ML20235R060

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Insp Rept 50-312/87-20 on 870530-0710.Violations Noted. Major Areas Inspected:Operational Safety Verification,Maint, Surveillance & Followup Items
ML20235R060
Person / Time
Site: Rancho Seco
Issue date: 09/18/1987
From: Dangelo A, Miller L, Myers C, Pereira D, Perez G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML20235R007 List:
References
50-312-87-20, NUDOCS 8710070780
Download: ML20235R060 (34)


See also: IR 05000312/1987020

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'U. S. NUCLEAR REGULATORY COMMISSION

REGION V

, Report No: 50-312/87-20

' Docket'No; '50-312 s

. License No. DPR-54

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Licensee: -Sacramento' Municipal. Utility District

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P. 0. Box 15830

Sacramento, California -95813

Facility Name: Rancho Seco Unit 1

Inspection at: Herald, California (Rancho Seco Site)

Inspection'conductep May 30 - July 10, 1987

Inspectors: /  !

Mb'.D'AnMM

A.-J o, Senior #Esident Inspector Cate Signed

> > Ju ~ > - V~l8~D

C. J. My s, F esident Inspector Date Signe'd

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G e ez, hf d t Inspector Date Signed

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Difereira, Regiorfal Unspector

7/mf7

Date Signed

Accompanying Personnel: G. Johnston, M. Ely, Lawrence Livermore National

La atory

Approved By: / /

IL/ F. Miller, Chief, Reactor ProjectsSection II D&te Signed

Summary:

Inspection between May 30 and July 10, 1987 (Report 50-312/87-20)

Areas Inspected: This routine inspection by three Resident Inspectors and

by two Regional Inspectors, involved the areas of operational safety

verification, maintenance, surveillance, and followup items. During this

inspection, Inspection Procedures 25573, 30702, 30703, 35701, 37700, 37701,

42700,.55050, 55150, 61726, 62702, 62703, 71707, 71710, 72701, 92700, 92701,

92702,' 93702 and 94702 were used.

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Results: In the areas inspected, two violations were identified: failure to

use an appropriate heat treating process procedure and failure to properly

install certain cables, and associated electrical equipment.

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DETAILS

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1. Persons Contacted

a. Licensee Personnel

G. C. Andognini, Chief Executive Officer, Nuclear

  • J. Firlit, AGM, Nuclear Fower Production
  • W. Bibb, Deputy ' Restart. Implementation Manager

G. Coward, AGM, Technical and Administrative Services

  • D. Keuter, Director, Nuclear Operations and Maintenance
J. McColligan, Director, Nuclear Plant Support

D. Brock, Acting Nuclear Maintenance Manager

.B. Croley, Nuclear Technical Manager

G. Cranston, Nuclear Engineering Manager

-*W. Kemper, Nuclear Operations Manager

J. Shetler, Director, System Review and Test Program

T. Tucker, Nuclear Operations Superintendent

J. Grimes, Nuclear Mechanical Maintenance. Superintendent

L. Fossom, Deputy Implementation Manager

R. Colombo, Regulatory Compliance Superintendent

J. Field,-Plant Support Engineering Manager

S. Crunk, Technical Assistant, AGM

F. Kellie, Radiation Protection Superintendent

J.,Vinquist, Quality Assurance Manager

C. Stephenson, Senior Regulatory Compliance Engineer

R. Cherba, Quality Engineering Supervisor 1

T. Shewski, Quality Engineer

L. Conklin, Technical Assistant, AGM

D. Ross, Security

Other licensee employees contacted included technicians, operators,

mechanics, security and office personnel.

  • Attended the Exit Meeting on July 14, 1987

2. Operational Safety Verification

The inspectors reviewed control room operations, including access

control, staffing, observation of decay heat removal system alignment, ,

and review of control room logs. Discussions with the shift supervisors j

and operators indicated understanding by these personnel of the reasons l

for annunciator indications, abnormal plant conditions and maintenance

work in progress. The inspectors also verified, by observation of valve

and switch position indications, that emergency systems were properly 4

aligned for the cold shutdown condition of the facility.

During this period, the licensee still relied on the operability of the

steam generators and auxiliary feedwater system for decay heat removal.

Tours of the auxiliary, reactor, and turbine buildings, including

exterior areas, were made to assess equipment conditions and plant

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conditions. Also, the tours were made to assess the effectiveness of

a . radiological controls and adherence to regulatory requirements. The.

inspectors also. observed plant housekeeping and cleanliness, looked for

potential . fire and safety hazards, and observed security and safeguards

practices.

Plant housekeeping appeared degraded in that tours made of the auxiliary

butiding roof revealed some trash such as Styrofoam coffee cups and food

containers, newspaper and cigarette butts on the floor. By the end of

this inspection, plant management had responded to the conditions noted,

had cleaned the' area, and, in addition, were having water jet cleaning of

the protected area of.the site performed.

No violations of regulatory requirements or deviations were identified.

'3. ESF System Walkdown

The "A" auxiliary feedwater system was walked down and found to be

operable. Required surveillance had been performed by the licensee and

found to meet requirements. Electrical bus lineups were found to be in

compliance with procedures. Valve positions were found to be proper and

in accordance with the current valve line-up procedure.

No violations of. regulatory requirements or deviations were identified.

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4. Monthly Maintenance 0bservation

TDI Turbocharger Temporary Support Inspection

The inspector observed portions of the preoperational startup testing of

'the new Transamerica DeLaval Incorporated (TDI) diesel generators under

STP-1009, " Diesel Generator Integrated System Phase 2 Testing." The

inspector noted the addition of a support for the turbocharger which was

not present during the previous testing of the diesel generators. The

inspector questioned whether the installation of the support was an

approved modification of the qualified final configuration of the diesel

. generators. In response to the inspector's concern, licensee personnel

identified the following controls established for the temporary support:

a. Turbocharger vibration on the "B" diesel generator during previous

testing had been determined to exceed the manufacturer's

. recommendations. In pursuing a solution to the problem with the

manufacturer, the licensee had designed and installed the temporary

support under a Drawing Change Notice (DCN).

b. The temporary support was shown to reduce turbocharger vibration to

within acceptable values during test runs of the diesel generators.

c. A permanent support was being designed to replace the temporary

support. This permanent support would be installed prior to

turnover of the diesel generators to operations. However in the

interim, preoperational testing of the diesel generators would

continue with the temporary support installed.

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. The inspector reviewed the. licensee's' engineering' analysis for the

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temporary turbocharger support and found that the analysis. appeared

adequate for the structural design of the support. However, the

inspector found limited analysis of the effect of the temporary support

on the turbocharger itself to ensure that its performance was not

affected by the support. The licensee acknowledged.that the

acceptability of the diesel generator test results was at risk pending an

-analysis of the acceptability of.the temporary support compared with the

permanent design support. No analysis on the effect of the support which

was not part of~the configuration of the engine which had been seismically

qualified had been performed. The licensee was conducting an evaluation

of what testing needed to be performed on the diesel generator when all

modifications were completed, including the turbocharger support, at the

end of this inspection. Plans which the licensee was considering

. included additional vibration measurements and disassembly of the

turbocharger after operation with the new support in place.

The inspector reviewed the installation of the temporary support and

found that the DCN contained an installation note that required the

support to remain unbolted from the turbocharger until the diesel

generator had stabilized at its " keep warm" temperature. The inspector

noted that STP-1009 had not been revised to include the support

installation note. After bringing this omission to the licensee's

attention, a caution tag'was subsequently hung on the electric keep warm

heater breaker requiring unbolting of the support before deenergizing the

heaters. The inspector concluded that this corrective action was

adequate.

The licensee was experiencing additional vibrations with the engines.

Excessive vibration apparently caused pipe wall and pipe support failures

in the lube oil return and engine jacket water systems. Although the

licensee's corrective action had not been finalized, during the

inspection period, the licensee had not determined the root cause of

piping and pipe support failures. The licensee had not established any

plan to pursue the failures to root cause other than to continue

measurement of engine vibrations and modify piping as required. No

documented comparison had been performed by the licensee of their engine

vibrations to other licensees with similar engines. The lack of root

cause determination for engine vibration will be followed as an open item

(50-312/87-20-01).

No violations or deviations were identified.

Review of Maintenance of Motor Operated Valves (MOVs)

a. During post maintenance testing of safety related valve SFV-25003,

excessive noise was observed by maintenance personnel. Subsequent

disassembly of the valve operator disclosed extensive gear damage.

Further investigation by the licensee identified that a spring

retaining washer required for that particular style operator

(Limitorque SMB-2) had not been installed during refurbishment. The

inspector observed that the maintenance instructions did not

include instructions to install the spring retaining washer. The

licensee considered the procedural discrepancy to have resulted due

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to inadequate procedures developed from insufficient vendor

descriptive data. The licensee determined that only one other safety i

related operator of this style was applied in the plant and also

found the missing washer to also sist on that operator.

The inspector observed portions of the troubleshooting activities

and damaged components and found that the licensee exercised careful

controls over the troubleshooting activities to identify the root

cause of the failure.

The inspector reviewed the vendor technical manual information for

the affected operator' style. Although difficult to clearly identify

as a distinct part due to the small scale of the assembly drawing,

the inspector found that the required spring retainer washer was

identified in the drawing part list and was called out in the

assembly drawing for the operator.

