|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E8021999-10-0707 October 1999 CPSES Unit 1 Cycle 8 Colr ML20217G4151999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Cpses,Units 1 & 2 ML20212F7671999-09-24024 September 1999 SER Granting Relief Request C-4 Pursuant to 10CFR50.55a(g)(6)(i) for Unit 2,during First 10-year ISI Interval & Relief Requests B-15,B-16 & B-17 Pursuant to 10CFR50.55a(g)(6)(i) ML20216J5701999-09-16016 September 1999 Rev 2 to CPSES Unit 2 Cycle 5 Colr TXX-9920, Monthly Operating Repts for Aug 1999 for Cpses.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Cpses.With ML20211M2981999-08-0606 August 1999 Rev 1 to CPSES Fuel Storage Licensing Rept, CPSES Credit for Soluble Boron & Expansion of Spent Fuel Storage Capacity, Consisting of Revised Title Page and 4-1 ML20210U4081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Cpses,Units 1 & 2 ML20210D8321999-07-23023 July 1999 Safety Evaluation Accepting Relief Requests Re Use of 1998 Edition of Subsections IWE & Iwl of ASME Code for Containment Insp ML20209H7661999-07-15015 July 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Comanche Peak Steam Electric Station,Units 1 & 2 ML20209H2721999-07-0909 July 1999 2RF04 Containment ISI Summary Rept First Interval,First Period,First Outage ML20209H2631999-07-0909 July 1999 2RF04 ISI Summary Rept First Interval,Second Period,Second Outage ML20209G7501999-07-0808 July 1999 SER Finding That Licensee Individual Plant Exam of External Events Complete with Regard to Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given Design, Operation & History of Comanche Peak Steam Electric Station ML20196L0191999-07-0808 July 1999 Safety Evaluation Granting Request Relief B-6 (Rev 2),B-7 (Rev2),B-12,B-13,B-14 & C-9,pursuant to 10CFR50.55a(g)(6)(i).Technical Ltr Rept Also Encl ML20210J9391999-06-30030 June 1999 CPSES Commitment Matl Change Evaluation Rept 0003,for 970802-990630 ML20209G0801999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Cpses,Units 1 & 2 ML20196J0621999-06-29029 June 1999 Safety Evaluation Supporting Proposed Changes to Emergency Plan Re Licenses NPF-87 & NPF-89 Respectively ML20195G5141999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Comanche Peak Steam Electric Station,Units 1 & 2.With ML20216E0711999-05-21021 May 1999 1999 Graded Exercise - Comanche Peak Steam Electric Station ML20206Q0091999-05-14014 May 1999 Safety Evaluation Accepting GL 92-08, Thermo-Lag 330-1 Fire Barriers, Dtd 921217,for Comanche Peak Electric Station,Unit 1 ML20206H2061999-05-0606 May 1999 SER Accepting Exemption to App K Re Leading Edge Flowmeter for Plant,Units 1 & 2 ML20196L2241999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Cpses,Units 1 & 2 ML20205R5701999-04-14014 April 1999 Rev 6 to ER-ME-067, TU Electric Engineering Rept,Evaluation of Thermo-Lag Fire Barrier Sys ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205J7831999-04-0101 April 1999 Rev 0 to ERX-99-001, CPSES Unit 2 Cycle 5 Colr ML20205N3101999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Cpses,Units 1 & 2 ML20204H6371999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Comanche Peak Units 1 & 2 ML20205N1481999-02-28028 February 1999 Corrected Monthly Operating Rept for Feb 1999 for CPSES, Units 1 & 2 ML20203A4881999-02-0303 February 1999 Safety Evaluation Granting Requests for Relief B-3 - B-6,C-2 & C-3 for Plant,Unit 2 ML20210J9201999-02-0101 February 1999 CPSES 10CFR50.59 Evaluation Summary Rept 0008,for 970802- 990201 ML20202D0101999-01-27027 January 1999 Safety Evaluation Supporting First 10-yr Interval ISI Program Plan Requests for Relief B-9,B-10 & B-11 for CPSES, Unit 1 ML20199E9961998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Cpses,Units 