ML20059B185

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Forwards Results of Commitment Mgt Audit Conducted at Plant on 930419-23
ML20059B185
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 10/19/1993
From: Steven Bloom
Office of Nuclear Reactor Regulation
To: Tira Patterson
OMAHA PUBLIC POWER DISTRICT
References
TAC-M86011, NUDOCS 9310280076
Download: ML20059B185 (16)


Text

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j NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 2056E4001 4

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% . . . . + '# October 19, 1993 Docket No. 50-285 Mr. Terry L. Patterson Division Manager - Nuclear Operations Omaha Public Power District 444 South 16th Street Mall Mail Stop 8E-EP4 Omaha, Nebraska 68102-2247

Dear Mr. Patterson:

SUBJECT:

SPECIAL AUDIT OF CONTROL PROCESSES FOR COMMITMENTS AND CURRENT LICENSING BASIS, FORT CALHOUN STATION, UNIT I (TAC NO. M860ll)

I am forwarding the results of the commitment management audit conducted by the Office of Nuclear Reactor Regulation at the Fort Calhoun Station on April 19-23, 1993. As you are aware, the staff conducted audits at a cross section of reactor plants to assess the processes used by licensees for controlling commitments that affect the plants' current licensing basis.

Fort Calhoun was the third site visited by the staff, and our audit report is enclosed with this letter.

The team focused on three principal areas: (1) managing commitments made to the U.S. Nuclear Regulatory Commission (NRC), (2) reporting changes to commitments made to the NRC, and (3) maintaining and updating the final safety analysis report. In addition to reviewing the governing programs for these areas, the team reviewed the status of commitments made to the NRC in response to specific issues (in selected generic letters, bulletins, licensee event reports, and notices of violation and deviation) in order to examine the programs in actual practice.

In general, the team found that commitments affecting the plant's current licensing basis were being implemented and maintained. However, the team found that your current programs for commitment management were more thorough than the previous programs. Previous programs were effective in implementing commitments, but provided no positive controls to ensure that ongoing commit-ments were not inadvertently changed or deleted. Although the team identified several examples of inadvertently changed or deleted commitments, it found no safety-significant deficiencies. The team also found that you rely on the expertise and experience of your licensing personnel to determine the need for notifying the NRC of changes to commitments. Finally, the team found that the commitments it reviewed that affected the plant updated final safety analysis report (USAR) were captured by the USAR update process. The team did not identify any items of safety significance in its review of :ommitments made in response to the specific issues.

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F , .r Mr. Terry L. Patterson Although not a documented commitment, the team found that the plant staff had not considered the steam binding issue discussed in NRC Bulletin 85-01 when it installed its third auxiliary feedwater pump. The team believes that the issue should have been considered because the pump was installed to increase system reliability. It is my intent to work with the plant and NRC staff to resolve this issue.

The team thanks the plant staff for its candor and the excellent support it  ;

provided to the team under difficult circumstances.

If you have any questions '

or comments.concerning this report, please contact me or Eric Leeds at (301) 504-1133.

Sincerely, -

ORIGINAL SIGNED BY- l Steven D. Bloom, Project Manager Project Directorate IV-1 Office of Nuclear Reactor Regulation

Enclosure:

Commitment Management Audit of the Fort Calhoun Station, April 19-23, 1993 cc w/ enclosure:

See next page DISTRIBUTION:

Docket File NRC & Local PDRs PD4-1 Reading .

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t Mr. Terry L. Patterson -

Although not a documented commitment, the team found that the plant staff had not considered the steam binding issue discussed in NRC Bulletin 85-01 when it installed its third auxiliary feedwater pump. The team believes that the issue should have been considered because the pump was installed to increase system reliability. It is my intent to work with the plant and NRC staff to resolve this issue.

The team thanks the plant staff for its candor and the excellent support it provided to the team under difficult circumstances. If you have any questions or comments concerning this report, please contact me at (301) 504-1313 or Eric Leeds at (301) 504-1133.