The licensee acknowledged the inspector's concern and indicated that

a previously planned review of the implementation of vendor

preventative maintenance manual data would be accelerated and

addressed as part of the licensee's new preventive maintenance =

program to be implemented by September, 1987. A review of the

preventative maintenance program is currently underway by the

inspector and will be documented in a subsequent inspection report.

b. During post-maintenance testing of refurbished motor operated valve

SFV-25003, the licensee observed cracks in the cast yoke of the

valve. The licensee subsequently modified the yoke to weld a

stiffener to the yoke in addition to repair welding the defect area.

A similar modification was made to the identical valve in the "B"

train.

The inspector observed portions of the repair activity. During

repair welding the licensee encountered unexpected distortion of the

yoke which required hot working to return the yoke to an acceptable

condition. The inspector found that the heat treating was not

controlled within the scope of the original work request nor was the

work request changed to include the expanded scope. Rather, work I

was controlled under verbal instructions from the welding engineer

without a procedure or other written instruction.

This is an apparent violation of the licensee's Quality Assurance

program and 10 CFR 50 Appendix B, Criterion IX, " Control of Special

Processes" (50-312/87-20-08).

c. During maintenance refurbishment of valve SFV-25003, the licensee

installed a manufacturer supplied conversion kit on the operator of I

the valve to reduce the inertia over thrust resulting due to the

fast acting response of the valve. The conversion unit adapted the

operator to install a spring pack above the stem nut to allow the

stem nut to move vertically after the stem had seated to absorb the

excess momentum in the operator.

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The 'inspec' tor observed that the conversion kit completely enclosed

the normally exposed rising valve stem, thereby eliminating the

normal indication of the open valve position. Furthermore, the

conversion kit included a spring pack compression indicator which

was labeled " stem movement". The inspector was concerned that

~1abeling was inaccurate and might be misinterpreted by operators

during manual' operation.

The inspector expressed his concern to. licensee management who

acknowledged the potential for confusion and agreed to review the

adequacy of'the local valve position indication resulting from the

addition of the SP conversion units on the valve operators.

d. The' inspector discussed the lack of a formal program document for

the licensee's program in response to NRC Information Bulletin (IB)

85-03 in several. meetings with licensee representatives. The

previous submittals to the NRC had referenced the licensee's

f' program" and summarized the status of its implementation. However,

no program document had been prepared. Due to the expanding and

contracting nature of the MOV refurbishment effort during the

restart effort, the inspector was concerned that the lack'of a

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controlled program defining the IB 85-03 commitments could result in

inadequate control of the program to insure that it is implemented

.as committed.

'The inspector noted, for example, that some portions of the program

originally submitted to the NRC were outdated and were no longer

being implemented as part of the MOV effort. Specifically, a torque

wrench was to be used to establish proper torque switch settings as

part of the existing MOV program submittals to the NRC, but one was

not being used due to changes in the practices used for valve

adjustment.

The licensee acknowledged the inspector's concerns and committed to

submit a formal complete program description to update their

commitments in response to IEB 85-03.

One violation of NRC requirements was identified.

5. Radiological Controls

The inspector observed controlled area refresher training conducted on

June 22, 1987. In general, the inspector found that the training

appeared to be appropriate and effective.

The inspector noted that approximately 75% of the multiple choice

examination questions in one copy of the exam administered after the ,

refresher training lecture had blue ink tick marks associated with

selected answers. The inspector noted that the examination booklet l

l contained general instructions prohibiting making any marks on the '

examination booklet. The inspector discussed his observation with the

instructor and subsequently with the Training department management and

expressed concern that lack of control of the test copies may compromise

the effectiveness of the training. The licensee responded to the

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inspector's concerns by reviewing all test copies and found no other

cases of answer markings. In addition to quarterly reissue of the

examination, the licensee committed to add a unique identification of-

each~ examination copy to be. recorded with each answer sheet to establish ~

traceability to deter future marking occurrences.

The inspector found the licensee's response to be. appropriate.

No violations or deviations were identified.

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.6. Facility Modifications

During the current outage, 57 facility modifications have been made to

the plant and will become operable for this restart. The installation of

the EFIC system (Emergency Feedwater Initiation and Control System) and

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the TDI (Transamerica DeLaval Industries) emergency diesel generators

E' were the two major modifications. selected for inspection.

The inspections were performed by Lawrence Livermore National Laboratory

(LLNL) personnel for the USNRC under supervision of the resident staff.

'LLNL's report is attached to this. inspection report. The NRC discussion-

of the LLNL findings is contained herewith.

Nuclear Welding General Inspection Procedure

-Inspection of Mechanical Installation of EFIC

Inspection of the mechanical and welding areas did not reveal any

violations of regulatory requirements. However, a concern was discovered

during thejinspection and pertained to the installation of the four EFIC

level tap nozzles on each steam generator.

During the inspector's observation of completed welds for the EFIC taps

on the steam generators, an apparent base metal reduction was discovered

near weld "I". The repair had been authorized, however, due to an error

in preparing the weld repair record form, the weld had not been repaired.

The EFIC system had not been turned over to the station at the time of

the inspection and therefore, the final inspections by the licensee had

not been completed.

The licensee committed at the exit meeting to reinspect the four EFIC

nozzles on each steam generator for any additional undercut on the EFIC

sensing lines which had not been repaired. In addition, the licensee

committed.to a review of all work request packages related to EFIC level'

taps on both stesm generators to identify any work activity which could

reduce base metal, such as grinding to prepare'for nondestructive

examination and ensure adequate measures existed to detect base l

, reduction.

No violations or deviations were identified.

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Inspection of Electrical Installations of EFIC and TDI Emergency

Diesel Generators

Electrical Cable Separation

Electrical cable separation within panels HISS (E), H4FWB, H2 DEA 2 and

H2 DEB 2 did not appear to meet separation criteria as described in Nuclear

Engineering Procedure (NEP) 5304.8c. The criteria which the licensee has

established was under review by the Office of Nuclear Reactor Regulation

(NRR). The NRR was reviewing the extent to which the licensee's

separation criteria was in conformance with IEEE Standard 384 (Electrical

Separation Criteria for Nuclear Power Plants).

The issue of electrical cable separation criteria will remain an open

item (50-312/87-20-02) pending NRR review of the licensee's separation

criteria and followup inspection.

No violations or deviations were identified.

Design, Design Changes and Modifications

Review of Design Drawings vs. As-Built Plant Configuration

A review of drawings associated with ECNs A-5415AA and A-5415AH

identified four drawing discrepancies. The four differences identified

appeared to have been approved, however, the design drawings did not

reflect this approved configuration. Both ECNs had not received final

review and approval, and, therefore, the facility modification had not

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The licensee's drawing control system will be reviewed in a subsequent

inspection for outstanding drawing change notices to be incorporated into

the base drawing. This will remain as an open item (50-312/87-20-03).

No-violations or deviations were identified.

Electric Cable Inspection of Completed Work - TDI Building

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The following is a summary of concerns raised as a result of the review

of completed TDI building work,

a. In manhole number 47 which contained safety-related electrical

raceway between the TDI building and the Nuclear Services Electrical

Building (NSEB), safety-related instrumentation cable was found

laying across safety-related power cable. The appropriateness of

this and the issue of electrical cable separation criteria

applicability to underground raceway was also under review by NRR, i

and will be tracked with a previous open item number

(50-312/87-20-02).

b. Mounting bolts for thermocouple TE55701 were found during the

inspection to be bottomed-out within their mounting channel. This ,

has caused the lockwasher under the bolt head to not be compressed )

against the base plate.

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Thermocouple TE55701 extension wires were also found to be

mislabeled in that the wire materials were not correctly shown.

These labels were used to correctly terminate the thermocouple to

field cable. The as found terminations were found correct with the

labels incorrect. Additional inspection by the licensee also

discovered cracked insulation on these wires. Following these

findings, the licensee generated NCR 56810 to document both NRC and

subsequent similar licensee findings.

Mislabeling of a HVAC damper actuator (HV-55713) model number was

identified on drawing M17.07-6 of ECN-3748.

These issues will remain as a single open item pending review of

licensee's corrective action program. (50-312/87-20-04)

c. TDI buiiding essential HVAC air handling unit (AH-DG-1B) motor

termination box contained electric power cable which was bent

tighter than the allowable bend radius. The discovered bend radius

was approximately 3/4" and the allowable radius for the 4 AWG cable,

as specified by licensee procedures MPEM 8304.8c was 1.6". Quality

control inspection of this connection had occurred on October 17,

1984. Apparently, the motor connection box was not of sufficient ,

volume to accommodate the larger cable with adequate cable radii.

The licensee documented this finding on NCR 56845, subsequent to

this finding.

An inspection was conducted of electrical cable as they exited

electrical conduit and entered electrical cable trays. Cable trays

A57El and L5782 both contained cables which entered the tray irom

conduit A57015 and L57046 where the cable crosses over the cable

tray side channel. To prevent electrical cable jacket deformation,

licensee procedure NPEM 5304.7.c required tray edge bumpers to be

installed.

