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 Issue dateTitleTopic
ML20024E6604 August 1983RO 83-18:on 830804,during Maint Insps on Hydraulic Snubbers, Two Small Bore Snubbers Identified as Being Installed on RCS Hot Leg Vent Piping Downstream of Valves RC-V15A & B.Caused by Personnel Error
ML20050A54318 March 1982Ro:On 820318,water W/Ph of 3.5 Was Discharged from Secondary Waste Water Neutralizing Tank WT-T-1 Into Plant Discharge Effluent Stream.Caused by Accidental Overflow of Approx 2,500 Gallons of Water from Neutralizing Tank
ML20039C63323 December 1981RO 81-14:nine Pipe Support & Structural Interfacing Areas Identified Requiring Further Evaluation & Potential Corrective Action.Failure of Pipe Supports Could Damage safety-related Components.Followup Rept Expected in 14 Days
ML19345A97417 November 1980RO 80-013/03L-0 Committed to Forwarding Final Valve Testing Evaluation by 801101.Investigation Requires More Time than Anticipated.Requests Extension Until 801219
ML19338F54623 September 1980RO 80-17:on 800923,determined That There Is Insufficient Documentation to Demonstrate Environ Qualification of Brakes on Motor Operators for Purge Valves AH-V1B & AH-V1C. Cause Not Stated.Corrective Action Will Be Submitted
ML19337A86323 September 1980RO 80-17:determined Insufficient Documentation to Demonstrate That Brakes on Motor Operators for Purge Valves AH-V1B & AH-V1C Environmentally Qualified.Redundant Valves Fully Qualified
ML19330C3044 August 1980Ro:On 800716,during Radiation Emergency Exercise,Use of Emergency Notification Sys Phone Line Became Uncertain, Making Accurate Info Transfers Questionable.Recommends That Microphone Headset Be Made Available to Allow Mobility
ML19326E20622 July 1980RO 80-15/4P:confirming 800722 Telcon,On 800721,river Water Discharge Temp Was More than 3 F Below Inlet River Water Temp for Approx 6-h.Incident Will Be Reviewed to Determine Corrective Action.Review to Be Included in Followup Rept
ML19326E08427 June 1980RO 80-12/IP:during Review of Equipment Required by IE Bulletin 79-01B,found That post-accident Pressure & Temp Would Be Higher than Postulated in NSC 730705 Rept.Short & long-term Action to Be Discussed in Followup Rept
ML19323H3426 June 1980RO-80-10/1P:on 800603,B&W Ltr Informed Util of Potential Reportability of Steam Generator Tube Rupture Safety Analysis.Caused by Nonconservative Error in Fsar.Corrective Action Will Be Addressed in Followup Rept
ML19323D51523 April 1980RO 80-07/TP:on 800423 Results of Radiographic Exams of Piping Welds Associated W/Reactor Bldg Penetrations 415-16 for Leak Rate Test Sys Showed Several Welds Not within Tech Specs.Unit Is Shut Down
ML19309A78326 March 1980RO 80-06/1P:on 800325,during Refueling Frequency Reactor Bldg Local Leak Rate Test of Valve RB-V7,updated Total Leakage Exceeded Tech Specs.Testing Is Continuing W/Approx 1/4 of Test Program Complete
ML19322B5088 November 1979RO 79-17/1P:on 791108 Support Boltings for Rigid Anchor DHH-127A Found to Be Inadequate in Design & Installation. Details & Corrective Action Will Be Addressed in Followup Rept
ML19308A5242 February 1978RO 78-08/1P:on 780202,util Informed by NSSS of Deviation Discovered Between FSAR Steam Line Break Analysis & Actual Operating Parameters.Procedure Mod Will Limit Secondary Site Water Volume
ML19308A50820 January 1978RO 78-05/1P:on 780119,Plant Operations Review Committee Determined That Containment Integrity Had Been Violated by Opening of Valve BS-V47A & B Following Test of BS-P1A & B. Procedure Mod Will Terminate Operation of BS-V-47A & B
ML19308A50917 January 1978Confirms Telcon on 780117 Re Excessive Leak Off from 1A Makeup Pump Discharge Isolation Valve MU-V-74A Resulting in Gaseous Release 500 Times in Excess of 10CFR20 Limits for Xe-133 & Xe-135.Valve Back Seated,Isolating Leak Off
