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| | issue date = 07/24/1997 | | | issue date = 07/24/1997 |
| | title = LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold | | | title = LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold |
| | author name = OLIVE G | | | author name = Olive G |
| | author affiliation = CAROLINA POWER & LIGHT CO. | | | author affiliation = CAROLINA POWER & LIGHT CO. |
| | addressee name = | | | addressee name = |
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| {{#Wiki_filter:NRC FORM 366 14B5)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)(See reverse for required number of digits/characters for each block)I APPROVED BY OMB NO.3150-0104 EXPIRES 04/30196 ESTIMATED BURDEN PER RESPONSE'TO COMPLY W)TH THS MANDATORY)NFORMATION COLIECTION REOUEST.503)HRS.REPORTED lESSONS LEARNED ARE INCORPORATED INTO THE UCENSING PROCESS ANO FEO BACK TO INDUSTRY.FORWARD COMMENTS REGARDING BURDEN ES11MATE TO THE INFORMATION ANO RECORDS MANAGEMENT BRANCH IT%F33l US.NUCLEAR REGUlATORY COMMSSION, WASHINGTON. | | {{#Wiki_filter:NRC FORM 366 14B5) |
| DC 20555000). | | U.S. NUCLEAR REGULATORY COMMISSION I |
| AND TO THE PAPERWORK REDUCTION PROJECT l3150.0)04L OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON. | | APPROVED BY OMB NO. 3150-0104 EXPIRES 04/30196 ESTIMATED BURDEN PER RESPONSE 'TO COMPLY W)TH THS MANDATORY |
| OC 20503.FAGIUTY NAME Il)Harris Nuclear Plant Unit-1 DOCKET NUMBER (2)50-400 PAGE (3)1 OF 3 TITLE 14)Unescorted access inappropriately granted to contract outage workers.MONTH OAY YEAR EVENT DATE (5)LER NUMBER (6)YEAR SEQUENTIAL REVISION NUMBER NUMBER REPORT DATE (7)MONTH OAY FACIUTY NAME OTHER FACILITIES INVOLVED (6)DOCKETNUMBER 4 5 OPERATING MODE (9)POWER LEVEL (10)97 05'7-S01-00 7 24 97 FACIUTY NAME DOCKET NUMBER 05000 20.2201 (b)20.2203(a) | | )NFORMATION COLIECTION REOUEST. 503) HRS. REPORTED lESSONS LEARNED ARE INCORPORATED INTO THE UCENSING PROCESS ANO FEO BACK TO INDUSTRY. |
| (1)20.2203(a) | | LICENSEE EVENT REPORT (LER) FORWARD COMMENTS REGARDING BURDEN ES11MATE TO THE INFORMATION ANO RECORDS MANAGEMENT BRANCH IT% F33l US. NUCLEAR REGUlATORY COMMSSION, (See reverse for required number of WASHINGTON. DC 20555000). AND TO THE PAPERWORK REDUCTION PROJECT l3150. |
| (2)(i)20.2203(a) | | digits/characters for each block) 0)04L OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON. OC 20503. |
| (2)(ii)20.2203(a)(2)(iii)20.2203(a) | | FAGIUTY NAME Il) DOCKET NUMBER (2) PAGE (3) |
| (2)(iv)20.2203(a) | | Harris Nuclear Plant Unit-1 50-400 1 OF 3 TITLE 14) |
| (2)(v)20.2203(a) | | Unescorted access inappropriately granted to contract outage workers. |
| (3)(il 20.2203(a)(al(ii) 20.2203(al(4) 50.36(cl(1) 50.36(c)(2) 50.73(a)(2)(i)50.73(a)(2)(ii)50.73(a)(2)(iii)50.73(a)(2)(iv)50.73(a)(2)(vl 50.73(a)(2)(vii)50.73(a)(2)(viii)50.73(a)(2)(x) | | EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (6) |
| X 73.71 OTHER Specify in Abstract below or In NRC Form 3BBA THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more)(11)NAME LICENSEE CONTACT FOR THIS LER George Olive, Sr.Support Analyst-HNP Security (12)TELEPHONE NUMBER Iinoiude Ates Code)(919)362-2684 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DES CRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPROS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPROS SUPPLEMENTAL REPORT EXPECTED (14)X YES (If yas, complete EXPECTED SUBMISSION DATE).NO EXPECTED SUBMISSION DATE (15)MONTH OAY 8 30 YEAR 97 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single.spaced typewritten lines)(16)On June 24, 1997, it was determined that an outage contract worker, granted unescorted access for outage work during the Harris Nuclear Plant refueling outage (RFO-7), omitted pertinent information from his Personal History Questionnaire (PHQ), which was subsequently determined to be disqualifying for unescorted access under Carolina Power and Light's criteria.The individual involved was granted unescorted access from April 5, 1997 through May 15, 1997.During further review of background investigation case files following this event, an additional instance was identified where an individual was inappropriately granted unescorted access without a valid/approved psychological evaluation.
