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| {{#Wiki_filter:CATEGORY 1~REGULATORY INFORMATION DISTRIBUTION; SYSTEM (RIDS)f ACCESSION NBR:9802240350 DOC.DATE;98/02/20 NOTARIZED: | | {{#Wiki_filter:CATEGORY 1 ~ |
| NO DOCKET FACIL:50-400 Shearon Harris.Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH.NAME AUTHOR AFFILIATION VERRILLI,M. | | REGULATORY INFORMATION DISTRIBUTION; SYSTEM (RIDS) f ACCESSION NBR:9802240350 DOC.DATE; 98/02/20 NOTARIZED: NO DOCKET FACIL:50-400 Shearon Harris. Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH.NAME AUTHOR AFFILIATION VERRILLI,M. Carolina Power & Light Co'. |
| Carolina Power&Light Co'.DONAHUE,J.W. | | DONAHUE,J.W. Carolina Power &, Light Co. |
| Carolina Power&, Light Co.RECIP.NAME RECIPIENT AFFIL'IATXON | | RECIP.NAME RECIPIENT AFFIL'IATXON |
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| ==SUBJECT:== | | ==SUBJECT:== |
| LER 98-002-00:on 980101,solid state protection sys testing deficiency occurred.Caused by inadequate review of initial Tech Specs.TS testing frequency for P-11 permissive revised.W/980217 ltr'.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE!TITLE: 50,.73/50.9 Li.censee Event Report (LER), Incident Rpt,~etc.RECIPIENT 1D CODE/NAME PD2-1 PD COPIES RECIPIENT LTTR ENCL ID CODE/NAME 1 1 FLANDERS,S NOTES:Appli.cation for permit, renewal,fi.led. | | LER 98-002-00:on 980101,solid state protection sys testing deficiency occurred. Caused by inadequate review of initial Tech Specs.TS testing frequency for P-11 permissive revised. |
| COPIES LTTR ENCL 1 1 (05000400(vl (INTERNAL: ACRS AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HXCB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DET/EIB EXTERNAL: L ST LOBBY WARD NOAC POORE,W.NRC PDR 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 m~~sg ENTE DX/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN2 FILE 01 LITCO BRYCE,J H NOAC QUEENER,DS NUDOCS FULL TXT 2 2'1 1, 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 NOTE TO ALL"RIDS" RECIPIENTS: | | W/980217 ltr'. |
| PLEASE HELP US TO REDUCE WASTE~TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION L1ST OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTRO DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUXRED: LTTR 25 ENCL 25 | | DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE! |
| | TITLE: 50,.73/50.9 Li.censee Event Report (LER), Incident Rpt, ~etc. |
| | NOTES:Appli.cation for permit, renewal,fi.led. (05000400( |
| | vl |
| | ( |
| | RECIPIENT COPIES RECIPIENT COPIES 1D CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-1 PD 1 1 FLANDERS,S 1 1 INTERNAL: ACRS AEOD/SPD/RRAB 1 |
| | 1 1 |
| | 1 m~~sg ENTE 2 |
| | '1 2 |
| | 1, NRR/DE/ECGB 1 1 DX/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HXCB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DET/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS: |
| | PLEASE HELP US TO REDUCE WASTE TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION L1ST |
| | ~ |
| | OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTRO DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUXRED: LTTR 25 ENCL 25 |
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| | 0 ~ 4 CP&l Carolina Power 8 Light Company Harris Nuclear Plant Po 8ox 165 New Hill NC 27562 |
| | ~ ~ |
| | FEB 1 7 1998 U.S. Nuclear Regulatory Commission Serial: HNP-98-014 ATTN: NRC Document Control Desk 10CFR50.73 Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 98-002-00 Sir or Madam: |
| | In accordance with 10CFR50.73, the enclosed Licensee Event Report (LER) is submitted. This LER describes a Solid State Protection System testing deficiency that resulted in a violation of Technical Specification required surveillance testing. |
| | Sincerely, J. W. Donahue 1-" |
| | Director of Site Operations Zq i Harris Plant Enclosure ~-<<Q c: Mr. J. B. Brady (HNP Senior NRC Resident) |
| | Mr. L. A. Reyes (NRC Regional Administrator, Region II) |
| | Mr. S. C. Flanders (NRC - NRR Project Manager) 9802240350 'It80220 PDR ADOCK 05000400 8 PDR IIII IIIIIIIIIIII IIIIIIIIIIIIIIIIIIIIII State Road ll34 New Hill NC |
| | |
| | U. S. Nuclear Regulatory Commission Document Control Desk / HNP-98-014 Page 2 of 2 bcc: Ms. D. B. Alexander Mr. R. W. Baylor Mr. T. C, Bell Mr. H. K. Chernoff (RNP) |
| | Mr. B. H. Clark Mr. G. W."Davis Mr. W. J. Dorman (BNP) |
| | Ms. J. P. Gawron (BNP) |
| | Mr. H. W. Habermeyer Mr. W. J. Hindman Ms. C. W. Hobbs (HEEC) |
| | Mr. W. D. Johnson Mr. R. M. Krich Mr. M. B. Keef (HEEC) |
| | Ms. W. C. Langston Mr. C. W. Martin (BNP) |
| | Mr. R. D. Martin Mr. J. W. McKay Mr. B. A. Meyer Mr. P. M. Odom (RNP) |
