ML20126B447

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Insp Repts 50-266/92-23 & 50-301/92-23 on 921013-1122. Violation Noted.Major Areas Inspected:Corrective Actions on Previous Insp Findings,Plant Operations,Radiological Controls,Maint & Surveillance & Emergency Preparedness
ML20126B447
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 12/08/1992
From: Jackiw I
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20126B431 List:
References
50-266-92-23, 50-301-92-23, NUDOCS 9212220090
Download: ML20126B447 (17)


See also: IR 05000266/1992023

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Report No. 50-266/92023(DRP); 50-301/92023(DRP)

Docket No. 50-266; 50-301 License No. DPR-24; DPR-27

Licensee: Wisconsin Electric Company

231 West Michigan

Milwaukee, WI 53201

Facility Name: Point Beach Units 1 and 2

Inspection At: Two Rivers, Wisconsin

Dates: October 13 through November 22, 1992

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Inspectors: K. R. Jury

J. Gadzala

G. F. O'Dwyer

Approved By: / /24 * M Y 'f,2.

T.A. Jackiv,' Chief rate

Reactor Pr4jects Section 3A

Inspection Summary

Jnspection from October ~13 throuah November 22. 1992

(Recorts No. 50-266/92023(DRP): No. 50-301/92023(DRP)

Areas-Inspected: Routine, unannounced inspection by resident inspectors of

corrective actions on previous findings; plant operations; radiological-'

controls; maintenance and surveillance; emergency preparedness;. security;-

engineering and technical support; and safety assessment / quality verification.

Results: One violation of _NRC requirements was identified. An Executive

Summary Follows.

Plant Operations

On October 14, the Unit 1 " white" instrument bus inverter failed and caused a

plant transient due to loss of power to the reference- temperature circuit

(paragraph 3.a.).

Unit 2 completed a'52-day refueling outage (number 18) and was placed on line

November 18. Due to the additional steam generator tube plugging performed

during the outage, the unit is only able to achieve 98.7 percent power. At

9212220090 92120B

PDR- ADOCK 05000266

G PDR

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the end of the report period, reactor power was being maintained at 95 percent

due to reduced reactor coolant system flow rates (paragraph 3.b.).

A strength was identified in the pre-evolution briefings performed prior to

mid-loop operations, steam generator crevice flushing, and Unit 2 startup

(paragraphs 3.b.).

During Unit 2 refueling operations, effective communications were maintained

between the control room, the refueling level in containment, and spent fuel

pit personnel (paragraph 3.c.).

Maintenance / Surveillance

A violation was cited for a failuce to follow a surveillance procedure during

performance of a loss of voltage relay test on October 26, resulting in

deenergization of 4160 VAC safeguards bus 2A06 and 480 VAC safeguards bus 2B04

(paragraph 4.b.).

The gas turbine overhaul was completed and post maintenance testing was

conducted. The generator was load tested October 16, and post maintenance

testing was completed October 24 at which time G05 was declared back in

service. The temporary skid mounted diesel generator (G10) remains in place

pending completion of G05 reliability testing (paragraph 4.a.).

Emeraency Preparedness

An emergency pre,'aredness medical exercise was conducted November 20

(paragraph 5.).

Enaineerina and Technical Support

On October 20, the plant identified that one breaker affected by the Unit 2

non-safeguards equipment electrical lockout relay for 480 VAC safeguards bus

2B04 did not open as required during testing (paragraph 6.a.).

Two unit specific non-safety related 60 cell station batteries, ID-205 and

2D-205, were installed during the current outage to allow the plant to remove

non-safety loads from safety related station batteries 0-05 and D-06

(paragraph 4.b.).

Safety Assessment /0uality Verification

Outage risk assessment initiatives failed to recognize the potential impact of

performing a surveillance during reduced inventory conditions (paragraph

7.a.).

On November 20 the Nuclear Powet Otpartment announced a reorganization of the

corporate office (paragraph 7.b.).

