RO 77-12/3L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Operability of Redundant Pump.Caused by Personnel Error.Redundant Pump Tested Satisfactorily on 770519.Forwards LER 77-12/03L| ML19261F336 |
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Crane  |
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| Issue date: |
06/09/1977 |
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Herbein J METROPOLITAN EDISON CO. |
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| ML19261F337 |
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| References |
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| GQL-0790, GQL-790, NUDOCS 7910250795 |
| Download: ML19261F336 (3) |
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LER-1977-012, RO 77-12/3L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Operability of Redundant Pump.Caused by Personnel Error.Redundant Pump Tested Satisfactorily on 770519.Forwards LER 77-12/03L |
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| 2891977012R00 - NRC Website |
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DATC CF OCCU?.tCU T Metropolitan Edison Company 6/9/77 Mr. J. P. O'Reilly Reading, Pa.
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METROPOLITAN EDISON COMPANY POST OFFICE BOX 542 READING. PENNSYLVANI A 19603 TELEPHON
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June 9, 1977
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Dear Sir:
Docket No. 50-289 Operating license No. DPR-50 In accordance with the Technics 1 Specifications of cur Three Mile Island Nuclear Station Unit 1 (TMI-1), we are reporting the folleving reportable occurrence.
(1) Report Number: 77-12/3L (2a) Required Report Date: 06-17-77 (2b) Date of Occurrence: 05-19-77 (3) Facility: Three Mile Island Nuclear Station - Unit I (k) Identificaticn of Occurrence:
Title: Engineered Safeguards pu=p was removed prior to testing redundant pu=p.
Type: A reportable occurrence as defined by Technical Specificatiens 6.9.2.3.(3) in that, Engineered Safeguard pump MU-P-1A was removed frem service prior to testing the operability of the redundant pu=p, MU-P-lC, violating sections 3.3.4, of the Technical Specifications, and resulting in an inadequacy in the implementation of procedural acntrols which threatened to cause a reducticn in the degree of redundancy of an engineered safety fe ature.
(5) Conditions Prior to Occurrence Pcwer: Core: 192h Elec: 631 RC Flev:
lhhx106 lbs/hr RC Pressure:
2155 psig RC Te=p:
579cy 1482 072 P'iZR Level:
220 inches PR"R Te=p:
oL5 F (6) Descriptien of Occurrence:
While escalating to 755 pcVer felleving the refueling cutage Engineered Safeguards pump, MU-P-1A, was re=cved frem service prier to testing the Operability Of the redundant Engineered Safeguard pump, MU-P-lC.
7 71 i 7' "3 ^7
June 9,1977 Mr. J. P. O'Reilly GQM 0790 (T) Apparent Cause of Occurrence:
The cause of this occurrence has been determined to be personnel in that, at the time MU-P-1A was removed from service the Shift Foreman failed to Lnplement the req 2 ire =ent to test the redundant pump.
(3) Ana2yais of Occurrence:
It has been determined that this occurrence did not constitute a threat to the health and safety of the public in that, the redundant pump, MU-P-1C, had been demonstrated cperable ten (10) days prior to the occurrence, and again found operable five (5) hours after the occurrence. Therefere:
MU-P-lC was operable during the time of this occurrence.
(9) Corrective Action:
Inmediate : At 1230 heurc en May 19, 1977, the redundant Es pump, MU-P-lc, was tested satisfactorily.
Long Tern: The Shift Supervisors, Unit I Shift Foreman, and the Centrol Roc = Operators have been briefed on this cccurrence and reminded of the general need for =cre e=phasis to follow procedures and the specific requirements of Technical Specification 3.3.4.
The Plant Operations Review Cc=mittee and Unit Superintendent have reviewed and approved the above corrective action and have taken steps to assure its cc=pletion.