| | Mr. W. R. Robinson Mr. R. F. Saunders Mr. F. E. Strehle Mr. D. L. Tibbitts Mr. C. A. VanDenburgh Mr. R. L. Warden (RNP) |
| | HNP Real Time Training INPO Harris Licensing File Nuclear Records |
| | |
| | NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB No. 3160%104 (405) 'EXPIRES 04/30/96 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH T)DS MAHDATORT OIFORMATION COILECTION REDDEST: SLD HRS. REPORTED LESSONS LEARNED ARE LZCENSEE EVENT REPORT (LER) OICORPORATED )HTO THE UCEHSING PROCESS ANO FED BACK TO OIOUSTRY. |
| | FORWARD COMMENTS REGAROUIG BURDEN ESTIMATE TO THE INFORMATIDN AND RECORDS MANAGEMENT BRANCH IT@ F33L US, NUCLEAR REGULATORY COMMISS)OH, (See reverse for required number of WASHUIGTO)L DC 20555000), ANO TO THE PAPERWORK REOUCTIOH PROJECT 0150 digits/characters for each block) OI04L OFHCE OF MANAGEMENT ANO BUDGET, WASHUIGTOH, DC 205DL FACIUTY NAME It) DOCKET NUMBER )2) PAGE I3) |
| | Harris Nuclear Plant Unit-1 50-400 1 OF3 TITLE I4) |
| | Solid State Protection System (P-11 Permissive) Testing Deficiency EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (6) |
| | FACIUTY NAME DOCKET NUMBER MONTH SEOUENTIAL REVISION DAY MONTH DAY NUMBER NUMBER FACIUTY NAME 1 21 98 98 002 00 20 98 DOCKET NUMBER 05000 OPERATING THIS REPORT IS SUBMITTED PUR SUANTTO THE REQUIREMENTS OF 10 CFR O: (Check one or more) (11) |
| | MODE (9) 20.'2201 (b) 20.2203(a)(2)(v) X 50.73(a)(2)0) 50.73(a)(2)(viii) |
| | POWER 20.2203(a) (1) 20.2203(a) (3) (i) 50.73(a)(2)(ii) 50.73(a) (2)(x) |
| | LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a) (2)(iii) 73.71 20.2203(a)(2) (ii) 20.2203(a)(4) 50.73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c) (1) 60.73(a) (2) (v) Spec)fy In Abstract below or In NRC Form 366A 20.2203(a) (2) (iv) 50.36(c)(2) 50.73(a)(2)(vii) |
| | LICENSEE CONTACT FOR THIS LER (12) |
| | NAME TELEPHONE NUMBER Urrorude Area Code) |
| | Michael Verrilli Sr. Analyst - Licensing (919) 362-2303 COMPLETE ONE LINE FOR EACH.COMPONENT FAILURE DES CRIBED IN THIS REPORT. (13) |
| | CAUSE COMPONENT REPORTABLE REPORTABLE MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER TO NPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED YES SUBMISSION (lf yes, complete EXPECTED SUBMISSION DATE). X No DATE (16) |
| | ABSTRACT (Umit to 1400 spaces, i.o., approximately 15 single-spaced typewritten lines) (16) |
| | On January 21, 1998, with the plant at approximately 100% power in. Mode 1, Harris Plant Engineering personnel determined that Westinghouse Nuclear Safety Advisory Letter (NSAL) 97-011 was applicable to the HNP Solid State Protection System (SSPS). This NSAL notified the industry that the current SSPS design did not allow for complete overlap testing of the P-11 (Pressurizer Low Pressure) Permissive function at power. |
| | The P-11 Permissive provides the following functions below 2000 psig; (1) allows low pressurizer safety injection to be blocked, (2) allows steamline low pressure safety injection to be blocked, (3) blocks automatic operation of the ressurizer,power operated relief valves, (4) blocks the automatic opep signal for the safety injection accumulators;- |
| | : 5) enables Main Steam Isolation on high steam pressure rate decrease. |
| | NSAL 97-011 explained that the capability to test the P-11 Permissive from the process protection system at power is limited to the setpoint and does not include the overlap to the SSPS logic input relay since the bistable test switch is opened prior to testing the channel. Opening the bistable test switch is required by the SSPS system design to satisfy the test logic for safety injection. Since the SSPS input relay is de-energized above 2000 psig pressurizer, opening of the bistable test switch does not allow the input relay to change state during bistable setpomt verification; and therefore, complete overlap testing for the SSPS input relay is not accomphshed. This condition constitutes a TS surveillance testing violation. |
| | This condition was caused by an inadequate review of initial Technical Specifications for consistency and the capability for testing SSPS permissive signals at power. |
| | Corrective actions will include a revision to the Technical Specification testing frequency for the P-11 Permissive. |
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| CP&l 0~4 Carolina Power 8 Light Company Harris Nuclear Plant Po 8ox 165 New Hill NC 27562 FEB 1 7 1998~~U.S.Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 Serial: HNP-98-014 10CFR50.73 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO.50-400 LICENSE NO.NPF-63 LICENSEE EVENT REPORT 98-002-00 Sir or Madam: In accordance with 10CFR50.73, the enclosed Licensee Event Report (LER)is submitted.
