05000289/LER-1977-012, RO 77-12/3L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Operability of Redundant Pump.Caused by Personnel Error.Redundant Pump Tested Satisfactorily on 770519.Forwards LER 77-12/03L

From kanterella
(Redirected from ML19261F336)
Jump to navigation Jump to search
RO 77-12/3L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Operability of Redundant Pump.Caused by Personnel Error.Redundant Pump Tested Satisfactorily on 770519.Forwards LER 77-12/03L
ML19261F336
Person / Time
Site: Crane 
Issue date: 06/09/1977
From: Herbein J
METROPOLITAN EDISON CO.
To:
Shared Package
ML19261F337 List:
References
GQL-0790, GQL-790, NUDOCS 7910250795
Download: ML19261F336 (3)


LER-1977-012, RO 77-12/3L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Operability of Redundant Pump.Caused by Personnel Error.Redundant Pump Tested Satisfactorily on 770519.Forwards LER 77-12/03L
Event date:
Report date:
2891977012R00 - NRC Website

text

a C.v(.C m.m U.S. NU CLL A H M E C.ULATOR Y C.

'OloN DOCKC T NUMcr n i

as7 10$

,m SC-2-87 NaC DISTRIBUTION ran PART 50 DOCKET MATERIAL hW '

stanu w n INCIDEtiT REPCRT TO:

FROM:

DATC CF OCCU?.tCU T Metropolitan Edison Company 6/9/77 Mr. J. P. O'Reilly Reading, Pa.

047c neceivec J. G. Herbein 6/16/77 ETTER ONoTonizto enor ispur son?e sureeca or Copies stC iv cc R GIN AL N NC LASSIFI E D g[

'X S "R; P is o N ENCLOGU R E Licensee Event Report (R0 50 289/77-12/3L) on i 5/19/77 concerning Emgineered Safeguards pump

'p.,

.l being removed prior to testing redundant pump.

,'G _,. v,,

Q.,

~ J ' Q oo i e ): jwl, a, m N

r, p

n: r D

D c

t hIV l iiii

" u a u e U U \\. !['L a PLM:T NAME:

o oJ3 Three Mile Island Unit No. 1 (2-P)

(1-P)

RJL 6/16/77 NOTE:

IF PERSC; iEL E"POSURE IS INVOLVED SEND DIF,ICTLY TO ICLEGER/J. COLLI::S l

f FOR ACT:C:J /iN F O R'.1 ATION l l BRAN.,H CliIEF:

I [/c / /

u[3 CYS ICR ACTICN

~I I

LIC. ACST.:

3 pr q p v i U/ / Cis CM C.

AC5f~f D Y3 1.; 2/ g.iT # _5 t

l I l

I

[

INTERNAL C;3TR'CUTICN I

I lc i... ~ 2.. A l

I~i I & 2 (2) l I MII;

j i SC:'mEE ER/IP!CLITO l l 4 EG;:J T F.I I

I i 1:07.7.J /CitECK I i Grit ES l

I i

B iT_f'_.. I.'.R 1W'.WE R l

_ _TEDZ5CO/M_iCCARY l

i E U"-.'."%" * "t

_)_BAI R I

I I I SIMO

-~i I

'5'i,I 555!/El5:li l

T-

.. _.. R:... c. R t.T. C C.

i_., -

uu l l D'.TE R N A L L ISTi U Ti t. '!

CC a. n' t..t.

. ci i

lr _.T..t.c.: _

I__

[.L'@_:]fa m % fg 1482 071 k *

.4..__--

. -. ~. ~.

n p _ ; _ _.. ___.

__4._ _ _

t._

_._1..___.

No i

"'rn' 7910350 7 E

/.

)

8MM w a nwm f{, n m -

m.

&y) 3' ~...., -

.- j.

METROPOLITAN EDISON COMPANY POST OFFICE BOX 542 READING. PENNSYLVANI A 19603 TELEPHON

, p f.7.

June 9, 1977

/ s.' '

s N

\\g' GQL 0790 g

[E

$/[/jy50 o C.

  • W

<s

?Ir. J. P. O'Reilly, Directer K.:

f'yb h*'.

~

Cffice of Inspections and Fnforcement, Regicn I

-?

    • 'D'M'oey -k U. S. Nuclear Regulatory Cum =issien

', y,

%-ff 631 Park Avenue King of Prussia, Pa.

19h06

'M l I #

Dear Sir:

Docket No. 50-289 Operating license No. DPR-50 In accordance with the Technics 1 Specifications of cur Three Mile Island Nuclear Station Unit 1 (TMI-1), we are reporting the folleving reportable occurrence.

(1) Report Number: 77-12/3L (2a) Required Report Date: 06-17-77 (2b) Date of Occurrence: 05-19-77 (3) Facility: Three Mile Island Nuclear Station - Unit I (k) Identificaticn of Occurrence:

Title: Engineered Safeguards pu=p was removed prior to testing redundant pu=p.

Type: A reportable occurrence as defined by Technical Specificatiens 6.9.2.3.(3) in that, Engineered Safeguard pump MU-P-1A was removed frem service prior to testing the operability of the redundant pu=p, MU-P-lC, violating sections 3.3.4, of the Technical Specifications, and resulting in an inadequacy in the implementation of procedural acntrols which threatened to cause a reducticn in the degree of redundancy of an engineered safety fe ature.

(5) Conditions Prior to Occurrence Pcwer: Core: 192h Elec: 631 RC Flev:

lhhx106 lbs/hr RC Pressure:

2155 psig RC Te=p:

579cy 1482 072 P'iZR Level:

220 inches PR"R Te=p:

oL5 F (6) Descriptien of Occurrence:

While escalating to 755 pcVer felleving the refueling cutage Engineered Safeguards pump, MU-P-1A, was re=cved frem service prier to testing the Operability Of the redundant Engineered Safeguard pump, MU-P-lC.

7 71 i 7' "3 ^7

June 9,1977 Mr. J. P. O'Reilly GQM 0790 (T) Apparent Cause of Occurrence:

The cause of this occurrence has been determined to be personnel in that, at the time MU-P-1A was removed from service the Shift Foreman failed to Lnplement the req 2 ire =ent to test the redundant pump.

(3) Ana2yais of Occurrence:

It has been determined that this occurrence did not constitute a threat to the health and safety of the public in that, the redundant pump, MU-P-1C, had been demonstrated cperable ten (10) days prior to the occurrence, and again found operable five (5) hours after the occurrence. Therefere:

MU-P-lC was operable during the time of this occurrence.

(9) Corrective Action:

Inmediate : At 1230 heurc en May 19, 1977, the redundant Es pump, MU-P-lc, was tested satisfactorily.

Long Tern: The Shift Supervisors, Unit I Shift Foreman, and the Centrol Roc = Operators have been briefed on this cccurrence and reminded of the general need for =cre e=phasis to follow procedures and the specific requirements of Technical Specification 3.3.4.

The Plant Operations Review Cc=mittee and Unit Superintendent have reviewed and approved the above corrective action and have taken steps to assure its cc=pletion.

(10) Failure Data: NA Similar Occurrences: 76 h9 Sincerely, t$h

'J. G. Herbein Vice President JGH:DGM:J=r

Enclosure:

LER 1482 073