ML20236V662

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Insp Repts 50-266/98-11 & 50-301/98-11 on 980526-0706. No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20236V662
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 07/29/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20236V649 List:
References
50-266-98-11, 50-301-98-11, NUDOCS 9808040118
Download: ML20236V662 (24)


See also: IR 05000266/1998011

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U.S. NUCLEAR REGULATORY COMMISSION

REGION 111

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Docket Nos:

50-266; 50-301

Licenses Nos:

DPR-24; DPR-27

Report No:

50-266/98011(DRP); 50-301/98011(DRP)

Licensee:

Wisconsin Electric Power Company

Facility:

Point Beach Nuclear Plant, Units 1 & 2

Location:

6612 Nuclear Road

Two Rivers, WI 54241-9516

Dates:

May 26 through July 6,1998

Inspectors:

P. Louden, Resident inspector

P. Simpson, Resident inspector

M. Kunowski, Project Engineer

Approved by:

J. W. McCormick-Barger, Chief

Reactor Projects Branch 7

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EXECUTIVE SUMMARY

Point Beach Nuclear Plant, Units 1 & 2

NRC Inspection Report 50-266/98011(DRP); 50-301/98011(DRP)

This inspection included aspects of licensee n erations, engineering, maintenance, and plant

support. The report covers a 6-week inspect.on period by the resident inspectors.

Operations

Control room operators and supervisors demonstrated a safety-focused and conservative

approach to the Unit 1 reactor startup. Briefings for infrequently performed tests or

evolutions were good to outstanding, and reactor operator performance during the

approach to criticality was good with consistent three-way communications and constU

control board monitorir.g and attentiveness evident. Operators had to contend with

unnecessary challenges from secondary system components which distracted their

attention and complicated their efforts during the Unit 1 startup. (Section 01.1)

Unit 1 fuel movements were performed in a careful and deliberate manner and

distractions for fuel handling personnel from concurent activities in the containment were

kept to a minimum. (Section 01.2)

The licensee had not effectively implemented a recently developed defense-in-depth,

system maintenance planning matrix. This did not constitute a violation of NRC

requirements; however, it represented a deficiency within the production planning group.

(Section O3.1)

The inspectors discussed with station management deficiencies with scheduling an

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emergency diesel generator post-maintenance test involving the potential inappropriate

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entry into limiting conditions for opeinion for the Unit 1 Train "A" residual heat removal

system. Upon further review of this issue by station management, the testing was

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rescheduled to allow for correct plant conditions to be established for performing the test.

(Section O3.2)

A valve mispositioning event was the result of operator error in recalling the specific valve

required to be closed. The licensee identified the error and aggressively took actions to

evaluate and correct the problem. (Section 04.1)

Maintenance

Engineering personnel provided good support to the maintenance personnelinvolved in

the troubleshooting, repair, and testing of a Unit 1 "A" main steam line snubber.

Maintenance personnel adhered to applicable procedures during the repair work.

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Appropriate controls existed for foreign material exclusion and use of replacement parts.

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(Section M1.2)

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The installation of the Unit i reactor vessel head was conducted in a safe manner.

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However, a job supervisor's understanding of the requirements of Nuclear Business Unit

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Procedure 1.1.4," Procedure Use and Adherence," regarding procedural adherence was

inaccurate. (Section M1.3)

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The licensee identified and effectively corrected a problem regarding the failure to

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maintain the environmental qualification status of the containment hydrogen monitors for

both Units 1 and 2. A Non-Cited Violation was identified involving the failure to provide

an adequate procedure to maintain the EQ status of a safety-related component.

(Section M3.1)

Enaineerina

The licensee identified a calculational error in the service water system hydraulic flow

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model and subsequently implemented adequate interim administrative operational

restrictions as corrective actions. Licensee management committed to submit a

Technical Specification change request no later than July 31,1998, to address the error

in the long-term. (Section E2.1)

The licensee's procedures used during reactor startups and the approach to criticality

contained deficiencies which reflected a non-conservative approach to reactivity

management since the procedures did not incorporate well-established industry guidance

for criticality estimations when using boron dilution to achieve criticality. (Section E3.1)

A recently completed quality assurance audit of design engineering activities contained

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additional examples of previously identified concerns with the design engineering

organization. The inspectors concluded that, overall, the audit was probing and thorough

and appropriately identified design engineering deficiencies. (Section E7.1)

Plant Support

Radiological postings accurately depicted the radiological conditions in areas inspected.

Most areas were maintained free of contamination or kept to a very low contamination

level, allowing for access to areas by operators and providing good working environments

for the general outage workforce. (Section R1.1)

Health physics and emergency preparedness staff appropriately responded during a

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contaminated injured worker drill. The responding medical staff maintained a clear focus

on the health and safety of the " victim" that was not overridden by minor radiological

control concems. (Section P1.1)

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Repod Details

Summary of Plant Status

During this inspection period, Unit 2 operated at approximately 100 percent rated thermal power

and Unit 1 completed a scheduled refueling outage which began on February 14,1998. Unit 1

was made critical on June 27,1998, at 10:25 p.m. and was placed on line on June 30,1998,

at 12:26 p.m.

1. Operations

01

Conduct of Operations

01.1

Unit 1 Reactor Startup

a.

Inspection Scope (Inspection Procedures (IPs) 71707 and 71711)

The inspectors observed operations activities for the Unit 1 startup from the Cycle 24

refueling outage. The activities included the approach to criticality and subsequent power

ascension. During this inspection, the inspectors reviewed the following documents:

Operations Manual (OM) 1.1, Revision 2, " Conduct of Plant Operations"

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Reactor Engineering Surveillance Procedure (RESP) 4.1, Revision 13, " Initial

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Criticality and All Rods Out (ARO) Physics Tests"

Operations Procedure (OP) 18, Revision 32, " Reactor Startup"

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OP 1C, Revision 65, " Low Power Operation To Normal Power Operation"

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b.

Observations and Findinas

On June 27,1998, at 10:25 p.m., the Unit i reactor was made critical following the

Cycle 24 refueling outage. The inspectors observed operations activities from the

approach to criticality through power ascension to 20 percent rated thermal power.