(10) Failure Data: NA Similar Occurrences: 76 h9 Sincerely, t$h
'J. G. Herbein Vice President JGH:DGM:J=r
Enclosure:
LER 1482 073
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| 05000289/LER-1977-001, Forwards LER 77-001/01T.Provides Supplemental Info | Forwards LER 77-001/01T.Provides Supplemental Info | | | 05000289/LER-1977-001-01, /01T:on 770203,w/diesel Generator B Out of Svc,A Generator Was Lost,Causing Operation at Limiting Condition Less Conservative than Tech Specs.Generator a Out of Svc Due to Binding of Oil Pressure Low Speed Switch | /01T:on 770203,w/diesel Generator B Out of Svc,A Generator Was Lost,Causing Operation at Limiting Condition Less Conservative than Tech Specs.Generator a Out of Svc Due to Binding of Oil Pressure Low Speed Switch | | | 05000289/LER-1977-002-04, /04T-0:on 770304,river Water Discharge Exceeded Inlet River Water Temp by 14 F,Violating 12 F Limit During Normal Operation.Caused by Atmospheric Conditions & Personnel Error.Standby Decay Heat Water Pump Reduced Temp | /04T-0:on 770304,river Water Discharge Exceeded Inlet River Water Temp by 14 F,Violating 12 F Limit During Normal Operation.Caused by Atmospheric Conditions & Personnel Error.Standby Decay Heat Water Pump Reduced Temp | | | 05000289/LER-1977-003-03, /03L:on 770309,reactor Bldg Spray Pump Suction Isolation Valve Motor Failed.Caused by Excessive Grease in Operators Spring Pack Which Stopped Normal Compression of Spring,Preventing Torque Switch Sensing Force to Be Applied | /03L:on 770309,reactor Bldg Spray Pump Suction Isolation Valve Motor Failed.Caused by Excessive Grease in Operators Spring Pack Which Stopped Normal Compression of Spring,Preventing Torque Switch Sensing Force to Be Applied | | | 05000289/LER-1977-003, Forwards LER 77-003/03L.Provides Supplemental Info | Forwards LER 77-003/03L.Provides Supplemental Info | | | 05000289/LER-1977-004-01, /01T:on 770415,error in Safety Analysis Discovered.Caused by Personnel Using Erroneous Combined Relief Valve Capacity Figures from Vendor Valve Drawing in Safety Analysis | /01T:on 770415,error in Safety Analysis Discovered.Caused by Personnel Using Erroneous Combined Relief Valve Capacity Figures from Vendor Valve Drawing in Safety Analysis | | | 05000289/LER-1977-004, Forwards LER 77-004/01T.Provides Supplemental Info | Forwards LER 77-004/01T.Provides Supplemental Info | | | 05000289/LER-1977-005, Forwards LER 77-005/04T.Provides Supplemental Info | Forwards LER 77-005/04T.Provides Supplemental Info | | | 05000289/LER-1977-005-04, /04t on 770319,change in River Water Discharge Temp More than 2 Degrees in Hour Period Violated Ets.Caused by Failure of Mechanical Cooling Tower C Fan.Fan to Be Repaired During Current Refueling Outage | /04t on 770319,change in River Water Discharge Temp More than 2 Degrees in Hour Period Violated Ets.Caused by Failure of Mechanical Cooling Tower C Fan.Fan to Be Repaired During Current Refueling Outage | | | 05000289/LER-1977-006-01, /01T:on 770324,during Reactor Refueling,Tech Specs for Leakage of Valves & Penetrations Were Exceeded. Caused by Inability of Carbon Steel Gate Valves in Cooling Water Sys to Keep Tight Seals Between Tests | /01T:on 770324,during Reactor Refueling,Tech Specs for Leakage of Valves & Penetrations Were Exceeded. Caused by Inability of Carbon Steel Gate Valves in Cooling Water Sys to Keep Tight Seals Between Tests | | | 05000289/LER-1977-006, Forwards LER 77-006/01T-0 | Forwards LER 77-006/01T-0 | | | 05000289/LER-1977-007, Forwards LER 77-007/01T.Provides Supplemental Info | Forwards LER 77-007/01T.Provides Supplemental Info | | | 05000289/LER-1977-007-01, /01T:on 770509,both Doors of Reactor Bldg Emergency Personnel Access Hatch Open at Same Time,Violating Tech Specs.Caused by Door Design Flaw Allowing Free Travel If Closed Against Obstruction,Causing Interlock Stress | /01T:on 770509,both Doors of Reactor Bldg Emergency Personnel Access Hatch Open at Same Time,Violating Tech Specs.Caused by Door Design Flaw Allowing Free Travel If Closed Against Obstruction,Causing Interlock Stress | | | 05000289/LER-1977-008-03, /03L:on 770504 Snubbers Failed to Perform within Acceptable Criteria,Resulting in Operation in Degraded Mode. Caused by Improperly Adjusted Locking Devices & O-ring Seal Leaks.Cause of Failure of Eight Snubbers Unknown | /03L:on 770504 