ML20133C113

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Insp Rept 50-482/96-21 on 961007-11 & 21-25.Violations Noted.Major Areas Inspected:Effectiveness of Sys & Design Engineering Organizations,Performance of Safety & Operability Evaluations & self-assessment Activities
ML20133C113
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 12/31/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20133C088 List:
References
50-482-96-21, NUDOCS 9701070037
Download: ML20133C113 (55)


See also: IR 05000482/1996021

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ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.: 50-48.2

License No.: NPF-42

Report No.: 50-482/96-21

Licensee: Wolf Creek Nuclear Operating Corporation

Facility: Wolf Creek Generating Station

Location: 1550 Oxen Lane, NE

Burlington, Kansas

Dates: October 7-11 and 21-25,1996

Team Leader: J. Tedrow, Senior Resident inspector

Inspectors: R. Azua, Project Engineer

P. Campbell, Mechanical Engineer

M. Fallin, Consultant, Scientech, Inc.

P. Goldberg, Reactor inspector

F. Ringwald, Senior Resident inspector

J. Stone, Project Manager

Approved By: C. VanDenburgh, Chief, Engineering Branch

Division of Reactor Safety

Attachment: Supplemental Information

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9701070037 961231

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TABLE OF CONTENTS ,

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EXEC UTIVE S U M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv I

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R e p o rt D e t a il s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .. . . . . . . . . . . . . . . . . . . . 1 j

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111. En g i n e e ri n g . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 l

El- Conduct of Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

E1.1 G eneral Comme nts . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 i

E1.2 Permanent Plant Modification Review . . . . . . . . . . . . . . . . . . . . . 1

E1.3 Temporary Plant Modification Review . . . . . . . . . . . . . . . . . . . . . 4 {

E1.4 Review of Engineering Calculations . . . . . . . . . . . . . . . . . . . . . . 5

E1.5 Review of Performance Improvement Requests . . . . . . . . . . . . . . 6

E1.6 Work Pac k age Review . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

E2 Engineering Support of Facilities and Equipment .................. 7

E2.1 General Com ments . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

E2.2 Review of Facility and Equipment Conformance to the Final

Safety Analysis Report . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

E2.3 10 CFR 50.59 lmplementation . . . . . . . . . . . . . . . . . . . . . . . . . 10

E2.4 Unsupported Operability Determination . . . . . . . . . . . . . . . . . . 19  ;

E2.5 System Walkdowns (37550) . . . . . . . . . . . . . . . . . . . . . . . . . . 20 l

E2.6 Engineering Work Backlog . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

E2.7 Surveillance Te sting . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

E2.8 Industry Event Assessment and Lessons Learned ........... 27

E3 Engineering Procedures and Documentation .................... 28

E3.1 Review of Design Basis Documents .................... 28

E5 Engineering Staff Training and Qualification .................... 29

E5.1 System Engineering Staff Training and Qualification . . . . . . . . . . 29

E6 Engineering Organization and Administration . . . . . . . . . . . . . . . . . . . . 30

E6.1 System Engine ering . . .. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30

E6.2 Desig n Enginee ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32

E7 Quality Assurance in Engineering Activities . . . . . . . . . . . . . . . . . . . . . 33

E8 Miscellaneous Engineering Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33

E8.1 (Closed) Inspection Followup Item 50-482/9504-03: Use of

gear operator stop nut for actuator braking . . . . . . . . . . . . . . . . 33

E8.2 (Closed) Licensee Event Report 50-482/96001: Loss of

circulating water due to icing on traveling screens . . . . . . . . . . . 34

E8.3 (Closed) Licensec Event Report 50-482/96002: Loss of

essential service water train due to !cing on trash racks . . . . . . . 34

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V. M a n a g e m e nt M e e tin g s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34

X1 Exit M eeting Sum m a ry . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34

ATTACHMENT: Supplemental Information

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EXECUTIVE SUMMARY

Wolf Creek Generating Station

NRC Inspection Report 50-482/96-21

This team inspection evaluated the effectiveness of the Wolf Creek system and design  !

engineering organizations to respond to routine and reactive site activities which included I

the identification and resolution of technical problems. The performance of safety and

operability evaluations, and self-assessment activities were also included in this inspection.

Enaineerina

  • The inspection team found that modification packages included appropriate safety l

evaluations, and appropriately specified post-modification testing. In addition,  !

associated drawings and procedures were generally updated as required, and the

engineering calculations were satisfactory. However, the inspection identified a I

design control violation regarding the use of outdated calculations for capping

containment air cooler tubes. In addition, the team considered the licensee's

control of the design basis information to support the safety function of the

emergency core cooling system to properly operate following a postulated internal l

missile generation and impact to be poor (Sections E1.2 a.'d E1.4).

  • The inspection team determined that the administrative procedures that the licensee

had developed for the review and evaluation of changes in accordance with

10 CFR 50.59 were appropriate. However, the team found numerous discrepancies

between the Updated Safety Analysis Report and the actual plant conditions and

identified problems in the licensee's implementation of the 10 CFR 50.59 review

process. The team identified one apparent violation involving four examples, which

were indicative of a programmatic breakdown in the control of this activity. These

examples involved. (1) the Operation nf the essential service water self-cleaning

strainer backwash setpoint differently than described in the Updated Safety

Analysis Report, (2) the performance of inservice inspection and testing of the ,

reactor coolant pump flywheel examination differently than described in the l

Technical Specifications, (3) the performance of underground pressure testing of I

essential service water piping differently than described by the Updated Safety

Analysis Report, and (4) the performance of a safety evaluation regarding changing

the main turbine overspeed protection test frequency without performing sufficient

evaluation to conclude that an unreviewed safety question was not involved

(Sections E2.2, E.2.3, and E2.7).

  • Although the licensee's cc,rrective action for a 1993 quality assurance audit required

the performance of a 10 CFR 50.59 screening of Technical Specification

clarifications, the screening did not identify potential conflicts between the

Technical Specifications and the clarifications. Specifically, the licensee screenings i

of nine Technical Specification clarifications, which were performed to resolve the i

concerns of the quality assurance audit, failed to determine that these clarifications

involved unauthorized changes to the Technical Specification requirements. In

addition, a followup quality assurance audit failed to recognize that the conditions

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found during the original audit were not corrected. This f ailure was identified as an

apparent violation involving inadequate corrective action. The inspectors also noted

that the screenings of the Technical Specification clarifications were subsequently

reviewed by the Plant Safety Review Committee, and they also failed to identify the

issues involving Technical Specification compliance (Section E2.3).

  • Based on the number of findings in the 10 CFR 50.59 area and the recent

indications of improper screenings for Updated Safety Analysis Report change

requests, the team concluded that training did not appear to have been effective in

avoiding continuing deficiencies (Section E2.3).

  • The team identified that a shift supervisor violated the licensee's administrative

procedures regarding operability determinations when he relied, in part, on an

out-of-date calculation. Previous examples identified by NRC inspectors indicated a

declining trend in the performance of on-shift operability determinations

(Section E2.4).

  • The team found that housekeeping was generally very good and noted that the

material condition of system components had little evidence of boric acid leakage

and few deficiencies. A very good threshold for deficiency identification had been

established. However, the inspection team identified that system walkdowns by

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the safety injection system engineers did not include all plant areas where system

components were located (Section E2.5).

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  • The team considered temporary shielding controls to be weak because they did not

require an engineering review of erected temporary shielding and periodic

inspections of installed temporary shielding. Ir- Jdition, the residual heat removal

system engineer was not knowledgeable of the condition of temporary shielding,

even though it had been installed for several years (Section E2.5).

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  • The licensee managed the engineering open item workload appropriately, but the

licensee did not have a formal program to control the backlog. The inspectors were

concerned that the program had a high threshold for backlog criteria, and f ailed to

trend the impact on engineering personnel workload (Section E2.6).

  • In general, the inspection team found that surveillance tests for the systems

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selected had been accomplished in accordance with Technical Specification

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requirements and were performed at the correct periodicity. However, the team

identified one violation associated with an inadequate procedure to verify {

emergency core cooling throttle valve mechanical position stops (Section E2.7). '

  • Uncontrolled and out-of-date design basis notebooks hindered the licensee's control

of design basis information. The licensee's control of design basis information was

found to be weak, in that, it did not provide a central location for the design basis

information. In general, licensee personnel had difficulty retrieving some design

basis information (Section E3.1).

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Although system engineering knowledge was excellent, it appeared to be the result

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of the personalinitiative taken by system engineers and their immediate supervisors, '

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and not due to any specific management guidance or administrative requirement.

j Training guidance was found to be very general and did not provide a minimum

standard for system engineer training or knowledge. Overall, licensee management

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communication of system engineering expectations has improved; however, the

weaknesses identified in the previous NRC engineering inspection in May 1995, had

not been corrected (Sections E5.1 and E6.1).

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Report Details

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E1- Conduct of Engineering

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E1.1 General Comments (37550)

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Using Inspection Procedure 37550, the team reviewed three safety-related systems

, to verify the licensee's ability to maintain these systems in an operable status. The

l three systems reviewed were: (1) essential service water, (2) residual decay heat

removal, and (3) safety injection. The team reviewed the adequacy of the
licensee's plant modification processes (permanent and temporary), engineering

! calculations, performance improvement requests, and documentation of work

performed on system components.

E1.2 Permanent Plant Modification Review

a. Inspection Scooe

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i The team reviewed several safety-related plant modification records listed in the

attachment to verify conformance with applicable installation and testing

i requirements as prescribed by procedures. Specific attributes reviewed and/or

i verified by the team included: (1) 10 CFR 50.59 safety evaluations, (2) post-

i modification testing requirements, (3) safety-related drawing updates, (4) Updated

j Safety Analysis Report updates, (5) training requirements, and (6) field installation.

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b. Observations and Findinos

in general, the team found the modification packages reviewed included appropriate

safety evaluations. The specified post-modification testing in the modification j

packages was appropriate and associated drawings and procedures were genera!!y )

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updated as required.

Outdated Calculations Used for Cabbino Containment Air Cooler Tubes

The essential service water system supplies the containment air coolers under

accident conditions. The system contains four coolers total, with two coolers for

each of two safety-related trains of essential service water. Each cooler has

12 coils with 32 circuits of 6 multiple passes, totaling 2304 tubes per cooler.

' The team reviewed Configuration Change Package CCP-07111, Revision 0, which

was initiated on October 17,1996, to address a leaking tube which had developed

in one of the 12 cooler coils in Containment Air Cooler SGN-01C, one of the two in

the A train of essential service water. The package was issued to assess the effect l

of plugging (or capping) the tube and continuing to use the cooler. A 7-day action

statement was entered on October 17,1996, and an engineering review was

initiated. The assessment for this change concluded that up to 64 tubes could be

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plugged based on Calculations SA-90-030, CWR-02424-90, and GN-MW-005. The

team noted that these calculations used a flow rate of 2000 gpm through each .

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cooler instead of more recent calculations which were based on a flow rate of

1000 gpm through each cooler.

Change Package CCP-07111, Revision 1, was issued, and approved by the Plant  !

Safety Review Comn ntee, on October 18,1996, because cooler SGN-01C ,

continued to have leakage problems. Plans were to install a blind flange on the

supply header flange and on the return header flange to the leaking coil. The one

l affected coil was to be abandoned in place until it could be replaced. The change

l package stated that the removal of one coil bundle,32 circuits, would reduce total

flow through the containment cooler pair by a maximum of 2 percent and

referenced Calculation GN-MW-005, Revision O. The change package also stated -

that the removal of one coil bundle would reduce the heat transfer capacity

Contair..nent Coolers SGN01 A and SGN01C, by approximately 1/24, which was

previously analyzed under Calculation SA-90-030. Calculations SA-90-030, dated

April 23,1990, and GN-MW-005, dated April 25,1990, used a flow rate of

2000 gpm per cooler (4000 gpm per pair of coolers).

Change Package CCP-07111, Revision 2, was issued, and approved by the Plant

Safety Review Committee, on October 20,1996, when a second coil on cooler

SGN-01C developed a leak. The package stated that one objective was to allow up

to three cooling coils to be blanked off if needed. The package stated that the

removal of one coil bundle,32 circuits, will reduce total flow through the

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containment cooler pair by a maximum of 2 percent for a total of 6 percent with

three coils removed and again referenced Calculation GN-MW OOS, Revision O. The

change package also stated that a sensitivity study was performed to determine the

effect of degraded performance of containment coolers on the containment pressure

and temperature response fc!!owing a postulated main steam line break accident. c

The change pukege referenced Calculation SA-90-025, dated April 9,1990, which

stau ubed 2000 gpm flow through each cooler, for this sensitivity study.

Subsequent to these calculations, the licensee had identified that the essential

service water system total flow had degraded due to erosion and corrosion in the

system and was concerned that the analyzed flow rate to the containment air

coolers, along with other cooling loads, may not be assured. Calculation

SA-90-057, dated November 1990, determined the containment peak temperature

and pressure that.would resul+. if the capacity of the containment air coolers were

assumed to be only 45 percent of the original capacity due to a reduction in the

flow rate through each cooler from 2000 to 1000 gpm, or 4000 gpm per train to

2000 gpm per train. The calculation supported Technical Specification Amendment

50, issued November 4,1991, which changed the required minimum flow rate

specified in Technical Specification 4.6.2.3.b from 4000 gpm per cooler group to

2000 gpm per cooler group. Calculation SA-90-057 concluded that sufficient heat

removal capability existed with the lower flow rate.