| | FACIUTY NAME DOCKETNUMBER SEQUENTIAL REVISION MONTH OAY YEAR YEAR MONTH OAY NUMBER NUMBER FACIUTY NAME DOCKET NUMBER 4 5 97 S01 00 7 24 97 05000 OPERATING THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more) (11) |
| The cause of these events was personnel error on the part of individuals responsible for the review and adjudication of information provided as a part of the background investigation process.Corrective actions include additional investigation/analysis of the event, restricting the involved individuals access on the Personal Access Data System (PADS), and an examination of background investigation files that were reviewed/adjudicated for temporary clearance and unescorted access during the RFO-7 period.NR 97073000i5 970724 PDR ADOCK 05000400 S PDR (4 ip NRC fORM 366A)4.95)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION US.NUCLEAR REGUULTORY COMMISSION FACILITY NAME I)I Shearon Harris Nuclear Plant~Unit)I)1 DOCKET 50400 LER NUMBER IS)SEOUENTIAL REVISION NUMBER NUMBER 97-S01-00 PAGE)3)2 OF 3 TEXT Pl mort spssv fs ssvvvsd, vsv sdditiml sopis ol hlrC Fee 3SQI I)7)EVENT DESCRIPTION: | | MODE (9) |
| At approximately 1500, June 24, 1997, a Corporate Security representative reported to the Site Security.Superintendent that a contract (non-licensee) employee had been granted unescorted access to plant protected and vital areas without the benefit of adjudication of derogatory information contained within his PHQ that was potentially disqualifying. | | POWER 05'7 20.2201 (b) 20.2203(a) (1) 20.2203(a) (2) (v) 20.2203(a) (3) (il 50.73(a)(2) (i) 50.73(a)(2) (ii) 50.73(a) (2) (viii) 50.73(a)(2)(x) |
| The individual was granted unescorted access from April 5, 1997 through May 15, 1997.The subject individual completed a PHQ on March 31, 1997 at the Plant Access Authorization Facility.The individual answered"yes" to a question on the PHQ asking"Have you ever been convicted of an alcohol or a controlled substance related offense, which includes driving while impaired (DWI), or do you presently have such a case pending?" The PHQ further advises that," if you answered yes to any question, specific details must be given explaining the circumstances surrounding the case".The individual failed to annotate any details to explain his yes answer to the question.The initial review of the PHQ by plant access authorization personnel failed to identify the"yes" response, which in turn resulted in a failure to seek additional information to explain the response.A subsequent review of the PHQ by Corporate Access Authorization also failed to adjudicate the information resulting in approval/granting unescorted access to plant protected and vital areas on April 5, 1997.On June 23, 1997, a criminal history record was received from the Federal Bureau of Investigation, together with a criminal records check received from the North Augusta Department of Public Safety, indicating that the individual was convicted of simple possession of an illegal controlled substance on January 20, 1996.In accordance with the Carolina Power and Light criteria for unescorted access, this conviction would disqualify the individual for unescorted access to the company's nuclear plants.During further review of background investigation case files following this event, an additional instance was identified where an individual was inappropriately granted unescorted access without a valid/approved'psychological evaluation (MMPI).This individuals access should have been denied pending satisfactory resolution of possible alcohol abuse.Due to this error, unescorted access was granted during the period of time from April 8, 1997 through May 13, 1997.CAUSE: The cause of these events was personnel error.The individuals involved in reviewing the background investigation case file records did not apply adequate attention to detail.For the first instance, the initial reviewer in Plant Access Authorization failed to question the individual and obtain the needed information regarding the"yes" answer on the PHQ.In addition, the reviewer at Corporate Access Authorization failed to question or adequately adjudicate the"yes" answer on the subject individual's PHQ and subsequently approved the individual unescorted access.In the second instance, the reviewer at Corporate Access Authorization failed to recognize the need for further evalution of MMPI results regarding possible alcohol abuse.These errors are contrary to CP&L procedures, AA-DI-02 (Personal History Questionnaire) and NGGS-SEC-1002 (Personal History Questionnaire), and SEC-NGGC-2101 (Nuclear Worker Screening Program for Unescorted Access).There were no unusual characteristics of the work location that would directly contribute to the errors.All personnel involved, with the exception of the contract individual, were licensee employees. | | LEVEL (10) 20.2203(a) (2)(i) 20.2203(a)(al(ii) 50.73(a)(2) (iii) X 73.71 20.2203(a) (2)(ii) 20.2203(al(4) 50.73(a)(2) (iv) OTHER 20.2203(a)(2) (iii) 50.36(cl(1) 50.73(a)(2)(vl Specify in Abstract below or In NRC Form 3BBA 20.2203(a) (2)(iv) 50.36(c)(2) 50.73(a) (2) (vii) |
