Letter Sequence Other |
---|
|
|
MONTHYEARML20204E3301980-07-0202 July 1980 Discusses Objectives & Conclusions Re Helium Circulator C-2102 Insp.Forwards Ga Co rept,GA-C15847,re Insp Results. Requests Review of Proposed Inservice Insp Program in Draft Tech Specs Submitted 800331.W/o Rept Project stage: Draft Other ML20237K2111987-07-31031 July 1987 Monthly Operating Rept for Jul 1987 Project stage: Other ML20237G7401987-08-21021 August 1987 Notification of 870911 Meeting W/Util in Arlington,Tx to Discuss Plant Circulator Failure & Recovery Project stage: Meeting ML20235H4731987-09-11011 September 1987 Preliminary Rept of Helium Circulator S/N C-2101 Damage & Justification for Returning to Power Operation Project stage: Other 05000267/LER-1987-018, Summarizes Util Commitments to Support Continued Operation of Plant,Per 870911 Meeting W/Nrc Re Damage in Helium Circulator C-2101 (Ref LER 87-018)1987-09-21021 September 1987 Summarizes Util Commitments to Support Continued Operation of Plant,Per 870911 Meeting W/Nrc Re Damage in Helium Circulator C-2101 (Ref LER 87-018) Project stage: Meeting ML20235H4401987-09-21021 September 1987 Summary of 870911 Meeting W/Util in Arlington,Tx Re Failure of Plant Circulator S/N C-2101 & Licensee Program to Recover from Failure.Licensee Rept, Preliminary Rept of Helium Circulator S/N C-2101 Damage & Justification... Encl Project stage: Meeting ML20236U5651987-11-20020 November 1987 Forwards Interim Safety Evaluation Re Helium Circulator S/N C-2101 Damage & Util Commitments for Continued Plant Operation.Reactor Will Be Shut Down Until Corrective Actions Are Completed Project stage: Approval ML20236U5761987-11-20020 November 1987 Safety Evaluation Re Helium Circulator S/N C-2101 Damage. Util Corrective Action Program Initiated Project stage: Approval ML20237A8151987-12-0808 December 1987 Forwards List of Questions Re New Bolting Matls for Helium Circulator C2101,per 871118 Telcon.One of Key Issues Was Util Decision to Use A286 Spec Bolts to Fasten circulator- Steam Scroll to Bearing Housing Project stage: Other ML20148G8301987-12-14014 December 1987 Metallurgical Analysis of Components from Helium Circulator C-2101 Project stage: Other ML20148G7711988-01-22022 January 1988 Forwards Rept of Helium Circulator S/N C-2101 & Inlet Piping S/N 2001 Repair & Mod Activities, Per Commitment in . Insp Findings & Proposed Tech Spec Amend to Be Submitted 8 Months Following Removal of Circulator for Insp Project stage: Other ML20148G7941988-01-22022 January 1988 Rept of Helium Circulator S/N C-2101 & Inlet Piping S/N 2001 Repair & Mod Activities Project stage: Other ML20148G8511988-01-22022 January 1988 Helium Circulator Insp Schedule Project stage: Other ML20153A8551988-03-0909 March 1988 Summary of 880304 Meeting W/Util to Discuss 880122 Submittal Re Helium Circulator Failure & Recovery.Attendee List & Viewgraphs Encl Project stage: Meeting ML20151L8911988-04-14014 April 1988 Discusses Revised Helium Circulator Outage Schedule,Per NRC 880304 Meeting.Schedule for 12 Wk Outage for Refurbishment of Helium Circulators Will Start on 880705 Instead of 880502 Project stage: Meeting ML20195K0591988-06-15015 June 1988 Forwards SER Concurring W/Util Proposed Corrective Actions in Engineering Rept Entitled, Helium Circulator S/N C-2101 Damage & Inlet Piping S/N 2001 Repair & Mod Activities Project stage: Approval ML20195K0651988-06-15015 June 1988 SER Concurring W/Util Proposed Corrective Actions in Engineering Rept Entitled, Rept of Helium Circulator S/N 2101 Damage & Inlet Piping S/N 2001 Repair & Mod Activities Project stage: Other 1987-08-21
[Table View] |
|
---|
Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20246J3261989-08-30030 August 1989 Safety Evaluation Supporting Amend 72 to License DPR-34 ML20245J3781989-08-14014 August 1989 Safety Evaluation Supporting Amend 71 to License DPR-34 ML20245J4511989-08-0808 August 1989 Safety Evaluation Responding to Issues Re Tech Spec Upgrade & Plant Defueling.Stated Tech Spec Sections Should Be Upgraded ML20246J3131989-07-0707 July 1989 Safety Evaluation Concluding That Operators Role in Mitigating High Energy Line Break at Facility Acceptable ML20247R2261989-05-26026 May 1989 Final Safety Evaluation Re LER 87-20 Concerning Interactions Between Steamline Rupture Detection/Isolation Sys,Plant Protective Sys & Control Sys at Facility ML20245C5031989-04-18018 April 1989 Safety Evaluation Supporting Amend 70 to License DPR-34 ML20248D6501989-03-31031 March 1989 Safety Evaluation Supporting Amend 69 to License DPR-34 ML20236A1401989-02-27027 February 1989 Safety Evaluation Supporting Amend 68 to License DPR-34 ML20235T4511989-02-24024 February 1989 Safety Evaluation Re Facility Core Support Flow Vent Sys. Continued Operation of Facility W/Current Core Support Flow Sys Configuration Acceptable ML20235J3421989-02-16016 February 1989 Safety Evaluation Supporting Util Action in Response to Generic Ltr 83-28,item 2.1 (Part 2) Confirming Establishment of Interface W/Either NSSS Vendor or Vendors of Each Component in Reactor Trip Sys ML20235J3841989-02-13013 February 1989 Safety Evaluation Concluding That Continued Operation of Facility Not Affected by Steam Generator Tube Failures Experienced by Advanced gas-cooled Reactors ML20195D3911988-10-27027 October 1988 Safety Evaluation Supporting Corrective Actions of LER 86-017 ML20205G0021988-10-24024 October 1988 Safety Evaluation Supporting Amend 65 to License DPR-34 ML20154J8021988-09-15015 September 1988 Safety Evaluation Supporting Amend 64 to License DPR-34 ML20154J4621988-09-15015 September 1988 Safety Evaluation Supporting Amend 63 to License DPR-34 ML20207F0571988-08-10010 August 1988 Safety Evaluation Supporting Util 870206 Submittal Re Safe Shutdowns During Postulated Accident Conditions ML20207F0431988-08-0505 August 1988 Safety Evaluation Supporting Amend 61 to License DPR-34 ML20207F2411988-08-0505 August 1988 Safety Evaluation Supporting Amend 62 to License DPR-34 ML20151M1601988-07-21021 July 1988 Safety Evaluating Supporting Requirements for Redundancy in Responding to Rapid Depressurization Accident ML20151A9961988-06-20020 June 1988 Safety Evaluation Supporting Amend 60 to License DPR-34 ML20195K0651988-06-15015 June 1988 SER Concurring W/Util Proposed Corrective Actions in Engineering Rept Entitled, Rept of Helium Circulator S/N 2101 Damage & Inlet Piping S/N 2001 Repair & Mod Activities ML20195F9661988-06-15015 June 1988 Safety Evaluation Re Destructive Exam Rept for Fuel Test Assembly-2.Fuel Represented by Fuel Test Assembly-2 Predicted to Be Safe for Operation in Facility for 1,800 EFPDs ML20154F8891988-05-10010 May 1988 Safety Evaluation Re Proposed Safe Shutdown Sys & Exemption Requests Concerning 10CFR50,App R.Licensee Request for Exemptions in Listed Areas Should Be Granted.Concept for Providing post-fire Shutdown Acceptable ML20148S6031988-04-0707 April 1988 Safety Evaluation Supporting Amend 59 to License DPR-34 ML20151B6651988-04-0101 April 1988 Supplemental Safety Evaluation Supporting Util Compliance w/10CFR50.App R Re Safe Shutdown DHR Capacity ML20150C4541988-03-10010 March 1988 Safety Evaluation Concluding That Seismic Analysis Methods for Bldg 10 & Walkover Structure Conservative.Gaps Provided Adequate to Accommodate Relative Motions Which Occur Between Subj Structures & Walkover Structure & Turbine Bldg ML20147C8181988-02-25025 February 1988 Safety Evaluation Supporting Changes to Interim Tech Specs 3/4.1.7, Reactivity Change W/Temp NUREG-1220, Safety Evaluation Accepting Plant Special Senior Licensed Fuel Handler Initial & Requalification Operator Training Program,Per NUREG-1220, Training Review Criteria & Procedures1988-01-13013 January 1988 Safety Evaluation Accepting Plant Special Senior Licensed Fuel Handler Initial & Requalification Operator Training Program,Per NUREG-1220, Training Review Criteria & Procedures ML20237D7631987-12-18018 December 1987 Safety Evaluation Updating 861118 Fire Protection