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| number = ML17326A222
| number = ML17326A222
| issue date = 11/22/2017
| issue date = 11/22/2017
| title = Watts Bar - Integrated Inspection Report 05000390/2017003, 05000391/2017003
| title = Integrated Inspection Report 05000390/2017003, 05000391/2017003
| author name = Blamey A J
| author name = Blamey A
| author affiliation = NRC/RGN-II/DRP/RPB6
| author affiliation = NRC/RGN-II/DRP/RPB6
| addressee name = Shea J W
| addressee name = Shea J
| addressee affiliation = Tennessee Valley Authority
| addressee affiliation = Tennessee Valley Authority
| docket = 05000390, 05000391
| docket = 05000390, 05000391
Line 15: Line 15:
| page count = 32
| page count = 32
}}
}}
See also: [[followed by::IR 05000390/2017003]]
See also: [[see also::IR 05000390/2017003]]


=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION  
{{#Wiki_filter:UNITED STATES
REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257
                                  NUCLEAR REGULATORY COMMISSION
  November 22, 2017  
                                              REGION II
Mr. Joseph W. Shea  
                              245 PEACHTREE CENTER AVENUE NE, SUITE 1200
Vice President, Nuclear Licensing
                                      ATLANTA, GEORGIA 30303-1257
Tennessee Valley Authority  
                                        November 22, 2017
Mr. Joseph W. Shea
Vice President, Nuclear Licensing
Tennessee Valley Authority
1101 Market Street, LP 3D-C
Chattanooga, TN 37402-2801
SUBJECT: WATTS BAR NUCLEAR PLANT - NUCLEAR REGULATORY COMMISSION
              INTEGRATED INSPECTION REPORT 05000390/2017003, 05000391/2017003
Dear Mr. Shea:
On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an
inspection at your Watts Bar Nuclear Plant, Unit 1 and Unit 2. On October 25, 2017, the NRC
inspectors discussed the results of this inspection with Mr. Tom Marshall and other members of
your staff. A re-exit was conducted on November 8, 2017, with Ms. Kim Hulvey. The results of
this inspection are documented in the enclosed inspection report.
The NRC inspectors documented three findings of very low safety significance (Green) in this
report which also involved violations of NRC requirements. Additionally, inspectors documented
six licensee-identified violations which were determined to be of very low safety significance in
this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with
Section 2.3.2.a of the Enforcement Policy. If you contest these violations or significance of
these NCVs, you should provide a response within 30 days of the date of this inspection report,
with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document
Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator, Region
II; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C.
20555-0001; and the NRC Resident Inspector at the Watts Bar Nuclear Plant.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the
Watts Bar Nuclear Plant.


1101 Market Street, LP 3D-C
J. Shea                                      2
This letter, its enclosure, and your response (if any) will be available for public inspection and
copying at http://www.nrc.gov/reading-rm/adams.html and in the NRC Public Document Room
in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections,
Exemptions, Requests for Withholding.
                                              Sincerely,
                                              /RA/
                                              Alan Blamey, Chief
                                              Reactor Projects Branch 6
                                              Division of Reactor Projects
Docket Nos.: 50-390, 50-391
License Nos.: NPF-90, 96
Enclosure:
IR 05000390/2017003, 05000391/2017003
  w/Attachment: Supplemental Information
cc Distribution via ListServ


Chattanooga, TN  37402-2801
SUBJECT: WATTS BAR NUCLEAR PLANT - NUCLEAR REGULATORY COMMISSION INTEGRATED INSPECTION REPORT 05000390/2017003, 05000391/2017003
Dear Mr. Shea:
On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an


inspection at your Watts Bar Nuclear Plant, Unit 1 and Unit 2. On October 25, 2017, the NRC
  ML17326A222
inspectors discussed the results of this inspection with Mr. Tom Marshall and other members of
OFFICE        RII: DRP    RII: DRP        RII: DRP    RII: DRP  RII: DRP    RII: DRP
your staff.  A re-exit was conducted on November 8, 2017, with Ms. Kim Hulvey.  The results of this inspection are documented in the enclosed inspection report.
NAME          RTaylor      BDavis          GCrespo      BBishop    JEargle      ELea
DATE          10/31/2017  11/8/2017        10/31/2017  10/31/2017 11/6/2017    11/6/2017
The NRC inspectors documented three findings of very low safety significance (Green) in this report which also involved violations of NRC requ
OFFICE        RII: DRP    RII: DRP        RII: DRP    R:II DRP  NCP Approver
irements. Additionally, inspectors documented six licensee-identified violations which were determined to be of very low safety significance in
NAME          JHamman      JJandovitz      ABlamey      JNadel    MFranke
this report.  The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.  If you contest these violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report,
DATE          10/31/2017  11/3/2017        11/21/2017  11/7/2017 11/22/2017
with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:  Document
                                     
Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator, Region
              U.S. NUCLEAR REGULATORY COMMISSION
II; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Watts Bar Nuclear Plant
                                REGION II
Docket Nos.:      50-390, 50-391
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your
License Nos.:      NPF-90, NPF-96
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the
Report No.:        05000390/2017003, 05000391/2017003
Watts Bar Nuclear Plant.  
Licensee:          Tennessee Valley Authority (TVA)
 
Facility:          Watts Bar Nuclear Plant, Units 1 and 2
Location:          Spring City, TN 37381
 
Dates:            July 1 through September 30, 2017
J. Shea 2
Inspectors:        J. Nadel, Senior Resident Inspector
  This letter, its enclosure, and your response (if any) will be available for public inspection and
                  J. Hamman, Resident Inspector
copying at http://www.nrc.gov/reading-rm/adams.html and in the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, "Public Inspections, Exemptions, Requests for Withholding."
                  J. Jandovitz, Senior Resident Inspector
                  E. Lea, Regional Government Liaison Officer
      Sincerely,
                  S. Freeman, Senior Reactor Analyst
                  J. Eargle, Senior Construction Inspector
                  B. Bishop, Project Engineer
                  G. Crespo, Senior Construction Inspector
                  C. Rapp, Senior Project Engineer
                  R. Taylor, Senior Project Inspector
                  B. Davis, Senior Construction Inspector
Approved by:      Alan Blamey, Chief
                  Reactor Projects Branch 6
                  Division of Reactor Projects
                                                              Enclosure


      /RA/
                                            SUMMARY
      Alan Blamey, Chief 
IR 05000390/2017-003; 05000391/2017-003; July 1, 2017 - September 30, 2017; Watts Bar
      Reactor Projects Branch 6  
Nuclear Plant; Operability Evaluations, Surveillance Testing.
      Division of Reactor Projects
The report covered a three-month period of inspection by the resident inspectors. Three Green
non-cited violations (NCV) were identified. The significance of most findings is indicated by their
color (i.e., Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC)
0609, "Significance Determination Process," (SDP) dated April 29, 2015. Cross-cutting aspects
are determined using IMC 0310, Aspects Within Cross-Cutting Areas, dated
December 04, 2014. All violations of NRC requirements are dispositioned in accordance with
the NRCs Enforcement Policy, dated November 1, 2016. The NRCs program for overseeing
the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor
Oversight Process, Revision 6. Documents reviewed by the inspectors not identified in the
Report Details are listed in the Attachment.
Cornerstone: Mitigating Systems
*  Green. An NRC-identified NCV was identified for the failure to maintain written procedures
    for emergencies. Emergency procedure 1-E-1, Revision 7 and 2-E-1 Revision 0, both titled
    Loss of Reactor or Secondary Coolant, were updated to include steps directing
    inappropriate actions that would have affected emergency raw cooling water (ERCW) supply
    flow during an accident. The immediate corrective action was to remove the inappropriate
    steps. This violation was documented in the licensees corrective action program (CAP) as
    CR 1331422.
    The performance deficiency was more than minor because it affected the Mitigating
    Systems Cornerstone attribute of Procedure Quality and adversely affected the cornerstone
    objective in that the reduced ERCW flow caused by the inappropriate steps affects the heat
    removal capability of the ERCW and component cooling systems (CCS) during a loss of
    coolant accident (LOCA). The finding was determined to require a detailed risk evaluation
    because it represented an actual loss of function of at least a single train for greater than its
    TS allowed outage time. The result was less than 1E-6 for each unit which would be a
    finding of very low significance (Green). The risk was mitigated because the performance
    deficiency would affect operation only when a LOCA occurred and simultaneous loss of two
    shutdown boards. The finding has a cross-cutting aspect in the documentation attribute of
    the Human Performance area because the licensee did not maintain the accuracy of 1-E-1
    through its revisions and did not maintain procedure 2-E-1 accurate at its creation. (H.7)
    (Section 1R15)
*  Green. An NRC-identified NCV of Technical Specification (TS) 5.7.1.1.a, Procedures, was
    identified for the failure to maintain TVA procedures 1-GO-6 and 2-GO-6, both titled Unit
    Shutdown from Hot Standby to Cold Shutdown. The licensee failed to update the
    procedures prior to commencing dual unit operation to include steps that would shut down
    the running motor driven auxiliary feedwater pump prior to starting a third ERCW pump
    during the time period where the opposite unit has been shut down less than 48 hours. The
    licensees immediate corrective actions included revising both procedures to add the
    required steps. This violation was documented in the licensees CAP as CR 1318176.


Docket Nos.:  50-390, 50-391 
                                                  3
License Nos.:  NPF-90, 96
    The performance deficiency was more than minor because it affected the Mitigating
    Systems Cornerstone attribute of Equipment Performance and adversely affected the
    cornerstone objective in that failure to maintain the procedures resulted in a situation where
    the emergency diesel generator would have been rendered inoperable during a design basis
    event. The inspectors determined the finding was of very low safety significance (Green)
    because the finding did not represent an actual loss of function of a single train for greater
    than its TS allowed outage time. The finding had a cross-cutting aspect in the Avoid
    Complacency attribute of the Human Performance area because engineering missed a
    critical aspect of the required procedure changes associated with design change notice
    62151 when performing the prompt determination of operability and the review process was
    unsuccessful at identifying the error [H.12]. (Section 1R15)
Cornerstone: Initiating Events
*   Green. A self-revealed NCV of (TS) 5.7.1.1.a, Procedures, was identified for the failure to
    follow TVA procedure 2-SI-68-86, 18 month Channel Calibration of Remote Shutdown
    Monitoring Narrow Range Pressurizer Pressure Loop 2-LPP-68-337C, revision 4. The
    licensee failed to properly follow step 6.2.6 [1.3], which resulted in the inadvertent lifting of a
    pressurizer power operated relief valve (PORV). The licensees immediate corrective
    actions included revising the procedure. This violation was documented in the licensees
    CAP as CR 1309345.
    The performance deficiency was more than minor because it affected the Initiating Events
    Cornerstone attribute of Human Performance and adversely affected the cornerstone
    objective in that failing to follow procedure 2-SI-68-86 caused a depressurization of the plant
    that had to be stopped by operator action. The finding was determined to be very low safety
    significance (Green) because the resultant leakage from the open PORV would be
    self-limiting such that it would stop before impacting the operating method of decay heat
    removal. The finding had a cross-cutting aspect in the Challenge the Unknown component
    of the Human Performance area as defined in NRC IMC 0310, because the technicians
    failed to recognize that the output was already set to 0, but proceeded anyway to toggle the
    output which resulted in setting it to 1 [H.11]. (Section 1R22)
Six violations of very low safety significance, identified by the licensee, have been reviewed by
the NRC. Corrective actions taken or planned by the licensee have been entered into the
licensees CAP. These violations and the corrective action tracking numbers are listed in
Section 4OA7 of this report.


                                        REPORT DETAILS
Enclosure:   
Summary of Plant Status
IR 05000390/2017003, 05000391/2017003
Unit 1 operated at 100 percent rated thermal power (RTP) for the entire reporting period.
   w/Attachment: Supplemental Information
Unit 2 began the reporting period shutdown for repairs to the main condenser. The unit was
started up on July 23, 2017, but was shutdown to hot standby later that day due to equipment
cc Distribution via ListServ
problems. On July 25, 2017, startup resumed, but the reactor was tripped before criticality due
to rod position indication problems during the startup. Startup commenced again on
July 27, 2017, but was stopped due to additional rod position indication problems. Unit 2 started
up after rod position indication repairs on July 30, 2017, and achieved 29 percent RTP on
August 2, 2017. The unit remained at that power until August 8, 2017, when the turbine was
tripped due to a steam leak on a turbine drain line. The unit stabilized at 8 percent RTP and
remained there until power ascension resumed after drain line repairs. Unit 2 reached
100 percent RTP on August 8, 2017, and remained there for the remainder of the reporting
period.
1.      REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection (71111.01)
        External Flood Protection Inspection
  a.   Inspection Scope
        The inspectors reviewed the licensees readiness to cope with external flooding.
        External flooding from a probable maximum precipitation (PMP) or design basis flood
        (DBF) had the potential for internal flooding of a portion of a number of the plant
        structures. The inspectors reviewed the feasibility of the licensees flooding mitigation
        plans and design features and verified that they were consistent with the licensees
        design requirements and the risk analysis assumptions for coping with this type of
        event. The inspectors performed walkdowns of selected areas to observe grading, yard
        drains, and curbs in the vicinity of the south valve vault rooms. The inspectors also
        checked status of the flood mode boat. The inspectors reviewed external flood
        protection features at the intake pumping station and condition of the strainer room sump
        pumps. Additionally, the inspectors reviewed the licensees related corrective action
        documents (condition reports) to ensure any non-conforming conditions related to
        potential flooding were properly addressed. The inspection was performed prior to the
        expected rainfall from Hurricane Irma. This activity constituted one Adverse Weather
        Protection inspection sample, as defined in Inspection Procedure (IP) 71111.01.
  b.   Findings
        No findings were identified.


   
                                                5
 
1R04 Equipment Alignment (71111.04)
    Partial System Walkdowns
a.  Inspection Scope
    The inspectors conducted the equipment alignment partial walkdowns listed below to
    evaluate the operability of selected redundant trains or backup systems prior to unit
    transition into the mode of applicability for the systems. This also included that
    redundant trains were returned to service properly. The inspectors reviewed the
    functional system descriptions, the Updated Final Safety Analysis Report (UFSAR),
    system operating procedures, and TS to determine correct system lineups for the current
    plant conditions. The inspectors performed walkdowns of the systems to verify that
    critical components were properly aligned and to identify any discrepancies which could
    affect operability of the redundant train or backup system. This activity constituted six
    inspection samples, as defined in IP 71111.04.
    *    2A and 2B train of motor-driven auxiliary feedwater and Unit 2 turbine-driven
          auxiliary feedwater prior to mode change
    *    2A and 2B train of safety injection prior to mode change
    *    2A train of containment spray prior to mode change
    *    2B train of containment spray prior to mode change
    *    2A-A emergency diesel generator prior to mode change
    *    2B-B emergency diesel generator prior to mode change
b. Findings
    No findings were identified.
1R05 Fire Protection (71111.05AQ)
    Fire Protection Tours
a.  Inspection Scope
    The inspectors conducted tours of the areas important to reactor safety listed below to
    verify the licensees implementation of fire protection requirements as described in: the
    Fire Protection Program, Nuclear Power Group Standard Programs and Processes
    (NPG-SPP)-18.4.6, Control of Fire Protection Impairments; NPG-SPP-18.4.7, Control of
    Transient Combustibles; and NPG-SPP-18.4.8, Control of Ignition Sources (Hot Work).
    The inspectors evaluated, as appropriate, conditions related to: 1) licensee control of
    transient combustibles and ignition sources; 2) the material condition, operational status,
    and operational lineup of fire protection systems, equipment, and features; and 3) the
    fire barriers used to prevent fire damage or fire propagation.


ML17326A222  OFFICE RII: DRP RII: DRP RII: DRP RII: DRP RII: DRP RII: DRP NAME RTaylor BDavis GCrespo BBishop JEargle ELea DATE 10/31/2017 11/8/2017 10/31/2017 10/31/2017 11/6/2017 11/6/2017 OFFICE RII: DRP RII: DRP RII: DRP R:II DRP NCP Approver  NAME JHamman JJandovitz ABlamey JNadel MFranke  DATE 10/31/2017 11/3/2017 11/21/2017 11/7/2017 11/22/2017    
                                                6
Enclosure U.S. NUCLEAR REGULATORY COMMISSION
    This activity constituted three inspection samples, as defined in IP 71111.05AQ.
REGION II
    *  Auxiliary building elevation 713
    
    *  Auxiliary building elevation 676
Docket Nos.:   50-390, 50-391
    *  Control building elevation 729 and 741 (cable spreading room)
  b. Findings
    No findings were identified.
1R11 Licensed Operator Requalification and Performance (71111.11)
.1  Licensed Operator Requalification Review
  a. Inspection Scope
    On September 12, 2017, the inspectors observed licensed operator training
    examinations on the simulator per scenario 3-OT-SRE-1017, revision 7. The scenario
    included a feedwater line break and subsequent loss of all main and auxiliary feed
    capability. The inspectors specifically evaluated the following attributes related to the
    operating crews performance:
    *  Clarity and formality of communication
    *  Ability to take timely action to safely control the unit
    *   Prioritization, interpretation, and verification of alarms
    *  Correct use and implementation of abnormal operating instructions and emergency
        operating instructions
    *   Timely and appropriate Emergency Action Level declarations per emergency plan
        implementing procedures
    *   Control board operation and manipulation, including high-risk operator actions
    *  Command and Control provided by the unit supervisor and shift manager
    The inspectors also attended the critique to assess the effectiveness of the licensee
    evaluators, and to verify that licensee-identified issues were comparable to issues
    identified by the inspector. This activity constituted one Observation of Requalification
    Activity inspection sample, as defined in IP 71111.11.
  b. Findings
    No findings were identified


                                                7
.2  Observation of Operator Performance
License Nos.:   NPF-90, NPF-96
  a. Inspection Scope
    
    Inspectors observed and assessed licensed operator performance in the plant and main
Report No.:   05000390/2017003, 05000391/2017003
    control room, particularly during periods of heightened activity or risk and where the
    activities could affect plant safety. Inspectors reviewed various licensee policies and
    procedures such as procedures OPDP-1, Conduct of Operations; NPG-SPP-10.0, Plant
    Operations; and GO-4, Normal Power Operation. Inspectors used activities such as
    post-maintenance testing, surveillance testing and refueling, and other outage activities
    to focus on the following conduct of operations as appropriate. This activity constituted
    one Observation of Operator Performance inspection sample, as defined in IP 71111.11.
    *  Operator compliance and use of procedures
    *  Control board manipulations
    *  Communication between crew members
    *  Use and interpretation of plant instruments, indications and alarms
    *  Use of human error prevention techniques
    *   Documentation of activities, including initials and sign-offs in procedures
    *  Supervision of activities, including risk and reactivity management
    *  Pre-job briefs
   b. Findings
    No findings were identified.
1R12 Maintenance Effectiveness (71111.12)
   a. Inspection Scope
    The inspectors reviewed the performance-based problem listed below. A review was
    performed to assess the effectiveness of maintenance efforts that apply to scoped
    structures, systems, or components (SSCs) and to verify that the licensee was following
    the requirements of TI-119, Maintenance Rule Performance Indicator Monitoring,
    Trending, and Reporting - 10 CFR 50.65, and NPG-SPP-03.4, Maintenance Rule
    Performance Indicator Monitoring, Trending, and Reporting - 10 CFR 50.65. Reviews
    focused, as appropriate, on: 1) appropriate work practices; 2) identification and
    resolution of common cause failures; 3) scoping in accordance with 10 CFR 50.65;
    4) characterizing reliability issues for performance monitoring; 5) tracking unavailability
    for performance monitoring; 6) balancing reliability and unavailability; 7) trending key
    parameters for condition monitoring; 8) system classification and reclassification in
    accordance with 10 CFR 50.65(a)(1) or (a)(2); 9) appropriateness of performance criteria


   
                                                8
  LicenseeTennessee Valley Authority (TVA)  
    in accordance with 10 CFR 50.65(a)(2); and 10) appropriateness and adequacy of
    10 CFR 50.65 (a)(1) goals, monitoring and corrective actions. This activity constituted
    one Maintenance Effectiveness inspection sample, as defined in IP 71111.12.
Facility:   Watts Bar Nuclear Plant, Units 1 and 2
    *  Condition Report (CR) 1316520, Unit 2 function 063-B Train A (2A safety injection
        pump) exceeded performance criteria
b. Findings
    No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
  a.  Inspection Scope
    The inspectors evaluated, as appropriate, for the work activities listed below:
    1) the effectiveness of the risk assessments performed before maintenance activities
    were conducted; 2) the management of risk; 3) that, upon identification of an unforeseen
    situation, necessary steps were taken to plan and control the resulting emergent work
    activities; and 4) that maintenance risk assessments and emergent work problems were
    adequately identified and resolved. The inspectors verified that the licensee was
    complying with the requirements of 10 CFR 50.65 (a)(4); NPG-SPP-07.0, Work Control
    and Outage Management; NPG-SPP-07.1, On Line Work Management;
    NPG-SPP-09.11.1, Equipment Out of Service Management; and TI-124, Equipment to
    Plant Risk Matrix. This activity constituted four Maintenance Risk Assessment
    inspection samples, as defined in IP 71111.13.
    *   Risk assessment for August 11, 2017, with the 1A emergency diesel generator
        (EDG) out of service (OOS) for an extended planned maintenance outage and
        applicability of TS 3.8.1.B.5 for the extended limiting condition for operation time
        period based on FLEX EDG availability
    *  Risk assessment for August 4, 2017, with 1B-B auxiliary feedwater train OOS and
        replacement main transformer movement under dedicated offsite power lines
    *  Risk assessment for August 29, 2017, with both sources of offsite power inoperable
        due to a disqualified grid
    *   Risk assessment for work week 0905 with 1A-A motor driven auxiliary feedwater,
        1A-A component cooling system pump OOS for maintenance and high risk work on
        Unit 1 turbine electrohydraulic controls, and A main control room chiller OOS
b.  Findings
    No findings were identified.


   LocationSpring City, TN 37381
                                                9
1R15 Operability Evaluations (71111.15)
   a. Inspection Scope
    The inspectors reviewed the operability evaluations affecting risk-significant mitigating
    systems listed below, to assess, as appropriate: 1) the technical adequacy of the
    evaluations; 2) whether continued system operability was warranted; 3) whether the
    compensatory measures, if involved, were in place, would work as intended, and were
    appropriately controlled; 4) where continued operability was considered unjustified, the
    impact on TS Limiting Conditions for Operation (LCO) and the risk-significance in
    accordance with the significant determination process (SDP). The inspectors verified
    that the operability evaluations were performed in accordance with NPG-SPP-03.1,
    CAP. Additional documents reviewed are listed in the Attachment. This activity
    constituted seven Operability Evaluation inspection samples, as defined in IP 71111.15.
    *  Immediate determination of operability (IDO) for CR 1320214, momentary indication
        of Unit 2 reactor rod control bank A rod L5 fully inserted
    *  Prompt determination of operability (PDO) for CR 1320012, Unit 2 intermittent solid
        state protection system (SSPS) train B general warning alarm
    *  Past operability evaluation (POE) for CR 1303309, Unit 1 steam generator 1 and 2
        power operated relief valve nitrogen supply found isolated
    *  PDO for CR 1322853, 2B1 emergency diesel generator engine lube oil circulating
        pump shaft shear
    *  PDO for CR 1316395, ERCW system design bases and procedural errors potentially
        impacting system function
    *  POE for CR 1316395, ERCW system design bases and procedural errors potentially
        impacting system function
    *  Review of CR 1333550, emergency diesel generator 2B inoperable due to low
        crankcase oil level
   b. Findings
.1  Failure to Maintain Procedures for Response to a Loss of Coolant Accident
    Introduction. An NRC-identified Green NCV (NCV) was identified for the failure to
    maintain written procedures as required by TS 5.7.1.1.a. Emergency procedures 1-E-1,
    revision 7, and 2-E-1 revision 0, both titled Loss of Reactor or Secondary Coolant,
    contained steps that would have reduced ERCW flow to the A and B CCS HXs and
    potentially impacted the operability of the A train header of ERCW and CCS for both
    units.
    Description. During an NRC review of a licensee-identified issue regarding the CCS
    heat exchanger (HX) ERCW outlet and outlet bypass valves, the inspectors found that
    emergency procedures 1-E-1and 2-E-1 both included a step that directed opening valve
    1-FCV-67-458, CCS HX A supply from ERCW header 1B, during a loss of either A train
    or B train power. This procedural action would be implemented during a loss of coolant
    accident (LOCA) on one unit with a coincident single active failure causing a loss of train


                                          10
(A or B) power while the other unit was using the residual heat removal (RHR) system
Dates:    July 1 through September 30, 2017
for decay heat cooling. These conditions were incorporated into the design bases for
Unit 2 during plant licensing. Procedure 2-E-1 was created with the inappropriate steps
on October 8, 2015. Procedure 1-E-1 was updated with identical steps on
December 28, 2015. The licensee removed the inappropriate steps in both procedures.
The licensee evaluated the past operability of the ERCW system for the time period
where the steps were incorporated into the procedure and determined that the condition
resulted in the A train of ERCW/CCS being inoperable for Unit 2 for 11 days.
Analysis. The failure to maintain written procedures for emergencies as required by TS
5.7.1.1.a was a performance deficiency. The performance deficiency was more than
minor because it affected the Mitigating Systems Cornerstone attribute of Procedure
Quality and adversely affected the cornerstone objective in that reduced ERCW flow
caused by the inappropriate steps resulted in the Unit 2A train of ERCW/CCS being
inoperable for 11 days. This finding was assessed using NRC inspection Manual
Chapter 0609, Attachment 4, Initial Characterization of Findings. Using Appendix A,
Exhibit 2, Mitigating Systems Screening Questions, the finding was determined to
require a detailed risk evaluation because it represented an actual loss of function of at
least a single train for greater than its TS allowed outage time when the 2A train of
ERCW/CCS was inoperable for 11 days. A regional SRA performed the detailed risk
evaluation using SAPHIRE Version 8.1.6 and Version 8.50 of the SPAR Model for both
units combined. The SRA modified the fault trees for the ERCW 1B & 2A Supply
Headers to reflect the inappropriate steps for opening Valve 1-FCV-67-458 given a
power loss of either A or B train power, assumed the affected header would fail if the
valve were opened, and used an exposure time of one year. The result was less than
1E-6 for each unit which would be a finding of very low significance (Green). For Unit 1,
the dominant sequences were related to loss of offsite power where the performance
deficiency fails ERCW Header 2A leading to loss of seal cooling. For Unit 2, the
dominant sequences were similar with the performance deficiency failing ERCW Header
1B. The risk was mitigated because the performance deficiency would affect operation
only when a LOCA occurred with the simultaneous loss of two shutdown boards.
The finding had a cross-cutting aspect in the Documentation attribute of the Human
Performance area because the licensee did not maintain the accuracy of 1-E-1 through
its revisions and did not maintain procedure 2-E-1 accurate at its creation. (H.7).
Enforcement. TS 5.7.1.1.a, Procedures, required, in part, that written procedures be
established, implemented, and maintained covering activities related to procedures
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory
Guide 1.33, revision 2, Appendix A, Section 6, Procedures for Combating Emergencies
and Other Significant Events recommends procedures for loss of coolant. Contrary to
the above, since October 8, 2015, 2-E-1, revision 0, was not properly established when
a procedural step directing opening of valve 1-FCV-67-458 was included. Also, since
December 28, 2015, procedure 1-E-1, revision 7, was not maintained when the same
procedural step was added. This violation was entered in to the licensees CAP as
CR 1331422 and procedures 1-E-1 and 2-E-1 have been revised to remove this step.


