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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E8021999-10-0707 October 1999 CPSES Unit 1 Cycle 8 Colr ML20217G4151999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Cpses,Units 1 & 2 ML20212F7671999-09-24024 September 1999 SER Granting Relief Request C-4 Pursuant to 10CFR50.55a(g)(6)(i) for Unit 2,during First 10-year ISI Interval & Relief Requests B-15,B-16 & B-17 Pursuant to 10CFR50.55a(g)(6)(i) ML20216J5701999-09-16016 September 1999 Rev 2 to CPSES Unit 2 Cycle 5 Colr TXX-9920, Monthly Operating Repts for Aug 1999 for Cpses.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Cpses.With ML20211M2981999-08-0606 August 1999 Rev 1 to CPSES Fuel Storage Licensing Rept, CPSES Credit for Soluble Boron & Expansion of Spent Fuel Storage Capacity, Consisting of Revised Title Page and 4-1 ML20210U4081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Cpses,Units 1 & 2 ML20210D8321999-07-23023 July 1999 Safety Evaluation Accepting Relief Requests Re Use of 1998 Edition of Subsections IWE & Iwl of ASME Code for Containment Insp ML20209H7661999-07-15015 July 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Comanche Peak Steam Electric Station,Units 1 & 2 ML20209H2721999-07-0909 July 1999 2RF04 Containment ISI Summary Rept First Interval,First Period,First Outage ML20209H2631999-07-0909 July 1999 2RF04 ISI Summary Rept First Interval,Second Period,Second Outage ML20209G7501999-07-0808 July 1999 SER Finding That Licensee Individual Plant Exam of External Events Complete with Regard to Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given Design, Operation & History of Comanche Peak Steam Electric Station ML20196L0191999-07-0808 July 1999 Safety Evaluation Granting Request Relief B-6 (Rev 2),B-7 (Rev2),B-12,B-13,B-14 & C-9,pursuant to 10CFR50.55a(g)(6)(i).Technical Ltr Rept Also Encl ML20210J9391999-06-30030 June 1999 CPSES Commitment Matl Change Evaluation Rept 0003,for 970802-990630 ML20209G0801999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Cpses,Units 1 & 2 ML20196J0621999-06-29029 June 1999 Safety Evaluation Supporting Proposed Changes to Emergency Plan Re Licenses NPF-87 & NPF-89 Respectively ML20195G5141999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Comanche Peak Steam Electric Station,Units 1 & 2.With ML20216E0711999-05-21021 May 1999 1999 Graded Exercise - Comanche Peak Steam Electric Station ML20206Q0091999-05-14014 May 1999 Safety Evaluation Accepting GL 92-08, Thermo-Lag 330-1 Fire Barriers, Dtd 921217,for Comanche Peak Electric Station,Unit 1 ML20206H2061999-05-0606 May 1999 SER Accepting Exemption to App K Re Leading Edge Flowmeter for Plant,Units 1 & 2 ML20196L2241999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Cpses,Units 1 & 2 ML20205R5701999-04-14014 April 1999 Rev 6 to ER-ME-067, TU Electric Engineering Rept,Evaluation of Thermo-Lag Fire Barrier Sys ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205J7831999-04-0101 April 1999 Rev 0 to ERX-99-001, CPSES Unit 2 Cycle 5 Colr ML20205N3101999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Cpses,Units 1 & 2 ML20204H6371999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Comanche Peak Units 1 & 2 ML20205N1481999-02-28028 February 1999 Corrected Monthly Operating Rept for Feb 1999 for CPSES, Units 1 & 2 ML20203A4881999-02-0303 February 1999 Safety Evaluation Granting Requests for Relief B-3 - B-6,C-2 & C-3 for Plant,Unit 2 ML20210J9201999-02-0101 February 1999 CPSES 10CFR50.59 Evaluation Summary Rept 0008,for 970802- 990201 ML20202D0101999-01-27027 January 1999 Safety Evaluation Supporting First 10-yr Interval ISI Program Plan Requests for Relief B-9,B-10 & B-11 for CPSES, Unit 1 ML20199E9961998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Cpses,Units 1 & 2 ML20207D6091998-12-31031 December 1998 1998 Annual Operating Rept for Cpses,Units 1 & 2. with ML20197K2371998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Cpses,Units 1 & 2 ML20195F3161998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Cpses,Units 1 & 2 ML20154M8841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Cpses,Units 