| | LICENSEE CONTACT FOR THIS LER (12) |
| | NAME TELEPHONE NUMBER Iinoiude Ates Code) |
| | George Olive, Sr. Support Analyst - HNP Security (919) 362-2684 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DES CRIBED IN THIS REPORT (13) |
| | REPORTABLE REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER TO NPROS TO NPROS SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH OAY YEAR YES SUBMISSION X (If yas, complete EXPECTED SUBMISSION DATE). |
| | NO DATE (15) 8 30 97 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single. spaced typewritten lines) (16) |
| | On June 24, 1997, it was determined that an outage contract worker, granted unescorted access for outage work during the Harris Nuclear Plant refueling outage (RFO-7), omitted pertinent information from his Personal History Questionnaire (PHQ), which was subsequently determined to be disqualifying for unescorted access under Carolina Power and Light's criteria. The individual involved was granted unescorted access from April 5, 1997 through May 15, 1997. During further review of background investigation case files following this event, an additional instance was identified where an individual was inappropriately granted unescorted access without a valid/approved psychological evaluation. The cause of these events was personnel error on the part of individuals responsible for the review and adjudication of information provided as a part of the background investigation process. Corrective actions include additional investigation/analysis of the event, restricting the involved individuals access on the Personal Access Data System (PADS), and an examination of background investigation files that were reviewed/adjudicated for temporary clearance and unescorted access during the RFO-7 period. |
| | 97073000i5 970724 PDR ADOCK 05000400 S PDR NR (4 |
| | |
| | ip NRC fORM 366A US. NUCLEAR REGUULTORY COMMISSION |
| | )4.95) |
| | LICENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION FACILITY NAME I)I DOCKET LER NUMBER IS) PAGE )3) |
| | SEOUENTIAL REVISION NUMBER NUMBER Shearon Harris Nuclear Plant ~ Unit )I)1 50400 2 OF 3 97 - S01 - 00 TEXT Pl mort spssv fs ssvvvsd, vsv sdditiml sopis ol hlrC Fee 3SQI I)7) |
| | EVENT DESCRIPTION: |
| | At approximately 1500, June 24, 1997, a Corporate Security representative reported to the Site Security. |
| | Superintendent that a contract (non-licensee) employee had been granted unescorted access to plant protected and vital areas without the benefit of adjudication of derogatory information contained within his PHQ that was potentially disqualifying. The individual was granted unescorted access from April 5, 1997 through May 15, 1997. |
| | The subject individual completed a PHQ on March 31, 1997 at the Plant Access Authorization Facility. The individual answered "yes" to a question on the PHQ asking "Have you ever been convicted of an alcohol or a controlled substance related offense, which includes driving while impaired (DWI), or do you presently have such a case pending?" The PHQ further advises that, |
| | " if you answered yes to any question, specific details must be given explaining the circumstances surrounding the case". The individual failed to annotate any details to explain his yes answer to the question. The initial review of the PHQ by plant access authorization personnel failed to identify the "yes" response, which in turn resulted in a failure to seek additional information to explain the response. A subsequent review of the PHQ by Corporate Access Authorization also failed to adjudicate the information resulting in approval/granting unescorted access to plant protected and vital areas on April 5, 1997. |
| | On June 23, 1997, a criminal history record was received from the Federal Bureau of Investigation, together with a criminal records check received from the North Augusta Department of Public Safety, indicating that the individual was convicted of simple possession of an illegal controlled substance on January 20, 1996. In accordance with the Carolina Power and Light criteria for unescorted access, this conviction would disqualify the individual for unescorted access to the company's nuclear plants. |