Sys Safety Evaluation.Util Alternate Fire Protection Configuration Acceptable ML20149E1621987-12-18018 December 1987 Marked-up Safety Evaluation Re Proposed Safe Shutdown Sys & Exemption Requests Concerning 10CFR50,App R ML20236U6961987-11-23023 November 1987 Safety Evaluation Supporting Amend 57 to License DPR-34. Addendum to Review of Proposed Tech Spec Change:Core Inlet Valves/Min Helium Flow & Max Core Region Temp Rise,Limiting Condition for Operation..., Technical Evaluation Rept Encl ML20236U5761987-11-20020 November 1987 Safety Evaluation Re Helium Circulator S/N C-2101 Damage. Util Corrective Action Program Initiated ML20236R3001987-11-13013 November 1987 Safety Evaluation Supporting Util Responses to Generic Ltr 83-28,Item 2.2.1 Re Equipment Classification Programs for All safety-related Components ML20238C7621987-09-0202 September 1987 Safety Evaluation Concurring W/Util 870702 & 27 Ltrs & 870818 Telcon Re Elimination or Reduction of Maint Requirements on Certain Fire Seals ML20235N6491987-07-13013 July 1987 Safety Evaluation Supporting Amend 56 to License DPR-34 ML20235F5281987-07-0202 July 1987 Safety Evaluation Re Safe Shutdown of Steam Generator Matls. Under Severe Transient Conditions,Fuel Temp Can Be Maintained Under Accepted Temp Limits & Plant Can Be Safely Shutdown ML20235F5151987-07-0202 July 1987 Safety Evaluation Re Safe Emergency Shutdown of Reactor Sys. Operation at 82% Acceptable ML20235F5441987-07-0202 July 1987 Safety Evaluation Re Effect of Firewater Cooldown on Steam Generator Structural Integrity.All Tests Acceptable ML20235E5281987-06-29029 June 1987 Safety Evaluation Supporting Amend 55 to License DPR-34 ML20216G9511987-06-24024 June 1987 Revised Safety Evaluation Re Steam Line Rupture Detection & Isolation Sys (Slrdis).Slrdis Meets Requirements of 10CFR50, App A,Gdc 20 & GDC 4 ML20216G9911987-06-24024 June 1987 Supplemental Safety Evaluation Supporting Application for Amend to License DPR-34 Re Tech Specs for Steam Line Rupture Detection & Isolation Sys ML20215J5401987-06-22022 June 1987 Draft Safety Evaluation Re Safe Emergency Shutdowns.Facility Operation at 82% Power Acceptable ML20216J1921987-06-17017 June 1987 Safety Evaluation Re Mods to Reduce Moisture Ingress Into Reactor Vessel.Periodic Insps & Preventive Maint Should Be Performed on Pertinent Components.Operational Performance Should Be Continuously Upgraded ML20214M4681987-05-20020 May 1987 Safety Evaluation Supporting Amend 54 to License DPR-34 ML20215J8271987-05-0505 May 1987 Safety Evaluation Supporting Amend 53 to License DPR-34 ML20209D7561987-04-22022 April 1987 Safety Evaluation Supporting Util 870211 Submittal Re Performance Enhancement Program,Finding 4-10 ML20206J9331987-04-0606 April 1987 Safety Evaluation Supporting Amend 52 to License DPR-34 ML20205S1141987-03-31031 March 1987 Safety Evaluation Accepting Util 831104 Response to Generic Ltr 83-28,Item 4.5.2, Reactor Trip Sys Reliability On-Line Testing. Facility Designed to Permit on-line Functional Testing,Including Testing of Reactor Trip Contactors 1997-05-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
[Table view] |
Text
- o
' ~g UNITED STATES 8 n NUCLEAR REGULATORY COMMISSION
. y : p WASHINGTON, D. C. 20655
%,*..*/
SAFETY EVALUATION REPORT BY THE OFFICE OF NUCLEAR REACTOR REGULATION ON THE HELIUM CIRCUL/.0R S/N C-2101 FAILURE AND REC 0VERY FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO LICENSE NO. DPR-34: DOCKET N0. 50-267 l INTRODUCTION A meeting was held with the Public Service Company of Colorado (the licensee) l on March 4, 1988, at the Fort St. Vrain Nuclear Generating Station to review the engineering report, "Report of Helium Circulator S/N C-2101 Damage and Inlet Piping S/N 2001 Repair and Modification Activities." The purpose of the meeting was to discuss the design changes and controls to be implemented at Fort St. Vrain as a result of the analyses performed on ccmpenents from the failed circulator and associated inlet piping assembly.