Sincerely, b.

Steven D. Bloom, Project Manager Project Directorate IV-1 Office of Nuclear Reactor Regulation P

Enclosure:

Commitment Management Audit of the fort Calhoun Station, April 19-23, 1993 cc w/ enclosure:

See next page

r Mr. Terry L. Patterson

, Omaha Public Power District Fort Calhoun Station, Unit I cc:

Mr. Michael F. McBride, Esq.

LeBoeuf, Lamb, Leiby & MacRae j 1875 Connecticut Avenue, NW i Washington, D.C. 20009-5728 .

Mr. Jack Jensen, Chairman  ;

Washington County Board  ;

of Supervisors '

Blair, Nebraska 68008 Mr. Raymond P. Mullikin, Resident Inspector U.S. Nuclear Regulatory Commission Post Office Box 309  ;

Fort Calhoun, Nebraska 68023 Mr. Charles B. Brinkman, Manager Washington Nuclear Operations Combustion Engineering, Inc.

12300 Twinbrook Parkway, Suite 330 Rockville, MD 20852 Regional Administrator, Region IV ,

U.S. Nuclear Regulatory Commission 1 611 Ryan Plaza Drive, Suite 1000 Arlington, Texas 76011 Harold Borchert, Director Division of Radiological Health J Nebraska Department of Health l 301 Centennial Hall, South Post Office Box 95007 Lincoln, Nebraska 68509 ,

Mr. James W. Chase, Manager Fort Calhoun Station  !

Post Office Box 399 Fort Calhoun, Nebraska 68023

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l ENCLOSURE COMMITMENT MANAGEMENT AUDIT OF THE FORT CALHOUN STATION APRIL 19-23, 1993 .i I. Scope and Participants The purpose of the audit conducted at Fort Calhoun was to assess the effec-  ;

tiveness of the Omaha Public Power District's programs for identifying and l controlling commitments that affect the facility's current licensing. basis.- 1 The audit focused on three principal areas: (1) managing comitments made to  !

the U.S. Nuclear Regulatory Commission (NRC), (2) reporting changes to  :

commitments made to the NRC, and (3) maintaining and updating the final safety  !

analysis report (FSAR). The team reviewed the licensee's administrative i procedures involving commitment management; reporting; action tracking;  !

control of design, configuration, tests, and experiments; and others. To  :

examine the programs in actual practice, the team reviewed the status of  !

commitments made by the licensee to the NRC in response to specific issues.  ;

Five of these issues were generic in nature and are addressed in the follow-ing: .

. NUREG-0737, Item I.C.5, " Procedures for Feedback of Operating Experi-ence to Plant Staff" The remaining issues were specific to Fort Calhoun, including commitments .

made in licensee event reports (LERs) and in responses to notices of violation  !

and deviation. The team also reviewed the licensee's design basis reconstitu-  !

tion and documentation program to determine how a commitment from the program would be captured in the commitment management process.

The team relied on standard NRC inspection practices in conducting the review of specific commitments. The team performed system walkdowns,  !

reviewed documentation (including design change packages, training records, and procedures), and interviewed plant staff. A detailed review for each issue specified above is contained in the appendix.

The audit team consisted of the following NRC personnel:

  • Steven R. Stein, Team Leader I

. Steven Bloom, NRR Project Manager  ;

  • James E. Beall l

. Anthony J. D'Angelo l

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II. Findings and Conclusions The following are the team's findings and conclusions for the three major areas of focus: (1) comitment management, (2) reporting changes to comit-ments made to the NRC, and (3) updating the FSAR.

Comitment Manaaement: In general, the team found that comitments affecting the plant's current licensing basis were being implemented and maintained.

The licensee's current programs for managing new comitments were more thorough than the previous programs. Previous programs were effective in implementing comitments, but provided no positive controls to ensure that ongoing comitments were not inadvertently changed or deleted. At the time of the audit, the licensee was already aware of potential problems with histori-cal comitments and was considering possible corrective actions. Although the team identified several examples of inadvertently changed or deleted comit- i ments, it found no safety-significant deficiencies in identifying, tracking, completing, and maintaining licensee comitments for design, hardware, proce-dures, and programs.

