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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E8021999-10-0707 October 1999 CPSES Unit 1 Cycle 8 Colr ML20217G4151999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Cpses,Units 1 & 2 ML20212F7671999-09-24024 September 1999 SER Granting Relief Request C-4 Pursuant to 10CFR50.55a(g)(6)(i) for Unit 2,during First 10-year ISI Interval & Relief Requests B-15,B-16 & B-17 Pursuant to 10CFR50.55a(g)(6)(i) ML20216J5701999-09-16016 September 1999 Rev 2 to CPSES Unit 2 Cycle 5 Colr TXX-9920, Monthly Operating Repts for Aug 1999 for Cpses.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Cpses.With ML20211M2981999-08-0606 August 1999 Rev 1 to CPSES Fuel Storage Licensing Rept, CPSES Credit for Soluble Boron & Expansion of Spent Fuel Storage Capacity, Consisting of Revised Title Page and 4-1 ML20210U4081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Cpses,Units 1 & 2 ML20210D8321999-07-23023 July 1999 Safety Evaluation Accepting Relief Requests Re Use of 1998 Edition of Subsections IWE & Iwl of ASME Code for Containment Insp ML20209H7661999-07-15015 July 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Comanche Peak Steam Electric Station,Units 1 & 2 ML20209H2721999-07-0909 July 1999 2RF04 Containment ISI Summary Rept First Interval,First Period,First Outage ML20209H2631999-07-0909 July 1999 2RF04 ISI Summary Rept First Interval,Second Period,Second Outage ML20209G7501999-07-0808 July 1999 SER Finding That Licensee Individual Plant Exam of External Events Complete with Regard to Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given Design, Operation & History of Comanche Peak Steam Electric Station ML20196L0191999-07-0808 July 1999 Safety Evaluation Granting Request Relief B-6 (Rev 2),B-7 (Rev2),B-12,B-13,B-14 & C-9,pursuant to 10CFR50.55a(g)(6)(i).Technical Ltr Rept Also Encl ML20210J9391999-06-30030 June 1999 CPSES Commitment Matl Change Evaluation Rept 0003,for 970802-990630 ML20209G0801999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Cpses,Units 1 & 2 ML20196J0621999-06-29029 June 1999 Safety Evaluation Supporting Proposed Changes to Emergency Plan Re Licenses NPF-87 & NPF-89 Respectively ML20195G5141999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Comanche Peak Steam Electric Station,Units 1 & 2.With ML20216E0711999-05-21021 May 1999 1999 Graded Exercise - Comanche Peak Steam Electric Station ML20206Q0091999-05-14014 May 1999 Safety Evaluation Accepting GL 92-08, Thermo-Lag 330-1 Fire Barriers, Dtd 921217,for Comanche Peak Electric Station,Unit 1 ML20206H2061999-05-0606 May 1999 SER Accepting Exemption to App K Re Leading Edge Flowmeter for Plant,Units 1 & 2 ML20196L2241999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Cpses,Units 1 & 2 ML20205R5701999-04-14014 April 1999 Rev 6 to ER-ME-067, TU Electric Engineering Rept,Evaluation of Thermo-Lag Fire Barrier Sys ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205J7831999-04-0101 April 1999 Rev 0 to ERX-99-001, CPSES Unit 2 Cycle 5 Colr ML20205N3101999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Cpses,Units 1 & 2 ML20204H6371999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Comanche Peak Units 1 & 2 ML20205N1481999-02-28028 February 1999 Corrected Monthly Operating Rept for Feb 1999 for CPSES, Units 1 & 2 ML20203A4881999-02-0303 February 1999 Safety Evaluation Granting Requests for Relief B-3 - B-6,C-2 & C-3 for Plant,Unit 2 ML20210J9201999-02-0101 February 1999 CPSES 10CFR50.59 Evaluation Summary Rept 0008,for 970802- 990201 ML20202D0101999-01-27027 January 1999 Safety Evaluation Supporting First 10-yr Interval ISI Program Plan Requests for Relief B-9,B-10 & B-11 for CPSES, Unit 1 ML20199E9961998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Cpses,Units 1 & 2 ML20207D6091998-12-31031 December 1998 1998 Annual Operating Rept for Cpses,Units 1 & 2. with ML20197K2371998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Cpses,Units 1 & 2 ML20195F3161998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Cpses,Units 1 & 2 ML20154M8841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Cpses,Units 