ML19290D643

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LER 80-002/03L-0:on 800111,while Performing in-place Charcoal Absorber Leak Rate Test on Standby Gas Treatment sys,1.93% Leakage Found.Caused by Damaged Gasket on 4x4 Inch Access Plate.Gasket Replaced
ML19290D643
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 02/07/1980
From: Kan S
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19290D638 List:
References
LER-80-002-03L-02, LER-80-2-3L-2, NUDOCS 8002220445
Download: ML19290D643 (1)


Text

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LICENSEE EVENT REPORT NTROL BLOCK:

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EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES h IOTT1I While performina the Standby Gas Treatment System inolace Charcoal Adsorber leak o a l Rate Test, procedure QTS 160-2, the 1/2-B-7509 Standby Gas Treatment System (SBGT) l l0 l4 l l charcoal bed was found to have a leakage of 1.93% which was in excess of the 1 o s l Technical Specification 3.7.B.2.a.2 1% allowable penetration. Each of the two SBGT l l0 l6 Ll systems has a 100t, flow capacity, thus only one system is needed to maintain l

[O l7] l secondary containment integrity. The 1/2 A SBGT system was demonstrated operable 1 o 4 l prior to the test. 1 DE CODE SUSC E CcMPONENrCODE SU8 CODE SU E lTTT] l Ml B j@ lE l@ lB l@ F l l l L l T l E l R [@ y@ l Zl @ '

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33 34 35 J6 40 41 42 43 44 CAUSE DESCRIPTION AND CORRECTIVE ACHONS h i o l An inspection revealed a damaged casket on a 4 X 4 inch access olate. The nasket I i i l was replaced and a second test was performed satisfactorily. The charcoal I gl adsorbent itself was intact and functional, i 1 3 l l i 4 l l 7 8 9 80 STA S  % POWER OTHERSTATUS DIS O HY DISCOVERY 0ESCRIPTION Q l El@ l 0 l 9 l 7 l@l NA l lBl@l Routine Test l ACTivtTY CO TENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELE ASE 1 6 l Zl @ l Z lg NA l l NA l 7 as 9 to i 44 45 80 PERSONNEL EXPOSURES NUM8ER TYPE DE SCRIPTION NA

  • 7 10 l 0 l0 l@l Z l@l l PERSONNE L INJUHIES NUM8ER DESCRIPTION i a 0 l 0 l0 lgl NA l 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY h h y,,200 7

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PU 8 L ICIT Y NRC USE ONLY ISSU E D DESCRIPTION

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NAME OF PREPARER S . Ka n PHONE: 309-654-2241 Ext. 174 2,