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DETAILS

1. Persons Contacted-

G. J. Maxfield, Plant Manager

J. C. Reisenbuechler, Manager - Operations & Technical Support

T. J. Koehler, Manager - Maintenance & Engineering

N. L. Hoefert, Manager - Operations

  • J. G. Schweitzer, Manager - Maintenance

W. B. Fromm, Sr. Project Engineer - Construction & Engineering

J, A. Palmer, Manager - Instrument & Controls

  • W. J. Herrman, Manager - Technical Services

J. J. Bevelecqua, Manager - Health Physics

  • J. F. Becka, Manager - Regulatory & Staff Services
  • R. J. Chojnacki, Coordinator - Emergency Planning
  • F. A. Flentje, Administrative Specialist

Other company employees were also contacted including members of the

technical and engineering staffs, and reactor and auxiliary operators.

  • Denotes the personnel attending the management exit interview.

2. Corrective Action on Previous Inspection Findinns (92701) (92702)

a. LClosed) Violation (301/92014-01): Excessive Cooldown of the

Reactor Coolant System

On May 27, 1992, the technical specification cooldown rate of

100 F/hr (56 C/hr) was exceeded during performance of Refueling

Procedure RP-68, " Steam Generator Crevice Cleaning." The largest

cooldown over a one hour period was 141 F (78" C). Additionally,

the procedure did not prescribe adequate instructions to prevent

exceeding the maximum heatup and cooldown rates. -A civil penalty

was imposed for these violations.

An analysis was performed by the reactor vessel's vendor to

evaluate the effects of the cooldown transient. This analysis

calculated that the ratio of the crack initiation toughness to the

total stress intensity factor was 1.18. Since this ratio was

greater than 1.00, it was concluded that the structural integrity

of the vessel was assured and that acr7ptable margins of-safety

would be maintained during subsequent operations.

As corrective measures, the operators involved with this event

were disciplined and Procedure RP-6B was rewritten to provide

adequate guidance for conducting crevice cleaning. The changes

implemented for this evolution included: lowering the temperature

band at which steam generator cleaning is performed from 290-300 F

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(143-149 C) to 240-250 F (116-121 C); operating reactor coolant

i- pumps throughout the boiling period to make up for heat losses;

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maintaining component cooling water temperatures at elevated

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levels to minimize heat removal during the operation; assigning an

additional-licensed operator to plot heatup and cooldown rates and

a third senior reactor operator to supervise the entire evolution;

and precautions were added to the procedure to emphasize both the

administrative and technical specification cooldown and heatup

limits, and to clarify actions required if limits are exceeded. 1

Additionally, the licensee effectively implemented applicable

portions of procedure PBNP 3.4.19, " Infrequently Performed Tests

or Evolutions"'(see paragraph 3.b. for additional details).

The inspector reviewed the revised procedure _and observed steam

generator crevice cleaning performance utilizing the revised

process on November 13, during the Unit 2 refueling outage. Plant

management presence was noted during the evolution, reactor

coolant system temperatures were maintained within administrative

limits, and the evolution was strictly controlled. Further

concerns were not identified and this item is closed,

b. (Closed) Violation (301/92014-02): Deprivation of Required Decay

Heat Removal Capability

On November 10, 1991, all residual heat removal and reactor

coolant loops were secured while fuel was in the core and reactor '

coolant temperature was between 140 F and 350 F, contrary to

technical specification requirements. This violation occurred ,

during steam generator crevice cleaning when the pumps were I

secured to prevent excessive cooldown of the reactor coolant

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system.

The corrective actions discussed in item 2a. encompass this

violation as well as the violation discussed above. - As such, this

item is closed.

c. (Closed) Unresolved Item (266/92015-02): Instrument Cabinet

Seismic Mounting Adequacy

On-August 18, 1992, the plant discovered that Unit I analog.

instrumentation racks were not adequately seismically mounted.-

These racks were consequently declared inoperable, requiring entry

into a three-hour limiting condition for operation (LCO) as the

configuration was outside of the TS and plant design bases. The

company requested and was granted a temporary waiver of compliance. ,

from this LC0 for a period of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> to effect repairs on the R

cabinets without requiring the unit to be subjected.to a thermal  ;

transient by shutting it down. '

-These cabinets were installed during initial plant construction

and their mounting configuration is not believed to have-changed

since that time. This condition was initially identified in late

June 1992, as part of a formal plant initiative. Plant

management's initial determination was that the existing hold down

clips were adequate to restrain the cabinets in the event of a

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safe shutdown earthquake (SSE). A detailed evaluation

subsequently determined that the clips were inadequate to restrain

the cabinets during an SSE.