, Contrary to procedure requirements, the tray edge bumpers were not

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installed on the tray conduit junctions of A57El with A57015 and

l L5782 with L57046. Quality control inspections of cable trays were

l performed on May 5, 1985, September 18, 1984 and September 19, 1984,

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which did not detect this condition. The licensee has documented

l the inspector's findings on NCR 56844, after this finding.

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Raceway color labeling was required by the licensee procedures in j

order to distinguish electrical cable separation groups. I

Specifically, procedure NPEM 5304.7c required the color markings be

installed, however, electrical pull box H7J2995 contained a

safety-related "A" channel cable and should have had a red label,

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but was found with a black (non-safety related) label.

The findings in this paragraph appeared to have been a violation of

the licensee's quality assurance program and 10 CFR Appendix B,

Criterion X, " Inspections." (50-312/87-20-05)

d. The inspector questioned the cable raceway system used by the

licensee in manhole number 47. The design of the raceway system

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used within this manhole consisted of a cantilevered arm which

attaches to a wall mounted bracket. The arm remained in place due

only to the deadweight load of the cable and arm'itself. There was

-no mechanical fastener for the arm such as a bolt.

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L ' functional during a postulated seismic event with positive and

negative vertical ground acceleration. In response,.the licensee

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committed-to provide the existing analysis to support the design of

the' raceway system.

An additional concern was raised on the mechanical expansion anchor'

l- bolts used to secure wall brackets to the concrete. The bolts did

not have any markings to indicate a quality control inspection. The

licensee used a paint marking on all above ground bolt installations

to show the inspection has occurred. Also, two bolts appear to not

o be perpendicular.to the wall. This item will remain open pending

inspection of the QC documentation on the installation of the bolts

and a review of; installation criteria for acceptable  ;

perpendicularity criteria. i

These questions will remain open pending further inspections.

.(50-312/87-20-06)

e. The inspector observed that the licensee had irtseveral

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authorized and used."Siltex" or "Fiberfrax" tape to meet required

cable separation criteria. The inspector requested the test reports

for qualification of the use of the Siltex or Fiberfrax tape as an

acceptable barrier. The-licensee committed to provide for

inspection the qualification records of the fire barrier.used.

This item will remain open pending review of the qualification

reports against the installed configuration of electrical cable

(50-312/87-20-07).

7.. Modification Testing / Monthly Surveillance Observation

Review of System Review and Test Program (SRTP)

The following test outlines were reviewed against the system functional

requirements as described in the System Status Reports (SSRs). No

significant deficiencies were identified.

STP-1030 Maximum Differential Pressure Test of Seal Return Valve

SFV-24004 and Seal Injection Valve SFV-23616

RT-HVS-011 Refueling Interval Inspection of Hardcast Tape and Drain

. Loop Seal on CR/TSC HVAC.

STP-1045 Letdown Valves Interlock Test

STP-970 Diesel Generator (G-886A) Synchronization Check Relay-

l Functional Test

STP-1074 Demonstration of Alternate Decay Heat Removal Methods

STP-1078 Hydrogen Recombiner Functional Test

STP-660 Rev.1 ICS Tuning at Power

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RT-HVS-013 Special Frequency Reactor Building Emergency Cooling

Performance Test

RT-HVS-012 Special Frequency Rx. Bldg. Normal Cooling Performance

Test

RT-HVS-014. Special Frequency Rx. Bldg. Cavity Cooling Performance

Test

STP-7928 "B" HPI Pump Lube Oil Modification

-STP-667 EFIC Hot Functional Test

STP-1063A/B Essential Filtration Unit Air / Aerosol Mixing Uniformity

Test Train "A" & "B"

STP-1057B "B" Component Cooling Water Pump P-4628 Performance

Monitoring Test

STP-199 NSEB Fire Zone 76 Carbon Dioxide System Concentration Test

STP-1033A- DHS Pump P-261A Performance

STP-1033B DHS Pump P-261B Performance

STP-1063A CR/TSC Essential Filtration Unit Air / Aerosol Mixing

Uniformity Test Train "A"

STP-792C Makeup Pump Lube Oil Modification Test

STP-1053 CCW Component Flow Verification

STP-790 Rev.1 RPS Module Removal Interlock Verification

STP-432 Rev.1 Post Accident Sampling System Gaseous Functional Test

STP-791 IDADS Calculated Points for EFIC

STP-7928 "B" HPI Pump Lube Oil Modification Test

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STP-10638 CR/TSC Essential Filtration Unit Air Aerosol Mixing 1

Uniformity Test Train "B" q

STP-1031B Nuclear Service Raw Water (NSRW) Component Flow _j

Verification Loop "B"

STP-783 MU Pump /MU Tank Outlet Valve Controls Verification

STP-1045 Letdown Valves Interlock Test

STP-1012 Emergency Diesel Generator (G-886B) Post Modification Test

STP-966 NSEB, Cross-Zoned Suppression (Fire Zones 81 & 82) Test

STP-974 HV-20596, HV-20569, HV-30801 differential pressure MOVATS

Test

STP-779A Rev.2 CR/TSC Essential Air Flow Transmitter Data Collection

Train "B"

STP-7798 Rev.1 CR/TSC Essential Air Flow Transmitter Data Collection

Train "B"

STP-1030 Maximum DP Test of Seal Bleedoff Isolation Valve SFV-24004

and Seal Supply Isolation Valve SFV-23616

STP-774 IAS Backup to TBV, CCW CIVs, FWS Cont. Valves; MFW, SFW,  ;

AFW and ADV using CLBB and ADVs using App. R Bottles Test  !

STP-780 Instrumentation Cross Correlation Test i

STP-1065 Rev.1 Flow Path Verification of the Waste Water System Piping

Mods

STP-1009B New Diesel Generator G-100B/GEB2 Engine Integrated System

Phase 2 Testing

During the period, the inspector observed the performance of STP-1009A.

) Testing witnessed was conducted in accordance with the procedure and

recorded data was documented per the procedure.  !

During the performance of this test, the licensee continued with their I

program for monitoring TDI diesel engine vibration. Several piping and l

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or pipe support failures occurred during the testing. These included two

failures of pipe supports (cracked welds) in the jacket water system.

Also, failures (pipe wall tear and a pipe support weld crack) occurred on

both engines in the lube oil return lines.

The licensee believed these failures were all related to engine vibration

and the licensee was preparing a repair. The inspector was concerned

with licensee efforts to make repairs in that there was not a plan by the

licensee to determine why the failures occurred, including their root

cause. This item will be tracked as open item 50-312/87-20-01 discussed i

earlier. in this report.

Review of Surveillance Performed on the Nuclear Service Raw Water

Heat Exchanger

On June 18, 1987, the licensee discovered complete blockage of the  !

bearing cooling water supply and return lines for the bearing lube oil

cooler on the "B" reactor building spray pump. Previously, a similar

condition had been identified in the "A" train component but with partial

blockage.

The inspector observed portions of the maintenance activities involved in

investigating the extent of the fouling problem including disassembly and

visual inspection of the lube oil cooling water lines, and cleaning

activities involved with the nuclear service spray ponds. Samples of

potential micro-biologically induced corrosion attached to the interior

surface of the internally coated carbon steel piping were removed for

additional vendor analysis. The inspector found that the licensee's

corrective actions appeared to be thorough and appropriate.

The licensee determined that the event was reportable under 10 CFR 50.73

and initiated preparation of an LER. Followup of this item will be

conducted in review of the forthes ing LER.

No violations or deviations were identified.

Transamerica DeLaval Inc. (TDI) Diesel Generator Testing

The inspector observed portions of the preoperational testing of the TOI

diesel generators under STP-1009. The inspector noted that the diesel

governor oil was found to be contaminated with foreign particles a second

time. (Previously, the licensee had found the governors to have been

internally contaminated and removed and returned them to the manufacturer

for cleaning.) Reoccurrence of the contamination after reinstallation of

the governors caused the licensee to more closely inspect the control oil

reservoirs. Extensive flushing and visual inspection of the reservoirs

disclosed additional debris not previously noted.

The inspector questioned licensee personnel on the source of the debris.

The licensee considered that since the debris contained silica sand, that

it most likely was construction contamination which had not been cleaned

up during previous flushes of the system. The licensee responded to the

inspector's concerns by repeated flushes of the oil reservoirs to

_

12

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establish a baseline cleanliness for the system and by lockwiring the

filler caps for the reservoir to avoid tampering.

The inspector found that the licensee's actions appeared to be

appropriate to assess any further. repeat occurrences.

No violations or deviations were identified.

8. Review of Problem Statement Prioritization (0 pen)

Nuclear Service Cooling Water System (NSRW) Status Report Review

The inspector reviewed the licensee's System Status Report (SSR) for the

NSRW system for the acceptable prioritization of problem statements as

partLof an inspection of the licensee's Plant Performance and Management

Improvement Program (Safety Evaluation Report Item No. 2.3.2). The

inspector's criteria for acceptability as a post-restart item was whether

all regulatory requirements related to the item and system would be met

even if the item was not performed prior to restart.

The inspector noted that the NSRW system status report, Revision.1,

approved on 11/6/86, identified twenty-one problems. Of these problems,

four were considered priority 1, eleven were considered priority 2 and

six were considered priority 3. The inspector reviewed the priority 2

and priority 3 items (these items are considered post-restart by the

licensee) with the system engineer for the NSRW system and agreed with

the licensee's prioritization of them. In addition, it appeared that a

majority of the priority 2 and 3 items had already been completed.

