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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E8021999-10-0707 October 1999 CPSES Unit 1 Cycle 8 Colr ML20217G4151999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Cpses,Units 1 & 2 ML20212F7671999-09-24024 September 1999 SER Granting Relief Request C-4 Pursuant to 10CFR50.55a(g)(6)(i) for Unit 2,during First 10-year ISI Interval & Relief Requests B-15,B-16 & B-17 Pursuant to 10CFR50.55a(g)(6)(i) ML20216J5701999-09-16016 September 1999 Rev 2 to CPSES Unit 2 Cycle 5 Colr TXX-9920, Monthly Operating Repts for Aug 1999 for Cpses.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Cpses.With ML20211M2981999-08-0606 August 1999 Rev 1 to CPSES Fuel Storage Licensing Rept, CPSES Credit for Soluble Boron & Expansion of Spent Fuel Storage Capacity, Consisting of Revised Title Page and 4-1 ML20210U4081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Cpses,Units 1 & 2 ML20210D8321999-07-23023 July 1999 Safety Evaluation Accepting Relief Requests Re Use of 1998 Edition of Subsections IWE & Iwl of ASME Code for Containment Insp ML20209H7661999-07-15015 July 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Comanche Peak Steam Electric Station,Units 1 & 2 ML20209H2721999-07-0909 July 1999 2RF04 Containment ISI Summary Rept First Interval,First Period,First Outage ML20209H2631999-07-0909 July 1999 2RF04 ISI Summary Rept First Interval,Second Period,Second Outage ML20209G7501999-07-0808 July 1999 SER Finding That Licensee Individual Plant Exam of External Events Complete with Regard to Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given Design, Operation & History of Comanche Peak Steam Electric Station ML20196L0191999-07-0808 July 1999 Safety Evaluation Granting Request Relief B-6 (Rev 2),B-7 (Rev2),B-12,B-13,B-14 & C-9,pursuant to 10CFR50.55a(g)(6)(i).Technical Ltr Rept Also Encl ML20210J9391999-06-30030 June 1999 CPSES Commitment Matl Change Evaluation Rept 0003,for 970802-990630 ML20209G0801999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Cpses,Units 1 & 2 ML20196J0621999-06-29029 June 1999 Safety Evaluation Supporting Proposed Changes to Emergency Plan Re Licenses NPF-87 & NPF-89 Respectively ML20195G5141999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Comanche Peak Steam Electric Station,Units 1 & 2.With ML20216E0711999-05-21021 May 1999 1999 Graded Exercise - Comanche Peak Steam Electric Station ML20206Q0091999-05-14014 May 1999 Safety Evaluation Accepting GL 92-08, Thermo-Lag 330-1 Fire Barriers, Dtd 921217,for Comanche Peak Electric Station,Unit 1 ML20206H2061999-05-0606 May 1999 SER Accepting Exemption to App K Re Leading Edge Flowmeter for Plant,Units 1 & 2 ML20196L2241999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Cpses,Units 1 & 2 ML20205R5701999-04-14014 April 1999 Rev 6 to ER-ME-067, TU Electric Engineering Rept,Evaluation of Thermo-Lag Fire Barrier Sys ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205J7831999-04-0101 April 1999 Rev 0 to ERX-99-001, CPSES Unit 2 Cycle 5 Colr ML20205N3101999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Cpses,Units 1 & 2 ML20204H6371999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Comanche Peak Units 1 & 2 ML20205N1481999-02-28028 February 1999 Corrected Monthly Operating Rept for Feb 1999 for CPSES, Units 1 & 2 ML20203A4881999-02-0303 February 1999 Safety Evaluation Granting Requests for Relief B-3 - B-6,C-2 & C-3 for Plant,Unit 2 ML20210J9201999-02-0101 February 1999 CPSES 10CFR50.59 Evaluation Summary Rept 0008,for 970802- 990201 ML20202D0101999-01-27027 January 1999 Safety Evaluation Supporting First 10-yr Interval ISI Program Plan Requests for Relief B-9,B-10 & B-11 for CPSES, Unit 1 ML20199E9961998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Cpses,Units 1 & 2 ML20207D6091998-12-31031 December 1998 1998 Annual Operating Rept for Cpses,Units 1 & 2. with ML20197K2371998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Cpses,Units 1 & 2 ML20195F3161998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Cpses,Units 1 & 2 ML20154M8841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Cpses,Units 1 & 2 ML20154B5741998-09-30030 September 1998 Safety Evaluation Re Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Motor-Operated Valves. Licensee Has Established Acceptable Program