Snubbers Failed to Perform within Acceptable Criteria,Resulting in Operation in Degraded Mode. Caused by Improperly Adjusted Locking Devices & O-ring Seal Leaks.Cause of Failure of Eight Snubbers Unknown | | | 05000289/LER-1977-008, Forwards LER 77-008/03L.Provides Supplemental Info | Forwards LER 77-008/03L.Provides Supplemental Info | | | 05000289/LER-1977-009-01, /01T:on 770512,loose Steam Generator LOCA Restraint Bolt Found.Caused Either by Improper Tightening During Installation or Loosening Due to Thermal Cycling & Bolt Relaxation in Svc | /01T:on 770512,loose Steam Generator LOCA Restraint Bolt Found.Caused Either by Improper Tightening During Installation or Loosening Due to Thermal Cycling & Bolt Relaxation in Svc | | | 05000289/LER-1977-009, Forwards LER 77-009/01T.Provides Supplemental Info | Forwards LER 77-009/01T.Provides Supplemental Info | | | 05000289/LER-1977-010, Forwards LER 77-010/01T.Provides Supplemental Info | Forwards LER 77-010/01T.Provides Supplemental Info | | | 05000289/LER-1977-011, Forwards LER 77-011/01T.Provides Supplemental Info | Forwards LER 77-011/01T.Provides Supplemental Info | | | 05000289/LER-1977-011-01, T:On 770519,engineered Safeguards Motor Control Center Tripped During Power Operation.Caused by Binding of a Phase Overload Device Tripping Stem.Preventive Maint Will Be Modified to Check for Tripping Stem Resetting | T:On 770519,engineered Safeguards Motor Control Center Tripped During Power Operation.Caused by Binding of a Phase Overload Device Tripping Stem.Preventive Maint Will Be Modified to Check for Tripping Stem Resetting | | | 05000289/LER-1977-012, RO 77-12/3L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Operability of Redundant Pump.Caused by Personnel Error.Redundant Pump Tested Satisfactorily on 770519.Forwards LER 77-12/03L | RO 77-12/3L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Operability of Redundant Pump.Caused by Personnel Error.Redundant Pump Tested Satisfactorily on 770519.Forwards LER 77-12/03L | | | 05000289/LER-1977-012-03, /03L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Redundant Pump. Caused by Personnel Error.Redundant Pump Tested Satisfactorily.Personnel Instructed in Procedures | /03L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Redundant Pump. Caused by Personnel Error.Redundant Pump Tested Satisfactorily.Personnel Instructed in Procedures | | | 05000289/LER-1977-013-04, /04T:on 770523,during Normal Operation,Waste Concentration in River Water Discharge Found in Excess of Designated Max.Caused by Slug of Suspended Solids Breaking Loose During Sampling.Discharge Terminated | /04T:on 770523,during Normal Operation,Waste Concentration in River Water Discharge Found in Excess of Designated Max.Caused by Slug of Suspended Solids Breaking Loose During Sampling.Discharge Terminated | | | 05000289/LER-1977-014-03, /03L:on 770524,during Reactor Bldg Cooling & Isolation Sys Logic Channel & Component Test,Reactor Bldg Cooling Return Isolation Valve RB-V7 Failed to Close Upon Receipt of Signal.Caused by Dirt on Valve Diaphragm | /03L:on 770524,during Reactor Bldg Cooling & Isolation Sys Logic Channel & Component Test,Reactor Bldg Cooling Return Isolation Valve RB-V7 Failed to Close Upon Receipt of Signal.Caused by Dirt on Valve Diaphragm | | | 05000289/LER-1977-015, Notes Error in LER 77-15/3L Submitted 770628.Both Drawings in Section 9 Should Be Numbered 207-011 | Notes Error in LER 77-15/3L Submitted 770628.Both Drawings in Section 9 Should Be Numbered 207-011 | | | 05000289/LER-1977-015-03, /03L:on 770529,during Normal operation,230 Kv Substation Bus 4 Was de-energized by Differential Relay 87BB-1.Caused by Wiring Error on Auxiliary Transformer Due to Drawing Error.Bus & Transformer Returned to Svc | /03L:on 770529,during Normal operation,230 Kv Substation Bus 4 Was de-energized by Differential Relay 87BB-1.Caused by Wiring Error on Auxiliary Transformer Due to Drawing Error.Bus & Transformer Returned to Svc | | | 05000320/LER-1977-016, /01T-0 on 770924:half Trip of Steam & Feedwater Rupture Control Sys Resulted in Opening of Pressurizer Power Relief Valve.Possibly Caused by Loose Connections at Terminal Boards | /01T-0 on 770924:half Trip of Steam & Feedwater Rupture Control Sys Resulted in Opening of Pressurizer Power Relief Valve.Possibly Caused by Loose