1 & 2 ML20154B5741998-09-30030 September 1998 Safety Evaluation Re Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Motor-Operated Valves. Licensee Has Established Acceptable Program ML20151W0361998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Cpses,Units 1 & 2. with ML20151Q1211998-08-14014 August 1998 Rev 0 to Control of Hazard Barriers ML20237C4061998-08-14014 August 1998 Safety Evaluation Supporting Request to Implement Risk Informed IST Program ML20237C6721998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Cpses,Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236R0711998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Cpses,Units 1 & 2 ML20249B2581998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Cpses,Units 1 & 2 ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20247G3241998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Cpses,Units 1 & 2 ML20216B8661998-04-0101 April 1998 Rev 0 to ERX-98-001, CPSES Unit 1 Cycle 7 Colr ML20216J3061998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Cpses,Units 1 & 2 ML20216J1861998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Comanche Peak Steam Electric Station ML20197A6951998-02-24024 February 1998 Inservice Insp Summary Rept,First Interval,Second Period, First Outage ML20199J5391998-02-0202 February 1998 CPSES Commitment Matl Change Evaluation Rept 0002 for 960202-970801 1999-09-30
[Table view] |
Text
_ _ . . _ . .
t M
E Log # TXX-91077
g File i 10200 910.4 7UELECTRIC Ref. # 50.73(a)(2)(iv)
March 12, 1991 2,DOIU,r,,,am, U. S. Nuclear Regulatory Comission Attn: Document Control Desk Washington, D. C. 20555
SUBJECT:
COMANCHE PEAK STEAM ELECTRIC STATION (CPSEd)
DOCKET NO. 50-445 MANUAL OR ALTTOMATIC REACTOR PROTECTION SYSTEM ACTUATION LICENSEE EVENT REPORT 91-004-00 Gentlemen:
Enclosed is Licensee Event Report 91-004-00 for Comanche Peak Steam Electric Station Unit 1 " Reactor Trip Caused by Personnel Error and Insufficient Labeling of Sensitive Equipment."
Sincerely, d A.
William J. Cahill, Jr. '
JAA/daj e - Mr. R. )). Martin, Region IV Resident Inspectors, CPSES (3)
'I
'9803130246 910312 400 North Olive Street LB 81 Dal!as, Texas 75201 S' PDR ADOCK 05000445 '
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. Enclosure to TXX 91077 NHO FQ8W q U 6 NUCd AP, RtOVLATORT COMW'SSON 4pP40WD OMB NO Sim0W EkprRES A%U2
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On February 10,1991, Comanche Peak Steam Electric Station Unit 1 was in Mode 1, Power Operation, at 80 percent reactor power. Whi!e conducting on-the-job training, an Auxiliary Operator opened the 6.9 KV switchgear bus "1 A3" auxiliary cabinet potential transformer drawer resulting in a load shed signal for the bus loads, which included Reactor Coolant Pump 103, followed by a reactor trip due to a loss of flow in reactor coolant loop 3. The root causes were determined to be inadequate labeling on the potential transformer drawer and poor judgement in opening a drawer without knowing the effect it would have on the plant.
Corrective actions include labeling the potential transformer drawers, identifying equipment or panels t at have interlocks or special sensitivity for equipment actuation, and issuing guidance to personnel on opening switchgear doors.
. .'5nclosure to TXX 91077 NRC FORM 3a0A , u.6. Nucd AR ne otAA roRY COWW888CN APPROWD OMt NO. 31t00104 ESTIMATED DURDEN PER RES SE O COMPLY WTH TH18 PFonMATioN LICENSEE EVENT REPORT (LER)- MC'%,g','; ,'f"geg,",*,S
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- l. DESCRIPTION.0F_THE REPO'1 TABLE EVENT A. REPORTABLE EVENT CLASSIFICATION ,
Any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System.
B. PLANT OPERATING COND!TIONS PRIOR TO THE EVENT On February 10,1991, just prior to the event, Comanche Peak Steam Electric Station (CPSES) Unit 1 was in Mode 1, Power Operation, with reactor power at 80 percent.
C. STATUS OF STRUCTURES, SYSTEMS, OR COMPONENTS THAT WERE INOPERABLE AT THE START OF THE EVENT AND THAT CONTRIBUTED TO THE EVENT There were no inoperable structures, systems or components that contributed to the event.