ML20151W0361998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Cpses,Units 1 & 2. with ML20151Q1211998-08-14014 August 1998 Rev 0 to Control of Hazard Barriers ML20237C4061998-08-14014 August 1998 Safety Evaluation Supporting Request to Implement Risk Informed IST Program ML20237C6721998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Cpses,Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236R0711998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Cpses,Units 1 & 2 ML20249B2581998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Cpses,Units 1 & 2 ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20247G3241998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Cpses,Units 1 & 2 ML20216B8661998-04-0101 April 1998 Rev 0 to ERX-98-001, CPSES Unit 1 Cycle 7 Colr ML20216J3061998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Cpses,Units 1 & 2 ML20216J1861998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Comanche Peak Steam Electric Station ML20197A6951998-02-24024 February 1998 Inservice Insp Summary Rept,First Interval,Second Period, First Outage ML20199J5391998-02-0202 February 1998 CPSES Commitment Matl Change Evaluation Rept 0002 for 960202-970801 1999-09-30
[Table view] |
Text
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-- . Log' # TXX-90211 F9 File # 10200-i, 3 E -
~ 906.2 910.3 i
L NJELECTR/C Ref. f.50.73 (a)(2)(i) ,
at J Edl,E,Yu rm,s,,, June 13,-1990 U. :S. Nuclear Regulatory Commission Attn: Document Control- Desk Washington, D. C.- 20555.- -
SUBJECT:
COMANCHE F'iAK-STEAM ELECTRIC STATION DOCKET NO. 50-445 i CONTAINMENT PENETRATION NOT PROPERLY ISOLATED &
LICENSEE EVENT' REPORT 90-014-00
~ Gentlemen: -
Enclosed is Licensee Event Report 90 014-00 for Comanche Peak Steam Electric Station Unit ~ 1, " Containment Penetration Not Properly Isolated Due to Personnel Error."
Sincerely, y William J. Cahill, Jr.
l
.JRW/daj l
l Enclosure -
l c EMr. R. D. Martin, Region IV -
~
-Resident Inspectors, CPSES'(3) y I
9006190073 900613 /),
PDR ADOCK 05000443 V S PDC e)O North Olive Street LB81 Dallas, Texas 73201
,e Enclesur,e.to TXX 90211 NRC FORM 366 U.S. NUCLk AR REOut.ATORY COMMISSON APPROVED OWB NO. 3150*0104 l EXPIRE 8:4/3@92 ESTiuATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATON COLLECTON REQUEST: 60bHRS. FORWARD COMWENTS REGARDING SUR EN ESTIMATE T THE RE R S AN REP RT8 MANA EWENT LICENSEE EVENT REPORT (LER) BRANCH (P-630). U.S. NUCLE AR REGULATORY COMMISSON, WASHtNOTON.
DC. 20665, AND TO THE PAPERWORK REDUCTION PROJECT (31540104)
OFFICE OF WANAGEMENT AND BUDGET,WASHINOTON,DC.20503.
Page (3)
Ft.cacy Name (1) Dod.t Nurvtier (2)
COMANCHE PEAK - UNIT 1 01510101014i415 1 I or 10i7 Ita (4)
CONTAINMENT PENETRATION NOT PROPERLY ISOL ATED DUE TO PERSONNEL ~r,-,.,-.,
ERROR
- na,. e a e ~- ae- on,. m Month Day Year Year [ hun u Month Day Year Ols 1 14 910 910 011l4 -
010 016 113 910 N/A TNs resxwi e suometed pursuant to the reaunemerus of to CFR $ :(Check one or move of the tonowingi(t ti 015I010101 I I Operating Mode (93 2 ,,, 20.402(b) _ N).406A _ 60.73(a)(2)(iv) _ 73.71M Vove , 20.406(a)(1)(l) _ 60.36lc)(1) _ 60.73(a)(2)(v) _ 73.71(c)
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Teesprene Nurreer Area Code G P.McGEE SUPERVISOR. COMPLIANCE 8 l 117 8 ! 917 l- I 5 I 417 I 7 Corroisse One Line For Eads Convenere Falure Deecnhed in The Report (13)
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I III II I MM SutWetental Report E spected (14) Expected wonm Day v ear Sutmosen Cyes (It yes, conWete Expeded Sutmason Datel @ No l I I Aostract (Urrat to 1400 spaces Lo., approximately fdteen single space typewnsen Imos) (16)
At 1530 on May 14,1990, it was discovered that a containment penetration had not been properly isolated (for approximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />) in accordance with Technical Specification 3.6.3 while containment isolation valve 1-HV-2409 was inoperable for repairs. With 1 HV 2409 Inoperable, manual isolation valve 1 MS 0324 had been closed to isolate the containment penetration and to satisfy the Technical Specification Action Statement. Subsequently, the entire clearance for 1-HV-2409 was released (including the opening of 1MS-0324) to allow valve calibration at the completion of the repairs without ensuring that actions would be taken to satisfy the Action Statement.