The inspectors observed several briefings for licensee-categorized, infrequently

performed tests or evolutions. These briefings ranged in quality from generally good to

outstanding. The outstanding briefing, by a senior operations manager, contained a

review of procedural notes with an emphasis on precautions and limitations,

communication standards, roles and responsibilities of personnel, industry events and

contingency actions. In addition, during the approach to criticality briefing conducted by

reactor engineering personnel, the operations shift crew displayed an excellent

questioning attitude (see Section E3.1).

Reactor operator (RO) performance during the approach to criticality was good as

illustrated by consistent three-way communications and constant control board monitoring

and attentiveness. Command and control was generally good as reactivity changes and

startup activities were directed by a senior reactor operator (SRO) specifically dedicated

to Unit 1. Previous inspector-observed command and control weaknesses, documented

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in inspection Reports (irs) 50-266/97016(DRP); 50-301/97016(DRP) and

50-266/97020(DRP); 50-301/97020(DRP), such as a reactor engineer inappropriately

directing reactivity changes, were not evident during this reactor startup.

Several times during the Unit 1 startup, operators were challenged or startup activities

were delayed by problems with secondary system components. The "A" condensate

pump had to be removed from service when its lower motor bearing temperature

exceeded pump operating limits. The "A" feedwater pump was tagged-out because of

lube oil and casing leaks. The main generator disconnect indicator displayed an

intermediate position when the disconnect was actually closed. This later prot ed to be a

position limit switch problem. The "A" motor-driven auxiliary feedwater (AFW) pump

developed a leak in its minimum flow recirculation line. This resulted in the "A" motor-

driven AFW pump being declared inoperable. The main turbine had to be removed from

the tuming gear periodically to clean shaft lift pump oil filters because no replacement

filters were available. These equipment problems did not meet the operators

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expectations of what the plant material condition should be for a unit which had just

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completed a refueling outage.

c.

Conclusions

Control room operators and supervisors demonstrated a safety-focused and conservative

approach to the Unit 1 reactor startup. Briefings for infrequently performed tests or

evolutions were good to outstanding, and reactor operator performance during the

approach to criticality was good with consistent three-way communications and constant

control board monitoring and attentiveness evident. Operators had to contend with

unnecessary challenges from secondary system components which distracted their

attention and complicated their efforts during the Unit 1 startup.

01.2 Conduct of Unit 1 Fuel Reloadina Operations (IP 71707)

The inspectors observed Unit 1 fuel reloading activities. The inspectors noted that the

fuel movements were well-coordinated among personnelin the Unit 1 containment, at the

spent fuel pool, and in the control room. The SROs involved displayed good command

and control of the activities. Previously identified inspector concerns regarding

distractions during fuel handling operations (IR 50-266/98003(DRP);

50-301/98003(DRP), Section 01.4) did not recur. The fuel movements were performed in

a careful and deliberate manner, and distractions for fuel handling personnel from

concurrent activities in the containment were kept to a minimum.

O3

Operations Procedures and Documentation

O3.1

Defense-in-Depth Matrix Use Deficiencies

a.

Inspection Scope (IP 71707)

The inspectors reviewed the use and operator understanding of a recently developed

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equipment out-of-service matrix for safeguards, non-Technical Specification (T/S), and

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non-emergency safety features equipment.

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b.

Observations and Findinas

During a tour of the control room, the inspectors observed a " Defense-in-Depth" matrix

status board hanging on the control room wall. The inspectors noted that the matrix

contained cross-train maintenance references for safety-related, non-T/S plant

equipment. The notes section of the matrix also provided information regarding

out-of-service combinations which should be avoided. One of the notes stated that

" planned maintenance of the gas turbine shall not be undertaken if any of the emergency

diesel generators (EDGs) are out-of-service."

Plant conditions at the time consisted of the gas turbine generator (G05) being

out-of-service for maintenance and the Unit 1 Train "A" EDG being out-of-service for an

overhaul. The inspectors asked the control room supervisors about the current

configuration in reference to the statement on the matrix. Two of the supervisors were

not familiar with the matrix, and a third was aware that it had been developed but did not

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know its purpose. A condition report (CR) (98-2119) was subsequently generated

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regarding the EDG and gas turbine configuration. Based on a follow-up review of the

configuration, the licensee determined that no T/S had been violated and that the specific

note referenced was directed at dual-unit operations.

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The inspectors discussed this matter with the supervisor of the production planning group

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(PPG) whose organization was responsible for the implementation of the matrix. The

inspectors' concerns focused on the control room supervisors' lack of familiarity with the

matrix. If the matrix was not be,. $g used, it created a possible distraction in the control

room.

The PPG supervisor stated that the new Defense-in-Depth matrix had not been effectively

implemented and that operations department personnel had not received training on the

new matrix. Corrective actions to be taken in response to CR 98-2119 included training

operators and PPG work-week m nagers on the use of the Defense-in-Depth matrix.

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c.

Conclusions

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The inspectors concluded that the licensee had not effectively implemented a recently

developed defense-in-depth, system maintenance planning matrix. This did not

constitute a violation of NRC requirements; however, it represented a deficiersey within

the PPG.

03.2 Unit 2 Train "A" EDG Test Problems

a.

Inspection Scope (IP 71707)

The inspectors reviewed a planned EDG test and evaluated the appropriateness of the

licensee entering certain T/S limiting conditions for operation (LCOs) during the test.

Observations and Findinas

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On June 5,1998, while reviewing Point Beach Test Procedure (PBTP) 091, " Transient

Response of G02 Governor Following Maintenance Activity," Revision 0, a test to be

performed a few days later, the inspectors noted that the test required declaring the

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Unit 1 Train "A" residual heat removal (RHR) system out-of-sarvice. During a discussion

of the test with an RO, the inspectors questioned the planned Unit 1 decay heat removal

(DHR) configurations for the test. The RO indicated that he had raised the question

about the configuration at an earlier shift briefing but was informed that the condition was

allowable by T/S.

