ML20126A029

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Monthly Operating Repts for Nov 1992 for Lgs,Units 1 & 2
ML20126A029
Person / Time
Site: Limerick  Constellation icon.png
Issue date: 11/30/1992
From: Meck K
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
Shared Package
ML20126A027 List:
References
NUDOCS 9212170196
Download: ML20126A029 (10)


Text

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3921066460 Docket No. #50-352 Attachment to Monthly Operating Report-for November 1992 LIMERICK OENERATING STATION UNIT 1 NOVEMBER 1 THROUGH NOVEMBER 30, 1992 I. NARRATIVE

SUMMARY

OF OPERATING EXPERIENCES Limerick Unit 1 began the month of November at a nominal 100%

of rated thermal power. On Thursday, November 5,. reactor power was reduced to 80% for control rod scram time testing and control valve testing. Reactor power was restored to 100%

of rated on Friday, November 6. On Friday, November 27, per the load dispatcher's request, reactor power was reduced to 88% rated thermal power due to excess generating capacity.

Reactor power was restored to 100% of rated on the same day.

Unit 1 ended this operating period at a nominal 100% of rated thermal power.

II. CHALLENGES TO MAIN STEAM SAFETY R* LIEF VALVES There were no challenges to the Main Steam Sa Nty Relief Valves during the month.

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AVERAGE DAILY UNIT POWER LEVEL DOCKET No. 50 - 352  !

UNIT LIMERICK UNIT 1  ;

4 DATE DECEMBER

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COMPANY PHILADELPHIA ELECTRIC COMPANY [

i KARL MECK REPORTS SUPERVISOR ,[

BUSINESS UNIT LIMERICK GENERATING STATION r r

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327-1200 EXTENSION 3320 '[

TELEPHONE'_(215) ____________________________

4 MONTH NOVEMBER 1992 t DAY AVERAGE DAILY POWER LEVEL DAV AVERAGE DAILY POWER LEVEL (MWE-NET) (MwE-NET) 1 .1053 17 1054 i

2 1051 18 1055 3 1043 .19 1052 9 4 4 -1040 20 1045 i

5 1001' 21 1038 6 1054 22' 1042 7 1048 23- 1041 8 1061- 24. .1050- 1 9 '10551 25 1041 {

'I 10 1052 26 1053 1 ', 1044' 27 1030 .l 12 1038 28 1049 29 1057- (>d ' j 13 1044 sg3- ~

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6 OPERATING DATA REPORT DOCKET NO. 50 - 352

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DATE DECEMBER 14 1992 COMPLETED BY PHILADELPHIA ELECTRIC COMPANY KARL MECK l REPORTS SUPERVISOR BUSINESS UNIT i >

LIMERICA GENERATING STATION . -

TELEPHONE (215) 327-12OJ EXTENSION 3320 OPERATING STATUS

1. UNIT NAMEi LIVERICK UNIT 1 NOTES: THERE WERE ONE LOAD DROP 1

, 2. REPORTING.; PERIOD: NOVEMBER. 1992-_ GREATER THAN 20% FOR SCRAM l

3. LICENSED THERMAL. POWER (MWT): 3293 TIME TESTING AND CONTROL 4 NAMEPLATE RATING (GROS $ MwE): 1138 ' VALVE TESTING.
5. DESIG" ELECTRICAL RATING (NET MWE): 1055  !

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6. MAXIMUM DEPENDABLE CAPACITV (GROSS MWE): 1092 y

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7. MAXIMUM DEPENDABLE CAPACITY-(NET MWE): 1055 l
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT. GIVE REASONS:

I 1

9. POWER LEVEL TO WHICH RESTRICTED. IF ANY (NET MWE):

!O. REASONS FOR RESTRICTIONS. IF ANY:

THIS MONTH YR-TO-DATE CUMULATIVE

, II. HOURS IN REPORTING PERIOD 720 8.040 59.880-

12. NUMB 2R OF HOURS. REACTOR WAS CRITICAL 720.0 5.496.4 46.805.2 .;

t 13. REACTOR RESERVE SHUTDOWN HOURS' O.0 0.0 0.0 - 1 5

14 HOURS GENERATOR ON-LINE 720.0 S.372.3 45.814.2

15. UNIT. RESERVE SHUTDOWN HOURS 0.0 0.0 0.0

~~ 16. GROSS THERMAL ENERGY GENERATED (MwH) 2.363.599 17.344.074' 139.332.990 t

17. GROSS ELECTRICAL ENERGY GENERATED (wwH) 781.050 5.677.590 .45.178.530 ,

. .