The root cause of the event is an inadequate review of the work order by the Unit Supervisor prior to authorizing release of the entire clearance rather than authorizing a partial release of the clearance (just the air supply to the valve). Corrective actions include counselling of the Unit Supervisor, issuance of a Shift Order to caution control room operators of the event, and several program enhancements to more readily identify the tie between a clearance and associated Action Statement.
?
. Encl:sure to.TXX 90211=
NffC FORM 366A U.S. NUCLE AR REOULATURY COMMISSION APPROVED OMB NO. 31540104 ESTIMATED BURDEN PCR f4E E COMPW WITH THS INFORMATION
" ^
LICENSEE EVENT REPORT (LER) go'l,'%,"j,y,",'s 1 l"l' egg,7, @',"g'fs, TEXT CONTINUATION g
' 7,i t'g* ll , $ ' ,^t O ,"* ^,1
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F6cday Name (1) Docket Nurnbar (2) LE A Nuriter (6) Pepe (3)
- v. m w -
m COMANCHE PEAK - UNIT 1 0151010l01414l5 910 -
0l114 -
0l0 0l2 OF 017 i..n % . % . - RCr.,m3=A.>on I. DESCRIPTION OF THE REPORTABLE EVENT A. PLANT OPERATING CONDITIONS BEFORE THE EVENT j
! On May 14,1990, Comanche Peak Steam Electric Station (CPSES) Unit 1 was in l
Mode 2 operating at 3 percent reactor power.
q l
B. STATUS OF STRUCTURES. SYSTEMS. OR COMPONENTS l THAT WERE INOPERABLE AT THE START OF THE EVENT AND THAT CONTRIBUTED TO THE EVENT i
Main Steam Line Drain Pot Isolation Valve (Ells:(ISV)(SB)) 1-HV-2409 had been declared Inoperable on May 12,1990 in order to repair a body to bonnet leak.1-HV-2409 is an air operated automatic containment isolation valve which is normally open but falls closed.
L C. REPORTABLE EVENT CLASSIFICATION Any operation or condition prohibited by the plant's Technical Specifications.
D. NARRATIVE
SUMMARY
OF THE EVENT. INCLUDING DATE AND l APPROXIMATE TIMES in preparation for the performance of corrective maintenance to repair a body-to-bonnet leak on va!ve 1-HV 2409, the appropriate clearance tags were attached and subsequently accepted by the (midnight shift) Shift Technical Advisor (utility, licensed) on May 12,1990 at 0455. The approved clearance required isolating the air suppiy to 1-HV 2409 and closing several manual isolation valves including the upstream manualisolation valve (1MS 0324) (Ells:(ISV)(SB)) for 1-HV 2409. These actions isolated the valve from normal operating pressure and allowed the work order to be performed. !
l 1
l I
1 Enclosure to TXX-90211
~
NRC FORM 3eeA U.S. NUCLE AR REGULATORY COMMISSION APPROVED OWS No. 3194010s ESTIMATED BURDEN PER RES 8 Y WITH THIS INFORMATION LICENSEE EVENT REPORT (LER) gl,,'t,",'M8'; 1 l"yggy,,l,gg8, "'f"%
1 TEXT CONTINUATION "g ; "i % ,"l @ ,"lo % % % " L8'0 "ic Q " @
OFFICE OF MANAGEMENT AND BUOGET, WASHINGTON, DC. 20603.