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| This LER describes a Solid State Protection System testing deficiency that resulted in a violation of Technical Specification required surveillance testing.Sincerely, J.W.Donahue Director of Site Operations Harris Plant Zq i 1-" Enclosure~-<<Q c: Mr.J.B.Brady (HNP Senior NRC Resident)Mr.L.A.Reyes (NRC Regional Administrator, Region II)Mr.S.C.Flanders (NRC-NRR Project Manager)9802240350
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| 'It80220 PDR ADOCK 05000400 8 PDR State Road ll34 New Hill NC IIIIIIIIIIIIIIIIIIIIII IIII IIIIIIIIIIII U.S.Nuclear Regulatory Commission Document Control Desk/HNP-98-014 Page 2 of 2 bcc: Ms.D.B.Alexander Mr.R.W.Baylor Mr.T.C, Bell Mr.H.K.Chernoff (RNP)Mr.B.H.Clark Mr.G.W."Davis Mr.W.J.Dorman (BNP)Ms.J.P.Gawron (BNP)Mr.H.W.Habermeyer Mr.W.J.Hindman Ms.C.W.Hobbs (HEEC)Mr.W.D.Johnson Mr.R.M.Krich Mr.M.B.Keef (HEEC)Ms.W.C.Langston Mr.C.W.Martin (BNP)Mr.R.D.Martin Mr.J.W.McKay Mr.B.A.Meyer Mr.P.M.Odom (RNP)Mr.W.R.Robinson Mr.R.F.Saunders Mr.F.E.Strehle Mr.D.L.Tibbitts Mr.C.A.VanDenburgh Mr.R.L.Warden (RNP)HNP Real Time Training INPO Harris Licensing File Nuclear Records NRC FORM 366 (405)U.S.NUCLEAR REGULATORY COMMISSION LZCENSEE EVENT REPORT (LER)(See reverse for required number of digits/characters for each block)APPROVED BY OMB No.3160%104'EXPIRES 04/30/96 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH T)DS MAHDATORT OIFORMATION COILECTION REDDEST: SLD HRS.REPORTED LESSONS LEARNED ARE OICORPORATED)HTO THE UCEHSING PROCESS ANO FED BACK TO OIOUSTRY.FORWARD COMMENTS REGAROUIG BURDEN ESTIMATE TO THE INFORMATIDN AND RECORDS MANAGEMENT BRANCH IT@F33L US, NUCLEAR REGULATORY COMMISS)OH, WASHUIGTO)L DC 20555000), ANO TO THE PAPERWORK REOUCTIOH PROJECT 0150 OI04L OFHCE OF MANAGEMENT ANO BUDGET, WASHUIGTOH, DC 205DL FACIUTY NAME It)Harris Nuclear Plant Unit-1 TITLE I4)Solid State Protection System (P-11 Permissive)
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| Testing Deficiency DOCKET NUMBER)2)50-400 PAGE I3)1 OF3 EVENT DATE (5)LER NUMBER (6)REPORT DATE (7)OTHER FACILITIES INVOLVED (6)MONTH DAY 1 21 98 SEOUENTIAL NUMBER REVISION NUMBER 98-002-00 MONTH DAY 20 98 FACIUTY NAME FACIUTY NAME DOCKET NUMBER DOCKET NUMBER 05000 OPERATING MODE (9)SUANTTO THE REQUIREMENTS OF 10 CFR O: (Check one or more)(11)THIS REPORT IS SUBMITTED PUR 50.73(a)(2)(viii)
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| X 50.73(a)(2)0) 20.'2201 (b)20.2203(a)(2)(v)
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| POWER LEVEL (10)20.2203(a)
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| (1)20.2203(a)(2)(i) 20.2203(a)(2)(ii)20.2203(a)(2)(iii) 20.2203(a)
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| (2)(iv)20.2203(a)
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| (3)(i)20.2203(a)(3)(ii) 20.2203(a)(4) 50.36(c)(1)50.36(c)(2)
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| LICENSEE CONTACT FOR THIS LER (12)50.73(a)(2)(ii) 50.73(a)(2)(iii)50.73(a)(2)(iv) 60.73(a)(2)(v)50.73(a)(2)(vii) 50.73(a)(2)(x)73.71 OTHER Spec)fy In Abstract below or In NRC Form 366A NAME Michael Verrilli Sr.Analyst-Licensing TELEPHONE NUMBER Urrorude Area Code)(919)362-2303 CRIBED IN THIS REPORT.(13)COMPLETE ONE LINE FOR EACH.COMPONENT FAILURE DES CAUSE COMPONENT MANUFACTURER REPORTABLE TO NPRDS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14)YES (lf yes, complete EXPECTED SUBMISSION DATE).X No EXPECTED SUBMISSION DATE (16)MONTH DAY YEAR ABSTRACT (Umit to 1400 spaces, i.o., approximately 15 single-spaced typewritten lines)(16)On January 21, 1998, with the plant at approximately 100%power in.Mode 1, Harris Plant Engineering personnel determined that Westinghouse Nuclear Safety Advisory Letter (NSAL)97-011 was applicable to the HNP Solid State Protection System (SSPS).This NSAL notified the industry that the current SSPS design did not allow for complete overlap testing of the P-11 (Pressurizer Low Pressure)Permissive function at power.The P-11 Permissive provides the following functions below 2000 psig;(1)allows low pressurizer safety injection to be blocked, (2)allows steamline low pressure safety injection to be blocked, (3)blocks automatic operation of the ressurizer,power operated relief valves, (4)blocks the automatic opep signal for the safety injection accumulators;-
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| 5)enables Main Steam Isolation on high steam pressure rate decrease.NSAL 97-011 explained that the capability to test the P-11 Permissive from the process protection system at power is limited to the setpoint and does not include the overlap to the SSPS logic input relay since the bistable test switch is opened prior to testing the channel.Opening the bistable test switch is required by the SSPS system design to satisfy the test logic for safety injection.
| |