The licensee's current requirements in its modification program were an example of the improvement in its programatic controls for commitments. The program required the design engineers to conduct a specific search for previous comitments that might affect a planned change and suggested the use of the licensing group's comitment database for the search.

A potential weakncss existed in the licensee's comitment management program I in that the program would not identify existing activities as ongoing comit-  ;

ments if the existing activities were used to satisfy a new or existing j regulatory requirement. An example of this practice was the licensee's response and actions pertaining to NRC Bulletin 85-01, " Steam Binding of ,

Auxiliary Feedwater Pumps," which is discussed in more detail in the appendix of this report. .

Reportina Chances to Commitments Made to the NRC: The licensee relied on ,

the expertise and experience of its licensing personnel to determine the need for notifying the NRC of commitment changes and indicated that the type of I notification would depend on the significance of the change. Although its  :

procedures did not specifically address the reporting to the NRC of changes to ,

commitments, procedural requirements included reporting to the licensing l organization of changes to ongoing comitments. Changes in intent or signifi-cant schedule changes would be placed on the docket by a letter. Less significant changes might be discussed with the NRC resident inspector with ,

the licensee documenting the discussion in a memo to file. The licensee  ;

provided the team with examples of letters to the NRC that documented changes 1 to several commitments, inciuding one made in an LER. l

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The team did not identify in the comitments it reviewed any significant changes that would have required notification of the NRC. It did note several j letters from the licensee that provided additional information or clarifica-  ;

tion for comitments made in response to notices of violation.  ;

Maintainina and Updatino The Updated Final Safety Analysis Report: The team found the comitments it reviewed that affected the plant's updated final safety analysis report (USAR) were captured by the USAR update process. The team's review of several plant modifications to identify changes to plant i

systems and verify incorporation of the changes in the USAR showed that all affected text descriptions and system drawings in the USAR were properly .

revised to reflect the associated modifications. The USAR revision process was documented in procedures and included updating the USAR drawings on an ad hoc basis. In accordance with the Fort Calhoun modification control program, engineers annotated revisions to plant drawings and sent the revisions to the nuclear licensing group for inclusion in the annual update of the USAR. A similar method was used for revisions of USAR text.

III. Discussion A. Commitment Manaaement In general, the team found that comitments affecting the plant's current licensing basis were being implemented and maintained. The current programs for managing new commitments were more thorough than the previous programs.

Previous programs were effective in implementing commitments, but provided no positive controls to ensure that ongoing comitments were not inadvertently changed or deleted. At the time of the audit, the licensee was already aware of potential problent with historical commitments and was considering possible corrective actions.

The team identified commitments made in response to three LERs and one generic letter that had been inadvertently changed or deleted in procedures, although none of the changes or deletions had safety significance. The team found no safety-significant deficiencies in identifying, tracking, completing, and maintaining commitments for design, hardware, procedures, and programs.

Initially, the licensee's commitment action tracking system (CATS) was devel-oped as one of the corrective actions following the 1985 NRC safety system outage modification inspections. The CATS was described in several docketed letters to the NRC and originally did not provide controls for the continued implementation of commitments by such measures as procedure notes denoting commitments. The CATS subsequently was upgraded to indicate those commitments that were ongoing. Procedure steps implementing commitments were identified as such, and the source documents were listed in the reference section of procedures. Not all historical comitments had been recaptured at the time of the audit, but the licensee was reviewing past correspondence to verify the identification of commitments and their classification as ongoing.

The licensee, in its modification process, separated its review for previous commitments from its review pursuant to 10 CFR 50.59. The licensee required, through an engineering instruction (gel-3), a review for previously made commitments during the preparation of design change packages. Instruction GEI-3 contained a step specifying that the engineer was to determine if a planned change to plant equipment and procedures might be affected by com-mitments to the NRC that were not explicitly in the USAR. It also suggested using the CATS to identify existing comitments.

