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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E8021999-10-0707 October 1999 CPSES Unit 1 Cycle 8 Colr ML20217G4151999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Cpses,Units 1 & 2 ML20212F7671999-09-24024 September 1999 SER Granting Relief Request C-4 Pursuant to 10CFR50.55a(g)(6)(i) for Unit 2,during First 10-year ISI Interval & Relief Requests B-15,B-16 & B-17 Pursuant to 10CFR50.55a(g)(6)(i) ML20216J5701999-09-16016 September 1999 Rev 2 to CPSES Unit 2 Cycle 5 Colr TXX-9920, Monthly Operating Repts for Aug 1999 for Cpses.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Cpses.With ML20211M2981999-08-0606 August 1999 Rev 1 to CPSES Fuel Storage Licensing Rept, CPSES Credit for Soluble Boron & Expansion of Spent Fuel Storage Capacity, Consisting of Revised Title Page and 4-1 ML20210U4081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Cpses,Units 1 & 2 ML20210D8321999-07-23023 July 1999 Safety Evaluation Accepting Relief Requests Re Use of 1998 Edition of Subsections IWE & Iwl of ASME Code for Containment Insp ML20209H7661999-07-15015 July 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Comanche Peak Steam Electric Station,Units 1 & 2 ML20209H2721999-07-0909 July 1999 2RF04 Containment ISI Summary Rept First Interval,First Period,First Outage ML20209H2631999-07-0909 July 1999 2RF04 ISI Summary Rept First Interval,Second Period,Second Outage ML20209G7501999-07-0808 July 1999 SER Finding That Licensee Individual Plant Exam of External Events Complete with Regard to Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given Design, Operation & History of Comanche Peak Steam Electric Station ML20196L0191999-07-0808 July 1999 Safety Evaluation Granting Request Relief B-6 (Rev 2),B-7 (Rev2),B-12,B-13,B-14 & C-9,pursuant to 10CFR50.55a(g)(6)(i).Technical Ltr Rept Also Encl ML20210J9391999-06-30030 June 1999 CPSES Commitment Matl Change Evaluation Rept 0003,for 970802-990630 ML20209G0801999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Cpses,Units 1 & 2 ML20196J0621999-06-29029 June 1999 Safety Evaluation Supporting Proposed Changes to Emergency Plan Re Licenses NPF-87 & NPF-89 Respectively ML20195G5141999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Comanche Peak Steam Electric Station,Units 1 & 2.With ML20216E0711999-05-21021 May 1999 1999 Graded Exercise - Comanche Peak Steam Electric Station ML20206Q0091999-05-14014 May 1999 Safety Evaluation Accepting GL 92-08, Thermo-Lag 330-1 Fire Barriers, Dtd 921217,for Comanche Peak Electric Station,Unit 1 ML20206H2061999-05-0606 May 1999 SER Accepting Exemption to App K Re Leading Edge Flowmeter for Plant,Units 1 & 2 ML20196L2241999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Cpses,Units 1 & 2 ML20205R5701999-04-14014 April 1999 Rev 6 to ER-ME-067, TU Electric Engineering Rept,Evaluation of Thermo-Lag Fire Barrier Sys ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205J7831999-04-0101 April 1999 Rev 0 to ERX-99-001, CPSES Unit 2 Cycle 5 Colr ML20205N3101999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Cpses,Units 1 & 2 ML20204H6371999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Comanche Peak Units 1 & 2 ML20205N1481999-02-28028 February 1999 Corrected Monthly Operating Rept for Feb 1999 for CPSES, Units 1 & 2 ML20203A4881999-02-0303 February 1999 Safety Evaluation Granting Requests for Relief B-3 - B-6,C-2 & C-3 for Plant,Unit 2 ML20210J9201999-02-0101 February 1999 CPSES 10CFR50.59 Evaluation Summary Rept 0008,for 970802- 990201 ML20202D0101999-01-27027 January 1999 Safety Evaluation Supporting First 10-yr Interval ISI Program Plan Requests for Relief B-9,B-10 & B-11 for CPSES, Unit 1 ML20199E9961998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Cpses,Units 1 & 2 ML20207D6091998-12-31031 December 1998 1998 Annual Operating Rept for Cpses,Units 1 & 2. with ML20197K2371998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Cpses,Units 1 & 2 ML20195F3161998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Cpses,Units 1 & 2 ML20154M8841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Cpses,Units 1 & 2 ML20154B5741998-09-30030 September 1998 Safety Evaluation Re Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Motor-Operated Valves. Licensee Has Established Acceptable Program ML20151W0361998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Cpses,Units 1 & 2. with ML20151Q1211998-08-14014 August 1998 Rev 0 to Control of Hazard Barriers ML20237C4061998-08-14014 August 1998 Safety Evaluation Supporting Request to Implement Risk Informed IST Program ML20237C6721998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Cpses,Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236R0711998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Cpses,Units 1 & 2 ML20249B2581998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Cpses,Units 1 & 2 ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20247G3241998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Cpses,Units 1 & 2 ML20216B8661998-04-0101 April 1998 Rev 0 to ERX-98-001, CPSES Unit 1 Cycle 7 Colr ML20216J3061998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Cpses,Units 1 & 2 ML20216J1861998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Comanche Peak Steam Electric Station ML20197A6951998-02-24024 February 1998 Inservice Insp Summary Rept,First Interval,Second Period, First Outage ML20199J5391998-02-0202 February 1998 CPSES Commitment Matl Change Evaluation Rept 0002 for 960202-970801 1999-09-30
[Table view] |
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_ _- File # 10200'- ;
907.3 C C 910.4 '
1UELECTRIC 915 2 Ref. # 50.73 (a)(2)(iv)
E ifNe e,nu,,,, June 26, 1990
- s.