D. NARRATIVE
SUMMARY
OF THE EVENT, INCLUDING DATES AND APPROXIMATE TIMES At 0530 on February 10,1991, an Auxiliary Operator (AO) (utility, non licensed) was conducting on the-job training with a trainee (utility, non licensed). The AO and trainee were trying to locate the reset switches for the Circulating Water Pumps 103 and 1-04 (Ells:(KE)(P)), While looking for the reset switch for Circulating Water -
l Pump 103, the AO opened the potential transformer drawer (Ells:(EA)(FD)) at the L bottom of the switchgear bus "1 A3" auxiliary cubicle (Ells:(EA)(BU)). The AO did not i realize that the drawer was position interlocked with fuses for the bus undervoltage load shed circuitry (Ells:(EA)(RLY 94)). There was no warning or caution label on
~
the drawer. Opening the drawer resulted in a load shed signal for the bus loads,
- which included Reactor Coolant Pump 103 (Ells
- (AB)(P)), followed by a reactor trip due to loss of flow in reactor coolant loop 3. Also lost when the drawer was opened were Condensate Pump 1-01 (Ells:(SG)(P)), Turb!ne Plant Cooling Water Pump 1-01 (Ells:(KB)(P)) and Service Air Compressor 1-01 (Ells:(LF)(CMP)). Circulating Water Pump 1-03 (Ells:(KE)(P)) would also have tripped if it had been in service.
Folbwing the trip, Control Room personnel responded in accordance with J
i
. Enclosure to TXX 91077 NRC FORM 366A U.$sNUGli AR R4 GMIORY COMW$$ ION gpFROWD OMS NO 3166 0104
($1edATED BURDEN PER Rt8 NSE County wifw THis p*oRuAttoN LICENSEE EVENT REPORT (LER) Q'ty%g','; y','","*cl[o"*70 E'uEi TEXT CONTINUATION 'g"f7g,y,@,',ll$^70 f,7,"l$3cQ7,Q '
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COMANCHE PEAK - UNIT 1
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0IO OI3 OF 017 emergency operating procedures. Plant systems responded as expected, except for the situations discussed below. The plant was stabilized in Mode 3, Hot Standby, at 0632. At 0720 the NRC was notified of the event via the Emer0ency Notification System in accordance with 10CFR50.72.
Following the reactor trip, three momentary Steam Generator level signals (Ells:(JE)(RLY 83)) were received. LO LO Level signals were received for Steam Generators 2 and 3 at approximately 1.69 seconds and a HI HI Level signal was received for Steam Generator 2 at approximately 2.18 seconds after the trip. The Turbine Driven Auxiliary Feedwater Pump (Ells:(BA)(P)) did not start and Steam Generator Blowdown and Sampling (Ells:(KN)(RLY 56)) did not isolate. A Main Feedwater isolation signal was generated as a result of the Hi HI Level signal with Main Feedwater Pump 1 A tripping (Ells:(SJ)(P)). Main Feedwater Pump 1B did not trip. The steam dump turbine load rejection interlock (Ells:(JI)(IEL)) would not reset.
i i The momentary Steam Generator level signals had been previously identified in i another event as the resu!t of steam pressure oscillations following a turbine trip.
l Two channels on all four Stearn Generators are susceptible to low level spikes and two channels on Steam Generators 1 and 2 are susceptible to high level spikes. The l
level transmitters share the same impulse lines as the steam flow transmitters and as l a result, the narrow range level transmitters are susceptible to level spikes whenever l rapid changes in steam flow occur Due to the short duration of the spikes, less than 0.2 seconds, the signals were not present long enough to start Turbine Driven Auxiliary Feedwater Pump, isolate Steam Generator Blowdown and Sampling, or trip l Main Feedwater Pump 18. During the post trip recovery the slave relays for these signals were tested and showed that both trains were satisfactory and would respond as designed to actual Steam Generator LO LO or HI HI signals. A bad Lead / Lag card was found in the Steam Dump Turbine Load Rejection circuitry which l was replaced and calibrated with all alarms functioning and the interlock resetting correctly.