The team interviewed four design engineers and found that the engineers were conducting specific searches of the licensee's records for comitments pre-viously made to the NRC, although the search methods differed among the engineers. Most of the engineers conducted their reviews for comitments by using the design-basis documents (DBDs) and did not always use the CATS, as suggested by Instruction GEI-3. The team also noted that the Fort Calhoun

DBDs were detailed documents, which maintained system history by contain-ing the description of modifications made to the system and identifying

  • docketed correspondence between the NRC and the licensee in which comitments were made that affected the system. The team concluded that the program requirement to search for comitments and the engineers' practice of relying ,

on the DBDs to identify previous comitments was a strength because of the licensee's current practice of updating the DBDs.

The team identified what it believes to be a potential weakness in the licensee's comitment management program. It found that the program would not identify as ongoing comitments existing activities, such as programs, procedures, or procedural requirements, if the existing activities were used to satisfy a new or existing regulatory requirement in a notice of violation, bulletin, or generic letter. An example of this practice was the licensee's response and actions pertaining to NRC Bulletin 85-01, " Steam Binding of Auxiliary feedwater Pumps," which is discussed in more detail in the appendix of this report.

In a related issue, the team found that the licensee had not considered the steam binding issue discussed in NRC Bulletin 85-01 when it installed its third auxiliary feedwater pump. The issue should have been considered because the pump, although not classified as safety related, was installed to increase system reliability. The NRC project manager will follow this issue with the licensee.

B. Reportina Chances to Comitments Made to the NRC Although the licensee's procedures did not specifically address the reporting to the NRC of changes made to comitments, the current Operations Department procedure for ongoing comitments included specific requirements for revising documents that implemented ongoing comitments. The requirements included informing the licensing organization of changes that affected any ongoing comitments. The licensee relied on the expertise and experience of its licensing personnel to determine the need for notifying the NRC of comitment changes and indicated that the type of notification would depend on the sig-nificance of the change. Changes in intent or significant schedule changes would be placed on the docket by a letter. Less significant changes might be discussed with the NRC resident inspector with the licensee documenting the discussion in a memo to file. The licensee provided the team with examples of letters to the NRC that documented changes to several comitments. One of the letters was a change to a comitment that had been made in an LER; the licen-see indicated that it typically changed LER comitments by means of a letter.

The team did not identify in the comitments it reviewed any significant changes that would have required notification of the NRC. It did note several letters from the licensee that provided additional information or clarifica-tion for comitments made in response to notices of violation.

C. Maintainina and Updatino the Vodated Final Safety Analysis Report The team found the comitments it reviewed that affected the plant's USAR were captured in the USAR update process. The USAR revision process was documented in procedures and included updating the USAR drawings on an ad hoc basis. In accordance with the Fort Calhoun modification control program, engineers annotated revisions to plant drawings and sent the revisions to the nuclear

licensing group for inclusion in the annual update of the USAR; a similar * '

method was used for revisions of USAR text. The licensee determined if changes to its USAR were necessary through its procedure for evaluations pursuant to 10 CFR 50.59. This procedure, N00-QP-3, required the engineer preparing a design change package to (1) be a qualified reviewer in regard to 10 CFR 50.59; (2) determine if the systems, structures, and procedures i described in the USAR would be changed by the proposed design change; and (3) prepare the necessary revisions to the affected documents. Engineering Instruction GEI-3, which controlled the preparation of DCPs, also required the engineer to evaluate the USAR text and figures that might require updating as a result of the proposed modification.