The general adequacy of the licensee's seismic design was reviewed

by an NRC contractor preoperationally'as documented in Appendix D

of the NRC's Safety Evaluation of the Point Beach Nuclear Plant,

dated July 15, 1970. The review noted that some control room

cabinets were not bolted to the floor but did not identify the

seismic inadequacy of the design.

The plant's corrective action for the mounting inadequacy

consisted of bolting angle irons to the base of the cabinets on

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the two long sides of each row. The angle irons were then bolted

to the concrete floor using concrete expansion anchors. Work was

completed within the 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> allowed by the temporary waiver.

The inspectors monitored installation of the new mounting brackets

and verified implementation of compensatory measures. Further

concerns were not identified and this item is closed.

d. (Closed) Unresolved Item (266/92004-02): Loss of Normal Boration

Flow Path

On January 20 and May 9,1992, two similar blockages occurred in

the normal boration flow paths for Unit I and Unit 2 respectively.

Heat tracing circuits in a section of piping were controlling

temperature below the normal setpoints and the boric acid.in these

sections crystallized. Heat lamps were used to return the boric

acid to solution and the heat tracing thermostats-were adjusted.

Insulation was also improved on these sections of piping. The

emergency boration flow path was verified to have remained

operable in all cases.

To ensure that additional flow blockages do not go undetected, a

weekly surveillance was added to require that boration' flow paths

be physically verified by a flow check.: The inspector reviewed

the plant's corrective actions and did not have additional

concerns. This item is closed.

e. (Closed) Unresolved Item (266/92004-03): Control of Axial Flux

Difference (AFD)

On August 16, 1990, and January 20, 1992, a turbine runback caused

AFD to appear to transcend its control band. Operators were not

able to return AFD to its control band within the required 15

minute interval based on plant process computer indication, even

though control board indications showed AFD returning to its

control band within 15 minutes. The reason for the disparity is

the approximately two minute delay time inherent in the' process

computer indication due to its time weighted algorithm for this

parameter.

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To correct this problem, a modification was installed in

September 1992 to update the computer software to increase the

sample frequency for AFD so the computer indication will not

substantially lag the actual AFD value. The revised calculation,

instead of using a one-minute average of nuclect instrument

readings and updating the display once per minute, now uses

current nuclear instrument readings and updates the display once

every four seconds. The technical specification basis regarding

AFD was changed to reflect the updated operation of the process

computer. The inspector revi'wed these changes and did not have

further concerns. This item is closed.

f. (Closed) Violation (266/92004-04): Inadequate Independent

Verification

A Unit 1 turbine runback was caused on January 20, 1992, by an

elet .rician inadvertently installing a jumper across two terminals

in the wrong breaker cubicle. Activities to verify that the

jumper installation conformed to procedural requirements were not

adequately performed. The personnel involved were counselled

regarding their actions and other maintenance electricians were

informed of this event.

To prevent recurrence, the plant revised the Point Beach " Writer's

Guide for Maintenance Procedures", to implement a concurrent

verification system. Information concerning human factors issues

was also expanded. Although the procedure used during this event

was determined to have been accurate, it was deemed that

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additional information on the specific location of the terminals

to be jumpered may have prevented the improper jumpering.

Consequently, the Writer's Guide was also revised to require that

a more detailed description of jumper locations be provided. The

inspector reviewed the Writer's Guide changes and did not have

further concerns. This item is closed.

3. Plant Ooerations (71707) (60710) (93702)

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with regulatory

requirements. These activities were confirmed by direct observation,

facility tours, interviews and discussions with liceasee personnel and

management, verification of safety system status, and review of facility

records.

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l To verify equipment operability and compliance'with technical

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specifications (TS), the inspectors reviewed shift logs, Operations'

records, data' sheets, instrument traces, and records of equipment

mal functions . Through work observations and discussions with Operations

staff members, the inspectors- verified the staff was knowledgeable of

plant conditions, responded promptly and properly to alarms, adhered to

procedures and applicable administrative controls, was cognizant of in

progress surveillance and maintenance activities, and was aware of

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inoperable equipment status. The inspectors performed channel

verifications and reviewed component status and safety related

parameters to verify conformance with TS. Shift char.ges were observed,

verifying that system status continuity was maintained and that proper i

control room staffing existed. Access to the control room was

restricted and operations personnel carried out their assigned duties in.

an effective manner. The inspectors noted professionalism in most

facets of control room operation.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment, and to

verify that radiological controls, fire protection controls, physical

protection controls, and equipment tag out procedures were properly

implemented,

a. Unit 1 Operational Sta.tg

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l The unit continued to operate at full power with the exception of

l power being briefly reduced to 75 percent on October 24 as a

l precautionary measure during installation of the new swing battery

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into the DC distribution system.