  Inspectors:  J. Nadel, Senior Resident Inspector
                                            11
    J. Hamman, Resident Inspector
  This violation is being treated as an NCV consistent with Section 2.3.2 of the NRC
    J. Jandovitz, Senior Resident Inspector
  Enforcement Policy and is identified as NCV 05000390, 391/2017003-01, Failure to
    E. Lea, Regional Government Liaison Officer    S. Freeman, Senior Reactor Analyst    J. Eargle, Senior Construction Inspector B. Bishop, Project Engineer    G. Crespo, Senior Construction Inspector
  Maintain Procedures for Response to a Loss of Coolant Accident.
    C. Rapp, Senior Project Engineer
.2 Inadequate Procedure for Unit Cooldown from Hot Standby to Cold Shutdown
    R. Taylor, Senior Project Inspector    B. Davis, Senior Construction Inspector
  Introduction: An NRC-identified finding of very low safety significance (Green) and
  associated NCV of TS 5.7.1.1.a, Procedures, was identified for the failure to maintain
  TVA procedures 1-GO-6 and 2-GO-6, both entitled Unit Shutdown from Hot Standby to
Approved by:  Alan Blamey, Chief  Reactor Projects Branch 6  Division of Reactor Projects
  Cold Shutdown. The licensee failed to update the procedures based on a PDO to
 
  include steps that would shutdown the running motor driven auxiliary feedwarer pump
  SUMMARY  IR 05000390/2017-003; 05000391/2017-003; July 1, 2017 - September 30, 2017; Watts Bar Nuclear Plant; Operability Evaluations, Surveillance Testing.  
  (MDAFW) prior to starting a third ERCW pump during the period where the opposite unit
  has been shutdown less than 48 hours.
The report covered a three-month period of inspection by the resident inspectors.  Three Green
  Discussion: TVA design change notification (DCN) 62151 was issued to ensure the dual
non-cited violations (NCV) were identified. The significance of most findings is indicated by their color (i.e., Green, White, Yellow, Red)  and determined using Inspection Manual Chapter (IMC)  
  unit system alignment and flow settings for the ERCW system would support operability
0609, "Significance Determination Process," (SDP) dated April 29, 2015. Cross-cutting aspects are determined using IMC 0310, "Aspects Within Cross-Cutting Areas," dated              December 04, 2014. All violations of NRC requirements are dispositioned in accordance with
  and conform to the design bases for both units as Unit 2 transitioned from construction
the NRC's Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing
  to full commercial operation. The DCN identified procedural changes necessary to
  comply with Unit 1 license amendment 104, which added TSs 3.7.16, Component
  Cooling System - Shutdown, and 3.7.17, Essential Raw Cooling Water System -
  Shutdown, and the Unit 2 operating license. TS 3.7.16 and 3.7.17 required additional
  CCS and ERCW pumps to be operable within 48 hours of a unit shutdown. One of the
  procedure changes discussed in DCN 62151 was necessary to ensure the ERCW
  system was able to meet the limiting design bases event discussed in Unit 1 license
  amendment 104 and the Unit 2 operating license which consisted of a design bases
  LOCA on one unit coincident with a dual unit LOOP, while the other (non-accident) unit
  is on RHR shutdown cooling within 48 hours after shutdown and experiences a single
  active failure in the form of a loss of power to one train. The changes consisted of
  procedure revisions to require starting a third ERCW pump and having provisions to load
  it as the second ERCW pump on a single diesel generator (EDG) during the limiting
  design basis event. It was recognized, during the license amendment process, that the
  diesel generator loading analysis assumed the MDAFW pump was not running on the
  non-accident unit. However, the limiting design bases event assumes a dual unit LOOP
  where MDAFW pumps would be automatically loaded onto the non-accident units
  EDGs. As a result, DCN 62151 required the emergency procedures be revised to direct
  the MDAFW pumps for the non-accident unit be stopped and placed in pull to lock and
  then activate the applicable ERCW pump interlock bypass switch.
  On July 12, 2017, the licensee identified that a previously unknown and unanalyzed
  failure mode may be more limiting than the limiting design bases event. As part of this
  discovery the licensee realized the procedural changes in DCN 62151 had not been
  implemented despite Unit 2 starting commercial operation in September of 2016. As a
  result, several emergency procedures did not reflect the required ECRW valve position
  and flow requirements to properly mitigate a limiting design bases accident on Unit 2.
  The licensee completed a PDO on July 16, 2017. The PDO identified four
  compensatory actions necessary to restore operability. The four actions were all
  associated with Unit 1 and Unit 2 emergency and general operating procedure changes.


the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 6. Documents reviewed by the inspectors not identified in the Report Details are listed in the Attachment.  
                                              12
    The inspectors reviewed the PDO and determined that the need to stop a running
Cornerstone: Mitigating Systems
    MDAFW pump prior to loading an EDG with a second ERCW pump, to prevent
* Green.  An NRC-identified NCV was identified for the failure to maintain written procedures for emergencies.  Emergency procedure 1-E-1, Revision 7 and 2-E-1 Revision 0, both titled Loss of Reactor or Secondary Coolant, were updated to include steps directing inappropriate actions that would have affected emergency raw cooling water (ERCW) supply flow during an accident.  The immediate corrective action was to remove the inappropriate
    overloading of the EDG, was not recognized as a required compensatory action to
steps.  This violation was documented in the licensee's corrective action program (CAP) as
    restore operability. The licensee agreed that the procedure changes to stop the running
CR 1331422.  
    MDAFW pump were required and they revised the PDO on July 17, 2017, to include the
The performance deficiency was more than minor because it affected the Mitigating Systems Cornerstone attribute of Procedure Quality and adversely affected the cornerstone objective in that the reduced ERCW flow caused by the inappropriate steps affects the heat
    necessary procedure changes.
removal capability of the ERCW and component cooling systems (CCS) during a loss of
    Analysis: The licensees failure to maintain TVA procedures 1-GO-6, revision 8 and
coolant accident (LOCA).  The finding was det
    2-GO-6, revision 6 was a performance deficiency. The performance deficiency was
ermined to require a detailed risk evaluation because it represented an actual loss of function of at least a single train for greater than its TS allowed outage time. The result was less than 1E-6 for each unit which would be a finding of very low significance (Green).  The risk was mitigated because the performance deficiency would affect operation only when a LOCA occurred and simultaneous loss of two shutdown boards.  The finding has a cross-cutting aspect in the documentation attribute of  
    more than minor because it affected the Mitigating Systems Cornerstone attribute of
the Human Performance area because the licensee did not maintain the accuracy of 1-E-1
    Equipment Performance and affected the cornerstone objective in that failure to maintain
through its revisions and did not maintain procedure 2-E-1 accurate at its creation. (H.7)
    the procedures resulted in a condition where the EDG would have been overloaded and
(Section 1R15)
    rendered inoperable in response to a design basis event. The inspectors evaluated the
* Green.  An NRC-identified NCV of Technical Specification (TS) 5.7.1.1.a, "Procedures," was identified for the failure to maintain TVA procedures 1-GO-6 and 2-GO-6, both titled Unit Shutdown from Hot Standby to Cold Shutdown.  The licensee failed to update the
    significance of this finding using IMC 0609, Attachment 4, Appendix A, Exhibit 2, and
procedures prior to commencing dual unit operation to include steps that would shut down
    determined that this finding was of very low safety significance (Green) because the
the running motor driven auxiliary feedwater pump prior to starting a third ERCW pump during the time period where the opposite unit has been shut down less than 48 hours. The licensee's immediate corrective actions included revising both procedures to add the  
    finding did not represent an actual loss of function of a single train for greater than its TS
required steps. This violation was documented in the licensee's CAP as CR 1318176.  
    allowed outage time.
3   The performance deficiency was more than minor because it affected the Mitigating Systems Cornerstone attribute of Equipment
    The finding had a cross-cutting aspect in the Avoid Complacency component of the
  Performance and adversely affected the cornerstone objective in that failure to maintain the procedures resulted in a situation where the emergency diesel generator would have been rendered inoperable during a design basis event.  The inspectors determined the finding was of very low safety significance (Green)  
    Human Performance area as defined in NRC IMC 0310 because the organization failed
because the finding did not represent an actual loss of function of a single train for greater
    to recognize the possibility of mistakes and use appropriate error reduction tools. [H.12].
than its TS allowed outage time.  The finding had a cross-cutting aspect in the Avoid
    Enforcement: TS 5.7.1.1.a, Procedures, required, in part, that written procedures be
Complacency attribute of the Human Performance area because engineering missed a
    established, implemented, and maintained covering activities related to procedures
critical aspect of the required procedure changes associated with design change notice
    recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory
62151 when performing the prompt determination of operability and the review process was unsuccessful at identifying the error [H.12]. (Section 1R15)  
    Guide 1.33, Section 2(j), General Plant Operating Procedures, required procedures for
    Hot Standby to Cold Shutdown. Contrary to the above, from July 16, 2017 to
    July 17, 2017, the licensee failed to maintain their procedures for unit shutdown from hot
    standby to cold shutdown, 1-GO-6, revision 8 and 2-GO-6, revision 6, because they did
    not include steps to prevent an EDG overload by stopping the running MDAFW pump.
    The licensees immediate corrective actions included revising both procedures to add
    the required steps. This violation was entered into the CAP as CR 1318176 and is being
    treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy. It is
    identified as NCV 05000391, 390/2017003-02, Inadequate Procedure for Unit Cooldown
    from Hot Standby to Cold Shutdown.
1R19 Post-Maintenance Testing (71111.19)
  a.  Inspection Scope
    The inspectors reviewed the post-maintenance test procedures and/or test activities,
    (listed below) as appropriate, for selected risk-significant mitigating systems to assess
    whether: 1) the effect of testing on the plant had been adequately addressed by control
    room and/or engineering personnel; 2) testing was adequate for the maintenance
    performed; 3) acceptance criteria were clear and adequately demonstrated operational
    readiness consistent with design and licensing basis documents; 4) test instrumentation
    had current calibrations, range, and accuracy consistent with the application; 5) tests
    were performed as written with applicable prerequisites satisfied; 6) jumpers installed or


Cornerstone:  Initiating Events
                                                13
* Green. A self-revealed NCV of (TS) 5.7.1.1.a, "Procedures," was identified for the failure to follow TVA procedure 2-SI-68-86, 18 month Channel Calibration of Remote Shutdown Monitoring Narrow Range Pressurizer Pressure Loop 2-LPP-68-337C, revision 4.  The licensee failed to properly follow step 6.2.6 [1.3], which resulted in the inadvertent lifting of a
      leads lifted were properly controlled; 7) test equipment was removed following testing;
pressurizer power operated relief valve (PORV).  The licensee's immediate corrective
      and 8) equipment was returned to the status required to perform its safety function. The
actions included revising the procedure. This violation was documented in the licensee's
      inspectors verified that these activities were performed in accordance with
CAP as CR 1309345.  
      NPG-SPP-06.9, Testing Programs; NPG-SPP-06.3, Pre-/Post-Maintenance Testing; and
  The performance deficiency was more than minor because it affected the Initiating Events
      NPG-SPP-07.1, On Line Work Management. This activity constituted five Post
Cornerstone attribute of Human Performance and adversely affected the cornerstone
      Maintenance Testing inspection samples, as defined in IP 71111.19.
objective in that failing to follow procedure 2-SI-68-86 caused a depressurization of the plant
      *  WO 118921021, 2-SI-68-120, 184 day channel operational test reactor coolant flow
that had to be stopped by operator action. The finding was determined to be very low safety
          loop 3 channel III, loop 2-LPF-68-48D (F-436)
significance (Green) because the resultant leakage from the open PORV would be          self-limiting such that it would stop before impacting the operating method of decay heat removal. The finding had a cross-cutting aspect in the Challenge the Unknown component
      *  WO 118851496, 2-SI-99-10-B, 62 day functional test of SSPS train B and reactor trip
of the Human Performance area as defined in NRC IMC 0310, because the technicians
          breaker B following tester circuit board replacement
failed to recognize that the output was already set to 0, but proceeded anyway to toggle the
      *  WO 118921021, 2-SI-68-120, 184 day channel operational test reactor coolant flow
output which resulted in setting it to 1 [H.11].  (Section 1R22)  
          loop 3, channel III, loop 2-LPF-68-48D (F436) following EAGLE 21 DFP circuit board
Six violations of very low safety significance, identified by the licensee, have been reviewed by
          replacement
the NRC. Corrective actions taken or pl
      *  WO 119010949, 1-SI-30-902-A, Valve full stroke exercising during plant operation
anned by the licensee hav
          ventilation train A following replacement of quick exhaust valve on 1-FCV-30-40
e been entered into the licensee's CAP. These violations and the corrective action tracking numbers are listed in  
      *  WO 118985349, Post maintenance test following 2B2 EDG auxiliary lube oil pump
Section 4OA7 of this report.
          replacement
  REPORT DETAILS
  b. Findings
Summary of Plant Status
      No findings were identified.
  1R20 Refueling and Outage Activities (71111.20)
Unit 1 operated at 100 percent rated thermal power (RTP) for the entire reporting period.  
.1    Unit 2 Forced Outage (July 1, 2017 - August 8, 2017)
  a. Inspection Scope
      The Unit 2 began a forced outage on March 23, 2017, due to a structural failure of the B
      condenser waterbox. On July 1, 2017, the unit was in mode 5 until the unit began to heat
      up in preparation for startup. The reactor became critical on July 23, 2017, but returned
      to hot standby (Mode 3) due to equipment problems with the main feed pumps. On
      July 25, 2017, startup resumed, but the reactor was tripped before criticality due to rod
      position indication problems. Startup recommenced on July 27, 2017, but was stopped
      due to additional rod position indication problems. On July 30, 2017, Unit 2 started up
      after rod position indication repairs and achieved 29 percent rated thermal power (RTP)
      on August 2, 2017. The unit remained at 29 percent RTP until August 3, 2017, when the
      turbine was tripped due to a steam leak on a turbine drain line. The reactor stabilized at
      8 percent RTP and remained there until power ascension resumed after drain line
      repairs. Unit 2 reached 100 percent RTP on August 8, 2017, and remained there for the
      remainder of the reporting period.
      The inspectors observed the licensees mode changes and startups in order to verify that
      they were performed in accordance with station procedures and TSs. The inspectors
      made entry into containment prior to the unit restart to assess the material condition of
      SSCs, including the containment sump. The inspectors attended forced outage meetings


                                              14
Unit 2 began the reporting period shutdown for repairs to the main condenser. The unit was started up on July 23, 2017, but was shutdown to hot standby later that day due to equipment problemsOn July 25, 2017, startup resumed, but the reactor was tripped before criticality due
    and reviewed the daily risk assessments and condenser repair plans. The inspectors also
to rod position indication problems during the startup. Startup commenced again on             
    observed the performance of some surveillance testing being performed while the unit was
July 27, 2017, but was stopped due to additional rod position indication problems. Unit 2 started
    shutdown. This activity constituted one Refueling and Other Outage Activities sample, as
up after rod position indication repairs on July 30, 2017, and achieved 29 percent RTP on    August 2, 2017. The unit remained at that power until August 8, 2017, when the turbine was tripped due to a steam leak on a turbine drain line. The unit stabilized at 8 percent RTP and  
    defined in IP 71111.20.
remained there until power ascension resumed after drain line repairs.  Unit 2 reached         
b.  Findings
100 percent RTP on August 8, 2017, and remained there for the remainder of the reporting
    No findings were identified.
1R22 Surveillance Testing (71111.22)
aInspection Scope
    The inspectors witnessed the surveillance tests and/or reviewed test data of selected
    risk-significant SSCs listed below, to assess, as appropriate, whether the SSCs met the
    requirements of the TS; the UFSAR; NPG-SPP-06.9, Testing Programs;
    NPG-SPP-06.9.2, Surveillance Test Program; and NPG-SPP-09.1, ASME Section XI.
    The inspectors also determined whether the testing effectively demonstrated that the
    SSCs were operationally ready and capable of performing their intended safety
    functions. This activity constituted ten Surveillance Testing inspection samples; three
    in-service and seven routine; as defined in IP 71111.22.
    In-Service Test:
    * WO 118371917, 1-SI-62-901-A, Centrifugal charging pump 1A-A quarterly
        performance test
    * WO 118086192, 2-SI-67-908-B, Valve full stroke exercising and position indication
        verification during cold shutdown - essential raw cooling water (train 2B)
    * WO 118431243, 1-SI-74-901-A, Residual heat removal pump 1A quarterly
        performance test
    Other Surveillances
    * WO 118431170, 0-SI-82-12-A, Monthly diesel generator start and load test DG 2A-A
    * WO 118086055, 2-SI-0-710, Containment integrity: penetrations
    * WO 117823693, 2-SI-211-1-A, 18 month 6.9 KV shutdown board 2A-A automatic
        and manual transfer tests
    * WO 118061393, 2-SI-211-1-B, 18 month 6.9 KV shutdown board 2B-B Automatic
        and Manual Transfer Tests
    * WO 117823686, 2-SI-211-3-A, 18 month functional test on 6900V SD BD 2A-A
        degraded and undervoltage relays
    * WO 117823687, 2-SI-211-3-B, 18 month functional test on 6900V SD BD 2B-B
        degraded and undervoltage relays
    * WO 117823601, 2-SI-68-86, 18 month channel calibration of remote shutdown
        monitoring narrow range pressurizer pressure loop 2-LPP-68-337C


period. 1. REACTOR SAFETY
                                              15
b. Findings
  Introduction: A self-revealed finding of very low safety significance (Green) and
  associated NCV of TS (TS) 5.7.1.1.a, Procedures, was identified for the failure to follow
  TVA procedure 2-SI-68-86, 18 Month Channel Calibration of Remote Shutdown
  Monitoring Narrow Range Pressurizer Pressure Loop 2-LPP-68-337C, Revision 4. The
  licensee failed to properly follow step 6.2.6 [1.3], which resulted in the inadvertent lifting
  of a pressurizer power operated relief valve (PORV).
  Discussion: On June 21, 2017, instrumentation and control technicians were performing
  Surveillance 2-SI-68-86. The surveillance verified the function of the transfer switches
  for the PORV and its associated block valve to transfer power from the main control
  room to the auxiliary control room. Step 6.2.6 [1.3] of the procedure directed that the
  distributed control system (DCS) demand for the PORV be toggled to 0 (closed). When
  the technicians came to this step, they toggled the output as directed in the beginning of
  the procedure step. However, they did not recognize that the DCS demand was at 0
  and, therefore, toggled it to 1 (open). When the auxiliary transfer switch was operated,
  the PORV had an open signal present and opened. This resulted in a reactor coolant
  pressure drop from 335 psig to 310 psig. The main control room operators were alerted
  to this condition by an annunciator for high pressure in the pressurizer relief tank,
  properly diagnosed the inadvertent PORV opening, and shut the associated PORV block
  valve stopping the pressure decrease.
  Analysis: The licensees failure to follow TVA procedure 2-SI-68-86, was a performance
  deficiency. The performance deficiency was more than minor because it affected the
  Initiating Events Cornerstone attribute of Human Performance and adversely affected
  the cornerstone objective in that failing to follow procedure 2-SI-68-86 resulted in a
  temporary lowering of reactor coolant pressure and inventory. The finding was screened
  in accordance with NRC IMC 0609, Attachment 4, Appendix G, Shutdown Operations
  Significance determination process Phase 1 Initial Screening and Characterization of
  Findings. The finding was screened to Green based on the answers to questions 2 and
  3. The resultant leakage from the open PORV would not have caused the current decay
  heat removal method to fail if it went undetected and leakage would be self-limiting such
  that it would stop before impacting the operating method of decay heat removal.
  The finding had a cross-cutting aspect in the Challenge the Unknown component of the
  Human Performance area as defined in NRC IMC 0310, because the technicians failed
  to recognize that the output was already set to 0, but proceeded anyways to toggle the
  output which resulted in setting it to 1 [H.11].
  Enforcement: TS 5.7.1.1.a, Procedures, required, in part, that written procedures be
  established, implemented, and maintained covering activities related to procedures
  recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory
  Guide 1.33, Section 8, Procedures for Control of Measuring and Test Equipment and for
  Surveillance Tests, Procedures, and Calibrations requires procedures for surveillance
  tests. Contrary to the above, required surveillance procedure 2-SI-68-86, revision 4,
  was not implemented when step 6.2.6 [1.3] was not performed as written. Corrective
  actions taken or planned by the licensee include revisions to 2-SI-68-86 to clarify the


                                              16
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
    steps relating to toggling the DCS output, training for the craft, and management
    oversight of pre-job briefs. This violation was entered into the CAP as CR 1309345 and
    is being treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy.
    This violation is identified as NCV 05000391/2017003-03, Failure to Follow a
    Surveillance Procedure Led to an Inadvertent Lift of a Pressurizer Power Operated
    Relief Valve.
    Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation (71114.06)
  a. Inspection Scope
    On the dates listed below, the inspectors observed a licensee-evaluated emergency
    preparedness drill to verify that the emergency response organization was properly
    classifying the event in accordance with licensee procedure EPIP-1, Emergency Plan
    Classification Flowchart, and making accurate and timely notifications and protective
    action recommendations in accordance with EPIP-2, Notification of Unusual Event;
    EPIP-3, Alert; EIPIP-4, Site Area Emergency; EPIP-5, General Emergency; and the
    Radiological Emergency Plan. In addition, the inspectors verified that licensee
    evaluators were identifying deficiencies and properly dispositioning performance against
    the performance indicator criteria in Nuclear Energy Institute (NEI) 99-02, Regulatory
    Assessment Performance Indicator Guideline. This activity constituted two EP drill
    evaluation inspection samples.
    *    EP drill on July 17, 2017
    *    EP drill on August 16, 2017
  b. Findings
    No findings were identified.
4.  OTHER ACTIVITIES
4OA1 Performance Indicator (PI) Verification (71151)
.1  Cornerstone: Mitigating Systems
  a. Inspection Scope
    The inspectors sampled licensee submittals for the two PIs listed below. To verify the
    accuracy of the PI data reported from July 1, 2016 through June 30, 2017. PI definitions
    and guidance contained in NEI 99-02, Regulatory Assessment Indicator Guideline,
    Revision 7, were used to verify the basis in reporting for each data element.
    This activity constituted two performance indicator samples, as defined in IP 71151.