| | During further review of background investigation case files following this event, an additional instance was identified where an individual was inappropriately granted unescorted access without a valid/approved'psychological evaluation (MMPI). This individuals access should have been denied pending satisfactory resolution of possible alcohol abuse. |
| | Due to this error, unescorted access was granted during the period of time from April 8, 1997 through May 13, 1997. |
| | CAUSE: |
| | The cause of these events was personnel error. The individuals involved in reviewing the background investigation case file records did not apply adequate attention to detail. For the first instance, the initial reviewer in Plant Access Authorization failed to question the individual and obtain the needed information regarding the "yes" answer on the PHQ. In addition, the reviewer at Corporate Access Authorization failed to question or adequately adjudicate the "yes" answer on the subject individual's PHQ and subsequently approved the individual unescorted access. In the second instance, the reviewer at Corporate Access Authorization failed to recognize the need for further evalution of MMPI results regarding possible alcohol abuse. |
| | These errors are contrary to CP&L procedures, AA-DI-02 (Personal History Questionnaire) and NGGS-SEC-1002 (Personal History Questionnaire), and SEC-NGGC-2101 (Nuclear Worker Screening Program for Unescorted Access). |
| | There were no unusual characteristics of the work location that would directly contribute to the errors. All personnel involved, with the exception of the contract individual, were licensee employees. |
| SAFETY SIGNIFICANCE: | | SAFETY SIGNIFICANCE: |
| An interview with the Carolina Power and Light supervisor for the subject individuals was conducted, which determined that the individuals work performance was rated as good and that they did not work on any safety related equipment. | | An interview with the Carolina Power and Light supervisor for the subject individuals was conducted, which determined that the individuals work performance was rated as good and that they did not work on any safety related equipment. The work performed by the these individuals included piping replacement in the Turbine Building and crane rigging. This SER is being submitted per the requirements of 10CFR73.71, Reporting of Safeguards Events. |
| The work performed by the these individuals included piping replacement in the Turbine Building and crane rigging.This SER is being submitted per the requirements of 10CFR73.71, Reporting of Safeguards Events. | | |
| NRC FORM 366A (495)LlCENSEE EVENT REPORT (LER).TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FAc)L)TY NAME u)Shearon Harris Nuclear Plant~Unit//1 BUCKET 50400 LER NUMBER 16)YEAR SEOUENTIAL REVISION NUMBER NUMBER 97-S01-00 PAGE 13)3 OF 3 TEXT r)r Ivvsv spssv rs svpviaf, vsv vddl)vtvsr copes vl A'HC Pvae 3SQI (I 7)PREVIOUS SIMILAR EVENTS: A'similar event, contained in Safeguards Event Report Number 89-S05-00, occurred on October 19, 1989.This event was the result of a failure to adjudicate adverse criminal history information that was an element of a background investigation being performed by a contractor who certified a satisfactory full background investigation. | | NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (495) |
| | LlCENSEE EVENT REPORT (LER). |
| | TEXT CONTINUATION FAc)L)TY NAME u) BUCKET LER NUMBER 16) PAGE 13) |
| | SEOUENTIAL REVISION YEAR NUMBER NUMBER Shearon Harris Nuclear Plant ~ |
| | Unit //1 50400 3 OF 3 97 - S01 - 00 TEXT r)r Ivvsv spssv rs svpviaf, vsv vddl)vtvsr copes vl A'HC Pvae 3SQI (I 7) |
| | PREVIOUS SIMILAR EVENTS: |
| | A'similar event, contained in Safeguards Event Report Number 89-S05-00, occurred on October 19, 1989. This event was the result of a failure to adjudicate adverse criminal history information that was an element of a background investigation being performed by a contractor who certified a satisfactory full background investigation. |
| CORRECTIVE ACTIONS COMPLETED: | | CORRECTIVE ACTIONS COMPLETED: |
| 1.The access files for the individuals inappropriately granted unescorted access were placed on access hold in the Personal Access Data system (PADS).This access information has not been transferred to any other utility and flags have been put in place to prevent such transfer in both records.2.A second file review was added to the Corporate Access Authorization adjudication process as an interim measure, pending implementation of permanent corrective actions.3.An initial review of background investigation case files was completed on July 24, 1997, for personnel who were granted temporary unescorted access similar to the subject individuals. | | : 1. The access files for the individuals inappropriately granted unescorted access were placed on access hold in the Personal Access Data system (PADS). This access information has not been transferred to any other utility and flags have been put in place to prevent such transfer in both records. |