EVALUATIO_N:
Metellurgical analyses on 24 different components from the helium circulator j showed that component failure and/or damage occurred as a result of caustic stress corrosion cracking. The primary source fcr caustic cortamination was the steam used for the turbine drive. A review of Fort St. Vrain cperation record indicated that major steam contamination occurred during the period from December 1983, until April 1985. Significant amounts of sodium hydroxide and sodium phosphate were injected into the auxiliary bciler steam in order to reduce corrosion in the system. The controlling procedure for the chemistry of the condensate /feedwater during plant shutdown specifies a limit of 1000 ppb sodium where the demireralizers are bypassed and 20 ppb where they are in service.
The procedure is being revised at present so that the permissible sodium limit for the condensate /feedwater during power operation is 3 ppb at the outlet to the dcmineralizers. The revised procedure will require auxiliary boiler system clean-up in the event the sodium content of the auxiliary boiler steam exceeds 3 ppb.
The metallurgical evaluation showed that failure occurred in different materiais in several components. Pitting and stress corrosion cracking (SSC) was observed in Type 410 stainless steel labyrinth seal mounting bolts, steam turbine stator cap screws and socket head cap screws and in the plain carbon steel spring plunger. Stress corrosion cracking was observed in the Type A-286 stainless steel steam duct bolts and pressure tap bolt. SCC was observed in Monel 400 lockwire, Inconel 600 expansion jcint, 5% chrome nozzie bolt assembly, and SAE 4140 nozzle support socket cap screws and the bellows support ring cap screws.
8806290335 800615 PDR ADOCK 05000267 P PDR
Pechanical darage was observed in Inconel 718 steam duct and Type 430 stainless steel labyrinth spacer and seal and insulation ccver. Slight pitting and cor-rosion was observed on Type 422 stainless steel steam turbine rotor disk and 5%
chrone special studs. Cracking due to inadequate weld was observed in plain carbon steel steam deflector plate. No damage was observed in Inconel 718 Pelton-wheel bolt and nut, Inconel 600 Pelton wheel lock washer, Inconel 600 lockwire for cap screws and Type 304 stainless steel lockwire for bolts.
The corrrron environment to all the failed materials was the steam used to drive the helium circulator. High levels of caustic carried ever into the circulater by the auxiliary boiler stear was considered to be the major cause of the corrosion and the 500. Althcugh nolybdenum disulfide was used for bolt lubrica-tion, SCC was observed en nonlubricated components, such as the expansion bellows and the fractured surface of the pressure tap bolt, the major cause of the ob-served SCC was net attributed to the degradation prcoucts of melybdenum disulfide.
A survey was corducted to determine the bolting materials for use in the helium circulator rest rcsistant to SCC in a steam or water environtent containing caustic, chlcride and/or molybderum disulfide degradatier piccuct. Thc survey indicated that no bolting mattrial was entirely irrune to caustic SCC under conditions believed to have occurred in the darage helium circulator auxiliary boiler reheat steam. Inconel X-750 in the solution heat treated, overaged conoitior, was generally favored to be the most cerrosion resistart, high strength, high temperature material for use in circulator refurbishment. The heat treat-rent reccrrended is solution anneal at 2025 25 F for I to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and overage at 1300 25'F for 20 to 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />, corresponding to EPP.! draft specification 2227 - 16322 - HC2.
The prelcad reouf rement for each fastener application in the circulater was evaluated. The objective was to mininize preload stress in order te avoia SCC but to exceed a tightening value where fastener loosening might occur. One of the most critical application was the steam ducting to bearing assembly bolts.
Inconel X-750 was not suitable for this application because of the stress re-quired to maintain secondary interspace pressurization. Type A-286 was origi-nally specified and performed satisfactorily for an estinated 60,000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br />. As
! an enhanced circulator inspection program is being implemented, including moni-toring of the secondary inrerspace pressure, the specification for these bolts was not changed.