                                              17
1R01 Adverse Weather Protection (71111.01)  
    *  High Pressure Safety Injection MSPI
    *  RCS leak rate
External Flood Protection Inspection  
  b. Findings
a. Inspection Scope
    No findings were identified.
The inspectors reviewed the licensee's readiness to cope with external flooding. External flooding from a probable maximum precipitation (PMP) or design basis flood
4OA2 Problem Identification and Resolution (71152)
(DBF) had the potential for internal flooding of a portion of a number of the plant
.1  Review of Items Entered into the CAP
structures.  The inspectors reviewed the feasibility of the licensee's flooding mitigation
    As required by Inspection Procedure 71152, Problem Identification and Resolution, and
plans and design features and verified that they were consistent with the licensee's
    in order to help identify repetitive equipment failures or specific human performance
design requirements and the risk analysis assumptions for coping with this type of event.  The inspectors performed walkdowns of selected areas to observe grading, yard drains, and curbs in the vicinity of the south valve vault rooms. The inspectors also
    issues for follow-up, the inspectors performed a daily screening of items entered into the
checked status of the flood mode boat. The inspectors reviewed external flood
    licensees CAP. This review was accomplished by reviewing daily condition report (CR)
protection features at the intake pumping station and condition of the strainer room sump
    summary reports and attending daily CR review meetings
pumps. Additionally, the inspectors reviewed the licensee's related corrective action documents (condition reports) to ensure any non-conforming conditions related to potential flooding were properly addressed. The inspection was performed prior to the
.2  Annual Sample: Review of CR 129727, Watts Bar Elevation Letter - Operations
expected rainfall from Hurricane Irma. This activity constituted one Adverse Weather
    Leadership Formality and Rigor
Protection inspection sample, as defined in Inspection Procedure (IP) 71111.01.  
  a. Inspection Scope
    The inspectors reviewed CR 1297271, WBN Elevation Letter - Operations Leadership
    Formality and Rigor, in detail to evaluate the effectiveness of the licensees corrective
    actions intended to address operator performance concerns. The CR was written to
    address the continued lack of formality, rigor, and discipline by operators in monitoring
    and controlling the plant. The inspectors assessed whether issues were properly
    identified, documented accurately and completely, properly classified and prioritized,
    adequately considered extent of condition, generic implications, common cause, and
    previous occurrences, adequately identified root causes/apparent causes, and identified
    appropriate and timely corrective actions. The inspector reviewed processes contained in
    the licensees Conduct of Operations procedure (OPDP-1) and CAP (NPG-SPP-22.300).
    This activity constituted one sample of in-depth review as defined in IP 71152.
  b. Observations and Findings
    To address the concerns identified in CR 1297217, the licensee developed a High
    Intensity Training (HIT) program. The training was developed to refocus training
    personnel and license operators of standards, behaviors and expectations associated
    with plant operations. The inspector discussed the licensees HIT program with
    members of the licensees training staff, operations management, and licensee
    operators during a four day period. During the discussions, the inspector was able to
    obtain a clear understanding of why and how HIT was developed.
    During the four days of observing HIT activities, the inspectors observed two operating
    crews and two crews of evaluators in a training environment. The inspector also
    observed classroom training and critiques following each simulator scenario. Many of


b. Findings
                                                18
    the training activities were also observed by a member of the licensees corporate
No findings were identified.
    training staff, onsite operations management, a contract third party evaluator, and a peer
5  1R04 Equipment Alignment (71111.04)
    evaluator from another utility.
  Partial System Walkdowns
    The training sessions were found to be very intense and operational focused. The
a. Inspection Scope 
    evaluators were extremely critical of crew performance. The evaluators took every
    opportunity to identify and address concerns. Whenever a concern/issue was identified,
The inspectors conducted the equipment alignment partial walkdowns listed below to evaluate the operability of selected redundant trains or backup systems prior to unit transition into the mode of applicability for the systems. This also included that
    the scenario was stopped and the issues was discussed with the crew. Stopping the
redundant trains were returned to service properly. The inspectors reviewed the  
    scenario and holding discussions occurred numerous times throughout each scenario.
functional system descriptions, the Updated Final Safety Analysis Report (UFSAR),
    Following each discussion, the simulator was reset to the desired point and reran. The
system operating procedures, and TS to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify that critical components were properly aligned and to identify any discrepancies which could  
    discussions were very interactive. During the discussions, the evaluators constantly
affect operability of the redundant train or backup system. This activity constituted six
    focused on procedural requirement and licensee expectations. The evaluators were
inspection samples, as defined in IP 71111.04.
    often challenged/questioned by crew members. The evaluators adequately addressed
* 2A and 2B train of motor-driven auxiliary feedwater and Unit 2 turbine-driven
    each question or concern identified by the crew. The inspector also observed critiques
auxiliary feedwater prior to mode change
    following scenarios.
* 2A and 2B train of safety injection prior to mode change
    From the inspectors observation it was clear that HIT was designed to address
* 2A train of containment spray prior to mode change
    operational performance issues identified in the CR. The effectiveness of HIT can only
* 2B train of containment spray prior to mode change
    be evaluated by observing operator and plant performance over time. The inspectors
* 2A-A emergency diesel generator prior to mode change
    concluded that the training provided during HIT, if embraced, should decrease lack of
* 2B-B emergency diesel generator prior to mode change 
    formality, increase rigor, and improve discipline by operators in monitoring and
b. Findings
    controlling the plant. The HIT would also be expected to improve operators
No findings were identified.
    implementation of standards outlined in OPDP-1, Conduct of Operations. The
    inspectors will continue to monitor operator and plant performance in the control room,
    during actual plant events and in licensed operator simulator training, as required by the
    baseline inspection program. No findings were identified.
.3  Semiannual Trend Review
  a. Inspection Scope
    The inspectors performed a review of the licensees CAP and associated documents to
    identify trends that could indicate the existence of a more significant safety issue. The
    review was focused on trends in risk management, long-standing minor equipment
    deficiencies, housekeeping, TS compliance, corrective action screening and condition
    adverse to quality documentation.
  b. Observations and Findings
    No findings were identified. The inspectors had several observations regarding the
    trends listed above. Regarding risk management, the inspectors noted that the
    environmental factor for the equipment out of service computer program (EOOS) was
    not consistently adjusted per procedure to reflect activities in the plant switchyard. This
    was initially identified to the licensee in 2016. The condition report written at that time
    documented the issue as an NRC question, rather than a failure to follow the EOOS
    procedure, and the corrective action was to respond to the NRC to ensure that their
    question was answered, rather than address procedure non-compliance. The inspectors
    re-visited this with the licensee when they observed switchyard work in progress without


1R05 Fire Protection (71111.05AQ)
                                                19
  Fire Protection Tours
    the environmental factor setting in EOOS being per procedure. This time the licensee
  a. Inspection Scope
    properly characterized the issue as procedure non-compliance in their CAP. The
    inspectors used the EOOS test module and verified that risk remained GREEN during
The inspectors conducted tours of the areas important to reactor safety listed below to  
    instances when the environmental factor adjustment was not properly set. The
    inspectors noted that, for the work performed when the environmental factor was not
    properly set, the licensee did implement physical risk mitigation controls at the work sites
    that were in accordance with the appropriate work management procedures.
    The inspectors also noted a trend in long-standing equipment issues eventually
    becoming either operator distractions or worse conditions. In one instance valve leakby
    in the chemical volume and control system gave erroneous indication that the reactor
    coolant system was either being borated or diluted. This required the operating crew to
    enter procedures to then verify that the RCS truly was neither borated nor diluted. In
    another instance, known leakage on the 1A high pressure fire pump shaft seal worsened
    to the point that protective measures had to be taken to shield water spray from the
    power supply conduit of the pump.
    Since the completion of Unit 2 construction, the inspectors noted a reduction in the
    amount of temporary equipment stored in the plant auxiliary building and general
    housekeeping improvements in the auxiliary building. CAP review during the first and
    second quarter of 2017 showed a more aggressive approach by the license in improving
    housekeeping and removing lingering temporary equipment. Documents reviewed show
    that the licensee accomplished this through frequent health and safety walkdowns and
    challenging temporary equipment tags that were out of date. The inspectors observed
    the results of these efforts in their routine walkdowns of risk-significant areas.
    Specifically, in regards to a large scaffold storage area near the Unit 2 713 level
    penetration. Although temporary equipment tags were present and up to date, the area
    appeared to have become a convenient location to temporarily store a wide variety of
    items beyond scaffolding. The licensee identified this in their CAP and then completely
    removed all of the items stored in the area.
    The inspectors also identified negative trends in the treatment of C-level CRs in the CAP
    and with TS compliance issues. Inspectors identified multiple C-level CRs during the
    inspection period that exhibited one of the following issues: inadequate documented
    condition details; inadequate screening of conditions adverse to quality (CAQs) to
    non-CAQ status; and failure to promptly identify CAQs. Inspectors also noted several
    examples of issues with TS compliance and proper TS application during the inspection
    period. The licensee has identified these issues in their CAP.
4OA3 Event Followup (71153)
.1  (Closed) Licensee Event Report (LER) 05000390, 391/2016-010-00, Emergency Diesel
    Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a
    Tornado
    A condition involving the potential impact of a tornado on the EDGs was identified during
    an NRC Component Design Basis lnspection at the Sequoyah Nuclear Plant. The EDGs
    were designed with a crankcase pressure trip setpoint of approximately one inch of
    water which is bypassed during an emergency start. A tornado could potentially induce


verify the licensee's implementation of fire protection requirements as described in: the Fire Protection Program, Nuclear Power Group Standard Programs and Processes
                                                20
(NPG-SPP)-18.4.6, Control of Fire Protection Impairments; NPG-SPP-18.4.7, Control of Transient Combustibles; and NPG-SPP-18.4.8, Control of Ignition Sources (Hot Work). The inspectors evaluated, as appropriate, conditions related to:  1) licensee control of transient combustibles and ignition sources; 2) the material condition, operational status,  
    a pressure spike which could cause actuation of the crankcase pressure trip due to
and operational lineup of fire protection sy
    different vent paths between the EDG room and the EDG crankcase. Actuation of the
stems, equipment, and features; and 3) the fire barriers used to prevent fire damage or fire propagation.  
    crankcase pressure trip would energize the shutdown relay causing an EDG lockout
    condition. The EDG lockout condition would prevent all EDG starts until operators
    manually reset the lockout condition. Because the EDGs at Watts Bar were essentially
    identical designs, this condition was reviewed for applicability to Watts Bar. The
    licensee determined this condition placed both units in an unanalyzed condition that
    could have potentially affected all four EDGs simultaneously. This was a legacy EDG
    protective logic circuitry design that did not anticipate the interaction between the
    crankcase pressure trip and the outside atmospheric pressure spike during a tornado.
    This condition was documented in the licensee CAP as CR 1179264. A compensatory
    action was established of starting the EDGs in the emergency mode when notified of a
    Tornado Warning and ran while the Tornado Warning was in effect ensuring the EDGs
    would be available to perform their required safety function. The licensee also
    implemented DCN 66376 to remove the sealin function of the crankcase differential
    pressure switches and retain the alarm function of the switches for all four EDGs. This
    LER was reviewed by the inspectors. A licensee-identified violation is documented in
    Section 4OA7.
.2  (Closed) LER 05000390/2016-001-00, Channel Mode Switch in Incorrect Position
    Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable.
  a. Inspection Scope
    On January 12, 2016, at 1645 Eastern Standard Time (EST), Watts Bar Nuclear Plant
    (WBN) Maintenance personnel were performing a 92 day channel operational test for
    radiation monitor 1-RM-90-1064, Lower Containment Atmosphere Particulate Radiation
    Monitor, and found the mode switch in the "DlFF" position, which was not expected. The
    surveillance was stopped and an investigation was conducted. It was determined that
    the design required the mode switch to be in the "lNT" position to be operable. The
    mode selector switch was placed in the "lNT" position and the surveillance was
    completed. The radiation monitor was restored to OPERABLE status at 1743 EST on
    January 12, 2016. Placing the mode selector switch in the "DlFF" position resulted in 1-
    RM-90-1064 being INOPERABLE due to the loss of alarm function of the monitor.
    Investigation determined that the switch had been repositioned on December 8, 2015.
    Because the containment particulate radiation monitor was inoperable for a period of
    time greater than permitted by TS 3.4.15, this condition was reportable as an operation
    or condition prohibited by TS per 10 CFR 50.73(a)(2)(i)(B). During the time the monitor
    was inoperable, other means of leak detection (e.g., containment pocket sump level
    indication, reactor coolant system inventory balance) remained available. This LER was
    reviewed by the inspectors. No additional findings or violations of NRC requirements
    were identified.
.3  (Closed) LER 05000390/2016-005-00, Both Trains of Unit 1 Emergency Gas Treatment
    System Inoperable During Unit 2 Testing


   
                                                  21
6  This activity constituted three inspection samples, as defined in IP 71111.05AQ.
    On March 14, 2016, Watts Bar Nuclear Plant (WBN) Unit 1 determined through
* Auxiliary building elevation 713'
    engineering analysis that both trains of emergency gas treatment system (EGTS) were
* Auxiliary building elevation 676'
    inoperable for 8 minutes, 10 seconds during preoperational testing of Unit 2 EGTS. The
* Control building elevation 729' and 741' (cable spreading room)
    inoperability of A and B trains of Unit 1 EGTS took place on October 22, 2015, while
b. Findings
    Unit 1 was in Mode 1 and two trains of EGTS were required to be operable in
 
    accordance with TS LCO 3.6.9, "Emergency Gas Treatment System (EGTS). At the
No findings were identified.  
    time of the event, Unit 2 was in "no mode," prior to initial fuel loading. With both trains of
    EGTS inoperable, the specified safety functions of Unit 1 EGTS were not capable of
    being performed. Therefore, this condition was reported pursuant to
    10 CFR 50.73(a)(2)(v)(C) and 10 CFR 50.73(a)(2)(v)(D), "Event or Condition That Could
    Have Prevented Fulfilment of a Safety Function." This LER was reviewed by the
    inspectors. No additional findings or violations of NRC requirements were identified.
.4   (Closed) LER 05000390/2016-004-00, Automatic Reactor Trip Due to Actuation of Over
    Temperature Delta Temperature Bistables
    On March 22, 2016, at 1131, Watts Bar Nuclear Plant Unit 1 experienced an automatic
    reactor trip. The initiating reactor trip first out received was 76-C Over-temperature Delta
    T. The turbine trip first out received was 73-C Rx Trip Breakers RTA and BYA Open.
    Prior to the unit trip, Unit 1 was in Mode 1 at 100 percent power. Concurrent with the
    reactor trip, the auxiliary feedwater system actuated. All control rods inserted upon the
    reactor trip and safety systems functioned as expected. This LER was reviewed by the
    inspectors. No additional findings or violations of NRC requirements were identified.
  .5 (Closed) LER 05000390/2016-006-00, Undersized Room Cooler Fan Shaft Results in
    Loss of Centrifugal Charging Pump
    On May 13, 2016, Watts Bar Unit 1 determined that a condition prohibited by TSs had
    previously occurred. During the Fall 2015 outage, maintenance performed on the 1B-B
    centrifugal charging pump (CCP) room cooling fan introduced a condition that resulted in
    a subsequent bearing failure of the room cooling fan. This condition would have
    prevented the 1B-B CCP pump from performing its function for its designed mission
    time. Based on the reduced reliability of the fan, the 1B-B CCP was considered to be
    inoperable from October 7, 2015, until the fan was repaired and returned to service on
    December 6, 2015. During this time, there were several short periods when the 1A-A
    CCP was also inoperable. A NCV for this condition was documented in NRC Inspection
    Report 05000390, 391/2016002-02. The LER was reviewed by the inspectors. No
    additional findings or violations of NRC requirements were identified.
.6  (Closed) LER 05000390/2016-011-00, Loss of Centrifugal Charging Pump Due to
    Repeat Failure of Associated Room Cooler
    On August 3, 2016, Wafts Bar Nuclear Plant Unit 1 (WBN1) determined that a condition
    prohibited by TS had previously occurred. During maintenance of the 1B-B CCP room
    cooler, the bearing was found in a degraded condition requiring repair. This fan was
    required to support Operability of the 1B-B CCP. The fan had been previously repaired
    on December 6, 2015, and had less than 100 days of operation since its overhaul. The


                                                22
1R11 Licensed Operator Requalification and Performance (71111.11)
      mission time of the CCPs is specified in design documents as 100 days. Based on the
  .1  Licensed Operator Requalification Review
      inability of the CCP to meet its mission time, the 1B-B CCP was considered to be design
a. Inspection Scope  
      inoperable since its overhaul on December 6, 2015. This represents a condition
On September 12, 2017, the inspectors observed licensed operator training
      prohibited by TS for the 1B-B CCP being inoperable for greater than its allowed outage
examinations on the simulator per scenario 3-OT-SRE-1017, revision 7. The scenario included a feedwater line break and subsequent loss of all main and auxiliary feed capability. The inspectors specifically evaluated the following attributes related to the  
      time. The LER was reviewed by the inspectors. No findings or violations of NRC
operating crews' performance:
      requirements were identified.
* Clarity and formality of communication
4OA5
* Ability to take timely action to safely control the unit
  .1  IP 93100 Safety-Conscious Work Environment Issue of Concern Follow Up
* Prioritization, interpretation, and verification of alarms
  a. Inspection Scope
* Correct use and implementation of abnormal operating instructions and emergency operating instructions 
      The inspectors assessed the TVA Nuclear corporate safety-conscious work
* Timely and appropriate Emergency Action Level declarations per emergency plan implementing procedures 
      environment (SCWE) by conducting safety culture interviews of individuals from the
* Control board operation and manipulation, including high-risk operator actions
      engineering, licensing, and operations groups. Inspectors interviewed a total of 22
* Command and Control provided by the unit supervisor and shift manager
      individuals to determine if indications of a chilled work environment exist, employees are
The inspectors also attended the critique to assess the effectiveness of the licensee  
      reluctant to raise safety and regulatory issues, and employees are being discouraged
evaluators, and to verify that licensee-identified issues were comparable to issues
      from raising safety or regulatory issues. Information gathered during the interviews was
identified by the inspector. This activity constituted one Observation of Requalification
      used in aggregate to assess the work environment at TVA Nuclear corporate.
Activity inspection sample, as defined in IP 71111.11.  
  b. Assessment
b. Findings
      Based on the interviews conducted, the inspectors determined that licensee
No findings were identified
      management emphasized the need for all employees to identify and report problems
      using the appropriate methods established within the administrative programs, including
      the CAP and Employee Concerns Program. These methods were readily accessible to
      all employees. Based on discussions conducted with a sample of employees from
      various departments, the inspectors determined that employees felt free to raise safety
      and regulatory issues, and that management encouraged employees to place issues into
      the CAP for resolution. The inspectors did not identify any reluctance on the part of the
      licensee staff to report safety concerns.
4OA6 Meetings, including Exit
      On October 25, 2017 and November 8, 2017, the resident inspectors presented the
      inspection results to members of the licensee staff. The inspectors confirmed that none
      of the potential report input discussed was considered proprietary.
4OA7 Licensee-Identified Violations
      The following licensee-identified violations of NRC requirements were determined to be
      of very low safety significance and met the NRC Enforcement Policy criteria for being
      dispositioned as NCVs.
      *    Technical Specification 5.7.1.1.a, Procedures, required, in part, that written
          procedures be established, implemented, and maintained covering activities
          related to procedures recommended in Regulatory Guide 1.33, Revision 2,
          Appendix A, 1978. Regulatory Guide 1.33, Revision 2, Appendix A, Section 6,


                                        23
 
  Procedures for Combating Emergencies and Other Significant Events requires
  procedures for a reactor trip. Contrary to the above, from May 23, 2016, until
 
  July 16, 2017, procedure 2-E-0, Revision 5, Reactor Trip and Safety Injection, was
7   .2 Observation of Operator Performance
  not maintained which resulted in a condition where CCS Heat Exchanger B
a. Inspection Scope
  (ERCW/CCS Train 2A) would not have been able to remove sufficient heat during
  sump recirculation following a LOCA on Unit 2 for approximately 75 days. This
Inspectors observed and assessed licensed operator performance in the plant and main
  condition was caused by the licensees failure to implement ERCW system
control room, particularly during periods of heightened activity or risk and where the  
  DCN 62151 as written. A detailed risk evaluation was performed using SAPHIRE
activities could affect plant safety. Inspectors reviewed various licensee policies and procedures such as procedures OPDP-1, Conduct of Operations; NPG-SPP-10.0, Plant Operations; and GO-4, Normal Power Operation.  Inspectors used activities such as  
   Version 8.1.5 and Version 8.50 of the SPAR Model for both units combined. The
post-maintenance testing, surveillance testing and refueling, and other outage activities
  result was less that 1E-6/year for Unit 2, which would be a finding of very low
to focus on the following conduct of operations as appropriate. This activity constituted
  significance (Green). This violation was entered in to the licensees CAP as
one Observation of Operator Performance inspection sample, as defined in IP 71111.11.  
  CR 1316395.
* Operator compliance and use of procedures
* Technical Specification 5.7.1.1.a stated, in part, that written procedures shall be
* Control board manipulations
  established, implemented, and maintained covering the applicable procedures in
* Communication between crew members
  Regulatory Guide 1.33 Rev. 2, Appendix A, February 1978. Procedures for locking
* Use and interpretation of plant instruments, indications and alarms
  and tagging are applicable procedures under REG GUIDE 1.33 Appendix A, 1.c
* Use of human error prevention techniques
  Equipment Control. Contrary to this requirement, Step 3.2.4.M of procedure
* Documentation of activities, including initials and sign-offs in procedures
  NPG-SPP-10.2, Clearance Procedure to Safely Control Energy, Revision 18 was
* Supervision of activities, including risk and reactivity management
  not followed when nitrogen supply isolation valves 2-ISIV-1-408L and
* Pre-job briefs
  2-ISIV-1-408M and isolation valves 2-ISIV-1-405L and 2-ISIV-1-405M were closed
b. Findings
  and tagged but not documented as tagged in the Electronic Shift Operations
No findings were identified.
  Management System (eSOMS). As a result, the valves remained closed resulting
  in the inability to operate the Unit 2 SG#1 and #2 PORVs using back-up nitrogen.
  The finding was determined to be Green because having the nitrogen supply to
  two out of four steam generator PORVs isolated only affects the ability to achieve
  and maintain cold shutdown. The licensee documented this violation as
  CR 1303309.
* Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, required, in part, a
  testing program to demonstrate that quality related SSCs will perform satisfactorily
  in service and performed in accordance with written test procedures. Contrary to
  the above, from at least 2010 until July 2017, various safety-related valves were
  unacceptably preconditioned prior to required as-found testing. This finding was of
  very low safety significance (Green) because the finding did not represent an
  actual loss of function of a single train for greater than its TS allowed outage time.
  The licensee documented this violation as CRs 1276605, 1316712, 1319298,
  1319304.
* 10 CFR Part 50, Appendix B, Criterion III, Design Control, stated, in part, that,
  measures shall be established for the selection and review for suitability of
  application of materials, parts, equipment, and processes that are essential to the
  safety-related functions of SSCs. Contrary to the above, for at least the past
  twenty years, the licensee failed to assess the effects of a tornado on the
  crankcase over-pressure trip which could prevent EDGs from fulfilling their
  safety-related function. A regional senior reactor analyst performed a detailed risk
  evaluation and determined the dominant accident sequences involved a
  weather-related loss of offsite power with all four EDGs failing due to the


1R12 Maintenance Effectiveness (71111.12)
                                        24
a. Inspection Scope
  performance deficiency and the operators recovering one of the failed EDGs. The
The inspectors reviewed the performance-based problem listed below.  A review was  
  risk of this performance deficiency was not greater than Green due to the low
performed to assess the effectiveness of maintenance efforts that apply to scoped
  frequency of tornados/high winds and the potential for operator recovery. The
structures, systems, or components (SSCs) and to verify that the licensee was following the requirements of TI-119, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting - 10 CFR 50.65, and NPG-SPP-03.4, Maintenance Rule
  licensee documented this violation as CR 117926.
Performance Indicator Monitoring, Trending, and Reporting - 10 CFR 50.65.  Reviews
* Technical Specification LCO 3.6.3, Containment Isolation Valves, required that each
focused, as appropriate, on:  1) appropriate work practices; 2) identification and
  containment isolation valve shall be operable in modes 1, 2, 3, and 4. TS Required
resolution of common cause failures; 3) scoping in accordance with 10 CFR 50.65;  4) characterizing reliability issues for performance monitoring; 5) tracking unavailability for performance monitoring; 6) balancing reliability and unavailability; 7) trending key
  Action statement A.1 required that the affected penetration flow path be isolated,
parameters for condition monitoring; 8) system classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2); 9) appropriateness of performance criteria 
  and Required Action A.2, directed that the penetration flow path is verified to be
  isolated once per 31 days. Contrary to the above, on May 18, 2017, containment
  isolation valve 1-FCV-31-330 was tagged closed for maintenance; however no
  verification that the flow path was isolated was performed until August 23, 2017.
  This finding was of very low safety-significance (Green) because it did not represent
  an actual open pathway in the physical integrity of reactor containment and was not
  related to hydrogen ignitors. The licensee documented this violation as
  CR 1331287.
* Unit 1 Operating License condition 2.F required, in part, that TVA shall implement
  and maintain in effect all provisions of the approved Fire Protection Program. The
  Fire Protection Report was developed to ensure compliance with the requirements of
  this licensee condition. Fire Protection Report, Part II, is the Fire Protection Plan
  (FPP). FPP Subsection 14.10, Fire Safe Shutdown Equipment, required
  nonfunctional equipment listed in Table 14.10 be restored to its functional status
  within 30 days. If this 30 day requirement cannot be met, then the equipment be
  placed in its fire safe shutdown (FSSD) position. Contrary to the above, during a
  surveillance on June 10, 2017, backdraft damper 0-BKD-31-592, equipment listed in
  Table 14.10, was identified as not being able to achieve its FSSD position. However,
  actions to place the damper in its FSSD position were not taken until July 11, 2017.
  This finding was of very low safety significance because there was a fully functional
  automatic suppression system on either side of the fire barrier. This violation was
  documented as CR 1316058.