| This included a review of MMPI test results and PHQ records that required adjudication of"yes" answers.The review disclosed one (1)additional adjudication error that was logged in the HNP Safeguards Event Log (SEL).A'detailed review of all case files for personnel granted temporary unescorted access for the HNP refueling outage (RFO-7)is approximately 55%complete and disclosed the second adjudication failure identified in the event description above.This review has also identified an additional fifteen (15)case file review/adjudication errors that were not reportable, but were logged in the HNP SEL in accordance with 10CFR73.71. | | : 2. A second file review was added to the Corporate Access Authorization adjudication process as an interim measure, pending implementation of permanent corrective actions. |
| The individuals responsible for making these errors at Corporate Access Authorization and Plant Access Authorization received appropriate disciplinary actions.CORRECTIVE ACTIONS PLANNED: 1.A detailed record review for those personnel granted similar temporary unescorted access to HNP for Refueling Outage 7 is continuing in conjunction with a root cause analysis.This is currently being performed to further investigate the event and identify additional causal factors and corrective measures to preclude recurrence. | | : 3. An initial review of background investigation case files was completed on July 24, 1997, for personnel who were granted temporary unescorted access similar to the subject individuals. This included a review of MMPI test results and PHQ records that required adjudication of "yes" answers. The review disclosed one (1) additional adjudication error that was logged in the HNP Safeguards Event Log (SEL). A'detailed review of all case files for personnel granted temporary unescorted access for the HNP refueling outage (RFO-7) is approximately 55% complete and disclosed the second adjudication failure identified in the event description above. This review has also identified an additional fifteen (15) case file review/adjudication errors that were not reportable, but were logged in the HNP SEL in accordance with 10CFR73.71. |
| The results of this review and any other pertinent investigation findings will be provided in a supplement to this SER.The on-going review/investigation will be completed to support an August 30, 1997, SER revision submittal.}} | | The individuals responsible for making these errors at Corporate Access Authorization and Plant Access Authorization received appropriate disciplinary actions. |
| | CORRECTIVE ACTIONS PLANNED: |
| | : 1. A detailed record review for those personnel granted similar temporary unescorted access to HNP for Refueling Outage 7 is continuing in conjunction with a root cause analysis. This is currently being performed to further investigate the event and identify additional causal factors and corrective measures to preclude recurrence. The results of this review and any other pertinent investigation findings will be provided in a supplement to this SER. The on-going review/investigation will be completed to support an August 30, 1997, SER revision submittal.}} |
LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access HoldML18012A837 |
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Harris |
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Issue date: |
07/24/1997 |
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From: |
Olive G CAROLINA POWER & LIGHT CO. |
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To: |
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Shared Package |
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ML18012A836 |
List: |
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References |
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LER-97-S01, LER-97-S1, NUDOCS 9707300015 |
Download: ML18012A837 (4) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. 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Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:RO)