Facday Name (1) Dmmet Nunter (2} LE R Nont.t (6) Page (3) v~ m 2:~ - m COMANCHE 0l51010l0l414l5 910 -
0l114 -
0IO Ol3 OF 017 um. .. . PEAK .
..UN,IT sRc orm 1 3 A., o 73 t
In accordance with Technical Specification 3.6.3, isolation of the containment penetration (Ells:(PEN)(NH)) was required within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of the inoperability of a containment isolation valve associated with that penetration. Closing 1MS 0324 provided isolation of the containment penetration associated with 1 HV 2409. A Limiting Condition for Operation Action Requirement (LCOAR) was initiated to document the entrance into a Technical Specification Action Statement and identify the necessary requirements to restore operability following completion of the work.
Repairs were subsequently completed on the valve with the exception of the required valve calibration (bench set) and a request was made to control room personnel by an Instrument and Control (l&C) Technician to release the clearance on the valve, l&C needed the air supply isolation removed to allow stroking of the valve during the valve calibration. At 2147 on May 13,1990, the (evening shift) Unit Suparvisor (utility, licensed) performed a review of the work order and authorized the release of the entire clearance, including the opening of 1MS 0324, to allow l&C to calit rate the valve. The valve calibration was successfully completed at 0424 on May 14,1990, and at 1039 the same day,1 HV-2409 was successfully stroked by Operations to meet the post work testing requirements. The post work test results were subsequently reviewed, the LCOAR closed out, and 1-HV-2409 was declared operable at 1327.
At 1530 on May 14,1990, it was discovered that 1-HV-2409 had been inoperable without 1 MS-0324 being shut for approximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> (2147, May 13 to 1327, May 14,1990). Therefore, CPSES Unit 1 had been in violation of Technical Specification 3.6.3 since 0147 on May 14,1990 (4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> after the initial release of L the clearance and the subsequent opening of 1MS 0324).
E. THE METHOD OF DISCOVERY OF EACH COMPONENT OR SYSTEM FAILURE OR PROCEDURAL OR PERSONNEL ERROR On May 14,1990, at 1530, just after assuming licensed duties for the evening shift, the Unit Supervisor identified the fact that he had released the clearance and unisolated the containment penetration prior to completion of the required operability testing. The discovery occurred during shift turnover when the status of 1-HV-2409 was being discussed. At the time of the event discovery,1-HV-2409 had already been declared operable.
Enclosure to TXX 90211 U.8, NUCLE AR REQULATORY COMMISSON APPROVED OWB NO. stb 0104 NRC FORM 366A ESTIMATED BURDEN PER RE8 9 COMPW wtTH THIS INFORMATON LICENSEE EVENT REPORT (LER) g,c ,
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- 1. im - . mo. .. .= NRe f o,m mA.ma ll. COMPONENT OR SYSTEM FAILURES A. FAILURE MODE. MECH ANISM AND E-2ECT OF EACH FAILED COMPONENT Not applicable - no failed components have been identified.
B. CAUSE OF EACH COMPONENT OR SYSTEM FAILURE Not applicable - no component or system failures have been identified.
C. SYSTEMS OR SECONDARY FUNCTIONS THAT WERE AFFECTED BY FAILURE OF COMPONENTS WITH MULTIPLE FUNCTIONS Not applicable - no components failures have been identified.
D. FAILED COMPONENT INFORMATION Not applicable - no failed components have been identified.
Ill.. ANALYSIS OF THE EVENT A. SAFETY SYSTEM RESPONSES TH AT OCCURRED Not applicable - there were no manual or automatic safety system responses as a result of this event.
B. DUR ATION OF SAFETY SYSTEM INOPERABILITY Not applicable - there were no safety systems which were rendered inoperable due to a failure.
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l C. SAFETY CONSEQUENCES AND IMPLICATIONS OF THE EVENT q
Based on the following discussion, the event did not adversely affect the safe operation of CPSES Unit 1 or the health and safety of the public.
Upon releasing the clearance,1MS-0324 was opened which eliminated the isolation ,
provision established to meet the requirements of Technical Specification 3.6.3.