                              SUPPLEMENTARY INFORMATION
 
                                KEY POINTS OF CONTACT
8  in accordance with 10 CFR 50.65(a)(2); and 10) appropriateness and adequacy of      10 CFR 50.65 (a)(1) goals, monitoring and corrective actions. This activity constituted one Maintenance Effectiveness inspection sample, as defined in IP 71111.12.  
Licensee Personnel
G. Arent, Director, WBN Site Licensing
M. Casner, Director, Engineering
L. Cross, Manager, Electrical Systems
T. Detchemendy, Manager, Site Emergency Preparedness
E. Ellis, Senior Manager, Nuclear Site Security
D. Erb, Operations Director
K. Hulvey, Watts Bar Licensing Manager
J. James, Director, Maintenance
B. Jenkins, Director, Plant Support
T. Marshall, Plant Manager
C. Rice, Operations Superintendent
P. Simmons, Site Vice President
A. White, Senior Manager, Site Quality Assurance
                                                        Attachment


* Condition Report (CR) 1316520, Unit 2 function 063-B Train A (2A safety injection pump) exceeded performance criteria
                              LIST OF REPORT ITEMS
b. Findings
Opened and Closed
  No findings were identified.  
NCV 05000390, 391/2017003-01          Failure to Maintain Procedures for Response to a
                                      Loss of Coolant Accident (Section 1R15.1)
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
NCV 05000391, 390/2017003-02          Inadequate Procedure for Unit Cooldown from Hot
a. Inspection Scope
                                      Standby to Cold Shutdown (Section 1R15.2)
The inspectors evaluated, as appropriate, for the work activities listed below: 
NCV 05000391/2017003-03              Failure to Follow a Surveillance Procedure Led to
                                      an Inadvertent Lift of a Pressurizer Power Operated
                                      Relief Valve (Section 1R22)
Closed
LER 05000390, 391/2016-010-00        Emergency Diesel Generator Crankcase Pressure
                                      Switches Not Analyzed to Withstand the Effects of
                                      a Tornado (Section 4OA3.1)
LER 05000390/2016-001-00              Channel Mode Switch in Incorrect Position Renders
                                      Lower Containment Atmosphere Particulate
                                      Radiation Monitor Inoperable (Section 4OA3.2)
LER 05000390/2016-005-00              Both Trains of Unit 1 Emergency Gas Treatment
                                      System inoperable During Unit 2 Testing (Section
                                      4OA3.3)
LER 05000390/2016-004-00              Automatic Reactor Trip Due to Actuation of Over
                                      Temperature Delta Temperature Bistables (Section
                                      4OA3.4)
LER 05000390/2016-006-00              Undersized Room Cooler Fan Shaft Results in Loss
                                      of Centrifugal Charging Pump (Section 4OA3.5)
LER 05000390/2016-011-00              Loss of Centrifugal Charging Pump Due to
                                      Repeat Failure of Associated Room Cooler
                                      (Section 4OA3.6)


1) the effectiveness of the risk assessm
                              LIST OF DOCUMENTS REVIEWED
ents performed before maintenance activities were conducted; 2) the management of risk; 3) that, upon identification of an unforeseen
Section 1R01: Adverse Weather Protection
situation, necessary steps were taken to plan and control the resulting emergent work activities; and 4) that maintenance risk assessments and emergent work problems were adequately identified and resolved. The inspectors verified that the licensee was
0-MI-17.003, Flood Mode Preparation Storage Locations and Periodic Inventory, Rev. 0012
complying with the requirements of 10 CFR 50.65 (a)(4); NPG-SPP-07.0, Work Control
0-TI-444, External Flood Protection Program, Rev. 0003
and Outage Management; NPG-SPP-07.1, On Line Work Management;                 
Section 1R04: Equipment Alignment
NPG-SPP-09.11.1, Equipment Out of Service Management; and TI-124, Equipment to
Procedures
Plant Risk Matrix. This activity constituted four Maintenance Risk Assessment inspection samples, as defined in IP 71111.13.  
2-SI-63-8, ECCS Valve Alignment Verification, Rev. 0002
* Risk assessment for August 11, 2017, with the 1A emergency diesel generator (EDG) out of service (OOS) for an extended planned maintenance outage and applicability of  TS 3.8.1.B.5 for the extended limiting condition for operation time
2-SI-3-130, AFW Valve Alignment Verification, Rev. 0004
period based on FLEX EDG availability
2-SOI-63.01 ATT 1V, Safety Injection System, Rev. 0005
* Risk assessment for August 4, 2017, with 1B-B auxiliary feedwater train OOS and replacement main transformer movement under dedicated offsite power lines
2-SI-70-1, Component Cooling System, Safety-Related Valves: Alignment Verification, Rev.
* Risk assessment for August 29, 2017, with both sources of offsite power inoperable
    0004
due to a disqualified grid
2-SOI-72.01, Containment Spray System, Rev. 0005
* Risk assessment for work week 0905 with 1A-A motor driven auxiliary feedwater, 1A-A component cooling system pump
2-SOI-72.01 Containment Spray System Valve Checklist 2-71.01V, ATT 1V, Rev. 0001
OOS for maintenance and high risk work on Unit 1 turbine electrohydraulic controls, and A main control room chiller OOS
0-SOI-82.03, Diesel Generator (DG) 2A-A, Rev. 0012
b. Findings
0-SOI-82.03, Diesel Generator 2A-A Power Checklist 82.03-1P, ATT 1P, Rev. 0000
No findings were identified.  
0-SOI-82.03, Diesel Generator 2A-A Valve Checklist 82.03-1V, ATT 1V, Rev. 0010
0-SOI-67.01, Essential Raw Cooling Water System Supply Header 1A Valve Alignment
    Checklist 0-67.01-3V, ATT 3V, Rev. 0017
0-PI-OPS-17.0, 18 Month Locked Valve Verification, Rev. 0082
0-TI-31.08, Flow Balancing Valves Setpoint Positions, Rev. 0003
0-SOI-82.04, Diesel Generator (DG) 2B-B, Rev. 0010
0-SOI-82.04. Diesel Generator 2B-B Power Checklist 82.04-1P, ATT 1P, Rev. 0000
0-SOI-82.04, Diesel Generator 2B-B Valve Checklist 82.04-1V, ATT 1V, Rev. 0010
0-SOI-67.01, Essential Raw Cooling Water System Supply Header 1B Valve Alignment
    Checklist 0-67.01-4V, ATT 4V, Rev. 0017
Section 1R05: Fire Protection
CRs 1262925, 1343002
Fire Protection Report, Part VI - Fire Hazards Analysis, Rev. 52
WBN-Prefire Plan, AUX-0-692-01, Rev. 4
WBN-Prefire Plan, AUX-0-692-02, Rev. 3
Drawing 47A472-1
Drawing 47W866-11
Drawing 47W920-2
Drawing 47A381-20
Drawing 47A381-127
WBN Prefire Plan AUX-0-713-01, Rev. 1
WBN Prefire Plan AUX-0-713-02, Rev. 3
WBN Prefire Plan AUX-0-713-03, Rev. 4
WBN Prefire Plan CON-0-729-01, Rev. 2
WBN Prefire Plan AUX-0-676-01, Rev. 3


 
                                          4
 
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
9   1R15 Operability Evaluations (71111.15)
0-TI-12.16, Diesel Generator Outage T/S or SR Contingency Actions, Rev. 0005
a. Inspection Scope
    WO 118934650
The inspectors reviewed the operability evaluations affecting risk-significant mitigating
0-SI-82-2, 8 Hour Diesel Generator AC Power Source Operability Verification, Rev. 0025
systems listed below, to assess, as appropriate:  1) the technical adequacy of the
    WO 118928550
evaluations; 2) whether continued system operability was warranted; 3) whether the compensatory measures, if involved, were in place, would work as intended, and were appropriately controlled; 4) where continued operability was considered unjustified, the
CRs 1727208, 1327472
impact on TS Limiting Conditions for Operation (LCO) and the risk-significance in
NPG-SPP-09.11.1, Equipment Out of Service Management, Rev. 0012
accordance with the significant determination process (SDP). The inspectors verified
NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 0021
that the operability evaluations were performed in accordance with NPG-SPP-03.1, CAP. Additional documents reviewed are listed in the Attachment.  This activity constituted seven Operability Evaluation inspection samples, as defined in IP 71111.15.  
PWR operational risk review - red sheet for WO 118819797, Hose replacement on Unit 1 main
    turbine electro-hydraulic control
High risk management plan for WO 119013421, Freeze seal for isolation of valve, dated 9/7/17
Section 1R15: Operability Determinations and Functionality Assessments
WOs 118882781, 113861046, 113860919, 118991891
WBN-SDD-N3-85-4003, Control Rod Drive System, Rev. 15
WBN-SDD-N3-99-4003, Reactor Protection System, Rev. 24
Drawings 1082H70-6, Rev. N; 1082H70, Rev. AK; 1082H70-17, Rev. AF
Operational Decision-Making Issue Evaluation Document, dated July 22, 2017
    Drawing 2-47W880-4, Rev. 0
0-PI-OPS-17.0, 18 Month Locked Valve Verification, Rev. 0081
N3-67-4002, Essential Raw Cooling Water System
1-E-1, Loss of Reactor or Secondary Coolant, Rev. 0009
WBN-SDD-N3-67-4002, Essential Raw Cooling Water System, System 67, Rev. 0035
0-TI-31.08, Flow Balancing Valves Setpoint Positions, Rev. 0003
0-TI-12.11, Emergency Operating Instruction (EOI) Control, Rev. 0001
TI-78, Lubrication Program, Rev. 0011
NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 0009
WB-DC-40-64, Design Basis Events Design Criteria
Westinghouse STS, B 3.8.3, Diesel Fuel Oil, Lube Oil, and Starting Air, Rev. 4.0
0-SOI-82.01, Diesel Generator (DG) 1A-A, Rev. 0009
WBN-VTD-P318-0020, Instructions for EMD Lubricating Oil System
Section 1R19: Post Maintenance Testing
CR 1325844
2-SI-68-114, 184 Day Channel Operational Test RCS Flow Loop 1 Channel III Loop 2-LPF-68-
    6D (F-416), Rev. 0003
WO 118921021
2-IMI-99.100, EAGLE 21 Rack Diagnostics, Rev. 0002
WO 117829913
1-SI-30-901-A, Valve Full Stroke Exercising During Plant Operation - Ventilation (Train A), Rev.
    0017
PM 600124762
Drawing 1-47W866-1, Rev. 68


* Immediate determination of operability (IDO) for CR 1320214, momentary indication of Unit 2 reactor rod control bank A rod L5 fully inserted
                                            5
* Prompt determination of operability (PDO) for CR 1320012, Unit 2 intermittent solid state protection system (SSPS) train B general warning alarm
Section 1R22: Surveillance Testing
* Past operability evaluation (POE) for CR 1303309, Unit 1 steam generator 1 and 2 power operated relief valve nitrogen supply found isolated
WOs 118628055, 116153069
* PDO for CR 1322853, 2B1 emergency diesel generator engine lube oil circulating
CRs 1322136, 1276914, 1314124, 1314688, 1309892, 1309602, 1309207
pump shaft shear 
0-SOI-82.03, Diesel Generator (DG) 2A-A, Rev. 0010
* PDO for CR 1316395, ERCW system design bases and procedural errors potentially impacting system function
2-SI-67-908-B, Valve Full Stroke Exercising and Position Indication Verification During Cold SD
* POE for CR 1316395, ERCW system design bases and procedural errors potentially impacting system function
  - ERCW (Train 2B), Rev. 0003
* Review of CR 1333550, emergency diesel generator 2B inoperable due to low crankcase oil level
2-SI-67-908-B, Valve Full Stroke Exercising and Position Indication Verification During Cold SD
b. Findings
  - ERCW (Train 2B), Rev. 0004
2-SI-67-908-B, Valve Full Stroke Exercising and Position Indication Verification During Cold SD
.1 Failure to Maintain Procedures for Response to a Loss of Coolant Accident
  - ERCW (Train 2B), Rev. 0005
1EP6: EP Drill Evaluation
Introduction.  An NRC-identified Green NCV (NCV) was identified for the failure to maintain written procedures as required by TS 5.7.1.1.a.  Emergency procedures 1-E-1, revision 7, and 2-E-1 revision 0, both titled Loss of Reactor or Secondary Coolant, contained steps that would have reduced ERCW flow to the A and B CCS HXs and
Controllers package for July 17, 2017, training drill dated 7/17/17
potentially impacted the operability of the A train header of ERCW and CCS for both
CRs 1319059, 1318956, 1318824, 1318834, 1319057, 1318822, 1318830, and 1318823
 
Section 4OA3: Followup of Events and Notices of Enforcement Discretion
units.
Documentation of Information Sharing - Title: Radiation Meter 1-RM-90-106A
Design Change Notice #66212, Rev. A for Equipment: Various/System 65 (Emergency Gas
Description.  During an NRC review of a lic
Treatment System) to revise SDD N3-65-4001 to Incorporate Test Requirements,
ensee-identified issue regarding the CCS heat exchanger (HX) ERCW outlet and outlet bypass valves, the inspectors found that emergency procedures 1-E-1and 2-E-1 both included a step that directed opening valve
  dated: 2/11/2016
1-FCV-67-458, CCS HX A supply from ERCW header 1B, during a loss of either A train
CR 11430756 Level 2 Evaluation Action 007 dated: 07/15/2016
or B train power.  This procedural action would be implemented during a loss of coolant
Past Operability Evaluation Documentation for CR 1143076 signed on 3/10/2016.
accident (LOCA) on one unit with a coincident single active failure causing a loss of train 
Routine WO 117688915, Equipment Description: EH Fluid Display Subpanel, Unit 1 Reactor
10  (A or B) power while the other unit was using the residual heat removal (RHR) system for decay heat cooling.  These conditions were incorporated into the design bases for Unit 2 during plant licensing.  Procedure 2-E-1 was created with the inappropriate steps
  Trip. Dated: 3/22/2016.
on October 8, 2015.  Procedure 1-E-1 was updated with identical steps on     
Level 2 Evaluation - CR Number 1152462, Rev 0 dated 4/26/2016.
December 28, 2015.  The licensee removed the inappropriate steps in both procedures. 
NPG Technical Pre-Job Briefing Checklist AEC CR1152462 dated 3/31/2016
The licensee evaluated the past operability of the ERCW system for the time period
TVA Corrective Action 1152462-006 Completed 12/21/2016.
where the steps were incorporated into the procedure and determined that the condition resulted in the A train of ERCW/CCS being inoperable for Unit 2 for 11 days.
TVA Condition Report 1152462 draft: 03/22/2016 Unit 1 Reactor Trip
Operations Log for 8/17/2017
Analysis.  The failure to maintain written procedures for emergencies as required by TS 5.7.1.1.a was a performance deficiency.  The performance deficiency was more than
minor because it affected the Mitigating Systems Cornerstone attribute of Procedure Quality and adversely affected the cornerstone objective in that reduced ERCW flow caused by the inappropriate steps resulted in the Unit 2A train of ERCW/CCS being
inoperable for 11 days.  This finding was assessed using NRC inspection Manual
Chapter 0609, Attachment 4, "Initial Characterization of Findings."  Using Appendix A,
Exhibit 2, "Mitigating Systems Screening Questions," the finding was determined to require a detailed risk evaluation because it represented an actual loss of function of at least a single train for greater than its TS allowed outage time when the 2A train of ERCW/CCS was inoperable for 11 days.  A regional SRA performed the detailed risk evaluation using SAPHIRE Version 8.1.6 and Version 8.50 of the SPAR Model for both units combined.  The SRA modified the fault trees for the ERCW 1B & 2A Supply Headers to reflect the inappropriate steps for opening Valve 1-FCV-67-458 given a power loss of either A or B train power, assumed the affected header would fail if the valve were opened, and used an exposure time of one year.  The result was less than 1E-6 for each unit which would be a finding of very low significance (Green).  For Unit 1, the dominant sequences were related to loss of offsite power where the performance deficiency fails ERCW Header 2A leading to loss of seal cooling.  For Unit 2, the dominant sequences were similar with the performance deficiency failing ERCW Header 1B.  The risk was mitigated because the performance deficiency would affect operation only when a LOCA occurred with the simultaneous loss of two shutdown boards.
 
The finding had a cross-cutting aspect in the Documentation attribute of the Human
Performance area because the licensee did not maintain the accuracy of 1-E-1 through its revisions and did not maintain procedure 2-E-1 accurate at its creation. (H.7).
Enforcement.  TS 5.7.1.1.a, "Procedures," required, in part, that written procedures be established, implemented, and maintained covering activities related to procedures
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978.  Regulatory Guide 1.33, revision 2, Appendix A, Section 6, "Procedures for Combating Emergencies and Other Significant Events" recommends procedures for loss of coolant.  Contrary to
the above, since October 8, 2015, 2-E-1, revision 0, was not properly established when
a procedural step directing opening of valve 1-FCV-67-458 was included.  Also, since
December 28, 2015, procedure 1-E-1, revision 7, was not maintained when the same
procedural step was added.  This violation was entered in to the licensee's CAP as    CR 1331422 and procedures 1-E-1 and 2-E-1 have been revised to remove this step. 
11  This violation is being treated as an NCV consistent with Section 2.3.2 of the NRC Enforcement Policy and is identified as NCV 05000390, 391/2017003-01, Failure to Maintain Procedures for Response to a Loss of Coolant Accident.
.2 Inadequate Procedure for Unit Cooldown from Hot Standby to Cold Shutdown
Introduction:  An NRC-identified finding of very low safety significance (Green) and associated NCV of TS 5.7.1.1.a, "Procedures," was identified for the failure to maintain TVA procedures 1-GO-6 and 2-GO-6, both entitled Unit Shutdown from Hot Standby to
Cold Shutdown.  The licensee failed to update the procedures based on a PDO to
include steps that would shutdown the running motor driven auxiliary feedwarer pump (MDAFW) prior to starting a third ERCW pump during the period where the opposite unit has been shutdown less than 48 hours.
Discussion:  TVA design change notification (DCN) 62151 was issued to ensure the dual unit system alignment and flow settings for the ERCW system would support operability and conform to the design bases for both units as Unit 2 transitioned from construction
to full commercial operation.  The DCN ident
ified procedural changes necessary to comply with Unit 1 license amendmen
t 104, which added TSs 3.7.16, Component Cooling System - Shutdown, and 3.7.17, Essential Raw Cooling Water System -
Shutdown, and the Unit 2 operating license.  TS 3.7.16 and 3.7.17 required additional
CCS and ERCW pumps to be operable within 48 hours of a unit shutdown.  One of the
 
procedure changes discussed in DCN 62151 was necessary to ensure the ERCW system was able to meet the limiting design bases event discussed in Unit 1 license amendment 104 and the Unit 2 operating license which consisted of a design bases
LOCA on one unit coincident with a dual unit LOOP, while the other (non-accident) unit
is on RHR shutdown cooling within 48 hours after shutdown and experiences a single
active failure in the form of a loss of power to one train.  The changes consisted of procedure revisions to require starting a third ERCW pump and having provisions to load it as the second ERCW pump on a single diesel generator (EDG) during the limiting
 
design basis event.  It was recognized, during the license amendment process, that the diesel generator loading analysis assumed the MDAFW pump was not running on the
non-accident unit.  However, the limiting design bases event assumes a dual unit LOOP
 
where MDAFW pumps would be automatically loaded onto the non-accident unit's EDGs.  As a result, DCN 62151 required the emergency procedures be revised to direct the MDAFW pumps for the non-accident unit be stopped and placed in pull to lock and
then activate the applicable ERCW pump interlock bypass switch.
 
On July 12, 2017, the licensee identified that a previously unknown and unanalyzed failure mode may be more limiting than the limiting design bases event.  As part of this discovery the licensee realized the procedural changes in DCN 62151 had not been
implemented despite Unit 2 starting commercial operation in September of 2016.  As a
result, several emergency procedures did not reflect the required ECRW valve position and flow requirements to properly mitigate a limiting design bases accident on Unit 2.  The licensee completed a PDO on July 16, 2017.  The PDO identified four compensatory actions necessary to restore operability.  The four actions were all associated with Unit 1 and Unit 2 emergency and general operating procedure changes. 
 
 
12  The inspectors reviewed the PDO and determined that the need to stop a running MDAFW pump prior to loading an EDG with a second ERCW pump, to prevent overloading of the EDG, was not recognized as a required compensatory action to
restore operability.  The licensee agreed that the procedure changes to stop the running
MDAFW pump were required and they revised the PDO on July 17, 2017, to include the
necessary procedure changes. 
 
Analysis:  The licensee's failure to maintain TVA procedures 1-GO-6, revision 8 and    2-GO-6, revision 6 was a performance deficiency.  The performance deficiency was more than minor because it affected the Mitigating Systems Cornerstone attribute of
Equipment Performance and affected the cornerstone objective in that failure to maintain
the procedures resulted in a condition where the EDG would have been overloaded and rendered inoperable in response to a design basis event.  The inspectors evaluated the significance of this finding using IMC 0609, Attachment 4, Appendix A, Exhibit 2, and
determined that this finding was of very low safety significance (Green) because the
finding did not represent an actual loss of function of a single train for greater than its TS
allowed outage time. 
The finding had a cross-cutting aspect in the Avoid Complacency component of the
Human Performance area as defined in
NRC IMC 0310 because the organization failed to recognize the possibility of mistakes and use appropriate error reduction tools.  [H.12].
 
Enforcement:  TS 5.7.1.1.a, "Procedures," required, in part, that written procedures be established, implemented, and maintained covering activities related to procedures
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory
Guide 1.33, Section 2(j), "General Plant Operating Procedures," required procedures for
Hot Standby to Cold Shutdown.  Contrary to the above, from July 16, 2017 to           
July 17, 2017, the licensee failed to maintain their procedures for unit shutdown from hot standby to cold shutdown, 1-GO-6, revision 8 and 2-GO-6, revision 6, because they did not include steps to prevent an EDG overload by stopping the running MDAFW pump. 
The licensee's immediate corrective actions included revising both procedures to add
the required steps.  This violation was entered into the CAP as CR 1318176 and is being
treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy.  It is
identified as NCV 05000391, 390/2017003-02, Inadequate Procedure for Unit Cooldown from Hot Standby to Cold Shutdown.
1R19 Post-Maintenance Testing (71111.19)
a. Inspection Scope
The inspectors reviewed the post-maintenance test procedures and/or test activities, 
(listed below) as appropriate, for selected risk-significant mitigating systems to assess
whether:  1) the effect of testing on the plant had been adequately addressed by control
room and/or engineering personnel; 2) testing was adequate for the maintenance
performed; 3) acceptance criteria were clear and adequately demonstrated operational readiness consistent with design and licensing basis documents; 4) test instrumentation had current calibrations, range, and accuracy consistent with the application; 5) tests
were performed as written with applicable prerequisites satisfied; 6) jumpers installed or 
13  leads lifted were properly controlled; 7) test equipment was removed following testing; and 8) equipment was returned to the status required to perform its safety function.  The inspectors verified that these activities were performed in accordance with             
NPG-SPP-06.9, Testing Programs; NPG-SPP-06.3, Pre-/Post-Maintenance Testing; and
NPG-SPP-07.1, On Line Work Management.  This activity constituted five Post
Maintenance Testing inspection samples, as defined in IP 71111.19.
 
* WO 118921021, 2-SI-68-120, 184 day channel operational test reactor coolant flow loop 3 channel III, loop 2-LPF-68-48D (F-436)
* WO 118851496, 2-SI-99-10-B, 62 day functional test of SSPS train B and reactor trip breaker B following tester circuit board replacement
* WO 118921021, 2-SI-68-120, 184 day channel operational test reactor coolant flow loop 3, channel III, loop 2-LPF-68-48D (F436) following EAGLE 21 DFP circuit board
replacement
* WO 119010949, 1-SI-30-902-A, Valve full stroke exercising during plant operation ventilation train A following replacement of quick exhaust valve on 1-FCV-30-40
* WO 118985349, Post maintenance test following 2B2 EDG auxiliary lube oil pump
replacement
b. Findings
No findings were identified.
1R20 Refueling and Outage Activities (71111.20)
.1 Unit 2 Forced Outage (July 1, 2017 - August 8, 2017)
a. Inspection Scope
The Unit 2 began a forced outage on March 23, 2017, due to a structural failure of the B condenser waterbox. On July 1, 2017, the unit was in mode 5 until the unit began to heat up in preparation for startup.  The reactor became critical on July 23, 2017, but returned to hot standby (Mode 3) due to equipment problems with the main feed pumps.  On      July 25, 2017, startup resumed, but the reactor was tripped before criticality due to rod
position indication problems.  Startup recommenced on July 27, 2017, but was stopped
 
due to additional rod position indication problems.  On July 30, 2017, Unit 2 started up after rod position indication repairs and achieved 29 percent rated thermal power (RTP)
on August 2, 2017.  The unit remained at 29 percent RTP until August 3, 2017, when the turbine was tripped due to a steam leak on a turbine drain line.  The reactor stabilized at 8 percent RTP and remained there until power ascension resumed after drain line
repairs.  Unit 2 reached 100 percent RTP on August 8, 2017, and remained there for the
remainder of the reporting period.
 