1 & 2 ML20154B5741998-09-30030 September 1998 Safety Evaluation Re Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Motor-Operated Valves. Licensee Has Established Acceptable Program ML20151W0361998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Cpses,Units 1 & 2. with ML20151Q1211998-08-14014 August 1998 Rev 0 to Control of Hazard Barriers ML20237C4061998-08-14014 August 1998 Safety Evaluation Supporting Request to Implement Risk Informed IST Program ML20237C6721998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Cpses,Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236R0711998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Cpses,Units 1 & 2 ML20249B2581998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Cpses,Units 1 & 2 ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20247G3241998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Cpses,Units 1 & 2 ML20216B8661998-04-0101 April 1998 Rev 0 to ERX-98-001, CPSES Unit 1 Cycle 7 Colr ML20216J3061998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Cpses,Units 1 & 2 ML20216J1861998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Comanche Peak Steam Electric Station ML20197A6951998-02-24024 February 1998 Inservice Insp Summary Rept,First Interval,Second Period, First Outage ML20199J5391998-02-0202 February 1998 CPSES Commitment Matl Change Evaluation Rept 0002 for 960202-970801 1999-09-30
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I ~2 LNe#TXX-90337 F # 10200 905.4 Ref. # 100FR50.73 10CFA50.73(a)(2)(i)
MlELECTRIC wim. J.c.hiii.Jr. September 27, 1990 tmwn nar,na-U. S. Nuclear Regulatory Comicsion Attn: Document Control Desk Washington, D. C. 20555
SUBJECT:
COMANCHE PEAK STEAM ELECTRIC STATION 2
DOCKET NO.50-44f OP..ATION PROHIBITED BY TECHNICAL SPECIFICATION '
LICENSEE EVENT REPORT 90 076-00 Gentlemen:
Enclosed is Licensee Event Report 90 026-00 for Comanche Peak Steam Electric Station Unit 1, " Missed Surveillance Due to Inadequate Procedural Requirements."
Sincerely, A
3 w- w-William :. Cahill, Jr.
JAA/daj Enclosure c - Mr. R. D. Martin, Region IV Resident Inspectors, CPSES (3) 9010040261 900927 l' goa Anoen Oso g s pF onca _,, _, s , m . , e..... m., _
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l Enclosure to TXX 90337 l
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LICENSEE EVENT REPORT (LE9) BRANCH (P $3:1), U.S. NUCLE AR REOULATORY C0bWISSON. WASHINGTON 3C 20bM. AND TO THE PA.ERwoRK REDUCTON PROJECT (3150 0104)
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On June 15,1990, the Residual Heat Removal Pump 01 (RHRP 01) quarterly inservice test (IST) was satisfactorily performed. On July 2,1990, post test data review determined that RHRP-01 was in ALERT status due to low differential pressure, as defined by American Society of Mechanical Engineers Boiler and Pressure V( , 91 Code,Section XI. As a result, the test frequency for RHRP 01 was increased to once p, 46 days.
On July 25,1990, a Surveillance Work Order (SWO) was manually printed in accordance with the increased test frequency requirement. However, the test frequency for this activity had not been revised in the Managed Maintenance Computer Program Surveillance Activity Data Base. As a result, the actual due date and violation date was not reflected on the SWO On August 12,1990, the required surveillance exceeded the violation date. On August 14,1990, the required surveillance was performed satisfactorily. On August 28,1990, while compiling test data for several IST components, the missed surveillance was discovered.
The root cause was deteimined to be inadequate manual surveillance scheduling method.
Corrective actions include revisions to station procedures.
1 i
Enclosure to TXX 90337 Ns,c p Onw.3M,A . W.S. NAE AR HLGAA1084v LOWW4 SON gpPRDVED0ut NO.312010s CSTNATED SVRDEN PER RES T COMPEY wrTH 1 Hit NF0feuATON
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TEXT CONTINUATION '"'"*"**'"*""'**^'"'*""***""'*""'"-
- 30. Ions, AND TO THE PAPE RWORK REDJCTON PROJECT ($140104) 0FFCE OF WANA0EMENT AND BUDGET WASHINGTON.DC.30603.
