IR 05000390/2021011

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Triennial Fire Protection Inspection Report 05000390/2021011 and 05000391/2021011
ML21103A254
Person / Time
Site: Watts Bar  Tennessee Valley Authority icon.png
Issue date: 04/13/2021
From: Scott Shaeffer
Division of Reactor Safety II
To: Jim Barstow
Tennessee Valley Authority
References
IR 2021011
Download: ML21103A254 (20)


Text

April 13, 2021

SUBJECT:

WATTS BAR - TRIENNIAL FIRE PROTECTION INSPECTION REPORT 05000390/2021011 AND 05000391/2021011

Dear Mr. Barstow:

On February 25, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Watts Bar and discussed the results of this inspection with Mr. Anthony Williams and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. Two of these findings involved violations of NRC requirements. We are treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Watts Bar.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC Resident Inspector at Watts Bar. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Scott M. Shaeffer, Chief Engineering Branch 2 Division of Reactor Safety Docket Nos. 05000390 and 05000391 License Nos. NPF-90 and NPF-96

Enclosure:

As stated

Inspection Report

Docket Numbers: 05000390 and 05000391 License Numbers: NPF-90 and NPF-96 Report Numbers: 05000390/2021011 and 05000391/2021011 Enterprise Identifier: I-2021-011-0033 Licensee: Tennessee Valley Authority Facility: Watts Bar Location: Spring City, TN Inspection Dates: February 01, 2021 to February 25, 2021 Inspectors: J. Dymek, Reactor Inspector W. Monk, Senior Reactor Inspector J. Montgomery, Senior Reactor Inspector D. Strickland, Reactor Inspector Approved By: Scott M. Shaeffer, Chief Engineering Branch 2 Division of Reactor Safety Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a triennial fire protection inspection at Watts Bar, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Inadequate Sprinkler System Surveillance Requirement - Heavy Loading on 480V Transformer Rooms Sprinkler Heads Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green [H.1] - 71111.21N.

Systems NCV 05000390,05000391/2021011-01 Resources 05 Open/Closed The inspectors identified a Green finding and associated Non-cited violation (NCV) of Watts Bar Nuclear Plant Technical Specifications (TS) 5.7.1.1 when the licensee failed to properly establish and/or follow surveillance procedures for inspection of credited fire suppression systems.

Inadequate Fire Safe Shutdown Analysis for FZ 737.0-A3 Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green None (NPP) 71111.21N.

Systems NCV 05000390/2021011-02 05 Open/Closed The inspectors identified a Green finding and associated Non-cited violation (NCV) of Watts Bar Nuclear Plant Unit 1 Operating License Condition 2.F when the licensee failed to provide an adequate 10 CFR Part 50, Appendix R Fire Safe Shutdown (FSSD) evaluation.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.21N.05 - Fire Protection Team Inspection (FPTI) Structures, Systems, and Components (SSCs) Credited for Fire Prevention, Detection, Suppression, or Post-Fire Safe Shutdown Review (IP Section 03.01)

The inspectors verified that components and/or systems will function as required to support the credited functions stated for each sample. Additional inspection considerations are located in the fire hazards analysis (FHA) or safe shutdown analysis (SSA).

(1) a. Review deficiencies or open fire protection impairments for the selected system, including any temporary modifications, operator workarounds, or compensatory measures.

b. Verify that operator actions can be accomplished as assumed in the licensees FHA, or as assumed in the licensees fire probabilistic risk assessment (FPRA)analysis and SSA.

c. Review repetitive or similar maintenance work requests which could be an indicator of a design deficiency and could affect the ability of the components to perform their functions, when needed.

d. Ensure that post maintenance and/or surveillance activities are performed as scheduled.

e. Perform a walkdown inspection to identify equipment alignment discrepancies.

Inspect for deficient conditions such as corrosion, missing fasteners, cracks, and degraded insulation.

f. Ensure the selected SSCs that are subject to aging management review (AMR)pursuant to 10 CFR Part 54 are being managed for aging (e.g., loss of material, cracking, reduction of heat transfer) in accordance with appropriate aging management programs. Verify that the licensees aging management program activities (such as, Fuel Oil Analysis or Selective Leaching Aging Management Program) associated with FP equipment are being implemented.

g. If a review of operating experience issues will be completed for the selected inspection sample, verify that the licensee adequately reviewed and dispositioned the operating experience in accordance with their processes.