ML19308A51112 January 1978RO 78-2/1P:on 780112,it Was Recognized That Continuous Fire Watch Was Not Established for 63-h After a Emergency Diesel Room Sprinkler Isolation Valve FS-V-156 Was Closed.Caused by Personnel Error.Fire Watch Established on 780112Continuous fire watch
Fire Watch
ML19261F2956 January 1978RO 78-01/1P:on 780106,util Informed by B&W That During Certain Transients,Difference Between out-of-core Detectors & Heat Balance May Exceed 4% of Full Power.Frequency of Heat Balance Checks Increased
ML19261F29619 December 1977RO 77-29/1P:on 771216,B&W Informed Met Ed That Volume Per Tech Specs Was Insufficient to Bring Reactor to Cold Shutdown condition.TMI-1 Immediately Increased Volume of Source of Concentrated Boric Acid SolutionBoric Acid
ML19268B96819 December 1977RO 77-30/1P:on 771216,B&W Informed Met Ed That Software Used to Calculate Incore Imbalance Was in Error,In That Background Correction Was Misapplied as Detector Depletes. Error Will Be Corrected Prior to Cycle 4 Operation
ML19308A5135 December 1977RO 77-27/1P:on 771203,technician Unable to Open Outer Door of Reactor Bldg Personnel Air Lock.Caused by Jammed Linkage. Reactor Shut Down During Repair of Door Closing Mechanism
ML19308A51615 November 1977RO 77-26/1P:on 771114,quadrant Power Tilt Exceeded +2.66% W/Reactor at 15% Full Power During Power Escalation Following Reactor Trip.Within 4-h,quadrant Power Tilt Not Reduced
ML19261F3095 October 1977RO 77-23/1T:on 770920,both Doors of Reactor Bldg Emergency Personnel Access Hatch Open Simultaneously.Caused by Personnel Error.Doors Closed.Forwards LER 77-23/1T
ML19261F31220 September 1977RO 77-23/1P:on 770920,containment Integrity Violated When Both Doors in Reactor Bldg Personnel Access Hatch Were Open for Approx 10 Minutes.Caused by Problem W/Door Interlock. Interlock & Door Seals Tested
ML19261F3139 September 1977RO 77-22/1T:on 770825,B&W-required Operating Restrictions on Decay Heat Removal Pumps Found Contrary to Description of Pump Operating Capability Per Fsar.Caused by B&W Failure to Perform Safety Evaluation.Corrective Action by 770923.W/LER
ML19308A52026 August 1977RO 77-22/1P:confirms 770825 Telcon That as Result of B&W New Decay Heat Pump Operating Limitations,Remedial or Corrective Action Could Be Required to Prevent Unsafe Condition. Procedure Change Initiated to Incorporate New Limitations
ML19261F31612 August 1977RO 77-19/3L:on 770713,leak in Miscellaneous Waste Evaporator Feed Tank Immersion Heater Shorted Out Heater & Feed Pump. Caused by Matl Failure in Heater Temp Element.Heater Replaced & Operating Procedure Modified.Forwards LER
ML19261F3199 August 1977RO 77-21/1T:on 770726,radiation Monitor RM-A2 Out of Svc & Sample of Reactor Bldg Atmosphere Not Taken within 8-h. Caused by Improper Reassembly Following 770725 Surveillance Test.Monitor Repaired & Sample Taken.Forwards LERGrab sample
ML19210A5445 August 1977Followup Rept to 770707 Ltr Re Ro:On 770613,radwaste Shipment Leak Discovered.Caused by Acidic Attack of Mild Steel Container at Locations of Incomplete Coverage W/Internal Corrosion Resistant Coating
ML19261F32227 July 1977RO 77-18/31:on 770629,Nuclear Svcs River Water Pump NR-P1C Shaft Failed While Operating,Leading to Operation in Degraded Mode.Caused by Mechanical & Procedural Problems. Pump Overhauled,Preventive Maint Procedures to Be Changed
ML19308A52127 July 1977RO 77-21/1P:on 770726,radiation Monitor RM-A2 Out of Svc & Sample of Reactor Bldg Atmosphere Not Taken within 8-h. Caused by Improper Reassembly Following 770725 Surveillance Test.Monitor Repaired & Valid Sample Taken
ML19308A52320 July 1977RO 77-20/4P:on 770719,ETS Violated in That Plant River Water Discharge Temp Exceeded Limit of 3 F Below Inlet River Water Temp for 10 Minutes.Caused by Passing Storm Front Which Decreased Ambient Air Temp from 94 to 82 F
ML19308A52220 July 1977RO 77-20/4P:on 770619,ETS Violated in That Plant River Water Discharge Temp Exceeded Limit of 3 F Below Inlet River Water Temp.Caused by Passing Storm Front Which Lowered Ambient Air Temp from 94 to 82 F