Based on the inspectors' understanding regarding the nature of the EDG test, it did not

appear that the testing fell under the surveillance aspects of T/S 15.3.1.A.3.b.4, which

states that when reactor coolant temperature is less than 140 Fahrenheit (F), one of the

two RHR loops may be temporarily out-of-service to meet surveillance requirements. The

inspectors discussed this matter with a senior stction manager who indicated that he

would look into the matter further.

On June 6,1998, the operations manager and the plant manager informed the inspectors

that their reviews of the matter resulted in the determination that the intent of the T/S was

to allow for required surveillance as discussed in T/S Section 15.4. The T/S was not

appropriate for use when performing post-maintenance testing. As a result, PBTP 091

was re-scheduled and performed at a later time in the outage when the steam generators

were available for DHR. This alleviated the concern with the out-of-service configuration

of the Unit 1 Train "A" RHR system.

c.

Conclusions

The inspectors identified deficiencies with scheduling an EDG post-mainteriance test

involving the potential inappropriate entry into LCOs for the Unit 1 Train "A" RHR system.

Upon further review of this issue by station management, the testing was rescheduled to

a point in the outage when plant conditions would be appropriate.

04

Operator Knowledge and Performance

04.1 Valve Mispositionino Event Durino Safety iniection (SI) Check Valve Testino

a.

Inspection Scope (IP 71707)

The inspectors reviewed the circumstances and operator responses surrounding a valve

mispositioning event which occurred during SI system check valve testing.

b.

Observations and Findinos

On June 16,1998, the operations department conducted a routine surveillance test to

determine the Unit 1 SI system check valve leak rates as required by T/S 15.4.16. Unit 1

status at the time of the test was: reactor coolant system (RCS) temperature at

approximately 160"F, RCS pressure at approximately 340 pounds per square inch gauge

(psig), the "A" reactor coolant pump in operation, and the Train "A" RHR system in

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operation in the normal DHR mode.

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The operators in the control room and in the primary auxiliary building were in the process

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of aligning the Train "B" RHR system for the check valve testing. During the performance

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of Step 4.8.2 of Technical Specification Test Procedure (TS) 30, "High and Low Head

Safety injection Check Valve Leakage Test," Revision 17, an in-plant operator, after

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reviewing the required valve position and verifications for the step, entered a

contaminated area to perform the tasks. The first valve manipulation required was to

shut the 1RH704B RHR *B" pump suction valve; however, the operator began to close

the 1RH704A RHR *A" pump suction valve. The operator heard unexpected flow

turbulence with the valve about three-quatters of the way shut and reverified with an

assisting operator, who was standing outside the contaminated area, which valve was to

be closed. The assisting operator stated that 1RH704B was the valse to be shut, and the

first operator immediately re-opened the 1RH704A valve.

During this time, the Unit 1 RO received a Train "A" RHR low flow alarm in the control

room, noted the decreasing flow, and took action to restore RHR flow and control RCS

pressure which had started to increase. Approximately 30 seconds later, RHR flow had

been restored and the RO subsequently stabilized the primary system. Operators noted

that the Train "A" flow had decreased from 1500 gallons per minute to approximately

220 gallons per minute during the valve closing. The highest RCS pressure observed

was approximately 370 psig which was below the low temperature over-pressure

protection system set point of 415 psig.

Control room supervision suspended the test while the event was investigated. The

momentary reduction in RHR Train "A" system fie v brought into question the operability of

the "A" RHR pump. An operability determination (OD) was requested to evaluate any

possible pump degradation as a result of the event. The OD concluded that the

"A" RHR pump remained operable because the lowest flow rate encountered was above

the vendor specification for minimum flow for the pump.

Based on interviews and other data evaluated by operations department corrective

actions personnel, the root cause of the event was determined to be operator error. The

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operator had read the step which called for the appropriate valve to be manipulated;

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however, the operator closed the opposite train valve. The two valves were physically

located next to each other. The licensee determined that contributing factors for the

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event involved the failure to maintain good repeat-back communications when executing

procedure steps and the failure to maintain a " continuous use" procedure "in hand" within

a contaminated area,

Corrective actions included re-emphasizing self-checking, clear repeat-back

communications, and the need for individuals working with a " continuous use" procedure

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to maintain an "in hand" copy regardless of the location of the work activity.

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The inspectors noted that the manipulation of the wrong RHR system valve involved a

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failure to follow prescribed procedures and was considered a violation of 10 CFR Part 50,

Appendix B, Criterion V, " Instructions, Procedures, and Drawings." However, this

non-repetitive, licensee-identified and corrected violation is being treated as a Non-Cited

Violation (NCV), consistent with Section Vll.B.1 of the NRC Enforcement Policy

(NCV-50-266/98011-01(DRP)).

c.

Conclusion

The inspectors concluded that the valve mispositioning was the result of operator error in

recalling the specific valve required to be closed. The inspectors determined that the

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licensee had identified the error and aggressively took actions to evaluate and correct the

problem. The resultant violation was considered an NCV.

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06

Operations Organization and Administration

06.1 Operations Department Organizational Chanoes

On June 25,1998, the licensee announced that one of the current assistant operations

superintendents would assume a new position in the engineering department. The new

assistant operations superintendent was selected from the existing duty shift

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superintendent (DSS) pool, that is, the pool of second-line supervisory SROs. The

vacancy in the DSS pool would be filled by a current duty operations supervisor, a

first-line supervisory SRO. These changes were scheduled to be effective in

mid-July 1998. The inspectors did not identify any obvious negative impact on the

operations department as a result of the changes.

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Miscellaneous Operations issues

08.1 (Closed) Violation (VIO) 50-266/96007-01(DRP): 50-301/96007-01(DRP): This violation

involved three examples of operators fainng to follow station procedures. Subsequently,

the licensee revised the subject procedures and re-emphasized standards for operator

conduct with the operations staff. Over the past year, NRC inspectors have reviewed the

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implementation of these standards, described in Operations Manual (OM) 1.1, " Conduct

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of Operations." Based on the results of this review, the inspectors concluded that

operator performance, including procedure adherence, has significantly improved (for

example, see irs 50-266/97006(DRP); 50-301/97006(DRP),50-266/97010(DRS);

50-301/97010(DRS), 50-266/97020(DRP); 50-301/97020(DRP), 50-266/97023(DRS);

50-301/97023(DRS), and 50-266/97026(DRP); 50-301/97026(DRP)).