The team selected the following SSCs as samples:

  • Automatic Preaction Sprinkler System in room 772.0-A2 (480V Board Room 1B)

(2)

  • CO2 Suppression System in room 708.0-C1 (Unit 1 Auxiliary Instrument Room)

(3)

  • Unit 1 Component Cooling Water System (CCS)

(4)

  • Unit 1 480VAC Shutdown Power System

Fire Protection Program Administrative Controls (IP Section 03.02) (1 Sample)

The inspectors verified that the following fire protection program administrative control was implemented in accordance with the licensees current licensing basis. The inspectors ensured that the licensees FPP contained adequate procedures to implement the selected administrative control. The team also verified that the selected administrative control met the requirements of all committed industry standards.

(1)

  • Fire Brigade Training Program

Fire Protection Program Changes/Modifications (IP Section 03.03) (2 Samples)

The inspectors reviewed the following changes to ensure that they did not constitute an adverse effect on the ability to safely shutdown post-fire, to verify that fire protection program documents and procedures affected by the changes were updated, and to verify that post-fire SSD operating procedures, such as abnormal operating procedures, affected by the modification were updated:

(1)

  • RIS 2005-07 evaluation for CR 1574031, 2-FCV-1-109 Failure

INSPECTION RESULTS

Inadequate Sprinkler System Surveillance Requirement - Heavy Loading on 480V Transformer Rooms Sprinkler Heads Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green [H.1] - 71111.21N.0 Systems NCV 05000390,05000391/2021011-01 Resources 5 Open/Closed The inspectors identified a Green finding and associated Non-cited violation (NCV) of Watts Bar Nuclear Plant Technical Specifications (TS) 5.7.1.1 when the licensee failed to properly establish and/or follow surveillance procedures for inspection of credited fire suppression systems.

Description:

During walk downs of the 480V Transformer Rooms, NRC inspectors identified thick dust accumulation present on the majority of the sprinkler heads above and surrounding each 480V transformer. Above each of the 480V transformers are large air vents that expel air from the rooms to the outside. These large air vents contribute to a high air flow in the area that results in dust and particulate matter being moved throughout the space, and some of this dust and particulate matter landing on the sprinkler heads. The physical presence of the dust accumulation created two concerns. First, the thermal insulating effect of the dust surrounding the heads fusible link could impact the response time index (RTI) of the sprinkler head by delaying the time required for the link to heat up to the designed melting temperature to allow water to be released from the head. Second, the loading on the heads could impede the ability of the licensee to visually verify the acceptance criteria of the surveillance requirement.

Functionality of this sprinkler system was verified using procedure 0-FOR-26-3, 18 Month Inspection of Fire Protection Sprinkler Systems in Accessible Safety-Related Areas. The procedure visually checks for signs of corrosion, paint, and physical damage of the heads. Thick dust accumulation on the sprinkler heads created a material condition deficiency that impeded the ability to visibly verify the acceptance criteria of the surveillance. The procedure was not properly established because no specific steps, acceptance criteria, nor inspection guidance was provided to ensure that sprinkler heads were free of loading of foreign materials, or, the procedure was not adequately followed. The surveillances acceptance criteria could not be met because the sprinkler heads were coated in a thick layer of dust/debris, which prevented the licensee staff from visually verifying the acceptance criteria of the surveillance requirement.

Most likely, the dust coating on the sprinkler heads had been present for a significant time period, and present during the last performance of the surveillance. The last two surveillances were completed in August 2019 and April 2018 with no sprinkler head issues of concern noted.

Corrective Actions: The licensee took actions to clean the fire suppression sprinkler heads in the 480V Transformer Rooms by compressed air to remove the heavy loading condition.

Additionally, extent of condition walkdowns were performed by the licensee to check the plants other fire suppression systems for this heavy loading material condition deficiency. An additional CR was generated by the licensee in order to correct dust loading issues on the Unit 1 Air Intake Rooms sprinkler heads.

The licensee also wrote a CR to revise surveillance procedure 0-FOR-26-3 to provide additional guidance for the acceptance criteria to ensure sprinkler heads are free of debris, obstructions, dust accumulation, etc. and that the fusible link elements within the sprinkler heads are physically visible to allow verification of the surveillances acceptance criteria.