! On October 14, the " white" instrument bus inverter, IDYO3, failed.

This initiated a plant transient due to loss of power to the

reference temperature circuit, which caused control rods to drive

, in. Control operators promptly identified the cause of the

transient and responded by taking manual control of control rods

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and shifting " white" instrument busses to the swing inverter,

j DYOC. Transferring the affected bus to the swing inverter

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restored' instrument power and allowed operators to restore control

c systems to normal alignment. The plant is in the process of

installing automatic bus transfer devices to prevent inverter

failures from leading to major plant transients. The inspector

discussed this event with plant personnel and did not have further

Concerns.

! b. Unit 2 Operational Status

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The unit completed a 52-day refueling outage (number 18),

achievirq criticality on November 16. It was placed on line

November 18 and reached 98.7 percent power hvember 21. Due to

the additional steam generator tube plugging performed during the

outage the unit was only able to achieve 98.7 percent power with

all four turbine governor valves fully opened and Tavg at the

midpoint of the normal operating band. Equivalent tube plugging

levels for the Unit 2 steam generators were 12.9 percent for the A

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steam generator and 13.0 percent for the B steam generator. The-

l tube plugging also affected total reactor coolant system flow

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rate, which was determined to be 181,873 gpm at 95 percent power.

This is only 73 gpm above the minimum flow allowed by technical

specifications at rated power. Therefore power-was maintained at

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to 95 percent pending completion of engineering testing and

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analysis to verify flow rates and determine the minimum allowable

flow rates and the corresp9nding operating power level.

A strength was identified in the pre-evolution briefings performed

prior to mid-loop operations, steam generator crevice flushing,

and Unit 2 startup. These briefings were performed as part of

procedure PBNP 3.4.19, " Infrequently Performed Tests or

Evol utions . " The inspectors observed the pre-evolution briefings

and noted that they were sufficiently thorough and effective in

delineating the appropriate cautions, interfaces, expected plant

response, and operator actions. '

c. Refuelina activities

Effective communications were maintained between the control room,

the refueling level in containment, and spent fuel pit personnel

whenever changes in core geometry were taking place. On the

refueling floor, housekeeping was good and excellent control was

maintained to prevent loose objects from falling into the reactor .

vessel.

4. Maintenance / Surveillance Observation (62703) (61726)

a. Maintenance

The inspectors observed safety related maintenance activities on

systems and componerts to ascertain that these activities were

conducted in accordance with TS, approved procedures, and

appropriate industry codes and standards. The inspectors

determined that these activities did not violate LCOs and that

required redundant components were operable. The inspectors

verified that required administrative, material, testing,

radiological and fire prevention controls were adhered to.

Specifically, the inspectors observed / reviewed the following

maintenance activities:

  • G05 gas turbine generator overhaul

The gas turbine overhaul was completed and post maintenance

testing was conducted. The generator was . load tested

October 16 and post maintenance testing completed October

24, at which time G05 was declared back in service.

Reliability testing to meet the station blackout rule was

then initiated, which includes twice per week starting and

loading of G05 until attainment of 95 percent reliability

can be demonstrated. The licensee's acceptance test program

consists of completion of-20 tests with two or fewer

failures as specified in Wisconsin Electric Company's letter

to the NRC dated July 23, 1992. The test program is

detailed in procedure PBNP 3.2.15, " Gas Turbine Generator

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(G-05) Reliability Program". The temporary skid mounted

diesel generator (G10) remains in place pending completion

of G05 reliability testing. See Inspection ~ Reports 50- '

266/92024; 50-301/92024 for additional details.

The plant coordinated removal of G02 from service with

restoration of the G05 gas turbine generator and completion

of reduced inventory operation on Unit 2.