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08.2 (Closed) VIO 50-266/96007-02(DRP): 50-301/96007-02(DRP): This violation comprised

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three examples where procedures used by operators resulted in inadequate equipment

configuration control. The individual procedures were revised to correct the configuration

control errors and, as part of a larger effort to improve the quality of procedures, the

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licensee reviewed numerous station procedures and equipment lineup checklists to

ensure that proper equipment configuration control was maintained. Tnis broader-scope

corrective action, which was discussed in Section M8.1 of IR 50-266/98009(DRP);

50-301/98009(DRP), has been effective, overall, in reducing the number of configuration

control problems.

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08.3 (Closed) VIO 50-266/96008-01(DRP): 50-301/96008-01(DRP): This violation comprised

two examples of inadequate procedures orinstructions. In one example, reactor

engineering procedures allowed reactor power to reach 3.5 percent with only one reactor

coolant pump operating. This conflicted with T/S 15.3.5-2 and 15.3.5-4 for maintaining a

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minimum number of reactor coolant temperature channels operable during power

operations. The procedures were subsequently revised and T/S 15.3.1.A.1.a was also

revised to correct a similar conflict.

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The second example involved the failure to provide licensee personnel with adequate

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instructions for performing a weekly qualitative assessment of leakage from a temporary

patch on a section of service water (SW) system pipe. After the inspectors notified the

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licensee of the failure, adequate instructions were provided to personnel. The pipe was

subsequently repaired.

II. Maintenance

M1

Conduct of Maintenance

M1.1 Observed Tests and Surveillance UP 61726)

During this inspection period, the inspectors observed all or portions of the tests and

surveillance listed below. The inspectors observed that workers involved with the

activities were following the requirements in the appropriate procedures. Operators were

attentive to their responsibilities during the activities and system / test engineers were

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actively involved in the evolutions.

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PBTP 090," Transient Response Test of G01 Governor 1-ollowing Maintenance

Adjustment," Revision 0

PBTP 091, " Adjustment and Transient Load Response Test of G02 Governor."

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Revision 0

Operations Refueling Test (ORT) 38, " Safety injection Actuation with Loss of

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Engineered Safeguards AC [ alternating current)(Train B) Unit 1," Revision 29

ORT 4, * Main Turbine Mechanical Overspeed Trip Device Unit 1," Revision 11

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The inspectors also noted that the performance of the control room operators involved

with the PBTP 091 test was excellent. The control room operators displayed consistent

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questioning attitudes, discussed upcoming steps and plant responses among each other,

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and raised questions to the SRO in charge of the test.

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M1.2 Repair of "A" Steam Generator Main Steam Line Snubber 1HS-2

a.

Inspection Scope UP 62707)

The inspectors observed maintenance activities associated with the repair of Unit 1

steam generator "A" main steam header east snubber,1HS-2.

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b.

Observations and Findinas

During snubber inspections on June 23,1998, at 11:00 a.m. with the Unit 1 RCS greater

than 400 F, the licensee identified that the hydraulic fluid reservoir for the "A" side steam

generator snubbers was overflowing. The licensee initiated CR 98-2501 to document the

condition. The overflowing reservoir supplied hydraulic fluid to a total of five snubbers,

three on the "A" steam generator and two on the "A" main steam line. Engineering

personnei evaluated the condition and recommended that all five snubbers be declared

inoperable. Operations personnel declared all five snubbers inoperable on June 23,

1998, at 6:00 p.m. Technical Specification 15.3.13.2 requires the snubbers to be

restored to an operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or an orderly shutdown be initiated. The

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licensee initiated an around-the-clock effort to determine and correct the cause of the

problem.

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The licensee discovered during troubleshooting that snubber 1HS-2 was low on hydraulic

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fluid. Maintenance personnel removed 1HS-2 for as-found testing under the control of

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Work Order 9811536. Performance testing indicated that a problem existed with the

intemal control unit portion of the snubber. From inspection of the internal control unit by

maintenance and engineering personnel, the licensee identified that a check valve had

stuck shut. The stuck check valve caused fluid to be ported back to the hydraulic fluid

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reservoir rather than to the opposite side of the snubber cylinder whenever the snubber

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piston moved, thus resulting in the overflowing of the reservoir. The licensee did not

determine a definitive root cause for the stuck closed check valve because of insufficient

conclusive evidence. The snubber was eventually repaired and re-installed and post-

maintenance testing results were satisfactory. The snubbers were then declared

operCie on June 26,1998, at 4:43 a.m.

The inspectors concluded that engineering personnel's continuous involvement in the

evaluation and repair process was an illustration of good support to the maintenance

organization. During the troubleshooting and repair phases of the activity, the inspectors

noted that maintenance personnel appropriately followed procedures. Additionally, the

inspectors noted good foreign material exclusion and material control practices were

exercised during the initial disassembly as well as during reassembly of the snubber. The

inspectors also observed appropriate implementation of quality control hold points.

c.

Conclusions

The inspectors concluded that the testing and the repair work were performed in

accordance with approved procedures. Engineering personnel provided good support to

the maintenance personnelinvolved in the troubleshooting, repair, and testing of snubber

1HS-2. Appropriate controls existed for foreign material exclusion and use of

replacement parts.

M1.3 Reactor Vessel Head Installation Activities

a.

Inspection Scope (IP 61707)

The inspectors observed the installation of the Unit i reactor vessel head en

May 30,1998.

b.

Observations and Findinas

The inspectors attended the pre-job briefing conducted for the installation of the Unit 1

reactor vessel head. Mechanical maintenance personnel performed the work which was

directed by Routine Maintenance Procedure (RMP) 9096, " Reactor Vessel Head Removal

and Installation," Revision 16. The job supervisor thoroughly discussed the various

aspects of the evolution. The job foreman presented the position assignments to each

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worker ensuring that all personnelinvolved understood their responsibilities. A health

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physics (HP) supervisor reviewed radiological controls requirements and answered

questions from the workers.