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A9151999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Shearon Harris Npp. with 991012 Ltr ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18017A8621999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Harris Nuclear Plant.With 990908 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18017A8361999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Shearon Harris Nuclear Power Plant.With 990811 Ltr ML18016B0151999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Shearon Harris Npp. with 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990614 Ltr ML18017A8981999-05-12012 May 1999 Technical Rept Entitled, Harris Nuclear Plant-Bacteria Detection in Water from C&D Spent Fuel Pool Cooling Lines. ML18016A9581999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990513 Ltr ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8941999-04-0505 April 1999 Revised Pages 20-25 to App 4A of non-proprietary Version of Rev 3 to HI-971760 ML18016A9101999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Shearon Harris Nuclear Power Plant.With 990413 Ltr ML18016A8661999-03-31031 March 1999 Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept. ML18017A8931999-02-28028 February 1999 Risks & Alternative Options Associated with Spent Fuel Storage at Shearon Harris Nuclear Power Plant. ML18016A8551999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Shearon Harris Npp. with 990312 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8531999-02-18018 February 1999 Non-proprietary Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFP 'C' & 'D'. ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18022B0631999-02-0404 February 1999 Rev 0 to Nuclear NDE Manual. with 28 Oversize Uncodable Drawings of Alternative Plan Scope & 4 Oversize Codable Drawings ML20202J1161999-02-0101 February 1999 SER Accepting Relief Requests Associated with Second 10-year Interval Inservice Testing Program ML18016A8041999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Shearon Harris Nuclear Power Plant.With 990211 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7801998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Shearon Harris Npp. with 990113 Ltr ML18016A7671998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Shnpp,Unit 1.With 981215 Ltr ML18016A9731998-11-28028 November 1998 Changes,Tests & Experiments, for Harris Nuclear Plant.Rept Provides Brief Description of Changes to Facility & Summary & of SE for Each Item That Was Implemented Under 10CFR50.59 Between 970608-981128.With 990527 Ltr ML18016A8351998-11-28028 November 1998 ISI Summary 8th Refueling Outage for Shearon Harris Power Plant,Unit 1. ML18016A7411998-11-25025 November 1998 Rev 1 to Shnpp Cycle 9 Colr. ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A7071998-11-0303 November 1998 Rev 0 to Harris Unit 1 Cycle 9 Colr. ML18016A7201998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Shearon Harris Nuclear Power Plant.With 981113 Ltr ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves ML18016A6201998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Harris Nuclear Power Plant.With 981012 Ltr ML18016A5971998-09-21021 September 1998 Rev 1 to Harris Unit 1 Cycle 8 Colr. ML18016A5881998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Shnpp,Unit 1.With 980914 Ltr ML18016A5071998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Shearon Harris Nuclear Plant.W/980811 Ltr ML18016A9431998-07-0707 July 1998 Rev 1 to QAP Manual. ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A9371998-06-30030 June 1998 Technical Rept on Matl Identification of Spent Fuel Piping Welds at Hnp. ML18016A4861998-06-30030 June 1998 Monthly Operating Rept for June 1998 for SHNPP.W/980715 Ltr ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18016A4521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Shearon Harris Nuclear Power Plant.W/980612 Ltr ML18016A7711998-05-26026 May 1998 Non-proprietary Rev 2 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris Spent Fuel Pools 'C' & 'D'. 1999-09-30
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NRC FORM 366 14B5)
U.S. NUCLEAR REGULATORY COMMISSION I
APPROVED BY OMB NO. 3150-0104 EXPIRES 04/30196 ESTIMATED BURDEN PER RESPONSE 'TO COMPLY W)TH THS MANDATORY
)NFORMATION COLIECTION REOUEST. 503) HRS. REPORTED lESSONS LEARNED ARE INCORPORATED INTO THE UCENSING PROCESS ANO FEO BACK TO INDUSTRY.
LICENSEE EVENT REPORT (LER) FORWARD COMMENTS REGARDING BURDEN ES11MATE TO THE INFORMATION ANO RECORDS MANAGEMENT BRANCH IT% F33l US. NUCLEAR REGUlATORY COMMSSION, (See reverse for required number of WASHINGTON. DC 20555000). AND TO THE PAPERWORK REDUCTION PROJECT l3150.
digits/characters for each block) 0)04L OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON. OC 20503.
FAGIUTY NAME Il) DOCKET NUMBER (2) PAGE (3)
Harris Nuclear Plant Unit-1 50-400 1 OF 3 TITLE 14)
Unescorted access inappropriately granted to contract outage workers.
EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (6)
FACIUTY NAME DOCKETNUMBER SEQUENTIAL REVISION MONTH OAY YEAR YEAR MONTH OAY NUMBER NUMBER FACIUTY NAME DOCKET NUMBER 4 5 97 S01 00 7 24 97 05000 OPERATING THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more) (11)
MODE (9)
POWER 05'7 20.2201 (b) 20.2203(a) (1) 20.2203(a) (2) (v) 20.2203(a) (3) (il 50.73(a)(2) (i) 50.73(a)(2) (ii) 50.73(a) (2) (viii) 50.73(a)(2)(x)
LEVEL (10) 20.2203(a) (2)(i) 20.2203(a)(al(ii) 50.73(a)(2) (iii) X 73.71 20.2203(a) (2)(ii) 20.2203(al(4) 50.73(a)(2) (iv) OTHER 20.2203(a)(2) (iii) 50.36(cl(1) 50.73(a)(2)(vl Specify in Abstract below or In NRC Form 3BBA 20.2203(a) (2)(iv) 50.36(c)(2) 50.73(a) (2) (vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER Iinoiude Ates Code)
George Olive, Sr. Support Analyst - HNP Security (919) 362-2684 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DES CRIBED IN THIS REPORT (13)
REPORTABLE REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER TO NPROS TO NPROS SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH OAY YEAR YES SUBMISSION X (If yas, complete EXPECTED SUBMISSION DATE).
NO DATE (15) 8 30 97 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single. spaced typewritten lines) (16)
On June 24, 1997, it was determined that an outage contract worker, granted unescorted access for outage work during the Harris Nuclear Plant refueling outage (RFO-7), omitted pertinent information from his Personal History Questionnaire (PHQ), which was subsequently determined to be disqualifying for unescorted access under Carolina Power and Light's criteria. The individual involved was granted unescorted access from April 5, 1997 through May 15, 1997. During further review of background investigation case files following this event, an additional instance was identified where an individual was inappropriately granted unescorted access without a valid/approved psychological evaluation. The cause of these events was personnel error on the part of individuals responsible for the review and adjudication of information provided as a part of the background investigation process. Corrective actions include additional investigation/analysis of the event, restricting the involved individuals access on the Personal Access Data System (PADS), and an examination of background investigation files that were reviewed/adjudicated for temporary clearance and unescorted access during the RFO-7 period.
97073000i5 970724 PDR ADOCK 05000400 S PDR NR (4
ip NRC fORM 366A US. NUCLEAR REGUULTORY COMMISSION
)4.95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME I)I DOCKET LER NUMBER IS) PAGE )3)
SEOUENTIAL REVISION NUMBER NUMBER Shearon Harris Nuclear Plant ~ Unit )I)1 50400 2 OF 3 97 - S01 - 00 TEXT Pl mort spssv fs ssvvvsd, vsv sdditiml sopis ol hlrC Fee 3SQI I)7)
EVENT DESCRIPTION:
At approximately 1500, June 24, 1997, a Corporate Security representative reported to the Site Security.
Superintendent that a contract (non-licensee) employee had been granted unescorted access to plant protected and vital areas without the benefit of adjudication of derogatory information contained within his PHQ that was potentially disqualifying. The individual was granted unescorted access from April 5, 1997 through May 15, 1997.
The subject individual completed a PHQ on March 31, 1997 at the Plant Access Authorization Facility. The individual answered "yes" to a question on the PHQ asking "Have you ever been convicted of an alcohol or a controlled substance related offense, which includes driving while impaired (DWI), or do you presently have such a case pending?" The PHQ further advises that,
" if you answered yes to any question, specific details must be given explaining the circumstances surrounding the case". The individual failed to annotate any details to explain his yes answer to the question. The initial review of the PHQ by plant access authorization personnel failed to identify the "yes" response, which in turn resulted in a failure to seek additional information to explain the response. A subsequent review of the PHQ by Corporate Access Authorization also failed to adjudicate the information resulting in approval/granting unescorted access to plant protected and vital areas on April 5, 1997.
On June 23, 1997, a criminal history record was received from the Federal Bureau of Investigation, together with a criminal records check received from the North Augusta Department of Public Safety, indicating that the individual was convicted of simple possession of an illegal controlled substance on January 20, 1996. In accordance with the Carolina Power and Light criteria for unescorted access, this conviction would disqualify the individual for unescorted access to the company's nuclear plants.