U. S. Nuclear Regulatory Commission i Attn:
Document Control Desk Washington, D.,C. 20555
SUBJECT:
COMAN'CHE PEAK STEAM ELECTRIC STATION !
DOCKET N0..50-445
. ENGINEERED SAFETY FEATURE ACTUATION LICENSEE EVENT REPORT 90-017-00 Gentlemen: . t Enclosed is Licensee Event Report 90-017-00 for Comanche Peak Steam Electric
' Station Unit 1, " Reactor Trip Due to Feedwater Control Valve Solenoid failure."
Sincerely, l_ '
William J. Cahill, Jr.
FSP/dai Enclosure c - Mr.-R. D. Martin, Region IV
' Resident Inspectors, CPSES (3) i i
. 9006280113 900626
/
PDR- ADOCK 03000445 S~ PDC SX) North Ohve Street LB81 Dallas. Texas 75201
1 Enclosure to TXX 90213 j NRC FORM 306 - , U.S. NUCLE AR REGULATORY COMMIS$ON APPROVED OMB NO. 31640104
+ EXPIRE 8:4/3492 ESilMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATON COLLECTON REQUEST: 60.0 HRS. FORWARD COMMENTS REGARDING BUR EN ESMATE T THE RECORDS AND REPORTS MANAGEMENT LICENSEE EVENT REPORT (LER) BRANCH (P430), U.S. NUCLEAR REOULATORY COMMISSION, WASHINGTON,
- 30. 20665. AND TO THE PAPERWORa( REDUCTON PROJECT (31640104).
OFFCE OF MANA05 MENT AND BUDGET, WASHINGTON. DC. 20503.
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On May 27,1990, at 0126 while performing Steam Generator Atmospheric Relief Valve (ARV) l capacity testing, a Main Feedwater Flow Control Valve (FCV) failed closed. This resulted in 3 reduced feedwater flow and decreasing Steam Generator (SG) No. 3 water level. The Operator closed the ARV, which was open for test purposes, and started to manually ramp down the main turbine to reduce reactor power. The Operator then opened the bypass flow L control valve around the failed closed FCV, but the SG water level continued to decrease. At L 0128, when No. 3 SG water level reached approximately 30 percent (automatic reactor trip is at L 28 percent GG water level), the operator manually tripped the reactor. All other plant systems operated properly.
The cause of the event was the failure of a solenoid valve coli, associated with No. 3 SG FCV, l due to rain water intrusion (FCV's are located outside). A temporarily removed covar allowed water to enter a junction box then drain via conduit to the solenoid coil housing.
C_orrective action included the replacement of the failed solenoid coil and inspection of the other solenoids for water / moisture intrusion. An evaluation will determine if additional critical components exist in a similar configuration. Guidance for the conduct of outdoor maintenance activities will be addressed programatically.
1 i
1 JEncl,osure to TXX-90213'-
NRC FOHM 306A . U.S. NUCLEAR REOVLA10RY COMM4 SON APPROVED OMB NO. 31660104 ESTIMATED PURDEN PER RES NS T COMPtY WITH THE INFORMATON LICENSEE EVENT REPORT (LER)- ,
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- 1. DESCRIPTION OF THE REPORTABLE EVENT A. PLANT OPERATING CONDITIONS BEFORE THE EVENT On May 27,1990 at 0126, Comanche Peak Steam Electric Station (CPSES) Unit 1
" was in Mode 1, Power Operation, with reactor power at 43 percent. ;
I B. REPORTABLE EVENT CLASSIFICATION !