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The licensee's most recent flow balancing of the essential service water system

was conducted in the 1994 refueling outage and set the measured flows, by

throttling valves to the desired position, as follows:

Train A: Cooler SGN01 A 1022 gpm

Cooler SGN01C 1034 gpm

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Train 8: Cooler SGN018 1150 gpm l

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Cooler SGN01D 1440 gpm

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The team determined that Calculations GN-MW-005, SA-90-025, and SA-90-30 did

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not reflect the current operation of the coolers (i.e.,1000 gpm current flow versus I'

2000 gpm flow) and predated the calculation for 1000 gpm and the subsequent

. Technical Specification change. Both Revisions 1 and 2 of Change Package

CCP-07111 included an unreviewed safety question determination concluding that

the removal of three coils from service did not constitute an unreviewed safety

question. The conclusion was based on the outdated calculations discussed above.

None of the referenced calculations based on a 2000 gpm flow rate for each cooler

3 were denoted as either out-of-date or as not reflecting the current configuration of

the equipment. However, the essential service water system engineer, who
coordinated the efforts, was aware that the flow rate had been reduced to j

approximately 1000 gpm per cooler subsequent to the Technical Specification l

amendment.

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Performance Improvement Request PIR-962669 was initiated on October 20,1996,

based on questions from the Plant Safety Review Committee on the 10 CFR 50.59

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safety determination associated with Change Package CCP-07111, Revision 2. In

this improvement request, the difference in the margins between the capacity of the

coole:3 with 1000 gpm versus 2000 gpm was explained, and the impact of

blocking three coils was addressed. The improvement request concluded that the

containment peak pressure would not be exceeded based on Calculation SA-90-057

results. As of October 25,1996, Change Package CCP-07111, Revision 2, had not

been revised to reference the design information that reflected current operation of

the coolers with a flow rate of 1000 gpm each (or 2000 gpm flow rate per a group

of two coolers). However, the team considered the information provided in the

improvement requests addressed the current operability conclusion of the cooiers

with the blocked coils (2 of 12 in the C cooler).

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10 CFR 50, Appendix B, Criterion 111, requires, in part, that rneasures be established l

to assure that regulatory requirements and the design basis are correctly translated

into specifications, drawings, procedures, and instructions. These measures shall

include provisions to assure that appropriate quality standards are specified and

included in design documents. The suitability of continued use of Containment Air

Cooler SGN-01C with 2 of 12 coils blocked from essential service water flow,

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assessed in Change Package CCP-07111, was determined based on calculations

that did not reflect the current operating configuration of the equipment (i.e., the

reduction in flow requirements from 4000 gpm per cooler group to 2000 gpm per

cooler group), which is considered to be a violation of 10 CFR 50, Appendix B,

Criterion lli (50-482/96021-01).

Licensee management stated that they considered references to outdated

calculations and information to be acceptable as long as current data was utilized in

present calculations. The team recognized that the licensee could have used the

calculations based on 2000 gpm flow per cooler as a comparison analysis for

1000 gpm flow per cooler if the engineering analysis had stated such,

c. Conclusions

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In general, the team found the modification packages reviewed included appropriate

safety evaluations. The specified post-modification testing in the modification

packages was appropriate and associated drawings and procedures were generally ,

updated as required. The team identified one violation regarding the use of  !

outdated calculations for capping containment air cooler tubes. '

E1.3 Temocrarv Plant Modification Review

a. Inspection Scope

The team reviewed a number of the licensee's active safety-related temporary

modifications listed in the Attachment. This effort was performed to verify that

these modifications were in conformance with plant procedures. In addition,  ;

nonsafety-related temporary modifications were also reviewed to determine if they

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were appropriately categorized, and if 10 CFR 50.59 evaluations were appropriately

performed,

b. Observations and Findinas

The team identified that the licensee had only 14 temporary modifications installed

in the plant. Of these modifications, five were identified as safety related. The

team reviewed these temporary modifications against the requirements of

Administrative Procedure AP 211-001," Temporary Modifications," Reviainn 1, and

did not note any discrepancies. Affected procedures and drawings were also

reviewed to determine if appropriate changes were annotated. No problems were

noted.

The licensee had assigned an engineering supervisor to monitor temporary  ;

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modifications in the plant. The licensee maintained a computerized log of these

modifications, with assigned durations. The team interviewed the engineering

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supervisor and found him to be cognizant of the temporary modifications installed in

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the plant. The team noted that this effort was designed to identify those temporary

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plant modifications that could be easily removed or corrected, and to make sure that

long term corrective actions were applied to the remaining temporary modifications

in a reasonable time,

c. Conclusions

The licensee efforts in reducing the number of temporary modifications in the plant

have been very successful.

E1.4 Review of Enaineerina Calculations

( a. Insoection Scope

The team reviewed the adequacy of several design engineering calculations listed in

the Attachment associated with the three subject systems to determine whether the

calculation assumptions were technically reasonable Lnd properly supported.

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b. Observations and Findinas

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The team found that the licensee's calculations were satisfactory. The calculations

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revbwed provided sufficient information and assumptions to reach the conclusion

stated. ".; *aam found some minor mistakes in the calculations regarding the

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correct atmospheric pressure for the elevation of the plant, and conversion of pump

horsepower to heat transferred to the coolant system, which did not adversely

affect the calculation's conclusion. Licensee personnel were informed of these

mistakes for correction.

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Inadeauate Suocort of Desian Basis

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The team reviewed Calculation IMS-01, " Missiles," Revision 0, to verify a statement

in the Updated Safety Analysis Report, Section 6 31.1, regarding the design bases

for the emergency core cooling system. The Updated Safety Analysis Report

contained general information that stated the system was designed to withstand the

effect of generated missiles. The calculation also contained an unlisted attachment

which listed the summary of rotating equipment in safety-related areas, by room

number. This attachment utilized Resolutions (1) and (2) which stated that room

coolers and pumps were not considered to be credible missile sources based on

"The Internal Missile Hazards Analysis Program Overview," items B.4.C and B.4.A.

The team requested these documents for review, but the licensee was unable to

locate or retrieve them during the inspection. No other documentation was

available to justify these assumptions. The team was, therefore, unable to

determine if the design of the system was adequate to support the system's safety

, function under postulated generated missiles.

On November 8,1996, the licensee obtained the missing information from the

architect-engineer. These documents were provided to the team on November 12,

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1996. The documents were hand-written and contained justification for omitting

the pumps as credible missile sources due to the thickness of the pump casings.

The licensee stated that they disagreed with the inspection team's finding, in that,

the missing information was not part of the design bases of the plant and,

therefore, need not be readily available. The team noted that the missing

, information was an element of the licensing basis for the emergency core cooling

system as described in the Updated Safety Analysis Report, Section 6.3.1.1,in

Safety Design Basis Two. Since the design basis includes information identifying ,

the specific safety functions of the system and supporting analysis for reference l

bounds for the system design, the team considered the plant design basis to be

inadequately supported without this documentation. Due to the difficulty the

licensee experienced with retrieving this information, the team considered the

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licensee's control of this design information to be poor.

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c. Conclusions

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in general, the calculations were found to be satisfactory. The control of the design I

basis information to support the safety function of the emergency core cooling

system to properly operate following a postulated internal missile generation and

impact was considered to be poor.

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E1.5 Review of Performance Imorovement Reauests

a. Inspection Scope

l The licensee issued performance improvement requests as a means to identify

problems with components and systerns and to place these problems in their

corrective action system for resolution. The team reviewed performance

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improvement requests listed in the Attachment associated with the three subject

systems to determine the adequacy of the resolution, whether the systems'

operability was properly determined, and that the proposed corrective actions were

adequate to preclude recurrence.

b. Observations and Findinas

1 The team found that the performance improvement requests had resolutions with

. proper engineering justification and that the proposed corrective actions were

adequate to preclude recurrence.

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a. inspection Scope

The team reviewed work packages listed in the Attachment associated with the

three subject systems, and work history printouts, to determine if repetitive

problems existed and to determine the present material condition of the system.

This information was compared with the results of the system walkdowns.

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b. Observations and Findinas

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The team found that the work packages were performed in accordance with their

l instructions and the engineering staff was knowledgeable of the work performed.

No recurrent problems were noted. The team's walkdown results indicated that the

[ licensee was maintainm9 the systems in good condition and a very low threshold

for deficiency identification had been established.

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E2 Engineering Support of Facilities and Equipment

E2.1 General Comments (37550)

To ascertain engineering support of plant activities, the team walked down the

selected systems with the system engineer, reviewed the system description

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provided in the Updated Safety Analysis Report, compared the Updated Safety

Analysis Report description with design basis information, evaluated the engineering

work backlog, compared surveillance testing records and test . >cedures with

design basis information and Technical Specifications, and re- swed the engineering

disposition of selected industry events for lessons learned.

E2.2 Review of Facility and Ecuioment Conformance to the Final Safety Analvsis Reoort

Descriotion

a. Insoection Scoce

A recent discovery of a licensee operating its facility in a manner contrary to the l

Safety Analysis Report description highlighted the need for a special focused review

that compares plant practices, procedures and/or parameters to the Safety Analysis

Report description. While performing the inspections discussed in this inspection

report, the inspectors reviewed the applicable sections of the Final Safety Analysis

Report that related to the selected inspection areas,

b. Observations and Findinas

The team found that the Final Safety Analysis Report was generally consistent with

the actual plant configuration. The team noted several discrepancies in the

descriptions as noted below:

Imorocer Chanae to Essential Service Water Self-Cleanina Strainer Backwash

Setooint

The team reviewed Section 9.2.1, " Station Service Water System," and

Table 9.2-5, " Essential Service Water System Component Data," of the Wolf Creek

Updated Safety Analysis Report. The team noted that Table 9.2-5 for the essential

service water system self-cleaning strainers listed a strainer capacity of 15,000 gpm

with a maximum differential pressure of 3.0 psi. The team asked the licensee to

verify the capacity at this differential pressure. The licensee stated that the signal i

to start the self-cleaning strainers was 5.0 * 0.5 psi not the 3.0 psi stated in

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Table 9.2-5. During the first week of the inspection, the licensee was not able to

determine the reason for the difference in the maximum strainer differential

pressure.

i

During the inspection, the licensee contacted the strainer vendor to determine if a

maximum strainer differential pressure of 5.5 psi was acceptable. The licensee

stated that setting the maximum differential pressure at 6.0 psi would not cause

any physical damage to the strainer. However, it might detract from the strainers

ability to self clean upon initiation of the backwash cycle. The licensee stated that

the vendor indicated that a pressure drop of 1.0 psi, clean, across the strainer was

4

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based on laboratory tests and did not account for the pressure drop across the inlet

and outlet connections, or specific piping connections, in addition, the vendor i

recommended a strainer backwash initiation at a pressure drop 2.0 psi greater than

the clean pressure drop.

The team reviewed vendor data on the strainers. One chart plotted pressure loss l

versus flow. The team noted that for a clean strainer there was a pressure drop of

1.0 psi at a flow of 15,000 gpm. The team reviewed another plot of pressure loss

versus percent of strainer clogged. The team noted that, with a differential

pressure of 5.0 psi, the plot indicated that the strainer surface was 95 percent

clogged in additbn, the team reviewed the licensee's data on strainer differential

pressure and system flow. The team found that, since 1994, the normal differential  ;

pressure across the strainers has been approximately 3.0 to 3.5 psi and the system

flow was approximately 15,000 gpm. In addition, the team reviewed startup test

data from 1984 which listed a strainer differential pressure less than 1 psi at a flow

'

over 15000 psi. The licensee could not explain what caused the pressure to

increase from less than 1.0 psi in 1984 to more than 3.0 psi in 1994.  ;

The team considered the Updated Safety Analysis Report setpoint discrepancy to be

important since a change in strainer differential pressure could directly affect system

flow rates. Based on reviewing the licensee's recent test data, which showed

system flow greater than the design flow rate of 15,000 gpm, the team concluded

that there were no operability concerns on account of the discrepancies.

10 CFR 50.59(a)(1) allows the holder of a license to make changes to the facility I

and procedures as described in the final safety analysis report without prior

Commission approval unless the proposed change involves a change in the

Technical Specifications or an unreviewed safety question.

The team reviewed setpoint Change Request EF-84-01, dated March 13,1984.

This document requested a setpoint change for the self cleaning strainer pressure l

. instruments to change the setpoint to 5.5 psid. The cover sheet was annotated

with an "N/A" following questions concerning if any Updated Safety Analysis

Report section or limit was affected by the change. The modification had a

10 CFR 50.59 screening, but no safety analysis. The team found that the screening

stated that the change described in the primary document did not involve a change

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to the Updated Safety Analysis Report. However, the strainer table was a part of

the Updated Safety Analysis Report and included the 3.0 psi maximum differential j

pressure for a dirty strainer. The team considered the licensee's failure to perform a

'

safety evaluation to be the first example of an apparent violation of 10 CFR 50.59

(50-482/96021-02). l

Emeraency Core Coolina System Water Hammer

i

The team noted that Updated Safety Analysis Report, Section 6.3.2.2, stated that

all emergency core cooling system discharge piping is water solid during plant

operation and, therefore, water hammer in the injection line is precluded. The team  ;

questioned this statement since solid pipe operation alone will not always preclude l

waterhammer events depending upon the piping configuration and flow  ;

characteristics. The licensee responded by acknowledging that this statement was I

not appropriate. The licensee initiated Plant Improvement Request 96-2675 and

stated that the Updated Safety Analysis Report would be revised to clarify the l

water hammer statement. The licensee provided applicable sections of the safety

evaluation report which discussed now the residual heat removal system design

features and Mper venting and filling procedures prevented water hammer. The

team concluded that no operability concern existed.