The inspector brought to the licensee's attention at the exit meeting a

problem dealing with a resolution of an item identified in the SSR. The

item (QTS 26.0192) was classified as priority 2; it identified the

possible flaking of interior epoxy coating of the raw water piping. The

resolution defined for the problem was to monitor the pressure drop for

for the NSRW heat exchangers and if the pressure drop became excessive,

"... problem will be represented to PAG for possible upgrading to

Priority 1 status". The inspector's concern for this resolution was that

the monitoring of the pressure drop was considered priority 2, but, if

the results of the monitoring effort were poor then the problem would be

considered as a possible restart item. However, when the priority 2 item

was completed the plant would have already been restarted, and upgrading

the item to priority 1 at that time would be ineffective. The licensac

acknowledged this discrepancy, and noted that a "true-up" program had

been established to address similar inconsistencies systematically. The

inspector will continue to followup this issue and review the completed

work after the "true-up" program has resolved these types of issues.

No violations or deviations were identified.

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9. Inspection of Allegations

Characterization

Temporary power plant mechanics are inadequately trained for their work

assignments in most cases. (Allegation RV-A-87-10)

Implied Significance

Work activity performed on safety related equipment could possibly effect

the performance of equipment and not be detected by post maintenance

testing or surveillance. Such failures would then be prevented only by

carefully planned and conducted work activity by qualified crafts people.

Assessment of Safety' Significance

The individual is specifically commenting on the amount of supervision

crafts people received during the work activity. The alleger believed

there was inadequate supervision, leading to higher radiation exposure.

The concern centers on .a one-of-a-kind work activity which was being

performed for the first time.

The inspector reviewed three work requests covering work on motor

operated valves and installation of the Hydrogen Recombiners in

containment. In both cases, the work request /ECN covering the work

activity was properly documented and contained sufficient instructions to

perform the work. Craft foremen were observed by the inspector to be

carefully observing work practices of their respective crews. During

breaks or other periods of reduced work activity the crews were observed

to adhere to ALARA principles if they were in a high radiation areas. In

discussions with the crews they all appeared to have discussed their work

activity prior to commencing the job. In the case of MOV work all crafts

people had received training for their activity.

Staff Position

No evidence of inadequate training of temporary plant mechanics was

discovered. The allegation was not substantiated. (CLOSED) j

'

Action Required

None

Characterization l

The allegation (Allegation RV-A-87-16) concerns the following aspects

involved in welding:

a. Harassment by supervisors for raising quality / safety concerns

b. Inadequate welder training

c. Inadequate weld rod control

d. Supervisory pressure to weld without pre-heat

e. Inadequate welding tools

f. Inappropriate use of welder I.D. stamp

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.

Implied Significance

Safety'related welding activities must be performed in accordance with

committed codes and standards to insure that designed strengths are ,

obtained. Such inadequacies as discussed above could lead to failures of '

structures or plant systems.

Assessment of Safety Significance

Concern number 1 addressed the harassment due to the raising of a safety

or quality concern. For the work which occurred on safety related

equipment, Quality Control Inspectors were present to witness hold

points. The inspector questioned two QC personnel who inspect welding to

identify if they believed harassment had occurred or if they were told of

any harassment. Both stated that they are not aware of any harassment i

occurring. They also stated that they would report to Quality Management ,

any safety and or quality concerns raised to them. j

1

Concern number 2 addressed welder training onsite. All safety related

welding onsite was made in accordance with either ASME, ANSI or AWS

welding codes. All require welder training and performance tests. The

licensee's program for performance testing and training was in accordance

with committed code requirements.

Concern number 3 addressed weld rod control. The licensee subsequently

identified problems with weld rod control; this subject was discussed in,

Inspection Report 50-312/87-13. The problems were addressed by the

licensee's Quality Department, a report was made to licensee plant

management and a stop work was issued on onsite welding, The major issue

identified by Quality and the ANI concerned the traceability of weld

filler material. At the time of the inspection, onsite welding was in

progress with traceability maintained in accordance with requirements.

Concernnumber4addressedtgeuseofpre-heat. For most onsite welding,

a material temperature of 60 F was required. For all welding observed by

the inspector, the required temperatures were achieved without any

external heat source needed. In cases where a higher pre-heat

temperature was needed, QC was required to verify that the preheat

temperature was achieved. No instances were observed by the inspector

where pre-heat temperature was not maintained.

Concern number 5 centered on inadequate welding tools being used. The

inspector observed in process welding equipment onsite and welding

equipment in storage at the tool room. All equipment was in good working

,

'

order and delivering the required amount of current to the welding torch.

All hand-held welding devices were found to be operating properlys

Concern number 6 addressed the improper use of welder I.D. stamps. The

attached LLNL report in paragraph B.4 addresses a problem discovered by

the inspector of an incorrect I.D. apparently being used. The concern

here is similar. The traceability required is also achievable by

checking the " Weld Filler Material Withdrawal Slip" for welder I.D.

However, the proper I.D. stamp number must be used. This subject was

raised with licensee management and with the licensee welding engineer by

_ - _ _ _ _ _ _ _ _ . _ _ _ _ _ __.

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the inspector. ' Additional direction w.d provided to welders for defrect

use of their I.D. number. N, f

,

No specific welds were heatified by the concerned individual Wnne' ' !i i/

incorrect welder I.D. numbers were used. J ...

Staff Position \ ,

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"pWocedures or records were

Noinadequateoranacceptableweldirgkeallegationwaspartially

discovered riuring this inspectich. . T. t

substantiated (Concerns 3 and 6?) The lf< ensee corrective action i \

discussed in inis paragraph and p3repa,ph 6 appears adequate. Th;s

allegation is' closed. .

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Acti,on Required s

None.  ; i

s,

10. Followup on NRC Open Items '

,

3

Due to the ;1icensee's luge iGC ohen iden lis't, the licensee hai been

involved fri a program to providM aAore timely closure of NRC 'dentified "

4

open items. In this program a 'clor,ure /qckage for an item is assembled

and reviend by the licensing department and then verified as closed by

the quality assu'rance department. Af ter this procitss the package 'ir, i

available for the irdspector's review and inspection.

In previous inspection reports the'Hcensee's closure packages have been

discussed; however, it has. been apparent. that although there still exirts

a large number of open items, the raw of closure reportt3Mt have baen

available for inspection is very lcw 'In fut during this~ report period

there were times when no package; were avai'lable to inspect. The

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inspector discussed the need, duMng the exit meeting, to providr ,

information for open items on a timely tasis to facilitate the closure of

the open items. The inspecter will continw to inspect the licenseef s /

process for closing open items in a future inspection.

Enforcement Items

!

Violation 87-05-0} (CLOMD), " Voiding of NCR #S614(P

Inspection Report 87-06 identified a Notice ;,f Violation (Severity

Level IV) concerning licensee's measures which did not assure.that the

cause of the significant condition adverse to quality identified by

Nonconforming Report (NCR)-56140 dated 12/09/86 (emergency diesel

generator nonconforming condition) n s determined. In dadition, licensee

measures did not assure that corrective action to preclude repetition df 1

the significant condition adverse to quality identified by NCR-S6140 was j

taken. ,

I

The inspector's review of the licensee's responseidetermined the j

following: >

a. The licensee a$aitted that the violation occurred as stated.

.

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'f i The reason for the violation was a lack of communication between the

4 1 individual requesting the voiding of NCR-S6140 and the initiator.

f ' Under normal circumstances NCRs are voided only when no

3. i

'

, ' nonconforming condition actually existed, and in this case, it was

y a? j initially thought that no nonconformance existed. However, later

,,9l .

during a reevaluation subsequent to the voiding of NCR-56140,

Quality Assurance determined that the actual as-found condition was

, nonconforming.

I c. The corrective actions taken and the results achieved were that

Quality Assurance ~ Procedure QAP-17, " Nonconforming Material Control"

had been revised via Revision 5, dated March 16, 1987, to read "For

'

voided NCRs the QE Supervisor, or his designated representative,

will stamp, sign and date the NCR.. The originator or his supervisor

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must concur (sign and date) with the voiding. The Manager, Quality,

I can void an NCR without. concurrence of the originator."

(<t

In additien,sNCR-56140 was reopened by Revision 1 and processed in

accordance with QAP-17, Revision 5. The Governor Drive Coupling set

," screws were verified tight on 2/10/8'7 per work request #125701, and

NCR-56140 Revision 1 was closed.

+ The inspector concluded that the licensee's corrective action for this

violation was adequate.

, Violation 87-06-01 (CLOSED), " Failure to Issue NCR for Leaking Pipe"

Inspection Report 87-06 identified a Notice of Violation (Severity

Level IV) concerning that a Nonconforming Report (NCR) was not written

for non-isolable pipe leakage in the "A" train of the nuclear service raw

water (NSRW) system as identified in Work Request No. 110755 dated

2/2/86.

The inspector's review of the licensee's response determined the

following:

( a. The licensee admitted that the violation occurred as stated.