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The inspectors determined that the pre-job briefing was conducted well, overall.

However, one topic of discussion did reveal some confusion regarding procedural

adherence requirements. During the course of the procedure review, the job supervisor

stated that if steps had to be performed out-of-sequence, Nuclear Business Unit

Procedure (NP) 1.1.4, " Procedure Use and Adherence," allowed a supervisor to alter

steps with no further action. Work crew personnel questioned this position given that the

procedure was a " continuous use" procedure. The job supervisor maintained that the NP

allowed for this discretionary supervisory action. The inspectors discussed this matter

with the job supervisor following the briefing.

The inspectors subsequently discussed the procedural adherence interpretation given by

the maintenance supervisor with the maintenance managei. The maintenance manager

indicated that the supervisor was mistaken and that he would immediately ensure that all

maintenance supervisors understood the intent of NP 1.1.4 regarding this matter.

Condition Report 98-2244 was written documenting the issue.

The inspectors have previously discussed procedural adherence issues and plant staff

misunderstanding of the intent of NP 1.1.4 in IR 50-266/98006(DRP);

50-301/98006(DRP), Section M1.2. A Notice of Violation (NOV) was issued regarding

this matter. The inspectors did not identify any procedural adherence violations during

vessel head installation; however, the job supervisor's understanding of NP 1.1.4

requirements was inaccurate.

The inspectors had no concerns regarding the actual conduct of the reac'or vessel head

movement. The evolution was conducted in a careful and safety-focused manner. All

individuals involved with the evolution were observed to be following good radiological

controls practices, and the crew leader provided clear direction to the work crew.

c.

Conclusions

The inspectors concluded that the installation of the Unit i reactor vessel head was

conducted in a safe manner. However, the job supervisor's understanding of the

requirements of NP 1.1.4 regarding procedural adherence was inaccurate.

M3

Maintenance Procedures and Documentation

M3.1 Containment Hydroaen Monitor Environmental Qualification Problems

a.

Inspection Scope OP 37751)

The inspectors reviewed the circumstances surrounding the licensee's identification that

the environmental qualification (ecd requirements for the Unit 1 and Unit 2 containment

hydrogen monitors had not been followed.

b.

Observations and findinos

During a review of the need to replace the existing containment hydrogen monitors,

engineering personnelidentified that the EQ standards for the hydrogen monitors had not

been maintained. The vendor manual for the monitors specified that whenever the

connections for the hydrogen sensors were disconnected and reconnected, the terminals

12

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_

were to be coated with an epoxy-type material to provide protection from the

environment. Other than records for initial installation, the licensee could not locate any

j

documents or records that indicated the coating had been applied following

l

repair /cahbration activities,

j

Subsequently, all the hydrogen monitors for both Unit 1 and Unit 2 containments were

declared out-of-service at 1:16 p.m. on June 15,1998. A notification was made to the

NRC in accordance with 10 CFR Part 50.72(b)(2)(iii)(D) for the inoperable condition of a

safety system which prevented it from fulfilling its safety function of mitigating the

consequences of an accident. Technical Specification Table 15.3.5-5, item 10, requires

that a minimum of one hydrogen monitor be operable during power operations. Declaring

the monitors out-of-service placed Unit 2 in a 72-hour l_CO.

The licensee subsequently obtained an equivalent silicone coating material and applied

the silicone two days later. The procedure was also revised to include the vendor's

requirements for use of the coating. The licensee performed an OD to account for the

curing time of the silicone coating because the recommended curing time exceeding the

,

allowed outage time per T/S. The inspectors and technical specialists from the

I

NRC Office of Nuclear Reactor Regulation reviewed the OD and had no concerns.

The root cause of the failure to maintain the EQ of the hydrogen monitors was the

absence of a step from the routine maintenance procedure (RMP) 10.34, " Containment

Hydrogen Monitors," Revision 11, to apply the terminal coating tollowing repairs. The lack

of the terminal epoxy coating invalidated the EQ of the monitors. This non-repetitive,

licensee-identified and corrected violation of Criterion V, " Instructions, Procedures, and

Drawings," Appendix B,10 CFR Part 50, is considered an NCV (50-266/9801102(DRP);

50-301/98011-02(DRP)) consistent with Section Vll.B.1 of the NRC Enforcement Policy.

c.

Conclusions

The inspectors concluded that the licensee identified and effectively corrected a problem

regarding the failure to maintain EQ status of the containment hydrogen monitors for both

Units 1 and 2. A Non-Cited Violation was identified involving the failure to provide an

adequate procedure to maintain the EQ status of a safety-related component.

M8

Miscellaneous Maintenance issues

M8.1 (Closed) VIO 02073 from Enforcement Action (EA) 96-273: irs 50-266/96006(DRP):

50-301/96006(DRP) and 50-266/96007(DRP): 50-301/96007(DRP): This issue,

pertaining to frequently out of-calibration pressure gauges on the discharge line of the Si

pumps, was discussed in IR 50-266/96006(DRP); 50-301/96006(DRP) and considered

with other problems for escalated enforcement. On December 3,1996, an NOV was

issued for those problems (EA 96-273) and included, for the pressure gauges, a violation

(VIO 02073) of Criterion Xil, " Control of Measuring and Test Equipment," of Appendix B,

10 CFR Part 50. A civil penalty of $325,000 was imposed with the NOV. The licensee

committed to extensive corret,'ve actions in its response to the NOV in a letter dated

January 31,1997. For the pressure gauge issue, these actions included the replacement

of the local-readout analog gauges with more accurate and reliable remote

instrumentation. The licensee eventually installed Foxboro flow transmitters near the

pumps and digital flow indicators in the main control room. In addition, the licensee

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.

reestablished the tracking and trending of instrumentation and calibration equipment,

reemphasized with instrumentation and calibration personnel the use of the condition

reparting system for adverse calibration trends and out-of-calibration equipment, and

conducted a special review of allinstalled inservice testing program support

instrumentation. Results of reviews by the resident inspectors and by a regional

specialist (IR 50-301/98010(DRS)) indicated that the programmatic corrective actions

have been effective. During the corrent inspection, based on a discussion of the new

instrumentation with the responsible engineer and the results of a review of calibration

records, the inspectors concluded that previous problems with maintaining the SI pump

discharge pressure gauges in calibration had been corrected.