| Since the SSPS input relay is de-energized above 2000 psig pressurizer, opening of the bistable test switch does not allow the input relay to change state during bistable setpomt verification; and therefore, complete overlap testing for the SSPS input relay is not accomphshed.
| |
| This condition constitutes a TS surveillance testing violation.
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| This condition was caused by an inadequate review of initial Technical Specifications for consistency and the capability for testing SSPS permissive signals at power.Corrective actions will include a revision to the Technical Specification testing frequency for the P-11 Permissive.
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| i~ | | i~ |
| KRC FORM 366A 16as)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION US.NUClEAR REGUIATORT COMMISSION FACIUTT KAME II)Shaaron Harris Nuciaar Plant~Unit Pl TEXTPlmmewrirnqehCasr~ayerolHRCfemaBQI IIT)DOCKET 50400 LER NUMBER N)TEAR SEOUENTIAl REVISION NUMBER NUMBER 98-002-00 PAGE 0>2 OF 3 EVENT DESCRIPT)OK: | | KRC FORM 366A US. NUClEAR REGUIATORT COMMISSION 16as) |
| On January 21, 1998, with the plant at approximately 100%power in Mode 1, Harris Plant Engineering personnel determined that Westinghouse Nuclear Safety Advisory Letter (NSAL)9711 was applicable to the HNP Solid State Protection System (SSPS).This NSAL notified the industry that the current SSPS design did not allow for complete overlap testing of the P-11 (Pressurizer Low Pressure)Permissive. | | LICENSEE EVENT REPORT (LER) |
| Specifically, the monthly Analog Channel Operational Test (ACOT)required by Technical Specification (TS)4.3.2.1 Table 4.3-2 Item 10a for the P-11 function could not be adequately performed at power.The P-11 Permissive, provides the following functions below 2000 psig;(1)allows low pressurizer safety injection to be blocked, (2)allows steamline low pressure safety injection to be blocked, (3)blocks automatic operation of the pressurizer power operated relief valves, (4)blocks the automatic open signal for the safety injection accumulators, (5)enables Main Steam Isolation on high steam pressure rate decrease, NSAL 97-011 explained that the capability to test the P-11 Permissive from the process protection system at power is limited to the setpoint and does not include the overlap to the SSPS logic input relay since the bistable test switch is opened prior to testing the channel.Opening the bistable test switch is required by the SSPS system design to satisfy the test logic for safety injection. | | TEXT CONTINUATION FACIUTT KAME II) DOCKET LER NUMBER N) PAGE 0> |
| Since the SSPS input relay is de-energized above 2000 psig pressurizer, opening of the bistable test switch does not allow the input relay to change state during bistable setpoint verification; and therefore, complete overlap testing for the SSPS input relay is not accomplished. | | SEOUENTIAl REVISION TEAR NUMBER NUMBER Shaaron Harris Nuciaar Plant ~ |
| At 1025 hours on January 21, 1998, this condition was determined to be a violation of TS surveillance requirement 4.3.2.1 due to inadequate past testing of the P-11 Permissive. | | Unit Pl 50400 2 OF 3 98 - 002 - 00 TEXTPlmmewrirnqehCasr~ayerolHRCfemaBQI IIT) |
| TS 4.0.3 was entered at this time to allow proper P-11 testing.NSAL 97-011 recommended that a Technical Specification change be initiated to revise the ACOT surveillance frequency to"Refueling" based on relay reliability and consistency with other Reactor Protection System permissive signals.Alternately, a modification was also recommended to allow failing of the P-11 function low for testing.HNP initially elected to revise the surveillance procedure to fail the P-11 low by lifting transmitter leads.However, during a Hams Plant Engineering review of the proposed procedure changes intended to implement the recommended testing, a potential unreviewed safety question was identified per 10CFR50.59. | | EVENT DESCRIPT)OK: |
| This potential unreviewed safety question was related to the failure to comply with single failure criterion of IEEE Standard 338 (1971), while in the temporary test configuration. | | On January 21, 1998, with the plant at approximately 100% power in Mode 1, Harris Plant Engineering personnel determined that Westinghouse Nuclear Safety Advisory Letter (NSAL) 9711 was applicable to the HNP Solid State Protection System (SSPS). This NSAL notified the industry that the current SSPS design did not allow for complete overlap testing of the P-11 (Pressurizer Low Pressure) Permissive. Specifically, the monthly Analog Channel Operational Test (ACOT) required by Technical Specification (TS) 4.3.2.1 Table 4.3-2 Item 10a for the P-11 function could not be adequately performed at power. |