1 & 2 ML20207D6091998-12-31031 December 1998 1998 Annual Operating Rept for Cpses,Units 1 & 2. with ML20197K2371998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Cpses,Units 1 & 2 ML20195F3161998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Cpses,Units 1 & 2 ML20154M8841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Cpses,Units 1 & 2 ML20154B5741998-09-30030 September 1998 Safety Evaluation Re Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Motor-Operated Valves. Licensee Has Established Acceptable Program ML20151W0361998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Cpses,Units 1 & 2. with ML20151Q1211998-08-14014 August 1998 Rev 0 to Control of Hazard Barriers ML20237C4061998-08-14014 August 1998 Safety Evaluation Supporting Request to Implement Risk Informed IST Program ML20237C6721998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Cpses,Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236R0711998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Cpses,Units 1 & 2 ML20249B2581998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Cpses,Units 1 & 2 ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20247G3241998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Cpses,Units 1 & 2 ML20216B8661998-04-0101 April 1998 Rev 0 to ERX-98-001, CPSES Unit 1 Cycle 7 Colr ML20216J3061998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Cpses,Units 1 & 2 ML20216J1861998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Comanche Peak Steam Electric Station ML20197A6951998-02-24024 February 1998 Inservice Insp Summary Rept,First Interval,Second Period, First Outage ML20199J5391998-02-0202 February 1998 CPSES Commitment Matl Change Evaluation Rept 0002 for 960202-970801 1999-09-30
[Table view] |
Text
. _ _ _ _ _ _
Y *
=
I
=
~~2
=
Log # TXX-91145 File # 10200 Ref. # 50.73(a)(2)(v) nlELEC7RIC April 25, 1991
?$$!$l?$
U. S. Nuclear Regulatory Comission Attn Document Control Desk Washington, D. C. 20555
$UBJECT: COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)
DOCKET NO. 50-445 EVENT OR CONDITION THAT COULD HAVE PREVENTED FULFILLMENT OF THE SAFETY FUNCTION OF STRUCTURES OR SYSTEMS LICENSEE EVENT REPORT 91-012-00 Gentlemen:
Enclosed is Licensee Event Report 91-012-00 for Comanche Peak Steam Electric Station Unit 1. " Potential Gas Binding of Centrifugal Charging Pumps due to Voids its the Boric Acid Gravity Feed Line."
Sincerely.
William J. Cahill Jr.
By: _[
Manager. Site Lit'nsing JAA/bm c - Mr. R. D. Martin, Region IV ResidentInspectors.CPSES(2)
(l 26 0 /10
,mnm, so., un. n n no_ u2o, ['
{hg42gggggg;gggjp
Enclosure to TXX 91145 j' NHC IOHW Dee U $ N44 L AH H6 uAAIL)HV (41WWibn>N WW D e cwM. W..S.M OW E81NAftD DucLN PER M 889 Net 10 00MPLT Wf1H THit NIORWATKW M LLC 1 KIN Mi & l311 60,0 HRS FONWAC 00WW(NTS REGAIMANO
" " * ' " " ' " ' ' ' ' '"5*****'*""""***'"'"'"'
LICENSEE EVENT REPORT (LER) BRAWH (P 6X1), u 8. NUCLE AR M OLil Af D8tY COWWS$KsN, W A9HINGTON EC Nebs, AND 10 THE PAP (RWORK REDUCTKIN PROJICT Q@01041
- 38 fICC Of uANA(W WI NT AND IkKKitT. WASHINGin8( DC. M603.
r.-,N m w w,,.. m r-COMANCHE PEAK - UNIT 1 015101010l4l4l5 1I (* IOt6 POTENTIAL GAS BINDING OF CENTRIFUGAL CHARGING PUMPS DUE TO VOIDS IN THE BORIC ACID GRAVITY FEED LINE
, ,..u.. e a .,. . m,. m o, .. -. -
n., v, v J 'e c 9 e= W.+ o., v,
' ;g - ppg i o , o , , ,
. 013 21s 91 911 01112 w........s.,,~,-..
010 014 215 9 11
. . ... ,ownrcu N/A
.. . ,n_,
0151010101 1 I a,
- =** 5 _ n ewm _ n.== no ruxm _ mnm n,
_ namne _ uwam Z no2=.umm _ nnm T 01010 -
_ m.
" **m*0 enneH'8 wwem nonmmm m>>=mee se23.unweiA3 cm.ts,-4, Nac t.= m At- wi . wmT.4 i ,> ,,,,, N.06 tax 1Hh4 _ 90 72.HB(it _ to tt. Mane (s) en <www mem umt. w .
