ML20042A530

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LER 82-003/03L-0:on 820224,differential Pressure Switch DPIS 2-1360-1B+ Failed to Operate.Caused by Instrument Drift.Switch Recalibr & Tested Satisfactorily
ML20042A530
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 03/11/1982
From: Reynolds S
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20042A522 List:
References
LER-82-003-03L-02, LER-82-3-3L-2, NUDOCS 8203230526
Download: ML20042A530 (2)


Text

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14 7 60 61 DOCK ET NUMetR 68 43 EVENT OATE 15 REPORTD475 EVENT DESCRIPTION ANO PROS A8LE CONSEQUENCES h i ITTTl l On February 24, 1982, while performing the quarterly RCIC Steam Line High Flow __

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o 2 l Calibration and Functional Test, QlS 18, OPIS 2-1360-1B+ failed to operate. I gl This switch is associated with the DPIS 2-1360-1B differential pressure cell I i

lo is t I which Isolates the RCIC steam line on high flow. The redundant di f ferential I gl pressure cell DPIS 2-1360-I A was found operable and would have isolated the l j

[T{T) l RCIC steam line on high flow. At the time of the calibration, Unit Two had l been shutdown since January 18, 1982, and Primary Containment was

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' 3J J4 36 J6 3 40 el 42 43 l CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h j gl The cause of this occurrence was instrument drif t of the DPIS 2-1360-1B+. l l

gi di f ferential pressure swi tch. The switch was recalibrated and tested I l mI satisfactorily. As a resul t of a recent increase in the tendency for these l

' 1 I switches to drift. all Unit One and Unit Two high steam flow di f ferential I l i 14 I I pressure switches will be renlaced like-for-like, 1 7 8 9 90

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1. LER NUMBER: LER/R0 82-3/03L-0
11. LICENSEE NAME: Commonwealth Edison Company Quad-Cities Nuclear Power Station ill. FACILITY NAME: Unit Two IV. DOCKET NUMBER: 050-265 V. EVENT DESCRIPTION:

On February 24, 1982, while performing QlS 18, RCIC Steam Line High Flow Calibration and Functional Test, it was found that switch DPIS 2-1360-1B+

would not operate. Technical Specification 3.2.A. (Table 3.2. l .) requi res that the trip setting be less than or equal to 300 percent of rated flow.

VI. PROBABLE CONSEQUENCES OF THE OCCURRENCE:

The differential pressure cell monitors flow in the RCIC steam line in order to detect a potential break in the line. At 300 percent of the rated flow, o signal is required to be initiated to give a Group V isolation signal. Each of the two redundant dif ferential pressure cells, DPIS 2-1360-IA and IB, has two switches; one each in the positive and negative direction. The negative switches sense a low pressure sensing line break while the positive switches sense both a high pressure line break and high flow (DP). Any one of these four switches is capable of initiating the Group V isolation signal. The DPIS 2-1360-1A cell was found to function properly, thereby, ensuring the isolation would have been Initiated had a steam line break occurred.

Vll. CAUSE:

The cause of this occurrence was setpoint drif t of the high side switch, it is a Bellows Type, Model 288 Barton instrument. The switch was last calibrated and functionally tested on November 25, 1981.

Vlli. CORRECTIVE ACTION:

The switch was adjusted and recalibrated to trip at 186" H2O (229 percent of rated flow) and functionally tested satisfactorily on February 24, 1982.

Several of the RCIC high steam flow isolation differential pressure switches have recently shown an increased tendency to drift. This trend has been attributed to normal contact wear. As a precaution, all Unit One and Unit Two RCIC high steam flow micro switches will be replaced with new switches of the same type, if they have not been replaced recently.