The inspectors observed the licensee's mode changes and startups in order to verify that they were performed in accordance with station procedures and TSs.  The inspectors
made entry into containment prior to the unit restart to assess the material condition of
SSCs, including the containment sump.  The inspectors attended forced outage meetings 
14  and reviewed the daily risk assessments and condenser repair plans. The inspectors also observed the performance of some surveillance testing being performed while the unit was shutdown.  This activity constituted one Refueling and Other Outage Activities sample, as defined in IP 71111.20.
b. Findings
  No findings were identified.
1R22 Surveillance Testing (71111.22)
a. Inspection Scope
The inspectors witnessed the surveillance tests and/or reviewed test data of selected
risk-significant SSCs listed below, to assess, as appropriate, whether the SSCs met the
requirements of the TS; the UFSAR; NPG-SPP-06.9, Testing Programs;                 
NPG-SPP-06.9.2, Surveillance Test Program; and NPG-SPP-09.1, ASME Section XI.  The inspectors also determined whether the testing effectively demonstrated that the SSCs were operationally ready and capable of performing their intended safety
functions.  This activity constituted ten Surveillance Testing inspection samples; three  in-service and seven routine; as defined in IP 71111.22.
 
In-Service Test:
* WO 118371917, 1-SI-62-901-A, Centrifugal charging pump 1A-A quarterly performance test
* WO 118086192, 2-SI-67-908-B, Valve full stroke exercising and position indication verification during cold shutdown - essential raw cooling water (train 2B)
* WO 118431243, 1-SI-74-901-A, Residual heat removal pump 1A quarterly performance test
Other Surveillances
* WO 118431170, 0-SI-82-12-A, Monthly diesel generator start and load test DG 2A-A
* WO 118086055, 2-SI-0-710, Containment integrity: penetrations
* WO 117823693,  2-SI-211-1-A, 18 month 6.9 KV shutdown board 2A-A automatic and manual transfer tests
* WO 118061393,  2-SI-211-1-B, 18 month 6.9 KV shutdown board 2B-B Automatic and Manual Transfer Tests
* WO 117823686, 2-SI-211-3-A, 18 month functional test on 6900V SD BD 2A-A
degraded and undervoltage relays
* WO 117823687, 2-SI-211-3-B, 18 month functional test on 6900V SD BD 2B-B
degraded and undervoltage relays
* WO 117823601, 2-SI-68-86, 18 month channel calibration of remote shutdown monitoring narrow range pressurizer pressure loop 2-LPP-68-337C
 
15  b. Findings
Introduction:  A self-revealed finding of very low safety significance (Green) and associated NCV of TS (TS) 5.7.1.1.a, "Procedures," was identified for the failure to follow
TVA procedure 2-SI-68-86, 18 Month Channel Calibration of Remote Shutdown
Monitoring Narrow Range Pressurizer Pressure Loop 2-LPP-68-337C, Revision 4.  The
licensee failed to properly follow step 6.2.6 [1.3], which resulted in the inadvertent lifting of a pressurizer power operated relief valve (PORV). 
Discussion:  On June 21, 2017, instrumentation and control technicians were performing Surveillance 2-SI-68-86.  The surveillance verified the function of the transfer switches
for the PORV and its associated block valve to transfer power from the main control room to the auxiliary control room.  Step 6.2.6 [1.3] of the procedure directed that the distributed control system (DCS) demand for the PORV be toggled to 0 (closed).  When
the technicians came to this step, they toggled the output as directed in the beginning of
the procedure step.  However, they did not recognize that the DCS demand was at 0
and, therefore, toggled it to 1 (open).  When the auxiliary transfer switch was operated, the PORV had an open signal present and opened.  This resulted in a reactor coolant pressure drop from 335 psig to 310 psig.  The main control room operators were alerted
to this condition by an annunciator for high pressure in the pressurizer relief tank,
 
properly diagnosed the inadvertent PORV opening, and shut the associated PORV block
valve stopping the pressure decrease.
 
Analysis:  The licensee's failure to follow TVA procedure 2-SI-68-86, was a performance deficiency.  The performance deficiency was more than minor because it affected the Initiating Events Cornerstone attribute of Human Performance and adversely affected
the cornerstone objective in that failing to follow procedure 2-SI-68-86 resulted in a
temporary lowering of reactor coolant pressure and inventory.  The finding was screened in accordance with NRC IMC 0609, Attachment 4, Appendix G, "Shutdown Operations Significance determination process Phase 1 Initial Screening and Characterization of
Findings."  The finding was screened to Green based on the answers to questions 2 and
3.  The resultant leakage from the open PORV would not have caused the current decay
heat removal method to fail if it went undetected and leakage would be self-limiting such
that it would stop before impacting the operating method of decay heat removal.
The finding had a cross-cutting aspect in the Challenge the Unknown component of the
Human Performance area as defined in NRC IMC 0310, because the technicians failed
to recognize that the output was already set to 0, but proceeded anyways to toggle the
output which resulted in setting it to 1 [H.11].
Enforcement:  TS 5.7.1.1.a, "Procedures," required, in part, that written procedures be established, implemented, and maintained covering activities related to procedures
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory
Guide 1.33, Section 8, "Procedures for Control of Measuring and Test Equipment and for
Surveillance Tests, Procedures, and Calibrations" requires procedures for surveillance tests.  Contrary to the above, required surveillance procedure 2-SI-68-86, revision 4, was not implemented when step 6.2.6 [1.3] was not performed as written.  Corrective
actions taken or planned by the licensee include revisions to 2-SI-68-86 to clarify the 
16  steps relating to toggling the DCS output, training for the craft, and management oversight of pre-job briefs.  This violation was entered into the CAP as CR 1309345 and is being treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy. 
This violation is identified as NCV 05000391/2017003-03, Failure to Follow a
Surveillance Procedure Led to an Inadvertent Lift of a Pressurizer Power Operated
 
Relief Valve.
Cornerstone:  Emergency Preparedness
1EP6 Drill Evaluation (71114.06)
a. Inspection Scope
On the dates listed below, the inspectors observed a licensee-evaluated emergency
 
preparedness drill to verify that the emergency response organization was properly classifying the event in accordance with licensee procedure EPIP-1, Emergency Plan
Classification Flowchart, and making accurate and timely notifications and protective action recommendations in accordance with EPIP-2, Notification of Unusual Event;
EPIP-3, Alert; EIPIP-4, Site Area Emer
gency; EPIP-5, General Emergency; and the Radiological Emergency Plan.  In addition, the inspectors verified that licensee
evaluators were identifying deficiencies and properly dispositioning performance against
the performance indicator criteria in Nuclear Energy Institute (NEI) 99-02, Regulatory
Assessment Performance Indicator Guideline.  This activity constituted two EP drill evaluation inspection samples.
* EP drill on July 17, 2017
* EP drill on August 16, 2017
b. Findings
No findings were identified.
 
4. OTHER ACTIVITIES
4OA1 Performance Indicator (PI) Verification (71151)
.1 Cornerstone:  Mitigating Systems
a. Inspection Scope
The inspectors sampled licensee submittals for the two PIs listed below.  To verify the
accuracy of the PI data reported from July 1, 2016 through June 30, 2017.  PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Indicator Guideline, Revision 7, were used to verify the basis in reporting for each data element. 
This activity constituted two performance indicator samples, as defined in IP 71151. 
17    * High Pressure Safety Injection MSPI
* RCS leak rate
b. Findings
No findings were identified.
4OA2 Problem Identification and Resolution (71152)
.1 Review of Items Entered into the CAP
As required by Inspection Procedure 71152, Problem Identification and Resolution, and
in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's CAP.  This review was accomplished by reviewing daily condition report (CR) summary reports and attending daily CR review meetings 
.2 Annual Sample:  Review of CR 129727, Watts Bar Elevation Letter - Operations Leadership Formality and Rigor
a. Inspection Scope
  The inspectors reviewed CR 1297271, WBN Elevation Letter - Operations Leadership Formality and Rigor, in detail to evaluate the effectiveness of the licensee's corrective
actions intended to address operator performance concerns. The CR was written to
address the continued lack of formality, rigor, and discipline by operators in monitoring and controlling the plant.  The inspectors assessed whether issues were properly identified, documented accurately and completely, properly classified and prioritized,
adequately considered extent of condition, generic implications, common cause, and
previous occurrences, adequately identified root causes/apparent causes, and identified
appropriate and timely corrective actions.  The inspector reviewed processes contained in the licensee's Conduct of Operations procedure (OPDP-1) and CAP (NPG-SPP-22.300).  This activity constituted one sample of in-depth review as defined in IP 71152.
b. Observations and Findings 
To address the concerns identified in CR 1297217, the licensee developed a High Intensity Training (HIT) program.  The training was developed to refocus training personnel and license operators of standards, behaviors and expectations associated
with plant operations.  The inspector discussed the licensee's HIT program with
members of the licensee's training staff, operation's management, and licensee
operators during a four day period.  During the discussions, the inspector was able to obtain a clear understanding of why and how HIT was developed. 
During the four days of observing HIT activities, the inspectors observed two operating
crews and two crews of evaluators in a training environment.  The inspector also
observed classroom training and critiques following each simulator scenario.  Many of 
18  the training activities were also observed by a member of the licensee's corporate training staff, onsite operations management, a contract third party evaluator, and a peer
evaluator from another utility. 
 
The training sessions were found to be very intense and operational focused.  The
evaluators were extremely critical of cr
ew performance.  The evaluators took every opportunity to identify and address concerns.  Whenever a concern/issue was identified, the scenario was stopped and the issues was discussed with the crew.  Stopping the scenario and holding discussions occurred numerous times throughout each scenario. 
Following each discussion, the simulator was reset to the desired point and reran.  The
discussions were very interactive.  During the discussions, the evaluators constantly
focused on procedural requirement and licensee expectations.  The evaluators were often challenged/questioned by crew members.  The evaluators adequately addressed each question or concern identified by the cr
ew.  The inspector also observed critiques following scenarios. 
 
From the inspector's observation it was clear that HIT was designed to address operational performance issues identified in the CR.  The effectiveness of HIT can only be evaluated by observing operator and plant performance over time.  The inspectors
concluded that the training provided during HIT, if embraced, should decrease lack of
formality, increase rigor, and improve discipline by operators in monitoring and
controlling the plant.  The HIT would also be expected to improve operators'
implementation of standards outlined in OPDP-1, Conduct of Operations.  The inspectors will continue to monitor operator and plant performance in the control room, during actual plant events and in licensed operator simulator training, as required by the
baseline inspection program.  No findings were identified.
.3 Semiannual Trend Review
a. Inspection Scope
The inspectors performed a review of the licensee's CAP and associated documents to
identify trends that could indicate the existence of a more significant safety issue.  The
review was focused on trends in risk management, long-standing minor equipment deficiencies, housekeeping, TS compliance, corrective action screening and condition adverse to quality documentation.
 
b. Observations and
Findings
No findings were identified.  The inspectors had several observations regarding the trends listed above.  Regarding risk management, the inspectors noted that the environmental factor for the equipment out of service computer program (EOOS) was not consistently adjusted per procedure to reflect activities in the plant switchyard.  This
was initially identified to the licensee in 2016.  The condition report written at that time
documented the issue as an NRC question, rather than a failure to follow the EOOS procedure, and the corrective action was to respond to the NRC to ensure that their question was answered, rather than address procedure non-compliance.  The inspectors
 
re-visited this with the licensee when they observed switchyard work in progress without 
19  the environmental factor setting in EOOS being per procedure.  This time the licensee properly characterized the issue as procedure non-compliance in their CAP.  The inspectors used the EOOS test module and verified that risk remained GREEN during
instances when the environmental factor adjustment was not properly set.  The
inspectors noted that, for the work performed when the environmental factor was not
properly set, the licensee did implement physical risk mitigation controls at the work sites that were in accordance with the appropriate work management procedures.      The inspectors also noted a trend in long-standing equipment issues eventually becoming either operator distractions or worse conditions.  In one instance valve leakby
in the chemical volume and control system gave erroneous indication that the reactor
coolant system was either being borated or diluted.  This required the operating crew to
enter procedures to then verify that the RCS truly was neither borated nor diluted.  In another instance, known leakage on the 1A high pressure fire pump shaft seal worsened to the point that protective measures had to be taken to shield water spray from the
 
power supply conduit of the pump.
 
Since the completion of Unit 2 construction, the inspectors noted a reduction in the amount of temporary equipment stored in the plant auxiliary building and general housekeeping improvements in the auxiliary building.  CAP review during the first and second quarter of 2017 showed a more aggressive approach by the license in improving
housekeeping and removing lingering temporary equipment.  Documents reviewed show that the licensee accomplished this through frequent health and safety walkdowns and
challenging temporary equipment tags that were out of date.  The inspectors observed the results of these efforts in their routine walkdowns of risk-significant areas.  Specifically, in regards to a large scaffold storage area near the Unit 2 713 level
penetration.  Although temporary equipment tags were present and up to date, the area
appeared to have become a convenient location to temporarily store a wide variety of
items beyond scaffolding.  The licensee identified this in their CAP and then completely removed all of the items stored in the area. 
The inspectors also identified negative trends in the treatment of C-level CRs in the CAP and with TS compliance issues.  Inspectors identified multiple C-level CRs during the
inspection period that exhibited one of the following issues: inadequate documented
condition details; inadequate screening of conditi
ons adverse to quality (CAQs) to    non-CAQ status; and failure to promptly identify CAQs.  Inspectors also noted several examples of issues with TS compliance and proper TS application during the inspection
period.  The licensee has identified these issues in their CAP.
4OA3 Event Followup (71153)
.1 (Closed) Licensee Event Report (LER) 05000390, 391/2016-010-00, Emergency Diesel Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a
Tornado  A condition involving the potential impact of a tornado on the EDGs was identified during an NRC Component Design Basis lnspection at the Sequoyah Nuclear Plant.  The EDGs were designed with a crankcase pressure trip setpoint of approximately one inch of
water which is bypassed during an emergency start.  A tornado could potentially induce 
20  a pressure spike which could cause actuation of the crankcase pressure trip due to different vent paths between the EDG room and the EDG crankcase.  Actuation of the crankcase pressure trip would energize the shutdown relay causing an EDG lockout
condition.  The EDG lockout condition would prevent all EDG starts until operators
manually reset the lockout condition.  Because the EDGs at Watts Bar were essentially
identical designs, this condition was reviewed for applicability to Watts Bar.  The
licensee determined this condition placed both units in an unanalyzed condition that could have potentially affected all four EDGs simultaneously.  This was a legacy EDG protective logic circuitry design that did not anticipate the interaction between the
crankcase pressure trip and the outside atmospheric pressure spike during a tornado. 
 
This condition was documented in the licensee CAP as CR 1179264.  A compensatory action was established of starting the EDGs in the emergency mode when notified of a Tornado Warning and ran while the Tornado Warning was in effect ensuring the EDGs would be available to perform their required safety function.  The licensee also implemented DCN 66376 to remove the sealin function of the crankcase differential pressure switches and retain the alarm function of the switches for all four EDGs.  This LER was reviewed by the inspectors.  A licensee-identified violation is documented in
 
Section 4OA7.
.2 (Closed) LER 05000390/2016-001-00, Channel Mode Switch in Incorrect Position Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable.
a. Inspection Scope
On January 12, 2016, at 1645 Eastern Standard Time (EST), Watts Bar Nuclear Plant (WBN) Maintenance personnel were performing a 92 day channel operational test for
radiation monitor 1-RM-90-1064, Lower Containment Atmosphere Particulate Radiation
Monitor, and found the mode switch in the "DlFF" position, which was not expected.  The
surveillance was stopped and an investigation was conducted.  It was determined that the design required the mode switch to be in the "lNT" position to be operable.  The mode selector switch was placed in the "lNT" position and the surveillance was
completed.  The radiation monitor was restored to OPERABLE status at 1743 EST on
January 12, 2016.  Placing the mode selector switch in the "DlFF" position resulted in 1-
RM-90-1064 being INOPERABLE due to the loss of alarm function of the monitor.  Investigation determined that the switch had been repositioned on December 8, 2015.  Because the containment particulate radiation monitor was inoperable for a period of
time greater than permitted by TS 3.4.15, this condition was reportable as an operation
or condition prohibited by TS per 10 CFR 50.73(a)(2)(i)(B).  During the time the monitor
was inoperable, other means of leak detection (e.g., containment pocket sump level
indication, reactor coolant system inventory balance) remained available.  This LER was
reviewed by the inspectors.  No additional fi
ndings or violations of NRC requirements
were identified. 
 
  .3 (Closed) LER 05000390/2016-005-00, Both Trains of Unit 1 Emergency Gas Treatment System Inoperable During Unit 2 Testing 
21    On March 14, 2016, Watts Bar Nuclear Plant (WBN) Unit 1 determined through engineering analysis that both trains of emergency gas treatment system (EGTS) were
inoperable for 8 minutes, 10 seconds during preoperational testing of Unit 2 EGTS.  The
inoperability of A and B trains of Unit 1 EGTS took place on October 22, 2015, while 
Unit 1 was in Mode 1 and two trains of EGTS were required to be operable in
accordance with TS LCO 3.6.9, "Emergency Gas Treatment System (EGTS).  At the time of the event, Unit 2 was in "no mode," prior to initial fuel loading.  With both trains of EGTS inoperable, the specified safety functions of Unit 1 EGTS were not capable of
being performed.  Therefore, this condition was reported pursuant to                           
10 CFR 50.73(a)(2)(v)(C) and 10 CFR 50.73(a)(2)(v)(D), "Event or Condition That Could
Have Prevented Fulfilment of a Safety Function."  This LER was reviewed by the inspectors.  No additional findings or violations of NRC requirements were identified.
.4 (Closed) LER 05000390/2016-004-00, Automatic Reactor Trip Due to Actuation of Over
Temperature Delta Temperature Bistables
On March 22, 2016, at 1131, Watts Bar Nuclear Plant Unit 1 experienced an automatic reactor trip.  The initiating reactor trip first out received was 76-C Over-temperature Delta
T.  The turbine trip first out received was 73-C Rx Trip Breakers RTA and BYA Open.
Prior to the unit trip, Unit 1 was in Mode 1 at 100 percent power.  Concurrent with the
reactor trip, the auxiliary feedwater system actuated.  All control rods inserted upon the reactor trip and safety systems functioned as expected.  This LER was reviewed by the inspectors.  No additional findings or violations of NRC requirements were identified.
.5 (Closed) LER 05000390/2016-006-00, Undersized Room Cooler Fan Shaft Results in Loss of Centrifugal Charging Pump
On May 13, 2016, Watts Bar Unit 1 determined that a condition prohibited by TSs had previously occurred.  During the Fall 2015 outage, maintenance performed on the 1B-B
centrifugal charging pump (CCP) room cooling fan introduced a condition that resulted in
a subsequent bearing failure of the room cooling fan.  This condition would have
prevented the 1B-B CCP pump from performing its function for its designed mission
time.  Based on the reduced reliability of the fan, the 1B-B CCP was considered to be inoperable from October 7, 2015, until the fan was repaired and returned to service on December 6, 2015.  During this time, there were several short periods when the 1A-A
CCP was also inoperable.  A NCV for this
condition was documented in NRC Inspection Report 05000390, 391/2016002-02.  The LER was reviewed by the inspectors.  No
additional findings or violations of NRC requirements were identified.
.6 (Closed) LER 05000390/2016-011-00, Loss of Centrifugal Charging Pump Due to
Repeat Failure of Associated Room Cooler 
On August 3, 2016, Wafts Bar Nuclear Plant Unit 1 (WBN1) determined that a condition
prohibited by TS had previously occurred.  During maintenance of the 1B-B CCP room cooler, the bearing was found in a degraded condition requiring repair.  This fan was required to support Operability of the 1B-B CCP.  The fan had been previously repaired
on December 6, 2015, and had less than 100 days of operation since its overhaul.  The 
22  mission time of the CCPs is specified in design documents as 100 days.  Based on the inability of the CCP to meet its mission time, the 1B-B CCP was considered to be design inoperable since its overhaul on December 6, 2015.  This represents a condition
prohibited by TS for the 1B-B CCP being inoperable for greater than its allowed outage
time.  The LER was reviewed by the inspectors.  No findings or violations of NRC
requirements were identified.
4OA5  .1 IP 93100 Safety-Conscious Work Environment Issue of Concern Follow Up
  a. Inspection Scope
The inspectors assessed the TVA Nuclear corporate safety-conscious work environment (SCWE) by conducting safety culture interviews of individuals from the engineering, licensing, and operations groups.  Inspectors interviewed a total of 22
individuals to determine if indications of a chilled work environment
exist, employees are reluctant to raise safety and regulatory issues, and employees are being discouraged from raising safety or regulatory issues.  Information gathered during the interviews was used in aggregate to assess the work environment at TVA Nuclear corporate.
  b. Assessment
Based on the interviews conducted, the inspectors determined that licensee management emphasized the need for all empl
oyees to identify and report problems using the appropriate methods established within the administrative programs, including
the CAP and Employee Concerns Program.  These methods were readily accessible to all employees.  Based on discussions conducted with a sample of employees from
various departments, the inspectors determined that employees felt free to raise safety and regulatory issues, and that management encouraged employees to place issues into the CAP for resolution.  The inspectors did not identify any reluctance on the part of the
licensee staff to report safety concerns.
4OA6 Meetings, including Exit
  On October 25, 2017 and November 8, 2017, the resident inspectors presented the inspection results to members of the licensee staff.  The inspectors confirmed that none
of the potential report input discussed was considered proprietary.
4OA7 Licensee-Identified Violations
The following licensee-identified violations of NRC requirements were determined to be
of very low safety significance and met the NRC Enforcement Policy criteria for being
dispositioned as NCVs.
 
* Technical Specification 5.7.1.1.a, "Procedures," required, in part, that written procedures be established, implemented, and maintained covering activities
related to procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978.  Regulatory Guide 1.33, Revision 2, Appendix A, Section 6, 
23  "Procedures for Combating Emergencies and Other Significant Events" requires procedures for a reactor trip.  Contrary to the above, from May 23, 2016, until    July 16, 2017, procedure 2-E-0, Revision 5, Reactor Trip and Safety Injection, was
not maintained which resulted in a condition where CCS Heat Exchanger B
(ERCW/CCS Train 2A) would not have been able to remove sufficient heat during
sump recirculation following a LOCA on Unit 2 for approximately 75 days.  This
condition was caused by the licensee's failure to implement ERCW system      DCN 62151 as written.  A detailed risk evaluation was performed using SAPHIRE Version 8.1.5 and Version 8.50 of the SPAR Model for both units combined.  The
result was less that 1E-6/year for Unit 2, which would be a finding of very low
significance (Green).  This violation was entered in to the licensee's CAP as     
 
CR 1316395.
* Technical Specification 5.7.1.1.a stated, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures in Regulatory Guide 1.33 Rev. 2, Appendix A, February 1978.  Procedures for locking
and tagging are applicable procedures under REG GUIDE 1.33 Appendix A, 1.c
 
Equipment Control.  Contrary to this requirement, Step 3.2.4.M of procedure 
NPG-SPP-10.2, Clearance Procedure to Safely Control Energy, Revision 18 was not followed when nitrogen supply isolation valves 2-ISIV-1-408L and                 
2-ISIV-1-408M and isolation valves 2-IS
IV-1-405L and 2-ISIV-1-405M were closed and tagged but not documented as tagged in the Electronic Shift Operations
Management System (eSOMS).  As a result, the valves remained closed resulting
in the inability to operate the Unit 2 SG#1 and #2 PORVs using back-up nitrogen. 
The finding was determined to be Green because having the nitrogen supply to two out of four steam generator PORVs isolated only affects the ability to achieve and maintain cold shutdown.  The licensee documented this violation as           
 
CR 1303309.
* Title 10 CFR Part 50, Appendix B, Criterion XI, "Test Control," required, in part, a testing program to demonstrate that quality related SSCs will perform satisfactorily in service and performed in accordance with written test procedures.  Contrary to the above, from at least 2010 until July 2017, various safety-related valves were unacceptably preconditioned prior to required as-found testing.  This finding was of
very low safety significance (Green) because the finding did not represent an
actual loss of function of a single train for greater than its TS allowed outage time. 
The licensee documented this violation as CRs 1276605, 1316712, 1319298,
 
1319304.
* 10 CFR Part 50, Appendix B, Criterion III, "Design Control," stated, in
part, that, measures shall be established for the selection and review for suitability
of application of materials, parts, equipment, and processes that are essential to the
safety-related functions of SSCs.  Contrary to the
above, for at least the past twenty years, the licensee failed to assess the effects of a tornado on the
crankcase over-pressure trip which could prevent EDGs from fulfilling their    safety-related function.  A regional senior reactor analyst performed a detailed risk evaluation and determined the dominant accident sequences involved a   
weather-related loss of offsite power with all four EDGs failing due to the 
24  performance deficiency and the operators recovering one of the failed EDGs.  The risk of this performance deficiency was not greater than Green due to the low frequency of tornados/high winds and the potential for operator recovery. The
licensee documented this violation as CR 117926.
* Technical Specification LCO 3.6.3, Containment Isolation Valves, required that each containment isolation valve shall be operable in modes 1, 2, 3, and 4.  TS Required Action statement 'A.1' required that the affected penetration flow path be isolated,
and Required Action 'A.2', directed that the penetration flow path is verified to be isolated once per 31 days.  Contrary to the above, on May 18, 2017, containment isolation valve 1-FCV-31-330 was tagged closed for maintenance; however no
verification that the flow path was isolated was performed until August 23, 2017. 
This finding was of very low safety-significance (Green) because it did not represent
an actual open pathway in the physical integrity of reactor containment and was not related to hydrogen ignitors.  The licensee documented this violation as               
CR 1331287.
* Unit 1 Operating License condition 2.F required, in part, that TVA shall implement and maintain in effect all provisions of the approved Fire Protection Program.  The Fire Protection Report was developed to ensure compliance with the requirements of
this licensee condition.  Fire Protection Report, Part II, is the Fire Protection Plan (FPP).  FPP Subsection 14.10, Fire Safe Shutdown Equipment, required nonfunctional equipment listed in Table 14.10 be restored to its functional status
within 30 days.  If this 30 day requirement cannot be met, then the equipment be
placed in its fire safe shutdown (FSSD) position.  Contrary to the above, during a
surveillance on June 10, 2017, backdraft damper 0-BKD-31-592, equipment listed in
Table 14.10, was identified as not being able to achieve its FSSD position.  However, actions to place the damper in its FSSD position were not taken until July 11, 2017.  This finding was of very low safety significance because there was a fully functional
automatic suppression system on either side of the fire barrier.  This violation was
documented as CR 1316058.
 