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Y ear Qjag,* Aq COMANCHE PEAK - UNIT 1 015101010l4I415 910 -
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010 012 OF 017 w -. .. . . - NRa . m ., o r, is DESCRIPTION OF THE REPORTABLE EVENT A. REPORTABLE EVENT Cl ASSIFICATION Any operation or condition prohibited by the plant's Technical Specifications, e B. PLANT OPERATING CONDITIONS BEFORE THE EVENT l
j On August 12,1990, Comanche Peak Steam Electdc Station (CPSES) Unit 1 was in Mode 1, Power Operation, at approximuly 90 percent power.
C. STATUS OF STRUCTURES. SYSTEMS. OR COMPONENTS I THAT WERE INOPER ABLE AT THE START OF THE EVENT AtiD THAT CONTRIBUTED TO THE EVENT i l- Not aor;licable no structures, systems or components were inoperable at the start of the event that contributed to the event, i
l D. NARRATIVE
SUMMARY
OF THE EVENT. INCLUDING DATES AND )
APPROXIMATE TIMES ,
At 0556, on June 15,1990, a quarterly inservice test (IST) was performed on Residual Heat Removal Pump 01 (RHRP 01) (Ells:(P)(BP)). The operability criteria for RHRP 01 was satisfied as required by Technical Specification Surveillance .
Requirements 4.5.2, 4.5.3, and 4.0.5. l l
On July 2,1990, the IST Coordinator (contractor, non licensed) notified the Operations Survelilance Test (OST) Coordinator (contractor, non licensed) that based on review of test data from the June 15,1990 test, RHRP-01 was in ALERT status. ALERT status is a condition identified by the American Society of Mechanical Engineers Boiler and Pressure Vessel (ASME BPV) Code,Section XI, in which a measured pump parameter has exceeded a predetermined threshold value and is approaching an operability limit, in such a case, the Code requires that the !
frequency of testing be doubled until the cause of the deviation is determined and l l
l
dnclosure to TXX 90337 NIGONW.366A . . NUCLE AR RLGJLA106W 00Mg3(4pN ADPPOWO OMO NO. 8W1M ESTIMATED SURDEN PER RE& T COW 8%Y WITH TNiB PFORWATON LICENSEE EVENT REPORT (LER) g3l'%,"j,y*,'; ,6 l"fegg'* g,'f&*,%
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,.nu - mi r, the condition corrected. The cause fo/ ALERT status on RHRP-01 was low differential pressure. The IST Coordinator requested that the test frequency be increased from once per 92 days to once per 46 days until further co' ice. The due date for this test would be July 31,1990. ;
On July 25,1530, the OST Coordinator manually printed a Surveillance Work Order (SWO) to perform the required RHRP 01 surveillance in accordance with the !
increased test frequency requirement. A scheduled date of August 8,1990 was selected to colqcide with scheduled routine pump runs. However, the test frequency -
for this activity had not been revised in the Managed Maintenance Computer :
Program (MMCP) Surveillance Activity Data Base, and as a result the act: ~ ' due :
date (July 31,1990) and violation date (August 12,1990) were not reflecteu oil the SWO. The SWO assigned September 14,1990, as the due date, and October 6, 1990 as the violation date, which correspond to the normal quarterly due and i violation dates. Delaying the required surveillance from July 31,1990, to August 8, 1990 was acceptable based on Technical Specification 4.0.2 which allows a 25 percent grace period or 11.5 days.
On August 8,1990, the scheduled surveillance was not performed due to CPSES Unit 1 recovery and subsequent startup following a reactor trip. The control room -
staff was u.iaware of the actual violation date for the required surveillance. At 1756 on Augurc 12,1990, the required surveillance exceeded the violation date. At 1550, August i4,1990, the required surveillance was performed satisfactorily.