An event or condition that resulted in the manual or automatic actuation of any b
- Engineered Safety Feature (ESF), including the Reactor Protection System (RPS),
C. STATUS OF STRUCTURES. SYSTEMS. OR COMPONENTS s THAT WERE INOPERABLE AT THE START OF THE EVENT -;
Atip THAT CONTRIBUTED TO THE EVENT Not applicable - no structures, systems, or components were inoperable at the start '
of the event that contributed to the event.
D. NARRATIVE
SUMMARY
OF THE EVENT. INCLUDING DATES AND APPROXIMATE TIMES At 0126 on May 27,1990, the Steam Generator Atmospheric Relief Valve (ARV) 1 (Ells:(RV)(SB)) capacity testing was in progress on Steam Generator (SG)
(Ells:(SG)(AB)) No. 4 when the SG No. 3 Feedwater Flow / Steam Fbw Mismatch -
Alarm (Ells:(ALM)(IB)) annunciated. The Reactor Operator (utility-licensed) observed the Main Feedwater Flow Control Valve (FCV)(Ells:(FCV)(SJ)) to SG No. 3 i indicated fully closed with a 100 percent open demand on the controller. A few seconds later, a SG No. 3 Low Level Alarm (Ells:(ALM)(IB)) annunciated. The Unit Supervisor (utility licensed) ordered the SG No. 4 ARV closed and the Main Feedwater Flow Control Bypass Valve (Ells:(FCV)(SJ)) to SG No. 3 opened. The Flow Control Bypass Valve was opened fully to increase feedwater flow to SG No. 3.
At this time SG No. 3 level was at approximately 35 percent. ihe Balance of Plant Operator (utility licensed) reduced load on the main turbine (Ells:(TRB)(TA)) to attempt to reduce steam flow to less than feedwater flow on SG No. 3. A discussion between the Unit Supervisor and the Reactor Operator followed and a decision was made to trip the reactor (Ells:(RCT)(AB)) if SG level could not be stabilized above 30
=_
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, Encl?sure to TXX 90213 NNC FORM 3e6A . U.S. NUCLE AR REOULAl'.)RY COMMISSION APPROWD OMB HO. 3160.tnN ESilMATED BURDEN PER RES NS COMPLY WITH THIS INFORMATION LICENSEE EVENT REPORT (LER) "',C't,"',T8';
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OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON DC.20603.
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percent on narrow range indication. At 0128, when SG level decreased to approximately 30 percent narrow range the Unit Supervisor ordered the Reactor Operator to manually trip the reactor. The reactor was tripped, all rods (Ells:(ROD)(AA)) fully inserted into the core. Steam dumps (Ells:(RV)(SB)) operated-normally. An Auxiliary Feedwater System (Ells:(BA)) actuatloa occurred as a result of Low Low SG Level Signal, and all components functioned as designed. All other plant systems operated properly. The plant was stabilized in Mode 3, Hot Standby.
An intermittent ground on Direct Current (DC) Bus 1 ED2 (Ells:(JA)(EJ)) was noticed the day before the event. This intermittent ground was never indicated for more than 10 seconds. Control Room personnel had reviewed the drawings for DC Bus 1ED2 before the event; however, the ground could not be located since the alarm was intermittent. Also, the loads of DC Bus 1ED2 are not conducive to isolation as they 4 feed protection / control related equipment and to isolate them in Mode 1 would cause a reactor trip. On May 27,1990, after the reactor trip, the ground indication was constant, j An event or condition that results in a manual or automatic actuation of any ESF, including the RPS is reportable within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> under 10CFR50.72(b)(2)(li). At i approximately 0201 on May 27,1990, the' Nuclear Regulatory Commission 1
Operations Center was notified of the event via the Emergency Notification System. 1 E. THE METHOD OF DISCOVERY OF EACH COMPONENT OR SYSTEM i FAILURE OR PROCEDURAL OR PERSONNEL ERROR The closure of SG No. 3 FCV was initially discovered as a result of a Feedwater Flow / Steam Flow Mismatch Alarm annunciation in the control room. Additionally, y intermittent ground alarms were received on DC Bus 1ED2. A Work Order was subsequently initiated to troubleshoot the ground on DC Bus 1ED2, which disclosed v water in the solenoid coil housing and associated conduit.
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010 014 OF 017 ll. COMPONENT OR. SYSTEM FAILUPES A. FAILURE MODE. MECHANISM AND EFFECT OF EACH FAILED COMPONENT The FCV closed because its position controlling solenoid had failed due to electrical grounding caused by water latrusion, resulting in loss of feedwater flow to SG No. 3.
B. CAUSE OF EACH COMPONENT OR SYSTEM FAILURE Water intrusion at the junction box (Ells:(JBX)(SJ)), creating partial submergence of r
the solenoid coll, has been determined to be the cause of the failure. When the i
solenold was disassembled the coil (Ells:(CL)(SJ)) was discovered to be sitting in~ '
cpproximately one inch of water.