Containment Pressure Used in Pumo Net Positive Suction Head Calculations

in Section 6.3.2.2 of the Updated Safety Analysis Report discussion about i

net-positive suction head, the statement is made that the calculation of available

net-positive suction head in the recirculation mode assumes that the vapor pressure j

of the liquid in the sump is equal to the containment ambient pressure. This is the

case only when containment ambient pressure is atmospheric in accordance with

Regulatory Guide 1.1, " Net Positive Suction Head for Emergency Core Cooling and

Containment Heat Removal System Pumps." The actual net-positive suction head

calculations use atmospheric ambient conditions. The team considered the Updated

Safety Analysis Report statement to be misleading. Licensee personnel

acknowledged the inspector's comment and initiated an Updated Safety Aaalysis l

Report change to clarify the wording.

Incorrect Capacity of Essential Service Water Pomo Prelube Storaae Tank

The team reviewed Section 9.2.1.2.2.2 0f the Updated Safety Analysis Report,

which stated that the essential service water prelube storage tank size was based

on supplying a minimum of 6 gpm water for 5 minutes to the essential service

water pump bearings without any makeup from the essential service water line.

The team asked the licensee how they verify this statement.

The licensee verified that the tank would hold enough water to supply 30 gallons of

water without any mekeup. However, the licensee determined that the maximum

flow to the bearings would only be 1.0 to 1.5 gpm due to the size of the piping

from the prelube tank to the pump bearings. The licensee stated that there was no

operability concern since the pump vendor had installed bronze bearings in the

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pump because of the possibility for pump start without prelubrication. Therefore,

the tank was not needed for pump operability requirements. In addition, the team

determined that the licensee did not knnw the necessary flow rate of water to

properly lubricate the bearings as recommended by the pump vendor to reduce

wear. The team noted that Table 9.2-5 listed the capacity of the prelube tank to be

43 gpm. The team determined that 43 gallons was the volume of the tank with a

usable volume of 35 gallons. The licensee prepared Plant improvement Request

96-2617, dated October 16,1996, to resolve these discrepancies and correct the

Updated Safety Analysis Report.

c. Conclusions

Although there were numerous discrepancies between the Updated Safety Analysis

Report and the actual plant conditions, the inspection team determined that the <

discrepancies did not present an operability concern. The inspection team identified

one apparent violation regarding operation of the essential service water self-

cleaning strainer backwash setpoint differently than described in the Updated Safety

Analysis Report. In addition, the team noted that the licensee had difficulty in

retrieving design information.

E2.3 10 CFR 60.59 Imolementation (37001)

a. Insoection Scooe

The team reviewed the licensee's program guidance, training program information, a

sample of 50.59 screenings and associated unreviewed safety question

determinations, a sample of 50.59 screenings that did not require an unreviewed

safety question determination, and interviewed a number of individuals who perform

( 50.59 screenings and prepare unreviewed safety question determinations. In

addition, a sample of Updated Safety Analysis Report changes were reviewed,

b. Observations and Findinas

The licensee's safety evaluation process for changes to the facility is controlled by

Procedure AP 26A-003," Screening and Evaluating Changes, Tests, and

Experiments," Revision 1. This procedure was recently revised in February 1996.

The procedure delineated the licensee's methods, training requirements, and

responsibilities to determine and document whether facility changes can be made

without prior NRC approval. The process used to determine if an unreviewed safety

question exists is a two step process. l

  • The first step was a screening process that made a determination as to

i whether or not the proposed change was a change to the facility as

j described in the Technical Specifications, Updated Safety Analysis Report,

nonradioactive liquid or gaseous discharges, nonradiological solid waste,

thermal discharges, security plan, safeguards contingency plan, security

. guard training plan, radiological emergency plan, an NRC or INPO

,

commitment, and physical changes within the site boundaries. If the answer

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to all questions was negative, then a change to the Updated Safety Analysis

Report was deemed not to exist and the change could proceed without an

unreviewed safety question determination prepared. An affirmative answer

to any of the questions required further evaluation. Or'/ if the screening

determined that it was a change to the Updated Safety Analysis Report, was

an unreviewed safety question determination required.

The second step involved documentation of an unreviewed safety question

determination on Form APF 26A-003-03,"10 CFR 50.59 Unreviewed Safety

Question Determination," by answering a series of questions and recording

the basis for each answer. If the answer to all questions was "no," then an

unreviewed safety question did not exist and the change could be

implemented without prior approval of the NRC. If the answer to any

question was "yes," then NRC approval was required prior to implementing

the proposed change. Procedure AP 26B-003," Revisions to the Updated

Safety Analysis Report," provided instructions for issuing changes to the

Updated Safety Analysis Report.

The team determined that these procedures provided appropriate guidance for the

development and approval of reviews and approvals under 10 CFR 50.59.

The licensee developed a training program for personnel that performed 50.59

screenings and prepared unreviewed safety question determinatinns. The team's

review of the training program determined that the program covered all the essential j

aspects of the 50.59 screenings and unreviewed safety question determinations. In  !

addition, there was a requirement that by the end of calendar year 1996, personnel j

performing 50.59 screenings and preparing unreviewed safety question i

determinations must have taken the training. The need for requalification training

will be determined by significant changes to Procedure AP 26A-003, an increasing

trend in the number of Plant improvement Requests indicating deficiencies in I

cornpleted screenings or unreviewed safety question determinations, self- i

'

assessment results and quality assurance audit results.

The team evaluated the implementation of the 50.59 program by reviewing a

sample of completed 50.59 screenings and determinations as contained in the Wolf

Creek Generating Station Annual Safety Evaluation Report for 1995, a listing of the

changes approved since January 1,1996, and interviewing a number of personnel

involved in the preparation of 50.59 screenings and determinations. Several

deficiencies were identified as delineated below:

Inadeauate Justification of Chanae to Turbine Overspeed Protection

Unreviewed Safety Question Determination 59 96-0067 and associated Updated

Safety Analysis Report Change Request 96-044 evaluated and changed the

surveillance frequency for the four high pressure turbine stop valve, six low

pressure turbine reheat stop valves and six low pressure reheat intercept valves

from once per seven days to once per 92 days. This change was based on NRC's

Generic Letter 93-05, "Line-Item Technical Specifications improvements to Reduce

11

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Surveillance Requirements for Testing During Power Operations." The guidance

provided in the generic letter for changing the turbine valve surveillance fraquency,

requested that licensees include a statement in their amendment request that the

proposed change is compatible with plant operating experience and a statement that

the turbine manufacturer concurred with the proposed change. However, the

inspection team noted that the unreviewed safety question determination did not

address the licensee's experience with the testing of these valves and did not

contain any information as to the acceptability, by the turbine vendor, of the

decreased surveillance frequency of the turbine valves. Based upon interview.s with

licensee personnel, the team determined that the licensee had not fully considered

these factors and that the turbine vendor had not been contacted.

10 CFR 50.59 (b)(1) requires that records of changes include a written safety I

evaluation which provides the bases for the determination that the change, test, or I

experiment does not involve an unreviewed safety question. Even though the ,

turbine test frequency change did not involve a licen:,e amendment, the licensee  !

should have been aware of the specific information the NRC deemed appropriate to

include in this unreviewed safety question determination based on the generic letter.

Therefore, the team determined that the basis included with this change did not

provide adequate information to come to the conclusion that an unreviewed safety j

question did not exist. The team considered the failure to fully evaluate that the

change did not involve an unreviewed safety question to be the second example of  ;

an apparent violation of 10 CFR 50.59 (50-482/96021-02). '

The licensee subsequently informed the team that the information needed to justify

the change did not involve an unreviewed safety question was available and the

determination would be revised to include it.

Inadeauate Screeninas of Technical Specification Clarifications

The team reviewed several proposed Updated Safety Analysis Report changes,

including three that would have incorporated Technical Specification clarifications

into the Updated Safety Analysis Report. These clarifications had been screened

and determined to neither change the Updated Safety Analysis Report nor the

Technical Specifications and had been issued for review and approval.

Change Request 96-094 was written is add existing Technical Specification

Clarification 009-85 for a Technical Specification that had been relocated to

Chapter 16 of the Updated Safety Analysis Report. The clarification allowed closing

the breaker and operation of a second centrifugal charging pump while swapping

pumps when in operating Modes 4,5, or 6. The team reviewed current Technical

Specifications 3/4.5.3 (applicable in Mode 4) and 3/4.5.4 (applicable in Modes 5

and 6) and determined that both allowed only one charging pump to be operable.

On October 2,1995, a change to Technical Specification 3/4.5.4 (Amendment 89)

was made that added a 4-hour action period to disable one pump.

The. team determined that the licensee had changed Operating Procedure

SYS BG-201, " Shifting Charging Pumps," in 1985 to incorporate the Technical

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Specification clan'.. cation. The clarification received a further screening in March

1994 as a result of a quality assurance finding. The team was informed that the

, operating procedure had been previously used, and the 4-hour action period

'

exceeded, on March 22 and 26,1996. In addition, during two occasions on

October 24,1994, while the plant was in Mode 5, both charging pumps were

operable. The team considered the initial screening done for the operating

procedure and the subsequent screening done for this clarification in 1994 to be

inadequate as they changed a Technical Specification requirement and resulted in

operation of a second charging pump while in Mode 5, contrary to Technical

Specification 3.5.4. Failure to perform the required actions of Technical

Specification 3.5.4 is considered to be an apparent violation of the Technical

Specification (50-482/96021-03).

The licensee subsequently voided this proposed change request and the Technical

Specification clarification. A revision to the operating procedure was also initiated

to prohibit this action.

Following the identification of the team's concerns about Technical Specification

clarifications, the licensee formed an internal investigatior, wam to review and

determine the adequacy of all 45 active clarifications and whether or not

compliance with Technical Specification requirements was being achieved. As a

,

result of that continuing review, the licensee identified two additional clarifications j

which were improperly screened and that resulted in Technical Specification

non-compliance as follows:

Technical Specification Clarification 004-86 allowed cold-leg accumulators to

be considered operable upon receipt of level and pressure alarms if

accumulator level and pressure was within prescribed limits. This

clarification involved a change to Technical Specification Surveillance

Requirements 4.5.1 and 4.0.3, which required the accumulators be

considered inoperable upon receipt of alarms.

The licensee determined that from September 25 to October 2,1996, the

associated level alarm was energized and the Technical Specification action

statement was not met because of the failure of one levelindication channel

on Cold Leg Accumulator B. The Technical Specification action statement

required restoration within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> or hot shutdown within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

followed by reactor coolant system depressurization below 1000 psig within

the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. The team noted, however, that the alarm function did not

affect the ability of the system to perform its safety function.

J

  • Technical Specification Clarification 005-94 allowed hot restart testing of an

emergency diesel generator to be per'ormed any time before or after the

24-hour load test, as long as the hot restart test was performed within

5 minutes of a 2-hour diesel run. This clarification involved a change to

Technical Specification 4.8.1.1.2 g,7, which specified that a hot restart test

be performed within 5 minutes following tne 24-hour test. There was a

footnote to the Technical Specification that allowed the hot restart test to be

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done following a warmup run if it failed the hot restart test following the load J

test. This clarification allowed the complete decoupling (i.e., allowing the l

hot restart test to be performed anytime after engine warmup and not  !

requiring a failure of the hot restart test following the load test) of the Joad

test and the hot restart test. This Technical Specification was changed by

the NRC with Amendment 101, issued on August 8,1996, and allows the i

decoupling of these two requirements. This amendment was implemented l

by the licensee on November 7,1990.

The licensee determined that prior to issuance of this amendment, hot restart

testing of the diesels was not performed in accordance with the Technical I

Specifications. Specifically, during Refueling Outage 7, Emergency Diesel l

Generator A was load tested on September 17,1994, and the hot restart

{

test was not performed until October 15,1994. Emergency Diesel j

Generator B was load tested on September 16,1994, and the Nt restart '

test was not performed until October 17,1994. I

!

The licensee also determined that during Refueling Outage 8, Emergency l

Diesel Generator A was load tested on February 6,1996, and the hot restart

test was not performed until March 26,1996. Emergency Diesel Generator

B was load tested on March 16,1996, and the hot restart test was not

performed until March 23,1996. Again, since the licensee's hot restart test I

method was allowed by the Technical Specifications under certain

conditions, the team considered the consequences of these violations to be

nnnor,

in addition, the team evaluated the licensee's review of all the clarifications and l

identified the following clarifications that provided guidance contrary to Technical

Specification requirements and could have resulted in non-compliance due to

inadequate screenings:

  • Technical Specification Clarification 010-85 allowed daiiy containment

closecut inspections following multiple containment entries in one day. This

clarification involved a change to Technical Specifications 3.5.3 and 4.5.2

which specify a containment visual inspection for loose debris be performed

following each containment entry.