E. THE METHOD OF DISCOVERY OF EACH COMPONENT OR SYSTEM FAILURE OR PROCEDURAL ERROR The reactor trip was annunciated by numerous alarms in the Control Room. The immediate cause of the trip was reported by the AO.
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0IO Ol4lOF 017 n.u, _ . - ~ w n w ..On ll. COMPONENT OR SYSTEM F AILURES A. FAILURE MODE, MECHANISM, AND EFFECT OF EACH FAILED -
COMPONENT No failed components contributed to this event.
B. CAUSE OF EACH COMPONENT OR SYSTEM FAILURE No failed components contributed to this event.
C. SYSTEMS OR SECONDARY FUNCTIONS THAT WERE AFFECTED BY FAILURE OF COMPONENTS WITH MULTIPLE FUNCTIONS No failed components contributed to this event.
D. FAILED COMPONENT INFORMATION No failed components contributed to this event.
Ill. ATLA 1.YSIS OF THE EVENT A. SAFETY SYSTEM RESPONSES THAT OCCURRED The Reactor Protection System (Ells:(JC)) and Auxiliary Feedwater System (Ells:(BA)) actuated during the event; all associated components within these systems functioned as designed. The Steam Generator level signals received immediately after the trip were not valid signals, as explained above, and did not affect the safe shutdown or recovery of the plant.
B. DURATION OF SAFETY SYSTEM TRAIN INOPERABILITY No safety system trains were inoperable as a result of this event.
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0l0 015 OF 017 u.i s - . - ~-A ., o n C. SAFETY CONSEQUENCES AND IMPLICATIONS OF THE EVENT The reactor trip was the resuu of the loss of Roactor Coolant Pump 1-03. The reactor trip event is discussed in Section 15.3.1 of the CPSES Final Safety Analysis Report under " Partial Loss of Forced Reactor Coolant Flow." The analysis uses conservative assumptions to demonstrate that Departure from Nucleate Boiling Ratio (DNBR) will never decrease below the limiting value of 1.30 during the event. The event of February 10,1991, occurred at 80 percent reactor power, and all protective functions responded as designed. The event is completely bounded by the FSAR accident analysis which assumes an initial power level of 102 percent and makes conservative assumptions which reduce the capability of safety systems to mitigate the consequences of the transient. The event of February 10 did not adversely affect the safe operation of CPSES Unit 1 or the health and safety of the public.
IV. C AUSE OF THE EVENT A. ROOT CAUSE
- 1. The 6.9 KV switchgear bus "1 A3" auxi'iary cabinet potential transformer drawer did not have an adequate label. This drawer contains a vital position interlock with bus undervoltage load shedding circuitry, but was not labeled as such.
- 2. The AO used poor judgement in opening a drawer without knowing the effect it would have on the plant. Operators are expected to know the result of any action they take in the plant.
B. GENERIC CONSIDERATIONS Similar equipment needs to be identified and labeled to prevent similar events from occurring.
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0i0 016 OF 0l7 u o - - ~ ~w- =A .ni n V. CORRECTIVE ACTIONS CORRECBVE ACBONS TO PREVENT RECURRENCE A. ROOT CAUSE i
- 1. The 6.9 KV switchgear bus "1 A3" auxiliary cabinet potential Ensformer drawer did not heve an adequate label.
CORRECBVE ACBON Labels have been affixed to the 6.9 KV switchgear bus "1 A1", "1 A2", "1 A3", and "1 A4" auxiliary cabinet potential transformer drawers.
- 2. The AO used poorjudgement in opening a drawer without knowing the effect it would have on the plant. Operators are expected to know the result of any action they take in tha plant.
CORRECTIVE ACTION Operations Management has issued a memorandum that provides additional guidance on opening switchgear doors. This memorandum has been included in the Control Room " Lessons Learned" notebook.
B. GENERIC CONSIDERATIONS Similar equipment needs to be identified and labeled to prevent similar events from occurring.
CORRECTIVE ACTION A survey will be conducted to identify equipment that could cause similar
- problems. The equipment will be labeled appropriately. .
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VI. PREVIOUS SIMILAR EVENTS There have been no previous reactor trips attributed to the causes identified during this event investigation. No previous reactor trips have been caused by personnel taking action in the plant that was not covered by a procedure or work control process, nor have any previous reactor trips been caused by insufficient labeling of plant equipment.
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The times listed in the report are approximate and Central Standard Time, L
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