  • 18. NET ELECTRICAL ENERGV GENERATED (MWH) 753.658 5.461.509 43.272.964 ,

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'k 39210l664601, OPERATING DATA REPORT (CONTINUED) DOCKET NO. 50 - 352 3

DATE DECEMBER 14 1992 THIS MONTH VR-TO-DATE CUMULATIVE

' 19. UNIT SERVICE FACTOR 100.0 66.8 76.5 [

20. UNIT AVAILABILITY FACTOR 100.0 66.8 76.5 21.' UNIT CAPACITV FACTOR (USING MDC NET) 99.2 64.4 69.5

- 22. UNIT CAPACITV FACTOR (USING DER NET) 99.2 64.4 68.5

23. UNIT FORCED OUTAGE RATE. 0.0 11.1 5.4 24 SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE. AND DURATION OF EACH): y
25. IF SHUTDOWN AT END-OF REPORT PERIOD. ESTIMATED DATE OF STARTUP: [
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION): FORECAST ACHIEVED INITIAL CRITICALITY 12/19/04 12/22/84

' INITIAL ELECTRICITV MID APRIL 85 4/13/85 .;

COMMERCIAL OPERATION IST QTR 86 2/01/86

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392106M60 t> NIT S*VDOWNS AND POWER REDUCTIONS DOCKET NO. 50 - 352 l UNIT NAME LIMERICK UNIT 1-

  • DATE DECEMBER 14, 1992 REPORT MONTH NOVEMBER, 1992 COMDLETED BV PHILADELDHIA ELECTRIC COMPANY

' KARL MECM i REPORTS SUPERVISOR  ;

BUSINESS UNIT LIMERICK GENERATING STATION-TELEPHONE (215) 327-1200 EXTENSION 3320 j' METHOD OF LICENSEE ! SYSTEM COMPONENT CAUSE AND CORRECTIVE. -;

j' TYPE DURATION REASON SHUTTING DOWN -

EVENT CODE CODE ACTION TO <

NO.} DATE- (1) .v0VRS) (2) REACTOR (3) i REPORT s (4)' (5) PREVENT RECURRENCE 1 .

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32 921105 5- 000.0 e 4 N/A RB CRDRVE i LOAD WAS REDUCED 20% TO PERFORM SCRAM

TIME TESTING AND CONTROL VALVE TESTING i

33 921127-- S 000.0 H '4 N/A ] XX ZZZZZZ LOAD WAS REDUCED 12% DOE TO LOW SYSTEM DEMANO.

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,(1) (2) (3) (4) .!

F - FORCED ' REASON .

METHOD EXHIBIT G~ INSTRUCTIONS 1 - MANUAL FOR PREPARATION OF DATA- 'l.

S - SCHEDULED- A - EQUIPMENT FAILURE (EXPLAIN) .

ENTRY SHEETS FOR LICENSEE B - MAINTENANCE OR' TEST. 2 - MANUAL SCRAM.

C - REFUELING' 3 - AUTOMATIC SCRAM. EVENT REPORT (LER)

D - REGULATORV RESTRICTION . 4 - OTHER (EXPLAIN) ' FILE ( NUR E G-0161 ) :-

E'- OPERATOR TRAINING +l LICENSE EXAMINATION.