Attachment SUPPLEMENTARY INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel 
G. Arent, Director, WBN Site Licensing
M. Casner, Director, Engineering L. Cross, Manager, Electrical Systems T. Detchemendy, Manager, Site Emergency Preparedness
E. Ellis, Senior Manager, Nuclear Site Security
D. Erb, Operations Director
K. Hulvey, Watts Bar Licensing Manager  J. James, Director, Maintenance B. Jenkins, Director, Plant Support
T. Marshall, Plant Manager
C. Rice, Operations Superintendent
P. Simmons, Site Vice President
A. White, Senior Manager, Site Quality Assurance
  LIST OF REPORT ITEMS
Opened and Closed NCV 05000390, 391/2017003-01  Failure to Maintain Procedures for Response to a Loss of Coolant Accident (Section 1R15.1)
NCV 05000391, 390/2017003-02  Inadequate Procedure for Unit Cooldown from Hot
Standby to Cold Shutdown (Section 1R15.2)
NCV 05000391/2017003-03    Failure to Follow a Surveillance Procedure Led to an Inadvertent Lift of a Pressurizer Power Operated
 
Relief Valve (Section 1R22)
Closed LER 05000390, 391/2016-010-00 Emergency Diesel Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of
 
a Tornado (Section 4OA3.1)
LER 05000390/2016-001-00  Channel Mode Switch in Incorrect Position Renders
Lower Containment Atmosphere Particulate
Radiation Monitor Inoperable (Section 4OA3.2)
LER 05000390/2016-005-00  Both Trains of Unit 1 Emergency Gas Treatment System inoperable During Unit 2 Testing (Section
4OA3.3) 
LER 05000390/2016-004-00  Automatic Reactor Trip Due to Actuation of Over
Temperature Delta Temperature Bistables (Section
 
4OA3.4)  LER 05000390/2016-006-00  Undersized Room Cooler Fan Shaft Results in Loss
of Centrifugal Charging Pump (Section 4OA3.5)
LER 05000
390/2016-011-00
Loss of Centrifugal Charging Pump
Due to Repeat Failure of
Associated Room Cooler (Section 4OA3.6)
  LIST OF DOCUMENTS REVIEWED
Section 1R01:  Adverse Weather Protection 0-MI-17.003, Flood Mode Preparation Storage Locations and Periodic Inventory, Rev. 0012
0-TI-444, External Flood Protection Program, Rev. 0003
 
Section 1R04:  Equipment Alignment   
Procedures 2-SI-63-8, ECCS Valve Alignment Verification, Rev. 0002 2-SI-3-130, AFW Valve Alignment Verification, Rev. 0004
2-SOI-63.01 ATT 1V, Safety Injection System, Rev. 0005
 
2-SI-70-1, Component Cooling System, Safety-Related Valves: Alignment Verification, Rev.
0004 2-SOI-72.01, Containment Spray System, Rev.  0005 2-SOI-72.01 Containment Spray System Valve Checklist 2-71.01V, ATT 1V, Rev. 0001 0-SOI-82.03, Diesel Generator (DG) 2A-A, Rev. 0012
0-SOI-82.03, Diesel Generator 2A-A Power Checklist 82.03-1P, ATT 1P, Rev. 0000
0-SOI-82.03, Diesel Generator 2A-A Valve Checklist 82.03-1V, ATT 1V, Rev. 0010 0-SOI-67.01, Essential Raw Cooling Water System Supply Header 1A Valve Alignment Checklist 0-67.01-3V, ATT 3V, Rev. 0017 0-PI-OPS-17.0, 18 Month Locked Valve Verification, Rev. 0082
0-TI-31.08, Flow Balancing Valves Setpoint Positions, Rev. 0003
0-SOI-82.04, Diesel Generator (DG) 2B-B, Rev. 0010
0-SOI-82.04. Diesel Generator 2B-B Power Checklist 82.04-1P, ATT 1P, Rev. 0000 0-SOI-82.04, Diesel Generator 2B-B Valve Checklist 82.04-1V, ATT 1V, Rev. 0010 0-SOI-67.01, Essential Raw Cooling Water System Supply Header 1B Valve Alignment Checklist 0-67.01-4V, ATT 4V, Rev. 0017
Section 1R05:  Fire Protection
CRs 1262925, 1343002
Fire Protection Report, Part VI - Fire Hazards Analysis, Rev. 52
WBN-Prefire Plan, AUX-0-692-01, Rev. 4
WBN-Prefire Plan, AUX-0-692-02, Rev. 3
 
Drawing 47A472-1
 
Drawing 47W866-11
Drawing 47W920-2
Drawing 47A381-20
 
Drawing 47A381-127
WBN Prefire Plan AUX-0-713-01, Rev. 1
WBN Prefire Plan AUX-0-713-02, Rev. 3 WBN Prefire Plan AUX-0-713-03, Rev. 4 WBN Prefire Plan CON-0-729-01, Rev. 2
WBN Prefire Plan AUX-0-676-01, Rev. 3 
4  Section 1R13:  Maintenance Risk Assessments and Emergent Work Control
0-TI-12.16, Diesel Generator Outage T/S or SR Contingency Actions, Rev. 0005
WO 118934650 0-SI-82-2, 8 Hour Diesel Generator AC Power Source Operability Verification, Rev. 0025
WO 118928550
CRs 1727208, 1327472
NPG-SPP-09.11.1, Equipment Out of Service Management, Rev. 0012 NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 0021 PWR operational risk review - red sheet for WO 118819797, Hose replacement on Unit 1 main turbine electro-hydraulic control High risk management plan for WO 119013421, Freeze seal for isolation of valve, dated 9/7/17
Section 1R15:  Operability Determinations and Functionality Assessments WOs 118882781, 113861046, 113860919, 118991891 WBN-SDD-N3-85-4003, Control Rod Drive System, Rev. 15
WBN-SDD-N3-99-4003, Reactor Protection System, Rev. 24
Drawings 1082H70-6, Rev. N; 1082H70, Rev. AK; 1082H70-17, Rev. AF
Operational Decision-Making Issue Evaluation Document, dated July 22, 2017
Drawing 2-47W880-4, Rev. 0 0-PI-OPS-17.0, 18 Month Locked Valve Verification, Rev. 0081
N3-67-4002, Essential Raw Cooling Water System
1-E-1, Loss of Reactor or Secondary Coolant, Rev. 0009
WBN-SDD-N3-67-4002, Essential Raw Cooling Water System, System 67, Rev. 0035 0-TI-31.08, Flow Balancing Valves Setpoint Positions, Rev. 0003 0-TI-12.11, Emergency Operating Instruction (EOI) Control, Rev. 0001
TI-78, Lubrication Program, Rev. 0011
NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 0009
WB-DC-40-64, Design Basis Events Design Criteria Westinghouse STS, B 3.8.3, Diesel Fuel Oil, Lube Oil, and Starting Air, Rev. 4.0 0-SOI-82.01, Diesel Generator (DG) 1A-A, Rev. 0009
WBN-VTD-P318-0020, Instructions for EMD Lubricating Oil System
 
Section 1R19:  Post Maintenance Testing
CR 1325844 2-SI-68-114, 184 Day Channel Operational Test RCS Flow Loop 1 Channel III Loop 2-LPF-68-6D (F-416), Rev. 0003
WO 118921021
2-IMI-99.100, EAGLE 21 Rack Diagnostics, Rev. 0002
 
WO 117829913 1-SI-30-901-A, Valve Full Stroke Exercising During Plant Operation - Ventilation (Train A), Rev.
0017 PM 600124762
 
Drawing 1-47W866-1, Rev. 68 
5  Section 1R22:  Surveillance Testing WOs 118628055, 116153069 CRs 1322136, 1276914, 1314124, 1314688, 1309892, 1309602, 1309207  
0-SOI-82.03, Diesel Generator (DG) 2A-A, Rev. 0010  
2-SI-67-908-B, Valve Full Stroke Exercising and Position Indication Verification During Cold SD  
- ERCW (Train 2B), Rev. 0003 2-SI-67-908-B, Valve Full Stroke Exercising and Position Indication Verification During Cold SD  
- ERCW (Train 2B), Rev. 0004 2-SI-67-908-B, Valve Full Stroke Exercising and Position Indication Verification During Cold SD  
- ERCW (Train 2B), Rev. 0005  
1EP6: EP Drill Evaluation Controller's package for July 17, 2017, training drill dated 7/17/17  
CRs 1319059, 1318956, 1318824, 1318834, 1319057, 1318822, 1318830, and 1318823  
Section 4OA3: Followup of Events and Notices of Enforcement Discretion Documentation of Information Sharing - Title: Radiation Meter 1-RM-90-106A Design Change Notice #66212, Rev. A for Equipment: Various/System 65 (Emergency Gas Treatment System) to revise SDD N3-65-4001 to Incorporate Test Requirements,  
    dated: 2/11/2016  
CR 11430756 Level 2 Evaluation Action 007 dated: 07/15/2016  
Past Operability Evaluation Documentation for CR 1143076 signed on 3/10/2016.
Routine WO 117688915, Equipment Description: EH Fluid Display Subpanel, Unit 1 Reactor     Trip. Dated: 3/22/2016. Level 2 Evaluation - CR Number 1152462, Rev 0 dated 4/26/2016.  
NPG Technical Pre-Job Briefing Checklist AEC CR1152462 dated 3/31/2016  
 
TVA Corrective Action 1152462-006
Completed 12/21/2016. TVA Condition Report 1152462 draft: 03/22/2016 Unit 1 Reactor Trip Operations Log for 8/17/2017
}}
}}

Latest revision as of 06:31, 29 October 2019

Integrated Inspection Report 05000390/2017003, 05000391/2017003
ML17326A222
Person / Time
Site: Watts Bar  Tennessee Valley Authority icon.png
Issue date: 11/22/2017
From: Alan Blamey
Reactor Projects Region 2 Branch 6
To: James Shea
Tennessee Valley Authority
Shared Package
ML17326A219 List:
References
IR 2017003
Download: ML17326A222 (32)


See also: IR 05000390/2017003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

November 22, 2017

Mr. Joseph W. Shea

Vice President, Nuclear Licensing

Tennessee Valley Authority

1101 Market Street, LP 3D-C

Chattanooga, TN 37402-2801

SUBJECT: WATTS BAR NUCLEAR PLANT - NUCLEAR REGULATORY COMMISSION

INTEGRATED INSPECTION REPORT 05000390/2017003, 05000391/2017003

Dear Mr. Shea:

On September 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Watts Bar Nuclear Plant, Unit 1 and Unit 2. On October 25, 2017, the NRC

inspectors discussed the results of this inspection with Mr. Tom Marshall and other members of

your staff. A re-exit was conducted on November 8, 2017, with Ms. Kim Hulvey. The results of

this inspection are documented in the enclosed inspection report.

The NRC inspectors documented three findings of very low safety significance (Green) in this

report which also involved violations of NRC requirements. Additionally, inspectors documented

six licensee-identified violations which were determined to be of very low safety significance in

this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with

Section 2.3.2.a of the Enforcement Policy. If you contest these violations or significance of

these NCVs, you should provide a response within 30 days of the date of this inspection report,

with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document

Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator, Region

II; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C.

20555-0001; and the NRC Resident Inspector at the Watts Bar Nuclear Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the

Watts Bar Nuclear Plant.

J. Shea 2

This letter, its enclosure, and your response (if any) will be available for public inspection and

copying at http://www.nrc.gov/reading-rm/adams.html and in the NRC Public Document Room

in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections,

Exemptions, Requests for Withholding.

Sincerely,

/RA/

Alan Blamey, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Docket Nos.: 50-390, 50-391

License Nos.: NPF-90, 96

Enclosure:

IR 05000390/2017003, 05000391/2017003

w/Attachment: Supplemental Information

cc Distribution via ListServ

ML17326A222

OFFICE RII: DRP RII: DRP RII: DRP RII: DRP RII: DRP RII: DRP

NAME RTaylor BDavis GCrespo BBishop JEargle ELea

DATE 10/31/2017 11/8/2017 10/31/2017 10/31/2017 11/6/2017 11/6/2017

OFFICE RII: DRP RII: DRP RII: DRP R:II DRP NCP Approver

NAME JHamman JJandovitz ABlamey JNadel MFranke

DATE 10/31/2017 11/3/2017 11/21/2017 11/7/2017 11/22/2017

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.: 50-390, 50-391

License Nos.: NPF-90, NPF-96

Report No.: 05000390/2017003, 05000391/2017003

Licensee: Tennessee Valley Authority (TVA)

Facility: Watts Bar Nuclear Plant, Units 1 and 2

Location: Spring City, TN 37381

Dates: July 1 through September 30, 2017

Inspectors: J. Nadel, Senior Resident Inspector

J. Hamman, Resident Inspector

J. Jandovitz, Senior Resident Inspector

E. Lea, Regional Government Liaison Officer

S. Freeman, Senior Reactor Analyst

J. Eargle, Senior Construction Inspector

B. Bishop, Project Engineer

G. Crespo, Senior Construction Inspector

C. Rapp, Senior Project Engineer

R. Taylor, Senior Project Inspector

B. Davis, Senior Construction Inspector

Approved by: Alan Blamey, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Enclosure

SUMMARY

IR 05000390/2017-003; 05000391/2017-003; July 1, 2017 - September 30, 2017; Watts Bar

Nuclear Plant; Operability Evaluations, Surveillance Testing.

The report covered a three-month period of inspection by the resident inspectors. Three Green

non-cited violations (NCV) were identified. The significance of most findings is indicated by their

color (i.e., Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," (SDP) dated April 29, 2015. Cross-cutting aspects

are determined using IMC 0310, Aspects Within Cross-Cutting Areas, dated

December 04, 2014. All violations of NRC requirements are dispositioned in accordance with

the NRCs Enforcement Policy, dated November 1, 2016. The NRCs program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 6. Documents reviewed by the inspectors not identified in the

Report Details are listed in the Attachment.

Cornerstone: Mitigating Systems

  • Green. An NRC-identified NCV was identified for the failure to maintain written procedures

for emergencies. Emergency procedure 1-E-1, Revision 7 and 2-E-1 Revision 0, both titled

Loss of Reactor or Secondary Coolant, were updated to include steps directing

inappropriate actions that would have affected emergency raw cooling water (ERCW) supply

flow during an accident. The immediate corrective action was to remove the inappropriate

steps. This violation was documented in the licensees corrective action program (CAP) as

CR 1331422.

The performance deficiency was more than minor because it affected the Mitigating

Systems Cornerstone attribute of Procedure Quality and adversely affected the cornerstone

objective in that the reduced ERCW flow caused by the inappropriate steps affects the heat

removal capability of the ERCW and component cooling systems (CCS) during a loss of

coolant accident (LOCA). The finding was determined to require a detailed risk evaluation

because it represented an actual loss of function of at least a single train for greater than its

TS allowed outage time. The result was less than 1E-6 for each unit which would be a

finding of very low significance (Green). The risk was mitigated because the performance

deficiency would affect operation only when a LOCA occurred and simultaneous loss of two

shutdown boards. The finding has a cross-cutting aspect in the documentation attribute of

the Human Performance area because the licensee did not maintain the accuracy of 1-E-1

through its revisions and did not maintain procedure 2-E-1 accurate at its creation. (H.7)

(Section 1R15)

identified for the failure to maintain TVA procedures 1-GO-6 and 2-GO-6, both titled Unit

Shutdown from Hot Standby to Cold Shutdown. The licensee failed to update the

procedures prior to commencing dual unit operation to include steps that would shut down

the running motor driven auxiliary feedwater pump prior to starting a third ERCW pump

during the time period where the opposite unit has been shut down less than 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. The

licensees immediate corrective actions included revising both procedures to add the

required steps. This violation was documented in the licensees CAP as CR 1318176.

3

The performance deficiency was more than minor because it affected the Mitigating

Systems Cornerstone attribute of Equipment Performance and adversely affected the

cornerstone objective in that failure to maintain the procedures resulted in a situation where

the emergency diesel generator would have been rendered inoperable during a design basis

event. The inspectors determined the finding was of very low safety significance (Green)

because the finding did not represent an actual loss of function of a single train for greater

than its TS allowed outage time. The finding had a cross-cutting aspect in the Avoid

Complacency attribute of the Human Performance area because engineering missed a

critical aspect of the required procedure changes associated with design change notice

62151 when performing the prompt determination of operability and the review process was

unsuccessful at identifying the error [H.12]. (Section 1R15)

Cornerstone: Initiating Events

  • Green. A self-revealed NCV of (TS) 5.7.1.1.a, Procedures, was identified for the failure to

follow TVA procedure 2-SI-68-86, 18 month Channel Calibration of Remote Shutdown

Monitoring Narrow Range Pressurizer Pressure Loop 2-LPP-68-337C, revision 4. The

licensee failed to properly follow step 6.2.6 [1.3], which resulted in the inadvertent lifting of a

pressurizer power operated relief valve (PORV). The licensees immediate corrective

actions included revising the procedure. This violation was documented in the licensees

CAP as CR 1309345.

The performance deficiency was more than minor because it affected the Initiating Events

Cornerstone attribute of Human Performance and adversely affected the cornerstone

objective in that failing to follow procedure 2-SI-68-86 caused a depressurization of the plant

that had to be stopped by operator action. The finding was determined to be very low safety

significance (Green) because the resultant leakage from the open PORV would be

self-limiting such that it would stop before impacting the operating method of decay heat

removal. The finding had a cross-cutting aspect in the Challenge the Unknown component

of the Human Performance area as defined in NRC IMC 0310, because the technicians

failed to recognize that the output was already set to 0, but proceeded anyway to toggle the

output which resulted in setting it to 1 [H.11]. (Section 1R22)

Six violations of very low safety significance, identified by the licensee, have been reviewed by

the NRC. Corrective actions taken or planned by the licensee have been entered into the

licensees CAP. These violations and the corrective action tracking numbers are listed in

Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at 100 percent rated thermal power (RTP) for the entire reporting period.

Unit 2 began the reporting period shutdown for repairs to the main condenser. The unit was

started up on July 23, 2017, but was shutdown to hot standby later that day due to equipment

problems. On July 25, 2017, startup resumed, but the reactor was tripped before criticality due

to rod position indication problems during the startup. Startup commenced again on

July 27, 2017, but was stopped due to additional rod position indication problems. Unit 2 started

up after rod position indication repairs on July 30, 2017, and achieved 29 percent RTP on

August 2, 2017. The unit remained at that power until August 8, 2017, when the turbine was

tripped due to a steam leak on a turbine drain line. The unit stabilized at 8 percent RTP and

remained there until power ascension resumed after drain line repairs. Unit 2 reached

100 percent RTP on August 8, 2017, and remained there for the remainder of the reporting

period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

External Flood Protection Inspection

a. Inspection Scope

The inspectors reviewed the licensees readiness to cope with external flooding.

External flooding from a probable maximum precipitation (PMP) or design basis flood

(DBF) had the potential for internal flooding of a portion of a number of the plant

structures. The inspectors reviewed the feasibility of the licensees flooding mitigation

plans and design features and verified that they were consistent with the licensees

design requirements and the risk analysis assumptions for coping with this type of

event. The inspectors performed walkdowns of selected areas to observe grading, yard

drains, and curbs in the vicinity of the south valve vault rooms. The inspectors also

checked status of the flood mode boat. The inspectors reviewed external flood

protection features at the intake pumping station and condition of the strainer room sump

pumps. Additionally, the inspectors reviewed the licensees related corrective action

documents (condition reports) to ensure any non-conforming conditions related to

potential flooding were properly addressed. The inspection was performed prior to the

expected rainfall from Hurricane Irma. This activity constituted one Adverse Weather

Protection inspection sample, as defined in Inspection Procedure (IP) 71111.01.

b. Findings

No findings were identified.

5

1R04 Equipment Alignment (71111.04)

Partial System Walkdowns

a. Inspection Scope

The inspectors conducted the equipment alignment partial walkdowns listed below to

evaluate the operability of selected redundant trains or backup systems prior to unit

transition into the mode of applicability for the systems. This also included that

redundant trains were returned to service properly. The inspectors reviewed the

functional system descriptions, the Updated Final Safety Analysis Report (UFSAR),

system operating procedures, and TS to determine correct system lineups for the current

plant conditions. The inspectors performed walkdowns of the systems to verify that

critical components were properly aligned and to identify any discrepancies which could

affect operability of the redundant train or backup system. This activity constituted six

inspection samples, as defined in IP 71111.04.

auxiliary feedwater prior to mode change

  • 2A and 2B train of safety injection prior to mode change

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05AQ)

Fire Protection Tours

a. Inspection Scope

The inspectors conducted tours of the areas important to reactor safety listed below to

verify the licensees implementation of fire protection requirements as described in: the

Fire Protection Program, Nuclear Power Group Standard Programs and Processes

(NPG-SPP)-18.4.6, Control of Fire Protection Impairments; NPG-SPP-18.4.7, Control of

Transient Combustibles; and NPG-SPP-18.4.8, Control of Ignition Sources (Hot Work).

The inspectors evaluated, as appropriate, conditions related to: 1) licensee control of

transient combustibles and ignition sources; 2) the material condition, operational status,

and operational lineup of fire protection systems, equipment, and features; and 3) the

fire barriers used to prevent fire damage or fire propagation.

6

This activity constituted three inspection samples, as defined in IP 71111.05AQ.

  • Auxiliary building elevation 713
  • Auxiliary building elevation 676
  • Control building elevation 729 and 741 (cable spreading room)

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification and Performance (71111.11)

.1 Licensed Operator Requalification Review

a. Inspection Scope

On September 12, 2017, the inspectors observed licensed operator training

examinations on the simulator per scenario 3-OT-SRE-1017, revision 7. The scenario

included a feedwater line break and subsequent loss of all main and auxiliary feed

capability. The inspectors specifically evaluated the following attributes related to the

operating crews performance:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of abnormal operating instructions and emergency

operating instructions

  • Timely and appropriate Emergency Action Level declarations per emergency plan

implementing procedures

  • Control board operation and manipulation, including high-risk operator actions
  • Command and Control provided by the unit supervisor and shift manager

The inspectors also attended the critique to assess the effectiveness of the licensee

evaluators, and to verify that licensee-identified issues were comparable to issues

identified by the inspector. This activity constituted one Observation of Requalification

Activity inspection sample, as defined in IP 71111.11.

b. Findings

No findings were identified

7

.2 Observation of Operator Performance

a. Inspection Scope

Inspectors observed and assessed licensed operator performance in the plant and main

control room, particularly during periods of heightened activity or risk and where the

activities could affect plant safety. Inspectors reviewed various licensee policies and

procedures such as procedures OPDP-1, Conduct of Operations; NPG-SPP-10.0, Plant

Operations; and GO-4, Normal Power Operation. Inspectors used activities such as

post-maintenance testing, surveillance testing and refueling, and other outage activities

to focus on the following conduct of operations as appropriate. This activity constituted

one Observation of Operator Performance inspection sample, as defined in IP 71111.11.