| Based on this concern, it became apparent that testing would not be completed within the allotted 24 hours per TS 4.0.3;therefore, P-11 was declared inoperable. | | The P-11 Permissive, provides the following functions below 2000 psig; (1) allows low pressurizer safety injection to be blocked, (2) allows steamline low pressure safety injection to be blocked, (3) blocks automatic operation of the pressurizer power operated relief valves, (4) blocks the automatic open signal for the safety injection accumulators, (5) enables Main Steam Isolation on high steam pressure rate decrease, NSAL 97-011 explained that the capability to test the P-11 Permissive from the process protection system at power is limited to the setpoint and does not include the overlap to the SSPS logic input relay since the bistable test switch is opened prior to testing the channel. Opening the bistable test switch is required by the SSPS system design to satisfy the test logic for safety injection. Since the SSPS input relay is de-energized above 2000 psig pressurizer, opening of the bistable test switch does not allow the input relay to change state during bistable setpoint verification; and therefore, complete overlap testing for the SSPS input relay is not accomplished. |
| A comprehensive TS surveillance procedure review project is currently in progress to support HNP's conversion to the new Westinghouse Improved Standard Technical Specifications. | | At 1025 hours on January 21, 1998, this condition was determined to be a violation of TS surveillance requirement 4.3.2.1 due to inadequate past testing of the P-11 Permissive. TS 4.0.3 was entered at this time to allow proper P-11 testing. NSAL 97-011 recommended that a Technical Specification change be initiated to revise the ACOT surveillance frequency to "Refueling" based on relay reliability and consistency with other Reactor Protection System permissive signals. Alternately, a modification was also recommended to allow failing of the P-11 function low for testing. HNP initially elected to revise the surveillance procedure to fail the P-11 low by lifting transmitter leads. However, during a Hams Plant Engineering review of the proposed procedure changes intended to implement the recommended testing, a potential unreviewed safety question was identified per 10CFR50.59. This potential unreviewed safety question was related to the failure to comply with single failure criterion of IEEE Standard 338 (1971), while in the temporary test configuration. Based on this concern, it became apparent that testing would not be completed within the allotted 24 hours per TS 4.0.3; therefore, P-11 was declared inoperable. |
| This project had not reviewed the surveillance procedures associated with P-11 testing when this condition was identified. | | A comprehensive TS surveillance procedure review project is currently in progress to support HNP's conversion to the new Westinghouse Improved Standard Technical Specifications. This project had not reviewed the surveillance procedures associated with P-11 testing when this condition was identified. Review of this section of TS and the corresponding surveillance procedures are currently scheduled to begin in mid 1998. |
| Review of this section of TS and the corresponding surveillance procedures are currently scheduled to begin in mid 1998.6 CAUSE: This condition was caused by an inadequate review of initial Technical Specifications for consistency with other permissive signals and the capability for testing SSPS permissive signals at power.The TS testing frequency for the P-6, P-7, P-8, P-10 and P-13 permissives, which have the same relay reliability, are"once per refueling outage," which would allow testing while shutdown. | | 6 CAUSE: |
| E't NRC FORM 666A 1486)LICENSEE EVENT REPORT (LEB)'EXT CONTINUATION 0 US NUCKla REGULATORT COMMISSION lI'FACIUTT NAME (I)Shearon Harris Nuclear Plant~Unit fl OOGNET 50400.LER NUMBER 16)TEAR SEOUENTIAL NET)SION NUMBER NUMBER 98-002-00 PAGE 6))'3*OF" 3 TEXT Irr mn s)ssst Fs sFSaasL sssd id%')ssal copies oMRC hnss 36@I (IT)SAFETY SIGNIFICANCE: | | This condition was caused by an inadequate review of initial Technical Specifications for consistency with other permissive signals and the capability for testing SSPS permissive signals at power. The TS testing frequency for the P-6, P-7, P-8, P-10 and P-13 permissives, which have the same relay reliability, are "once per refueling outage," |
| There weie no actual safety.consequences associated with the failure to provide complete overlap testing for the P-11 perimssive function.The inability to completely test;the.P-11'function above 2000 psig pressurizer'pressure would potentially cause an inoperable SSPS input relay to remain undetected until pressurizer pressure drops below 2000 psig.If this inoperability existed, the operators would not be able to manually block safety injection. | | which would allow testing while shutdown. |