Site procedures required that major modifications be reviewed by the station modification acceptance and review team (SMART), a team of system engineers that included the engineer for the system being modified. The documented review was to assess system performance and operability, effec' on technical specifications, and adherence to 10 CFR 50.59 requirements. The SMART review '

provided another opportunity for identifying commitments that might affect the modification or system design.  ;

The team reviewed several plant modifications to identify changes to plant systems and verify incorporation of the changes in the USAR. The modifica-tions reviewed included modifications for the diverse scram system (DSS), the diesel starting air system, the instrument air system, and the hydrogen purge filter in the combustible gas control system. The team found that all affected text descriptions and system drawings in the USAR were properly revised to reflect the associated modification. The DSS was a new system that was added to the USAR, and the text descriptions adequately described the system. The team concluded that the licensee's system for updating the USAR was effective in identifying and incorporating plant changes.

APPENDIX l

SPECIFIC ISSUES REVIEWED AT FORT CALHOUN STATION l

The audit team reviewed the status of comitments made by the licensee in response to the specific issues addressed in the following to examine-the implementation of the licensee's comitment management and reporting programs:

l 10 CFR 50.62, " Requirements for Reduction of Risk From Anticipated Transients Without Scram (ATWS) Events" 4 Generic Letter 89-13 " Service Water System Problems Affecting Safety-Related Equipment"

. Generic Letter 88-14. " Instrument Air System Problems Affecting  :

Safety-Related Equipment" Bulletin 85-01, " Steam Binding of Auxiliary feedwater Pumps" [

NUREG-0737, I.C.5, " Procedures for Feedback of Operating Experience to Plant Staff" )

. Notices of Violation, 91-23, 90-02 A, 89-01 A and B, 87-02 A l

. Notices of Deviation, 90-02 A, 87-02 A l

. Licensee Event Reports, 89-18, 88-18, 88-15, 88-11, 87-22, 87-10, I 87-09, 87-08 -

The design basis reconstitution and documentation program  :

10 CFR 50.62. Anticipated Transients Without Scram The licensee added the diverse scram system (DSS) after the original plant license was issued to mitigate potential ATWS events at Fort Calhoun. The team found that the text and drawing descriptions of the DSS added to the updated safety analysis report (USAR) adequately described the system as  ;

installed in the plant. q The team verified the comitments the licensee made to the NRC in docketed correspondence for the DSS and found that the commitments had been incor- .

porated in physical plant modifications and procedures. Hardware changes to [

the plant coincided with the commitments for separate and diverse scram compo- '

nents. The DSS method was different from the reactor protection scheme for  ;

removing power from the rod control system by opening contactors and was in r agreement with licensee commitments for mitigating ATWS events.

The licensee conducted periodic testing as preventive maintenance instead of surveillance testing because the DSS was not described in the Fort Calhoun  ;

technical specifications. The team reviewed the preventive maintenance activ- i ities being conducted by the licensee and concluded the licensee was meeting its docketed commitments through its surveillance and maintenance procedures.

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l The maintenance procedures used to test the DSS incorporated the manufactur-

! ers' specific recomendations on the contactors and the molded-case circuit )

i breakers, as comitted to by the licensee in its November 16, 1984, response to a staff request for infomation. No major modifications had been made to I the DSS since the system was installed.

The team concluded that the comitments made by the licensee regarding the DSS had been maintained. ,

l Generic Letter 89-13. " Service Water System Problems Affectino Safety-Related -

fouioment" l i

The licensee documented actions taken to address GL 89-13 in its responses to the NRC dated January 26, 1990, and November 16, 1992. The team reviewed the i status of the licensee's comitments and found that all comitments were being controlled and implemented. The actions included minor modifications,  !

procedure revisions, and periodic tests. The installed codifications,  !

procedures, and tests were implemented in accordance with the documented comitments. i The Fort Calhoun systems affected by GL 89-13 were noted to have significant design margin so that flows in many of the small branch lines were not credited in accident analyses. The effect of this margin was generally to limit GL 89-13 actions to those associated with the intake structure, the major heat exchangers, and large-bore piping. The team confirmed that the '

remaining actions involving commitments had been entered into the licensee's commitment action tracking system (CATS).

