragm Valves

NPP- 311 Receipt, Inspection, and Control of QA Condition Revision 0

Materials, Parts And Components Except Nuclear Fuel

NSD-319 Vendor Technical Information Program Revision 2

NSD-319 Vendor Technical Information Program Superseded by Revision 5

AD-EG-ALL-1670, Vendor Technical Information Program

Implementation

PT/0/A/4350/021 Nordberg Diesel Engine 2 Year Periodic Maintenance Revision 44

PT/0/A/4350/030 Nordberg Diesel Engine 6 Year Periodic Maintenance Revision 29

PT/1/A/4200/001 VP VALVE LEAK RATE TEST Revision 24

N

PWROG-16003-P Evaluation of Potential Thermal Sleeve Flange Wear Revision 2

PWROG-21026-P CRDM Latch Assembly Wear - CAD Study and Decision Revision 0

Tree

Self- 02386909-05 Maintenance Rule Program Self-Assessment 06/23/2021

Assessments 02447981-05 Maintenance Rule Program Self-Assessment 10/27/2022

AS 1902585 McGuire Nuclear Station Maintenance Rule (a)(3) 11/20/2014

Assessment

AS 1971272 McGuire Maintenance Rule (a)(3) Periodic Assessment 06/23/2016

AS 2189797 Maintenance Rule Periodic Assessment For Maintenance 11/17/2017

Rule Implementation

PMCH 02481203 NRC Age-Related Degradation inspection self- 07/31/2023

assessment (AR 2479221),

QRPT 2291978 MNS Maintenance Rule (a)(3) Assessment 08/01/2019

QRPT 2386909 MNS Maintenance Rule (a)(3) Periodic Assessment 08/23/2021

Inspection Type Designation Description or Title Revision or

Procedure Date

QRPT 2447981 MNS Maintenance Rule (a)(3) Assessment 10/27/2022

Work Orders Work Orders WO-20257780-02, WO-02030303-25, WO-20464038-02,

(WO) WO-20378334, WO-20464038-07, WO-1839977-02, WO- 1839977-03, WO-1839977-07, WO-20085026-03, WO- 20085026-04, WO-20085026-05, WO-20085026-11, WO- 20184120-01, WO-20191609-01, WO-20287101-03, WO- 287101-04, WO-20287101-05, WO-20287101-11, WO- 287101-13, WO-20296864-01, WO-20296864-05, WO- 296864-06, WO-20296864-07, WO-20296864-10, WO- 296864-11, WO-20296864-12, WO-2131159-01, WO- 2131159-02, WO-2131159-03, WO-2131159-04, WO- 2131159-05, WO-2131159-06, WO-2131159-07, WO- 2131159-08, WO-20215944-01, WO-20228599-01, WO- 228599-02, WO-20258358-01, WO-20258358-02, WO- 258358-03, WO-20258358-04, WO-20258358-05, WO- 258358-06, WO-20258358-07, WO-20258358-08, WO- 258358-09, WO-20258358-10, WO-20258358-11, WO- 20399612-01, WO-20439620-01, WO-20439620-02,

WO-20439620-03, WO-20439620-04, WO-20439620-05,

WO-20439620-06, WO-20439620-07, WO-20439620-08,

WO-20439620-09, WO-20439620-10, WO-20439620-11,

WO-20439620-12, WO-02043847-01, WO-20179859-03,

WO-20157548-01, WO-2043847-02, WO-20179859-04,

WO-20367100, WO-20112178-01, WO-20257762-01,

WO-20366575-01, WO-20476892-01, WO-20215071-01,

WO-20219932-01, WO-20233880-01, WO-20238783-01,

WO-20257039-01, WO-20259283-01, WO-20276239-01,

WO-20277951-01, WO-20295501-01, WO-20298391-01,

WO-20312609-01, WO-20314742-01, WO- 20327298-01,

WO-20329603-01, WO-20347151-01, WO-20500762-01,

WO-20504388-01, WO-20519636-01, WO-20524561-01,

WO-20534858-01, WO-20539990-01, WO-20552480-01,

WO-20557497-01, WO-20568900-01, WO-20572411-01,

WO-20588630-01, WO-20589674-01, WO-20464037,

Inspection Type Designation Description or Title Revision or

Procedure Date

WO-2102410, WO-98452681, WO-513382, WO- 2097733, WO-20242840, WO-20277294, WO- 20319657, WO-20369629, WO-20462964, WO- 20469994-02, WO-20474480-02, WO-20482927-02, WO- 20488504-02, WO-20500180, WO-20544990-02, WO- 20549968-02, WO-20555435-02, WO-20591134, WO- 20597411-02, WO-20543600, WO-20580031, WO- 20324616, WO-20400717, WO-20202048, WO- 284681, WO-20355986, WO-20428877, WO- 20496394, WO-20563582

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