However, at this time,1 HV-2409 was in the closed position with the exception of several minutes while it was being stroked as part of the valve calibration and as part '
i of the post work operability testing. After the successful completion of the operability L
testing, the valve was left open in its normal operating position for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 44-minutes until the valve was declared operable. Cumulatively,1 HV 2409 was in the a open position for a maximum of 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 7 minutes during the time period following the clearance release until it was declared operable. This is less than the 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> limit allowed by Technical Specification 3.6.3 for an unisolated containment penetration. The reason that credit cannot be taken for 1-HV 2409 meeting the Technical Specification 3.6.3, Action Statement (isolating the penetration) is that it was not " deactivated" and " secured" while in the closed position.
In addition, since the work order did not affect the valve actuator, and the valve calibration as well as the post work operability testing were successfully completed, the valve would have been able to close in response to an isolation signal during the times it was open, if required.
IV. CAUSE OF THE EVENT ROOT CAUSE The root cause of the event is an inadequate review of the work order by the Unit Supervisor (utility, licensed) prior to authorizing release of the entire clearance. Only the release of the air supply to 1-HV-2409 needed to be authorized in order to allow l&C to perform the bench set. The inadequate review is considered a cognitive personnel error.
p (Enclosure to TXX-90211(
NRC FORW 3 sea _ U.S. NUCLE AR REOULATORY COWWISSION APPROVED OM8 NO. 3160104 ESTIMATED BURDEN PER RES E COMPLY WITH TH18 INFORMATION LICENSEE EVENT REPORT (LER) "5T%,g',';
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C V. CORRECTIVE ACTIONS i
A. CORRECTIVE ACTIONS TO PREVENT RECURRENCE The Unit Supervisor was counselled regarding the event and the need for attention to details.
- A Shift Order was issued on May 15,1990 to caution control room operators of the event.
A~ newly developed Impact Review Sheet has been implemented to provide a more thorough and structured review of work orders in order to ensure that any special circumstances related to the work order are identified and highlighted up front.
The shift turnover checklist has been revised to provide a section for logging any active' Limiting Condition of Operations (LCO). This will help provide continued 1 awareness of any epecial circumstances associated with an Action Statement.
The following program enhancements are being implemented to more readily identify the tie between a clearance and associated Action Statement (s), allowing for the appropriate disposition of the clearance by control room personnel.
- 1. . The LCOAR procedure will be revised to include the requirement that if it is *
' desired to maintain a component in a particular state (i.e., inoperable Containment Isolation Valve shut with power removed) to ensure compliance ,
~
with an Action Statement, the clearance tags hung on the affected components willlist the LCOAR Number and the required component configuration. '
Conversely, clearances being utilized to ensure compliance with an Action Statement will be required to be referenced on the LCOAR.
- 2. The CPSES Clearar Report Form will be revised to include a line within the placement and release authorization sections where the associated LCOAR
. number shall be documented.
, . Enclosure to TXX-90211 NRC FORM 306A U.S. NUCLE AR RECULATORY COMMISSON APPROVED OMB NO.3150 0104 CSTIMATED BURDEN PER RES 8T COMPLY WITH THIS lNFORMATON 5* *' ' "*
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! B. CORRECTIVE ACTION TAKEN ON GENERIC CONCERNS IDENTIFIED AS A DIRECT RESULT OF THE EVENT Following the event, a task team was formed to evaluate factors contributing to p Technical Specification noncompliance. The scope of this evaluation included CPSES Licensee Event Reports, Operations Notification and Evaluation (ONE) ,
Forms, and relevant procedures. Based on this evaluation, several actions have I been taken, including 1) the revision of the LCOAR form to require that both the Shift Technical Advisor (Modes 1 thru 4 only) and the affected Unit Supervisor review the form prior to LCO entry and termination (if the Shift Technical Advisor and Unit Supervisor positions are filled by different personnel) and 2) the removal of out of ;
L date information from the Standing Orders, Policy Book, and Lessons Learned Book.
VI. PREVIOUS SIMILAR EVENTS LER 90 000-00 involved a Technical Specification non-compliance resulting from the inadequate review cf a work order package. However, the specific causes of that event and the specific cause of the event described in this LER were sufficiently different such
- that the corrective action for LER 90 008 00 was not applicable to the event described in 1 L this LER. The corrective actions discussed in Section V should reduce the potential for j l
Technical Specification non-compliances resulting from both causes.
E l l Vll. AQD.lIlRNAl MQBMAT.lOH The times listed in the report are approximate and Central Daylight Savings Time (CDT).
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