Generic letter 88-14. " Instrument Air System Problems Affectino Safety-Related Eouioment" The licensee responded to GL 88-14 by letter dated February 21, 1989. It certified that it had completed all actions required by the GL in a letter dated February 14, 1991. The actions and programs for which the licensee took credit in its response to the generic letter were previous activities and comitments resulting from plant events and NRC inspections and violations for air system problems that predated the GL.

The team verified the current status of 14 actions discussed in the licensee's response to GL 88-14. These actions included program and procedure changes, updates to the USAR, and modifications to the plant's instrument air system.

The team found that the actions had been implemented and identified no significant changes. The only changes in commitments identified by the team were two ongoing commitments in procedures that the licensee had rewritten or moved within the procedures because of subsequent extensive revisions to the procedures. These changes did not materially affect the two comitments.

The team concluded that the comitments were incorporated and were being controlled.

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!WREG 0737. Item I.C.S. " Procedures for Feedback of Operatino Exoerience to Plant Staff" l

The licensee had adopted an operating experience review program that was designed to meet the comitments made by the licensee in response to the requirements of Item I.C.S. The program was well designed and implemented and ensured that all the operating experience information was analyzed to determine applicability to the plant and then distributed to the appropriate personnel by training, required readings, or any other method available to the licensee.

The team also reviewed the licensee's response to NRC Information Notice 92-36, "Intersystem LOCA [ loss-of-coolant-accident) Outside Contain-ment," to examine the licensee's implementation of its operating experience review program. The information notice had initially been reviewed by the operating experience review coordinator, who determined that further review 1 was needed. This further review was done by the Nuclear Engineering Depart-  :

ment. The licensee determined that this information notice was applicable to ,

Fort Calhoun and follow-up actions were assigned to the Training, Design Engineering, and Operations Departments. These actions were reviewed by the Plant Review Committee. The team also reviewed an evaluation by the Nuclear Safety Review Group of the program's effectiveness.

The team concluded that all actions taken in regard to the information notice were performed in accordance with the procedure for the operating experience review program.

NRC Bulletin 85-01. " Steam Bindino of Auxiliary Feedwater Pumos" In response to Bulletin 85-01, the licensee stated that it had previously initiated actions for relateo industry and NRC issues, thus satisfying the requirements of the bulletin. The licensee's actions were (I) installing surface temperature instrumentation on the discharge piping of the auxiliary feedwater (AFW) pumps with the temperatures recorded every shift and  ;

(2) establishing procedures and training to identify and mitigate steam binding and, if a pump was steam bound, to recover the pump in accordance with Procedures 01-AFW-3 and A0P-28.

The team reviewed the licensee's actions in response to the bulletin and found weaknesses in the implementation and control of the actions. In implementing the actions, the licensee did not provide an acceptance value for the temperatures being recorded, temperature values in various revisions of the procedures differed, and the two procedures were not fully consistent. l The licensee had not included the actions in the CATS. It did not r.onsider l the actions " ongoing commitments" within the scope of its commitment manage-  !

ment program because the actions were initiated before the bulletin was issued  !

and were not implemented in response to the bulletin requirements. In i addition, the licensee had not considered the applicability of Bulletin 85-01 to the third AFW pump, which although not safety related was installed because of reliability concerns.

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i The team considers the omission of the actions from the CATS as a potential weakness in the licensee's commitment management program. The NRC project .

manager will follow up with the licensee the issue of omission of consider-ation of Bulletin 85-01 for the third AFW pump.

NOV 91-23. Insufficient EDG Fuel Oil Capacity An NRC inspection report documented a noncited violation for a licensee-identified condition regarding the amount of fuel oil available to the emergency diesel generators. In its response to the inspection report, the licensee discussed its interim action plan and the enhancements of that plan it intended to use as a permanent solution. The NRC had not yet approved the permanent solution at the time of the audit. The licensee included four '

separate items in its CATS to control the enhancements of the interim plan.

The team verified the availability of equipment and the addition of emergency procedure requirements and found no significant differences. The licensee had not classified any of the commitments as ongoing because of the continuing discussions with the NRC.