Corrective Action References: CR 1669215, Sprinkler Heads Need to be Cleaned in 480V Transformer Rooms, 2/4/2021; CR 1670295, Impaired Sprinkler Heads in 480V Transformer Rooms, 2/9/2021; CR 1671391, During 0-TI-211 Walkdown in the U-1 Air Intake Rooms EL.737, 2/14/2021; CR 1671940, 2021 TFPI Dust on Sprinkler Head in 480V Transformer Room 1A, 2/16/2021; CR 1674388, 2021 TFPI - Enhancement Needed to 0-FOR-26-3, 2/25/2021

Performance Assessment:

Performance Deficiency: The licensee's failure to properly establish and/or follow surveillance procedures for inspection of credited fire suppression systems was a performance deficiency. Specifically, surveillance test procedure 0-FOR-26-3 did not contain specific steps, acceptance criteria, nor inspection guidance to ensure that sprinkler heads were free of loading of foreign materials.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Procedure Quality attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the surveillance procedure used by plant staff to inspect the sprinkler heads lacked sufficient detail and inspection guidance to ensure all relevant as-found material conditions would be considered and evaluated to meet the licensees Fire Protection Plan (FPP) testing and inspection requirement 14.3.d, which could increase the likelihood of a sprinkler system becoming degraded or nonfunctional to respond to a fire initiating event.

Significance: The inspectors assessed the significance of the finding using Appendix F, Fire Protection and Post - Fire Safe Shutdown SDP. Using IMC 0609, Appendix F, Fire Protection SDP the inspectors screened this issue as Green, because the inspectors determined the PD constituted low degradation of the fire suppression system. This low degradation is based on the fact that the fire protection sprinkler heads were not obstructed by the loading to the point of limiting water flow through the heads, but the sprinkler heads would have been delayed in the activation time for the water to begin flowing due to the heavy loading impacting the fusible links response time index (RTI). Additionally, in considering quantitative risk insights, given the circumstances of a fire in the affected areas, the Phase 2 SDP would give no credit for the suppression systems, even if they were fully functional and non-degraded. Therefore, the safety significance of this violation screens to Green, very low safety significance.

Cross-Cutting Aspect: H.1 - Resources: Leaders ensure that personnel, equipment, procedures, and other resources are available and adequate to support nuclear safety.

Specifically, leaders did not ensure adequate surveillance procedures and other resources, such as proper training for completing sprinkler head surveillances and specifically detailing the physical conditions which constitute adequate sprinkler head acceptance criteria.

Enforcement:

Violation: Watts Bar Nuclear Plant Technical Specifications Section 5.7.1.1 states that written procedures shall be established, implemented, and maintained covering fire protection program implementation.

Contrary to the above, the licensee failed to establish and implement adequate procedures covering fire protection program implementation. Specifically, procedure 0-FOR-26-3 was not properly established due to no specific steps, criteria, or guidance being given to ensure that sprinkler heads were free of loading of foreign materials. This resulted in sprinkler heads in the 1A, 1B, and 2B 480V Transformer Rooms containing a significant amount of loading of foreign material that was not discovered during the required surveillance -last completed in August 2019 and April 2018 with no sprinkler head problems noted.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Inadequate Fire Safe Shutdown Analysis for FZ 737.0-A3 Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green None (NPP) 71111.21N.0 Systems NCV 05000390/2021011-02 5 Open/Closed The inspectors identified a Green finding and associated Non-cited violation (NCV) of Watts Bar Nuclear Plant Unit 1 Operating License Condition 2.F when the licensee failed to provide an adequate 10 CFR Part 50, Appendix R Fire Safe Shutdown (FSSD) evaluation.

Description:

On February 16, 2021, the NRC inspectors walked down the credited fire protection wrap of the Component Cooling System (CCS) Pump 1-B power cables 1PL4742B

& 1PL4743B inside the Unit 1 Heat and Vent Room (FZ 737.0-A3) and identified that the 480Vac power cables for CCS Pump 1-B were not fire wrapped for the entirety of the room as stated and analyzed in the sites Fire Safe Shutdown Analysis (SSA) for Analysis Volume (AV) 39, which corresponds with FZ 737.0-A3. For CCS pump 1B-B, the SSA stated, Cables (1PL4742B & 1PL4743B) for CCS pump 1B-B (1-MTR-70-38-B) are being protected. Cables 1PL4742B, 1PL4743B are wrapped in FZ 737-A3. When inspectors viewed these cables in FZ 737-A3, they found an approximate 10-foot section of the conduits containing the power cables that was not fire wrapped from the rooms West wall, over the walkway, and then to Junction Box 4981 on the opposite side wall.

This credited cable wrap was installed as a part of DCN 52033, which commenced in 2006.

This DCN included numerous physical plant modifications and calculation changes to address fire protection issues. Inspectors determined that the DCN intended to install the fire wrap in the as-found configuration, and that the SSA would take credit for 20 feet of horizontal separation between the 1A-A CCS pump cables and the 1B-B CCS pump cables.

However, the SSA erroneously documented that the cables for the 1B-B pump were protected with fire wrap throughout the entire room.