M8.2 (Closed) VIO 50-266/96008-02(DRP): 50-301/96008-02(DRP): This violation comprised

three examples of failure to folicw procedures. In one example, the licensee had

recurrent problems with maintenance work request stickers or tags not being removed

after maintenance was completed. The licensee revised NP 8.1.1, "Werk Order

Processing," to clarify requirements and expectations for the use of work request stickers

l

and tags, including the provision of a step in each work order directing workers to remove

i

stickers or tags when maintenance is completed. in addition, training was provided to

plant personnel on the proper use and disposition of work request stickers and tags.

1

The second example involved the failure of plant personnel to write a CR for a washer

that had been installed without proper documentation on a casing cover of one of the

turbine-driven AFW pumps. Since identification of this problem, the licensee had

undertaken a major effort to increase worker participation in the condition reporting

process. As discussed in irs 50-266/97010(DRS); 50-301/97010(DRS) and

50-266/97023(DRS); 50-301/97023(DRS), the inspectors concluded, based on the results

of a followup review of the CR system, that this effort has been successful, overall.

During the current inspection, the inspectors noted that NP 8.1.1, " Work Order

Processing," included a requirement that the originator of a work request initiate the

appropriate CR in accordance with NP 5.3.1, " Condition Reporting System," and a

requirement that an SRO review the work order to ensure that a CR was initiated, if

I

necessary.

The third example involved several ..: stances of the failure of personnel to follow

NP 8.4.10," Exclusion of Foreign Material from Plant Components and Systems," and

maintain proper foreign material exclusion (FME) controls around the spent fuel pool.

Since these events, the licensee has revised the procedure to clarify recommendations

and requirements and has counseled personnel on the need for proper FME controls. In

addition, resident inspector observations of work activities and the results of reviews of

condition reports indicated that current FME controls were adequate,

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.

Ill. Enaineerina

E2

Engineering Support of Facilities and Equipment

E2.1

SW System Hydraulic Analysis Problem

a.

Inspection Scope (IP 37751)

The inspectors reviewed a licensee-identified error with the correct assumptions for the

isolation of some non-essential SW loads during an accident. This issue was identified

as part of an ongoing licensee review of the SW system hydraulic flow analysis model.

b.

Observations and Findinas

An error was identified in the SW hydraulic flow analysis which had taken credit for

isolating the non-essential SW loads during the injection phase of an accident. The

licensee identified that five non-essential SW loads would not be isolated. The five loads

involved service building, spent fuel pool heat exchanger, Unit 1 turbine building, Unit 2

turbine building, and water treatment sample room. The licensee determined, based on

further analysis, that some of the associated valves would close (or would be closed)

during the accident sequence; however, none of these valves would isolate all of the non-

essential SW loads. During periods when two or more SW pumps were out-of-service,

l

the failure to isolate these non-essentialloads would prevent the SW system from

maintaining adequate flow and pressure to support safe shutdown. However, if operators

were able to isolate the loads for the service building at a minimum, adequate flow and

pressure could be maintained for safe shutdown.

i

l

In response to the identJication of this problem, the licensee performed a 10 CFR 50.59

!

safety analysis and developed administrative operating limitation instructions for the

j

SW system, which were approved by the Manager's Supervisory Staff (the onsite review

committee) on May 29,1998. These instructions were intended to ensure that the

l

SW system configuration under normal plant conditions satisfied the associated

)

T/S LCOs. In addition, operator actions to iso l ate the loads were incorporated in

)

applicable emergency operating procedures.

I

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I

The licensee committed at the exit meeting held on July'9,1998, to submit a T/S change

request to the Office of Nuclear Reactor Regulation, no later than July 31,1998, to

specifically address isolation of non-essential SW loads. The submission of the

T/S change will be tracked as inspection Follow-up item 50-266/98011-03(DRP);

50-301/98011-03(DRP).

c.

Conclusions

The licensee identified a calculational error in the service water system hydraulic flow

model and subsequently implemented adequate interim administrative operational

restrictions as corrective actions. Licensee management committed to submit a T/S

l

change request no later than July 31,1998, to address the error in the long-term.

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_ _ _ _ ~

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E3

Engineering Procedures and Documentation

E3.1

Reactor Enaineerina Surveillance Procedure Deficiency Durina Unit 1 Reactor Startuo

a.

Inspection Scope (IP 71711)

The inspectors noted a deficiency with the adequacy of RESP 4.1, Revision 13, " Initial

Criticality and All Rods Out (ARO] Physics Tosts," and OP 1B, Revision 32, " Reactor

Startup," during Unit 1 approach to critical.

b.

Observations and Findinas

Prior to the Unit 1 approach to caticality on June 27,1998, reactor engineering personnel

conducted a pre-evolution brief for control room personnel. At the conclusion of the

briefing, the DSS asked the reactor engineer monitoring the startup evolution what the

upper and lower limits for the estimated critical boron concentration were and what

contingency actions should be taken if those limits were approached; the reactor was to

be made critical through dilution of the RCS with all control rods out. The reactor

engineer had not predetermined any estimated critical boron concentration limits nor any

contingency actions. This resulted in a delay while the reactor engineer and operators

determined what limits to use and then calculated the corresponding boron dilution

parameters. The limits established were the T/S limits for shutdown margin and

maintaining less than a +5"F moderator temperature coefficient. The DSS, in

consultation with the reactor engineer, then developed contingency actions to take if the

tolerances on estimated critical boron concentration were approached. Unit 1 went

critical at 1642 parts per million, very close to the estimated critical boron concentration of

1641 parts per million.