E. T.tiffiETHOD OF DISCOVERY OF EACH COMPONENT OR SYeTEM EML.'JRE OR PROCEDUR AL OR PERSONNEL ERROR On August 28 1990, while compiling test data for several IST components in ,
~
response to requests from Nuclear Regulatory Commission inspectors, the missed surveillan :e was discovered by the OST Coordinator. The missed surveillance was promptly documented via appropriate plant procedures.
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- 11. COMPONENT OR SYSTEM FAILUREF e
A. FAILURE MODE, MECHANISM AND EFFECT OF EACH FAILED COMPONENT Not applicable - there were no component failures associated with this event.
B. CAUSE OF EACH COMPONENT OR SYSTEM FAILURE Not applicable there were no component failures associated with this event.
C. SYSTEMS OR SECONDARY FUN
- FAILURE OF COMPONENTS Wn d MULTIPLE FUNCTIONS Not applicable there were no component failures associated with this event.
D. FAILED COMPONENT INFORMATION Not applicable - there were no component failures associated with this event.
Ill. ANALYSIS OF THE EVENI i A. SAFETY SYSTEM RESPONSES THAT OCCURRED Not applicable - no safety system responses occurred as a result of this event.
l B. DUR ATION OF SAFETY SYSTEM TRAIN INOPERABILITY Not applicable - there were no safety systems which were rendered inoperable.
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010 015 OF 017 1..u. .- . . .. - u % u .w, C. SAFETY CONSEQUENCES AND IMPLICATIONS OF THE EVENT I
The Residual Heat Removal (RHR)(Ells:(BP)) system is safety related bo 'n its I' normal function to remove decay heat during shutdown and in its post accident function to provide emergency core cooling. The RHR pumps, therefore, are surveillance tested to demonstrate that the minimum pump performance assumed in !
various analyses is available. Technical Specification 4.5.2 and 4.5.3 require that this testing be performed quarterly. ASME BPV Code,Section XI (Technical Specification 4.0.5), further requires that for a pump determined to be approaching .
its minimum performance limit (i.e., entered ALERT status), the frequency of testing
, be increased to once per 46 days. The more frequent testing of pumps in ALERT status reducas the likelihood that the plant would operate in a condition in which a -
given pump was not meeting its minimum performance requirements. ,
In the case of RHRP-01, the SWO, while performed late, demonstrated that the pump exceeded its minimum performance requirements and therefore the plant remained l within analyzed limits.
Based on the above discussion, the event did not adversely affect the safe operation ,
of CPSES Unit 1 or the health and safety of the public.
IV. CAUSE OF THE EVENT t
ROOT CAUSE The manual surveillance scheduling method selected was less than adequate. The
- control room staff was not properly informed of the actual violation date or the due date for the subject late surveillance. Although manualinitiation of a SWO and forwarding of the -
SWO to the control room in a timely manner are certainly aspects of a successful manual scheduling method, the failure to manually enter the true surveill::,1ce due date and violation date on the SWO allowed the method to fall.
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i..n. . . ~ . ~ . m - w .nia t V. CORRECILV1 ACTIONS A. CORRECTIVE ACTIONS TO PREVENT RECURRENCE ROOT CAUSE f
Inadequate manual surveillance scheduling method.
CORRECTIVE ACTION The Surveillanco Test Program procedure will be reviewed, and revised as required, [
to ensure that requirements for updating the frequency of surveillance activities, as ;
conditions change, are incorporated, B. CORRECTIVE ACTION TAKEN ON GENERIC CONCERNS IDENTIFIED l AS A DIRECT RESULT OF THE EVENT L
GENERIC CONSIDER ATION The possibility exists that a similar problem could occur in the manual methods used by the other Surveillance Test Coordinators.
CORRECTIVE ACTION A memo addressing this concern will be distributed to the Surveillance Test Coordinators.
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VI. PREVIOUS SIMILAR EVENTS Although'here have been several previous everi s (LER 90 005, LER 90 010, LER 90-024) resulting from failure to perform Technical Fpecification surveillance activities, the root causes of those events were ur.related to the root chuse of this event. The corrective actions taken to resolve the root causes of".e previous events would not have prevented this event. Therefore, no previous sim'iar eveists have been reported pursuant to n 10CFR50.73.
Vo ADDITION AL INFORMATION t
The times listed in the report are approximate and Central Daylight Savings Time (CDT).
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