  • Technical Specification Clarification 026-85 allowed increasing power while

the quadrant power tilt ratio exceeded a prescribed limit. This clarification

involved a change to Technical Specification 3.2.4.a.4 which prohibited

increasing power with the quadrant power tilt ratio greater than the

prescribed limit.

  • Technical Specification Clarification 033-85 allowed containment i

penetrations to be considered operable if dedicated operators were assigned

to close inoperable containment isolation valves. This clarification involved a

change to Technical Specification 3.6.1.1 which specified that all

containment penetrations be operable by automatic isolation valves.

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system to be cooled down, an activity which involves a positive reactivity

change, with one source range channel of nuclear instrumentation

inoperable. This clarification involved a change to Technical Specification 3.3.1, Table 3.3-1, Functional Unit 6.b, " Source Range Shutdown,"

Action 5, which specified that with one source range channelinoperable, all

operations involving positive reactivity changes be suspended.

Technical Specification Clarification 004-94 deleted emergency diesel

generator testing of the redundant dieselif the inoperable diesel was

rendered inoperable by a support system failure. This clarification involved a

change to Technical Specification 3.8.1.1 which specified that the redundant

emergency diesel generator be tested within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> if one emergency

diesel generator was inoperable for any reason except for preplanned

preventive maintenance, testing, or maintenance to correct a deficiency

which, if left uncorrected, would not affect the operability of the diesel

generator. This clarification extended this footnote to include inoperable

support systems on one diesel as a condition that would not require a start

test of the other diesel. This Technical Specification was changed by the

NRC with Amendment 101, issued on August 8,1996, and was

implemented by the licensee on November 7,1996.

  • Technical Specification Clarification 002-96 allows one of the two required

source range neutron flux monitors to be considered operable when in the

refueling condition when powered from a nonsafety-related power supply.

This clarification involved a change to Technical Specification 3.9.2, which

specifies that two source range neutron flux monitors to be OPERABLE in the

refueling condition (Mode 6). Although Technical Specification 3.9.2 does

not specify the power source requirement, the definition of OPERABILITY

does include a requirement for electric power, which refeis to the normal

safety-related power supply.

The licensee provided the result of an audit done of the existing clarifications by

their quality assurance group in February 1993. This audit identified the following

potential consequences that could result in the use of Technical Specification

clarifications:

  • Failure to comply with Regulatory, Technical Specification, or other

applicable requirements;

  • Poor performance ratings, concerns, or more severe actions from the fJRC

for a potentially inadequate or incorrect Technical Specification clarification

program;

e inappropriate actions being taken by operators;

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Potentially non-conservative actions which could require NRC approval prior

to implementation; and/or

  • Overly conservative actions for plant shutdown without consideration of

other risks involved. l

A-s a result of that audit, the licensee reviewed membership on the Technical

Specification clarification committee for appropriateness; reviewed guidance for

preparation of clarifications; and performed a 10 CFR 50.59 review (screenings) of

all current clarifications. In addition, the screenings of the clarifications were

reviewed and approved by the Plant Safety Review Committee. These activities

resulted in voiding eleven clarifications, revision of six clarifications, and one ,

clarification was considered for a Technical Specification amendmer>+ The l

remaining clarifications were deemed by the licensee to meet requim.ients. This

action was completed in March 1994. The quality assurance group performed a

follow up audit to evaluate the effectiveness of the corrective actions which

concluded that the corrective actions were adequate to resolve the concern. This  !

audit and review of the completed corrective actions failed to identify additional

potential conflicts between the clarifications and Technical Specifications.

10 CFR 50, Appendix B, Criterion XVI, requires in part, that measures be

established to assure that conditions adverse to quality are promptly identified and

corrected. The team determined that the licensee's corrective actions, done

following the quality assurance finding, were inadequate and failed to identify the

conflicting statements in the clarifications with the Technical Specifications. Based

upon the numerous deficiencies in this area, the team concluded that a

programmatic breakdown in the licensee's 10 CFR 50.59 screening program had i

'

occurred. This breakdown included the licensee's quality assurance group which

initially identified potential concerns with the clarifications, but did not properly

assess the adequacy of the licensee's corrective action, and the Plant Nuclear

Safety Review Committee which reviewed the clarification screenings and also

failed to note that changes to the Technical Specifications were involved. The

failure to perform adequate corrective action for the identified clarification

deficiencies is contrary to the requirements of 10 CFR 50, Appendix B,

Criterion XVI, and is considered to be an apparent violation (50-482/96021-04).

At the time of the exit meeting on November 8,1996, the licensee had reviewed

5 the clarifications and determined that occasions had occurred in which the

Technical Specifications were violated and planned to submit five licensee event

reports on these items, i

Imoroper Chanae to Reactor Coolant Pomo FivwheelInsoection Freauency

!

The team reviewed Updated Safety Analysis Report Change Request 95-003,

" Screening for Licensing Basis Changes," approved January 11,1996, regarding a

change in the examination schedule for the reactor coolant pump flywheels.

Specifically, the description of the proposed change stated that Regulatory

Guide 1.14, Revision 1, required a 10-year reactor coolant pump motor flywheel

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examination coinciding with the inservice inspection orogram interval. This change

clarified the intended examination schedule by revising Chapters 3A and 5.4.1 of

the Updated Safety Analysis Report to include an exception to the Regulatory Guide

examination schedule. The examination schedule was changed to 12 years to

accommodate the "D" reactor coolant pump flywheel which had not been inspected

per the previously established schedule. The response to Screening Question 2 on

whether the change results in a revision to the Operating License, including the

Technical Specifications, was marked "No."

Technical Specification 4.4.10, which was applicable January 9,1995, stated that

each reactor coolant pump flywheel shall be inspected in accordance with the

recommendations of Regulatory Position C.4.b of Regulatory Guide 1.14,

Revision 1, August 1975. This Technical Specification was subsequently

'

superseded by Technical Specification 6.8.5.b in License Amendment 89, issued

October 2,1995, which contained the same statement. Regulatory Guide 1.14,

" Reactor Coolant Pump Flywheel Integrity," Revision 1,1975, Paragraph C.4.b.(2)

states that a surface examination of all exposed surfaces and complete ultrasonic

volumetric examination of the flywheel be performed at approximately 10-year

intervals, during the plant shutdown coinciding with the inservice inspection

schedule as required by Section XI of the ASME Code.

The interval for inservice inspection is based on 120 months pursuant to 10 CFR

50.55a(g)(4), with the initial interval beginning on the date of commercial operation.

Commercial operation for the Wolf Creek plant commenced September 3,1985. >

Provisions in Paragraph IWA-2400(c) allowed that each inspection interval may be

decreased or extended by as much as 1 year. The provisions of Paragraph C 4 b of

Regulatory Guide 1.14 specified that the surface and ultrasonic examination of the

flywheel be performed ". . . at approximately 10-year intervals." Therefore, using

the code provisions for the inservice inspection interval, the surface examination of

all of the reactor coolant pump flywheels should have been completed by

September 3,1996. The licensee confirmed on October 25,1996, that the surface

and ultrasonic examination of the "D" reactor coolant pump flywheel has not yet

been performed and is currently scheduled for the Fall 1997 refueling outage during

reactor coolant pump maintenance.

Section 50.59, " Changes, Tests, and Experiments," allows licensees to make

changes to licensed f acilities or to perform tests and experiments at licensed

facilities when these changes, tests, and experiments (1) do not change the

parameters specified in the f acility operating license, including Technical

Specifications, or (2) present an unreviewed safety question. If the changes, tests,

or experiments change the operating license, including Technical Specifications, or

present an unreviewed safety question, NRC approvalis required prior to

implementing the change or performing the tests or experiments. By reference in

the Technical Specifications, any exceptions to the reactor coolant pump motor

flywheelinspection program delineated in paragraph C.4.b of Regulatory

Guide 1.14, must be approved by the NRC.

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The team considered r, change to the examination schedule would result in a

-

change to the Tec,hn! cal Specifications by reference in paragraph C.4.b of

Regulatory Guide 1.14. Therefore, the proposed change to the examination would

require NRC approval prior to implementing the change. Failing to properly perform

the screening for the proposed change to the surface examination schedcle for the

reactor coolant pump flywheels to identify a change to the Technical Specification

is contrary to 10 CFR 50.59 and is considered to the third example of the apparent

violation discussed in Section E2.2 of this report 6 0-482/96021-02).

.

'

Af ter being informed of this discrepancy, the licens. e performed an operability

determination for the "D' eactor coolant pump whic., concluded that the pump was

capable of performing its safety related design function. This determination was

3

based upon satisf actory examination results c i f.he flywheel keyways and bore

i

which were last performed during Refueling Ou'tage 7. In addition, nuclear industry

experience has indicated that a decrease in inspection requirements is appropriate in

!

some cases. Based upon this inf ormation sod consultation with the Office of

Nuclear Reactor Regulation, the taan< cmAded that continued operation of the

pump until the examination could be performed was not a safety concern.

c. Conclusions

Numerous problems were identified with the Fcensee's implementation of the 50.59

review process, which were indicatise of a programmatic breakdown. Further

. evidence of a continuing breakdown in the review process was evident by the

exister,ce of changes made since 1994in which the licensee did not recognize

changes to the Technical Specifications (reactor coolant pump flywheelissue) or

other NRC approved programs (esrential service water system buried pipe testing

discussed in Section E2.7).

1

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The team determined that the program procedures the licensee has developed for

'

the review and evaluation of changes in accordance with 10 CFR 50.59 were

appropriate. Based on the number of findings in the 50.59 area, and the recent

indications of improper screenings for Updated Safety Analysis Report change

requests, the team concluded that trairting did not appear to have been effective in

avoiding continuing deficiencies.

>

The licensee's corrective action for a quality assurance audit, initiated in 1993,

identified potential problems with the use of Technical Specification clarifications,

did not identify potential conflicts between the Technical Specifications and the

clarifications. The followup audit by quality assurance failed to recognize that the

conditions found during the original audit finding were not corrected. This was

considered to be an apparent violation involving inadequate corrective action. In

addition, the review of the clarifications by the Plant Safety Review Committee, and

their failure to identify continuing iss.ues involving Technical Specification

compliance, calls into question the performance of that group.

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E2.4 Unsucoorted Operability Determination l

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a. Inspection Scope (37550)

The team reviewed one operability determination made during the inspection by a

shift supervisor associated with team observations.

b. Observations and Findinas

On October 22,1996, the team noted that the shift supervisor reviewed an informal

listing of inspection issues raised by the team. Item 133 noted that several

different documents, Technical Specification requirements, Updated Safety Analysis

Report sections, and a calculation identified conflicting essential service water flows

through the containment air coolers. Item 133 also identified two questions

regarding the correct number for essential service water flow through the

containment air coolers and, the correct number for heat removal rate of a single

containment air cooler. The shift supervisor reviewed this listing, then logged the

following entry into the Shift Supervisor Log: "1410 Reviewed items 130-134 on  !

Engineering and Technical Services NRC Inspection list - No operability /reportability l

issues noted."

The team asked the shift supervisor what the basis was for the log intry identifying

no operability issues for item 133. The shift supervisor stated his baus was

Calculation GN-MW-OO5, Revision 2, which used 4000 gpm flowrate per cooler

group, and that the assumption had been made that, ' ...the engineers knew what

they were doing." The team noted that the flow information used by this

calculation had been superseded, and that the present containment cooler flow was

2000 gpm flowrate per cooler group. The team questioned the engineer regarding

how the list had been presented to the shift supervisor. The engineer stated that

the list had been handed to the shift supervisor, and that there had been no

substantive discussion regarding item 133.

Administrative Procedure ADM O2-024," Technical Specification Operability,"

Revision 3, step 5.3.2, required the shift supervisor to perform a number of actions

associated with the operability determination to ensure sufficient scope of review.

This step required the shift supervisor to determine the requirement or commitment

established for the equipment, and why the requirement or commitment may not be

met. In cases where the operability determination was not straightforward,

Procedure ADM O2-024 also required the shift supervisor to use the information

available to make the determination, and start the actions stated in

Procedure AP 28-001," Evaluation of Nor. conforming Conditions of Installed Plant

Equipment," Revision 4, to obtain sufficient information to completely answer all

questions.

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The team determined that the operability evaluation performed by the shift

supervisor failed to include all the required actions, in that, the shift supervisor did

not properly identify the minimum acceptable flow rate for the containment air

cooler given the conflicting statements of containment air cooler flow in the

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Updated Safety Analysis Report and other documents, and compare the actual

cooler flow with the minimum flow requirement as stated in Technical

Specification 4.6.2.3.b. This is a violation of 10 CFR 50, Appendix B, Criterion V

(50-482/96021-05).