N b. The reason for the violation was the lack of adequate training in

'

Quality Assurance Procedure, QAP-17, " Nonconforming Haterial

Control" of the persons involved.

c. The corrective actions taken and the results achieved were that an

NCR-56480 was initiated on Feb. 27, 1987 to address this

non-isolable pipe leakage, and Revision 5 of QAP-17 was made

concerning this item on March 16, 1987. In addition, as part of the

revision process, plant personnel identified as requiring training

have been trained on QAP-17.

s

1b The inspector reviewed the training records and briefing notes for

! , , Revision 5 of QAP-17 which indicated satisfactory coverage of QAP-17

? I topics and attendance. NCR-56480's disposition was to replace the spool

oiece and work request #110755 fabricated and installed the spool piece

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on 3/9/87. Based on the licensee's corrective actions, the inspector

considers Violation 87-06-01 closed.

Violation 87-06-02 (CLOSED), " Failure to Post Abnormal Tag for Repair"

Inspection Report 87-06 identified a Notice of Violation (Severity

Level IV) concerning the licensee's failure to prepare an Abnormal Tag

for the temporary modification of the "A" train nuclear service raw water ,

(NSRW) pressure boundary as identified in Work Request No. 110755 dated

2/2/86. The "A" train NSRW as returned to service with a rubber patch

clamped onto the exterior of a defective pipe section to control

non-isolable leakage. This condition existed for over one year.

The inspector's review of the licensee's response determined the

following:

a. The licensee admits that the violation occurred as stated.

b. The reason for the violation was a lack of adequate training in

AP-26, " Abnormal Tag Procedure" of the person involved.

c. The corrective actions taken and the results achieved were that the

person responsible for failing to write the Abnormal Tag was

retrained in the requirements of AP-26 by June 2, 1987, and training

in the requirements of AP-26 and QAP-17 were given to Maintenance

Department personnel involved in the performance of corrective

-

maintenance.

During this training period, personnel were asked to identify other

cases of failing to issue an Abnormal Tag. No cases were identified

during this session. This action was completed May 2, 1987.

Based on the above licensee's corrective actions, the inspector considers

Violation 87-06-02 closed.

Violation 87-06-03 (CLOSED), " Failure to Provide Immediate NRC

Notification for LER 85-13 and 85-20"

Inspection Report 87-06 identified a Notice of Violation (Severity

Level IV) in which the licensee did not notify the NRC Operations Center

as described below of the following events:

a. Actuation of the "A" diesel generator on June 22, 1985. (Required

under 50.72(b)(2)(ii) and later identified in LER 85-13.

b. Discovery on October 7, 1985 of a failure of the essential control

room HVAC system to function per design requirements and Technical

Specification requirements. (Required under 50.72(b)(2)(iii) and

later identified in LER 85-20.)

c. Discovery on January 7,1986 that insufficient voltage would be

available to the essential control room HVAC power supplies

following a design basis LOCA. (Required within four hours under

50.72(b)(2)(iii) and in LER 86-23.)

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The inspector's review of the licensee's response determined the

following:

L a. The licensee admitted that the violation occurred as . stated.

1

b. The reason for the violation was that' administrative procedures.

established to control the reporting of plant occurrences did not-

, adequately define the responsibilities and process for evaluation

and reporting of events in accordance with the requirements of-

'10 CFR 50.72.,

c. The corrective actions taken and the results achieved we're that

Administrative Procedure AP-22, " Occurrence Description Reports

(0DRs) Reporting and Resolution" has been revised to amplify the

reporting requirements of 10 CFR 50.72. A'-22, Revision 12, was j

issued.on January 16, 1987.' Personnel identifying an unsafe,

atypical, or off-normal condition are now required'to promptly

.

notify the Shift Supervisor and to provide an ODR to the Shift'

Supervisor with one hour. The Shift Supervisor has been clearly

designated as having the responsibility for evaluating 10 CFR 50.72 ,

deportability and initiating 10 CFR 50.72 reports. As part of

Senior License training and requalification training, the Shift

Supervisor received instruction on the requirements of 10 CFR 50.72.

Since revisions to AP-22 have been implemented, there had been no

additional deficiencies in the reporting of 10 CFR 50.72 occurrences.

The inspector reviewed AP-22, Revision 12, which provided instructions to

ensure that an unsafe,. atypical or off-normal condition is promptly

verbally notified to Shift Supervisor (Para. 4.1.1), and an ODR delivered

to the Shift Supervisor with I hour of initiating the ODR-(Para. 4.1.3).

The procedure phone notifications shall be made by the Shift Supervisor

in accordance with paragraph 4.3 of AP-22. Para. 4.3.2,-states that if

an NRC telephone notification is required, the Shift Supervisor shall

make the notification to the NRC Emergency Operations Center within the

time limit specified in 10 CFR 50.72. Based on the above licensee's

corrective actions, the inspector considers Violation 87-06-03 closed.

Violation 87-14-01 (CLOSED), " Failure to Issue NCR on Capscrew Heads

_

Broken"

Inspection Report 87-14 identified a Notice of Violation (Severity

Level IV) concerning broken capscrews for the bearing positioner on the

RCP at the time of the Inservice Inspection of Reactor Coolant Pump (RCP)

P-210B on April'15, 1985. This nonconforming condition was not reported

on an NCR'and dispositioned accordingly. .As a result the required

management review and approval were not completed.

The inspector's review of the licensee's response determined the

following:

a. The licensee admitted that the violation occurred as stated.

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L. b. The reason'for the violation was inadequate training of the

personnel who were responsible for implementing Quality Assurance

Procedure, QAP-14, " Nonconforming Material Control".

c. The corrective actions-taken and the results achieved were that

plant personnel who were identified as requiring additional training

in the Nonconformance Report (NCR) process have been trained in

QAP-17, Revision 5, dated March 16, 1987. The nonconforming Reactor

Coolant Pump capscrews were replaced after management review

. determined that replacement was the. prudent corrective action. This

corrective action.was reviewed by the Plant Review Committee (PRC),

t

MSRC, and upper plant management, including the. Quality Department,

!. through the Occurrence Description Report (0DR) response review

L- process. These capscrews apparently provide. support of the RCP

bearing assembly during assembly. The licensee contacted the pump

manufacturer, Bingham-Willamette Company, and determined that the

failure of the capscrews had occurred due to relaxation of the mild

,

fastening. torque.and cycle fatigue. The licensee requested and

received a change in the vendor technical manual torque value and

, installed new capscrews with the higher torque values.

Based on the above corrective actions, the inspector considers Violation

87-14-01 closed.

Unresolved Item (URI)

>

URI 85-31-01 (CLOSED), " Procedures for USAR Revisions"

This item identified that in an amendment to the licensee's Updated

Safety Analysis Report (USAR) the licensee inadvertently omitted

revisions to one section of the USAR but the revision was made to another

section of the USAR.

The inspector reviewed this item in report 87-11 and reported that the

licensee's corrective actions appeared to be appropriate; however, the

item remained open pending a review of an issued Nuclear Directive

prescribing USAR revisions. The procedure, LDAP-0003 Revision 0,

effective date, 7/3/87, "USAR Revision Control", appeared procedurally to

control the revision process, therefore this item is considered closed.

1

Licensee Event Reports (LERs)

LER 85-19-L0 (CLOSED), " Reactor Trip on High RCS Pressure" ,

i

This.LER dealt with the October 2, 1985 reactor trip and subsequent

cooldown. This event occurred with the reactor at approximately 15%

power in preparation for a turbine overspeed trip. The licensee provided

a brief description of the event in the LER and provided a reference to a

letter submitted to the NRC (October 18, 1985) which contained the

licensee's corrective actions.

I

The event and subsequent followup has been addressed in NRC inspection

reports. In addition, the NRC immediately issued a Confirmatory Action

Letter (CAL) to the licensee, on the day of the event, which requested an

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explanation of the event and corrective actions prior to restarting the

plant. The licensee responded to the CAL and subsequently restarted in

. late 1985.

The inspector reviewed the action list generated from'the event. It

appeared that appropriate actions'have been identified and corrective

actions have been implemented. In addition, due to the December 26, 1985

event, the licensee has developed a more far reaching improvement program

which is being implemented to date and for certain items will be

completed prior to restart. Therefore, this LER is closed.

LER 87-11-LO, 87-11-L1-(CLOSED), " Snubbers Found Out-of-Tolerance

per New Temperature Compensated Acceptance Criteria"

This LER reported that previous testing done on hydraulic snubbers used

inadequate acceptance criteria which allowed snubbers to be declared

operable when it was later demonstrated that they were not operable based

on the corrected acceptance criteria. The original LER was inspected and

documented in NRC report 87-12. The revision to this.LER was submitted-

to the NRC on May 14,:1987.

The inspector reviewed the LERs and found that the LER reflected the

appropriate reporting requirements and descriptions. The root cause of

the failure appeared to be appropriately determined and corrective .

actions should correct the cause of the event. The inspector reviewed

the procedure changes initiated by the corrective actions and had no

further-questions. Based on the above review and previous inspection,

this LER is closed. LER 87-11-LO, 87-11-L1 is closed.

LER 87-15-LO (OPEN), "CO, Deluge System Deactivated"

Licensee Event Report 87-15 described several carbon dioxide protected

fire zones CO, deluge systems left deactivated and the zones unattended.

These numerout occurrences happened because personnel who, for safety

reasons, disabled fire protection C03 systems in the plant, and then

failed to reactivate the deluge system for over an hour after the safety

concern for personnel was no longer present.