NOV 90-02 A.

Dearadation of Check Valves:

NOD 90-02 A. Cable Installations Not Meetino FSAR Commitments In response to the NOV, the licensee committed to revise its procedure for the preparation of safety analyses for operations. The commitment was listed in the CATS and identified Procedure N0D-QP-22 as the affected document. The current revision of NOD-QP-22 included the associated guidance and referenced the licensee's letter in response to the NOV as the source of the commitment.

In response to the N0D, the licensee committed to conduct an analysis that would also be used as a basis for a USAR update and to revise the associated engineering instruction and construction procedure. The CATS included two commitments associated with the deviation, one of Shich referenced the eng-ineering analysis. The team verified the existence and conclusions of the analysis and the incorporation in the USAR of the recommended change. The team also verified the changes made to the engineering instruction and con-struction procedure.

NOV 89-01 A. Unreviewed Safety-Related Modifications: NOV 89-01 B. Correctiy_q Action Hot Taken The NRC had issued the first violation because the licensee had made changes to safety-related equipment, including a temporary change to both emergency diesel generators, without determining as required, that the changes did not constitute unreviewed safety questions. In its response to the NOV, the licensee committed to incorporate the temporary changes to the diesel genera-tors in an existing permanent modification. The team found that the licensee had included the NRC inspection report number as a reference document in an existing commitment in the CATS for completing the permanent modification.

The team reviewed the modification package and the emergency diesel generators ,

and concluded the commitment had been completed as stated without any changes.

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. . t The NRC had issued the second violation because the licensee had altered, through a maintenance work order, a lighting circuit that interfered with a plant modification and had not returned the lighting circuit to its original configuration. In its response to the NOV, the licensee discussed changes to  :

two site procedures, Standing Orders S0-M-101 and S0-G-21, to better control maintenance work orders and modifications. The team found that the change to S0-M-101 still existed in the procedure, although the commitment was catego-rized as closed in the CATS. The team also noted that the commitment in the CATS was linked to the NRC inspection report that closed the violation. In addition, a similar change was made to an engineering instruction and the instruction listed the NOV response letter in its references / commitments section.

The change to S0-G-21 discussed in the response letter also existed in the revision of the procedure reviewed by the team. However, no ongoing commitment existed for the associated procedural requirement. The licensee explained that no commitment existed because the procedure change discussed in the response was not made to resolve the issues in the NOV and, therefore, did not meet its definition of " ongoing commitment." The team indicated to the licensee that their definition of ongoing commitment would not identify existing activities as commitments when the existing activities were used to satisfy a new or existing regulatory requirement. The team believed this to be a potential weakness in the licensee's commitment management program.

c NOV 87-02 A. Use of Outdated Documents: N00 87-02 A. Lack of Administrative Controls for Manual isolation Valves The NRC issued the violation when several outdated procedures and operator aids were discovered in the plant. In its response to the NOV, the licensee stated it had revised two documents. Procedure 50-0-41 was changed to provide space for the shift technical advisor to record the current revision of oper-ator aids during his quarterly verification. The shift technical advisor's turnover log, FC-163, was changed to include a requirement to review daily the list of operator aids in 50-0-41 to a list of newly issued procedure revi-  !

sions. The commitment to revise the two documents was listed in the CATS and  !

appeared in the current revision of the documents, although the commitments -

were not annotated as commitments in the documents. Team discussions with a shift technical advisor indicated that the requirement was understood and was being implemented.

The NRC issued the NOD when manual isolation valves in system branch lines were found not to be administrative 1y controlled, contrary to an FSAR commit-  ;

ment. In its response to the N0D, the licensee committed to lock or seal wire  ;

the manual valves and update operating instruction checklists and piping and  ;

instrumentation diagrams (P&lDs) to indicate the required status of the i valves. The commitment to revise operating checklists and P& ids was listed in i the CATS, although the specific procedures were not listed. The team verified I the locked condition of the valves and indication of the proper status on the P& ids and in Surveillance Test OP-ST-CONT-0001, " Locked Closed Manual Contain-ment Isolation Valve Alignment Check," and concluded that the commitments had been adequately implemented.