The inspection team noted that NRC Inspection Reports 50-482/96-012,

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50-482/96-11,and 50-482/96-09,had previously identified several examples where

the NRC had identified poorly supported operability determination.',. The team

determined that while the previous examples of poorly supported orarability

evaluations were not identified as violations of requirements, they indicated a

declining trend in performance. The violation identified in this paragraph was

determined to be more significant than the previous examples, in that, the shift

supervisor stated that the operability determination was, at least in part, based on

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an out-dated calculation and an unsupported reliance on engineering,

c. Conclusions

The team concluded that the shift supervisor violated 10 CFR 50, Appendix B,

Criterion V, when an operability determination failed to comply with the licensee's

procedure on operability determinations, and relied, at least, in part, on an out-dated

calculation. Previous examples identified by NRC inspectors indicated a declining

trend in the performance of operability determinations on shift.

E2.5 System Walkdowns (37550) '

a. Insoection Scope

,'

The team performed a walkdown of the three subject systems and other selected

plant areas to determine the overall material condition of equipment and

maintenance of housekeeping. In addition, the team walked down several portions

of the spent fuel pool cooling system, component cooling water system, and

instrument air system.

b. Observations and Findinas

The team found the housekeeping was generally very good. The team noted that  ;

the system engineers and design engineers were both knowledgeable of their

systems. The engineers demonstrated their knowledge during the walkdown by

explaining component deficiencies in detail and relating to the team specific

operational problems with system operation. The material condition of system

components was noted to be very good with little evidence of boric acid leakage  ;

and few deficiencies noted during the walkdown. The team noted that several '

minor system leaks had been previously identified by licensee personnel which

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indicated that a very gcad threshold for deficiency identification had been

established.

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The team reviewed the system engineers' notebooks for the three systems selected.

The team noted that these notebooks were maintained in a well organized manner,

and the separate sections were tabbed for easy reference. The safety injection

system engineer kept the trend data and system walkdown sheets current, and had

a sufficient breadth of material to support the stated description of system engineer

responsibilities.

The team asked the safety injection system engineer what the maintenance rule

performance goals and actual system performance was for the safety injection

system. Both the present and former system engineers knew that the safety

injection system performance was exceeding the goal by a wide margin. However,

neither engineer could readily identify the actual system performance statistics

without speaking with the maintenance rule coordinator. While the team did not

view this as a significant weakness, it did indicate that in this case the system

engineers did not have ready access to current maintenance rule performance

statistics for their system.

Safety Iniection Svstem Enaineer System Walkdown

The team noted that the safety injection system engineer had been assigned to this I

system 8 weeks prior to the inspection. During this period, the system engineer

had conducted only one joint walkdown with the previous system engineer. The

system engineer conducted system walkdowns approximately weekly, but

management only required these walkdowns biweekly. The system engineer's

supervisor had participated in one of these walkdowns.

During the walkdown with the team, the system engineer did not tour the

1988 foot elevation of the auxiliary building and was, therefore, unaware of a

flange leak on the suction line between the refueling water storage tank and the

common suction header supplying the eight emergency core cooling pumps. When

asked by the team, the prior system engineer stated that walkdowns had included i

portions of the 1988 elevation of the auxiliary building, but had never included the l

  • igh radiation area encompassing the pipe chase area. The system engineer

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.. dicated that these walkdowns took frorn 1.5 to 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> each, but that during

some weeks the system engineer would take credit for system engineer presence in

the field supporting maintenance as the system walkdown for the week. With the

exception of the 1988 elevation of the auxiliary building, the system engineer's j

walkdown was adequate.

The team discussed with licensee management their expectations for system .

engineering walkdowns. Management stated that they expected the system

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engineers to perform walkdowns in all areas containing system components,

although less frequently for high radiation areas due to exposure concerns. l

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Residual Heat Removal Temocrary Shieldina

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he team noted that temporary shielding had been erected on te ot-leg suction

piping for both trains of residual heat removal cooling and askeo >ut this situation l

and potential impact on system operability. The system engineer stated that this l

shielding was installed in 1991 per a temporary shielding request. The team j

reviewed the shielding request and scaffolding permits which controlled the erection  !

of scaffolding used to support the shielding off of the system piping. The team )

noted that the scaffolding permits did not address potential static loads which might l

be applied if the plastic straps which held the shielding to the scaffolding should  ;

fail. Licensee personnel acknowledged this deficiency in the scaffolding evaluation l

and inspected the erected scaffolding and temporary shielding. Licensee personnel

found that portions of the shielding were not secured by tie wraps as specified in

the evaluation and decided to remove the scaffolding pending completion of a new

evaluation.

The licensee completed a subsequent evaluation which determined that the secured

and unsecured shielding would not have adversely affected safety related piping

underneath the scaffolding. The team determined that the erected scaffolding and  !

shielding had not been reviewed by engineering personnel and the system engineer j

was not knowledgeable of the condition of this temporary shielding even though it

had been installed for several years. The team considered the temporary shielding .

controls to be weak for not requiring an engineering review of erected temporary i

shielding and periodic inspections of installed temporary shielding. The licensee j

subsequently revised Procedure AP 25A-700,"Use of Temporary Lead Shielding,"

to require periodic inspections, verify shielding installation conformed with the

engineering disposition, and evaluation of the need for permanent shielding if

temporary shielding is installed for 6 months.

c. Conclusions

The team found the housekeeping was generally very good. The team noted that,

in general, system engineers and design engineers were very knowledgeable of their

system. The material condition of system components was noted to be very good

with little evidence of boric acid leakage and few deficiencies. A very good

threshold for deficiency identification had been established. System walkdowns by

the safety injection system engineers did not include all plant areas were system

components were located.

The team considered temporary shielding controls to be weak for not requiring an

engineering review of erected temporary shielding and periodic inspections of

installed temporary shielding. The residual heat removal system engineer was not

knowledgeable of the condition of temporary shielding even though it had been

installed for several years.

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E2.6 Ennineerina Work Backloa (37550)

a. Insoection Scope

The team discussed the status of the engineering backlog with the Assistant to the

Vice President of Engineering. The discussions included actions taken by the

engineering organization to reduce the backlog.

b. Observations and Findinas

The licensee's engineering backlog program was managed by the Assistant to the

Vice President of Engineering. The team interviewed the program manager and

found him to be knowledgeable of his responsibilities, but noted that no one had

been assigned backup responsibilities for this effort. This observation was

compounded by the fact that this program was not proceduralized, and that the

data was manually collected and tracked. Therefore, the team considered the

program to be very susceptible to personnel changes in the organization. In

addition, it was noted that the open item information collected had not been trended

to determine the overall impact the open items had on the engineering department

workload.

The licensee's eng;neering backlog listed only 65 open items. The team found this

number to be artificially low because the licensee's threshold for backlog item.s was

j high (i.e., several categories listed backlog criteria as high as 1 to 3 years old). The

licensee explained that when the program was initially started in 1992, the backlog

, criteria was set high intentionally so as to identify those items which were the

, oldest, while keeping the number of backlog items at manageable levels (i.e., with

these backlog criteria, the licensee engineering backlog, at the time, was greater

than 700 open items). However, the team noted that by 1994 the licensee had

significantly reduced their engineering backlog, but had failed to adjust the backlog

criteria. The failure by the licensee to reduce the threshold of the backlog criteria

was considered a weakness.

To better understand the work load on engineering personnel, the team questioned

the number of open items presently assigned to the department. At the time of this

inspection, there were approximately 1508 total open items. To determine the

impact of the opca items and to assess the safety significance of items still open,

the team reviewed a number of the open items listed (plant improvement requests,

corrective work requests, licensee event reports, etc.). The team determined that

the open items had been appropriately categorized and given the appropriate

prioritization for correction and closecut.

A number of closed items were also reviewed. Licensee actions in closing these

items were considered to be appropriate.

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Finally, the team interviewed members of the engineering staff with regard to work

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backlog. Open items were tracked by engineering supervisors at the group level.

Engineers appropriately scheduled and worked on open items according to their

prioritization and procedural requirements.

The licensee indicated that according to their records, the overall number of open

items that are tracked has been generally on the decline. However, performance

improvement requests were the only open item group that had showed a steady

increase. The licensee attributed this to a lower threshold for issuance of these

reports and a heightened awareness by plant personnel due to increased training in

this area.

c. Conclusions

The licensee managed the engineering open item workload appropriately, but the

licensee backlog program was found to be behind the industry standard due to the

lack of a formalized program, high threshold for backlog criteria, and the failure to

trend the impact of the backlog on engineering personnel workload.

E2.7 Surveillance Testina

a. Insoection Scope

The inspector reviewed Technical Specification surveillance requirements for the

three systems selected and the most recently completd surveillance tests for each

of these surveillance requirements, j

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b. Observations and Findinas )

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The surveillance for the systems selected accomplished the Technical Specification

surveillance requirements and were performed at the correct periodicity. Exceptions

are noted below:

Imorocer Verification of Emeraency Core Coolina System Throttle Valve Mechanical

Stoo Position

Technical Specification Surveillance Requirement 4.5.2.g required the licensee to

verify the correct position of each mechanical position stop for the listed emergency

core cooling system valves every 18 months. This verification ensures that

sufficient cooling flow is available for post-accident conditions. The licensee i

accomplished this surveillance requirement by performing Procedures STS EM-001,

" Emergency Core Cooling System Throttle Valve Verification," Revision 11, and

STS BG-004, " Chemical and Volume Control System Seal Injection and Return Flow

Balance," Revision 4. These procedures required workers to measure the valve

stem height for the valves specified in the Technical Specification.

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The team asked how the surveillance procedures verified the position of the

mechanical position stops. The 12 EM (Safety injection) system valves listed in

Technical Specification 4.5.2.g, and Valve DGV-202, did not have mechanical

position stops, but were locked in place using a locked chain as specified in

Procedure AP 21G-001," Control of Locked Component Status," Revision 7. Seal

injection valves BGV-198, BGV-199, BGV-200, and BGV-201 had valve stem

locknuts to secure the valve in position, but they were not required to be tightened

or verified during performance of the surveillance test. In addition, the team noted

that the procedure contained a drawing of the valve which did not indicate the

presence of a locking nut.

The team considered the surveillance procedure to be deficient for not including the

specific design attributes of the mechanical stops and specific action necessary to

verify the correct position of the stops. In response to this concern, the licensee

checked the locknuts, and found them tight. The team interviewed two non-

licensed operators who had recently performed this surveillance procedure, and

found that the operators could not recall whether they tightened the locknuts during

this surveillance, or not. The system engineer also interviewed another non-

licensed operator who had recently performed this surveillance and also found that

the operator could not recall tightening the locknuts. The failure of

Procedure STS BG-004 to require the test performer to tighten the locknuts for

these valves is a violation of Technical Specification 6.8.1.a (50-482/96021-06).

Imoroner Essential Service Water Underaround Pioina Pressure Test

The team reviewed Performance Improvement Request 95-2326, which was

initiated on September 20,1995, to request a change in the test method for

essential service water system underground piping pressure tests. The description

of the problem stated that past performances of Test Procedure STS PE-049C,

" Essential Service Water System Underground Piping Leakage Test," Revision 1,

had proven to be very cumbersome and manpower intensive. This test was written

to satisfy the requirements of ASME Section XI as implemented by the licensee's

inservice inspection program for this Code Class 3 system. The test method being

used included the installation of blank flanges, isolating the system, and

determination of the rate of pressure loss. Because this portion of pipe is buried

underground, the initiator requested that the optional testing requirements in

Article WA-5244 of the ASME Code be considered for alternative testing of buried

components. Article IWA-5244 contains three options that are based on system

redundancy and piping isolation abilities:

(a) In non-redundant systems where the buried components are isolable

by means of valves, the visual examination VT-2 shall consist of a

leakage test that determines the rate of pressure loss. Alternatively,

the test may determine the change in flow between the ends of the

buried components. The acceptable rate of pressure loss or flow shall

be established by the owner.

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(b) In redundant systems where the buried components are nonisolable,

the visual examination VT-2 shall consist of a test that determines the

change in flow between the ends of buried components. In cases

where an annulus surrounds the buried components, the areas at each

end of the buried components shall be visually examined for evidence

of leAage in lieu of a flow test.

(c) In non-redundant systems where the buried components are

nonisolable, such as return lines to the heat sink, the visual

examination VT-2 shall consist only of a verification that the flow

during operation is non impaired.

In the evaluation for this request, the engineer concluded that each of the two trains

of essential service water could be considered a non-redundant system. This

interpretation determined that each train provided cooling water only to the loads )

associated with that train (i.e., Train A of essential service water supplies cooling )

water to Train A heat loads, and Train B of essential service water supplies cooling j

water to Train B heat loads, with no other cooling water supply to the separate l

trains). This interpretation was not based on an ASME Code definition or an official j

ASME Interpretation.  !

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As a result of the evaluation, the engineer further concluded that paragraph (c)

of Article IWA-5244, could be applied to the buried portions of the essential

, service water system. This conclusion resulted in revisions to Test

Procedure STS PE-049C, "A Train Underground Essential Service Water System

Piping Flow Test," and development of new Test Procedurs STS PE-049D,

"B Train B Underground Essential Service Water System Piping Flow Test," which

eliminated the previous method of performing the visual examination VT-2 (i.e.,

determination of the rate of pressure loss) and implemented visual examination VT-2

that consisted only of a verification that the flow during operation is not impaired.

Section 9.2.1.2, " Essential Service Water System," of the Updated Safety Analysis l

Report stats that the essential service water system consists of two redundant )

cooling water trains. The team considered the licensee's interpretation of system

non-redundancy to contradict this statement in the licensing basis.