| This would be~operational concern, but not a safety issue.Additionally, the reliability of the SSPS input relaysshas been excellent. | | |
| There have been no failures of the 258 input relays in 10 years of operation. | | E |
| i'his event is being reported.as a condition prohibited by TS per 10CFR50.73.a.2.i.B. | | 't |
| '")'REVIOUS SIMILAR EVENTS: LER 97-24 was submitted to the NRC on December 18,:1997.This LER also reported a SSPS testing'deficiency, but was specifically related to a logic card failure scenario.Therefore, the corrective actions completed for.LER 97-24 would not have been expected to identify'the P-11 overlap testing issue.CORRECTIVE ACTIONS PLANNED: 1.A revision to Technical Specification 4.3.2.1 Table 4.3-2 Item 10a will be developed and submitted to the NRC.This revision will change the P-11 and not P-11 ACOT to a"Refueling" frequency. | | |
| This will be completed by April 30, 1998. | | NRC FORM 666A 0 US NUCKla REGULATORT COMMISSION 1486) |
| P.l~t l}} | | LICENSEE EVENT REPORT (LEB) l I' |
| | 'EXT CONTINUATION FACIUTT NAME (I) OOGNET LER NUMBER 16) PAGE 6)) |
| | SEOUENTIAL NET)SION TEAR NUMBER NUMBER Shearon Harris Nuclear Plant ~ |
| | Unit fl 50400 . |
| | - - |
| | '3 |
| | * OF" 3 98 002 00 TEXT Irr mn s)ssst Fs sFSaasL sssd id%')ssal copies oMRC hnss 36@I (IT) |
| | SAFETY SIGNIFICANCE: |
| | There weie no actual safety. consequences associated with the failure to provide complete overlap testing for the P-11 perimssive function. The inability to completely test;the.P-11'function above 2000 psig pressurizer'pressure would potentially cause an inoperable SSPS input relay to remain undetected until pressurizer pressure drops below 2000 psig. If this inoperability existed, the operators would not be able to manually block safety injection. This would be~ operational concern, but not a safety issue. Additionally, the reliability of the SSPS input relaysshas been excellent. There have been no failures of the 258 input relays in 10 years of operation. |
| | i'his event is being reported. as a condition prohibited by TS per 10CFR50.73.a.2.i.B. |
| | SIMILAREVENTS: |
| | '")'REVIOUS LER 97-24 was submitted to the NRC on December 18,:1997. This LER also reported a SSPS testing'deficiency, but was specifically related to a logic card failure scenario. Therefore, the corrective actions completed for. |
| | LER 97-24 would not have been expected to identify'the P-11 overlap testing issue. |
| | CORRECTIVE ACTIONS PLANNED: |
| | : 1. A revision to Technical Specification 4.3.2.1 Table 4.3-2 Item 10a will be developed and submitted to the NRC. This revision will change the P-11 and not P-11 ACOT to a "Refueling" frequency. This will be completed by April 30, 1998. |
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| | P. |
| | l l |
| | ~ t}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:RO)
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A9151999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Shearon Harris Npp. with 991012 Ltr ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18017A8621999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Harris Nuclear Plant.With 990908 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18017A8361999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Shearon Harris Nuclear Power Plant.With 990811 Ltr ML18016B0151999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Shearon Harris Npp. with 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990614 Ltr ML18017A8981999-05-12012 May 1999 Technical Rept Entitled, Harris Nuclear Plant-Bacteria Detection in Water from C&D Spent Fuel Pool Cooling Lines. ML18016A9581999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990513 Ltr ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8941999-04-0505 April 1999 Revised Pages 20-25 to App 4A of non-proprietary Version of Rev 3 to HI-971760 ML18016A9101999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Shearon Harris Nuclear Power Plant.With 990413 Ltr ML18016A8661999-03-31031 March 1999 Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept. ML18017A8931999-02-28028 February 1999 Risks & Alternative Options Associated with Spent Fuel Storage at Shearon Harris Nuclear Power Plant. ML18016A8551999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Shearon Harris Npp. with 990312 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8531999-02-18018 February 1999 Non-proprietary Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFP 'C' & 'D'. ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18022B0631999-02-0404 February 1999 Rev 0 to Nuclear NDE Manual. with 28 Oversize Uncodable Drawings of Alternative Plan Scope & 4 Oversize Codable Drawings ML20202J1161999-02-0101 February 1999 SER Accepting Relief Requests Associated with Second 10-year Interval Inservice Testing Program ML18016A8041999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Shearon Harris Nuclear Power Plant.With 990211 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7801998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Shearon Harris Npp. with 990113 Ltr ML18016A7671998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Shnpp,Unit 1.With 981215 Ltr ML18016A9731998-11-28028 November 1998 Changes,Tests & Experiments, for Harris Nuclear Plant.Rept Provides Brief Description of Changes to Facility & Summary & of SE for Each Item That Was Implemented Under 10CFR50.59 Between 970608-981128.With 990527 Ltr ML18016A8351998-11-28028 November 1998 ISI Summary 8th Refueling Outage for Shearon Harris Power Plant,Unit 1. ML18016A7411998-11-25025 November 1998 Rev 1 to Shnpp Cycle 9 Colr. ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A7071998-11-0303 November 1998 Rev 0 to Harris Unit 1 Cycle 9 Colr. ML18016A7201998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Shearon Harris Nuclear Power Plant.With 981113 Ltr ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves ML18016A6201998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Harris Nuclear Power Plant.With 981012 Ltr ML18016A5971998-09-21021 September 1998 Rev 1 to Harris Unit 1 Cycle 8 Colr. ML18016A5881998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Shnpp,Unit 1.With 980914 Ltr ML18016A5071998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Shearon Harris Nuclear Plant.W/980811 Ltr ML18016A9431998-07-0707 July 1998 Rev 1 to QAP Manual. ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A9371998-06-30030 June 1998 Technical Rept on Matl Identification of Spent Fuel Piping Welds at Hnp. ML18016A4861998-06-30030 June 1998 Monthly Operating Rept for June 1998 for SHNPP.W/980715 Ltr ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18016A4521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Shearon Harris Nuclear Power Plant.W/980612 Ltr ML18016A7711998-05-26026 May 1998 Non-proprietary Rev 2 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris Spent Fuel Pools 'C' & 'D'. 1999-09-30
[Table view] |
Text
CATEGORY 1 ~
REGULATORY INFORMATION DISTRIBUTION; SYSTEM (RIDS) f ACCESSION NBR:9802240350 DOC.DATE; 98/02/20 NOTARIZED: NO DOCKET FACIL:50-400 Shearon Harris. Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH.NAME AUTHOR AFFILIATION VERRILLI,M. Carolina Power & Light Co'.
DONAHUE,J.W. Carolina Power &, Light Co.
RECIP.NAME RECIPIENT AFFIL'IATXON
SUBJECT:
LER 98-002-00:on 980101,solid state protection sys testing deficiency occurred. Caused by inadequate review of initial Tech Specs.TS testing frequency for P-11 permissive revised.
W/980217 ltr'.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE!
TITLE: 50,.73/50.9 Li.censee Event Report (LER), Incident Rpt, ~etc.
NOTES:Appli.cation for permit, renewal,fi.led. (05000400(
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RECIPIENT COPIES RECIPIENT COPIES 1D CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-1 PD 1 1 FLANDERS,S 1 1 INTERNAL: ACRS AEOD/SPD/RRAB 1
1 1
1 m~~sg ENTE 2
'1 2
1, NRR/DE/ECGB 1 1 DX/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HXCB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DET/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION L1ST
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OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTRO DESK (DCD) ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUXRED: LTTR 25 ENCL 25
0 ~ 4 CP&l Carolina Power 8 Light Company Harris Nuclear Plant Po 8ox 165 New Hill NC 27562
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FEB 1 7 1998 U.S. Nuclear Regulatory Commission Serial: HNP-98-014 ATTN: NRC Document Control Desk 10CFR50.73 Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 98-002-00 Sir or Madam:
In accordance with 10CFR50.73, the enclosed Licensee Event Report (LER) is submitted. This LER describes a Solid State Protection System testing deficiency that resulted in a violation of Technical Specification required surveillance testing.
Sincerely, J. W. Donahue 1-"
Director of Site Operations Zq i Harris Plant Enclosure ~-<
SEOUENTIAl REVISION TEAR NUMBER NUMBER Shaaron Harris Nuciaar Plant ~
Unit Pl 50400 2 OF 3 98 - 002 - 00 TEXTPlmmewrirnqehCasr~ayerolHRCfemaBQI IIT)
EVENT DESCRIPT)OK:
On January 21, 1998, with the plant at approximately 100% power in Mode 1, Harris Plant Engineering personnel determined that Westinghouse Nuclear Safety Advisory Letter (NSAL) 9711 was applicable to the HNP Solid State Protection System (SSPS). This NSAL notified the industry that the current SSPS design did not allow for complete overlap testing of the P-11 (Pressurizer Low Pressure) Permissive. Specifically, the monthly Analog Channel Operational Test (ACOT) required by Technical Specification (TS) 4.3.2.1 Table 4.3-2 Item 10a for the P-11 function could not be adequately performed at power.