L t.no Cc.i d l . Iht. LI R Ch u,,,. ,. ,,,n w .
T. A. HOPE COMPLIANCE SUPERVISOR 8I'll* 7 81917 l- l 613 I 710 c . o ti,.r.s.*c ...e.u.t .,vi n. ina c ,, er. co , a u.,,oin,. ,Wa A '
c.= or. , c.w- u. sm,,,.,
.M.a s <>q l l l l l l l I l Il l l l l l l l l l l l MRA l l l l l l l uM'
. . a u -.,n. . ,, W- % ..
$Jw.e.e.n Ov <> , . r a.4 sei . o. i G l l l
=,,- p .ac . . i. . . ~ , *, o .- , , n.,
Ultrasonic examination of the Chemical and Volume Control System (CVCS) suction piping was performed on March 4, through March 15,1991. These examinations revealed volds in the alternate boration line and the gravity feed line from the Boric Acid Storage Tank (BAT) Engineering evaluation shows that volds in the alternate boration line would not affect operability of the Centrifugal Charging Pumps (CCPs). However, engineering evaluation indicates that the vold in the gravity feed line from the BAT could cause damage to or gas binding of the CCPs.
The potential root cause was identified as hydrogen coming out of solution, in the lower
- pressure CCP suction header. Corrective actions include daily venting of the gravity feed line and further monitoring for hydrogen accumulation. Based on the results of this monitoring, venting requirements will be established.
Enclosure to TXX 91145 m , o,. a wa .oa.4 A m .m.m,u., ,,,,, ,oc . . , ,,,
( $f W Ail D 9V6C4 N P(R R $f f Msgy Wtf H THis WORW A Oh LICENSEE EVENT REPORT (LER) pg,,'y",,'Z','; ,"j ""*c/, n",*gg',',"l'f,,",*,
TEXT CONTINUATlON j c
""",ci u u*wat a Ae amt t wasa,evouc m3"i$l1 $' ,"Z' x
, m., w. m u.. ,. ei a 6 - .o , r. a
" e ,k * [.
COMANCHE PEAK - UNIT 1 015101010141415 911 Ol1l2 -
0IO Ol2 OF 016 u.nm ... . .- . +,a - ,.a .> o n
- 1. DESCRIPTION OF THE REPORTABLE EVENT ,
y A. REPORTABLE EVENT CL ASSIFICATION Any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to shutdown the reactor and maintain it in a safe condition, or mitigate the consequences of an accident.
B. PL ANT OPERATING CONDITIONS PRIOR TO THE EVENT On March 26,1991, Comancho Peak Steam Electric Station (CPSES) Unit 1 was in Mode 5, Cold Shutdown, with the Reactor Coolant System (RCS) (Ells:(AB)) at a temperature of 130 Jegrees Fahrenholt and pressure of approximately 300 pounds per square Inch-gage.
C. STATUS OF STRUCTURES. SYSTEMS OR COMPONENTS THAT WERE INOPERABLE AT THE START OF THE EVENT AND TH AT CONTRIBUTED TO THE EVENT There were no inoperable structures, systems or components that contributed directly to the event.
D. N ARR ATIVE
SUMMARY
OF THE EVENT. I'ACLUDING DATES AND APPROXIM ATE TIMES On October 29,1990, Westinghouse sont a Is'ter to CPSES regarding the formation and venting of hydrogen in the Chemical and Volume Control System (CVCS)
(Ells:(CB)) in response to Nuclear Regulatory Commission (NRC) Information Notice (lN) 90 64," Potential for Common Mode Failure of High Pressure Safety injection Pumps or Release of Reactor Coolant Outside Containment During a Loss of-Coolant Accident." In this letter Westinghouse, identified locations in the CVCS suction piping where gases would tend to accumulate. Westinghouse recommended ultrasonic examination to monitor the rate at which gas accumulates in these locations.