S - ADMINISTRATIVE (5)

G - OPERATIONAL ERROR (EXPLAIN)

H- OTHER(EXPLAIN) . EXHIBIT. I - SAME SOURCE -l

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3921066460 Docket No. #50-353 Attachment to Monthly Operating Report for November 1993 LIMERICK GENERATING STATION UNIT 2 NOVEMBER 1 THROUGH NOVEMBER 30, 1992 I. NARRATIVE

SUMMARY

OF OPERATING EXPERIENCES Limerick Unit 2 began the month of November in end-of-cycle coastdown at a nominal 91% of rated thermal power with core flow maximized. On Thursday, November 5, reactor power was reduced to 81% RTP to obtain a symmetric rod-pattern for Local Power Range Monitor calibrations. Reactor power was restored to 88% of rated on Monday, November 9. On Friday, November 20, at 0127 hours0.00147 days <br />0.0353 hours <br />2.099868e-4 weeks <br />4.83235e-5 months <br /> an Electro Hydraulic Control (EHC) leak was discovered on the #3 main turbine control valve. The main turbine was tripped at 0411 hours0.00476 days <br />0.114 hours <br />6.795635e-4 weeks <br />1.563855e-4 months <br /> and'the reactor remained critical on bypass valves with power a' 23% of rated. The main turbine was placed on-line at 025F hours on November 22, following repairs to the EHC piping. Reactor power was restored to 84% of rated by 1750 hours0.0203 days <br />0.486 hours <br />0.00289 weeks <br />6.65875e-4 months <br /> on November 22. Unit 2 ended this operating period at a nominal 79% of rated thermal power, in end-of-cycle coastdown with core flow maximized.

II. CHALLENGES TO MAIN STEAM SAFETY RELIEF VALVES There were no challenges to the Main Steam Safety Relief Valves during the month.

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AVERAGE' DAILY' UNIT POWER LEVEL

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---------------------- y DATE DECEM8ER 14 1992 v I COMPANY PHILADELPHIA ELECTRIC COMPANY '

KARL'MEC%

5 REPORTS SUPERVISOR BUSINESS UNIT-LIMERICK GENERATING STATION TELEPHONE (215) 327-1200 EXTENSION 3320

-MONTH NOVEMBER 1992 t

. DAY AVERAGE DAILV POWER LEVEL DAY AVERAGE DAILV POWER LEVEL (wwE-NET) (WWE-NET) 1 941 17 879 ,

a 2 935- 18 863 i-3 928 19 864 x

4 924 20 89 i

5 897 21 0 j 6 832 22 430 i 7 833 23 850 8 836 24 825 9 852 25 816 10 911 26 819 .;

11 893 27 E20 12 885 28 810 13 887. 29 812 14 886 30 805 ,

15 880 i i 16 878 e

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OPERATING DATA REDOFT 3 1 6 60 DOCKET NO. 50 - 353 DATE DECEMBER 14 1992 COMPLETED BV PHILADELPHIA E LECTR IC COMDAN'.'

KARL MECK REPORTS SUPERVISOR BUSINESS UNIT LIMERICK GENERATING STATION j- TELEPNONE !215) 327-1200 EXTENSION 3320 OPERATING STATUS

1. UNIT NAME: LIMERICK UNIT 2 NOTES: THE TURBINE GENERATOP
2. REPORTING PERIOD: NOVEMBER, 1992 wAS TAKEN OFF-LINE TO REPAIR i .

.3. LICENSED THERMAL power (MWT): 3293 1 AN EHC LEAK ON THE s3 MAIN j 4 NAMEPLATE RATING (GROSS MWE): 1138 l TURBINE CONTROL VALVE. I

5. DESIGN ELECTRICAL RATING (NET MwE): 1055 THE REACTOR REMAINED ON LINE i
6. MAXIWuu DEPENDABLE CAPACITV-(GROSS MwE): 1092 .

AT 22% THERMAL POWER.

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7. MAXIMUM DEPENDABLE CADACITV (NET MwE): 7055 i  ! ..

IF CHANGES OCCUR IN CAPACITV RATINGS (ITEMS NUMBER 3 THROUGH 7) SINCE LAST REPORT. GIVE REASONS:

8.