The P-11 Permissive, provides the following functions below 2000 psig; (1) allows low pressurizer safety injection to be blocked, (2) allows steamline low pressure safety injection to be blocked, (3) blocks automatic operation of the pressurizer power operated relief valves, (4) blocks the automatic open signal for the safety injection accumulators, (5) enables Main Steam Isolation on high steam pressure rate decrease, NSAL 97-011 explained that the capability to test the P-11 Permissive from the process protection system at power is limited to the setpoint and does not include the overlap to the SSPS logic input relay since the bistable test switch is opened prior to testing the channel. Opening the bistable test switch is required by the SSPS system design to satisfy the test logic for safety injection. Since the SSPS input relay is de-energized above 2000 psig pressurizer, opening of the bistable test switch does not allow the input relay to change state during bistable setpoint verification; and therefore, complete overlap testing for the SSPS input relay is not accomplished.
At 1025 hours0.0119 days <br />0.285 hours <br />0.00169 weeks <br />3.900125e-4 months <br /> on January 21, 1998, this condition was determined to be a violation of TS surveillance requirement 4.3.2.1 due to inadequate past testing of the P-11 Permissive. TS 4.0.3 was entered at this time to allow proper P-11 testing. NSAL 97-011 recommended that a Technical Specification change be initiated to revise the ACOT surveillance frequency to "Refueling" based on relay reliability and consistency with other Reactor Protection System permissive signals. Alternately, a modification was also recommended to allow failing of the P-11 function low for testing. HNP initially elected to revise the surveillance procedure to fail the P-11 low by lifting transmitter leads. However, during a Hams Plant Engineering review of the proposed procedure changes intended to implement the recommended testing, a potential unreviewed safety question was identified per 10CFR50.59. This potential unreviewed safety question was related to the failure to comply with single failure criterion of IEEE Standard 338(1971), while in the temporary test configuration. Based on this concern, it became apparent that testing would not be completed within the allotted 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> per TS 4.0.3; therefore, P-11 was declared inoperable.
A comprehensive TS surveillance procedure review project is currently in progress to support HNP's conversion to the new Westinghouse Improved Standard Technical Specifications. This project had not reviewed the surveillance procedures associated with P-11 testing when this condition was identified. Review of this section of TS and the corresponding surveillance procedures are currently scheduled to begin in mid 1998.
6 CAUSE:
This condition was caused by an inadequate review of initial Technical Specifications for consistency with other permissive signals and the capability for testing SSPS permissive signals at power. The TS testing frequency for the P-6, P-7, P-8, P-10 and P-13 permissives, which have the same relay reliability, are "once per refueling outage,"
which would allow testing while shutdown.
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NRC FORM 666A 0 US NUCKla REGULATORT COMMISSION 1486)
LICENSEE EVENT REPORT (LEB) l I'
'EXT CONTINUATION FACIUTT NAME (I) OOGNET LER NUMBER 16) PAGE 6))
SEOUENTIAL NET)SION TEAR NUMBER NUMBER Shearon Harris Nuclear Plant ~
Unit fl 50400 .
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- OF" 3 98 002 00 TEXT Irr mn s)ssst Fs sFSaasL sssd id%')ssal copies oMRC hnss 36@I (IT)
SAFETY SIGNIFICANCE:
There weie no actual safety. consequences associated with the failure to provide complete overlap testing for the P-11 perimssive function. The inability to completely test;the.P-11'function above 2000 psig pressurizer'pressure would potentially cause an inoperable SSPS input relay to remain undetected until pressurizer pressure drops below 2000 psig. If this inoperability existed, the operators would not be able to manually block safety injection. This would be~ operational concern, but not a safety issue. Additionally, the reliability of the SSPS input relaysshas been excellent. There have been no failures of the 258 input relays in 10 years of operation.
i'his event is being reported. as a condition prohibited by TS per 10CFR50.73.a.2.i.B.
SIMILAREVENTS:
'")'REVIOUS LER 97-24 was submitted to the NRC on December 18,:1997. This LER also reported a SSPS testing'deficiency, but was specifically related to a logic card failure scenario. Therefore, the corrective actions completed for.
LER 97-24 would not have been expected to identify'the P-11 overlap testing issue.
CORRECTIVE ACTIONS PLANNED:
- 1. A revision to Technical Specification 4.3.2.1 Table 4.3-2 Item 10a will be developed and submitted to the NRC. This revision will change the P-11 and not P-11 ACOT to a "Refueling" frequency. This will be completed by April 30, 1998.
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