  • Operator compliance and use of procedures
  • Control board manipulations
  • Communication between crew members
  • Use and interpretation of plant instruments, indications and alarms
  • Use of human error prevention techniques
  • Documentation of activities, including initials and sign-offs in procedures
  • Supervision of activities, including risk and reactivity management
  • Pre-job briefs

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed the performance-based problem listed below. A review was

performed to assess the effectiveness of maintenance efforts that apply to scoped

structures, systems, or components (SSCs) and to verify that the licensee was following

the requirements of TI-119, Maintenance Rule Performance Indicator Monitoring,

Trending, and Reporting - 10 CFR 50.65, and NPG-SPP-03.4, Maintenance Rule

Performance Indicator Monitoring, Trending, and Reporting - 10 CFR 50.65. Reviews

focused, as appropriate, on: 1) appropriate work practices; 2) identification and

resolution of common cause failures; 3) scoping in accordance with 10 CFR 50.65;

4) characterizing reliability issues for performance monitoring; 5) tracking unavailability

for performance monitoring; 6) balancing reliability and unavailability; 7) trending key

parameters for condition monitoring; 8) system classification and reclassification in

accordance with 10 CFR 50.65(a)(1) or (a)(2); 9) appropriateness of performance criteria

8

in accordance with 10 CFR 50.65(a)(2); and 10) appropriateness and adequacy of

10 CFR 50.65 (a)(1) goals, monitoring and corrective actions. This activity constituted

one Maintenance Effectiveness inspection sample, as defined in IP 71111.12.

  • Condition Report (CR) 1316520, Unit 2 function 063-B Train A (2A safety injection

pump) exceeded performance criteria

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors evaluated, as appropriate, for the work activities listed below:

1) the effectiveness of the risk assessments performed before maintenance activities

were conducted; 2) the management of risk; 3) that, upon identification of an unforeseen

situation, necessary steps were taken to plan and control the resulting emergent work

activities; and 4) that maintenance risk assessments and emergent work problems were

adequately identified and resolved. The inspectors verified that the licensee was

complying with the requirements of 10 CFR 50.65 (a)(4); NPG-SPP-07.0, Work Control

and Outage Management; NPG-SPP-07.1, On Line Work Management;

NPG-SPP-09.11.1, Equipment Out of Service Management; and TI-124, Equipment to

Plant Risk Matrix. This activity constituted four Maintenance Risk Assessment

inspection samples, as defined in IP 71111.13.

(EDG) out of service (OOS) for an extended planned maintenance outage and

applicability of TS 3.8.1.B.5 for the extended limiting condition for operation time

period based on FLEX EDG availability

replacement main transformer movement under dedicated offsite power lines

  • Risk assessment for August 29, 2017, with both sources of offsite power inoperable

due to a disqualified grid

1A-A component cooling system pump OOS for maintenance and high risk work on

Unit 1 turbine electrohydraulic controls, and A main control room chiller OOS

b. Findings

No findings were identified.

9

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the operability evaluations affecting risk-significant mitigating

systems listed below, to assess, as appropriate: 1) the technical adequacy of the

evaluations; 2) whether continued system operability was warranted; 3) whether the

compensatory measures, if involved, were in place, would work as intended, and were

appropriately controlled; 4) where continued operability was considered unjustified, the

impact on TS Limiting Conditions for Operation (LCO) and the risk-significance in

accordance with the significant determination process (SDP). The inspectors verified

that the operability evaluations were performed in accordance with NPG-SPP-03.1,

CAP. Additional documents reviewed are listed in the Attachment. This activity

constituted seven Operability Evaluation inspection samples, as defined in IP 71111.15.

  • Immediate determination of operability (IDO) for CR 1320214, momentary indication

of Unit 2 reactor rod control bank A rod L5 fully inserted

  • Prompt determination of operability (PDO) for CR 1320012, Unit 2 intermittent solid

state protection system (SSPS) train B general warning alarm

power operated relief valve nitrogen supply found isolated

pump shaft shear

  • PDO for CR 1316395, ERCW system design bases and procedural errors potentially

impacting system function

  • POE for CR 1316395, ERCW system design bases and procedural errors potentially

impacting system function

crankcase oil level

b. Findings

.1 Failure to Maintain Procedures for Response to a Loss of Coolant Accident

Introduction. An NRC-identified Green NCV (NCV) was identified for the failure to

maintain written procedures as required by TS 5.7.1.1.a. Emergency procedures 1-E-1,

revision 7, and 2-E-1 revision 0, both titled Loss of Reactor or Secondary Coolant,

contained steps that would have reduced ERCW flow to the A and B CCS HXs and

potentially impacted the operability of the A train header of ERCW and CCS for both

units.

Description. During an NRC review of a licensee-identified issue regarding the CCS

heat exchanger (HX) ERCW outlet and outlet bypass valves, the inspectors found that

emergency procedures 1-E-1and 2-E-1 both included a step that directed opening valve

1-FCV-67-458, CCS HX A supply from ERCW header 1B, during a loss of either A train

or B train power. This procedural action would be implemented during a loss of coolant

accident (LOCA) on one unit with a coincident single active failure causing a loss of train

10

(A or B) power while the other unit was using the residual heat removal (RHR) system

for decay heat cooling. These conditions were incorporated into the design bases for

Unit 2 during plant licensing. Procedure 2-E-1 was created with the inappropriate steps

on October 8, 2015. Procedure 1-E-1 was updated with identical steps on

December 28, 2015. The licensee removed the inappropriate steps in both procedures.

The licensee evaluated the past operability of the ERCW system for the time period

where the steps were incorporated into the procedure and determined that the condition

resulted in the A train of ERCW/CCS being inoperable for Unit 2 for 11 days.

Analysis. The failure to maintain written procedures for emergencies as required by TS 5.7.1.1.a was a performance deficiency. The performance deficiency was more than

minor because it affected the Mitigating Systems Cornerstone attribute of Procedure

Quality and adversely affected the cornerstone objective in that reduced ERCW flow

caused by the inappropriate steps resulted in the Unit 2A train of ERCW/CCS being

inoperable for 11 days. This finding was assessed using NRC inspection Manual

Chapter 0609, Attachment 4, Initial Characterization of Findings. Using Appendix A,

Exhibit 2, Mitigating Systems Screening Questions, the finding was determined to

require a detailed risk evaluation because it represented an actual loss of function of at

least a single train for greater than its TS allowed outage time when the 2A train of

ERCW/CCS was inoperable for 11 days. A regional SRA performed the detailed risk

evaluation using SAPHIRE Version 8.1.6 and Version 8.50 of the SPAR Model for both

units combined. The SRA modified the fault trees for the ERCW 1B & 2A Supply

Headers to reflect the inappropriate steps for opening Valve 1-FCV-67-458 given a

power loss of either A or B train power, assumed the affected header would fail if the

valve were opened, and used an exposure time of one year. The result was less than

1E-6 for each unit which would be a finding of very low significance (Green). For Unit 1,

the dominant sequences were related to loss of offsite power where the performance

deficiency fails ERCW Header 2A leading to loss of seal cooling. For Unit 2, the

dominant sequences were similar with the performance deficiency failing ERCW Header

1B. The risk was mitigated because the performance deficiency would affect operation

only when a LOCA occurred with the simultaneous loss of two shutdown boards.

The finding had a cross-cutting aspect in the Documentation attribute of the Human

Performance area because the licensee did not maintain the accuracy of 1-E-1 through

its revisions and did not maintain procedure 2-E-1 accurate at its creation. (H.7).

Enforcement. TS 5.7.1.1.a, Procedures, required, in part, that written procedures be

established, implemented, and maintained covering activities related to procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory

Guide 1.33, revision 2, Appendix A, Section 6, Procedures for Combating Emergencies

and Other Significant Events recommends procedures for loss of coolant. Contrary to

the above, since October 8, 2015, 2-E-1, revision 0, was not properly established when

a procedural step directing opening of valve 1-FCV-67-458 was included. Also, since

December 28, 2015, procedure 1-E-1, revision 7, was not maintained when the same

procedural step was added. This violation was entered in to the licensees CAP as

CR 1331422 and procedures 1-E-1 and 2-E-1 have been revised to remove this step.

11

This violation is being treated as an NCV consistent with Section 2.3.2 of the NRC

Enforcement Policy and is identified as NCV 05000390, 391/2017003-01, Failure to

Maintain Procedures for Response to a Loss of Coolant Accident.

.2 Inadequate Procedure for Unit Cooldown from Hot Standby to Cold Shutdown

Introduction: An NRC-identified finding of very low safety significance (Green) and

associated NCV of TS 5.7.1.1.a, Procedures, was identified for the failure to maintain

TVA procedures 1-GO-6 and 2-GO-6, both entitled Unit Shutdown from Hot Standby to

Cold Shutdown. The licensee failed to update the procedures based on a PDO to

include steps that would shutdown the running motor driven auxiliary feedwarer pump

(MDAFW) prior to starting a third ERCW pump during the period where the opposite unit

has been shutdown less than 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

Discussion: TVA design change notification (DCN) 62151 was issued to ensure the dual

unit system alignment and flow settings for the ERCW system would support operability

and conform to the design bases for both units as Unit 2 transitioned from construction

to full commercial operation. The DCN identified procedural changes necessary to

comply with Unit 1 license amendment 104, which added TSs 3.7.16, Component

Cooling System - Shutdown, and 3.7.17, Essential Raw Cooling Water System -

Shutdown, and the Unit 2 operating license. TS 3.7.16 and 3.7.17 required additional

CCS and ERCW pumps to be operable within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> of a unit shutdown. One of the

procedure changes discussed in DCN 62151 was necessary to ensure the ERCW

system was able to meet the limiting design bases event discussed in Unit 1 license

amendment 104 and the Unit 2 operating license which consisted of a design bases

LOCA on one unit coincident with a dual unit LOOP, while the other (non-accident) unit

is on RHR shutdown cooling within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> after shutdown and experiences a single

active failure in the form of a loss of power to one train. The changes consisted of

procedure revisions to require starting a third ERCW pump and having provisions to load

it as the second ERCW pump on a single diesel generator (EDG) during the limiting

design basis event. It was recognized, during the license amendment process, that the

diesel generator loading analysis assumed the MDAFW pump was not running on the

non-accident unit. However, the limiting design bases event assumes a dual unit LOOP

where MDAFW pumps would be automatically loaded onto the non-accident units

EDGs. As a result, DCN 62151 required the emergency procedures be revised to direct

the MDAFW pumps for the non-accident unit be stopped and placed in pull to lock and

then activate the applicable ERCW pump interlock bypass switch.

On July 12, 2017, the licensee identified that a previously unknown and unanalyzed

failure mode may be more limiting than the limiting design bases event. As part of this

discovery the licensee realized the procedural changes in DCN 62151 had not been

implemented despite Unit 2 starting commercial operation in September of 2016. As a

result, several emergency procedures did not reflect the required ECRW valve position

and flow requirements to properly mitigate a limiting design bases accident on Unit 2.

The licensee completed a PDO on July 16, 2017. The PDO identified four

compensatory actions necessary to restore operability. The four actions were all

associated with Unit 1 and Unit 2 emergency and general operating procedure changes.

12

The inspectors reviewed the PDO and determined that the need to stop a running

MDAFW pump prior to loading an EDG with a second ERCW pump, to prevent

overloading of the EDG, was not recognized as a required compensatory action to

restore operability. The licensee agreed that the procedure changes to stop the running

MDAFW pump were required and they revised the PDO on July 17, 2017, to include the

necessary procedure changes.

Analysis: The licensees failure to maintain TVA procedures 1-GO-6, revision 8 and

2-GO-6, revision 6 was a performance deficiency. The performance deficiency was

more than minor because it affected the Mitigating Systems Cornerstone attribute of

Equipment Performance and affected the cornerstone objective in that failure to maintain

the procedures resulted in a condition where the EDG would have been overloaded and

rendered inoperable in response to a design basis event. The inspectors evaluated the

significance of this finding using IMC 0609, Attachment 4, Appendix A, Exhibit 2, and

determined that this finding was of very low safety significance (Green) because the

finding did not represent an actual loss of function of a single train for greater than its TS

allowed outage time.

The finding had a cross-cutting aspect in the Avoid Complacency component of the

Human Performance area as defined in NRC IMC 0310 because the organization failed

to recognize the possibility of mistakes and use appropriate error reduction tools. [H.12].

Enforcement: TS 5.7.1.1.a, Procedures, required, in part, that written procedures be

established, implemented, and maintained covering activities related to procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory

Guide 1.33, Section 2(j), General Plant Operating Procedures, required procedures for

Hot Standby to Cold Shutdown. Contrary to the above, from July 16, 2017 to

July 17, 2017, the licensee failed to maintain their procedures for unit shutdown from hot

standby to cold shutdown, 1-GO-6, revision 8 and 2-GO-6, revision 6, because they did

not include steps to prevent an EDG overload by stopping the running MDAFW pump.

The licensees immediate corrective actions included revising both procedures to add

the required steps. This violation was entered into the CAP as CR 1318176 and is being

treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy. It is

identified as NCV 05000391, 390/2017003-02, Inadequate Procedure for Unit Cooldown

from Hot Standby to Cold Shutdown.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the post-maintenance test procedures and/or test activities,

(listed below) as appropriate, for selected risk-significant mitigating systems to assess

whether: 1) the effect of testing on the plant had been adequately addressed by control

room and/or engineering personnel; 2) testing was adequate for the maintenance

performed; 3) acceptance criteria were clear and adequately demonstrated operational

readiness consistent with design and licensing basis documents; 4) test instrumentation

had current calibrations, range, and accuracy consistent with the application; 5) tests

were performed as written with applicable prerequisites satisfied; 6) jumpers installed or

13

leads lifted were properly controlled; 7) test equipment was removed following testing;

and 8) equipment was returned to the status required to perform its safety function. The

inspectors verified that these activities were performed in accordance with

NPG-SPP-06.9, Testing Programs; NPG-SPP-06.3, Pre-/Post-Maintenance Testing; and

NPG-SPP-07.1, On Line Work Management. This activity constituted five Post

Maintenance Testing inspection samples, as defined in IP 71111.19.

  • WO 118921021, 2-SI-68-120, 184 day channel operational test reactor coolant flow

loop 3 channel III, loop 2-LPF-68-48D (F-436)

breaker B following tester circuit board replacement

  • WO 118921021, 2-SI-68-120, 184 day channel operational test reactor coolant flow

loop 3, channel III, loop 2-LPF-68-48D (F436) following EAGLE 21 DFP circuit board

replacement

  • WO 119010949, 1-SI-30-902-A, Valve full stroke exercising during plant operation

ventilation train A following replacement of quick exhaust valve on 1-FCV-30-40

  • WO 118985349, Post maintenance test following 2B2 EDG auxiliary lube oil pump

replacement

b. Findings

No findings were identified.

1R20 Refueling and Outage Activities (71111.20)

.1 Unit 2 Forced Outage (July 1, 2017 - August 8, 2017)

a. Inspection Scope

The Unit 2 began a forced outage on March 23, 2017, due to a structural failure of the B

condenser waterbox. On July 1, 2017, the unit was in mode 5 until the unit began to heat

up in preparation for startup. The reactor became critical on July 23, 2017, but returned

to hot standby (Mode 3) due to equipment problems with the main feed pumps. On

July 25, 2017, startup resumed, but the reactor was tripped before criticality due to rod

position indication problems. Startup recommenced on July 27, 2017, but was stopped

due to additional rod position indication problems. On July 30, 2017, Unit 2 started up

after rod position indication repairs and achieved 29 percent rated thermal power (RTP)

on August 2, 2017. The unit remained at 29 percent RTP until August 3, 2017, when the

turbine was tripped due to a steam leak on a turbine drain line. The reactor stabilized at

8 percent RTP and remained there until power ascension resumed after drain line

repairs. Unit 2 reached 100 percent RTP on August 8, 2017, and remained there for the

remainder of the reporting period.

The inspectors observed the licensees mode changes and startups in order to verify that

they were performed in accordance with station procedures and TSs. The inspectors

made entry into containment prior to the unit restart to assess the material condition of

SSCs, including the containment sump. The inspectors attended forced outage meetings

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and reviewed the daily risk assessments and condenser repair plans. The inspectors also

observed the performance of some surveillance testing being performed while the unit was

shutdown. This activity constituted one Refueling and Other Outage Activities sample, as

defined in IP 71111.20.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors witnessed the surveillance tests and/or reviewed test data of selected

risk-significant SSCs listed below, to assess, as appropriate, whether the SSCs met the

requirements of the TS; the UFSAR; NPG-SPP-06.9, Testing Programs;

NPG-SPP-06.9.2, Surveillance Test Program; and NPG-SPP-09.1, ASME Section XI.

The inspectors also determined whether the testing effectively demonstrated that the

SSCs were operationally ready and capable of performing their intended safety

functions. This activity constituted ten Surveillance Testing inspection samples; three

in-service and seven routine; as defined in IP 71111.22.

In-Service Test:

performance test

  • WO 118086192, 2-SI-67-908-B, Valve full stroke exercising and position indication

verification during cold shutdown - essential raw cooling water (train 2B)

performance test

Other Surveillances

  • WO 118086055, 2-SI-0-710, Containment integrity: penetrations

and manual transfer tests

and Manual Transfer Tests

degraded and undervoltage relays

degraded and undervoltage relays

monitoring narrow range pressurizer pressure loop 2-LPP-68-337C

15

b. Findings

Introduction: A self-revealed finding of very low safety significance (Green) and

associated NCV of TS (TS) 5.7.1.1.a, Procedures, was identified for the failure to follow

TVA procedure 2-SI-68-86, 18 Month Channel Calibration of Remote Shutdown

Monitoring Narrow Range Pressurizer Pressure Loop 2-LPP-68-337C, Revision 4. The

licensee failed to properly follow step 6.2.6 [1.3], which resulted in the inadvertent lifting

of a pressurizer power operated relief valve (PORV).

Discussion: On June 21, 2017, instrumentation and control technicians were performing

Surveillance 2-SI-68-86. The surveillance verified the function of the transfer switches

for the PORV and its associated block valve to transfer power from the main control

room to the auxiliary control room. Step 6.2.6 [1.3] of the procedure directed that the

distributed control system (DCS) demand for the PORV be toggled to 0 (closed). When

the technicians came to this step, they toggled the output as directed in the beginning of

the procedure step. However, they did not recognize that the DCS demand was at 0

and, therefore, toggled it to 1 (open). When the auxiliary transfer switch was operated,

the PORV had an open signal present and opened. This resulted in a reactor coolant

pressure drop from 335 psig to 310 psig. The main control room operators were alerted

to this condition by an annunciator for high pressure in the pressurizer relief tank,

properly diagnosed the inadvertent PORV opening, and shut the associated PORV block

valve stopping the pressure decrease.

Analysis: The licensees failure to follow TVA procedure 2-SI-68-86, was a performance

deficiency. The performance deficiency was more than minor because it affected the

Initiating Events Cornerstone attribute of Human Performance and adversely affected

the cornerstone objective in that failing to follow procedure 2-SI-68-86 resulted in a

temporary lowering of reactor coolant pressure and inventory. The finding was screened

in accordance with NRC IMC 0609, Attachment 4, Appendix G, Shutdown Operations

Significance determination process Phase 1 Initial Screening and Characterization of

Findings. The finding was screened to Green based on the answers to questions 2 and

3. The resultant leakage from the open PORV would not have caused the current decay

heat removal method to fail if it went undetected and leakage would be self-limiting such

that it would stop before impacting the operating method of decay heat removal.

The finding had a cross-cutting aspect in the Challenge the Unknown component of the

Human Performance area as defined in NRC IMC 0310, because the technicians failed

to recognize that the output was already set to 0, but proceeded anyways to toggle the

output which resulted in setting it to 1 [H.11].

Enforcement: TS 5.7.1.1.a, Procedures, required, in part, that written procedures be

established, implemented, and maintained covering activities related to procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, 1978. Regulatory

Guide 1.33, Section 8, Procedures for Control of Measuring and Test Equipment and for

Surveillance Tests, Procedures, and Calibrations requires procedures for surveillance

tests. Contrary to the above, required surveillance procedure 2-SI-68-86, revision 4,

was not implemented when step 6.2.6 [1.3] was not performed as written. Corrective

actions taken or planned by the licensee include revisions to 2-SI-68-86 to clarify the

16

steps relating to toggling the DCS output, training for the craft, and management

oversight of pre-job briefs. This violation was entered into the CAP as CR 1309345 and

is being treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy.

This violation is identified as NCV 05000391/2017003-03, Failure to Follow a

Surveillance Procedure Led to an Inadvertent Lift of a Pressurizer Power Operated

Relief Valve.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (71114.06)

a. Inspection Scope

On the dates listed below, the inspectors observed a licensee-evaluated emergency

preparedness drill to verify that the emergency response organization was properly

classifying the event in accordance with licensee procedure EPIP-1, Emergency Plan

Classification Flowchart, and making accurate and timely notifications and protective

action recommendations in accordance with EPIP-2, Notification of Unusual Event;

EPIP-3, Alert; EIPIP-4, Site Area Emergency; EPIP-5, General Emergency; and the

Radiological Emergency Plan. In addition, the inspectors verified that licensee

evaluators were identifying deficiencies and properly dispositioning performance against

the performance indicator criteria in Nuclear Energy Institute (NEI) 99-02, Regulatory

Assessment Performance Indicator Guideline. This activity constituted two EP drill

evaluation inspection samples.

  • EP drill on July 17, 2017
  • EP drill on August 16, 2017

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151)

.1 Cornerstone: Mitigating Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the two PIs listed below. To verify the

accuracy of the PI data reported from July 1, 2016 through June 30, 2017. PI definitions

and guidance contained in NEI 99-02, Regulatory Assessment Indicator Guideline,

Revision 7, were used to verify the basis in reporting for each data element.

This activity constituted two performance indicator samples, as defined in IP 71151.

17

  • High Pressure Safety Injection MSPI

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (71152)

.1 Review of Items Entered into the CAP

As required by Inspection Procedure 71152, Problem Identification and Resolution, and

in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a daily screening of items entered into the

licensees CAP. This review was accomplished by reviewing daily condition report (CR)

summary reports and attending daily CR review meetings

.2 Annual Sample: Review of CR 129727, Watts Bar Elevation Letter - Operations

Leadership Formality and Rigor

a. Inspection Scope

The inspectors reviewed CR 1297271, WBN Elevation Letter - Operations Leadership

Formality and Rigor, in detail to evaluate the effectiveness of the licensees corrective

actions intended to address operator performance concerns. The CR was written to

address the continued lack of formality, rigor, and discipline by operators in monitoring

and controlling the plant. The inspectors assessed whether issues were properly

identified, documented accurately and completely, properly classified and prioritized,

adequately considered extent of condition, generic implications, common cause, and

previous occurrences, adequately identified root causes/apparent causes, and identified

appropriate and timely corrective actions. The inspector reviewed processes contained in

the licensees Conduct of Operations procedure (OPDP-1) and CAP (NPG-SPP-22.300).

This activity constituted one sample of in-depth review as defined in IP 71152.

b. Observations and Findings

To address the concerns identified in CR 1297217, the licensee developed a High

Intensity Training (HIT) program. The training was developed to refocus training

personnel and license operators of standards, behaviors and expectations associated

with plant operations. The inspector discussed the licensees HIT program with

members of the licensees training staff, operations management, and licensee

operators during a four day period. During the discussions, the inspector was able to

obtain a clear understanding of why and how HIT was developed.

During the four days of observing HIT activities, the inspectors observed two operating

crews and two crews of evaluators in a training environment. The inspector also

observed classroom training and critiques following each simulator scenario. Many of

18

the training activities were also observed by a member of the licensees corporate

training staff, onsite operations management, a contract third party evaluator, and a peer

evaluator from another utility.

The training sessions were found to be very intense and operational focused. The

evaluators were extremely critical of crew performance. The evaluators took every

opportunity to identify and address concerns. Whenever a concern/issue was identified,

the scenario was stopped and the issues was discussed with the crew. Stopping the

scenario and holding discussions occurred numerous times throughout each scenario.

Following each discussion, the simulator was reset to the desired point and reran. The

discussions were very interactive. During the discussions, the evaluators constantly

focused on procedural requirement and licensee expectations. The evaluators were

often challenged/questioned by crew members. The evaluators adequately addressed

each question or concern identified by the crew. The inspector also observed critiques

following scenarios.

From the inspectors observation it was clear that HIT was designed to address

operational performance issues identified in the CR. The effectiveness of HIT can only

be evaluated by observing operator and plant performance over time. The inspectors

concluded that the training provided during HIT, if embraced, should decrease lack of

formality, increase rigor, and improve discipline by operators in monitoring and

controlling the plant. The HIT would also be expected to improve operators

implementation of standards outlined in OPDP-1, Conduct of Operations. The

inspectors will continue to monitor operator and plant performance in the control room,

during actual plant events and in licensed operator simulator training, as required by the

baseline inspection program. No findings were identified.