  • Unplanned Maintenance Work Request (UMWR) 1559, " Replace N11

terminal strips"

Terminal Nll is associated with circuitry that ensures non-

safety related loads are shed from the safeguards buses

after a safety injection signal.

  • MWR 925497, " Disassembly of Valve 2SI-825A"

Valve 2SI-825A, the refueling water storage tank (RWST)

outlet valve to the safety injection pumps, was disassembled

to allow insertion of a camera to boroscopically inspect the

Unit 2 common suction line between this valve and the RWST.

During insertion or withdrawal, the camera and its cabling

were not rotated to insure that all 360 degrees of the -

piping walls were being inspected. The inspectors discussed

this concern with the licensee and they confirmed the

boroscoping of this piping section was not adequate.

  • RMP 153 (Revision 2), SI-853A Check Valve Inspection, Unit 2

RMP 161 (Revision 2), SI-853C Check Valve Inspection, Unit 2-

This procedure was performed to identify and correct the

cause of these Event-V valves failing leak testing. A mock-

up was built to provide maintenance technicians with

familiarity in valve-internals repair. Repairs were

coordinated and conducted well, resulting in all affected

valves passing subsequent leak tests,

b. Surveillt.nce

The inspectors observed certain safety related surveillance

activities on systems and' components to ascertain-that these

activities were conducted in accordance with license requirements.

For the surveillance test procedures listed below, the inspectors

determined that precautions and 1.COs were adhered to, the required

administrative approvals and tag-outs were obtained prior to test-

initiation, testing was accomplished by qualified personnel in

acccrdance with an approved test procedure, test instrumentation

was properly calibrated, the tests were completed at the required

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frequency, and that the tests conformed to TS requirements. Upon

test completion, the inspectors verified the recorded test data

was complete, accurate, and met TS requirements; test

discrepancies were properly documented and rectified; and that the

systems were properly returned to- service.

Specifically, the inspectors witnessed / reviewed selected portions

of the following test activities:

  • RMP 74 (Revision 4) B Train Degraded and Loss of Voltage

Relay Test, Unit 2 (Monthly)_

During performance of this test on October 26, a maintenance

electrician did not open an isolation knife switch as

required by the procedure prior to depressir.g the relay test

button. This caused an undervoltage signal to be _

transmitted to 4160 VAC safeguards bus 2A06 and consequent ,

deenergization of that bus. The 480 VAC~ safeguards

bus 2B04, which is powered by bus 2A06, was also

deenergized. Emergency diesel generator G02 started as

required and energized bus 2A06.

RMP 74, step 3.2.1, directs that the knife switch cover be

removed, +he knife switch be opened, and a test point cover

be remov A caution statement preceding this step warns

that testing with the knife switch closed will trip the

associated bus power supply. Additionally, a similar

warning is printed adjacent to the relay test push button.

At this step, the electrician performing the test decided to

assist his helper by removing one cover while the helper

removed the other one. The electrician then initialed for

completion of that step without realizing.that the knife

switch had not been opened. This is a violation of

Technical Specification 15.6.8, which requires that=the

plant be operated and maintained in;accordance with approved

procedures (301/92023-01). Specific corrective actions--

regarding this violation had not_ been delineated by the end

of this inspection.

Unit 2 was in a reduced inventory condition at the time and

the 2P10B residual heat removal (RHR) pump was supplying

cooling water flow. Deenergization of bus 2004_resulted in

loss of power to this pump. Control operators _ responded by

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starting the 2P10A RHR pump and restoring cooling water flow

within one minute. After determining the cause of the-

safeguards bus loss, operators restored the electrical line-

up to normal and secured the emergency diesel. Additional

details surrounding this event are described in LER 92007

and paragraph 7.a.

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  • RMP 203 (Revision 0) Station Battery 1(2)D-205

Performance Test

Station batteries10-205 and 20-205 are unit specific ne -

safety related 60 cell batteries that were installed i

the current outage. This allowed the plant to remove nu,

safety loads such as the main turbine emergency lube oil

pumps from safety related station batteries D-05 and D-06.

Reducing the loading profile on D-05 and D-06 increases

their design margin and thereby helps extend the life of the

station batteries to 20 years per IEEE Standard 485-1983,

"IEEE Recommended Practice for Sizing Large Lead Storage

Batteries for Generating Stations and Substations".