Because of this assumption, the SSA credited the CCS Pump 1B-B as being available for any fire scenario within the room, and assumed the 1A-A pump was failed for the entire room; therefore, the operator action in SSD Procedure 0-AOI-30.2, Appendix C.39 was to start only the CCS Pump 1B-B from the Main Control Room (MCR). The missing operator action to ensure, either, the 1A-A or 1B-B pump was running could cause a fire SSD concern if the CCS Pump 1A-A was not running pre-fire and the fire location was where the CCS Pump Train B power cables were unprotected by fire wrap. Fire damage to the CCS Pump 1B-B unprotected cables could cause the pump breaker to trip, and without flow from CCS pump 1A-A to supply flow to the A CCS heat exchanger, there would be no cooling water for some of the plants credited fire SSD components.

Corrective Actions: The licensee completed a system Functional Evaluation and determined the CCS was functional but degraded. Their engineering evaluation also determined that the Appendix R FSSD analysis needed to be corrected in order to credit 20-foot separation analysis for both the CCS Pumps control circuit cables and add a MCR operator action to procedure 0-AOI-30.2 C.39 Fire Safe Shutdown Rooms 737-A3 to start the CCS Pump 1-A from the MCR for a fire event inside FZ 737.0-A3 (AV-039). In summary, the FSSD analysis will credit separation between the two CCS pumps and ensure both pumps started from the MCR ensuring that at least one of the CCS pumps provide water flow to the CCS A header and heat exchanger as required for FSSD.

Corrective Action References: CR 1672477, 2021 TFPI Missing Fire Wrap in 737.0-A3, 2/18/2021

Performance Assessment:

Performance Deficiency: The licensee's failure to provide an adequate safe shutdown analysis was a performance deficiency. Specifically, the inadequate procedure resulted in safe shutdown procedure 0-AOI-30.2, Appendix C.39 not containing a step to ensure flow through the A CCS heat exchanger.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Protection Against External Factors attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the inadequate safe shutdown analysis resulted in an inadequate safe shutdown operating procedure that could have adversely affected MCR operators ability to safely shut the plant down in response to a fire in the U1 Heat and Vent Equipment Room (FZ 737.0-A3).

Significance: The inspectors assessed the significance of the finding using Appendix F, Fire Protection Significance Determination Process. The initial review determined a Phase 2 quantitative screening approach was necessary because the finding had the potential to adversely affect the ability to reach and maintain hot shutdown/hot standby or safe and stable conditions using the credited safe shutdown success path. A regional Senior Reactor Analyst used SAPHIRE version 8.2.3 and Watts Bar SPAR model version 8.53 to perform an evaluation of the conditional core damage probability associated with the performance deficiency. The finding screened to Green, or very low safety significance, in Phase 2 at Step 2.5.4 of Attachment 1 to IMC 0609, Appendix F, because the screening increase in core damage frequency was less than 1E-06/year.

Cross-Cutting Aspect: Not Present Performance. No cross cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance.

Enforcement:

Violation: Watts Bar Operating License Condition 2.F requires that the licensee shall implement and maintain in effect all provisions of the approved fire protection program, as described in the Fire Protection Report for Watts Bar Unit 1, as approved in Supplements 18 and 19 of the SER (NUREG-0847). Fire Protection Report, Part V, Section 2.2, Unit 1 and Unit 2 Safe Shutdown Procedures states, in part, the fire safe shutdown procedures contained in 0-AOI-30.2 were developed based on calculations EDQ00099920090012, Unit 1 and 2 Appendix R Safe Shutdown Analysis and EDQ00099920090016, Manual Actions Required for Safe Shutdown Following a Fire.

Contrary to the above, since 2006, the licensee failed to perform an adequate calculation to support fire safe shutdown procedure 0-AOI-30.2. Specifically, for a fire in the U1 Heat and Vent Equipment Room, the licensee failed to ensure availability of CCS flow through the A heat exchanger because the analysis assumed the cables for the 1B-B CCS pump were fire wrapped for the entirety of the room. This oversight resulted in SSD procedure 0-AOI-30.2 C.39 being inadequate, as it only contained a step for operators to ensure the 1B-B pump was running and didnt account for the fact that a fire could possibly affect the credited 1B-B pump.

Enforcement Action: This violation is being treated as an non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On February 25, 2021, the inspectors presented the triennial fire protection inspection results to Mr. Anthony Williams and other members of the licensee staff.
  • On March 23, 2021, the inspectors presented the SDP Update inspection results to Mr.