The 10 CFR 50.59 screening for the test procedure change indicated that

Chapter 9.2 of the Updated Safety Analysis Report was reviewed. The screening j

did not discuss the discrepancy regarding redundant versus nonredundant j

definitions for the essential service water system trains. The licensee did not j

submit a request for NRC review and approval of the alternative test method, i

Neither did the licensee revise Chapter 9.2 of the Updated Safety Anansis Report to

indicate that the essential service water system trains could be considered

nonredundant systems. Therefore, the team considered that the screening for the

proposed change to the underground piping test procedures was deficient for not

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identifying that a change to the Updated Safety Analysis Report or inservice

inspection program (Technical Specification 4.0.5) was involved. This deficiency is

contrary to the requirements of 10 CFR 50.59 and is considered to be the fourth

example of the apparent violation (50-482/96026-02).

The revised Procedure STS PE-049C was used for the system pressure test

performed for the third 40-month period in the first 120-monthinterval. The test

was completed on January 17,1996. Likewise, Procedure STS PE-049D was

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performed during January 1996. Performance of the revised tests resulted in the l

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f ailure to comply with the requirements of Section XI of the ASME Code for buried l

piping in redundant systems and non-compliance with Technical Specification 4.0.5.

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During the exit meeting, the licensee disagreed with the tearn's conclusion that this

matter was a violation. The licensoe stated that since neither the AMSE Code nor

the Technical Specifications defined the term " redundant"; therefore, it was

appropriate for them to do so. The licensee's inservice inspection engineer had

l attended industry working group committee meetings, which discussed pressure

testing and the definition of redundant and non-redundant systems. The licensee )

l referred to the 1995 Addenda to the 1995 Edition of Section XI of the ASME Code,

! Article IWA-5244, which had been changed to differentiate test methods based

only on whether the piping is isolable or non-isolable, and removed references to

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redundant or nonredundant. The inservice inspection engineer utilized this

l knowledge when interpreting these requirements for underground piping pressure

testing. In addition, the onsite Authorized Nuclear Inservice inspector had reviewed '

the change to the test procedure and had no comment. However, the inspection

l team noted that the NRC has not yet endorsed the 1995 Addenda and the

Authorized Nuclear Inservice inspector has no responsibility under 10 CFR 50.59.

l c. Conclusions

in general, the team found that the surveillance for the systems selected

accomplished the Technical Specification surveillance requirements and were

performed at the correct periodicity. However, the team identified one violation

associated with an inadequate procedure to verify emergency core cooling throttle

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valve mechanical position stops, and an example of an apparent violation regarding

! pressure testing of essential service water system underground piping.

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l E2.8 Industrv Event Assessment and Lessons Learned

a. Insoection Scope

The team reviewed two industry events to determine the licensee's action to

prevent similar problems. Industry documented failures of 4.16 kV General Electric

Magne-Blast circuit breakers to properly close, and of improper refurbishment of

l 4.16 kV breakers by overhaul vendors, were selected for review due to generic

applicability to the plant.

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b. Observations and Findinas

The team tound that the licensee had received reports of these events and had

taken corrective actions to prevent occurrence of these problems at Wolf Creek.

Preventive maintenance procedures and procurement documentation had been

reviewed by licensee personnel and appropriate revisions made to identify and

correct similar problems.

E3 Engineering Procedures and Documentation

E3.1 Review of Desian Basis Documents

a. Lniggection

r Scoce

The team reviewed the design basis documents for the essential service water

system, the residual heat removal system, and the safety injection system to verify

the validity of the design basis and determine the ease of retrieving the information.

b. Observations and Findinas

The team reviewed the design basis notebook for the essential service water

system and determined that the notebook had been approved in May 1993 and had

not been updated since then. The team noted a statement in the notebook that

when the notebook was to be used for design input, the user should take into

account the changes issued after the approval date of the notebook. At the time of

the notebook approval, the notebook had been a controlled document.

The team reviewed interoffice Correspondence ED 96-0047, dated September 17,

1996, concerning design basis notebooks. The letter stated that due to downsizing

of engineering and the need to reorganize the work effort, design engineering had .

identified that the notebooks were an opportunity to reduce the demand on )

engineering services. Some of the licensee's actions were to keep the notebook for j

information only and not maintain it as a controlled document. In addition, the  !

licensee decided that the system description docurnents would be used to keep  !

design basis information in the future. The licensee further stated that the extent of

information added to the system description would vary depending on the  ;

judgement of the responsible engineer. The design engineering manager stated that i

there was no need for the notebooks since all of the engineers were very

experienced and knew where to find the design basis information.

Since the design basis notebooks provided information to support the design and

licensing basis and provided the location of other design bases documents, the team I

considered that uncontrolled and out-dated notebooks hindered the control of design

basis information. This conclusion was supported by the fact that no other

controlled document provided this information. The team also noted during the

inspection, there were times when the licensee had difficulty retrieving design basis

information. The team considered the licensee's control of design basis information

to be weak for not providing a centrallocation for the design basis information.

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c. Conclusions

Uncontrolled and out-of-date design basis notebooks hindered the control of design

basis information. The licensee's control of design basis information was found to

be weak,in that, it did not provide a centrallocation for the design basis

information. Licensee personnel had difficulty retrieving some design basis

information.

E5 Engineering Staff Training and Qualification

E5.1 System Enaineerina Staff Trainina and Qualification (37550)

a. inspection Scope

A review was performed of the system engineering training program. The team

reviewed Administrative Procedures AP-23-006," System Engineering Program, "

Revision 3, and AP 30F-OO1,"Engir:eering Support Personnel Training and

Qualification Program," Revision 2. The team discussed the training requirements

with a number of system engineers, and members of their direct management,

during individual interviews. In addition, the team reviewed the training records for

all of the system engineers.

b. Observations and Findinqs

The team found the guidance for system engineering training and management

expectations provided in the licensee's administrative procedures to be general in

nature. Training requirements for engineers newly assigned to the system

engineering department, were developed by the engineer's immediate supervisor,

and were found to consist of " Qualifying Activities," which included " Evaluation of

Nonconforming Conditions of Installed Plant Equipment," (i.e. operability

determinations) " Engineering Calculations," "Unreviewed Safety Question

Determination," etc. Specific training on assigned systems was not required and

was left to each engineer's discretion to take system-specific courses that

periodically were offered for operations personnel. With regard to those situations

in which system engineers were assigned to a specific system, but were later given

responsibility for another system, the team noted that little guidance on training was

available other than for " Qualifying Activities." Finally, none of the procedures

were found to specify a time period for completion of training requirements nor

were there any minimum criteria for system engineer acceptance in response to

this concern, the system engineering management issued a performance

improvement request.

In spite of the overall general guidance, the team found that the system engineer's

knowledge of each of their assigned systems was excellent. This was due, in part,

to a significant nurnber of engineers having been involved in operator systems

training prior to entering the system engineering program. In addition, the system

engineers and their immediate supervisors displayed excellent initiative to improve

their knowledge.

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F(,r example, the system engineers interviewed were knowledgeable of industry

problems and maintained periodic contact with other utilities and equipment

vendors. The system engineers also periodically walked down their systems in

accordance with a system walkdown schedule that had been reviewed and

approved by their immediate supervisors. The system engineering supervisors

encouraged their personnel to attend technical presentations, classes, and meetings I

held by vendors or other utilities. One specific example of the initiative taken by the 1

system engineering supervision involved the reactor coolant system engineer, who

had been recently assigned to take responsibility for this system. His supervisor

arranged a visit to the Callaway plant, which had an identical reactor coolant

system and was in an outage. This afforded the system engineer an opportunity to ,

walk down the reactor coolant system and become familiar with his system which I

he might not have been able to do at Wolf Creek until their next assigned refueling  ;

outage. l

Finally, almost all system engineers were found to have completed the appropriate

" Qualified Activities" training as indicated by their departments training records.

Those cases where engineers had not completed their assigned training was due

specifically to the fact that they had recently been assigned to their present

position.

C. Conclusions

System engineering knowledge was found to be excellent and was based on the ,

initiative taken by system engineers and their immediate supervisors, and not by "

any specific guidance provided in administrative procedures available. Training

guidance was found to be too general. Specifically,it did not provide a minimum

standard for system engineer training or knowledge.

E6 Engineering Organization and Administration

E6.1 System Enaineerina (37550)

a. Inspection Scope

The team interviewed the system engineering manager, three group supervisors,

and seven system engineers. The team focussed on licensee management

expectations of the system engineers and the system engineering program. This

included the method in which these expectations were communicated to the system

engineers, the mechanics of how plant problems were identified and corrected, and

the adequacy of communication between the system engineering department and

other plant organizations such as operations and maintenance. Additionally, the

system engineers were questioned on technicalinformation and outstanding

deficiencies for their assigned systems, including actions they were taking to

resolve those deficiencies.

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b. Observations and Findinas

The licensee management expectations of the system engineers and the

system engineering program were delineated in licensee Administrative

Procedure AP 23-006, " System Engineering Program," Revision 3, and

Administrative Instruction Al 23-002," System Engineering Plant Walkdowns,"

Revision O. Licensee management also communicated their expectations verbally

either directly or through the group supervisors.

As stated previously in this report (Section E5.1), the team found that the guidance

provided in the administrative procedures and instructions were general in nature.

More specific guidance was verbally provided to the system engineers, at the group

level, by their appropriate supervisors.

The system engineers stated that although engineering management expectations

were general in nature, they believed that the guidance being provided presently

was an improvement over the lack of guidance that existed in 1995. This

improvement was in part the result of Self Assessment Reports SEL 95-039,

" System Engineering," dated January 19,1996, and SEL 96-025, " System

Engineering Self Assessment Effectiveness Follow-up," dated September 16,1996.

The system engineers indicated that with a clearer definition of their job scope, they

have a better understanding as to what they are required to do and which type of

activities they can defer to another organization. The team found that system

engineers understood their management's expectation in which they would be the

" experts" of their assigned systems and take " ownership" of their assigned

responsibilities.

In accordance with the procedural guidance, system engineers also had developed

primary trending parameters, and walkdown guidelines for their assigned systems,

which were reviewed and approved by their group supervisors. However, the team

noted that the consistency of how these two aspects of the system engineers

workload were being performed was not closely monitored by engineering

management. In addition, the system engineers used system notebooks in an

inconsistent manner. Nonetheless, the system engineers knowledge of their

individual systems was excellent Operations and maintenance planning personnel

considered the system engineers as the " experts" of their assigned systems and as

the focal point for any questions on these systems. Operations personnel indicated

that they had confidence in system engineering personnel to provide them the

appropriate information to make operability determinations.

System engineers displayed " ownership" of their system by following maintenance

activities being performed on their assigned systems. Plus, system engineers

periodically reviewed corrective work requests to identify if any applied to their

assigned system. As mentioned in Section E2.6, system engineers demonstrated

this ownership during the system walkdowns with team members.

31

. - - ._ - . - - -

.

.

The team noted that the system engineering program did not specify the need for

backup system engineers for the safety-related equipment. The licensee had an

unofficial system engineer backup program, but it did not have any basic training

criteria or knowledge expectations, in addition, some of the system engineers were

unaware that they had been assigned as backup system engineers. and others were

not aware that any backup system engineers had been assigned to their system.

Finally, other plant personnel were unaware as to whom were the backup system l

engineers, and what systems they were responsible for. This is considered to be a

weakness in the system engineering program, and behind industry standards.

c. Conclusions

Overall, the system engineers were found to be knowledgeable of management

expectations and their responsibilities. Licensee management communication of

system engineering expectations has improved. The lack of assigned backup

system engineers was considered a program weakness.

E6.2 Desian Enaineerina (37550)

a. Inspection Scoce

The team conducted interviews with personnel from the maintenance planning, and

operations departments to evaluate tht, extent and effectiveness of design

engineering communications. The team also reviewed a number of change

packages and performanca improvement requests that required engineering

involvement, in an effort to determine how technical issues were resolved.

b. Observations and Findinas

The team identified that cooperation and communication among the design

engineering department and operatbns, and maintenance planning departments

were good. Engineers indicated that management encouraged identification of plant

problems. This has contributed to the increase in the number of performance

improvement requests.

The team found that the performance improvement requests and change packages

reviewed had technical resolutions with proper engineering justifications and that

the proposed corrective actions were adequate.

The team noted that engineers were appropriately utilizing available design basis

documents to determine if a proposed change was within the original design basis.

All personnel interviewed were aware that the design basis notebooks were not

controlled documents, and they only used them as reference documents.

c. Conclusions

The team concluded that the licensee was effectively implementing their program to

respond to requests for engineering resolution of plant problems.