l 1
Enclosuro to TXX 91145 NHC pong seeA U.S 14dCLL A14 llLQJLAlpN, (OMWi$$m gppqgygg ggg gg gg ggg,,
(511MA1TD DV86 DEN PtR & St t uptv WitH tHl8 9#0nWAtloN LICENSEE EVENT REPORT (LER) 3',Cs'g','; ,' l"ggin,*^", g%'gfg, a
TEXT CONTINUATlON f
' " "f Li ,"f, $ '","," g ' O cg *'8 0
- 7 0 af fICE OF MANAuf WLNT AND BUDO& t.W ASHINOTON DC_20V4
> ~., m w ,,- m a n, a COMANCHE u.n. .,_ . -
PEA K - UNIT 1
..u, - w .4 % n 015101010141415 911 -
0'1l2- 010 013 OF 0lB From March 4,1991, through March 15,1991, ultrasonic examination of various locations of the CVCS suction piping was performed. Locations examined included the 8 inch diameter suction header; the Positive Displacement Charging Pump (PDP) (Ells:(P)(CB)) suction line; the Centrifugal Charging Pump (CCP) 02 (Ells:(P)(CB)) mlniflow line; and all of the vertical piping connected to the 8 inch diameter suction header, including alternate boration, boric acid filter, chemical feed, and the gravity feed line from the Boric Acid Storage Tank (BAT) (Ells:(TK)(CB)).
The ultrasonic examinations revealed volds in two locations, the 2 inch diameter alternate boration line and the 3 inch diameter gravity feed line from the DAT. The size of the vold Identified in the alternate boration line was determined to bo relatively small. Engineering evaluation shows that a void in this line would not cause any significant degradation in CCP or PDP performance, or affect operability of the Emergency Core Cooling System (ECCS)(Ells:(BO)). The size of the vold.
found in the BAT gravity feed line was much larger. Engineering evaluation indicates that this void could potentially cause damage to or gas binding of the CCPs when the BAT gravity feed line is used for boration, forcing the gas bubble into the suction header, or when pr_ essure conditions change causing expansion of the bubble into the suction header.
On March 26,1991, this event was recorded via the appropriate administrative procedure. The reportability of this event was uncertain at first, however, after further evaluation it was determined to be reportable at 1645 on March 28,1991. At 1840 t on March 28,1991, the NRC Operations Center was notified via the Event Notification System.
E.
i THE METHOD OF DISCOVERY OF EACH COMPONENT OR SYSTEM FAILURE OR PROCEDURAL ERROR
- Ultrasonic examination of various locations of the CVCS suction piping was performed due to cocerns expressed by Westinghouse in their October 29,1990, !
letter. As a result of the examinations, conducted from March 4,1991, through March 15,1991, volds in two locations of CVCS suction piping were identified.
Enclosure to TXX 91145 NRC FORW 3%A U $ NtCL( AR HLOiAATORY COWWISSON AmetM00We W Nm (BilWATID BURDIN PER R i TO WMV Wif H THis IN80HWA f DN LICENSEE EVENT REPORT (LER) ;To?,'",,"j,y','; ,'",* 0$go'?",*0 %@"Jys"*,
TEXT CONTINUATION '"'*******'*"'*'"
- "'*" '"* "" " "'" "' *"8tIDL1CT ON P840Jt ct (s ik> ctDai 3C FJ66L AND TO THE PAPIfewoRet af FCf OF MANAGEWENT AND BJLGI1 % A9HI,$31ON. (C 20h03
, m.,N.,. m -
. m . N . ei .6 a N~ le r. a
'~ W: W:
COMANCHE 3..n. ~, . . - . mi PEAK .
NIT 1
- Umm.mn0151010l0141415 911 -
0l112 -
0IO OI4 OF 016 ll. COMPONENT OR SYSTEM FAILURES A. FAILURE MODE. MECH ANISM. AND EFFECT OF EACH FAILED COMPONENT Not applicable there were no component failures associated with this event.
B. CAUSE OF EACH COMPONENT OR SYSTEM FAILURE Not applicable there were no component failures associated with this event, C. S_YSTEMS OR SECONDARY FUNCTIONS THAT WERE AFFECTED BY FAILURE OF COMPONENTS WITH MULTIPLE FUNCTIONS Not applicable there were no component failures associated with this event.