Anthony Williams and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.21N.05 Calculations EPMTHJ102192 CO2 Fire Protection System Required Quantity Rev. 3

71111.21N.05 Calculations MDQ00299920110381 Appendix R - Operator Manual Action Evaluations 11/03/2020

71111.21N.05 Corrective Action CR 1493412 02/26/2019

Documents

71111.21N.05 Corrective Action CR 1528769 07/02/2019

Documents

71111.21N.05 Corrective Action CR 1567251 11/21/2019

Documents

71111.21N.05 Corrective Action CR 5583 BASED ON A REVIEW OF NRC INFORMATION 05/15/2003

Documents NOTICE 2002-24, WATTS BAR FIRE PROTECTION

NEEDS TO EVAL

71111.21N.05 Corrective Action PMCR 1409054 Change/Deferral Request for 480V SD BD 03/02/2020

Documents Maintenance

71111.21N.05 Corrective Action PMCR 1409054 PM Change/Deferral for 480 V SD BD Maintenance 03/02/2020

Documents

71111.21N.05 Corrective Action PMCR 1457157 11/25/2020

Documents

71111.21N.05 Corrective Action PMCR 1457158 PM Change/Deferral for 480 V SD BD Maintenance 11/25/2020

Documents

71111.21N.05 Corrective Action 1673842 NRC identified there is a typo on the pre-fire plan 2/23/2021

Documents (PFP) AUX-0-772-03. The 4th bullet in the section for

Resulting from Special Considerations of Hazards should say East of

Inspection Vital Battery Rm II instead of III.

71111.21N.05 Corrective Action 1674388 As part of the 2021 TFPI dust was identified on 2/25/2021

Documents various sprinklers. 0-FOR-26-3 should be revised to

Resulting from provide additional guidance for the acceptance criteria

Inspection to ensure sprinklers are free of debris, dust, etc and

fusible elements are visible. This guidance will

enhance the procedure to provide clear guidance to

support the inspectors performing this FOR.

71111.21N.05 Corrective Action CR 1668538 2021 TFPI - NRC Identified. Material Left from Work 02/2/2021

Documents Activities in the CSR

Inspection Type Designation Description or Title Revision or

Procedure Date

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1668539 2021 TFPI - NRC Identified - A Broom and Dustpan 02/2/2021

Documents Left in the CSR

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1668540 2021 TFPI - NRC Identified - A Ladder and Metal 02/2/2021

Documents Chair Found Un-restrained in CSR

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1668541 2021 TFPI - NRC Identified - The Trash Can in 02/2/2021

Documents Computer Room was Over Filled

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1668542 2021 TFPI - NRC Identified - Fire Protection Signage 02/2/2021

Documents Has Fallen Off the Wall and Laying in the Sink

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1669171 2021 TFPI - NRC Identified - Transient Combustible 02/4/2021

Documents Left in the 480V Transformer Room 2A-A

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1669215 Sprinkler Heads Need to be Cleaned in 480V 02/4/2021

Documents Transformer Rooms

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1670295 Impaired Sprinkler Heads in 480V Transformer 02/9/2021

Documents Rooms

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1671389 During 0-TI-211 walk down in the U-1 HVAC & Air 02/16/2021

Documents Intake rooms EL.737 Transients

Resulting from

Inspection

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.21N.05 Corrective Action CR 1671391 During 0-TI-211 walk down in the U-1 Air Intake 02/14/2021

Documents rooms EL.737 Sprinkler Loading

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1671394 During 0-TI-211 walk down in the U-1 Air Intake room 02/14/2021

Documents EL.737 Cob Webs

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1671395 During 0-TI-211 walk down in the U-2 HVAC & Air 02/16/2021

Documents Intake rooms EL.737 Transients

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1671397 During 0-TI-211 walk down at the IPS Found 02/16/2021

Documents Housekeeping Issues

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1671403 During 0-TI-211 walk down in the control Bldg. EL 692 02/16/2021

Documents Housekeeping Issues

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1671940 2021 TFPI Dust on Sprinkler Head in 480V 02/16/2021

Documents Transformer Room 1A

Resulting from

Inspection

71111.21N.05 Corrective Action CR 1672477 2021 TFPI Missing Fire Wrap in 737.0-A3 02/18/2021

Documents

Resulting from

Inspection

71111.21N.05 Drawings 0-47W843-1 Flow Diagram CO2 Storage, Fire Protection and Rev. 3

Purging System

71111.21N.05 Drawings 0-47W850-2 Flow Diagram Fire Protection Raw Service Water Rev. 6

71111.21N.05 Drawings 0-47W850-3 Flow Diagram Fire Protection Raw Service Water Rev. 5

71111.21N.05 Drawings 0-47W850-5 Flow Diagram Fire Protection Raw Service Water Rev. 3

71111.21N.05 Drawings 0-47W859-1 Mechanical Flow Diagram Component Cooling 09/18/2015

Inspection Type Designation Description or Title Revision or

Procedure Date

System

71111.21N.05 Drawings 1-45W751-1 Wiring Diagrams for 480V REAC MOV BDS 1A1-A 09/22/1990

Single Line SH-1

71111.21N.05 Drawings 1-45W751-2 Wiring Diagrams for 480V REAC MOV BD 1A1-A 09/22/1990

Single Line SH-2

71111.21N.05 Drawings 1-47A243-703-0 ERFBS Schedule Room 737-A3 (A703) Rev. 0

71111.21N.05 Drawings 1-47W859-2 Mechanical Flow Diagram Component Cooling 01/5/1990

System

71111.21N.05 Drawings 2-47W801-1 Flow Diagram for Main and RHEAT Steam Rev. 39

71111.21N.05 Drawings 45N824-7 Conduit & Grounding EL 713 1B CCS Rev. 42

71111.21N.05 Drawings 46W402-1 Architectural Plan EL 629 & EL 708 Rev. 11

71111.21N.05 Drawings 46W402-2 Architectural Plan EL 729 & EL 755 Rev. 27

71111.21N.05 Drawings 47BM491-5-10 Units 1 and 2 Aux Building Fire Protection 06/28/1977

71111.21N.05 Drawings 47BM491-68 Watts Bar Nuclear Plant Unit 1 and 2 Auxiliary Rev. 1

Building El 729', 757' & 782' Fire Protection

71111.21N.05 Drawings 47BM491-95 Watts Bar Nuclear Plant Unit 1 Auxiliary Building Fire Rev. 0

Protection

71111.21N.05 Drawings 47W491-31 Mechanical Fire Protection Rev. 8

71111.21N.05 Drawings 47W491-33 Mechanical Fire Protection Rev. 12

71111.21N.05 Drawings 47W491-37 Mechanical Fire Protection Rev. 11

71111.21N.05 Drawings 47W491-62 Mechanical Fire Protection Rev. 7

71111.21N.05 Drawings 47W491-82 Mechanical High Pressure Fire Protection Rev. 1

71111.21N.05 Drawings 47W491-86 Mechanical High Pressure Fire Protection Rev. 2

71111.21N.05 Drawings 47W491-87 Mechanical High Pressure Fire Protection Rev. 1

71111.21N.05 Engineering DCN 52033 Rev. A

Changes

71111.21N.05 Engineering DCN 52033-A CCS Pump Power Cable 20 Foot Separation Rev. 6

Changes

71111.21N.05 Engineering DCN WBN-18-126 Resolve App R Concern Associated with Steam Rev. 1

Changes Generator PORV Cables

71111.21N.05 Engineering Reverification and Revalidation of Appendix R Manual 04/15/2009

Evaluations Operator Actions

71111.21N.05 Engineering RIS 05-07 Evaluation for CR 1574031 - 2 - FCV-1- 12/30/2019

Inspection Type Designation Description or Title Revision or

Procedure Date

Evaluations 109 Failure

71111.21N.05 Engineering WBN-OSG4-165 Manual Actions Required for Safe Shutdown Rev. 5

Evaluations Following a Fire - 10 CFR Appendix R

71111.21N.05 Fire Plans CON-0-708-01 Unit 1 Auxiliary Instrument Room Rev. 3

71111.21N.05 Fire Plans WBN PreFire Plan AUX-0-772-01 Rev. 1

71111.21N.05 Fire Plans WBN PreFire Plan AUX-0-772-03 Rev. 5

71111.21N.05 Miscellaneous Vendor Purchase Contract Information for Fire 08/18/1977

Protection Equipment

71111.21N.05 Miscellaneous 00010187 LMS NO. Emergency Response Training Fire Brigade

Membership

71111.21N.05 Miscellaneous 00010188 ATIS LA. Emergency Response Training Fire Brigade Rev. 0

NO. leadership

71111.21N.05 Miscellaneous A21-0005 Transient Fire Load Permit - 5th Vital Battery Room 02/1/2021

71111.21N.05 Miscellaneous DS-M17.2.2 Mechanical Design Standard-Electrical Raceway Fire Rev. 8

Barrier Systems

71111.21N.05 Miscellaneous DS-M18.2.15 Fire Damper Application, Selection and Installation Rev. 3

71111.21N.05 Miscellaneous G-73 Installation, Modifications, and Maintenance of Fire Rev. 9

Protection Systems and Features

71111.21N.05 Miscellaneous IN2002-24 Potential Problems with Heat Collectors on Fire 2002

Protection Sprinklers

71111.21N.05 Miscellaneous NFPA 12-1973 Carbon Dioxide Fire Extinguishing Systems 1973

71111.21N.05 Miscellaneous NFPA 13-1975 Installation of Sprinklers 1975

71111.21N.05 Miscellaneous NFPA 80-1975 Fire Doors and Windows 1975

71111.21N.05 Miscellaneous NONE Administrative Qualification Matrix Report for Fire 1/14/2021

Brigade Members

71111.21N.05 Miscellaneous NONE UL Field Sample Testing of Automatic Sprinklers 6/01/2020

71111.21N.05 Miscellaneous NONE American Fire Sprinkler Association Sprinkler Age 11/01/2017

Publication "When is Loading Detrimental to Sprinkler

Performance"

71111.21N.05 Miscellaneous NUREG-0847 Watts Bar Units 1 & 2 Safety Evaluation Report, October

Supplement No. 18 1995

71111.21N.05 Miscellaneous SDD-N3-26-4002 High Pressure Fire Protection System Unit 1 / Unit 2 Rev. 21

71111.21N.05 Miscellaneous SDD-N3-62-4001 Chemical and Volume Control System Unit 1/Unit 2 Rev. 38

71111.21N.05 Miscellaneous Tennessee Valley Watts Bar Nuclear Plant Fire Protection Report Rev. 57

Inspection Type Designation Description or Title Revision or

Procedure Date

Authority

71111.21N.05 Miscellaneous WB-DC-40-62 Fire Protection Rev. 5

71111.21N.05 Miscellaneous WB-DC-40-62 Design Criteria Document Watts Bar Nuclear Plant Rev. 5

Unit1/Unit2 Fire Protection

71111.21N.05 Miscellaneous WBN-DCD-40-51 Fire Protection of Safe Shutdown Capability Rev. 8

71111.21N.05 Miscellaneous WBN-VTD AS06-0310 Operation and Service Manual for ASCOA CO2 Rev. 0

Storage Unit (24 Ton)

71111.21N.05 Miscellaneous WBN-VTD-AS06-0310 Operation and Service Manual for ASCOA Chemetron Rev. 0

Cardox CO2 Storage Unit (24 Ton)

71111.21N.05 Miscellaneous WBN-VTD-W120- 6.9KV/480V SD BD Transformer Vendor Manual Rev. 0

2352

71111.21N.05 Procedures 0-AOI-30.1 Plant Fires Rev. 11

71111.21N.05 Procedures 0-AOI-30.2 APP B Fire Safe Shutdown Elevation Diagrams Rev. 1

71111.21N.05 Procedures 0-AOI-30.2 C.36 Fire Safe Shutdown Rooms 737-A1A Rev. 4

71111.21N.05 Procedures 0-AOI-30.2 C.39 Fire Safe Shutdown Rooms 737-A3 Rev. 1

71111.21N.05 Procedures 0-AOI-30.2 C.39 Fire Safe Shutdown Rooms 737-A3 Rev. 2

71111.21N.05 Procedures 0-AOI-30.2 C.69 Fire Safe Shutdown Room Control Building Rev. 11

71111.21N.05 Procedures 0-FOR-13-636 18 Month Fire Detection And Suppression Test For Rev. 14

Panel L636

71111.21N.05 Procedures 0-FOR-26-3 18 Month Inspection of Fire Protection Sprinkler Rev. 13

Systems in Accessible Safety-Related Areas

71111.21N.05 Procedures 0-MI-57.015 Taping Of Electrical Terminations And Splices Rev. 0

71111.21N.05 Procedures 0-PI-OPS-1-FP Freeze Protection Rev. 27

71111.21N.05 Procedures 0-TI-2018 Demonstration of Appendix R Actions Rev. 1

71111.21N.05 Procedures 0-TI-211 Fire Protection Weekly Walkdown Rev. 1

71111.21N.05 Procedures FPDP-1 Conduct of Fire Operations Rev. 9

71111.21N.05 Procedures FPDP-5 Development and Evaluation of Fire Drills Rev. 6

71111.21N.05 Procedures NEDP-22 Operability Determinations and Functionality Rev. 21

Evaluations

71111.21N.05 Procedures NPG-SPP-01.3 Housekeeping Rev. 8

71111.21N.05 Procedures NPG-SPP-06.2 Preventive Maintenance Rev. 13

71111.21N.05 Procedures NPG-SPP-18.4.5 Fire Protection Quality Assurance Rev. 3

71111.21N.05 Procedures NPG-SPP-18.4.7 Control of Transient Combustibles Rev. 13

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.21N.05 Procedures TPD-FBT Fleet Fire Brigade Training Program Rev. 6