Connections at Terminal Boards | | | 05000289/LER-1977-016-01, /01T-0:on 770924,RCS Temp & Pressure Rose.Caused by Half Trip Condition from Steam & Feedwater Rupture Control Sys.Possible Cause of Half Trip Attributed to Loose Connection at Terminal Boards | /01T-0:on 770924,RCS Temp & Pressure Rose.Caused by Half Trip Condition from Steam & Feedwater Rupture Control Sys.Possible Cause of Half Trip Attributed to Loose Connection at Terminal Boards | | | 05000289/LER-1977-016, Forwards Supplemental Info to LER 77-016/01T-0 Re Half Trip in Steam Feedwater Rupture Control Sys | Forwards Supplemental Info to LER 77-016/01T-0 Re Half Trip in Steam Feedwater Rupture Control Sys | | | 05000289/LER-1977-017-03, /03L:on 770624,during Normal Operating & semi- Annual Leak Test,Leakage Observed Around Inner Door Seal of Personnel Accces Hatch of Reactor Bldg.Caused by Procedural Inadequacies Causing Improper Installation of Door | /03L:on 770624,during Normal Operating & semi- Annual Leak Test,Leakage Observed Around Inner Door Seal of Personnel Accces Hatch of Reactor Bldg.Caused by Procedural Inadequacies Causing Improper Installation of Door | | | 05000289/LER-1977-018-03, /03L:on 770629,during Normal Operation,Nuclear Svcs River Water Pump NR-P1C Shaft Failed During Pump Operation.Caused by Mechanical & Procedural Problems.Pump Lined Up & Repaired within 4-h | /03L:on 770629,during Normal Operation,Nuclear Svcs River Water Pump NR-P1C Shaft Failed During Pump Operation.Caused by Mechanical & Procedural Problems.Pump Lined Up & Repaired within 4-h | | | 05000289/LER-1977-019-03, /03L:on 770713,during Normal Operation,Leak in Miscellaneous Waste Evaporator Feed Tank Immersion Heater Shorted Out Heater & Feed Pump.Caused by Leak in Temp Probe on Heater.Heater Replaced & Operating Procedure Modified | /03L:on 770713,during Normal Operation,Leak in Miscellaneous Waste Evaporator Feed Tank Immersion Heater Shorted Out Heater & Feed Pump.Caused by Leak in Temp Probe on Heater.Heater Replaced & Operating Procedure Modified | | | 05000289/LER-1977-020, Forwards LER 77-20/04T-0 | Forwards LER 77-20/04T-0 | | | 05000289/LER-1977-020-04, /4T:on 770719,during Passage of Storm Front,Station River Water Discharge Temp Fell to in Excess of 3 F Below Inlet Temp.Caused by Storm Front.A & B Mechanical Draft Cooling Fans Stopped | /4T:on 770719,during Passage of Storm Front,Station River Water Discharge Temp Fell to in Excess of 3 F Below Inlet Temp.Caused by Storm Front.A & B Mechanical Draft Cooling Fans Stopped | | | 05000289/LER-1977-021-01, /01T:on 770726,during Normal Operation,Radiation Monitor RM-A2 Failed & Atmosphere Sampling of Reactor Bldg Not Performed.Caused by Improper Reassembly Following 770725 Surveillance Test.Monitor Repaired.Procedure to Be Revi | /01T:on 770726,during Normal Operation,Radiation Monitor RM-A2 Failed & Atmosphere Sampling of Reactor Bldg Not Performed.Caused by Improper Reassembly Following 770725 Surveillance Test.Monitor Repaired.Procedure to Be Revised | | | 05000289/LER-1977-022-01, /01T:on 770825,during Normal Operation Restrictions Placed on Decay Heat Removal Pumps Found Contrary to Pump Operating Capability Per Fsar.Restrictions Placed on Pump by B&W Due to Pump Failure at Other Util | /01T:on 770825,during Normal Operation Restrictions Placed on Decay Heat Removal Pumps Found Contrary to Pump Operating Capability Per Fsar.Restrictions Placed on Pump by B&W Due to Pump Failure at Other Util | | | 05000289/LER-1977-023-01, /01T:on 770926,during Heatup Operation Both Doors of Reactor Bldg Emergency Personnel Access Hatch Open Simultaneously.Caused by Failure of Interlock,Poor Hatch Design & Operator Error.Addl Interlock to Be Added | /01T:on 770926,during Heatup Operation Both Doors of Reactor Bldg Emergency Personnel Access Hatch Open Simultaneously.Caused by Failure of Interlock,Poor Hatch Design & Operator Error.Addl Interlock to Be Added | | | 05000289/LER-1977-023, RO 77-23/1T:on 770920,both Doors of Reactor Bldg Emergency Personnel Access Hatch Open Simultaneously.Caused by Personnel Error.Doors Closed.Forwards LER 77-23/1T | RO 77-23/1T:on 770920,both Doors of Reactor Bldg Emergency Personnel Access Hatch Open Simultaneously.Caused by Personnel Error.Doors Closed.Forwards LER 77-23/1T | |
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