Reducing the loading profile on D-05 and D-06 is also

expected to obviate the need for battery service testing.

The plant's calculations show that performance discharge

tests alone will completely envelope the w)rst case duty

cycles for these batteries once the emergency lube oil pumps

have been removed from them. IEEE Standard 450, section

i.2, allows a performance test to be used in lieu of a

st. ~ ice test when the performance test envelopes the service

test. Wisconsin Electric committed to install non-safety

batteries by December 31, 1992, in their letter to the NRC

dated September 11, 1992.

  • Post modification stroke testing of Unit 2 main steam

isolation valves per IWP MR 91-210*A

  • ORT 3 (Revision ~'i) Safety Injection Actuation with Loss

of Engineered Safeguards AC, Unit 2

Start Voltage and Breaker Closure

This test was performed as a followup to ORT 3 (above) when

it was discovered that the G-01 emergency diesel ge.nerator

output breaker shut at a voltage of 2744 VAC. The minimum

specified voltage was 3744 VAC. One of two parallel speed

sensing relays in the output breaker closing circuit was

found to be actuating at too low an engine speed on the

diesel. The relay was adjusted and the test repeated

satisfactorily. The plant intends to temporarily increase

the periodicity of this annual test to evaluate any

potential drif t on the relay settings.

  • TS-31 (Rev 13), High and Low Head Safety Injection Check

Valve Leakage Test (Cold Shutdown): Unit 2

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  1. 5. Emeraency Preparedness (71707)

An emergency preparedness medical exercise was conducted November 20.

The scenario involved a contaminated injured man requiring transport to-

an offsite hospital. The plant appropriately declared an Unusual Event

classification for this situation. The inspectors observed drill

conduct and significant concerns were not identified.

6. Enaineerina and Technical Support (71707) (37828) (71711)

The inspectors evaluated engineering and technical support activities to

determine their involvement and support of facility operations. This-

was accomplished during the course of routine evaluation of facility

events and concerns, through direct observation of activities, and

discussions with engineering personnel,

a. Electrical Lockout Relav Incorrect 1v Wired

On October 20, the plant found that the Unit 2 non-safeguards

equipment electrical lockout relay for 480 VAC bus 2004 was in the

tripped position. This relay is designed to strip nonessential

equipment from its associated electrical bus upon receipt of a

safety injection signal, to prevent overloading the emergency

diesel generator. Since Unit 2 was in a refueling outage at the

time, most of the equipment affected by this relay was already

shutdown. The trip of the lockout relay was believed to have been

. caused by inadvertent bumping of relay 2-SI21X by plant personnel

during as-built wire tracing of the safeguards relay racks. The

plant notified the NRC of this event as required.

One breaker affected by this relay did not open as required. This

breaker supplies motor control center MCC-821. The plant's

investigation of the failure of this breaker to open revealed that

the actuation signal wire leads-from_the lockout relay to the MCC-

B21 breaker were not connected. Therefore, the lockout relay was

incapable of tripping the MCC-B21 breaker. Based on the condition

of the electrical tape covering the wire lead terminations, the

plant believes that these wires were never connected during

original plant construction.

A review of wiring drawings and_ interviews with plant personnel

familiar with original plant construction, determined that MCC-821

had not always been powered from Unit 2 bus 2B04 (B train bus).

During Unit I construction, it became necessary to energize MCC-

B21 because it contained some minor loads required for Unit 1.

Since bus 2B04 had not yet been built, MCC-B21 was connected to

Unit 1 bus 1801 (A train bus). Later, during March 1970, its

power source was transferred to breaker "28C" in Unit 2 bus 2B04,

where it remains to date.

However, initial plans were apparently to transfer MCC-821 to

breaker "35A" in Unit 2 bus 2B03 (A train bus). This was

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evidenced by several terminals on the wiring being incorrectly

identified with the "35A" breaker prefix. The lockout relay

control switch terminal strip was labeled with the same "35A"

breaker prefix, as were the wire leads attached to it. The plant

theorizes that although the modification was subsequently changed

to transfer MCC-B21 to bus 2B04 vice 2003, the drawings and

installation procedure were not adequately revised. Consequently,

the wiring between the MCC-B21 breaker and its associated lockout

relay was never connected.