C, SYSTEMS OR SECONDARY FUNCTIONS THAT WERE AFFECTED BY FAILURE OF COMPONENTS WITH MULTIPLE FUNCTIONS Not appicette no failures of components with multiple functions have been identified. !
D. EALLFACOMEONDLTMEORMATION 1 FCV 0530 SV1 Solenold Valve Manufacturer: ASCO Valver, Automatic Switch Co.
Model Number: 208 4921W (Solenoid Valve Coll)
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-lll. ANALYSIS OF THE EVENT A. SAEEI_Y_S.YSIBUigSPONSES TH AT OCCURRED. <
The following eLfety system actuations occurred as a result of the event:
Reactor Protection System (Ells:(JC))
Auxiliary Feedwater System (Ells:(BA))
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. =.i1 .m n B. DURATION OF SAFETY SYSTEM TRAIN INOPERABILITY Not applicable - there were no safety systems which were rendered inoperable due to a failure.
C. SAFETY CONSEQUENCES AND IMPLICATICNS OF THE EVENT The Main Feedwater System is designed to provide feedwater to the SGs. The Main Feedwater FCV's regulate feedwater flow to the SGs. Failure of the solenoid coil causes the FCV to close (Fall Safe Position), restricting / isolating feedwater flow to the SGs.
If the event had occurred at full power an automatic reactor trip would have occurred.
However, since the plant was operating at reduced power for testing, the operator was able to shutdown the reactor manually.
i This event is bounded by the Final Safety Analysis Report Accident Analysis (Section 15.2.7) regarding a Loss of Normal Feedwater, which assumes the worst single failure in the Auxillary Feedwater System. However,in this event, an Auxillary Feedwater System actuation occurred and all components functioned as designed.
Therefore, this event did not adversely affect the safe operation of CPSES Unit 1 or the health and safety of the public.
IV. CAUSE OF THE EVENT BOOT _CAUSE Water intrusion into SG No. 3 Main Feedwater Flow Control Valve 1 FCV 0530 Train "B" solenoid assembly (Ells:(SOL)(SJ)) and associated conduit caused the solenold coll to ground. Conduit from the solenoid assembly (approximately six feet long), connects to the bottom of the junction box. The configuration is installed with the junction box slightly elevated with respect to the solenold assembly. Water entering the junction box drained via the conduit into the ,
solenoid assembly, leading to the failure of the coll. It is concluded that the water intrusion resulted from maintenance activities which left the junction box cover I
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temporarily removed during a period of heavy rainfall. This in turn failed the Flow Control Valve closed and restricted / shutoff feedwater flow to SO No. 3, V. CORRECTIVE ACTIONS A. IMMEDIATE The junction box, conduit and solenoid valve housing were cleaned and dried. A new solenoid coil was installed.
B. CORRECTIVE ACTIONS TO PREVENT RECURRENCE ._
Root Cause Failure of SG No. 3 Main Feedwater FCV Train 'B' solenoid coil was caused by water intrusion resulting from outdoor maintenance activities during a period of heavy rainfall.
Corrective Action
- 1. All work organizations will review the event with personnel to stress the need to adequately protect equipment from external environmental conditions during ongoing work activities.
- 2. All work organizations will evaluate their programs to ensure that appropriate guidance is provided prior to performing work on outdoor equipment.
C. CORRECTIVE ACTION TAKEN ON GENERIC CONCERNS IDENTIFIED AS A DIRECT RESULT OF THE EVENT Generic Considerations i
Other solenold assemblies on the FCVs may have had moisture / water intrusion.
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010 017 OF 017 3.c u . . . . . a..e Nw.n mA.m n Corrective Action The Work Order v' . Msed to inspect all the solenoid assemblies on the other Main Feedwater FCV' . a toth i seven. All the solenoid coils were found dry with no signs of previou wator .nrusion. The Work Order also inspected for any other possible metns t v .er intrusion into the solenoid assemblies. No additional ;
intrusion paths we ' ,dentified. Based on the inspection of the other solenoid i assemblies this incident was determined to be an isolated case.
Generic Considerations Additional critical components may exist which have the potential for a similar ,
occurrence.
Corrective Action i The Single Point Failure Analysis identifies critical components whose failure can initiate a sequence of events, resulting in a reactor trip. This analysis will be reviewed to identify outdoor components which have the potential for a similar occurrence as the FCV solenold valve co:1. Inspections will be performed on any identified components.
VI. PREVIOUS SIMILAR EVENTS There have been no previous similar events .eported pursuant to 10CFR50.73.
Vll. AQDlIlRNALINEQBblAIl0B The times listed in the report are approximate ano ae, tral Day Ight Savings Time (CDT).
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