All lockwashers and lockwires exposed to the turbine drive steam are being changed to Inconel 600. Inconel 600 appeared to be superior to plain carbon and icw alloy steel and Type 300 and Type 400 series stainless steel. The steam l inlet piping mounting stud material is being changed from SA-193-B5 to SA-193-27 due te material availability. There are sixteen studs holding the piping to the steam scroll and preload stresses are less than 60% of yield strength. The turbine /Pelton wheel tie bolt and nut (Incorel 718) are not undergoing specifi-cation change. The preload is less than 60% yield strength and SCC was rot cbserved during the examination of the original material.
l k
s l The method for preloading each fastener was evaluated. The steam ducting to 1 bearing assembly bolts required preload extension of 0.008-in. to maintain the I pressure boundary seal. In addition to specifying parallel end-faces for these I
Type A286 bolts, an ultrasonic methed is being investigated to measure the elongation during component assembly. The turbinc/Pelton wheel tie belts will be ;
preloaded using a caliper to measure elongation during component assembly. The remainder of the fasteners will be preloaded using a precision torque wrench (Refer to Table 3 of subject report).
Fechanical means is being used to remove residual molybdenum disulfide lubri-cant frcm the fastener holes in the refurbished helium circulator. A revievi of potential lubricant indicated that Dow Corning Mclykote 505 was the preferred substitutt. Although a chemical analysis is planned to ensure environmental ccmpatibility, should constituents be found which may cause SCC, Holykote 505 will not be used. Never-Seez Pure Nickel Special and Felpro Grade N 1000 are being investigated concurrently fcr potential usage.
Technical Specification SR 5.2.18 is to be upgraded to include an enhanced inservice inspection surveillance requirement for fastener replacement and component inspection within a time frame of 40,000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> helium circulator operation. The purpose of the prcgram is to insure replacement of failed faster.ers and the spring plunger in the steam turbine /Pelten wheel area and to perfern a visual inspection of the components removed for fastener replacement.
The fastener replacement and component inspecticr. will be repeated within a time frame of 40,000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> operation. In addition, a second circulatcr will be disassembled within a ten-year period in conformance to the present Technical Specifications.
A comprehensive nenitcring program has been implemented to enhance circulatcr performance and to assist in the early detection of circulator failurt.
Circulator shaft wobble is at present being monitored on an interim basis. In an effort to increase monitoring capabilities, the comprehensive program should provide continuous wobble monitoring, alam, data acquisition and storage, trending and diagnostic capabilities.
C0hCLUSION The metallurgical analysis performed on the components frcm the failed helium circulator C-2101 indicated that caustic stress corrosion crackina was the pri-mary cause for compcnent failure. Significant levels of caustic (sodium hyroxide and trisodium phosphate) were injected into the feedwater to the auxiliary boiler steam to cure a corrosion problem during the period from December 1983, to April 1985. Component failure occurred in several different materials, some of which are not normally susceptible to SCC.
SCC was identified in the following circulator components: Type 410 stainless steel bolts, Type A286 stainless steel bolts, carbon steel spring 5. lunger, Monel 400 lockwires, and Inconel 600 bellows.
s 4 The staff cor. curs with the actions being taken by the licensee in the refurbish-ment of helium circulator C-2101 and to minimize the potential for the recurrence of SCC at the Fort St. Vrain Nuclear Generating Station. The fastener and lock-ing rechanism are being char.ged to Inconel X-750 and Inconel 600, respectively.
The Inconel X-750 fasteners are specified in the solution annealed and overaged condition. In certain hichly stressed applications, where significant preload in required to provide adecuate pressure capability and Inconel X-750 is not a suitable replacement, the original Type A-286 material is specified. An enhanced inservice inspecticn and monitoring crogram based on 40,000 hour0 days <br />0 hours <br />0 weeks <br />0 months <br /> circulator operation is being implemented. In eddition, water chemistry procedures have been instituted to reduce the sodium content of reheat steam used to drive the circulators. The staff concurs with these actions and believes that the new procedures will ensure the integrity of circulator ccaponents and reduce the poter.tial for the occurrence of stress corrosion cracking.
Dated: June 15,1988 Principal Contributor: F. Litton 1
1 1
l l
l l
I r