The licensee's corrective actions were reviewed by the inspector who

determined the following:

a. A letter was transmitted to all site employees on tag removal and

zone reactivation to raise the awareness'of those requirements,

b. An item was placed in the plant daily newsletter " WATTS HAPPENING"

on March 10, 1987 to reinforce the requirement for tag removal and

zone reactivation.

'

c Safety meetings added on agenda item concerning tag removal and zone

reactivation.

d. Administrative Procedure (AP) 30, " Entrance into Carbon Dioxide Fire

Protected Zones" has been revised to explicitly state if no other

identification tags are present, remove your identification tag.

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Procedure temporary change No. 87-0392 added paragraph 3.3.5.3 to

state: " Remove your identification tag" and was approved on

April 6, 1987.

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e. In addition, corrective action was instituted to provide an hourly i

verification that personnel are, in fact, in the deactivated CO 1

Zone when the system is deactivated. Thisverificationwillrebain

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in place until system design or the entry procedure is revised to

provide improved control of system and personnel status or until it

has been demonstrated to the Plant Review Committee that the

corrective measures have been effective. Per conversation with

Regulatory Compliance by the inspector revealed that there has been

a marked decrease in the number of Occurrence Description Reports

written for CO2 related events.

This LER will remain open based on findings discussed in inspection

report 50-312/87-15 and not yet resolved.

LER 87-19-L0 (CLOSED), " Failure to Post Fire Watch"

Licensee Event Report 87-19 described the failure to post a continuous

fire watch posting in Fire Zone 78 during a welding job, after removing

the fire detection system from service. After removing the detection

system from service the Control Room should have taken compensatory

measures, and established a continuous fire watch as required by

Technical Specification 3.14.6. The continuous fire watch posting was

required due to the breaches between the areas comprising the fire zone.

The Control Room did not upgrade the hourly fire watch patrol to a

continuous fire watch.

The licensee's corrective actions were reviewed by the inspector who

determined the following:

a. The Operations Department issued Special Order 87-15 to its staff.

Due to the complex nature of the fire protection components in the

plant, special order 87-15 requires that the Shift Supervisor must

rely on the Fire Protection Coordinator and his group to provide an

analysis of each situation to justify why a continuous fire watch

should not be used. AP.60, " Control of Fire Protection Limiting

Conditions for Operation", step 4.3.2.2.5.2, states, " Post a

continuous fire watch until the Nuclear Operations Fire Protection

Coordinator (N0FPC) can provide further analysis."

b. The corrective action regarding the missed continuous fire watch

posting in Fire Zone 78 was accomplished when detection was restored

on February 13, 1987, at 2:30 a.m.

,

c. This LER described an event which has recurred at Rancho Seco, and

the writing of the special order is an outgrowth of the review of

the licensee's fire watch policies.

,

Based on the above licensee's corrective actions, the inspector considers

Licensee Event Report 87-19-L0 closed.

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, 11. ' Unresolved Items

Unresolved items are. matters'about which more information is required to

o determine whether they are acceptable or may involve violations or_ -

? . deviations.

12. Significant Meetings

On June. 18, 1987, the. inspector attended the bimonthly meeting of

~

, ' licensee's board of supervisors at.the licensee's headquarters in-

Sacramento. The licensee's new Chief Executive Officer, Nuclear,
presented a revised-schedule for plant restart in January,1988, with an  ;)

. extensive power ascension test program to extend.into June, 1988. In

. addition, the licensee announced the selection of Karl Meyer as the

Nuclear Licensing Manager.

)

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A meeting was held at Rancho Seco on June 7, 1987 to discuss the status j

of the system' review and test program (SRTP). The attendees in the j

meeting. included J. Martin,.L. Miller,.and the resident staff of the NRC' '

and W. Bibb and G. Blackburn of SMUD.

The licensee presented.an overview of the SRTP which included in part the

organization chart, the system status report flow chart, system test

matrix. outline, and an outline for the hot shutdown and power ascension

testing.

13. Exit Meetina

The. inspector met with licensee representatives (noted in' Paragraph 1) at

various times during..the report period and formally on July 14, 1987.

The scope and findings of the inspection activities described in this

report were summarized at the meeting. Licensee representatives 1

acknowledged the inspector's findings and violations identified. l

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Enclosure C

Review Conducted by Lawrence Livermore National Laboratory Personnel

of Major Facility Modifications at Rancho Seco

The inspections performed and documented in this paragraph were performed by

Lawrence Livermore National Laboratory (LLNL) personnel for the USNRC, and

under the supervision of the Senior Resident Inspector. ,

I

The following documents, procedures, and standards were reviewed as background 1

for. inspection of recent construction involving the major plant modifications. {

i

- NRC Inspection Report #50-312/85-01

Re: NSEB Construction Review

- NRC Inspection Report #50-312/85-19 ,

Re: High-Point Vent Review I

- SMUD Procedure, NEP 4109

" Rancho Seco Configuration Control"

- SMUD Construction Specification, NEP C5307 series

Re: Installation of piping, welds, and supports

- SMUD Construction Specification, NEP C5303

Re: Expansion Anchors in Concrete

- SMUD Procedure, NEP 6405

" Pipe Supports"

- Rancho Seco Welding Manual

- Rancho Seco Nondestructive Examination Manual

- SMUD Procedure, NEP 6118

" Field Problem Report"

- ECN #A-5415 Major for EFIC

- ECN #A-5415A

Re: Level Taps on Steam Generator

- ECN #A-5415AB

Re: MOVs on MFW isolation

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ECN #A-5415AC

Re: MOVs on ADVs isolation of steam generator loop

- ECN #A-5415AD

Re: MOVs on Turbine Bypass isolation

A. Items Inspected

1. ECN #A-5415A Re: EFIC Level Taps on Steam Generator

The inspector used the as-built drawings in the field to verify

hardware condition and location for the four EFIC nozzles on Steam

Generator E-205-A. No hardware problems were found, dnd the

as-built drawings reflected the field condition adequately.

2. ECN #A-5415AC Re: MOVs on two ADVs

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The structural member upgrades, pipe support modifications, and the '

piping welds for installation of MOVA on two ADVs (in Areas 6 & 7

between the reactor building and the fuel storage building) were

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inspected. No field problems were encountered in comparing ,

Drawing C-612, sheets 1 & 2 with the hardware. '

3. ECN #A-5415AC Re: MOVs on Turbine Bypass isolation  !

Structural member upgrades, pipe support modifications, and piping  !

welds were field reviewed by the inspector for the installation of I

l four MOVs on the main steam turbine bypass lines (in Areas 6 & 7 J

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between the reactor building and the fuel storage building and the j

l fuel storage building). Drawing C-611, sheets 1, 4, & 6 adequately l

reflected the as-built condition of the hardware.

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! B. Followup Documentation Review

As part of the review of ECN #A-5415A involving the EFIC Nozzles on the

! steam generators, six work request (WR) packages were selected by the l

1 inspector: WR 125164, WR 125011, WR 125165, WR 116569, WR 125166, and I

WR 125167. These work request packages were checked for adequate {

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documentation of QC records, welder identification, material

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traceability, valve serial number, weld procedure, and weld {

identification. '

The following are findings made by the inspector:

l 1. For WR 125165 (line 20601 - 3/4" - CA, steam generator E-205-A) of

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ECN #A-5415A, there was no weld filler material issue (FMI) slip ,

l attached to the work request package, for the repair of weld "I" at (

l the steam generator shell. The FMI slip is routinely used to record

l the work request number, date, weld numbers, welding procedure,

I filler material size and type, heat number or lot number, and welder  ?

l identification. The weld repair record form in the work request

i package included instructions to the welder for which welding

i procedure and filler material to use and the location of the weld;

! but no record of heat number traceability was shown for the weld I

l repair. l

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This work request package (WR 125165) had been reviewed by the

licensee's " Filler Material Task Force" several weeks prior to

review by the inspector. The lack of heat number traceability in

the work request package for the weld repair was not detected by the l

! licensee during it's in-house review by the task force. The I

licensee decided to initiate an NCR for this discrepancy. The weld

inspection check list (ICL) for weld "I" indicated that it was

nuclear class 1 with ASME section III, subsection NB as it's

I applicable code. Also, the work request cover sheet lists the

welding of the EFIC nozzle to the steam generator shell as an ASME i

"Section XI work package". l

2. It should be noted that performance traceability of weld "I" was

possible in the field, since the welder identification (SM 319) was

stamped nearby the repaired weld on the pipe. In reconstructing

what had occurred, SMUD produced a copy of the FMI slip for Welder

SM 319, dated 12/22/86 for weld "A" on WR 116569. Weld "A" was only

3 inched away from weld "I" on the same line (20601) but a different

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work request package. When the licensee contacted Welder SM 319 on

6/10/87, he explained that he had noticed some base metal reduction

on weld "I" on 12/22/86.

Welder SM 319 concluded that the base metal reduction had occurred

during preparation of weld "I" for a magnetic particle test (MT) on

12/21/86 when some grinding at the toe of the weld occurred. The MT

report on 12/21/86 showed weld "I" as acceptable, with no mention of

base metal reduction. On 12/22/86, the plant welding engineer

authorized the repair of weld "I" by initiating a weld repair record

form, per information from Welder SM 319. At that time, WR 116569

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was entered at the top of the weld repair record form in error,

since the nearby weld "A: was what Welder SM 319 had been working

on.