ML19261F32520 July 1977RO 77-17/3L:on 770624,inner Door Seal on Personnel Access Hatch Leaked Excesively,Causing Total Reactor Bldg Local Leakage to Exceed Tech Spec 4.4.1.2.3.Caused by Improper Door Installation Procedures.Forwards LER
ML19261F3297 July 1977RO on 770713:Tri-State Motor Transit Co Driver Observed Radwaste Leaking from Container on Truck While at Rest Area. Caused by Pinhole Leak in One Liner.Truck Returned to Station Site
ML19261F33028 June 1977RO 77-15/3L:on 770529,one of Two Units of 230/4.16 Kv Auxiliary Transformer de-energized,leading to Operation in Degraded Mode Permitted by Tech Spec 3.7.2.b.Caused by Wiring Error on Current Transformers.Sys Repaired.Ler Encl
ML19261F33320 June 1977RO 77-14/3L:on 770524,reactor Bldg Isolation Valve RB-V7 Failed to Close on Engineering Safeguards Test Signal, Leading to Operation in Degraded Mode Permitted by Limiting Condition for Operation Per Tech Spec 3.6.6
ML19261F3369 June 1977RO 77-12/3L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Operability of Redundant Pump.Caused by Personnel Error.Redundant Pump Tested Satisfactorily on 770519.Forwards LER 77-12/03L
ML19261F3397 June 1977RO 77-13/4T:on 770523,analysis of Plant River Water Discharge Showed Concentration of 760 Parts Per Million. Caused Either by Slug of High Concentration of Suspended Solids from Filter Sump or by Poor Sample.Forwards LER
ML19322A43810 May 1977RO 77-07/1P:on 770510,both Reactor Containment Bldg Emergency Personnel Access Doors Open at Same Time.Caused by Closed Outer Door Mechanism While Door Still Was Open
ML19322A43918 April 1977RO 77-04/1P:on 770415,nonconservative Error Found in Safety Analysis to Support Increase in Pressurizer Code Safety Valve Setpoint to 2500 Psig.Caused by Erroneous Assumptions Made for Total Combined Relief Valve Capacity
ML19253B96322 March 1977RO 77-02/04T:on 770304,river Water Discharge Temp Exceeded Inlet River Water Temp Limitation by 14 F Per Ets.Caused by Insufficient Procedures,Personnel Error,Abnormal Ambient Conditions & Low River Water Temp.Ler Encl
ML19322A44020 March 1977RO 77-05/4P:on 770319,river Water Discharge Temp Differential Change More than 2 Degrees in 1-h.Steps Taken to Reduce Decay Heat Removal Load,Reducing River Water Temp Change
ML19253B9628 March 1977RO 77-02/04P:on 770304,river Water Discharge Temp Exceeded Inlet River Water Temp by 14 F,Violating 12 F Limit Per Ets. Caused by Low Inlet Temp & High Ambient Temp.Temp Reduced Below Limit
ML19210A2683 February 1977RO 77-1/1P:on 770202,both a & B Diesel Generators Had Conditions Affecting Starting Capabilities in Response to Loss of Offsite Power.Both Problems Caused by Cranking Timer Timing Out Prior to Oil Low Speed Switch Operation
ML19261F17729 December 1976RO 76-50/4O:on 761221,radionucleide Surface Water Level Ten Times Background Level.Probable Cause Is Chinese Weapons Test,Since Neither Zr-95 Nor Nb-95 Discharged to River from Station During Nov 1976
ML19261F18826 December 1976RO 76-047/01T:on 761216,sodium Hydroxide Tank Levels Fell Below Required Minimum.Caused by Personnel Misreading Tank Level Data & Technical Analyst Failing to Notice Mistake
ML19261F25320 December 1976RO 76-48/4o:on 761208,isotope Level Samples from TMI Environs Ten Times Background Levels.Chinese Weapons Tests Probably Caused Excesses of I-131,Zr-95,Nb-95,Ce-141 & Ru-103 in Sediment Samples from TMI
ML19261F25614 December 1976Nonroutine 30 Day Rept 75-03,advising That Heated Post Gap Measurements within Acceptable Values.Test Schedule Change Warranted from Weekly to After Each Startup,Once Full Steam Equilibrium Reached & on Monthly Basis Thereafter
ML19308A48113 December 1976RO 76-46/1P:on 761212,boron Concentrations in Borated Water Storage Tank Found Below Required Minimum.Boric Acid Injected to Return Concentration to Necessary Valve.Possibly Caused by Water Leakage from Reactor Coolant SysBoric Acid