.3 Semiannual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

review was focused on trends in risk management, long-standing minor equipment

deficiencies, housekeeping, TS compliance, corrective action screening and condition

adverse to quality documentation.

b. Observations and Findings

No findings were identified. The inspectors had several observations regarding the

trends listed above. Regarding risk management, the inspectors noted that the

environmental factor for the equipment out of service computer program (EOOS) was

not consistently adjusted per procedure to reflect activities in the plant switchyard. This

was initially identified to the licensee in 2016. The condition report written at that time

documented the issue as an NRC question, rather than a failure to follow the EOOS

procedure, and the corrective action was to respond to the NRC to ensure that their

question was answered, rather than address procedure non-compliance. The inspectors

re-visited this with the licensee when they observed switchyard work in progress without

19

the environmental factor setting in EOOS being per procedure. This time the licensee

properly characterized the issue as procedure non-compliance in their CAP. The

inspectors used the EOOS test module and verified that risk remained GREEN during

instances when the environmental factor adjustment was not properly set. The

inspectors noted that, for the work performed when the environmental factor was not

properly set, the licensee did implement physical risk mitigation controls at the work sites

that were in accordance with the appropriate work management procedures.

The inspectors also noted a trend in long-standing equipment issues eventually

becoming either operator distractions or worse conditions. In one instance valve leakby

in the chemical volume and control system gave erroneous indication that the reactor

coolant system was either being borated or diluted. This required the operating crew to

enter procedures to then verify that the RCS truly was neither borated nor diluted. In

another instance, known leakage on the 1A high pressure fire pump shaft seal worsened

to the point that protective measures had to be taken to shield water spray from the

power supply conduit of the pump.

Since the completion of Unit 2 construction, the inspectors noted a reduction in the

amount of temporary equipment stored in the plant auxiliary building and general

housekeeping improvements in the auxiliary building. CAP review during the first and

second quarter of 2017 showed a more aggressive approach by the license in improving

housekeeping and removing lingering temporary equipment. Documents reviewed show

that the licensee accomplished this through frequent health and safety walkdowns and

challenging temporary equipment tags that were out of date. The inspectors observed

the results of these efforts in their routine walkdowns of risk-significant areas.

Specifically, in regards to a large scaffold storage area near the Unit 2 713 level

penetration. Although temporary equipment tags were present and up to date, the area

appeared to have become a convenient location to temporarily store a wide variety of

items beyond scaffolding. The licensee identified this in their CAP and then completely

removed all of the items stored in the area.

The inspectors also identified negative trends in the treatment of C-level CRs in the CAP

and with TS compliance issues. Inspectors identified multiple C-level CRs during the

inspection period that exhibited one of the following issues: inadequate documented

condition details; inadequate screening of conditions adverse to quality (CAQs) to

non-CAQ status; and failure to promptly identify CAQs. Inspectors also noted several

examples of issues with TS compliance and proper TS application during the inspection

period. The licensee has identified these issues in their CAP.

4OA3 Event Followup (71153)

.1 (Closed) Licensee Event Report (LER) 05000390, 391/2016-010-00, Emergency Diesel

Generator Crankcase Pressure Switches Not Analyzed to Withstand the Effects of a

Tornado

A condition involving the potential impact of a tornado on the EDGs was identified during

an NRC Component Design Basis lnspection at the Sequoyah Nuclear Plant. The EDGs

were designed with a crankcase pressure trip setpoint of approximately one inch of

water which is bypassed during an emergency start. A tornado could potentially induce

20

a pressure spike which could cause actuation of the crankcase pressure trip due to

different vent paths between the EDG room and the EDG crankcase. Actuation of the

crankcase pressure trip would energize the shutdown relay causing an EDG lockout

condition. The EDG lockout condition would prevent all EDG starts until operators

manually reset the lockout condition. Because the EDGs at Watts Bar were essentially

identical designs, this condition was reviewed for applicability to Watts Bar. The

licensee determined this condition placed both units in an unanalyzed condition that

could have potentially affected all four EDGs simultaneously. This was a legacy EDG

protective logic circuitry design that did not anticipate the interaction between the

crankcase pressure trip and the outside atmospheric pressure spike during a tornado.

This condition was documented in the licensee CAP as CR 1179264. A compensatory

action was established of starting the EDGs in the emergency mode when notified of a

Tornado Warning and ran while the Tornado Warning was in effect ensuring the EDGs

would be available to perform their required safety function. The licensee also

implemented DCN 66376 to remove the sealin function of the crankcase differential

pressure switches and retain the alarm function of the switches for all four EDGs. This

LER was reviewed by the inspectors. A licensee-identified violation is documented in

Section 4OA7.

.2 (Closed) LER 05000390/2016-001-00, Channel Mode Switch in Incorrect Position

Renders Lower Containment Atmosphere Particulate Radiation Monitor Inoperable.

a. Inspection Scope

On January 12, 2016, at 1645 Eastern Standard Time (EST), Watts Bar Nuclear Plant

(WBN) Maintenance personnel were performing a 92 day channel operational test for

radiation monitor 1-RM-90-1064, Lower Containment Atmosphere Particulate Radiation

Monitor, and found the mode switch in the "DlFF" position, which was not expected. The

surveillance was stopped and an investigation was conducted. It was determined that

the design required the mode switch to be in the "lNT" position to be operable. The

mode selector switch was placed in the "lNT" position and the surveillance was

completed. The radiation monitor was restored to OPERABLE status at 1743 EST on

January 12, 2016. Placing the mode selector switch in the "DlFF" position resulted in 1-

RM-90-1064 being INOPERABLE due to the loss of alarm function of the monitor.

Investigation determined that the switch had been repositioned on December 8, 2015.

Because the containment particulate radiation monitor was inoperable for a period of

time greater than permitted by TS 3.4.15, this condition was reportable as an operation

or condition prohibited by TS per 10 CFR 50.73(a)(2)(i)(B). During the time the monitor

was inoperable, other means of leak detection (e.g., containment pocket sump level

indication, reactor coolant system inventory balance) remained available. This LER was

reviewed by the inspectors. No additional findings or violations of NRC requirements

were identified.

.3 (Closed) LER 05000390/2016-005-00, Both Trains of Unit 1 Emergency Gas Treatment

System Inoperable During Unit 2 Testing

21

On March 14, 2016, Watts Bar Nuclear Plant (WBN) Unit 1 determined through

engineering analysis that both trains of emergency gas treatment system (EGTS) were

inoperable for 8 minutes, 10 seconds during preoperational testing of Unit 2 EGTS. The

inoperability of A and B trains of Unit 1 EGTS took place on October 22, 2015, while

Unit 1 was in Mode 1 and two trains of EGTS were required to be operable in

accordance with TS LCO 3.6.9, "Emergency Gas Treatment System (EGTS). At the

time of the event, Unit 2 was in "no mode," prior to initial fuel loading. With both trains of

EGTS inoperable, the specified safety functions of Unit 1 EGTS were not capable of

being performed. Therefore, this condition was reported pursuant to

10 CFR 50.73(a)(2)(v)(C) and 10 CFR 50.73(a)(2)(v)(D), "Event or Condition That Could

Have Prevented Fulfilment of a Safety Function." This LER was reviewed by the

inspectors. No additional findings or violations of NRC requirements were identified.

.4 (Closed) LER 05000390/2016-004-00, Automatic Reactor Trip Due to Actuation of Over

Temperature Delta Temperature Bistables

On March 22, 2016, at 1131, Watts Bar Nuclear Plant Unit 1 experienced an automatic reactor trip. The initiating reactor trip first out received was 76-C Over-temperature Delta

T. The turbine trip first out received was 73-C Rx Trip Breakers RTA and BYA Open.

Prior to the unit trip, Unit 1 was in Mode 1 at 100 percent power. Concurrent with the

reactor trip, the auxiliary feedwater system actuated. All control rods inserted upon the

reactor trip and safety systems functioned as expected. This LER was reviewed by the

inspectors. No additional findings or violations of NRC requirements were identified.

.5 (Closed) LER 05000390/2016-006-00, Undersized Room Cooler Fan Shaft Results in

Loss of Centrifugal Charging Pump

On May 13, 2016, Watts Bar Unit 1 determined that a condition prohibited by TSs had

previously occurred. During the Fall 2015 outage, maintenance performed on the 1B-B

centrifugal charging pump (CCP) room cooling fan introduced a condition that resulted in

a subsequent bearing failure of the room cooling fan. This condition would have

prevented the 1B-B CCP pump from performing its function for its designed mission

time. Based on the reduced reliability of the fan, the 1B-B CCP was considered to be

inoperable from October 7, 2015, until the fan was repaired and returned to service on

December 6, 2015. During this time, there were several short periods when the 1A-A

CCP was also inoperable. A NCV for this condition was documented in NRC Inspection

Report 05000390, 391/2016002-02. The LER was reviewed by the inspectors. No

additional findings or violations of NRC requirements were identified.

.6 (Closed) LER 05000390/2016-011-00, Loss of Centrifugal Charging Pump Due to

Repeat Failure of Associated Room Cooler

On August 3, 2016, Wafts Bar Nuclear Plant Unit 1 (WBN1) determined that a condition

prohibited by TS had previously occurred. During maintenance of the 1B-B CCP room

cooler, the bearing was found in a degraded condition requiring repair. This fan was

required to support Operability of the 1B-B CCP. The fan had been previously repaired

on December 6, 2015, and had less than 100 days of operation since its overhaul. The

22

mission time of the CCPs is specified in design documents as 100 days. Based on the

inability of the CCP to meet its mission time, the 1B-B CCP was considered to be design

inoperable since its overhaul on December 6, 2015. This represents a condition

prohibited by TS for the 1B-B CCP being inoperable for greater than its allowed outage

time. The LER was reviewed by the inspectors. No findings or violations of NRC

requirements were identified.

4OA5

.1 IP 93100 Safety-Conscious Work Environment Issue of Concern Follow Up

a. Inspection Scope

The inspectors assessed the TVA Nuclear corporate safety-conscious work

environment (SCWE) by conducting safety culture interviews of individuals from the

engineering, licensing, and operations groups. Inspectors interviewed a total of 22

individuals to determine if indications of a chilled work environment exist, employees are

reluctant to raise safety and regulatory issues, and employees are being discouraged

from raising safety or regulatory issues. Information gathered during the interviews was

used in aggregate to assess the work environment at TVA Nuclear corporate.

b. Assessment

Based on the interviews conducted, the inspectors determined that licensee

management emphasized the need for all employees to identify and report problems

using the appropriate methods established within the administrative programs, including

the CAP and Employee Concerns Program. These methods were readily accessible to

all employees. Based on discussions conducted with a sample of employees from

various departments, the inspectors determined that employees felt free to raise safety

and regulatory issues, and that management encouraged employees to place issues into

the CAP for resolution. The inspectors did not identify any reluctance on the part of the

licensee staff to report safety concerns.

4OA6 Meetings, including Exit

On October 25, 2017 and November 8, 2017, the resident inspectors presented the

inspection results to members of the licensee staff. The inspectors confirmed that none

of the potential report input discussed was considered proprietary.

4OA7 Licensee-Identified Violations

The following licensee-identified violations of NRC requirements were determined to be

of very low safety significance and met the NRC Enforcement Policy criteria for being

dispositioned as NCVs.

procedures be established, implemented, and maintained covering activities

related to procedures recommended in Regulatory Guide 1.33, Revision 2,

Appendix A, 1978. Regulatory Guide 1.33, Revision 2, Appendix A, Section 6,

23

Procedures for Combating Emergencies and Other Significant Events requires

procedures for a reactor trip. Contrary to the above, from May 23, 2016, until

July 16, 2017, procedure 2-E-0, Revision 5, Reactor Trip and Safety Injection, was

not maintained which resulted in a condition where CCS Heat Exchanger B

(ERCW/CCS Train 2A) would not have been able to remove sufficient heat during

sump recirculation following a LOCA on Unit 2 for approximately 75 days. This

condition was caused by the licensees failure to implement ERCW system

DCN 62151 as written. A detailed risk evaluation was performed using SAPHIRE

Version 8.1.5 and Version 8.50 of the SPAR Model for both units combined. The

result was less that 1E-6/year for Unit 2, which would be a finding of very low

significance (Green). This violation was entered in to the licensees CAP as

CR 1316395.

established, implemented, and maintained covering the applicable procedures in

Regulatory Guide 1.33 Rev. 2, Appendix A, February 1978. Procedures for locking

and tagging are applicable procedures under REG GUIDE 1.33 Appendix A, 1.c

Equipment Control. Contrary to this requirement, Step 3.2.4.M of procedure

NPG-SPP-10.2, Clearance Procedure to Safely Control Energy, Revision 18 was

not followed when nitrogen supply isolation valves 2-ISIV-1-408L and

2-ISIV-1-408M and isolation valves 2-ISIV-1-405L and 2-ISIV-1-405M were closed

and tagged but not documented as tagged in the Electronic Shift Operations

Management System (eSOMS). As a result, the valves remained closed resulting

in the inability to operate the Unit 2 SG#1 and #2 PORVs using back-up nitrogen.

The finding was determined to be Green because having the nitrogen supply to

two out of four steam generator PORVs isolated only affects the ability to achieve

and maintain cold shutdown. The licensee documented this violation as

CR 1303309.

testing program to demonstrate that quality related SSCs will perform satisfactorily

in service and performed in accordance with written test procedures. Contrary to

the above, from at least 2010 until July 2017, various safety-related valves were

unacceptably preconditioned prior to required as-found testing. This finding was of

very low safety significance (Green) because the finding did not represent an

actual loss of function of a single train for greater than its TS allowed outage time.

The licensee documented this violation as CRs 1276605, 1316712, 1319298,

1319304.

measures shall be established for the selection and review for suitability of

application of materials, parts, equipment, and processes that are essential to the

safety-related functions of SSCs. Contrary to the above, for at least the past

twenty years, the licensee failed to assess the effects of a tornado on the

crankcase over-pressure trip which could prevent EDGs from fulfilling their

safety-related function. A regional senior reactor analyst performed a detailed risk

evaluation and determined the dominant accident sequences involved a

weather-related loss of offsite power with all four EDGs failing due to the

24

performance deficiency and the operators recovering one of the failed EDGs. The

risk of this performance deficiency was not greater than Green due to the low

frequency of tornados/high winds and the potential for operator recovery. The

licensee documented this violation as CR 117926.

  • Technical Specification LCO 3.6.3, Containment Isolation Valves, required that each

containment isolation valve shall be operable in modes 1, 2, 3, and 4. TS Required

Action statement A.1 required that the affected penetration flow path be isolated,

and Required Action A.2, directed that the penetration flow path is verified to be

isolated once per 31 days. Contrary to the above, on May 18, 2017, containment

isolation valve 1-FCV-31-330 was tagged closed for maintenance; however no

verification that the flow path was isolated was performed until August 23, 2017.

This finding was of very low safety-significance (Green) because it did not represent

an actual open pathway in the physical integrity of reactor containment and was not

related to hydrogen ignitors. The licensee documented this violation as

CR 1331287.

  • Unit 1 Operating License condition 2.F required, in part, that TVA shall implement

and maintain in effect all provisions of the approved Fire Protection Program. The

Fire Protection Report was developed to ensure compliance with the requirements of

this licensee condition. Fire Protection Report, Part II, is the Fire Protection Plan

(FPP). FPP Subsection 14.10, Fire Safe Shutdown Equipment, required

nonfunctional equipment listed in Table 14.10 be restored to its functional status

within 30 days. If this 30 day requirement cannot be met, then the equipment be

placed in its fire safe shutdown (FSSD) position. Contrary to the above, during a

surveillance on June 10, 2017, backdraft damper 0-BKD-31-592, equipment listed in

Table 14.10, was identified as not being able to achieve its FSSD position. However,

actions to place the damper in its FSSD position were not taken until July 11, 2017.

This finding was of very low safety significance because there was a fully functional

automatic suppression system on either side of the fire barrier. This violation was

documented as CR 1316058.

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

G. Arent, Director, WBN Site Licensing

M. Casner, Director, Engineering

L. Cross, Manager, Electrical Systems

T. Detchemendy, Manager, Site Emergency Preparedness

E. Ellis, Senior Manager, Nuclear Site Security

D. Erb, Operations Director

K. Hulvey, Watts Bar Licensing Manager

J. James, Director, Maintenance

B. Jenkins, Director, Plant Support

T. Marshall, Plant Manager

C. Rice, Operations Superintendent

P. Simmons, Site Vice President

A. White, Senior Manager, Site Quality Assurance

Attachment

LIST OF REPORT ITEMS

Opened and Closed

NCV 05000390, 391/2017003-01 Failure to Maintain Procedures for Response to a

Loss of Coolant Accident (Section 1R15.1)

NCV 05000391, 390/2017003-02 Inadequate Procedure for Unit Cooldown from Hot

Standby to Cold Shutdown (Section 1R15.2)

NCV 05000391/2017003-03 Failure to Follow a Surveillance Procedure Led to

an Inadvertent Lift of a Pressurizer Power Operated

Relief Valve (Section 1R22)

Closed

LER 05000390, 391/2016-010-00 Emergency Diesel Generator Crankcase Pressure

Switches Not Analyzed to Withstand the Effects of

a Tornado (Section 4OA3.1)

LER 05000390/2016-001-00 Channel Mode Switch in Incorrect Position Renders

Lower Containment Atmosphere Particulate

Radiation Monitor Inoperable (Section 4OA3.2)

LER 05000390/2016-005-00 Both Trains of Unit 1 Emergency Gas Treatment

System inoperable During Unit 2 Testing (Section

4OA3.3)

LER 05000390/2016-004-00 Automatic Reactor Trip Due to Actuation of Over

Temperature Delta Temperature Bistables (Section

4OA3.4)

LER 05000390/2016-006-00 Undersized Room Cooler Fan Shaft Results in Loss

of Centrifugal Charging Pump (Section 4OA3.5)

LER 05000390/2016-011-00 Loss of Centrifugal Charging Pump Due to

Repeat Failure of Associated Room Cooler

(Section 4OA3.6)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

0-MI-17.003, Flood Mode Preparation Storage Locations and Periodic Inventory, Rev. 0012

0-TI-444, External Flood Protection Program, Rev. 0003

Section 1R04: Equipment Alignment

Procedures

2-SI-63-8, ECCS Valve Alignment Verification, Rev. 0002

2-SI-3-130, AFW Valve Alignment Verification, Rev. 0004

2-SOI-63.01 ATT 1V, Safety Injection System, Rev. 0005

2-SI-70-1, Component Cooling System, Safety-Related Valves: Alignment Verification, Rev.

0004

2-SOI-72.01, Containment Spray System, Rev. 0005

2-SOI-72.01 Containment Spray System Valve Checklist 2-71.01V, ATT 1V, Rev. 0001

0-SOI-82.03, Diesel Generator (DG) 2A-A, Rev. 0012

0-SOI-82.03, Diesel Generator 2A-A Power Checklist 82.03-1P, ATT 1P, Rev. 0000

0-SOI-82.03, Diesel Generator 2A-A Valve Checklist 82.03-1V, ATT 1V, Rev. 0010

0-SOI-67.01, Essential Raw Cooling Water System Supply Header 1A Valve Alignment

Checklist 0-67.01-3V, ATT 3V, Rev. 0017

0-PI-OPS-17.0, 18 Month Locked Valve Verification, Rev. 0082

0-TI-31.08, Flow Balancing Valves Setpoint Positions, Rev. 0003

0-SOI-82.04, Diesel Generator (DG) 2B-B, Rev. 0010

0-SOI-82.04. Diesel Generator 2B-B Power Checklist 82.04-1P, ATT 1P, Rev. 0000

0-SOI-82.04, Diesel Generator 2B-B Valve Checklist 82.04-1V, ATT 1V, Rev. 0010

0-SOI-67.01, Essential Raw Cooling Water System Supply Header 1B Valve Alignment

Checklist 0-67.01-4V, ATT 4V, Rev. 0017

Section 1R05: Fire Protection

CRs 1262925, 1343002

Fire Protection Report, Part VI - Fire Hazards Analysis, Rev. 52

WBN-Prefire Plan, AUX-0-692-01, Rev. 4

WBN-Prefire Plan, AUX-0-692-02, Rev. 3

Drawing 47A472-1

Drawing 47W866-11

Drawing 47W920-2

Drawing 47A381-20

Drawing 47A381-127

WBN Prefire Plan AUX-0-713-01, Rev. 1

WBN Prefire Plan AUX-0-713-02, Rev. 3

WBN Prefire Plan AUX-0-713-03, Rev. 4

WBN Prefire Plan CON-0-729-01, Rev. 2

WBN Prefire Plan AUX-0-676-01, Rev. 3

4

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

0-TI-12.16, Diesel Generator Outage T/S or SR Contingency Actions, Rev. 0005

WO 118934650

0-SI-82-2, 8 Hour Diesel Generator AC Power Source Operability Verification, Rev. 0025

WO 118928550

CRs 1727208, 1327472

NPG-SPP-09.11.1, Equipment Out of Service Management, Rev. 0012

NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 0021

PWR operational risk review - red sheet for WO 118819797, Hose replacement on Unit 1 main

turbine electro-hydraulic control

High risk management plan for WO 119013421, Freeze seal for isolation of valve, dated 9/7/17

Section 1R15: Operability Determinations and Functionality Assessments

WOs 118882781, 113861046, 113860919, 118991891

WBN-SDD-N3-85-4003, Control Rod Drive System, Rev. 15

WBN-SDD-N3-99-4003, Reactor Protection System, Rev. 24

Drawings 1082H70-6, Rev. N; 1082H70, Rev. AK; 1082H70-17, Rev. AF

Operational Decision-Making Issue Evaluation Document, dated July 22, 2017

Drawing 2-47W880-4, Rev. 0

0-PI-OPS-17.0, 18 Month Locked Valve Verification, Rev. 0081

N3-67-4002, Essential Raw Cooling Water System

1-E-1, Loss of Reactor or Secondary Coolant, Rev. 0009

WBN-SDD-N3-67-4002, Essential Raw Cooling Water System, System 67, Rev. 0035

0-TI-31.08, Flow Balancing Valves Setpoint Positions, Rev. 0003

0-TI-12.11, Emergency Operating Instruction (EOI) Control, Rev. 0001

TI-78, Lubrication Program, Rev. 0011

NPG-SPP-07.3, Work Activity Risk Management Process, Rev. 0009

WB-DC-40-64, Design Basis Events Design Criteria

Westinghouse STS, B 3.8.3, Diesel Fuel Oil, Lube Oil, and Starting Air, Rev. 4.0

0-SOI-82.01, Diesel Generator (DG) 1A-A, Rev. 0009

WBN-VTD-P318-0020, Instructions for EMD Lubricating Oil System

Section 1R19: Post Maintenance Testing

CR 1325844

2-SI-68-114, 184 Day Channel Operational Test RCS Flow Loop 1 Channel III Loop 2-LPF-68-

6D (F-416), Rev. 0003

WO 118921021

2-IMI-99.100, EAGLE 21 Rack Diagnostics, Rev. 0002

WO 117829913

1-SI-30-901-A, Valve Full Stroke Exercising During Plant Operation - Ventilation (Train A), Rev.

0017

PM 600124762

Drawing 1-47W866-1, Rev. 68

5

Section 1R22: Surveillance Testing

WOs 118628055, 116153069

CRs 1322136, 1276914, 1314124, 1314688, 1309892, 1309602, 1309207

0-SOI-82.03, Diesel Generator (DG) 2A-A, Rev. 0010

2-SI-67-908-B, Valve Full Stroke Exercising and Position Indication Verification During Cold SD

- ERCW (Train 2B), Rev. 0003

2-SI-67-908-B, Valve Full Stroke Exercising and Position Indication Verification During Cold SD

- ERCW (Train 2B), Rev. 0004

2-SI-67-908-B, Valve Full Stroke Exercising and Position Indication Verification During Cold SD

- ERCW (Train 2B), Rev. 0005

1EP6: EP Drill Evaluation

Controllers package for July 17, 2017, training drill dated 7/17/17

CRs 1319059, 1318956, 1318824, 1318834, 1319057, 1318822, 1318830, and 1318823

Section 4OA3: Followup of Events and Notices of Enforcement Discretion

Documentation of Information Sharing - Title: Radiation Meter 1-RM-90-106A

Design Change Notice #66212, Rev. A for Equipment: Various/System 65 (Emergency Gas

Treatment System) to revise SDD N3-65-4001 to Incorporate Test Requirements,

dated: 2/11/2016

CR 11430756 Level 2 Evaluation Action 007 dated: 07/15/2016

Past Operability Evaluation Documentation for CR 1143076 signed on 3/10/2016.

Routine WO 117688915, Equipment Description: EH Fluid Display Subpanel, Unit 1 Reactor

Trip. Dated: 3/22/2016.

Level 2 Evaluation - CR Number 1152462, Rev 0 dated 4/26/2016.

NPG Technical Pre-Job Briefing Checklist AEC CR1152462 dated 3/31/2016

TVA Corrective Action 1152462-006 Completed 12/21/2016.

TVA Condition Report 1152462 draft: 03/22/2016 Unit 1 Reactor Trip

Operations Log for 8/17/2017