During further review of background investigation case files following this event, an additional instance was identified where an individual was inappropriately granted unescorted access without a valid/approved'psychological evaluation (MMPI). This individuals access should have been denied pending satisfactory resolution of possible alcohol abuse.
Due to this error, unescorted access was granted during the period of time from April 8, 1997 through May 13, 1997.
CAUSE:
The cause of these events was personnel error. The individuals involved in reviewing the background investigation case file records did not apply adequate attention to detail. For the first instance, the initial reviewer in Plant Access Authorization failed to question the individual and obtain the needed information regarding the "yes" answer on the PHQ. In addition, the reviewer at Corporate Access Authorization failed to question or adequately adjudicate the "yes" answer on the subject individual's PHQ and subsequently approved the individual unescorted access. In the second instance, the reviewer at Corporate Access Authorization failed to recognize the need for further evalution of MMPI results regarding possible alcohol abuse.
These errors are contrary to CP&L procedures, AA-DI-02 (Personal History Questionnaire) and NGGS-SEC-1002 (Personal History Questionnaire), and SEC-NGGC-2101 (Nuclear Worker Screening Program for Unescorted Access).
There were no unusual characteristics of the work location that would directly contribute to the errors. All personnel involved, with the exception of the contract individual, were licensee employees.
SAFETY SIGNIFICANCE:
An interview with the Carolina Power and Light supervisor for the subject individuals was conducted, which determined that the individuals work performance was rated as good and that they did not work on any safety related equipment. The work performed by the these individuals included piping replacement in the Turbine Building and crane rigging. This SER is being submitted per the requirements of 10CFR73.71, Reporting of Safeguards Events.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (495)
LlCENSEE EVENT REPORT (LER).
TEXT CONTINUATION FAc)L)TY NAME u) BUCKET LER NUMBER 16) PAGE 13)
SEOUENTIAL REVISION YEAR NUMBER NUMBER Shearon Harris Nuclear Plant ~
Unit //1 50400 3 OF 3 97 - S01 - 00 TEXT r)r Ivvsv spssv rs svpviaf, vsv vddl)vtvsr copes vl A'HC Pvae 3SQI (I 7)
PREVIOUS SIMILAR EVENTS:
A'similar event, contained in Safeguards Event Report Number 89-S05-00, occurred on October 19, 1989. This event was the result of a failure to adjudicate adverse criminal history information that was an element of a background investigation being performed by a contractor who certified a satisfactory full background investigation.
CORRECTIVE ACTIONS COMPLETED:
- 1. The access files for the individuals inappropriately granted unescorted access were placed on access hold in the Personal Access Data system (PADS). This access information has not been transferred to any other utility and flags have been put in place to prevent such transfer in both records.
- 2. A second file review was added to the Corporate Access Authorization adjudication process as an interim measure, pending implementation of permanent corrective actions.
- 3. An initial review of background investigation case files was completed on July 24, 1997, for personnel who were granted temporary unescorted access similar to the subject individuals. This included a review of MMPI test results and PHQ records that required adjudication of "yes" answers. The review disclosed one (1) additional adjudication error that was logged in the HNP Safeguards Event Log (SEL). A'detailed review of all case files for personnel granted temporary unescorted access for the HNP refueling outage (RFO-7) is approximately 55% complete and disclosed the second adjudication failure identified in the event description above. This review has also identified an additional fifteen (15) case file review/adjudication errors that were not reportable, but were logged in the HNP SEL in accordance with 10CFR73.71.
The individuals responsible for making these errors at Corporate Access Authorization and Plant Access Authorization received appropriate disciplinary actions.
CORRECTIVE ACTIONS PLANNED:
- 1. A detailed record review for those personnel granted similar temporary unescorted access to HNP for Refueling Outage 7 is continuing in conjunction with a root cause analysis. This is currently being performed to further investigate the event and identify additional causal factors and corrective measures to preclude recurrence. The results of this review and any other pertinent investigation findings will be provided in a supplement to this SER. The on-going review/investigation will be completed to support an August 30, 1997, SER revision submittal.