32

- . . _ . - - -_ _ -

I a

=

l

E7 Quality Assurance in Engineering Activities

a. Insnection Scope (37550)

I

The team reviewed four recent quality assurance self assessment reports related to

engineering activities. Self Assessment Report SEL 96-033," Licensee Event Report

Program," dated October 2,1996, SEL 96-025, " System Engineering Self

Assessment Effectiveness Follow-Up," dated September 9,1996, and SEL 95-056,

" Auxiliary Feedwater System," dated January 9,1996, were reviewed to evaluate

the effectiveness of the licensee's controls in identification and resolution of plant

problems. Although not complete, the inspection team reviewed the assessment

plan and preliminary findings for an auxiliary feedwater functional assessment.

b. Observations and Findinns

The team found that the self assessments were broad in scope and provided I

meaningful findings and recommendations for potential program enhancements. As l

an example, the auxiliary feedwater system self assessment resulted in a number of

improvement recommendations. These recommendations encompassed more than

enhancements to system performance and reliability but system engineering

program enhancements also. One such improvement recommendation included

placing the site wide trending program in a centralized location (e.g., trending data

is located in several groups and information exchanged is not formalized). Other

recommendations included a review of spare parts availability. Although

improvements since the previous self assessment (SEL 95-039) had occurred, the

system engineering self assessment identified weaknesses in management and

,

supervisory oversight of the system engineers. The self assessments resulted in the

issuance of a number of performance improvement requests to address the

weaknesses identified.

The team found that the auxiliary feedwater system functional assessment plan

included similar items that the team was reviewing in addition, some of the initial

findings from this self assessment effort were similar to those identified in this

report.

c. Conclusions

The team concluded that the licensee's self-assessment reports were effective.

E8 Miscellaneous Engineering issues

E8.1 (Closed) Inspection Followuo item 50-482/9504-03: Use of gear operator stop nut

for actuator braking.  ;

The licensee contacted the valve operator manuf acturer who reviewed the

licensee's procedures for setting the stop nuts and lirnit switch settings and

concurred with the licensee's actions. The load applied to the stop nuts was within

rated design load.

.

33

l

l

.

.

E8.2 (Closed) Licensee Event Report 50-482/96001: Loss of circulating water due to

icing on traveling screens.

This event was discussed in NRC Inspection Report 50-482/90-03 and was the

subject of a violation as listed in NRC letter EA96-124, dated February 29,1996,

item 06014. No new issues were revealed by the licensee everit report and

followup on the licensee's corrective actions will be performed during the review of

the violation.

E8.3 (Closed) Licensee Event Report 50-482/96002: Loss of essential service water

train due to icing on trash racks.

This event was discussed in NRC Inspection Report 50-482/96-03and was the

subject of two violations as listed in NRC letter EA96-124, dated February 29,

1996, items 02013 and 04013. No new issues were revealed by the licensee

event report and followup on the licensee's corrective actions will be performed

during the review of the violations.

V. Manaaement Meetinas  ;

l

X1 Exit Meeting Summary

The team presented the inspection results to members of licensee management at the

conclusion of the inspection on October 25,1996. An exit meeting was held via '

teleconference on November 8,1996. The licensee acknowledged the findings presented.

The overall scope and results of the inspection were discussed with Mr. Terry Damashek,

on December 31,1996.

The licensee did not identify that any propriety information was reviewed by the team.

l

34

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_ . - . .- . . . - . . . - - . . . - - . _

~ - . - - ._. -.

O

.

.

ATTACHMENT

,

'

SUPPLEMENTAL INFORMATION

i

PARTIAL LIST OF PERSONS CONTACTED

Licensee

G, Boyer, Director, Site Support

T. Damashek, Supervisor, Regulatory Compliance

R. Flannigan, Manager, Nuclear Engineering

a T. Garrett, Manager, Design Engineering i

l B. Grieves, Supervisor, Systems Engineering I

'

T. Hood, Supervisor, Design Engineering

i N. Hoodley, Manager, Support Engineering

I

R. Hubbard, Superintendent, Operations

O. Maynard, Chief Administrative Officer j
B. McKinney, Plant Manager i
T. Morrill, Manager, Regulatory Services  !

7

'

R. Muench, Vice President Engineering  !

G. Neises, Supervisor, Reactor Engineering  ;

'

D. Neufeld, Acting Manager, Integrated Planning and Scheduling  !

-

W. Norton, Manager, Performance improvement and Assessment

i' K. Scherrch, Supervisor, Systems Engineering

R. Sims, Manager, Systems Engineering

l- J. Stamm, Supervisor, Safety Analysis

l' C. Warren, Chief Operating Officer

C. Younie, Manager, Operations

. i

NRC )

1

S. Freeman, Residunt inspector

i

j INSPECTION PROCEDURES USED

IP 37550 Engineering

j IP 37001 10 CFR 50.59 Safety Evaluation Program

IP 92903 Followup - Engineering

.

e

1

i

,- .- . . ... _ _

. . . .

_ . _ _ _ . . _ . _ . _ . _ . - . . - _ . _ _ - _ _ _ _ _ _ _ _ _ _ _ _ .- _ -_ _

<

i

.

ITEMS OPENED AND CLOSED

Ooened

~

. 50-482/96021-01 VIO . Inadequate Cortrol of Design Bases (Section E1.2)

,

60-482/96021-02 APV Four Examples of the Failure to Properly Perform Safety

Evaluations (Sections E2.2, E2.3, E2.3, and E2.7)

, 50-482/96021-03 APV Failure to disable centrifugal charging pump while in cold

shutdown (Section E2.3)

l 50-482/96021 04 APV inadequate Corrective Action for Screening Technical

i Specification Clarifications (Section E2.3)

1

50-482/96021-05 VIO Unsupported Operability Determination for Containment

Cooler Flow (Section E2.4)

1

50-482/96021-06 VIO Inadequate Procedure for Verification of Emergency Core

Cooling Throttle Valves Mechanical Position Stops

j (Section E2.7)

Closed

50-482/95004-03 IFl Use of Gear Operator Stop Nut for Actuator Braking

l (Section E8.2)

]

50-482/96001 LER .oss of Circulating Water due to Ice (Section E8.3) i

l 50-482/96002 LER Loss of Essential Service Water train due to Ice

(Section E8.4)

i

j LIST OF DOCUMENTS REVIEWED

j Unreviewed Safety Question Determinations

i Number Title

'

59 93-0211 Main Steam Isolation Actuator Upgrade Modification, Revision O

i

j 59 94-0174 Deletion of Reporting Requirements from Updated Safety Analysis i

Report for Seismic Monitors, Revision 0

,

!

)

l

) 59 95-0003 Reactor Coolant Pump Flywheel Inspection Clarification, Revision O l

,

l 59 95-0016 Spent Fuel Pool Surveillance Level Indicator, Revision O

59 95-0034 Fire Area Combustible Load Evaluation, Revision 0

!

2

1

.- - .- ._

l

i

.

59 95-0046 Optional Opening Between Room 1203 and Roc,m 1204, Revision O

l

59 95-0057 Minimum Acceptance Criteria for Centrifugal Charging Pump B, l

Revision 0  !

59 95-0061 Transient Cable Separation Criteria, Revision O

59 95 0063 Biennial Relevancy Procedure Review Requirements, Revision 0

59 95-0109 Auxiliary Feedwater Pump Turbine Exhaust Line Upgrade, Revision 0

59 95-0129 Emergency Diesel Generator Design E.xplanation, Revision 0

59 95-0160 Auxiliary Feedwater Flowrate Revision, Revision 0

59 95-0151 Emergency Core Cooling System Flowrate Revision, Revision 0

59 95-0156 Boron injection Tank Recirculation Pump Removal and Removal of

Thermal Relief Valve, Revision 0

59 96-0032 Operation with Polypropylene Filter Membrane Material in Spent Fuel

Pool, Revision 0

59 96-0034 Delete Reporting Requirements for Meteorological Tower j

Instrumentation, Revision 0 '

59 96 0038 Use of Safety injection Pump for Boration in Mode 6, Revision 0

59 96-0086 Downgrade of Reactor Coolant Pump #1 Seal Leak Off Pressure

indicator, Revision 0

59 96-0109 Highpressure Feedwater Heater Bypass Test, Revision O

59 96-0115 Delete Program Descriptions from Updated Safety Analysis Report,

Revision 0 I

59 96-0143 Revise Updated Safety Analysis Report to Refle t use of Auxiliary

Feedwater in Residual Heat Removal Process, Revision 0

59 96-0148 Revise Scaffolding Procedure, Revision 0

59 96-0155 Clarification of Regulatory Guide 1.144, Revision 0

3

.

.

Updated Safety Analysis Report Change Requests Associated With

Technical Specification Amendments

Number Title

Amendment 89 Updated Safoty Analysis Report Change Request 95-137, dated

12/1/95, Borated Water Sources

Amendment 91 Updated Safety Analysis Report Change Request 95-138, dated

12/1/95, Refueling Water Storage Tank Boron Concentration

Amendment 93 Updated Safety Analysis Report Change Request 96-004, dated ,

1/11/96, Relocate Time Response Tables to Updated Safety Analysis !

Report

Amendment 94 Updated Safety Analysis Report Change Request 96-104, dated

9/17/96, Operation of Emergency Fuel Oil Transfer System I

Updated Safety Analysis Report Change Requests

Number Title

87-022 Corrections to Typographical Errors in Chapter 6, dated 7/15/87 l

1

96-031 Surveillance Frequencies fo'r Main Dam, Saddle Dams, and Baffle

Dikes, dated 2/16/96

96-094 incorporate Technical Specificsiion interpretation, dated 8/29/96

96-095 Incorporate Technical Specification Interpretation, dated 8/29/96

96-096 incorporate Technical Specification Interpretation, dated 8/30/96

96-104 Revise Emergency Diesei Generator Transfer Pump Logic, dated

9/17/96

i

96-118 Revise Spent Fuel Pool Rack Information, dated 9/26/96 )

l

91-047 Correction to Updated Safety Analysis Report Change Request  ;90-114, dated 7/10/91 j

4

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- . . . . . - . - . . - . . .- .- . ~ . - . - - - -. . . - - . - . - - _ . - - . . - . .

,

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Regulatory Screenings

-

l f

Number Title

t

j

i

05622 Revision 0, Motor Operated Valve  !

I  !

j 05720 Revision 0 and Revision 1, Pressure Locking Modification

l
05782 Revision 2, Turbine Driven Auxiliary Feedwater Pump Resistor Modifications *

'

!

05846 Revision 0, NK Battery Replacement '

i I

05900 Revision 0, Pressure Locking / Thermal Binding Evaluation  !

.

05906 Revision 0, Centrifugal Charging Pump High Temperature Alarm

i

t

05927 Revision 0, Low Flow Cavitation Limit Exceeded

I

i

06023 Revision 0, Pacific Valve Configuration Change ,

] 06025 Revision 0, Drain Holes in Code Relief Valves

1

06107 Revision 0, Relief From American National Standards Institute Code

i Hydrostatic Test Requirements

}

d

i 06183 Revision 0, Delete Thermal Relief Valves from Component Cooling Water

j System

06189 Revision 0, Battery Charger Alarm Setpoint

06252 Revision 0, Turbine Driven Auxiliary Feedwater Pump Valve Stem

Replacement

06285 Revision 0, Revised Thermal Design Flow

06304 Revision 0, Load Drop for New Fuel Storage Facility

06394 Revision 0, Safety injection Pump Rework

06445 Revision 0, New Safety injection Pump A and Rotating Element B Approval

2121 Revision 5, Flow Element EM FE0928 ALARA Concern i

3749 Revision 1, SMB-00 Torque Switch improvement

4055 Revision 4, Valve EM HV8807A & B Speed Reduction

4139 Revision 6, Motor-operated Valve - Concerns with EM HV8814A/B

5

.

-- . - - .- .. - . - - - - - -- - -- -- - - - - - - - - - - -

.

4

,

4145 Revision 4, Adjust Torque Switch Settings on EM HV8924  ;

i 1

4148 Revision 7, Motor-operated Valve - Disposition for EM HV8801 A/B & EM

j HV9903A/B

4150 Revision 5, Valve EM HV8835 Motor-operated Valve Disposition

,

4385 Revision 2, Main Control Board Switch Engraving Discrepancies i

,

4394 Revision 13, Target Rock Valves Replacement

i 4537 Revision 4, Boron injection Tank Recirculation Removal

i

'

6424 Revision 1, Fabrication of Thrust Collar Spacer for PEM01 A

6457 Revision 0, Safety injection Pump Motors PEMC1B Bolts Modification

Industry Technicalinformation Program Reports

i

! Number Title

l 02102 Liberty Technologies, 10-2-92: 10 Code of Federal Regulations Part 21

Notification, Stem Material Constants And Torque Calibrator Effects impact

! Votes Testing Accuracy, Potential For Overthrust

j O2340 NRC Information Notice 93-37: Eyebolts With Indeterminate Properties

installed in Limitorque Valve Operator Housing Covers

J

O2371 Limitorque Maintenance Update 92-02
Motor Pinion Keys, Motor

!

'

Performance, Declutch Tips, Torque Switch Repeatability, Actuator

Nameplate, Actuator Wiring

!

. 02372 Limitorque Maintenance Update 92-02: Motor Pinion Keys, Motor

Performance, Declutch Tips, Torque Switch Repeatability, Actuator

Nameplate, Actuator Wiring

02373 Limitorque Maintenance Update 92-02: Motor Pinion Keys, Motor

Performance, Declutch Tips, Torque Switch Repeatability, Actuator

Nameplate, Actuator Wiring

6

.

.

Calculations

!