Later, on 1/12/87, the Field Engineer corrected the weld repair

record form to show WR 125165 for weld "I". Also, Welder SM 319

explained that he originally described to the plant welding engineer

on 12/22/86 that weld "I" had 1/16-inch undercut all-around, instead

of the base metal reduction which he later described on 6/10/87. It

turned out that the required filler material for weld "A" and for

repair of weld "I" was the same type; but weld "I" had no record of

filler material issue.

3. In reviewing several work request packages, the inspector noted that

all of the records showed the proper weld identification (line

number plus alpha designator) except for the magnetic particle test

(MT) reports. The design drawing, weld inspection check list, weld

repair record form, and liquid penetrant test (PT) report typically

showed the proper weld identification. The MT reports should show

the same description of weld identification for clarity and

consistency in records.

4. The weld filler material issue (FMI) log on 1/5/87 and 1/6/87 showed

the welder somctimes as SM 314 and other times as SM 319. The

correct identification is SM 314 per the Master List of Welder

Qualifications.

Followup Actions by Licenses

At a pre-exit meeting on 6/12/87, the Plant Welding Engineer and the QC

Supervisor suggested that an improvement to the nondestructive

examination (NDE) manual would be to: .

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a. Require visual weld inspection (VT) on all NDE that required

grinding; and

b. Require that any post-weld heat treatment (PWHT) occur prior to

the " final" visual weld inspection (VT).

At the exit meeting on 6/12/87, the licensee committed to the following:

a. District will perform a re-inspection of the four EFIC Level

Tap nozzle welds on each steam generator; and

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. . b '. District will perform an additional. documentation review on the

i: . corresponding work request packages.

Electrical, Instrumentation and Control EI&C of.EFIC and TDI

Four EFIC Engineering Change Notice (ECN) packages were selected for-

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audit,- These were:

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'ECN A-5415B -Installation.of.new once throughisteam generator

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_ level transmitters

ECN A-5415E- . Electrical.and fiberoptic cable to the EFIC local

control panels

ECN A-5415AA Power and control to valve motor operators HV-20581'

and HV-20582

ECN A-5415AH ' Installation of the Control Room EFIC panel

These packages _were selected to. provide a representative sample of EFIC

construction work activity. These packages include power, instrument,

and control' circuits. They also provide a cross section of the EFIC work

in the Control Room, Containment, Nuclear Services Electrical Building-

(NSEB), and the Tank Farm.

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A number of. Design Change Notices (DCNs) were selected from each package.

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These were_ walked down to confirm that the'as-built configuration

conformed with the design.as defined by the DCNs, and Rancho Seco

construction specifications and procedures.- The specific items inspected

included:

Power cable routing to motor operated valves HV-20581 and HV-20582

including breakers.and terminations in load centers SOC 2, 50D2, and

several field terminal boxes.

Instrument cable routing between level transmitters LT-20505A, and

LT-205078 including terminations at transmitters, containment

penetrations, and field terminal boxes. _Also examined transmitter

installation to determine compliance with equipment qualification

requirements.

Selected terminations and channel separation in the HISS (E) panel.

Also inspected device installation and human factors enhancements.

Selected terminations and separation in the EFIC field panels H4E181

and H4FWB. 'Also examined fiberoptic cable installation in the H4FWB

panel.

Witness of electrical construction activities in panels S1B2 and

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S102. This work in progress is covered by Work Request 120609.

. The EFIC inspection included review of several Work Requests which

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implemented these ECNs. Work Requests include detailed work

instructions, material records, and inspection records.

Inspection of TDI construction included:

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Diesel engine. control panels H2 DEA 2 and H2DEAB2

-Safety related wiring on the "A" side diesel skid

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l "A" side raceway installation

Portions of the electrical' distribution system associated with the

TDI including both 480 volt and 4160 volt circuits

Portions of the TDI building essential Heating, Ventilating and Air

Conditioning (HVAC) system

The "A" side motor control system

The "A" side engine radiator fans

The "A" side fuel oil system pumps and level instrumentation >

Findings

Except for one issue, the EFIC items inspected conform with design.

The area of exception is wiring separation inside of control panels.

Three of the EFIC panels inspected had the potential for wiring

separation problems. Two of these contained separation problems

that were not detected by the licensee Quality Control (QC)

' inspections. ,

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ECN A-5415 AH, drawing change notice OE, to drawing N25.08-46,  ;

Revision 3 requires: "The wiring of individual channels (separation  !

groups) must be bundled together and separated from other channels

by a minimum of 6-inch air space. Where conduit or Siltemp is used

a minimum of 1 inch air space is required." Contrary to this

requirement, LLNL's inspection identified fifteen cases in control

room panel HISS (E) where vendor installed internal panel wiring of

different channels was not separated by 6 inches and was not

protected by Siltemp or conduit. The vendor installed wiring was  !

inspected and accepted by the district and the inspection documented.  ;

in a Source Inspection Data Report dated November 26, 1986.  !

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Nuclear Engineering Procedures (NEP) Manual section 5304.8C, I

" Electrical Cable Installation and Termination" requires that safety  ;

related and nonsafety-related cables, or different channels of )

safety related cables be separated by 6 inches of air space or a

metal barrier. It also allows an alternate barrier consisting of

Fiberfrax sleeving or tape covered by Scotch 69 tape where 6 inch

separation does not exist. Field cables entering the HISS (E) panel i

are protected in'this manner where the 6 inch separation criterion

cannot be met. In a number of cases, however, LLNL's inspection

found the Fiberfrax installation stopped short of the quick

disconnect connectors used as field wiring terminations.

Consequently, about 1/4 to 1/2 inch of cable is left unprotected  !

where the cable enters the connector. Additionally, the cable entry

hole in the connector backshell is not protected by fire retardant

material. This installation of field cables was installed,

inspected, and accepted by Work Request 124925 which was closed on j

March 21, 1987.

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A similar situation exists in panel H4FWB. Non-safety field cables

in this panel were wrapped with Fiberfrax tape to the point where ,

the cables pass through a hole in a terminal box which separates  :

non-safety terminal blocks from safety related terminal blocks. .

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LLNL's inspection found that the tape did not extend to the point

where 6 inch separation or a metal barri6r exists between safety

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related and nonsafety-related cables. This configuration was

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installed, inspected, and accepted by Work Request 111991, closed

out on February 2, 1987. Subsequent to the above inspection

finding, inspected the similar panels H4FWA, H4FWC, and H4 FWD and

found problems of the same nature in these panels as well.

The district issued Nonconforming Reports 56754, and S6847 to document

and resolve the above LLNL inspection findings.

Cable separation problems inside of panels.are not confined to the EFIC

modification. In the TDI system, diesel generator engine control panels

H2 DEA 2 and H2 DEB 2 both contain safety and nonsafety vendor installed

wiring separated by only 4 inches of air space. Also, they contain

nonsafety-related wiring installed bundled with safety related vendor

installed wiring. This LLNL inspection finding was documented by

Nonconforming Report S6811, dated July 3, 1987. The installed wiring was

installed and inspected under Work Requests 115274 and 115276, both of

which were closed out on March 27, 1987. Neither work request included l

requirements or criteria for the inspection of wiring separation.

Except for the case of internal panel wiring separation, the inspected

areas of EFIC El&C construction exhibited acceptable workmanship and

conformed with design. The minor differences between drawings and the

as-built condition were:

ECN A-5415AA, DCN 0, E-342, Sheet 88, Rev. O. The terminations

identified on this drawing as "***" were made in the field using a

different combination of Raychem tubing than specified on the

drawing. This deviation was approved by FPR-6 to ECN A-5415AA,

however, the drawing was not revised to reflect this change.

ECN A-5415AH: DCN 0, I-1485, Sheet 1, Rev. 1., DCN0, I-1486,

Sheet 1, Rev. 1; DCN 0, I-1487, Sheet 1, Rev. 2; DCN 0, I-1488,

Sheet 1, Rev. 2. These drawings indicate that the OTSG water level

and pressure indicators use soldered terminal connections. The 3

installed units use screw-compression terminal connectors.  !

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ECN A-5415AH: DCN 0, I-1485, Sheet 1, Rev. 1, DCN 0, I-1486, l

Sheet 1, Rev. 1. These drawings identify the control room EFIC 1

panel as numerical displays as three digit displays. The installed l

displays are four digit. l

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ECN A-5415AH, DCN 0, Sheet 3, E-402, Sheet 19A, Rev. O. The edges i

of the "EFIC Initiate / Test Matrix" label are not painted in I

accordance with the drawing.

None of the above deviations from design affect the functionality of EFIC

equipment.

LLNL's inspection of TDI EI&C construction indicated that the TDI I

construction exhibited more deviations from requirements than did the l

EFIC system. In one case a condition was noted which deviates from the i

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provisions for cable separation by voltage level described.in the Updated :

Safety Analysis Report (USAR).