This error was never discovered during testing for two reasons,

first, the breaker supplying MCC-B21 is also designed to open on

undervoltage. Second, an additional wiring error resulted in a

lockout contact for load breakers in bus 2B03, being connected to

the MCC-821 control circuit. Thus, whenever loads were stripped

from bus 2B03 on a safety injection signal, this additional wiring

connection would cause MCC-821 to strip from bus 2B04.

Testing of bus stripping functions was performed-in two phases.

In the first phase, a safety injection signal is actuated

coincident with a loss of power to the safeguards busses. Since

the breaker supplying MCC-B21 is also designed to open on

undervoltage, this breaker opened during this phase of the test on

the undervoltage signal, even though it did not receive the safety

injection signal. Because the breaker opened, the test was

considered successful. Another phase of the test is initiated by

only inserting a safety injection signal. However, both safety

injection train signals are inserted simultaneously. According to

intended design, the A train signal strips loads from 2B03 while

the B train signal strips 2B04. Although, unbeknownst to

operators, the B train signal did not strip MCC-821-from 2B04,

actuation of the lockout relay for bus 2B03 by the A train safety

injection signal, caused MCC-D21 to be shed from 2B04. The net

result was that all required loads were stripped and the test

appeared successful,

Since the purpose of the load stripping function is to protect the

emergency diesel generators (EDGs) from beirg overloaded, an

evaluation was performed on the safety significance of the

existent wiring configurations. This evaluation determined that

multiple coincident events would be required to overload an EDG.

A postulated scenario that would create such a condition would

require that- the Unit 2 B train safeguards !:usses were initially

being powered by their EDG without a prior loss of offsite power.

This prerequisite ensures that.MCC-B21 is not previously stripped

on loss of offsite power due to its undervoltage relay actuating.

If during such a condition, an actuation of safety injection

occurred where only the B train safety injection signal

functioned, MCC-B21 would not be stripped and the EDG could be

overloaded (during normal operation, MCC-B21 draws between 150 and

200 amps). The diesel would subsequently restart'and could then

be manually loaded as necessary by the operator.

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_ After this wiring discrepancy was identified, the plant removed

the extraneous wire connecting the 2B03 lockout relay with the

MCC-B21 control circuit. Wire terminations were then made up from

the 2B04 lockout relay to the MCC-B21 breaker trip contact. A

subsequent test of load stripping functions (ORT-3) was completed

satisfactorily on October 31. The inspector discussed this event

with plant management and observed testing of the load stripping

functions. This is an unresolved item 266/92023 pending a review

of the licensee's updated LER.

b. Installation and Testina of Modifications

The inspectors observed onsite activities and hardware associated

with the installation of selected plant modifications to ascertain

that modification activities are in conformance with requirements.

Selected portions of the following modifications were reviewed:

  • lWP 92-144*A, "CCW LW-63 and LW-64 Replacement to be

Performed During U2R18, Unit 2"

7. Safety Assessment /0uality Verification (40500) (90712) (92700)

a. Outa.ge Risk Assessment

During the Unit 2 refueling outage the licensee performed an

ongoing risk assessment of plant conditions (see IR 90018). As

part of this assessment, the licensee reviews scheduled and

emergent work's impact on the overall change of risk associated

with existing plant conditions. Monthly surveillance test RMP 074

was scheduled for Unit 1 on October 26. Although this test is not

required while shutdown, Unit 2's test was scheduled to coincide

with Unit 1 test performance to keep the test schedule for both

units in parallel. Unit 2 was in reduced inventory on that date,

and this test involves testing the 4160 VAC and 480 VAC safeguards

busses. Therefore, outage risk assessment would normally prohibit

test performance in this plant configuration. Due to the Unit 2

test being scheduled on an emergent basis (i.e. not identified as

a scheduled item in the initial Outage Safety Review), this

surveillance was not recognized as having adverse risk impact. As

discussed in paragraph 4.b., a personnel error during this test

resulted in a loss of one train's safeguards busses normal power

supply. The inspectors discussed this issue with management and

concluded it was an isolated occurrence. Additionally, the

licensee is reviewing emergent work controls for outage periods

with respect to risk.

b. Licensee Event Report (LER) Review

The inspectors reviewed LERs submitted to the NRC to verify that

the details were clearly reported, including accuracy of the

description and corrective action taken. The inspector determined

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whether further information was required, whether generic

implications were indicated, and whether the event warranted

onsite follow up. The following LERs were reviewed and closed:

266/92-008-00 Reactor Trip Following Closure of Main Steam

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Isolation Valve IMS-2018

This report discusses the reactor trip on October 5, 1992, caused

by inadvertent closure of IMS-2018, the Unit 1 A steam generator

main steam isolation valve, during the performance of quarterly

surveillance testing. Details are contained in Inspection Report

266/92018; 301/92018. The faulty solenoid valve was replaced and

tested satisfactorily. Both MSIVs were then tested prior to-

startup. The inspector observed the solenoid valve replacement

and selected corrective actions for the identified equipment

anomalies.

301/92-002-00 Radioactive Waste Disposal' System Component

Cooling Water Isolation Valves Outside Design

Basis

This report discusses the discovery of component cooling water

system (CCW) isolation valves LW-63 and LW-64 in a condition

outside of the plant's design basis. Valves LW-63 and LW-64 were

discovered to not be capable of providing the appropriate

interface between the Seismic Class 1 and Seismic Class III

portions of the CCW system, as specified in the Point Beach Final

Safety Analysis Report. This issue and the status of

classification of the CCW system as safety related remain

unresolved as stated in Inspection Report 266/92018; 301/92018.

Corrective action will ~ be tracked via the unresolved item.

301/92-003-00 One Train of Containment Spray Inoperable Due to

>- Foreign Material

301/92-003-01 One Train of Containment Spray Inoperable Due to

Foreign Material

This report describes an event which occurred on September 18

during performance of the containment spray system leakage test.

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The Unit 2 train A containment spray pump was rendered inoperable

due to a foreign material exclusion plug blocking the containment

spray pump suction. The plug had likely been left in the' piping

during installation of a full flow test line modification.

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Details are contained in Inspection Report 266/92018; 301/92018.

An enforcement conference was' held on this incident on November 6

and resolution of this item is pending the outcome of the

enforcement action.

301/92-004-00 Manual Reactor Trip During Hot Control Rod Drop

Testing

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This report discusses a manual trip which was initiated during

performance of Reactor Engineering Surveillance Procedure RESP

1.1, " Rod Control System: Rod Drop Testing." Details are

contained in' Inspection Report 266/92018; 301/92018. A lack of

clear communication was the principal cause of this event. Plant

management also recognized a procedural weakness _and initiated a

revision to the test procedure to insert a note alerting operators 4

to expected equipment response during the test. The inspector i

interviewed personnel involved in this test, reviewed the test

procedure, and did not have further concerns.

301/92-005-00 Steam Generator Tube Degradation

This report provides the results of the steam generator eddy

current testing performed during the most recent Unit 2 outage.

36 degraded tubes were found in the A steam generator and 49_in

the B steam generator. All of these tubes were subsequently

plugged. Growth rate of tube indications averages 4-5 percent per

year. The 800 psid leak test revealed four explosive plugs with

excessive leakage. These four explosive plugs were removed and

replaced with mechanical plugs. The inspection did not reveal

other unusual conditions in either steam generator,

c. Manaaer's Supervisory Staff Meetina

The inspector observed several sessions of the Manager's

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Supervisory Staff. Issues discussed included operability testing

of the emergency diesel generators, Quality Assurance audits of

supervisory staff meetings, technical specification change

requests, Licensee Event Reports, and safety related

classification of the component cooling water system.

d. Corocrate Manaaement Reoraanization

On November 20 the Nuclear Power Department announced a

reorganization of the corporate office. In addition to the

creation of an Assistant to the Vice: President, the following ,

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sections in the corporate office have new managers effective

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November 20, 1992: Engineering; Regulatory Services; Planning, '

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Systems and Support; and Quality Assurance. The inspectors ~

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discussed these changes with senior corporate management.

8. Exit Interview ,

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A verbal summary of preliminary findings was provided to the Wisconsin

Electric representatives denoted in Section 1 on November 23, at the

conclusion of the inspection. Written inspection material was not

provided to company personnel:during the inspection.

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The likely informational content of the inspection report with regard to-

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documents or processes reviewed during the inspection was also=

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discussed. Wisconsin Electric management did not identify any documents

or processes that were reported on as proprietary.

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