Number Title

C-1989-130 Seismic Reanalysis of Refueling Water Storage "anks, Revision 2

EF-M-014 Ultimate Heat Sink Thermal Analysis Review for Power Uprate,

Revision 1

EF-M-029 Minimum Essential Service Water Temperature Rise, Revision 1

EF-M-030 Determine Required Essential Service Water Warming Line Flow,

Revision O

EF-M-031 Determine Orifice Sizes for Ultimate Heat Sink Outlet, Warming Line

Outlets, and FE-3&4 Necessary to Ensure 5000 GPM Essential

Service Water Warming Line Flow and the Corresponding Maximum

Pressure Downstream of FE-3&4,

Revision O

l

EF-M-032 Determine Hydraulic Grade Line Elevation Required at the Essential l

Service Water Warming Line Branch, Revision 0

l

EF-M-033 Evaluate if 1" Thick Plate is Acceptable for EF-FE-03 & EF-FE-04,

Revision O

EF-M-034 investigate Design for Ultimate Heat Sink Discharge Orifice Plate on

Essential Service Water System, Revision 0

EF-M-035 investigate Design for Warming Line Discharge Orifice Plate on

Essential Service Water System, Revision 0

1

EF-M-036 Determiration of Maximum Lake Temperature for Operation with {

Warming Flow, Revision O

'

EF-M-037 Summary of Document Control Procedure 06349 M-11EF01 Flow

Diagram Changes, Revision 0

1

ECCS-5 Centrifugal Charging Pump "A" Net Positive Suction Head l

Determination During Cold Leg Recirculation, Revision 0

ECCS-6 Centrifuga' Charging Pump "B" Net Positive Suction Head

Determination During Cold Leg Recirculation, Revision O

ECCS-7 Centrifugal Charging Pump "A" Net Positive Suction Head

Determination During Hot Leg Recirculation from Residual Heat

Removal Sump "A," Revision O

7

?

I

'A.4

_ 4.m.-- 4-n-.--m+. 2-+e- km esM, -

- -"#--.*4mnE-d hwq s hM -.4 64.) h..a 4 -A= ~ Akm.+m4.~4,

, 1

i

.

ECCS-8 Centrifugal Charging Pump "B" Net Positive Suction Heaa l

Determination During Hot Leg Recirculation from Residual Heat

Removal Sump "A," Revision O

i

ECCS-9 Refueling Water Storage Tank to Safety injection Pump A - Criteria ,

Calc. (1 - 10), Revision 0 - '

ECCS-10 Residual Heat Removal Sump A to Safety injection Pump A Suction - l

Mode F, Revision 0

1

ECCS-11 Residual Heat Removal Sump A to Safety injection Pump B Suction - 1

Mode F, Revision O j

l

ECCS-17 Maximum Head Loss from Refueling Water Storage Tank to Either

Centrifugal Charging Pump During injection Phase of SIS, Revision O l

I

ECCS-32 Containment Sump "B" to Safety injection Pump "B" Inlet, Mode E,

Revision O

ECCS-36 Refueling Water Storage Tank to Safety injection Pump "B" Suction

Mode A, Revision O

ECCS-47 Safety injection Pumps Net Positive Suction Head from Refueling

Water Storage Tank, Revision O

EF-35 ESW Pump Head Requirement, Revision 2

EJ-29 Residual Heat Removal- Flow Orifice Sizing, Revision O

EJ-30 Residual Heat Removal Pumps A&B Net Positive Suction Head,

Revision 1

EJ-35 Residual Heat Removal Pump Minimum Flow Recirculation Line Orifice

Sizing, Revision 0

EJ-37 Residual Heat Removal Cold and Hot Leg Recirculation Orifices,

Revision O

!

EJ-38 Containment Recirculation Sump Screen, Revision O

EJ-40 Containment Recirculation Sump Screen Fluid Velocity, Revision O j

EJ-M-001 Verification of Relief Valve Capacity for Valves EJ8708A&B,

Revision O

EJ-M-017 Potential Susceptibility for Pressure Locking of Motor-operated Valves

EJHV8813A&B, Revision 2

8

. . _ . - . - - - - - . - . . - .. - - -. _ . . _ . . .. . . . - _ . - - - - -

.

.

EJ M-019 Sizing of Expansion Pipe for Valves EJHV8811 A&B for Pressure

Locking Concerns, Revision 1

EJ-MH-OO1 Heat Transfer for the Evaluation of Thermal Binding and/or Pressure

Locking of Valves EJ-HV8716A&B, Revision O

EJ S-OO3 Min. Wall Thickness Evaluation, Revision 1

1 -HBC-W Essential Service Water Discharge Piping Design Pressure and

Minimum Wall Thickness Determination, Revision 1

IMS-01 Missiles, Revision O

PB-01 Total Pipe Break Summary, Revision 1

BN-20 Refueling Water Storage Tank Level Set-Points, Revision 1

Modifications

Number Title

03377 Seismic Reanalyr.is of Refue! Water Tank, Revision O

03838 EF/EA Cross Tie Piping Modification, Revision O

Temporary Modification Order i

Number Title

96-018-EJ Installation of Pressure Gauge Downstream of Valve HV8840

96-024-BB Eliminate Nuisance Alarm of annunciator D074, Revision 2

i

'

96-038-FP Replace Plant Diesel Fire Pump with Temporary Pump While Fire Pump is

Repaired, Revision 1

96-040-SE Eliminate inadvertent alarm of Control Room Annunciators 828 and 83C,

Revision O

96-020-AB Install Temperature Monitoring Equipment on the Main Steam Isolation Valve

Accumulators, Revision O

96-021-BB Protect Vessel Hew # Seismic Support Plate from Excessive Leakage from the

Vessel Head Vent h..es, Revision O 'l

i

!

9

l

1

.-

o

Self Assessment Reports

Number Title

95-056 Auxiliary Feedwater System

95-039 System Engineering Self Assessment

96-025 System Engineering Self Assessment Effectiveaess Follow-Up

96-033 Licensee Event Report Program

Drawings

Number Title

M-12BB01 P&lD Reactor Coolant System, Revision 15

M 12BG03 P&lD Chemical & Volume Control System, Revision 16

M 12BN01 P&lD Borated Refueling Water Storage System, Revision 08

i

M-12EJ01 P&lD Residual Heat Removal System, Revision 15

M-12EM01 P&lD High Pressure Coolant injection System, Revision 16

M-12EM02 P&lD High Pressure Coolant injection System, Revision 09

M-12EMO3 P&lD High Pressure Coolant injection System Test Line, Revision 00

Reportability Evaluation Request Form I

Number Title j

i

96-035 Mechanical Position Stops on BG Valves, dated October 23,1996  !

!

Procedures

.

Number Title

28D-001 Self Assessment Process, Revision 2

05-004 Specifications, Revision 1

05-003 Design Document Change Notice, Revision 1

10

L

.

0

05C-002 Engineering Evaluation Requests, Revision 0

05 002 Dispositions and Change Packages, Revision 2

05-001 Change Package Planning and Implementation, Revision 2

211-001 Temporary Modifications, Revision 1

AP23L-001 Lake Water Systems Corrosion and Fouling Mitigation Programs,

Revision 0

SYS EF-205 ESW/ Circ Water Cold Weather Operations, Revision 1

STS EF-100A ES'N System inservice Pump A and ESW A/ Service Water Cross

Connect Valve Test, Revision 17

STS EF 100B ESW System inservice Pump B and ESW B/ Service Water Cross

Connect Valve Test, Revision 18

STS EF-001 Essential Service Water Valve Check, Revision 7

STS IC-917 Analog Channel Operation Test Essential Service Water To Air

Compressor Isolation, Revision 5

STS IC-602A Slave Relay Test K602 Train A Safety injection, Revision 8

STS IC-603A Slave Relay Test K603 Train A Safety injection, Revision 14

STS IC-608A Slave Relay Test K608 Train A Safety injection, Revision 11

STS IC-609A Slave Relay Test K609 Train A Safety injection, Revision 10

STS IC-927 ESW to Air Compressor High DP isolation, Revision 3

STS IC-918 Channel Calibration Essential Service Water to Air Compressor

Isolation, Revision 4

STS AL-005 Auxiliary feedwater Auto Pump Start and Valve Actuation, Revision

11

STS KJ-001 B Integrated D/G and Safeguards Actuation Test Train B, Revision 14

AP 14A-003 Scaffold Construction and Use, Revision 3

AP 21G-001 Control of Locked Component Status, Revision 7

STS BG-004 Chemical and Volume Control System SealInjection and Return Flow

Balance, Revision 5

11

. _ _ _ . _

.

o

STS EM-001 ECCS Throttle Valve Verification, Revision 11

MGE LT-012 SMB 000 Removal / Replacement, Revision 1

EMG ES-12 Transfer to Cold Leg Recirculation, Revision 7 j

AP 02 009 Chemistry Surveil!iance Program, Revision 2

l

STS EM-0038 ECCS (Safety injected Pump) Flow Balance, Revision 0 ,

l

STS EM-003A ECCS (Centrifugal' Char;;.ng Pump) Flow Balance, Revision 0 l

l

STS CR-001 Shift Logs for Modes 1,2, & 3, Revision 33

STS BG 002 ECCS Valve Check and System Vent, Revision 8

STS EM-003 ECCS Flow Balance, Revision li

STS IC-902A Actuation Logic Test Train A Residual Heat Removal Suction Isolation

Valves, Revision O

STS IC-902B Actuation Logic Test Train B Residual Heat Removal, Revision 0

STS KJ-001 A Integrated D/G And Safeguards Actuation Test - Train A, Revision 14 l

STS KJ-001 B Integrated D/G And Safeguards Actuation Test - Train B, Revision 14

STS IC-740A Residual Heat Removal Switchover to Recirculation Sump Test - Train

A, Revision 9

STS IC-740B Residual Heat Removal Switchover to Recirculation Sump Test -

Train B, Revision 9

Work Requests and Work Packages

Number Title

110110 Motor-operated valve motor insulation found designated incorrectly

104812 Residual Heat Removal Pump Mechanical Seal Leakage

104898 Replacement of Relief Valve EJ8856A

106028 Residual Heat Removal Heat Exchange A Shell to Waterbox i3olting Torque

Verification

10/013 Valve EJV0053 Needs Lubrication of Stem

12

t

e.

9

107292 Screens require refurbishment due to corrosion

108111 Essential service water pump motor oil level low

109892 Running of Residual Heat Removal Pumps Below 1700 gpm for Extended

Periods of Time

109954 Inspect Pump Internals Due to Material Found in Valve ME8956C

110193 Wall thickness due to corrosion

110524 Installation of Temporary Gauge @ EJV0063 Downstream of HV8840

110622 Valve EJHCV0606 Leaks By (open)

110955 Essential service water pump operation below flow limits

110959 Residual Heat Removal Pump A Run at Flow Rates Below 1700 gpm

113208 Essential service water pump casing line leaking

I

113614 Leaking valve

113731 Valve EJ HCV-8890BWill Not Open

114876 Verify Shell to Waterbox Bolting Torque for EEJ01 A (open)

115491 Check Valve EJ8730B Not Fully Seating (open)

108477 Essential service water pump prelube tank level indicator failed

109280 Cross tie valve failed leakage test

111729 Replacement of handle on essential service water tank screen

110136 Valve actuator shaft sheared off

Performance improvement Requests

Number Title

96-1488 Drawing change not properly removed from document control file

96-0634 Limit switch rotors not set correctly

96-0500 Drawing not added to ver. dor manual

13

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o

!

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,

s

96 1617 Questions related to essential service water icing event

96-1542 Non safety-related sealant used

96-1288 Confusion in throttle valve position i

96-0659 Multiple failures of actuator shear pins  !

96-0365 Level indicator problems

96 1684 Inservice Testing stroke time failure i

96-1214 Valve exceeded maximum alert stroke time

96 1741 incorrect stroke time in procedure  !

I

981836 Corroded bolt holes on essential service water tank basket

l

96-1395 Difficulties encountered with controlotron operation

96-0737 Severe corrosion on essential service water piping and valves

96-0579 Severe corrosion on essential service water strainer backwash piping

96-2502 Valve failed stroke time test

96-1953 Fuse blocks found swapped

l

961902 Procedure conflict with updated safety analysis report

96-267b USAR Statement on ECCS Water Hammer

i

96-2729 Missing Internal Missiles Design Basis Calculs'.:on Reference j

96-2733 Questionable Use of a Pipe Whip Assumption in a Design Basis

Calculation

95 0428 Industry event evaluation regarding St Pump Runout Potential

96-2710 Mechanical Position Stops on BG Valves

94-0427 Low Flow Cavitation Limit Exceeded

i

94-0092 Limitorque Maintenance Update 92-02

94-0090 Limitorque Maintenance Update 92-02

94-0089 Limitorque Maintenance Update 92-02

14-

(-

a l

l

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95-0910 CCW Return Thermal Relief Valve Not Reseating

i

95-2901 Plant Modification Prepared Without Referring to Interim Drawing  !

Changes

96-1014 Excessive Valve Local Leak Rates

l

94-0825 Potential for inadvertent Safety injection Actuation During

i

Surveillance Testing l

1

96-0308 Generic Letter 96-01

95-0625 Mitigation and Evaluation of Pressurizer Thermal Transients Caused

by insurges and Outsurges

95-0336 Lifting of Residual Heat Removal Relief Valves EJ8856A, B & EJ8842

96-0384 Thermal Binding Issue w/ Regard to Motor-operated valve EJ

HCV8840

!

15

N