The inspectors determined that neither procedure OP 1B nor RESP 4.1 contained any

requirements to determine in advance the tolerances for estimated critical boron

concentrations or associated contingency actions should those limits be exceeded. The

licensee's procedures for estimated critical control rod position does include control rod

position limits. Also, no procedural controls existed for maintaining the RCS boron

concentration within T/S limits during the approach to criticality. The reason for diluting to

criticality following a core refueling was to approach criticality in a slow, deliberate, and

controlled manner while verifying that the new reactor core responds as predicted. Based

on a review of industry operating experience, the inspectors noted that establishing limits

for both estimated critical rod position and critical boron concentration and the bases for

.

those limits is a common industry practice. In addition, proceduralized contingencies for

premature criticality or not achieving criticality within a pre-established band are

,

l

fundamental industry expectations for reactivity management. Noteworthy, was that the

licensee had recently performed a self-assessment (S-A-98-09) of the reactor engineering

organization, specifically examining reactivity management, and failed to identify this

fundamental deficiency. The inspectors discussed these concerns with plant

management.

I

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Upon further review of the procedure deficiencies, the licensee identified that the industry

operating experience guidance had been included in previous revisions of RESP 4.1.

However, sometime in 1992, during the procedure change process, the guidance was

deleted. The inspectors discussed with station management the observation that similar

problems of this type had occurred in the past.

l

c.

Conclusions

The inspectors concluded that the licensee's procedures used during reactor startups and

the approach to criticality contained deficiencies which reflected a non-conservative

approach to reactivity management since well-established industry guidance for criticality

estimations were not incorporated into the procedure.

E7

Quality Assurance (QA)in Engineering Activities

l

E7.1

QA Audit of Desian Enaineerino Processes

The licensee's QA organization conducted a biennial audit of design engineering

processes as summarized in Audit Report A-P-98-01, dated June 16,1998. All major

design control activities / products including modifications, temporary modifications, design

,

calculations, engineering specifications, control and review of vendor documents,

l

engineering change requests, and engineering work requests were reviewed to verify

compliance with 10 CFR Par 150, Appendix B, Criterion 111.

The licensee's audit team concluded that the overall design engineering processes were

marginally effective in ensuring the accurate documentation and implementation of design

controls. The audit team initiated a total of 22 CRs. In addition, the team could not close

two 1997 QA Program Significant issues related to calculations and translation of design

information due to a lack of improvement in those areas.

The inspectors reviewed Audit Report A-P-98-01 in light of recent design engineering

performance trends and determined that the audit findings typified previously identified

concerns with the design engineering organization. The inspectors concluded that

overall, the audit was probing and thorough and appropriately identified design

engineering deficiencies.

E8

Miscellaneous Engineering issues

E8.1

(Closed) VIO 03013 from EA 96-273: irs 50-266/96006(DRP): 50-301/96006(DRP) and

50-266/96007(DRP): 50-301/96007(DRP): This issue, pertaining to the number of

SW pumps needed for accident mitigation, was discussed in IR 50-266/96006(DRP);

50-301/96006(DRP) and in Licensee Event Report 50-266/96004-01; 50-301/96004-01,

and considered with other problems fur escalated enforcement. On December 3,1996,

an NOV was issued for those problems (EA 96-273) and included, for the SW pump

issue, a violation (VIO 03013) of T/S 15.3.3.D and Criterion XVI, " Corrective Action," of

Appendix B,10 CFR Part 50. A civil penalty of $325,000 was imposed with the NOV.

,

The licensee committed to extensive corrective actions in its response to the NOV in a

{

letter dated January 31,1997. For the SW pump issue, these actions included the

17

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prompt preparation and submittal of a license amendment request to correct

T/S 15.3.3.D, which did not specify the minimum number of pumps needed for accident

mitigation.

On July 9,1997, Amendments No.174 (Unit 1) and No.178 (Unit 2) were issued

specifying the minimum number of SW pump.s required for design basis accident

mitigation. Subsequently, during continuing refinement of its SW model, the licensee

identified additional problems with the SW LCO in that the lowest functional capability or

performance levels of equipment required for safe operation of the facility was not

i

specified. This issue is discussed further in Section E2.1.

E8.2

(Closed) Inspection Follow-Up Item (IFI) 50-266/96008-05(DRP): 50-301/96008-05(DRP):

The inspectors reviewed the issues associated with reverse direction leak testing of gate

valves. The licensee identified (in September 1996) that six containment isolation valves

(three for each Unit) associated with the containment heating steam system were

inappropriately being tested in the reverse direction (the direction opposite to normal

flow). The valves were subsequently removed via a modification in which the heating

steam supply line containment penetration and the condensate return line penetration

were cut and capped. The licensee had not used the containment heating steam system

for many years. No other instances of inappropriate leak testing of gate valves were

identified. This non-repetitive, licensee-identified and corrected violation of Section Ill.C.1

of Appendix J, " Primary Reactor Containment Leakage Testing for Water-Cooled Power

Reactors," of 10 CFR Part 50, which required that the valves be tested in the direction of

normal flow, is considered a NCV (NCV 50-266/98011-04(DRP); 50-301/98011-04(DRP))

consistent with Section Vll.B.1 of the NRC Enforcement Policy.

E8.3

(Closed) VIO 50-266/95014-01(DRP): 50-301/95014-01(DRP): This violation involved

four examples where safety evaluations for spent fuel dry cask activities were not

- conducted in accordance with Station Procedure NP 10.3.1," Authorization of Changes,

Tests, and Experiments (10 CFR 50.59 and 72.48 Reviews)." As stated in the cover

letter of IR 50-266/95014(DRP); 50-301/95014(DRP), the NRC concluded that the

licensee had taken appropriate corrective actions for this violation. These actions

included a revision of the procedure to clarify expectations and requirements and better

training on the procedure and regulations for personnel who conduct safety evaluations.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1

General Comments (IP 71750)

j

During this inspection period, the inspectors conducted frequent tours of the primary

auxiliary building and Unit 1 containment. The inspectors noted that postings accurately

depicted the radiological conditions in the areas. Most areas were maintained free of

contamination or kept to a very low contamination level, allowing for access to areas by

operators and creating good working environments for the general outage workforce.

