ML20091L277

From kanterella
Jump to navigation Jump to search
NPDES Noncompliance Notification:On 810228,effluent Sample Contained 75.9 Mg/L Suspended Solids.On 810110,13 & 28, Coliform Readings Were 1609 mpn/100 ml,1180 mpn/100 Ml & 1609 mpn/100 Ml,Respectively
ML20091L277
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 02/24/1981
From: Russell L
BALTIMORE GAS & ELECTRIC CO.
To: Riggin R
MARYLAND, STATE OF
Shared Package
ML20091K978 List:
References
NUDOCS 9201270342
Download: ML20091L277 (2)


Text

wgmA 1- .

.- "M '

{

(A'

~

))h:

w. ,. .

y ,

BALTIMORE G AS'AND-ELECTRIC COMP ANY

[ '

t P.O. B OX 14 7 s -

"V -

B ALTIMOR E. M A RYL AN D 212o3

..q - '

W

. NUCLE AR POWER DEPARTMENT .

' ' ; CALVERT CLIFFS NUCLE A R POWER PL ANT

. . LUSOY. M ARYL AND 20617..

q j February; 2k ,j l981 Statei of- Maryland

. Department of Natural-;.Pesources y Tuter Resources = Ad=inistration c

- Tave s . State.: Office Building -i A :  : Annapolis,7.D; 21h01

~

+ ..

" Attention: ~ ! Mr. Raymond E. Riggin s

n Re: - Maryland' State Discharge

," Pernit Nob Th-DP-0187A._

(NPDES No, MDL 0002399)-

  1. f IDearlMr. Riggins' m jp.dring the month'offJanuary, there vere four violations-in:the:sevage-

' plant operation;at the- Calvert 011f fs Nuclear Power Plsnt not previously

reported in accordance with :section IIJB.2- of!the; Maryland State Discharge Pemit No.17h-DP-0187A. Infomation. cencerning..these, violations,is pre-1 sented below:

~

-1)T ' On: January 128,lani effluent sample vas foundLto contain ,75 9 mg/1-suspended solids. This is' greater than the ' k5 - mg/1. authorized

- 2by .section iI.D. of ,the reference pemit.1 lIn addition Othe; monthly _ ' '

s 7 average suspended solidsTconcentration was calculated to be -

?[. ~

h0 5 mg/1, slightly greater ther. the:30 rg/J. pemitted.

'I 2)I On Janue.ry;10,13, and 28, the coliform readings were 1609:

^

c; -

l'% L mpn/100 m1,y t 1180 mpn/100 ml and 1609 mpn/100 ml respectively, 7 - ,

, igreate'.:Y,he.n the 'allovable 70 mpn/100 ml. ,

These even1;s were all dua to execptionally-high flows currently being experienced by the sewage treatuont' plant. Since October the Calvert-T* Cliffs Nuclear Power Plant (both Unit = 1 and ' Unit 2)!has been in a scheduled 5 , refueling / major modification outage , vP ch demands:- a- large work force popu-g'

--lationO The' euisting sevage 'treatnent plant has .not.been fully capable of

handling.this intweased flov.

t-ik-

," sp

t,s. (;
' .

P* >9201270342 920116

-PDR .ADOCK 0S000317 Wl,;<

% , , S; 3, ' , ,

PDR w m

'+ r ~rb. ,**4

,+

-. , , ~a. ,,

. . d' Mr. Raymond E. Riggin Page 2 To correct this situation, a staff engineer and two chemistry technicians are working toward a pinnt modification program designed to provide full compliance by June 1,1981. Also, larger or additional sewage treatmenc-f acility is being planned as. a major _ component of the Nuclear Pover Plant expansion.

Sincerely yours, L. B. Russel Plant Superintendent GEB:feb cc: J. A. Tiernan t

'=

i .. -i

' h .-

!1-r l-l