71111.21N.05 Procedures TRN-33 Fire Protection Employee Qualifications Rev. 4

71111.21N.05 Procedures WB-DC-30-13 10CFR50, App R, Type I, II, and III Circuits - Unit 1 / Rev. 10

Unit 2

71111.21N.05 Procedures WB-DC-30-27 AC AND DC CONTROL POWER SYSTEMS - (UNIT Rev. 35

/ UNIT 2)

71111.21N.05 Procedures WB-DC-30-28 LOW AND MEDIUM VOLTAGE POWER SYSTEMS - Rev. 23

UNIT 1 / UNIT 2

71111.21N.05 Work Orders Thermal Barrier Booster Pump Inspection and 06/04/2019

Maintenance

71111.21N.05 Work Orders 10-812441-000 Inspection of Switchgear Bus and MCC Perform MI- 04/21/2011

57.200

71111.21N.05 Work Orders 112794763 Inspection of Switchgear Bus and MCC Perform MI- 03/20/2012

57.200

71111.21N.05 Work Orders 117351301 480V SD BD Relay Functional Test 11/10/2017

71111.21N.05 Work Orders 117640933 Fire Damper (Internal) Visual Inspection-Auxiliary, 9/17/2016

Control and Diesel Generator Building

71111.21N.05 Work Orders 118562379 Fire Damper (Internal) Visual Inspection - Auxiliary 11/14/2017

Control and Diesel Generator Building

71111.21N.05 Work Orders 118586915 18 Month CO2 Fire Protection Inspection and Test for 12/31/2017

Power House Areas

71111.21N.05 Work Orders 118802289 3 Year HPFP Hydraulic Performance Verification 2/15/2018

71111.21N.05 Work Orders 118802306 18 Month Inspection of HPFP Sprinkler Systems in 10/25/2018

Accessible Safety Related Areas

71111.21N.05 Work Orders 119326030 3 Year HPFP Hydraulic Performance Verification 5/23/2019

71111.21N.05 Work Orders 119425287 Fire Damper (Internal) Visual Inspection - Auxiliary, 11/14/2018

Control and Diesel Generator Building

71111.21N.05 Work Orders 119837881 18 Month CO2 Fire Protection Inspection and Test for 4/06/2019

Power House Areas

71111.21N.05 Work Orders 120164870 18 Month Inspection of the HPFP Sprinkler Systems 10/18/2019

in Accessible Safety Related Areas

71111.21N.05 Work Orders 120164871 0-FOR-13-636 18 Month Fire Detection and 8/28/2018

Suppression Test For Panel L636

71111.21N.05 Work Orders 120240570 Component Cooling System Heat Exchanger A 05/07/2020

Inspection Type Designation Description or Title Revision or

Procedure Date

Performance Test

71111.21N.05 Work Orders 120804252 Thermal Barrier Booster PMPS and MTRS CCS 1B-B 07/13/2020

Inspection and Maintenance

71111.21N.05 Work Orders 120903626 Quarterly CO2 Flow Path Verification 6/15/2020

71111.21N.05 Work Orders 120903676 Component Cooling System Thermal Barrier Booster 06/13/2020

Pump 1B Quarterly Performance Test

71111.21N.05 Work Orders 12110034 Quarterly CO2 Flow Path Verification 9/14/2020

71111.21N.05 Work Orders 121162048 Component Cooling System Pump 1A-A Quarterly 10/09/2020

Performance Test

71111.21N.05 Work Orders 121162073 Weekly CO2 Storage Tank Level Verification 10/26/2020

71111.21N.05 Work Orders 121162075 Weekly Storage Tank Level Verification 11/02/2929

71111.21N.05 Work Orders 121233592 Component Flow Debris/Foreign Material Testing 11/19/2020

Utilizing Ultrasonic ERCW - (Train A)

71111.21N.05 Work Orders 121413261 Weekly CO2 Storage Tank Level Verification 2/08/2021

71111.21N.05 Work Orders 121924401 Sprinkler heads need to be cleaned in 480V 2/10/2021

Transformer rooms

71111.21N.05 Work Orders WO 121359676 TI-211 Fire Protection Weekly Inspection Report 01/18/2021

71111.21N.05 Work Orders WO 121359678 TI-211 Fire Protection Weekly Inspection Report 01/26/2021

71111.21N.05 Work Orders WO 121413380 TI-211 Fire Protection Weekly Inspection Report 01/31/2021

17