Personnel dose recorded for the Unit 1 outage was 169.7 person-rem (estimated from

plant staff records of self-reading dosimeter readings) versus a pre-outage goal of 130.0

person-rem. The main contributors to the higher than anticipated total exposure were 27

18

.

i

person-rem of exposure accrued because of emergent maintenance activities and a total

extension of the outage by 61 days.

P1

Conduct of Emergency Planning Activities

P1.1

Contaminated Injured Worker Emeraency Response Drill (IP 71750)

The inspectors observed an emergency response drill conducted on June 4,1998. The

drill targeted first responder, control room personnel, site medical, and offsite medical

response activities. The inspectors noted that health physics (HP) personnel provided

effective radiological controls at the " scene" and the " victim" was assayed for

contamination. Centrol room personnel used the appropriate emergency plan procedure

to request an ambulance from an area hospital. Medical workers responding to the

" scene" were not impeded unnecessarily by HP personnel. First responder assessment

of the " victim's" status was limited. The inspectors could not clearly ascertain if

radiological contamination concerns contributed to the first responder's actions.

However, upon the medical staffs' arrival at the " scene," a clear focus was maintained on

the health and safety of the " victim" and was not overridden by minor radiological control

concems.

V. Manaaement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management on July 9,

1998. The licensee acknowledged the findings presented. The inspectors asked the licensee

whether any materials examined during the inspection should be considered proprietary. No

proprietary information was identified.

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.

PARTIAL LIST OF PERSONS CONTACTED

,

Licensee

l

Wisconsin Electric Power Company

S. A. Patuiski, Site Vice President

M. E. Reddeman, Plant Manager

R. G. Mende, Operations Manager

W. B. Fromm, Maintenance Manager

C. R. Peterson, Director of Engineering

J. G. Schweitzer, Site Engineering Manager

R. P. Farrell, Health Physics Manager

V. M. Kaminskas, Regulatory Services and Licensing Manager

,

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INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and Preventing

Problems

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observation

I

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 71711:

Startup Following Refueling Outages

,

l

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-266/98011-01(DRP)

NCV

Failure to follow procedures, Appendix B,

Criterion V

,

50-266/98011-02(DRP)

NCV

inadequate maintenance procedure, Appendix B,

50-301/98011-02(DRP)

Criterion V

50-266/98011-03(DRP)

IFl

Licensee to submit T/S change request to address

!

50-301/98011-03(DRP)

service water model error

50-266/98011-04(DRP)

NCV

Improper leak testing of gate valves, Appendix J

50-301/98011-04(DRP)

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Closed

50-266/98011-01(DRP)

NCV

Failure to follow procedures, Appendix B,

Criterion V

50-266/98011-02(DRP)

NCV

Inadequate maintenance procedure, Appendix B,

l

50-301/98011-02(DRP)

Criterion V

50-266/96007-01(DRP)

VIO

Operator performance of shift duties

50-301/96007-01(DRP)

l

50-266/96007-02(DRP)

VIO

Configuration control

l

50-301/96007-02(DRP)

50-266/96008-01(DRP)

VIO

Leakage /SW leak patch / conditions outside TS

50-301/96008-01(DRP)

50-266/VIO 02073(DRP)

EA 96-273

Criterion Xfl, control of measuring and test

50-301/VIO 02073(DRP)

equipment

50-266/96008-02(DRP)

VIO

Failure to follow procedures

50-301/96008-02(DRP)

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50-266/VIO 03013(DRP)

EA 96-273

Criterion XVI, corrective action

50-301/VIO 03013(DRP)

50-266/98011-04(DRP)

NCV

Leak testing of gate valves, Appendix J

50-301/98011-04(DRP)

j

50 266/96008-05(DRP)

IFl

Containment isolation valve testing discrepancies

50-301/96008-05(DRP)

50-266/95014-01(DRP)

VIO

Inadequate safety evaluation /10 CFR 72.48

50-301/95014-01(DRP)

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LIST OF ACRONYMS USED IN POINT BEACH REPORTS

AC

Alternating Current

AFW

Auxiliary Feedwater

ASME

American Society of Mechanical Engineers

CFR

Code of Federal Regulations

CLB

Current Licensing Basis

CR

Condition Report

DHR

Decay Heat Removal

DRP

Division of Reactor Projects

DRS

Division of Reactor Safety

i-

DSS

Duty Shift Superintendent

EA

Enforcement Action

ECCS

Emergency Core Cooling System

EDG

Emergency Diesel Generator

EP

Emergency Planning

EQ

Environmental Qualification

F

Fahrenheit

FME

Foreign Material Exclusion

FSAR

Final Safety Analysis Report

!

HP

Health Physics

!

IFl

Inspection Follow-Up Item

!

IP

inspection Procedure

IPE

individual Plant Evaluation

IR

Inspection Report

ILRT

Integrated Leak Rate Test

IT

In-Service Test Procedure

LCO

Limiting Condition for Operation

LER

Licensee Event Report

NCV

Non-Cited Violation

,

NDE

Non-Destructive Examination

NOV

Notice of Violation

NP

Nuclear Power Business Unit Procedure

NRC

Nuclear Regulatory Commission

OD

Operability Determination

Ol

Operating Instruction

OM

Operations Manual

OOS

Out-of-Service

OP

Operations Procedure

ORT

Operations Refueling Test

PASS

Post-Accident Sampling System

PPG

Production Planning Group

i

psig

Pounds Per Square Inch Gauge

l

POD

Prompt Operability Determination

I

PBTP

Point Beach Test Procedure

!

QA

Quality Assurance

i

RCS

Reactor Coolant System

RESP

Reactor Engineering Surveillance Procedure

RHR

Residual Heat Removal

RMP

Routine Maintenance Procedure

23

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_

.

..

RO

Reactor Operator

RP

Radiation Protection

RWST

Refueling Water Storage Tank

SER

Safety Evaluation Report

I

SFP

Spent Fuel Pool

)

SI

Safety injection -

SRO

Senior Reactor Operator

SW

Service Water

TDAFW

Turbine Driven Auxiliary Feedwater

T/S

. Technical Specification

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TS

Technical Specification Test Procedure

URI

Unresolved item

VIO

Violation

VNCR

Control Room Ventilation

1

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