9. POWER LEVEL TO WHICH RESTRICTED. IF ANY (NET MwE):
10. REASONS FOR RESTRICTIONS. IF ANY:

4

! THIS MONTn YR-TO-DATE CUMULATIVE t

' It. HOURS IN REPORTING. PERIOD 720 8.040 25.392

12. NUMBER OF HOURS REACTOR WAS CRITICAL 720.0 8.040.0 22.628.3 i 13. REACTOR RESERVE SHUTDOWN HOURS 0.0' O.0 0.0 ,

. 14 HOURS GENERATOR ON-LINE 673.3 7.993.3 22.092.5

15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
16. GROSS THERMAL' ENERGY GENERATED (MwH) 1.868.602 25.327.860 70.599.256
17. GROSS ELECTRICAL ENERGV~ GENERATED (MwM) 596.990 8.385.760 23.317.396
18. NET. ELECTRICAL ENERGY GENERATED.(MwH)' 572.823 8.073.599 22.447.464

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  1. / o L .: r 0} 66460 DOCKET NO. 50 - 353 OPERATING DATA RECORT (CONTINUED)

DATE DECEMSER 14 1992 l

THIS MONTH VR-TO-DATE CUVULATIvr l 93.5 99.4 87.0

19. UNIT SERVICE FACTOR ------------ ------------ -------- - -

93.5 99,4 B7.0

20. UNIT AVAILABILITY FACTOR --- -------- - -------- - - --- ------

75.4 95.2 83.8 21, UNIT CAPACITV FACTOR (USING MDC NET) - ---------- -- --- ---- -------- ---

75.4 95.2 83.6

22. UNIT CAPACITV FACTOR (USING DER NET) - ----- ---- ------------ --- --------

6.5 0.6 4.0

23. UNIT FORCED OUTAGE RATE -- _- . -__- ----_------- ------------

24, SHUTDOWNS SCHEDULED OVER NEXT C MONTHS (TVPE. DATE. AND DURATION OF EACH):

SECOND REFUELING; 01/23/93: 60 DAYS

25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

FORECAST ACHIEVED

26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

C8/12/89 08/12/89 INITIAL CRITICALITY ---- - --- -- --- --

09/01/89 09/01/89 INITIAL ELECTRICITY -_-- --_-- -__.__---

02/07/90 01/08/90 COMMERCIAL OPERATION ---- ----- -- ------

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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50 --353


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UNIT NAME LIMERICK UNIT 2 DATE DECEMBER 14. 1992 REPORT MONTH NOVEMBER. 1992 COMPLETED BY PHILADELPHIA ELECTRIC COMPANY.

+ WARL MECK

' REPORTS SUPERVISOR BUSINESS UNIT LIMERICK GENERATING STATION TELEPHONE (215) 327-1200 EXTENSION 3320

-- - - - - - - - - - - - - - . . . - - - _ -----.- ----- ..-= ------------- ------.... ------------------ -------------------..

METHOD OF LICENSEE { SYSTEM' COMPONENT CAUSE AND CORRECTIVE TYPE DURATION REASON SHUTTING DOWN EVENT . l CODE CCDE ACTION TO

,- NO. DATE .(1) (HOURS) (2) REACTOR (3) REPORT s I (4) (5) PREVENT RECURRENCE

---= - __.--.. ...--.--..--- -- -

43 921105 S 000.0 B 4 N/A RB INSTRU LOAD WAS REDUCED 10% TO PERFORM LPRM- '

CALIBRATIONS.

I i 44 ~ 921120 F 046.7 A 4 i N/A HA l PIPEXx REACTOR POWER WAS REDUCED TO 22% AND THE TURBINE GENERATOR WAS TAKEN 04-LINE TO REPAIR

) AN EHC LEAK ON THE a3 MAIN TURBINE CONTROL g l VALVE.

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F . FORCED REASON METHOD EXHIBIT G - INSTRUCTIONS' }

FOR PREPARATION OF DATA j

- S -.SCHECULED A- EQUIPMENT "AILURE (EXPLAIN) 1 - MANUAL B - MAINTENANCE OR TEST. 2 - MANUAL SCRAM. ENTRY SHEETS FOR LICENSEE ,

C - REFUELING 3 - AUTOMATIC SCRAM. EVCNT REPORT (LER) ,

D - REGULATORY RESTRICTION 4 OTHER ( EXP L A.I N ) FILE-(NUREG-0161)--

E OPERATOR TRAINING + LICENSE' EXAMINATION

-F - ADMINISTRATIVE . ,

(5)- l 4

G - OPERATIONAL ERROR (EXPLAIN)' '

1: H - OTHER(EXPLAIN)- EXHIBIT I'- SAME SOURCE i

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