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- Licensee Event Reports (LERs) -

The audit team reviewed the implementation of corrective action commitments contained in a sample consisting of the following LERs:

87-08 Loss of Off-Site Power 87-09 Loss of Off-Site AC Power due to Personnel Error 87-10 Valve Stroke Test Requirements 87-22 Defects in Tank Manufactured by Eaton Metal Products Corporation 88-11 Potential failure to Maintain Containment Integrity When Required 88-15 Inadvertent Start of Stand-By Component Cooling Water Pump During Breaker Testing 88-18 Failure to Conduct Surveillance Test Within Prescribed Interval 89-18 Failure to Conduct Hourly Firewatch Patrol Due to Procedural Inadequacies The sampled LERs contained commitments to a wide variety of corrective actions, including hardware modifications, procedure revisions, plant labels, performance studies, and technical reviews. The team did not identify any safety-significant deficiencies with the licensee's meeting and maintaining the commitments in the sampled LERs, although it did identify several examples of omitted commitments in three LERs.

In LER 87-09, the licensee committed to revise the associated maintenance pro-cedure, listing which fuses to pull, to prevent a repeat occurrence of the wrong fuses being pulled. The affected procedure was correctly revised but later replaced with a different procedure, which did not list the fuses.

Other corrective actions regarding LER 87-09 remained in place, including signs mounted on the electrical switchgear warning which electrical buses would be deenergized if fuses were removed. The safety significance of deleting the fuse list was mitigated by the local signs cnd the normal controls in the licensee's tagging program.

In LER 88-11, containment integrity was compromised when a Swagelok cap had not been reinstalled on a test tee following a surveillance test. The licensee committed to revise the associated surveillance test to include detailed drawings that showed all test tees. The affected procedure was cor-rectly revised but later replaced with a different_ procedure, which showed on its drawings only the test tees being manipulated. Other LER 88-11 corrective actions were still in place, which mitigated the safety significance of the  ;

deletion of the test tees from the drawing. These actions included double, '

independent verification that caps had been reinstalled during the test and a .

separate double, independent verification of all caps before requiring l containment integrity. The team confirmed that the latter verification list '

included the caps deleted from the test drawing.

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4 In LER 89-18, the licensee comitted to revise a standing order, a procedure, and two forms to require the permission of the fire protection engineer (or control room shift supervisor in the absence of the engineer) to terminate an I hourly firewatch. The affected documents were correctly revised, but were later deleted or revised extensively. The procedure and the remaining form no longer contained the requirement, and the standing order language was not com-pletely clear. However, a new companion procedure used by the security force, which makes up most of the firewatches, did contain language similar to the LER 89-18 comitment.

With the exception of the items noted above, the comitments made in the sample of LERs remained in place. These comitments, made between 1987 and 1989, were not identified as comitments in the procedures but were entered in j

the CATS. The team noted that the procedures did contain specific references  :

to other, more recent comitments such as those made in 1992 and later.

Desian Basis Reconstitution and Documentation Proaram  !

The licensee initiated the design basis reconstitution and documentation program as one of the corrective actions following the NRC safety system outage modification inspections conducted in 1985. The program reviews included safety systems, major buildings, generic issues, key nonsafety systems, and other topics. About 1700 open items were generated and ranked in six priority groups. All the items in the two highest groups had been closed.

About 700 items that were associated with safety-related systems remained open. The team noted that the licensee had procedures in place that con-trolled the evaluation of the open items for operability, reportability, and b prioritization.

The design-basis documents (DBDs) identified the performance requirements associated with the topic reviewed by the itcensee, and the DBDs were used extensively by the licensee's engineering staff. The apparent usefulness of the DBDs and the licensee's stated intention to keep the DBDs current provided good assurance that significant commitments regarding system and component performance will be maintained.

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