Manhole'47, part of.the channel A underground raceway between the

TDI building and the NSEB, contains safety related and non-safety

related instrumentation cable intermingled with safety related power

cable. In one' case safety related instrumentation cable are laying

across 350 MCM, 480 VAC conductors. This is contrary to the

criteria for cable separation by voltage level described in

Rancho Seco USAR section 8.2.2.11.H.5. This section states " Power

and Control circuits are not mixed with instrumentation circuits in

any raceway in any system." LER 87-26 reported a similar but

separate occurrence of mixing power and instrumentation cables.

licensee engineering is taking action to address this finding.

(' In addition'to the above mentioned separation problems in the manhole and

diesel engine control panels, LLNL's inspection observed several

deviations from design documents or construction specifications in the

TDI building. Approximately one-half of the items inspected contained-

some deviation from requirements. The specific items noted are as

l follows. None of these were previously identified and documented by

L licensee inspections.

Three of the four mounting bolts attaching safety related

thermocouple TE55701 to it's Unistrut support are not snugged up to

l the thermocouple support base plate. The lock-washers were not

compressed and about 1/8 inch gap existed between the bolt heads and

the base plate. The bolts appeared to have been torqued, however,

the bolts bottomed'out against the base of the Unistrut to which

, they were attached before they seated against the thermocouple

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support's base. plate. Subsequent to LLNL's inspection, the licensee

documented these findings in NCR 56810.

The thermocouple extension wires for essential HVAC room temperature

thermocouple T#55701 were labeled such that the connections in the

thermocouple connection box appear to be reversed from the

connection drawing. Careful examination, however, showed that the

extension wires are properly connected,.but the wire number labels

are reversed. Licensee inspection noted also that the insulation of

the thermocouple extension wire was cracked. This wiring was

installed and inspected under Work Request 82910. The inspection

was conducted on October 4, 1984 as documented by the termination

cards. Licensee has documented LLNL's inspection findings in

NCR S6810.

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Essential HVAC damper actuator HV-55713 is shown on ECN-3748, DCN-0A

to drawing M17.07-6 as model number MNQ-12-8-1600, the installed

model number is MNQ-12-4-1600. Licensee documented this finding in

NCR 56813.

Essential HVAC air handling unit AH-DG-1B termination box contains

4 AWG triplex cable in which individual cables are bent tighter than

the allowable bend radius. The worst observed bend radius was about

3/4", the allowable specified by NPEM 8304.8C section 5.1.27 is 1.6

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inches. Installation and QC inspection of this item occurred under

Work Request 82910. QC inspection occurred on October 17, 1984 as

documented on the termination card. Licensee inspection determined i

that a similar condition exists in the terminal box of opposite j

train's air handling unit. Licensee has documented these inspection  !

findings in NCR 56845. l

Two cases were noted in which tray edge bumpers were not installed

as required by Licensee procedure NPEM 5304.7.C section 5.2(12) to

protect cable entering over the edge of the tray. These cases are

in tray A57El where cable enters from conduit A57015, and tray L5782

where cable enters from conduit L57046. In the former case

deformation of the cable jacket has resulted from contact with the I

tray edge. In the later case the cable does not actually rest on  ;

the tray lip because the cable hangs by rope from the tray above. l

This configuration is not addressed by licensee procedures, and it I

appears that the cable would rest on the tray edge if the rope were  !

removed. These items were respectively installed and QC inspected j

under Work Requests 84414 and 82910. Inspections occurred on j

May 5, 1985, September 18, 1984, and September 19, 1984 as j

documented by the pull cards. There remains some question whether

the construction specifications required the installation of bumpers

at the time of this installation. Nevertheless, licensee has

prepared NCR S6844 to track resolution of these items. The above

two items, dealing with the bend radius of cables in the HVAC air

handling unit and the lack of tray edge bumpers noted above are j

considered together as an apparent violation. (87-20-02). 1

Pull box H7J2995 is labeled as " black", i.e. , non-safety, when, in 3

fact, it is part of the channel "A" raceway system. NPEM 5304.7C )

requires installation of appropriate separation group color

markings. Licensee has prepared NCR S6843 to document this finding.

Terminal box H7J2968 has a cable labeled as 1G1DIEA2B installed in

the location where DCN OF sheet 2, ECN A3748, drawing #344 sheet 17 {

shows cable 1G1DGA2V drawing. NCR S6846 was prepared to document

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this finding.

In motor control center S2A4 cubicle 4, one of the wires to the i

starter contactor was terminated with a lug on which the barrel was l

bent backwards from the ring by about 90 degrees. This panel was

inspected and the condition accepted by licensee on

February 6-9, 1984, and on February 14, 1984 as documented by the

Source Inspection Data Report and the Receipt Inspection Data Report

for this motor control center. Licensee documented this finding in

NCR 56809.

Safety related terminal boxes H7J2967 and H7J2968 on the "A" TDI l

diesel skid contain several terminal lugs which do not have the i

required insulation crimp. Licensee has documented this inspection

finding in NCR 56846.

During walkdowns in the TDI building three " automotive type" electrical

"T" connectors were found adrif t in the HVAC mezzanine of the TDI

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building. This type of connector is not approved for plant use by the

licensee as it does not provide a reliable permanent connection. Even

temporary use damages conductor insulation. Inspection of nearby

terminal boxes failed to identify any evidence of their use. It is

possible, however, that the previously noted insulation damage of the

TE55701 extension wire may have been caused by this type of connector.

Licensee is evaluating the need for a program to determine if these kinds

of connectors are used at the plant, report on corrective action taken to

repair damage caused by these types of connectors, and establish controls

to prevent their use in the future.

The EFIC and TDI inspection also identified several items of potential  !

concern. Licensee was, however, unable to produce documentation during ,

the inspection to resolve these items or confirm that they represent {

deviations from their design, safety analysis, or commitments to NRC.

These open items are:

The cable within manhole 47 is supported on cable racks held in ,

place only by the weight of the cable. In addition, the supports

for the racks are anchored with concrete expansion anchors which are )

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not marked with torque stripes, and which, in some cases, do not

appear to be installed perpendicular to the concrete wall. During

the inspection the licensee was unable to provide documentation

which established the seismic qualification of this configuration.  ;

If indeed this is not a seismically qualified installation this

would be contrary to USAR Appendix 5B section 58.2 which indicates

" seismic class I structures and components are... designed to

withstand appropriate seismic loads and other applicable loads i

without loss of function." Licensee Engineering is investigating {

this issue. J

Attachment bolts for Unistrut used as supports for safety related ,

conduit L57065, and A57081 appear to have bottomed out against the

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embedded Unistrut to which they attach. While the lockwashers are

compressed in these cases, that the bolts are bottomed out raises i

the question whether torquing generated the intended preload.  !

ECN A-3748, DCN 5 to drawing C906 sheet 2 revision 1 identifies the I

torque requirements for these bolts. Followup inspection by

licensee determined that a number of similar cases exist in the TDI

building. Licensee is issuing an Engineering Action Request te

evaluate this potential problem.

Separation of redundant cables and separation of safety and

non-safety wiring within panels is sometimes provided using two

layers of Siltex or Fiberfrax tape or a single layer of Siltex or l

Fiberfrax tubing. These installations are in accordance with

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construction specification NPEM 5304.8C. Licensee, however, was not

able to produce test reports for the Fiberfrax to demonstrate that

this installation provides an adequate barrier. A portion of a test

report was available to demonstrate the capability of the Siltex

tape. Information was not, however, available to confirm that the

single layer of Siltex tubing provides protection equivalent to that

of two layers of tape.

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The inspection also' identified several items which are in accordance.with i

the design, and in compliance with site procedures and specifications yet-

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... i are. a. concern to the inspector and should be addressed by the licensee. i

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The following items will be tracked as one open item. (87-20-03).  ;

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The channel A cable ducts from the NSEB to the Auxiliary Building

contain channel.C flex conduits laying on the A channel cable.  !

Similarly, the' channel B ducts contain D channel flex conduits.  !

This condition was previously identified by licensee to.the NRC i

Division of Nuclear Reactor Regulation (NRR). NRR is reviewing- j

SMUD's justification for this deviation.from the physical separation .i

guidance of Regulatory Guide 1.75. '

Procedure NPEM-5204.13, Revision 0, " Preparation of Schematic. l

Diagrams" requires labeling of electrical schematic drawings as ;l

" Nuclear Safety Related" if the drawing includes safety related  !

circuits. Procedure NPEM-5205.1,~ Revision 0, " Instrumentation Loop

Diagrams", contains no such requirement. .The inconsiste.ncy.between '

the requirements for electrical:and instrumentation schematic

drawings may-cause confusion.in determining if instrumentation

circuits are safety related. D

-The human engineering review of the H1SS(E) panel was. performed on

the equivalent' simulator panel and on the de-energized control room

panel. While there are differences between the simulator panel and

the control room panel, there is no plan to review the energized

control room H1SS(E) panel against human factors design criteria.

Therefore, the HISS (E) panel will not be completely reviewed with

respect to those human engineering criteria which can only be-

evaluated using the energized panel.

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' Construction specification NPEM 5304.8C does not contain

requirements for separation of redundant' channels except within

equipment enclosures, or for separation of different voltage

classes. Therefore, QC inspectors have no clear basis for

inspection of cable separation in areas such as manholes or the

training of cables between raceway. Licensee procedures, in

general, do not acknowledge the licensee's commitment to meet the

intent of Regulatory Guide 1.75 for.TDI and EFIC construction.

Therefore, this attribute of the system design is not being

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inspected by QC.

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