D. FAILED COMPONENT INFORM ATION Not applicable there were no component failures associated with this event, Ill. AN ALYSIS OF THE EVENT A. SAFETY SYSTEM RESPONSES THAT OCCURRED Not applicable - there were no component failures associated with this event, B. DUR ATION OF SAFETY SYSTEM TRAIN INOPER ABILITY Not applicable there were no safety systems which were rendered inoperable due to a failure,
\/ ^^
Enclosure to TXX 91145 we ,os ,,o u . Nm6 Amummwoaw ,,,,,,,nc,,,,,,,,
L STwAT(D pasot N P(R M i bi TO CC MptV W!TH Tutt W5'04WATON LICENSEE EVENT REPORT (LER) lf,'3t,'7",,"3','; ,",'"l$co'ln"l^"o ',j%%'f;'u"Z,
'"'*"'""'""'"'**^**""****"*'*
TEXT CONTINUATION % P0666. AND TO THE PApt AWOHK HE DUC10N P840 JECT (31 WOW 1 J F CE (F WANAGI MENT AND DJ(UET, W ASHINGTON (C RW12 6 e..ny un, oj ;mei Wave la LE R 6"aw $ be di
~ tw w;:
COMANCHE PEAK
..m.. -,-- UN.IT 015101010141415 1 ., o n
~.a 911 -
0I1l2 -
010 OIS OF 016
-..n. .m.. .
C. SAFETY CONSEQUENCES AND IMPLICATIONS OF THE EVENT The operability of two independent ECCS subsystems, as required by Technical Specifications 3/4.5.2, ensures that sufficient emergency core cooling capability will be available in the event of a Loss of Coolant Accident assuming the loss of one subsystem through any single failure consideration. Either subsystem operating in conjunction with the accumulators (Ells:(ACC)(BP)) is capable of supplying sufficient core cooling to limit the peak cladding temperatures within acceptable limits.
During this event the potential for gas binding of the CCPs existed due to void accumulation in the CVCS suction piping. This increased the probability of a common mode failure of both independent ECCS subsystems.
IV. CAUSE OF THE EVENT ROOT C AUSf, Evaluation of this event has identified the potential root cause to be hydrogen coming out of solution in the lower pressure CCP suction header and collecting in the vertical piping.
This phenomenon is not present under current plant conditions (Mode 5), and therefore cannot be verified until normal RCS hydrogen concentration is re established.
V. CORRECTIVE ACTIONS A. Ifg1EDIATE The gravity feed line from the BAT was vented. Administrative controls were established to vent this line daily.
1 L . ' ', l Enclosure to TXX 91145 !
NitC 5ORW 3664 U 0 AAAI A4 f46 GJLAlDNV COWWiMION WMD W9 m WW (9flWA1(D BL)R:XN PER hta NGE TO W8%Y WTH THIS Pe0RWatKW LICENSEE EVENT REPORT (LER) 33,,,%,*','; ,"/",L'fo",*!" (07,',gg, TEXT CONTINUATION Of g,*,W,',,",agi','W ASHING TON. 00. Etc1 58C4 0F MANAQiWENT AND DVDGET eaosay Name(1) inseien N,nw pp LE R hwate lei Fap (Ji v.- '
W3.* 1 er C,u OMANCHE PEAK - UNIT uw- us1., o n 015101010l414l5 911 -
0l1l2 -
010 018 OF 0l8 1
B. CORRECTIVE ACTIONS TAKEN TO PREVENT RECURRENCE ROOT CAUSE Evaluation of this event has identified the potential root cause to be hydrogen coming out of solution in the lower pressure CCP suction header and collecting in the vertical piping.
CORRECTIVE ACTION The gravity feed line from the BAT will be monitored for hydrogen accumulation upon return to normal hydrogen concentration in the RCS Based on the results of this
' monitoring, venting requirements will be established.
VI. PREVIOUS SIMILAR EVENTS On October 4,1990, NRC IN 90 64 was issued. During evaluation of IN 90 64 it was concluded that a design error existed that could result in the common mode failure of the CCPs due to gas binding (the CCP suction piping, high point, solenold opereted isolation vent va!ves (SOLV) (Ells:(FSV)(CB)) were oriented in the wrong direction). This condition wae addressed in Licensee Event Report (LER) 90 035.
As a result of tha October 29,1990, letter from Westinghouse addressing the SOLV orientation, various locations in the CVCS suction piping were identified as having the pntential for gas to accumulate. The subsequent ultrasonic examinations are the subject of this LER (91012).
Vll. ADDITIONAL INFORMATION The times listed in the report are approximate and Central Standard Time.
l
__ _ . . - . _ ..___. _ _ _ _ _ . _ __ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _